IR 05000250/2015004

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Reissue - Turkey Point Nuclear Generating Station - NRC Integrated Inspection Report 05000250/2015004 and 05000251/2015004, October 1, 2015 to December 31, 2015
ML16095A172
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 04/04/2016
From: Ladonna Suggs
NRC/RGN-II/DRP/RPB3
To: Nazar M
Nextera Energy
References
IR 2015004
Download: ML16095A172 (42)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ril 4, 2016

SUBJECT:

REISSUE - TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000250/2015004 and 05000251/2015004

Dear Mr. Nazar:

On January 27, 2015, the U.S. Nuclear Regulatory Commission (NRC) issued the subject inspection report for Turkey Point Units 3 and 4 - NRC Integrated Inspection Report (IR)

05000250/2015004 and 05000251/2015004, (ADAMS Accession Number ML16027A147).

In the Inspection Scope of Section 4OA1 Performance Indicator Verification (IP 71151),

subsection .1 Barrier Integrity Cornerstone, of the previously issued IR, we documented an incorrect number of samples. We request that the entire report be replaced with the enclosure to this letter.

In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRC's "Agency Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)

component of the NRC's Agency wide Documents Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). If you have any questions, please contact me at (404) 997-4539.

Sincerely,

/RA/

LaDonna B. Suggs, Chief Reactor Projects Branch 3 Division of Reactor Projects

Enclosure:

As stated

REGION II==

Docket Nos: 50-250, 50-251 License Nos: DPR-31, DPR-41 Report Nos: 05000250/2015004, 05000251/2015004 Licensee: Florida Power & Light Company (FP&L)

Facility: Turkey Point Nuclear Generating Station, Units 3 & 4 Location: 9760 S. W. 344th Street Homestead, FL 33035 Dates: October 1 to December 31, 2015 Inspectors: T. Hoeg, Senior Resident Inspector M. Endress, Resident Inspector M. Bates, Senior Operations Engineer R. Williams, Senior Reactor Inspector B. Pursley, Health Physicist C. Dykes, Health Physicist J. Panfel, Health Physicist B. Kellner, Senior Health Physicist P. Capehart, Senior Operations Engineer Approved by: LaDonna B. Suggs, Chief Reactor Projects Branch 3 Division of Reactor Projects Enclosure

SUMMARY

IR 05000250/2015004, 05000251/2015004; 10/01/2015 - 12/31/2015; Turkey Point Nuclear

Generating Station, Units 3 and 4; Refueling Outage & Other Outage Activities.

The report covered a three-month period of inspection by the resident inspectors and specialist inspectors from the Region II office. One Green non-cited violation (NCV) was identified. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process, (SDP) dated April 29, 2015. The cross-cutting aspects were determined using IMC 0310, Aspects Within the Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements were dispositioned in accordance with the NRCs Enforcement Policy dated February 4, 2015. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision

NRC-Identified and Self-Revealing Findings

Cornerstone: Barrier Integrity

  • Green: A self-revealing NCV of Technical Specification (TS) 6.8.1, Procedures and Programs, was identified when the licensee failed to properly implement procedure 3-PMI-072.6, Steam Dump to Atmosphere Control Loop Calibration. Specifically, the licensee incorrectly installed a temporary electrical jumper in reactor operator console 3C02 instead of 3C04, in contrast to Step 6.3.2 of 3-PMI-072.6. This action resulted in actuation of a 3B 4160 volt (V) vital bus lockout circuit causing loss of power to the B train of Unit 3 (U3) spent fuel pool (SFP) cooling. Immediate corrective actions were taken to remove the jumper and restore the B train of SFP cooling. The licensee entered the condition in its corrective action program (CAP) as action request (AR)02088911 and 02088914.

The performance deficiency was determined to be more than minor because it was associated with the human performance attribute of the barrier integrity cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding, reactor coolant system (RCS), and containment)protect the public from radionuclide releases. In addition, the performance deficiency, if left uncorrected, had the potential to lead to a more significant safety concern. The finding was screened using IMC 0609, Significance Determination Process,

Attachment 0609.04, Initial Characterization of Findings, Tables 2 and 3, dated July 1, 2012, and Appendix G Attachment 1, Shutdown Operations Significance Determination Process Phase 1 Initial Screening and Characterization of Findings, Exhibit 4 for Barrier Integrity, dated May 9, 2014. The inspectors determined the finding was of very low safety significance (Green) because it was not associated with low temperature over pressurization, freeze seals, steam generator nozzle dams, criticality, drain down or leakage paths, or the containment barrier. Furthermore, one train of SFP cooling remained in operation, the rate of SFP temperature rise was low (~ 2 °F/hour), and additional methods remained available to limit SFP temperature rise. This finding was assigned a cross cutting aspect associated with the procedure adherence element of the human performance area because the licensee failed to correctly execute step 6.3.2 of procedure 3-PMI-072.6 (H.8). (Section 1R20)

Licensee-Identified Violations

Violations of very low safety or security significance or Severity Level IV that were identified by the licensee have been reviewed by the NRC. Corrective actions taken or planned by the licensee have been entered into the licensees CAP. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 3 began this inspection period at 100 percent of Rated Thermal Power (RTP) where it remained until October 19, 2015, when it was shut down for a scheduled refueling outage (RFO). Unit 3 was restarted November 29, 2015, and returned to 100 percent of RTP on December 9, 2015, where it remained through the end of this inspection period.

Unit 4 (U4) began this inspection period at 100 percent of RTP where it remained through the end of this inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection (IP 71111.01)

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

During the month of December, the inspectors reviewed and verified the status of actions taken by the licensee for winter readiness prior to the onset of cool weather. The inspectors reviewed licensee procedure OP-AA-102-1002, Seasonal Readiness, 7, Cold Weather Readiness Check List, and Attachment 14, Turkey Point Site Specific Guidance. The inspectors reviewed system health reports and open CAP ARs for the emergency diesel generators (EDGs) and auxiliary feedwater (AFW) pumps to determine if any deficiencies existed that could affect operation of equipment immersion heaters. The inspectors performed walk downs of systems that could be affected by cold weather as outlined in the licensee site specific guidance including the following areas:

  • U3 and U4 charging pumps

b. Findings

No findings were identified.

