IR 05000424/2014003: Difference between revisions
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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 August 6, 2014 | {{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION | ||
==REGION II== | |||
245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 August 6, 2014 | |||
EA-14-112 Mr. Dennis Madison | EA-14-112 Mr. Dennis Madison | ||
Line 160: | Line 163: | ||
Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
Sincerely,/RA/ Joel T. Munday, Director | Sincerely, | ||
/RA/ Joel T. Munday, Director | |||
Division of Reactor Projects | Division of Reactor Projects | ||
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Docket Nos.: 05000424, 05000425 License Nos.: NPF-68 and NPF-81 | Docket Nos.: 05000424, 05000425 License Nos.: NPF-68 and NPF-81 | ||
Enclosures: | |||
1. Inspection Report 05000424/2014003 and 05000425/2014003 | 1. Inspection Report 05000424/2014003 and 05000425/2014003 | ||
w/Attachment: Supplemental Information 2. Notice of Violation | |||
Supplemental Information 2. Notice of Violation | |||
cc Distribution via ListServ | cc Distribution via ListServ | ||
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PUBLIC RidsNrrPMVogtle Resource | PUBLIC RidsNrrPMVogtle Resource | ||
Enclosure 1 U. S. NUCLEAR REGULATORY COMMISSION REGION II Docket Nos.: 50-424, 50-425 | Enclosure 1 U. S. NUCLEAR REGULATORY COMMISSION | ||
==REGION II== | |||
Docket Nos.: 50-424, 50-425 | |||
License Nos.: NPF-68, NPF-81 | License Nos.: NPF-68, NPF-81 | ||
Line 803: | Line 810: | ||
No findings were identified. | No findings were identified. | ||
===Cornerstone:=== | ===Cornerstone: Emergency Preparedness=== | ||
{{a|1EP6}} | {{a|1EP6}} | ||
==1EP6 Drill Evaluation== | ==1EP6 Drill Evaluation== | ||
Line 1,285: | Line 1,291: | ||
data. Documents reviewed are listed in the Attachment. | data. Documents reviewed are listed in the Attachment. | ||
===Cornerstone:=== | ===Cornerstone: Barrier Integrity=== | ||
* reactor coolant system leak rate | * reactor coolant system leak rate | ||
* reactor coolant system specific activity | * reactor coolant system specific activity | ||
===Cornerstone:=== | ===Cornerstone: Occupational Radiation Safety=== | ||
The inspectors reviewed the occupational exposure control effectiveness PI results for | The inspectors reviewed the occupational exposure control effectiveness PI results for | ||
Line 1,303: | Line 1,307: | ||
report Attachment. | report Attachment. | ||
===Cornerstone: | ===Cornerstone: Public Radiation Safety:=== | ||
Public Radiation Safety: | |||
The inspectors reviewed the radiological control effluent release occurrences PI results | The inspectors reviewed the radiological control effluent release occurrences PI results |
Revision as of 09:45, 11 May 2019
ML14218A669 | |
Person / Time | |
---|---|
Site: | Vogtle |
Issue date: | 08/06/2014 |
From: | Munday J T Division Reactor Projects II |
To: | Madison D Southern Nuclear Operating Co |
References | |
EA-14-112 IR-14-003 | |
Download: ML14218A669 (50) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION
REGION II
245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 August 6, 2014
EA-14-112 Mr. Dennis Madison
Vice President - Vogtle
Southern Nuclear Operating Company, Inc.
Vogtle Electric Generating Plant
7821 River Road
Waynesboro, GA 30830
SUBJECT: VOGTLE ELECTRIC GENERATING PLANT - NRC INTEGRATED INSPECTION REPORT 05000424/2014003 AND 05000425/2014003, AND NOTICE OF
VIOLATION
Dear Mr. Madison:
On June 30, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
your Vogtle Electric Generating Plant, Units 1 and 2. On July 25, 2014, the NRC inspectors
discussed the results of this inspection with Mr. Tom Tynan and other members of the Vogtle
staff. Inspectors documented the results of this inspection in the enclosed inspection report.
The enclosed inspection report discusses a finding of low to moderate safety significance (White). As described in Section 4OA2.3 of the enclosed inspection report, a calculation error
resulted in the radiological threshold values for the RG1 (General Emergency) and RS1 (Site
Area Emergency) emergency action levels to be sixty times greater than the appropriate values.
This finding resulted in a potential safety concern for which appropriate immediate corrective
actions were taken. The correct threshold values were provided to the appropriate operations
staff decision makers which resolved the concern. The licensee took additional corrective
actions, including performing a causal determination, processing formal changes to the station's
emergency plan and associated implementing procedures, and performing extent of
condition/cause reviews throughout the Southern Nuclear Operating Company fleet. Following
the internal review process, the revised emergency plan and associated implementing
procedure were provided to the NRC.
In a telephone conversation on July 3, 2014, Mr. Brian Bonser, Chief, Plant Support Branch, Division of Reactor Safety, Region II, informed Mr. Tynan of the details of the preliminary
finding, the apparent violation, and advised Vogtle representatives that the finding satisfied the
"old design issue" criteria contained in NRC Inspection Manual Chapter 0305, "Operating
Reactor Assessment Program," Section 11.05, "Treatment of Items Associated with Enforcement Discretion," dated October 18, 2013.
The intent of this section is to establish reactor oversight process (ROP) guidance that supports the objective of enforcement discretion, which is to encourage licensee initiatives to identify and resolve problems, especially issues that are not likely to be identified by routine efforts. Additionally, Mr. Bonser advised Mr. Tynan that
based on the above, the NRC had sufficient information, including Vogtle's corrective actions, to
make a final significance determination and enforcement decision without the need for a
regulatory conference or a written response from you. Mr. Tynan indicated they did not believe
that a regulatory conference or written response was necessary.
