05000348/LER-1980-003-03, /03L-0:on 800104,determined Surveillance Test FNP-1-STP-109 Re Power Range Neutron Flux Channel Calibr Not Performed During Required Interval.Caused by Personnel Error.Test Performed & Personnel Instructed

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/03L-0:on 800104,determined Surveillance Test FNP-1-STP-109 Re Power Range Neutron Flux Channel Calibr Not Performed During Required Interval.Caused by Personnel Error.Test Performed & Personnel Instructed
ML19262C220
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 02/01/1980
From:
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19262C218 List:
References
LER-80-003-03L, LER-80-3-3L, NUDOCS 8002080367
Download: ML19262C220 (1)


LER-1980-003, /03L-0:on 800104,determined Surveillance Test FNP-1-STP-109 Re Power Range Neutron Flux Channel Calibr Not Performed During Required Interval.Caused by Personnel Error.Test Performed & Personnel Instructed
Event date:
Report date:
3481980003R03 - NRC Website

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