1R04 Equipment Alignment (IP 71111.04)

.1 Partial Equipment Walk Downs (Quarterly)

a. Inspection Scope

The inspectors conducted three partial alignment verifications of the safety-related systems listed below. These inspections included reviews using plant lineup procedures, operating procedures, and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified that the licensee had identified and resolved, by entering them in the CAP, equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers. Documents reviewed are listed in the Attachment. This inspection constitutes three samples.

  • 4A and 4B high head safety injection (HHSI) pumps while 3A and 3B HHSI pumps were OOS

b. Findings

No findings were identified.

1R05 Fire Protection (IP 71111.05)

.1 Fire Area Walk downs

a. Inspection Scope

The inspectors walked down the following five plant areas to evaluate conditions related to control of transient combustibles, ignition sources, material condition, and operational status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensees procedure 0-ADM-016, Fire Protection Plan and 10 CFR Part 50, Appendix R. The inspectors routinely reviewed the licensees fire impairment lists and monitored the associated corrective actions for completion. The inspectors reviewed the AR report database to verify that fire protection problems were being identified and appropriately resolved in the CAP. The inspectors tours of the selected areas verified the fire protection equipment was installed as shown on the applicable fire plan drawings and appeared functional and ready for usage. This inspection constitutes five samples. The following areas were inspected:

  • U4 Pipe and Valve Room, Fire Zone 030
  • U3 Containment Building, Fire Zone 060
  • U4 4B Vital Battery Room, Fire Zone 102
  • U3 and U4 Mechanical Equipment Room, Fire Zone 097
  • Auxiliary Building Electrical Equiptment Room, Fire Zone 025

b. Findings

No findings were identified.

.2 Fire Protection - Drill Observation

a. Inspection Scope

On December 9, 2015, the inspectors observed an unannounced fire drill that took place within the station power block just outside the 3D31/4D31 non vital 125 VDC switchgear room in the turbine building. The drill was observed to evaluate the readiness of the plant fire brigade to fight fires and the control room to make the proper emergency action level (EAL) classification. The inspectors verified that the licensee staff identified deficiencies, openly discussed them in a self-critical manner at the drill debrief meeting, and took appropriate corrective actions as required. Specific attributes evaluated were:

  • Proper wearing of fire protective gear and self-contained breathing apparatus
  • Proper use and layout of fire hoses
  • Employment of appropriate fire-fighting techniques
  • Sufficient fire-fighting equipment brought to the scene
  • Effectiveness of command and control
  • Search for victims and propagation of the fire into other plant areas
  • Smoke removal operations
  • Utilization of pre-planned strategies
  • Adherence to the pre-planned drill scenario
  • Drill objective The inspectors also observed the placement and charging of the fire hoses used to simulate extinguishing the fire.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities (IP 71111.08)

a. Inspection Scope

Non-Destructive Examination Activities and Welding Activities From October 26-29, 2015, the inspectors conducted an onsite review of the implementation of the licensees inservice inspection (ISI) program for monitoring degradation of the RCS boundary, risk-significant piping and component boundaries, and containment boundaries in U3.

The inspectors either directly observed or reviewed the following non-destructive examinations (NDEs) mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record: 2007 Edition with 2008 Addenda) to evaluate compliance with the ASME Code,Section XI and Section V requirements, and if any indications or defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement. The inspectors also reviewed the qualifications of the NDE technicians performing the examinations, to determine whether they were current and in compliance with the ASME Code requirements.

  • Ultrasonic Examination of Loop B 18-inch Feedwater Nozzle-to-Pipe weld, Augmented Examination (observed)
  • Ultrasonic Examination (UT) of Loop B 14-inch Feedwater Pipe-to-Elbow weld, Augmented Examination (observed)
  • Visual Examination (VT-3) of Spring Hanger 3-RCH-27, Class 1 Support (observed)
  • VT-3 of Dual Spring Hanger VS-1G-12, Class 1 Support (observed)

The inspectors either directly observed or reviewed the following welding activities, qualification records, and associated documents in order to evaluate compliance with procedures and the ASME Code,Section XI and Section IX requirements. Specifically, the inspectors reviewed the work order (WO), repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports.

During non-destructive surface and volumetric examinations performed since the previous RFO, the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service; therefore, no NRC review was completed for this inspection procedure (IP) attribute.

Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities The inspectors verified that for the U3 vessel head, a bare metal visual examination and a volumetric examination were not required during this outage, in accordance with the requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D).

The licensee did not identify any relevant indications that were accepted for continued service. Additionally, the licensee did not perform any welding repairs to the vessel head penetrations since the beginning of the last U3 RFO; therefore, no NRC review was completed for these IP attributes.

Boric Acid Corrosion Control Inspection Activities The inspectors reviewed the licensees boric acid corrosion control program activities to determine if the activities were implemented in accordance with the commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants, and applicable industry guidance documents. Specifically, the inspectors performed an onsite records review of procedures, and the results of the licensees containment walkdown inspections performed during the current RFO. The inspectors also interviewed the Boric Acid Corrosion Control (BACC) program owner, conducted an independent walkdown of containment to evaluate compliance with licensees BACC program requirements, and verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensees BACC and CAP.

The inspectors reviewed the following engineering evaluations, completed for evidence of boric acid leakage, to determine if the licensee properly applied applicable corrosion rates to the affected components; and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity in accordance with the licensee procedures.

  • AR 02086287, CV-3-2819 has corrosion on electrical connection

Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the CAP to determine if the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (IP 71111.11)

.1 Licensed Operator Requalification Exam

a. Inspection Scope

Annual Review of Licensee Requalification Examination Results: On December 30, 2015, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with 10 CFR 55.59(a)(2). The inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with IP 71111.11, Licensed Operator Requalification Program. These results were compared to the thresholds established in Section 3.02, Requalification Examination Results, of IP 71111.11.

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Review

a. Inspection Scope

The inspectors performed the following inspection sample of a simulator observation and assessed licensed operator performance while training. These observations included procedural use and adherence, response to alarms, communications, command and control, and coordination and control of the reactor plant operations.

On October 8, 2015, the inspectors assessed licensed operator performance in the plant-specific simulator during a training evolution. The training scenario was started with the unit in Mode 1 at 100 percent power and included a fire lasting greater than 15 minutes, a loss of reactor coolant accident (LOCA), a reactor trip, a safety injection, a residual heat removal (RHR) pump seal failure, and a radiological release to the environment.