Based on the above, the NRC has concluded that the finding is appropriately characterized as
White, a finding of low to moderate safety significance. Additionally, the NRC determined that
the White finding meets the criteria specified in IMC 0305 for treatment as an "old design issue."
The basis for the NRC's determination included the following: (1) the issue was licensee-
identified through an extent of condition review prompted by Southern Co. fleet operating
experience; (2) the issue was corrected within a reasonable time after discovery; (3) the issue
was not likely to be previously identified by recent ongoing licensee efforts; and (4) the issue
was not reflective of a current performance deficiency associated with existing programs, policy, or procedures. Therefore, in accordance with IMC 0305, the performance issue will not
aggregate in the Action Matrix with other performance indicators and inspection findings. Note
IMC 0305 specifies the need for an inspection in accordance with inspection procedure (IP)
95001 "Supplemental Inspection for One or Two White Inputs in a Strategic Performance Area,"
to review the licensee's root cause and corrective action plans even if the White finding meets
the criteria for treatment as an old design issue. The White finding will remain open until IP
95001 is completed.
The NRC has also determined that the failure to maintain the effectiveness of your emergency
plan is a violation of 10 CFR Part 50.54(q)(2), as cited in the attached Notice of Violation (Notice). The circumstances surrounding the violation are described in detail in the enclosed
inspection report. In accordance with the NRC Enforcement Policy, the Notice is considered
escalated enforcement action because it is associated with a White finding.
The NRC has concluded that the information regarding the reason of the violation, the corrective
actions taken to correct the violation and prevent recurrence, and the date when full compliance
was achieved is already adequately addressed on the docket in the enclosed inspection report.
Therefore, you are not required to respond to this letter unless the description therein does not
accurately reflect your corrective actions or your position.
NRC inspectors also documented three findings of very low safety significance (Green)
identified during this inspection period. These findings involved violations of NRC requirements.
The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with
copies to the Regional Administrator, Region II; the Director, Office of Enforcement, U.S Nuclear
Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the
Vogtle Electric Generating Plant. If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region II; and the NRC resident inspector at the
Vogtle Electric Generating Plant.
In accordance with Title 10 of the Code of Federal Regulations 2.390, "Public Inspections, Exemptions, Requests for Withholding," of the NRC's "Agency Rules of Practice and
Procedure," a copy of this letter, its enclosu res, and your response (if any) will be available electronically for public inspection in the NRC P ublic Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Document Access and
Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/ Joel T. Munday, Director
Division of Reactor Projects
Docket Nos.: 05000424, 05000425 License Nos.: NPF-68 and NPF-81
Enclosures:
1. Inspection Report 05000424/2014003 and 05000425/2014003
w/Attachment: Supplemental Information 2. Notice of Violation
cc Distribution via ListServ
_____ ________ SUNSI REVIEW COMPLETE FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS SIGNATURE Via email Via email Via email Via email Via email Via email Via email NAME MCain TChandler WPursley A Nielsen WLoo CDykes MSpeck DATE 7/11/2014 7/24/2014 7/14/2014 7/14/2014 7/24/2014 7/24/2014 7/15/2014 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:DRS RII:DRS RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP SIGNATURE Via email Via email JGW /RA/ AXA /RA/ FJE /RA/ MSL /RA/ JTM /RA/ NAME SSanchez GOttenberg JWorosilo AAlen FEhrhardt MLesser JMunday DATE 7/14/2014 7/14/2014 7/22/2014 7/22/2014 8/4/2014 8/4/2014 8/6/2014 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:EICS SIGNATURE SAP /RA/ NAME SPrice DATE 8/1/2014 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO Letter to Dennis Madison from Joel T. Munday dated August 6, 2014.
SUBJECT: VOGTLE ELECTRIC GENERATING PLANT - NRC INTEGRATED INSPECTION REPORT 05000424/2014003 AND 05000425/2014003, AND NOTICE OF
VIOLATION
DISTRIBUTION
- D. Gamberoni, RII
L. Douglas, RII
OE Mail RIDSNRRDIRS
PUBLIC RidsNrrPMVogtle Resource
Enclosure 1 U. S. NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos.: 50-424, 50-425
Report Nos.: 05000424/2014003 and 05000425/2014003
Licensee: Southern Nuclear Operating Company, Inc. (SNC)
Facility: Vogtle Electric Generating Plant, Units 1 and 2
Location: Waynesboro, GA 30830
Dates: April 1, 2014, through June 30, 2014
Inspectors: M. Cain, Senior Resident Inspector T. Chandler, Resident Inspector A. Alen, Project Engineer W. Pursley, Health Physics Inspector (2RS1, 2RS2, 2RS4, 4OA1) A. Nielsen, Senior Health Physicist (2RS1, 2RS3, 4OA1)
W. Loo, Senior Health Physicist (2RS1, 2RS3)
C. Dykes, Health Physicist (2RS5) M. Speck, Senior Emergency Preparedness Inspector (4OA2.3) S. Sanchez, Senior Emergency Preparedness Inspector
(4OA2.3) G. Ottenberg, Senior Reactor Inspector (4OA5)
Approved by: Frank Ehrhardt, Chief Reactor Projects Branch 2
Division of Reactor Projects Enclosure 1
SUMMARY OF FINDINGS
IR 05000424/2014003, 05000425/2014003; 04/01/2014 - 06/30/2014; Vogtle Electric
Generating Plant, Units 1 and 2; Maintenance Effectiveness, Radiological Hazard
Assessment and Exposure Controls, Identification and Resolution of Problems, Event
Follow-up The report covered a 3-month period of inspection by resident inspectors and regional inspectors. There was one NRC-identified and three self-revealing violations identified and documented in this report. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using
Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP)
dated June 2, 2011. The cross-cutting aspects are determined using IMC 0310,
"Aspects within the Cross-Cutting Areas" dated December 19, 2013. All violations of
NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy dated January 28, 2013. The NRC's program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight
Process," Revision 5.
