ML19262C219

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LER 80-001/03L-0:on 800106,fuel Storage Pool Area Radiation Monitor Declared Inoperable Due to hi-alarm Being Set Above Tech Specs.Caused by Setpoint Drift.Instrument Recalibr
ML19262C219
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 02/01/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19262C218 List:
References
LER-80-001-03L, LER-80-1-3L, NUDOCS 8002080359
Download: ML19262C219 (1)


Text

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7 6 60 GB DOCKET hur.'ITEH EVENT DATE EVEf4T DCSCRIPTION AND PRODASLE CON *,CQUCNCES h o 2 l At 1815 on 1/6/80, the Fuel Storage Pool Area Radiation Monitor (R-5) was declared I o 3 l inoperable due to Hi-alarm setpoint being found at 18 ur/hr. The Hi-alarm setpoint pet o . l Tech. Spec. should have been </=15 mr/hr. Tech. Spec. 3.3.3.1, in part, requires.'R-5 I o s I to b'e operable when fuel is in the storage pool. Tech. Spec. 3.3.3.1 action statement l

- o 6 l requirem ats were met. The health and safety of the public were not affected by this l s

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