During this simulator observation, the simulator board configurations were compared with actual plant control board configurations reflecting recent plant changes or modifications. The inspectors specifically evaluated the following attributes related to operating crew performance and the licensee evaluation:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of off-normal and emergency operating procedures and emergency plan implementing procedures
  • Control board operation and manipulation, including high-risk operator actions
  • Oversight and direction provided by shift supervisor, including ability to identify and implement appropriate TS actions and emergency plan classification and notification
  • Crew overall performance and interactions
  • Evaluators control of the scenario and post scenario evaluation of crew performance

b. Findings

No findings were identified.

.3 Control Room Observations

a. Inspection Scope

The inspectors performed daily assessments of licensed operators in the control room during their performance of routine operations. These observations included daily surveillance testing, log keeping, response to alarms, communications, shift turnovers, and coordination of plant activities. These observations were conducted to verify operator compliance with station operating guidelines, such as use of procedures, control and manipulation of components, and communications. The inspectors also performed the following three focused control room observations during reactivity manipulations and Mode changes:

On November 19, 2015, the inspectors performed a focused observation on U4 consisting of a RCS primary water dilution per 0-OP-046, Enclosure 6, Chemical Volume Control System Boron Concentration Control. Specifically, the inspectors observed the reactor operators performance of the pre-job brief per 0-ADM-200, 7, Planned Reactivity Manipulations for Maintaining Steady State Plant Conditions and verified the operators complied with the applicable procedure during the evolution.

On December 1, 2015 and December 2, 2015, the inspectors performed a focused observation in the U3 control room during low power physics testing in accordance with procedure 0-OSP-040.19, Low Power Physics Testing. The inspectors observed the pre-evolution operating crew brief, control rod movements, monitoring of subcritical multiplication, and data collection.

On December 3, 2015, the inspectors performed a focused observation on U3 during a reactor startup per procedure 3-GOP-301, Hot Standby to Power Operations. The inspectors reviewed the expected critical boron concentration calculation and the control rod pull sequence plan used during the observed reactor startup. The inspectors reviewed the recorded reactor startup physics data to ensure it was as calculated by the licensee reactor engineering staff.

This inspection constitutes three samples. The inspectors focused on the following conduct of operations attributes as appropriate:

  • Operator compliance and use of procedures
  • Control board manipulations
  • Communication between crew members
  • Use and interpretation of plant instruments, indications and alarms
  • Use of human error prevention techniques
  • Documentation of activities, including initials and sign-offs in procedures
  • Supervision of activities, including risk and reactivity management

b. Findings

No findings were identified.

.4 Biennial Requalification

a. Inspection Scope

The inspectors reviewed the facility operating history and associated documents in preparation for this inspection. During the weeks of November 30, 2015 through December 21, 2015, the inspectors reviewed documentation associated with the licensees operator requalification program biennial written examinations. The activity performed by the inspectors was conducted to assess the licensees effectiveness in implementing requalification requirements identified in 10 CFR Part 55, Operators Licenses. The evaluations were also performed to determine if the licensee effectively implemented operator requalification guidelines established in NUREG-1021, Operator Licensing Examination Standards for Power Reactors, and IP 71111.11, Licensed Operator Requalification Program. Documentation reviewed included two biennial written examinations. The records were inspected using the criteria listed in IP 71111.11. Documents reviewed during the inspection are documented in the List of Documents Reviewed.

The sample is now complete because the remainder of this sample was previously inspected and documented in the third quarter integrated inspection report (05000250&251/2015003).

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (IP 71111.12)

a. Inspection Scope

The inspectors reviewed known equipment problems associated with the U3 steam generator steam flow module FM-3-474D affecting the maintenance rule program and equipment performance history trends associated with the equipment. Specifically, the inspectors reviewed AR 02081538.

The inspectors reviewed the licensees activities to meet the requirements of 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, and licensee procedure NAP-415, Maintenance Rule Program Administration.

The inspectors focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of a(1) or a(2)performance criteria classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed or reviewed corrective maintenance activities. The inspectors verified that equipment problems were being identified and appropriately entered into the licensees CAP. The inspectors used the licensee maintenance rule database, system health reports, maintenance rule unavailability status reports, and the CAP as sources of information on tracking and resolution of issues. This inspection constitutes one sample.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (IP 71111.13)

a. Inspection Scope

The inspectors completed in-office reviews and control room inspections of the licensees risk assessment of five emergent or planned maintenance activities. The inspectors verified the licensees risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, Work Week Management; WM-AA-1000, Work Activity Risk Management; and 0-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensees contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee is assessment of aggregate risk using procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors discussed the on-line risk monitor (OLRM) results with the control room operators and verified all applicable OOS equipment was included in the OLRM calculation. The inspectors evaluated the following five risk assessment samples during the inspection period:

  • U3 3A 4kV Bus, U3 Startup Transformer (SUT), and 3A and 3B HHSI pumps OOS
  • U3 3A 4kV Bus, U3 SUT, and 3D Vital 480V Motor Control Cabinet (MCC) OOS
  • U3 3-312A Valve Inspection and Repair with Freeze Seal (WO 40411630)
  • U3 Train 2 AFW, U4 Train 2 AFW, and U3 3B Emergency Containment Cooler OOS

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (IP 71111.15)

a. Inspection Scope

The inspectors evaluated the technical adequacy of the licensee evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred for the five operability evaluations described in the ARs listed below. The inspectors reviewed applicable sections of the updated Final Safety Anaylsis Report (UFSAR) to determine if the system or component remained available to perform its intended function. In addition, when applicable, the inspectors reviewed compensatory measures implemented to verify that the affected equipment remained capable of performing its intended design function.

The inspectors also reviewed a sampling of CRs to verify that the licensee routinely identifed and corrected any deficiencies associated with operability evaluations. This inspection constitutes five samples.

  • AR 02082853, Pressurizer Steam Sample Line Containment Isolation Valve (CV-4-951) OOS

b. Findings

No findings were identified.

1R18 Plant Modifications (IP 71111.18)

Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed the following two permanent plant modifications. The inspectors reviewed the 10 CFR 50.59 screening and technical evaluation to verify that the modifications had not affected system operability or availability. The inspectors reviewed associated plant drawings, design analyses, and UFSAR documents impacted by these modifications and discussed the changes with licensee personnel to verify that the modifications were consistent with the WO and associated documents. The inspectors observed portions of the modifications and surrounding areas to determine if conditions resulted in any potential unsafe conditions not described in the engineering change documentation. Additionally, the inspectors reviewed and verified that any conditions associated with the modifications were being identified and entered into the CAP. This inspection constitutes two samples.

b. Findings

No findings were identified.