Cornerstone: Initiating Events
Green A self-revealing non-cited violation (NCV) of 10 CFR 50 Appendix B Criterion V, "Instructions, Procedures, and Drawings," was identified for failure to provide adequate work instructions in the maintenance procedure used for main steam isolation valve (MSIV) maintenance. Specifically, maintenance procedure 26854-C, "Main Steam
Isolation Valve Actuator Maintenance," used to perform maintenance on Rockwell
MSIV(s), did not provide adequate instructions for installing the lower manifold/cylinder
O-ring during reassembly. This resulted in a 'pinched' O-ring on 1HV3006B, a subsequent failure of the O-ring causing the MSIV to fail closed, and a manual reactor trip. The licensee conducted a root cause investigation and entered the event into their corrective action program (condition report (CR) 800018). The licensee replaced the O-
ring, performed an extent of condition evaluation for all other MSIVs, and revised the maintenance procedure to include specific instructions for the installation of the lower manifold/cylinder O-ring.
The finding was more than minor because it was associated with the procedure quality attribute of the reactor safety - initiating events cornerstone and it adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.
Specifically, the failure to provide an adequate procedure with adequate instructions for ensuring proper O-ring installation resulted in the failure of the Unit 1 loop 1 outboard
MSIV hydraulic actuator causing the loop 1 MSIV to fail closed and a subsequent manual reactor trip due to lowering steam generator water level. Because the inspectors answered "No" to all of the IMC 0609 Appendix A (dated June 19, 2012) Exhibit 1,
Section B, "Initiating Events Screening Questions," the inspectors concluded that the finding was of very low safety significance (Green). The inspectors determined the finding had a cross-cutting aspect of "resources" in the human performance area, because the maintenance procedure used to install manifold/cylinder O-ring did not provide adequate instructions for the proper installation of the O-ring. [H.1] (Section 1R12)
Green A self-revealing NCV of 10 CFR 50 Appendix B Criterion V, "Instructions, Procedures, and Drawings," was identified for failure to provide adequate work instructions as well as failure to follow the maintenance procedure used to install flexible and rigid conduit. Specifically, the work instructions did not provide adequate directions and/or precautions to properly slope conduit during installation to prevent water intrusion into a valve positioner. The work instructions referenced maintenance procedure 25008-
C, "Flexible and Rigid Conduit Installation." The maintenance procedure referenced Vogtle design specification X3AR01 Section E-8, "Raceway Systems," which provided sloping and tightness criteria for conduit installations. The licensee conducted a root cause investigation and entered the event into their corrective action program (CR 797929). The licensee repaired the improperly sloped conduit, replaced the positioner, and revised procedure 25008-C to specify standards for proper sloping of conduits.
The finding was more than minor because it was associated with the procedure quality and human performance attributes of the reactor safety - initiating events cornerstone and it adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the failure to provide adequate work instructions as well as failure to follow procedure 25008-C, "Flexible and Rigid Conduit Installation," resulted in the Unit 2 loop 3 main feedwater regulating valve (MFRV) positioner failing closed, causing a subsequent automatic reactor trip due to low-low steam generator (SG) water level. Because the inspectors answered "No" to all of the IMC 0609 Appendix A (dated
June 19, 2012) Exhibit 1, Section B, "Initiating Events Screening Questions," the inspectors concluded that the finding was of very low safety significance (Green). The inspectors determined that the finding had a cross-cutting aspect of "procedure adherence" in the human performance area because the maintenance electricians did not follow Vogtle design specification procedures or drawings resulting in the improper sloping of the MFRV flexible conduit [H.8] (Section 40A3)
Cornerstone: Occupational Radiation Safety
Green A self-revealing NCV of Technical Specification (TS) 5.7.1, "High Radiation Area", was identified for an entry into a high radiation area (HRA) without meeting the entry requirements as specified therein. Specifically, on March 17, 2014, an operator was authorized to enter an HRA on Unit 1 under conditions where dose rates were known to be changing. This allowed the operator entry into an HRA without knowledge of actual radiological conditions. He was not provided with a radiation monitoring device that continuously indicated dose rates in the area, nor was he accompanied by an individual qualified in radiation protection procedures with a radiation monitoring device providing positive control over his activities. Upon discovery of the condition, the licensee secured access to the area, performed follow-up surveys and convened a human performance review board to examine causal factors and identify corrective actions. The licensee entered this issue into the corrective action program as CR 787908. This finding was more than minor because it was associated with the occupational radiation safety cornerstone attribute of human performance and adversely affects the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. Specifically, workers permitted entry into HRAs with inadequate knowledge of current radiological conditions could receive unintended occupational exposures. The finding was evaluated using IMC 0609, Appendix C, "Occupational Radiation Safety
Significance Determination Process (SDP)", dated August 19, 2008. The finding was not related to As Low As Reasonably Achievable (ALARA) planning, nor did it involve an overexposure or substantial potential for overexposure and the ability to assess dose was not compromised. Therefore, the finding was determined to be of very low safety significance (Green). This finding had a cross-cutting aspect of "avoid complacency" in the human performance area because health physics (HP) personnel failed to verify plant conditions through available means when an evolution was in progress that was known to increase area dose rates prior to authorizing entry into an HRA. [H.12] (Section 2RS1)
Cornerstone: Emergency Preparedness
White: A finding and associated violation of 10 CFR 50.54(q)(2) was identified by the licensee for the failure to follow and maintain the effectiveness of emergency plans which use a standard emergency classification and action level scheme. Specifically, the licensee's emergency plan emergency action level (EAL) Category R - Abnormal
Radiological RG1 (General Emergency) and RS1(Site Area Emergency) specified threshold values which were sixty times too high due to a calculation error. As immediate corrective action, the licensee provided the corrected threshold values to appropriate management and decision-makers (shift managers/emergency directors).
