ML19262C220

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LER 80-003/03L-0:on 800104,determined Surveillance Test FNP-1-STP-109 Re Power Range Neutron Flux Channel Calibr Not Performed During Required Interval.Caused by Personnel Error.Test Performed & Personnel Instructed
ML19262C220
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 02/01/1980
From:
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19262C218 List:
References
LER-80-003-03L, LER-80-3-3L, NUDOCS 8002080367
Download: ML19262C220 (1)


Text

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EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h o 2 l At 1400 on 1-4-80, it was determined that surve:illance test FNP-1-STP-109 (Power l o 3 l Range Neutron Flux Channel Calibration (Heat Balance Only)) had not been performed l o . l within the surveillance interval (every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> i 25%) specified by Tech. Spec. l lo!Sj l 4.3.1.1, Table 4.3-1. The test should have be a performed no later than 0800 on 1-4-80l o a I (including + 25% time interval allowance). The test was satisfactorily: performed [

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