1R19 Post Maintenance Testing (IP 71111.19)

a. Inspection Scope

For the five post maintenance tests and associated WOs listed below, the inspectors reviewed the test procedures and either witnessed the testing or reviewed test records to determine whether the scope of testing adequately verified that the work performed was completed satisfactorily and demonstrated that the affected equipment was operable.

The inspectors verified that the requirements in licensee procedure 0-ADM-737, Post Maintenance Testing, were incorporated into the test requirements. The inspectors reviewed the following WOs consisting of five inspection samples:

  • WO 40281614, U3 Pressurizer Pressure Operated Relief Valve PCV-3-455C

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities (IP 71111.20)

.1 Unit 3 Refueling Outage PT3-28 (one sample)

a. Inspection Scope

Outage Planning, Control and Risk Assessment During daily outage planning activities by the licensee, the inspectors reviewed the risk reduction methodology employed by the licensee during RFO PT3-28 meetings including outage control center (OCC) morning meetings, operations daily team meetings, and schedule performance update meetings. The inspectors examined the licensee implementation of shutdown safety assessments during PT3-28 in accordance with administrative procedure ADM-051, Outage Risk Assessment and Control, to verify if a defense in depth concept was in place to ensure safe operations and avoid unnecessary risk. In addition, the inspectors regularly monitored outage planning and control activities in the OCC, and interviewed responsible OCC management personnel during the outage to ensure system, structure, and component configurations, and work scope were consistent with TS requirements, site procedures, and outage risk controls.

Monitoring of Shutdown Activities The inspectors performed walk downs of important systems and components used for RHR from the reactor core and SFP during the shutdown period, including the intake cooling water system, component cooling water (CCW) system, and SFP cooling system.

Outage Activities The inspectors examined outage activities to verify that they were conducted in accordance with TS, licensee procedures, and the licensees outage risk control plan.

Some of the more significant inspection activities accomplished by the inspectors were as follows:

  • Walked down selected safety-related equipment clearance orders
  • Verified operability of RCS pressure, level, flow, and temperature instruments during various modes of operation
  • Verified electrical systems availability and alignment
  • Evaluated implementation of reactivity controls
  • Reviewed control of containment penetrations
  • Examined foreign material exclusion (FME) controls put in place inside containment (e.g., around the refueling cavity, near sensitive equipment and RCS breaches) and around the SFP
  • Observed fuel loading and unloading in the SFP and in containment Monitoring of Plant Heat up and Containment Closure Activities The inspectors examined the applicable TS, license conditions, and verified administrative prerequisites were being met prior to reactor plant mode changes. The inspectors reviewed measured RCS leak rates, and verified containment integrity was properly established. The inspectors performed a containment closeout inspection prior to the reactor plant startup to verify no evidence of leakage or debris were left in containment that could affect plant operations.

Reactor Startup and Mode Changes On December 2, 2015, the inspectors observed the U3 reactor startup and turbine synchronization to the electrical grid and associated Mode changes. The inspectors reviewed the recorded reactor startup physics data in order to determine it was as-calculated by the licensee reactor engineering staff. The inspectors determined that startup and Mode changes were performed in accordance with licensee procedures 0-OSP-040.16, Initial Criticality After Refueling Outage and Nuclear Design Verification, and 3-GOP-301, Mode 3 to Power Operations.

Corrective Action Program The inspectors reviewed ARs generated during PT3-28 to evaluate the licensees threshold for initiating ARs. The inspectors reviewed CRs to verify priorities, Mode holds, and significance levels were assigned as required. Resolution and implementation of corrective actions of several ARs were also reviewed for completeness. The inspectors routinely reviewed the results of site oversight of daily surveillances of outage activities.

b. Findings

Introduction:

A Green self-revealing NCV of TS 6.8.1, Procedures and Programs, was identified for the licensees failure to correctly execute procedure 3-PMI-072.6, Steam Dump to Atmosphere Control Loop Calibration. The failure resulted in actuation of a 3B 4160 V vital bus lockout circuit causing loss of power to the B train of U3 SFP cooling.

Description:

On November 4, 2015, at 2112 hours0.0244 days <br />0.587 hours <br />0.00349 weeks <br />8.03616e-4 months <br />, Instrumentation and Controls technicians were performing procedure 3-PMI-072.6, Steam Dump to Atmosphere Control Loop Calibration, when a temporary electrical jumper was incorrectly installed in the control room reactor operator console 3C02 instead of 3C04, in contrast to step 6.3.2 of 3-PMI-072.6. At the time of the event, U3 was defueled with all of its fuel temporarily relocated to the SFP. The 3A 4160 V vital bus was de-energized for planned maintenance and all 480 V vital load centers were powered by the 3B 4160 V vital bus.

Separate load centers provided power to two separate trains of U3 SFP cooling pumps, and the 3A train pump was powered from Unit 4 electrical switchgear.

The incorrectly placed jumper actuated a 3B 4160 V vital bus lockout circuit causing all associated Unit 3 480 V vital load and motor control centers to de-energize. Numerous equipment was rendered OOS including the B SFP cooling pump and the 3B CCW pump. The 3B CCW pump provided cooling to both U3 SFP cooling heat exchangers.

Upon loss of the 3B CCW pump, the standby 3C CCW pump started on low pressure as designed, providing cooling to the 3A SFP cooling train. Immediate corrective action was taken to remove the jumper and restore the B train of SFP cooling. However, the loss of one train of SFP cooling for approximately four hours caused the SFP temperature to rise from approximately 110 °F to 117 °F. The licensee restored U3 load and motor control centers at 0207 hours0.0024 days <br />0.0575 hours <br />3.422619e-4 weeks <br />7.87635e-5 months <br /> on November 5, 2015, and by 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br /> the SFP temperature had returned to normal.

The licensee entered the condition in its CAP as AR 02088911 and 02088914.

Corrective actions included site-wide briefings of lessons learned from the event, quality reviews of procedure 3-PMI-072.6, and enhanced oversight of maintenance activities.