The licensee entered this issue into the corrective action program as CR 648248.
The performance deficiency was determined to be more than minor because it was associated with the emergency preparedness cornerstone attribute of procedure quality.
It impacted the cornerstone objective because it was associated with inappropriate EAL and emergency plan changes and their adequacy to protect the health and safety of the public in the event of a radiological emergency. Specifically, the licensee's ability to declare a Site Area Emergency and General Emergency based on effluent radiation monitor values was degraded in that event classification using these radiation monitors would be delayed. The finding was assessed for significance in accordance with NRC
Manual Chapter 0609, Appendix B, "Emergency Preparedness Significance
Determination Process," which states, "Failure to comply means that a program is noncompliant with a Regulatory requirement." The inspector determined that the issue of concern constituted a degraded rather than lost risk-significant planning standard (RSPS). The issue of concern was similar to the example in Table 5.4.1 (Degraded
RSPS) and was determined to be of low to moderate safety significance (White). The violation was determined to meet the IMC 0305 criteria for enforcement discretion as an old design issue. A cross-cutting aspect was not assigned based on the elapsed time since the performance deficiency occurred and because the inspectors determined it was not reflective of current licensee performance. (Section 4OA2)
REPORT DETAILS
Summary of Plant Status
Unit 1 started the reporting period shut down for a planned refueling outage. Operators
restarted the unit on April 11, 2014, and attained 100 percent rated thermal power (RTP) on
April 12, 2014. Operators manually tripped the unit on April 12, 2014, due to a failure of the
loop 1 main steam isolation valve (MSIV) failing closed at 100 percent RTP. Operators
restarted the unit on April 13, 2014 and attained 100 percent RTP on April 27, 2014. The unit
operated at essentially RTP for the rest of the inspection period.
Unit 2 started the report period at full RTP. The unit automatically tripped from 100 percent RTP
on April 8, 2014, due to low level in the loop 3 steam generator caused by the main feedwater
regulator valve (MFRV) failing closed. Operators restarted the unit on April 10, 2014, and
attained 100 percent power on April 11, 2014.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R01 Adverse Weather Protection
a. Inspection Scope
.1 Summer Readiness of Offsite and Alternate AC Power System
Because the licensee implemented modifications to the high and low voltage
switchyards, the inspectors reviewed the licensee's procedures for operation and
continued availability of offsite and onsite alternate AC power systems. The inspectors
also reviewed the communications protocols between the transmission system operator
and the licensee to verify that the appropriate information is exchanged when issues
arise that could affect the offsite power system.
The inspectors reviewed the material condition of offsite and onsite alternate AC power
systems (including switchyard and transform ers) by performing a walkdown of the switchyard. The inspectors reviewed outstanding work orders and assessed corrective
actions for any degraded conditions that impacted plant risk or required compensatory
actions. Documents reviewed are listed in the Attachment.
.2 Seasonal Extreme Weather Conditions
The inspectors conducted a detailed review of the station's adverse weather procedures
written for extreme high temperatures. The inspectors verified that weather related
equipment deficiencies identified during the previous year had been placed into the work
control process and/or corrected before the onset of seasonal extremes. The inspectors
evaluated the licensee's implementation of adverse weather preparation procedures and compensatory measures before the onset of seasonal extreme weather conditions.
Documents reviewed are listed in the Attachment.
The inspectors evaluated the following risk-significant systems:
- Unit 2 nuclear service cooling water (NSCW) system (both trains)
- Unit 1 emergency diesel generator (EDG) system (both trains)
b. Findings
No findings were identified.
1R04 Equipment Alignment
a. Inspection Scope
Partial Walkdown
The inspectors verified that critical portions of the selected systems were correctly
aligned by performing partial walkdowns. The inspectors selected systems for
assessment because they were a redundant or ba ckup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a
single-train system. The inspectors determi ned the correct system lineup by reviewing plant procedures and drawings. Documents reviewed are listed in the Attachment.
The inspectors selected the following four systems or trains to inspect:
- Unit 2 train "B" motor-driven auxiliary f eedwater system and the train "C" turbine-driven auxiliary feedwater system duri ng the train "A" EDG planned maintenance outage
- Unit 2 train "A" motor-driven auxiliary f eedwater system and the train "C" turbine-driven auxiliary feedwater system duri ng the train "B" EDG planned maintenance outage
b. Findings
No findings were identified.
1R05 Fire Protection
a. Inspection Scope
Quarterly Inspection The inspectors evaluated the adequacy of selected fire plans by comparing the fire plans
to the defined hazards and defense-in-depth features specified in the fire protection
program. In evaluating the fire plans, the inspectors assessed the following items:
- control of transient combustibles and ignition sources
- fire detection systems
- water-based fire suppression systems
- gaseous fire suppression systems
- manual firefighting equipment and capability
- passive fire protection features
- compensatory measures and fire watches
- issues related to fire protection contained in the licensee's corrective action program
The inspectors toured the following five fire areas to assess material condition and
operational status of fire protection equipment. Documents reviewed are listed in the
.
- Unit 2 component cooling water (CCW) heat exchanger rooms, fire zones 54, 55, 148, 23, 172, and 147
- Unit 1 centrifugal charging pump (CCP) rooms and the level "C" pipe penetration area in the Unit 1 auxiliary building, fire zones 14B, 19, 20, and 21
- Unit 2 control building level "A" west and east penetration areas, fire zones 87, 88, 89, 90 93, 102, 158 and 159.
- Unit 1 "B" train EDG building, fire zones 162 and 164
- Unit 2 auxiliary feedwater pump house, fire zones 155, 156, 157A and 157B
b. Findings
No findings were identified.
1R06 Flood Protection Measures
a. Inspection Scope
.1 Internal Flooding
The inspectors reviewed related flood analysis documents and walked down the area
listed below containing risk-significant stru ctures, systems, and components susceptible to flooding. The inspectors verified that plant design features and plant procedures for
flood mitigation were consistent with design requirements and internal flooding analysis
assumptions. The inspectors also assessed the condition of flood protection barriers
and drain systems. In addition, the inspectors verified the licensee was identifying and
properly addressing issues using the correct ive action program. Documents reviewed are listed in the Attachment.
- Unit 1 residual heat removal (RHR) and containment spray (CS) pump rooms (both trains) in auxiliary building 1 1R11 Licensed Operator Requalification Pr ogram and Licensed Operator Performance (71111.11)
a. Inspection Scope
.1 Resident Inspector Quarterly Review of Licensed Operator Requalification
The inspectors observed an evaluated simulator scenario administered to an operating
crew conducted in accordance with the licensee's accredited requalification training
program.
The inspectors assessed the following:
- licensed operator performance
- the ability of the licensee to administer the scenario and evaluate the operators
- the quality of the post-scenario critique
- simulator performance Documents reviewed are listed in the Attachment.
.2 Resident Inspector Quarterly Review of Licensed Operator Performance
The inspectors observed licensed operator performance in the main control room on
April 9, 2014, while operators were starting up the Unit 2 reactor.
The inspectors assessed the following:
- use of plant procedures
- control board manipulations
- communications between crew members
- use and interpretation of instruments, indications, and alarms
- use of human error prevention techniques
- documentation of activities
- management and supervision Documents reviewed are listed in the Attachment.
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors assessed the licensee's treatment of the two issues listed below in order
to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants".) The inspectors reviewed procedures and
records in order to evaluate the licensee's identification, assessment, and
characterization of the problems as well as their corrective actions for returning the
equipment to a satisfactory condition. The in spectors also interviewed system engineers and the maintenance rule coordinator to assess the accuracy of performance
deficiencies and extent of condition. Documents reviewed are listed in the Attachment.
- Unit 2, system 1305, 2HV5230 hydraulic leak
- Unit 1, system 1301, 1HV3006B maintenanc e preventable functional failure (MPFF)
b. Findings
Introduction
- A Green, self-revealing NCV of 10 CFR 50 Appendix B Criterion V, "Instructions, Procedures, and Drawings," was identified for failure to provide adequate
work instructions in the maintenance procedure used to reassemble Rockwell MSIVs.
Specifically, maintenance procedure 26854-C, "Main Steam Isolation Valve Actuator
Maintenance," which is used to perform maintenance on Rockwell MSIVs, did not
provide adequate instructions for installing of the lower manifold/cylinder O-ring during
reassembly using threaded guide rods to align the mating surfaces.
Description
- On April 12, 2014, Unit 1 was in Mode 1 ascending in power after the 1R18 refueling outage. At approximately 20:08, control room operators received an MSIV
actuator trouble alarm followed by the MSIV not fully open indication. Control room
operators identified lowering loop 1 steam generator (SG) #1 level and steam flow and
manually tripped Unit 1 at about 28 percent reactor power. Upon further investigation, operators discovered a severe leak on the loop 1 outboard MSIV hydraulic actuator, which had caused the valve to close. Operators stabilized the plant in Mode 3 and all
safety related equipment responded as expected. The licensee assembled an issue
response team (IRT) and a root cause team to investigate the cause of the hydraulic
leak and subsequent manual reactor trip and to determine the required corrective
actions. Further investigation revealed that the manifold to cylinder O-ring on the valve
actuator had failed catastrophically due to being pinched during actuator reassembly in
2012. Further research by the root cause team revealed that maintenance personnel
relied on "skill of the craft" to install the O-ring and used a hoist to align the cylinder with
the manifold body. Use of the hoist resulted in rotational and/or oscillatory movement of
the mating surfaces, pinching the O-ring. The maintenance procedure that the
mechanics used to reassemble the actuator did not contain adequate instructions for
installing the manifold/cylinder O-ring. Specifically, maintenance procedure 26854-C, "Main Steam Isolation Valve Actuator Maintenance," which is used to perform
maintenance on Rockwell MSIVs, did not provide adequate instructions for installing the
lower manifold/cylinder O-ring during reassembly using threaded guide rods to align the
mating surfaces. The licensee revised the maintenance procedure, replaced the O-ring, and conducted an extent of condition evaluation of all other MSIV actuators. The
licensee entered this issue into their corrective action program as CR 800018.
Analysis:
The failure to provide adequate procedures required by 10 CFR 50 Appendix B Criterion V was a performance deficiency. The inspectors determined that the
performance deficiency was more than minor because it was associated with the
procedure quality attribute of the initiating events cornerstone and it adversely affected
the cornerstone objective to limit the likelihood of events that upset plant stability and
challenge critical safety functions during shutdown as well as power operations.