Analysis:

The inspectors determined that the failure to correctly implement maintenance procedure 3-PMI-072.6 was a performance deficiency. The performance deficiency was determined to be more than minor because it was associated with the human performance attribute of the barrier integrity cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding, RCS, and containment) protect the public from radionuclide releases.

Specifically, the licensees failure to correctly execute step 6.3.2 of procedure 3-PMI-072.6 rendered one of two SFP cooling trains OOS, causing the SFP temperature to rise from approximately 110 °F to 117 °F over a four-hour period. While the performance deficiency did not directly challenge the integrity of the fuel cladding, if left uncorrected, the SFP temperature would have continued to increase, potentially affecting SFP inventory.

The finding was screened using IMC 0609, Significance Determination Process, 0609.04, Initial Characterization of Findings, Tables 2 and 3, dated July 1, 2012, and Appendix G Attachment 1, Shutdown Operations Significance Determination Process Phase 1 Initial Screening and Characterization of Findings, Exhibit 4 for Barrier Integrity, dated May 9, 2014. The inspectors determined the finding was of very low safety significance (Green) because it was not associated with low temperature over pressurization, freeze seals, steam generator nozzle dams, criticality, drain down or leakage paths, or the containment barrier. Furthermore, one train of SFP cooling remained in operation, the rate of SFP temperature rise was low (~2 °F/hour), and additional diverse compensatory methods remained available to limit SFP temperature rise. This finding was assigned a cross cutting aspect associated with the procedure adherence element of the human performance area because the licensee failed to correctly execute step 6.3.2 of procedure 3-PMI-072.6 (H.8).

Enforcement:

Technical Specification 6.8.1 requires that procedures required by the licensees Quality Assurance Topical Report (QATR) be established, implemented, and maintained. The QATR includes procedures listed in Appendix A of NRC Regulatory Guide 1.33, Revision 2, dated February 1978, including procedures for calibrations. The licensee implements TS 6.8.1 requirements, in part, using procedure 3-PMI-072.6, Steam Dump to Atmosphere Control Loop Calibration. Step 6.3.2 of procedure 3-PMI-072.6, requires that a jumper be installed in reactor operator console 3C02.

Contrary to this requirement, on November 4, 2015, at 2112 hours0.0244 days <br />0.587 hours <br />0.00349 weeks <br />8.03616e-4 months <br />, a maintenance technician mistakenly installed a jumper in reactor operator console 3C04. This action resulted in actuation of a 3B 4160 V vital bus lockout circuit causing loss of power to the B train of U3 SFP cooling. The licensee took immediate corrective action to remove the jumper. This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy, because it was of very low safety significance and was entered in the licensees CAP as AR 02088911 and 02088914. (NCV 05000250/2015004-01, Failure to correctly follow procedure 3-PMI-072.6, Steam Dump to Atmosphere Control Loop Calibration.)

1R22 Surveillance Testing (IP 71111.22)

a. Inspection Scope

The inspectors either reviewed or observed the following five surveillance tests to verify that the tests met the TS requirements, the UFSAR description, the licensees procedural requirements, and demonstrated that systems were capable of performing their intended safety functions and operational readiness. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the status required for the system to perform its safety function. The inspectors verified that any surveillance deficiencies were documented in the licensees CAP. This inspection constitutes two surveillance test samples, one inservice testing (IST) sample, and two containment isolation valve leak test samples. The inspectors reviewed the following tests:

Surveillance Test:

  • 0-OSP-059.13, U4 Flux Map
  • 3-OSP-072.5, U3 Main Steam Safey Valve Setpoint Verification In-Service Tests:
  • 3-OSP-206.1, Component Cooling Water MOV-3-1418 Valve Test (IST)

Containment Isolation Valve Test:

  • 3-OSP-051.5, U3 Local Leak Rate Test, Penetration 8 CV-3-951
  • 3-OSP-051.5, U3 Local Leak Rate Test, Penetration 14 CV-3-204

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (IP 71114.06)

.1 Emergency Preparedness Drill

a. Inspection Scope

On October 8, 2015, the inspectors observed an emergency preparedness drill and the performance of the licensees emergency response organization. The drill included a simulated fire in the U4 laydown area, a LOCA inside containment, followed by a RHR pump seal failure and radiological release to the environment. The fire, lasting greater than 15 minutes, required an unusual event emergency declaration and notification to state and local county officials and the NRC per licensee procedure 0-EPIP-20101, Duties of the Emergency Coordinator. The scenario progressed to a loss of two RCS barriers with the loss or potential loss of a third barrier requiring a general emergency declaration and an additional notification. The inspectors observed the crew in the plant simulator, including simulated implementation of emergency procedures. The inspectors observed the emergency response organization staff in the control room simulator and technical support center while they implemented the event classification guidelines and emergency response procedures. The inspectors determined that the emergency classification and notifications were made in accordance with the licensee emergency plan implementing procedure 0-EPIP-20101. The inspectors attended the licensees post drill critique, reviewed the licensees critique items, and discussed inspector observations with the licensee to verify that drill issues were identified and captured in the licensees CAP. This inspection constitutes one sample.

b. Findings

No findings were identified.

RADIATION SAFETY

(RS)

Cornerstones: Public Radiation Safety and Occupational Radiaition Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (IP 71124.01)

a. Inspection Scope

Hazard Assessment and Instructions to Workers. During facility tours, the inspectors directly observed labeling of radioactive material and postings for radiation areas, high radiation areas, and airborne radioactivity areas established within the radiologically controlled area (RCA) of the U3 containment building, auxiliary building, the Independent Spent Fuel Storage Installation (ISFSI), and radioactive waste processing and storage locations. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected RCA areas. The inspectors reviewed survey records for several plant areas including surveys for alpha emitters, airborne radioactivity, gamma surveys with a range of dose rate gradients, and pre-job surveys for upcoming tasks. The inspectors also discussed changes to plant operations that could contribute to changing radiological conditions since the last inspection. For selected outage jobs, the inspectors attended pre-job briefings and reviewed Radiation Work Permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers.

Hazard Control and Work Practices. The inspectors evaluated access barrier effectiveness for selected Locked High Radiation Area (LHRA) locations and discussed changes to procedural guidance for LHRA and Very High Radiation Area controls with Radiation Protection (RP) supervisors. The inspectors observed and evaluated controls for the storage of irradiated material within the SFP. Established radiological controls (including airborne controls) were evaluated for selected U3 RFO 28 (U3R28) tasks including RCP seal replacements, reactor cavity decontamination and reactor sump demobilization activities. In addition, the inspectors reviewed licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations.