Specifically, the failure to provide adequate instructions for the installation of the
manifold to cylinder O-ring resulted in failure of the loop 1 MSIV and a subsequent
manual reactor trip due to lowering SG water level and steam flow. The inspectors
evaluated the finding using IMC 0609, Appendix A, "The Significance Determination
Process (SDP) for Findings At-Power," dated June 19, 2012. Because the inspectors
answered "No" to all the Exhibit 1, Section B, "Initiating Events Screening Questions,"
the inspectors determined that the finding was of very low safety significance (Green).
The inspectors determined the finding had a cross-cutting aspect of "resources" in the
human performance area, because the maintenance procedure used to install
manifold/cylinder O-ring did not provide adequate instructions for the proper installation
of the O-ring. [H.1]
Enforcement
- 10 CFR 50 Appendix B Criterion V, "Instructions, Procedures, and Drawings," requires, in part, that procedures shall include appropriate quantitative or
qualitative acceptance criteria for determining that important activities have been
satisfactorily accomplished. Contrary to the above, the maintenance procedure used to
reassemble the MSIV hydraulic actuator did not provide adequate instructions for the
proper alignment of the manifold to cylinder mating surfaces resulting in a pinched O-
ring and subsequent MSIV actuator failure. Specifically, maintenance procedure 26854-
C, "Main Steam Isolation Valve Actuator Maintenance," which is used to perform
maintenance on Rockwell MSIVs, did not provide adequate instructions for installing the
lower manifold/cylinder O-ring during reassembly. To restore compliance, the licensee
revised the maintenance procedure, replaced the O-ring, and conducted an extent of
condition evaluation of all other MSIV actuators. This violation is being treated as an
NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. The violation was
entered into the licensee's corrective action program as CR 800018. (NCV
05000424/2014003-01, "Inadequate Maintenance Procedure Results in a Failed MSIV
and a Manual Reactor Trip")
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the five maintenance activities listed below to verify that the
licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and
licensee procedures. The inspectors assessed the adequacy of the licensee's risk
assessments and implementation of risk management actions. The inspectors also
verified that the licensee was identifying and resolving problems with assessing and
managing maintenance-related risk using the corrective action program. Additionally, for
maintenance resulting from unforeseen situations, the inspectors assessed the
effectiveness of the licensee's planning and control of emergent work activities.
Documents reviewed are listed in the Attachment.
- Unit 2, week of May 5, 2014, Yellow risk condition associated with the extended allowed outage time (AOT) of the Unit 2 "A" EDG
- Unit 2, week of May 12, 2014, Orange risk condition associated with the extended AOT of the Unit 2 "A" EDG
- Unit 1, week of May 19, Yellow risk condition associated with the extended AOT of the Unit 1 "A" NSCW cooling tower fan #3
- Unit 1, week of June 2, 2014, during a planned maintenance outage of "1A" CCW pump in conjunction with an unplanned inoperability of the Unit 1A control room
emergency fan system (CREFS)
- Unit 2, week of June 16, 2014, Yellow risk condition associated with the extended AOT of the Unit 2 "B" EDG
b. Findings
No findings were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors selected the five operability determinations or functionality evaluations
listed below for review based on the risk-significance of the associated components and
systems. The inspectors reviewed the technical adequacy of the determinations to
ensure that technical specification operability was properly justified and the components
or systems remained capable of performing their design functions. To verify whether
components or systems were operable, the inspectors compared the operability and
design criteria in the appropriate sections of the technical specification and updated final
safety analysis report to the licensee's evaluations. Where compensatory measures
were required to maintain operability, the inspectors determined whether the measures
in place would function as intended and were properly controlled. Additionally, the
inspectors reviewed a sample of corrective action documents to verify the licensee was
identifying and correcting any deficiencies associated with operability evaluations.
Documents reviewed are listed in the Attachment.
- CR 776584, Unknown chemical buildup on top of upper motor windings
- CR 808990, "2B" EDG jacket water leak
- CR 805473/CAR 210188, 1HV3036A MSIV control board red light flickering
- CR 807567/CAR 210214, Unit 2 turbine driven auxiliary feedwater pump (TDAFW)controller output reading low
- CR 607966, U1 CCW Pump "1A" inboard bearing over 160 degrees Fahrenheit
b. Findings
No findings were identified.
1R18 Plant Modifications
a. Inspection Scope
The inspectors verified that the two plant modifications listed below did not affect the
safety functions of important safety systems.
The inspectors confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk
significant structures, systems, and components. The inspectors also verified
modifications performed during plant configurations involving increased risk did not
place the plant in an unsafe condition. Additionally, the inspectors evaluated whether
system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training
materials, complied with licensee standards and NRC requirements. In addition, the
inspectors reviewed a sample of related corrective action documents to verify the
licensee was identifying and correcting any deficiencies associated with modifications.
Documents reviewed are listed in the Attachment.
- SNC417397, Temporary modification to install accelerometers and a pressure transducer on chemical volume control system (CVCS) letdown lines, Unit 1
b. Findings
No findings were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors either observed post-maintenance testing or reviewed the test results for
the six maintenance activities listed below to verify the work performed was completed
correctly and the test activities were adequate to verify system operability and functional
capability.
- Maintenance Work Order (MWO) SNC137725 - Replacement of "1E" D26 relays MCC21805S3ABE
- MWO SNC413540 - 2PV3020 Replace A/B solenoid
- MWOs SNC408041 - (1A NSCW Fan 2) - Replace agastat relay and SNC383989 -
(1A NSCW Fan 2) - Replace rubber bushings on fan couplings
- MWO SNC525486 - Unit "2A" EDG Undervoltage relay calibration
- MWO SNC516991 - Unit 1 delta T/Tavg loop 3 protection channel operational test and calibration
- MWO SNC488414 - Unit 2 delta T/Tavg loop 1 protection channel I 2T-411 operational test and calibration The inspectors evaluated these activities for the following:
- Acceptance criteria were clear and demonstrated operational readiness.