Through direct observations and interviews with licensee staff, the inspectors evaluated occupational workers adherence to selected RWPs and RP technician proficiency in providing job coverage. Electronic dosimeter (ED) alarm set points and worker stay times were evaluated against area radiation survey results for selected U3 RFO jobs, including the reactor sump demobilization and reactor cavity decontamination. The inspectors discussed the use of personnel dosimetry (extremity dosimetry and multibadging in high dose rate gradients) with RP staff. The inspectors also evaluated worker response to dose and dose rate alarms during selected work activities.

Control of Radioactive Material. The inspectors observed surveys of material and personnel being released from the RCA using small article monitor (SAM), personnel contamination monitor (PCM), and portal monitor instruments. As part of IP 71124.05, the inspectors reviewed the last two calibration records for selected release point survey instruments and discussed equipment sensitivity, alarm setpoints, and release program guidance with licensee staff. The inspectors reviewed records of leak tests on selected sealed sources and discussed nationally tracked source transactions with licensee staff.

Problem Identification and Resolution. The inspectors reviewed CAP documents associated with radiological hazard assessment and exposure control. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures. The inspectors also reviewed recent self-assessment results.

Radiation protection activities were evaluated against the requirements of the UFSAR Section 11; TS Sections 6.8 Procedures and Programs and 6.12 High Radiation Area; 10 CFR Parts 19 and 20; Regulatory Guide 8.38, Control of Access to High and Very High Radiation Areas in Nuclear Power Plants; and approved licensee procedures.

Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

2RS2 Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls

(IP 71124.02)

a. Inspection Scope

Work Planning and Exposure Tracking. The inspectors reviewed work activities and their collective exposure estimates for U3 RFO. The inspectors reviewed ALARA planning packages for the following high collective exposure tasks: SG cleaning (including bundle flushing, sludge lancing, and foreign object search and retrieval); refueling activities; RCP seal replacement; bottom mounted inspection, and; various valve work. For the selected tasks, the inspectors reviewed established dose goals and discussed assumptions regarding the bases for the current estimates with responsible ALARA planners. The inspectors evaluated the incorporation of exposure reduction initiatives and operating experience. Adjustments made to planned doses were also reviewed, along with the basis of those adjustments. Post-job reviews from both the current and previous RFO were assessed. Where applicable, the inspectors discussed changes to established estimates with ALARA planners and evaluated them against work scope changes or unanticipated elevated dose rates.

Source Term Reduction and Control. The inspectors reviewed the collective exposure three-year rolling average from 2012-2014 and reviewed historical collective exposure trends. The inspectors evaluated historical dose rate trends and compared them to current data.

Radiation Worker Performance. In conjunction with IP 71124.01, radiation worker performance was evaluated during several tasks both within containment and the auxiliary building. The inspectors specifically evaluated both the use of ALARA briefings and remote technologies, including teledosimetry and remote visual monitoring, to reduce dose.

Problem Identification and Resolution. The inspectors reviewed and discussed selected CAP documents associated with ALARA program implementation. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures. The inspectors also reviewed recent self-assessment results.

ALARA program activities were evaluated against the requirements of the UFSAR Section 11, applicable TS Sections 6.8 and 6.12, 10 CFR Part 20, and approved licensee procedure. Records reviewed are listed in the Attachment.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (IP 71124.03)

a. Inspection Scope

Engineering Controls: Licensee engineering controls used to control and mitigate airborne radioactivity were reviewed and discussed. The inspectors evaluated selected U3 engineering controls including temporary High Efficiency Particulate Air (HEPA)filtration systems for selected outage tasks with the potential for generating airborne activity conditions. The evaluations included procedural guidance, operability testing, and established configurations during specific outage tasks. In addition, plant guidance and its implementation for the monitoring of potential airborne beta-gamma and alpha-emitting radionuclides for outage tasks associated with refueling activities, head disassembly, and valve maintenance were reviewed and discussed with cognizant licensee representatives.

Use of Respiratory Protection Devices: Program guidance for issuance and use of respiratory protection devices were reviewed and discussed with responsible licensee representatives. The inspectors reviewed Total Effective Dose Equivalent (TEDE)

ALARA evaluations conducted for select U3 outage tasks. Use of respiratory protective equipment was evaluated for selected workers involved in U3 outage activities. The inspectors toured selected onsite compressors available for supplying breathing air for current outage activities and reviewed Grade D or greater air certification for permanent and temporary on-site compressors used for supplied-line breathing air and self-contained breathing apparatus (SCBA) bottle fill-station activities. Training, fit testing, and medical qualifications for selected RP, maintenance, and operations using respiratory protection for outage activities were reviewed and discussed with cognizant licensee representatives.

Self-Contained Breathing Apparatus for Emergency Use: The inspectors reviewed current status, operability and availability of select respiratory and SCBA equipment maintained within the U3 and U4 control rooms, B5B lockers, and U3 and U4 reactor auxiliary building locations. Maintenance activities for selected respiratory protective equipment (e.g., compressed gas cylinders, regulators, valves, and hose couplings), by certified vendor technicians were reviewed for selected SCBA units. Training, fit testing, and medical qualifications for selected RP, maintenance, and operations staff assigned Emergency Response Organization duties were reviewed and discussed with cognizant licensee representatives. For selected U3 and U4 control room operators, the inspectors discussed and reviewed annual hands-on SCBA training activities, including donning, doffing, and functionally checking SCBA equipment, bottle change out, and also reviewed availability of corrective lens, as applicable, for on-shift personnel.

Problem Identification and Resolution: The inspectors reviewed selected CAP documents within the area of radiological airborne controls and respiratory protection activities. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures PI-AA-104-1000, Corrective Action, Rev.

6, and 0-ADM-533, Corrective Action Program Guidance, Rev. 14. The inspectors also evaluated the scope of the licensees internal audit program and reviewed recent assessment results. Specific licensee CAP documents reviewed for airborne radionuclide concentration monitoring and mitigation are listed in the Attachment.

Radiation Protection program activities associated with airborne radioactivity monitoring and controls were evaluated against details and requirements documented in the UFSAR, TS Section 3/4.9.9, Containment Ventilation System, 3/4.9.13, Radiation Monitoring, and 6.8.1, Procedures and Programs; 10 CFR Part 20, and also approved licensee procedures. Documents reviewed are listed in the Attachment.

The inspectors completed all specified line-items detailed in IP 71124.03.

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment (IP 71124.04)

a. Inspection Scope

The inspector evaluated current RP program guidance and its implementation for monitoring and assessing occupational workers internal and external radiation exposure. The review included quality assurance activities, results, and responses to identified issues; and individual dose results for selected occupational workers.

External Dosimetry: The inspector reviewed and discussed RP program guidance for monitoring external and internal radiation exposures of occupational workers. The inspector verified National Voluntary Laboratory Accreditation Program certification data and discussed program guidance for storage, processing and results for dosimeters currently in use. The inspector also reviewed and discussed the comparison between ED and thermoluminescent dosimeter data.

Internal Dosimetry: Program guidance, instrument detection capabilities, and select results for assessing internally deposited radionuclides were reviewed and discussed in detail. The inspector evaluated licensee follow-up in vivo monitoring results and dose assignment for three workers involved in contamination events having the potential for internal deposition of radioactive material. In addition, the current licensee and contract vendor laboratory analysis capabilities for the collection and analysis of in vitro samples were reviewed and discussed in detail.

Special Dosimetric Situations: The inspector reviewed monitoring conducted and results for two declared pregnant workers since the last inspection. The methodology and results of monitoring occupational workers within non-uniform external dose fields and assignment of effective dose equivalent results were discussed in detail. In addition, the adequacy of dosimetry program guidance and its implementation for shallow dose assessments and supporting calculations for an individual involved in a select contamination event were evaluated. Neutron monitoring guidance and implementation for select at power containment entries were reviewed and discussed. RP staff proficiency involved in conducting skin dose assessments, neutron monitoring, and whole body counter (WBC) operations were evaluated through review and discussions of completed records and supporting data.

Problem Identification and Resolution: The inspectors reviewed and discussed selected CAP documents associated with occupational dose assessment. The reviewed items included ARs, self-assessments, and quality assurance audit documents. The inspectors evaluated the licensees ability to identify, characterize, prioritize, and resolve the identified issues in accordance with licensee procedures PI-AA-104-1000, Corrective Action, Rev. 6, and 0-ADM-533, Corrective Action Program Guidance, Rev. 14.

Radiation protection program occupational dose assessment guidance and activities were evaluated against the requirements of the UFSAR Section 11; TS Sections 6.8.1, Procedures and Programs, and 6.12, High Radiation Area; 10 CFR Parts 19 and 20; and approved licensee procedures. Records reviewed are listed in the Attachment.

The inspectors completed all specified line-items detailed in IP 71124.04.

b. Findings

No findings were identified.

2RS5 Radiation Monitoring Instrumentation (IP 71124.05)

a. Inspection Scope

Radiation Monitoring Instrumentation: During tours of the auxiliary building, turbine building, SFP areas, and RCA exit point, the inspectors observed installed radiation detection equipment including the following instrument types: area radiation monitors (ARMs), airborne monitors, liquid and gaseous effluent monitors, PCMs, SAMs, and portal monitors. The inspectors observed the physical location of the components, and noted the material condition.

In addition to equipment walkdowns, the inspectors observed source checks and alarm setpoint testing of various portable and fixed detection instruments, including ion chambers, telepoles, PCMs, SAMs, and portal monitors. For the portable instruments, the inspectors observed the use of a high-range check source and reviewed records of periodic output value testing for a calibration source. The inspectors reviewed recent calibration records and evaluated alarm setpoint values for selected ARMs, PCMs, portal monitors, SAMs, effluent monitors, and a WBC. This included a sampling of instruments used for post-accident monitoring such as containment high-range ARMs and effluent monitor high-range noble gas and iodine channels. Radioactive sources used to calibrate selected ARMs and effluent monitors were evaluated for traceability to national standards. Calibration stickers on portable survey instruments and air samplers were noted during inspection of storage areas for ready-to-use equipment. The inspectors also reviewed countroom quality assurance records for gamma ray spectrometry equipment and liquid scintillation detectors.

Problem Identification and Resolution: Selected licensee CAP documents associated with instrumentation were reviewed and assessed. The inspectors evaluated the licensees ability to identify and resolve the identified issues in accordance with licensee procedures. The inspectors also reviewed recent self-assessment results.

Operability and reliability of selected radiation detection instruments were reviewed against details documented in the following: 10 CFR Part 20; NUREG-0737, Clarification of Three Mile Island Action Plan Requirements; TS Section 3; UFSAR Chapters 11; and applicable licensee procedures. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings were identified.

4OA1 Performance Indicator Verification (IP 71151)

.1 Barrier Integrity Cornerstone

a. Inspection Scope

The inspectors reviewed licensee submittals for the Unit 3 and 4 Performance Indicators (PI) listed below for the period October 1, 2014, through September 30, 2015, to verify the accuracy of the PI data reported during that period. Performance indicator definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedure 0-ADM-032, NRC Performance Indicators Turkey Point, were used to check the reporting for each data element. The inspectors checked operator logs, plant status reports, CRs, system health reports, and PI data sheets to verify that the licensee had identified the required data, as applicable. The inspectors interviewed licensee personnel associated with PI data collection, evaluation, and distribution.

Cornerstone: Mitigating Systems

  • High Pressure Injection System
  • Emergency AC Power System
  • Heat Removal System
  • Cooling Water System

b. Findings

No findings were identified.

.2 Radiation Safety Cornerstones

a. Inspection Scope

Occupational Radiation Safety Cornerstone: The inspectors reviewed recent Occupational Exposure Control Effectiveness PI results for the occupational radiation safety cornerstone, and reviewed PI records generated from October 2014 through October 2015. For the assessment period, the inspectors reviewed ED alarm logs and selected CRs related to controls for exposure significant areas. Documents reviewed are listed in the Attachment.