- Effects of testing on the plant were adequately addressed.
- Test instrumentation was appropriate.
- Tests were performed in accordance with approved procedures.
- Equipment was returned to its operational status following testing.
- Test documentation was properly evaluated.
Additionally, the inspectors reviewed a sample of corrective action documents to verify
the licensee was identifying and correcting any deficiencies associated with post-
maintenance testing. Documents reviewed are listed in the Attachment.
b. Findings
No findings were identified.
1R20 Refueling and Other Outage Activities
a. Inspection Scope
For the Unit 1 refueling outage which continued from April 1 2014, through April 27 2014, the inspectors evaluated the following outage activities:
- outage planning
- heatup, and startup
- reactor coolant system instrumentation and electrical power configuration
- reactivity and inventory control
- decay heat removal and spent fuel pool cooling system operation
- containment closure The inspectors verified that the licensee:
- considered risk in developing the outage schedule
- controlled plant configuration in accordance with administrative risk reduction methodologies
- developed work schedules to manage fatigue
- developed mitigation strategies for loss of key safety functions
- adhered to operating license and technical specification requirements
Inspectors verified that safety-related and risk-significant structures, systems, and
components not accessible during power operations were maintained in an operable
condition. The inspectors also reviewed a sample of related corrective action
documents to verify the licensee was identifying and correcting any deficiencies
associated with outage activities. Documents reviewed are listed in the Attachment.
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the seven surveillance tests listed below and either observed
the test or reviewed test results to verify testing adequately demonstrated equipment
operability and met technical specification and licensee procedural requirements. The
inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.
Additionally, the inspectors reviewed a sample of related corrective action documents to
verify the licensee was identifying and correcting any deficiencies associated with
surveillance testing. Documents reviewed are listed in the Attachment.
Routine Surveillance Tests
- 14802A-2 Rev. 5, Train "A" NSCW Pump / Check Valve IST and Response Time Test
- 24568-2 Rev. 38, RCP 1 Train "A", Reactor Trip Relays Under Frequency (281-A), Under Voltage (227-A), Timing (262R-A) Trip Actuating Device Operational Test and
Channel Calibration and 24565-2, Rev. 37, RCP 2 Train "A", Reactor Trip Relays
Under Frequency (281-A), Under Voltage (227-A), Timing (262R-A) Trip Actuating
Device Operational Test and Channel Calibration
- 24449-2 Rev. 9, Diesel Generator Power Out Train 2Q-2791 Channel Calibration
- 21118-2 Rev. 3.2, Centrifugal Charging Pump (CCP) Train "A" Safety Grade Charging Flow Loop 2F-0138 Channel Calibration
Reactor Coolant System Leak Detection
- 14905-1 Rev. 69.0, RCS Leakage Calculation (Inventory Balance)
- 14905-2 Rev. 53.0, RCS Leakage Calculation (Inventory Balance)
In-Service Tests (IST)
- 14804B-1 Rev. 5.0, Safety Injection Pump "B" Inservice and Response Time Tests
b. Findings
No findings were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
a. Inspection Scope
The inspectors observed the emergency preparedness drill conducted on May 21, 2014.
The inspectors observed licensee activities in the simulator and alternate technical
support center to evaluate implementation of the emergency plan, including event
classification, notification, and protective action recommendations. The inspectors
evaluated the licensee's performance against criteria established in the licensee's
procedures. Additionally, the inspectors attended the post-exercise critique to assess
the licensee's effectiveness in identifying emergency preparedness weaknesses and
verified the identified weaknesses were entered in the corrective action program.
b. Findings
No findings were identified.
RADIATION SAFETY
2RS1 Radiological Hazard Assessment and Exposure Controls
a. Inspection Scope
Hazard Assessment and Instructions to workers During facility tours, the inspectors directly observed labeling of radioactive material and postings for radiation areas, HRAs
and airborne radioactivity areas established within the radiologically controlled area (RCA) of the Unit 1 containment, Unit 1 and Unit 2 auxiliary buildings, radwaste
processing facility, independent spent fuel storage installation, and selected storage
locations. The inspectors independently measured radiation dose rates or directly
observed conduct of licensee radiation surveys for selected RCA areas. The inspectors
reviewed survey records for several plant ar eas including surveys for alpha emitters, hot particles, airborne radioactivity, gamma surveys with a range of dose rate gradients, and
pre-job surveys for upcoming tasks. The inspectors also discussed changes to plant
operations that could contribute to changing radiological conditions since the last
inspection. For selected outage jobs, the inspectors attended pre-job briefings and
reviewed radiation work permit (RWP) details to assess communication of radiological
control requirements and current radiological conditions to workers.
Hazard Control and Work Practices The inspectors evaluated access barrier effectiveness for selected Unit 1 and Unit 2 locked high radiation area (LHRA) and very
high radiation area (VHRA) locations. Changes to procedural guidance for LHRA and
VHRA controls were discussed with HP supervisors. Controls and their implementation
for storage of irradiated material within the spent fuel pool were reviewed and discussed
in detail. Established radiological controls (including airborne controls) were evaluated
for selected Unit 1 refueling outage 18 (1R18) tasks including detensioning of the reactor
head, reactor head lift, upper internals lift, and scaffold building in Unit 1 containment. In addition, licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed.