Public Radiation Safety Cornerstone: The inspectors reviewed recent radiological control effluent release occurrences PI results for the public radiation safety cornerstone, and reviewed PI records generated from October 2014 through October 2015. For the assessment period, the inspectors reviewed cumulative and projected doses to the public contained in liquid and gaseous release permits and CRs related to radiological effluent TS/Offsite Dose Calculation Manual issues. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (IP 71152)

.1 Daily Review

a. Inspection Scope

As required by IP 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensees CAP. This review was accomplished by reviewing daily printed summaries of ARs and by reviewing the licensees electronic AR database. Additionally, RCS unidentified leakage was checked on a daily basis to verify no substantive or unexplained changes. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

.2 Annual Sample: Missed Fire Watch Tours

a. Inspection Scope

The inspectors selected AR 02056905, Missed Fire Watch Tours for a more in-depth review of the circumstances and the corrective actions that followed. The AR report was reviewed to ensure that an appropriate evaluation was performed and corrective actions were specified and prioritized in accordance with the licensees program. Other attributes checked included disposition of operability and resolution of the problem, including cause determination, past operability determination, and corrective actions.

The inspectors interviewed plant personnel and evaluated the CR in accordance with the requirements of the licensees corrective actions process as specified in licensees procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action. This inspection constitutes one sample.

b. Findings and Observations

No inspector findings were identified. A licensee-identified violation of very low safety significance (Green) is documented in Section 4OA7 of this report. The licensee identified that employees failed to perform hourly required fire watch roves. The inspectors noted that the licensees evaluation for the missed fire watch roves concluded that there was no violation of any TS requirement since TS do not require fire watches for degraded fire protection features. The licensee concluded that the missed roves represented a reduction in the effectiveness of the Fire Protection Program (FPP) and the loss of a defense-in-depth feature.

The licensee determined the root cause of the event to be that operations management was not engaged with the fire watch program. The licensee also determined that a direct cause was that fire watch employees willfully chose non-compliance with fire protection requirements. Immediate corrective actions for this event included the immediate denial of site access for the individuals who failed to conduct the roves. The licensee also updated the fire protection procedure, 0-ADM-016.4, to include Operations Management Responsibilities and Oversight that requires observations, audits, and assessments to ensure regulatory requirements are met. The licensee also conducted an extent of condition and determined that no other missed tours were present in other departments based on data collected and security access logs.

.3 Semi-Annual Trend

a. Inspection Scope

The inspectors performed a review of the licensees records including ARs, CAP health reports, apparent cause evaluation reports, and various corrective action review board reports to asses an adverse trend in the performance of reactor protection transmitters.

The inspectors reviewed licensee AR 02088175, which identified an adverse trend in protection transmitter calibration check results. The inspectors evaluated the effectiveness of the licensees corrective actions and the significance of the problems, including attributes such as accurate documentation, reportability, evaluation, corrective actions, and problem resolution. This inspection constitutes one sample.

b. Findings and Observations

No inspector findings were identified. The licensee noted that the transmitters in question, Rosemount pressure transmitters, are expected to drift a slight amount. The licensee also noted that both the transmitter age and replacement of components tended to exacerbate the transmitter drift through the calibration cycle. The licensee concluded that even with the noted transmitter drift, the transmitters still performed satisfactorily and were within TS compliance. The inspectors did not identify any additional trends not observed by the licensees trending activities.

4OA5 Other Activities

.1 Independent Spent Fuel Storage Facility Walk down (IP 60855.1)

a. Inspection Scope

On December 17, 2015, the inspector conducted a walk down of the ISFSI protected area per IP 60855.1, Operation of an ISFSI at Operating Plants. The inspectors observed each cask building temperature indicator and passive ventilation system to be free of any obstruction, allowing natural draft convection decay heat removal through the air inlet and air outlet openings. The inspectors observed associated cask building structures to be structurally intact and radiation protection access and security controls to the ISFSI area to be satisfactory.

b. Findings

No findings were identified.

4OA6 Meetings

The resident inspectors presented the inspection results to Mr. Tom Summers and other members of licensee management on January 15, 2016. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information.

4OA7 Licensee-identified Violation

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for being dispositioned as an NCV.

10 CFR 50.48 states that each operating nuclear power plant must have a fire protection plan that satisfies Criterion 3 of Appendix A of this part. Turkey Point Renewed Operating License condition D, for Units 3 and 4, states that the licensee shall implement and maintain in effect all provisions of the approved FPP as described in the UFSAR Appendix 9.6A. The approved FPP is implemented, in part, by 0-ADM-016, Fire Protection Program, as referenced in Section 7.2 of UFSAR Appendix 9.6A. Section 5.6 of 0-ADM-016 requires that, for non-functional post-fire safe shutdown components, engineering evaluations should identify appropriate compensatory actions, including hourly fire roves. Contrary to the above, between May 1st, 2014, and April 23rd, 2015, hourly fire watch patrols were not conducted on numerous occasions in fire zones that required regular hourly tours due to fire protection equipment impairment. The failure to perform the fire watch tours did not cause the inoperability of any equipment but resulted in the loss of a defense-in-depth feature for fire detection in fire zones affected by an impaired or non-functional fire safety component or feature. This violation was associated with the Mitigating Systems Cornerstone and affected the cornerstone objective of ensuring the availability, reliability and capability of the systems that respond to initiating events to prevent undesirable consequences. The inspectors determined the finding to be of very low safety significance (Green) after performing a detailed risk evaluation in accordance with Manual Chapter 0609, Appendix A, because the missed fire watch tours reflected a low degradation of the Fire Prevention and Administrative Controls FPP element in that other area fire protection defense-in-depth features such as automatic fire detection (smoke detectors), automatic fire suppression capability (sprinklers), manual suppression capability (fire brigade), and safe shutdown capability from the main control room were still available. The licensee entered this violation into their CAP as AR 02056905.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

F. Banks, Quality Manager
C. Cashwell, Training Manager
P. Czaya, Licensing
C. Domingos, Plant General Manager
T. Eck, Security Manager
M. Guth, Licensing Manager
O. Hanek, Licensing Engineer
A. Katz, Projects Manager
G. Melin, Operations Manager
S. Mihalakea, Licensing
K. Ohara, Emergency Preparedness Manager
J. Pallin, Engineering Director
D. Sluszka, Work Controls Manager
B. Stamp, Operations Director
T. Summers, Site Vice-President
D. Barrow, Maintenance Director
R. Hess, General Operations Training Supervisor
M. Wilson, Operations Training Supervisor

NRC Personnel

B. Bishop, Senior Project Engineer
A. Beaston, Project Engineer
A. Vargas, Project Engineer

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000251/2015004-01 NCV Failure to correctly follow procedure 3-PMI-072.6, Steam Dump to Atmosphere Control Loop Calibration.

(Section 1R20)

LIST OF DOCUMENTS REVIEWED