Occupational workers' adherence to selected RWPs and HP technician (HPT)
proficiency in providing job coverage were evaluated through direct observations and
interviews with licensee staff. Electronic dosimeter (ED) alarm set points and worker
stay times were evaluated against area radiation survey results for detensioning of the
reactor head, reactor head lift, upper internals lift, and scaffold building in Unit 1
containment. ED alarm logs were reviewed and worker response to dose and dose rate alarms during selected work activities was evaluated. For HRA tasks involving
significant dose rate gradients, the inspectors evaluated the use and placement of whole
body and extremity dosimetry to monitor worker exposure.
Control of Radioactive Material The inspectors observed surveys of material and personnel being released from the RCA using small article monitor (SAM), personnel
contamination monitor (PCM), and portal moni tor (PM) instruments. The inspectors reviewed selected calibration records for selected release point survey instruments and
discussed equipment sensitivity, alarm setpoints, and release program guidance with
licensee staff. The inspectors compared recent 10 CFR Part 61 results for the dry active
waste (DAW) radioactive waste stream with radionuclides used in calibration sources to
evaluate the appropriateness and accuracy of release survey instrumentation. The inspectors also reviewed records of leak tests on selected sealed sources and
discussed nationally tracked source transactions with licensee staff.
Problem Identification and Resolution CRs associated with radiological hazard assessment and control were reviewed and assessed. The inspectors evaluated the
licensee's ability to identify and resolve the issues in accordance with procedure NMP-
GM-002, "Corrective Action Program," Version (Ver.) 12.1. The inspectors also
evaluated the scope of the licensee's internal audit program and reviewed recent assessment results.
Radiation protection activities were evaluated against the requirements of Updated Final
Safety Analysis Report (UFSAR) Section 12; TS Sections 5.4 and 5.7; 10 CFR Parts 19
and 20; and approved licensee procedures. Licensee programs for monitoring materials
and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE
Circular 81-07, "Control of Radioactively Contaminated Material." Documents reviewed
are listed in the report Attachment.
b. Findings
Introduction
- A Green, self-revealing, NCV of TS 5.7.1, "High Radiation Area," was identified for permitting an individual entry into a HRA without meeting the entry
requirements as specified in TS 5.7.1.b.
Description
- On March 17, 2014, with the Unit 1 reactor shutdown for refueling, an operator was performing troubleshooting of Unit 1 containment sumps leakage. A
planned reactor coolant system crud burst was in progress on Unit 1. As a result of the
crud burst radiation levels in parts of the auxiliary building were elevated and areas were posted as high radiation areas. The operator observed a "Danger High Radiation Area -
HP Escort Required for Entry - Alarming Dosimetry," posting at the entrance to the
encapsulation vessel room and returned to the HP control point for further instructions.
The operator was briefed by an HP technician using a survey performed for the area on
March 6, 2014, that did not reflect the current postings or current radiological conditions.
The operator was informed by the HP technician that he could enter the area without an
HP escort because he was using an alarming ED. In the follow-up investigation the HP
technician stated that he was not aware the crud burst had started. Upon entry into the
encapsulation vessel room, the operator received a dose rate alarm on his ED. He
stopped immediately and exited the area. The worker's ED alarm setpoint was 250
millirem per hour (mrem/hr) and the highest exposure rate seen by the ED was 262 mrem/hr. Dose rates in the area were as high as 300 mrem/hr on contact and 193
mrem/hr at 30 cm based on a follow-up survey. The licensee entered this issue into
their corrective action program as CR 787908 and took immediate corrective actions
which included securing access to the area, performing follow-up surveys and convening
a human performance review board to examine causal factors for the purpose of
determining corrective actions.
Analysis:
The inspectors determined that entry into a HRA without meeting the entry requirements specified in T.S. 5.7.1 was a performance deficiency. This finding was
more than minor because it was associated with the occupational radiation safety
cornerstone attribute of human performanc e and adversely affects the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to
radiation from radioactive material during routine civilian nuclear reactor operation.
Specifically, workers permitted entry into HRAs with inadequate knowledge of current
radiological conditions could receive unintended occupational exposures. The finding
was evaluated using IMC 0609, Appendix C, "Occupational Radiation Safety
Significance Determination Process (SDP)", dated August 19, 2008. The finding was not
related to ALARA planning, nor did it involve an overexposure or substantial potential for
overexposure, and the ability to assess dose was not compromised. Therefore, the
inspectors determined the finding to be of very low safety significance (Green). The
inspectors noted that the operator responded properly to the ED dose rate alarm thereby
limiting his potential for unintended exposure. This finding had a cross-cutting aspect of
"avoid complacency" in the human performance area because HP personnel failed to
verify plant conditions through available m eans when an evolution was in progress that was known to increase area dose rates prior to authorizing entry into an HRA. [H.12]
Enforcement
- Technical Specification 5.7.1, "High Radiation Area", requires in part, individuals entering HRAs meet one or more of the following criteria: a) be provided with
a radiation monitoring device that continuously indicates radiation dose rate in the area;
b) a radiation monitoring device that continuously integrates the radiation dose rate in
the area and alarms when a preset integrated dose is received. Entry into such areas
with this monitoring device may be made after the dose rate levels in the area have been
established and personnel are aware of them or c) An individual qualified in radiation
protection procedures with a radiation dose rate monitoring device, who is responsible
for providing positive control over the activities within the area and shall perform periodic
radiation surveillance at the frequency specified by health physics supervision in the
RWP. Contrary to the above, on March 17, 2014, a worker entered a HRA without a device that continuously indicated dose rates in the area (survey meter), knowledge of the actual radiological conditions in the area and no trained escort with a survey meter.
This violation is being treated as an NCV, consistent with Section 2.3.2 of the
Enforcement Policy. The violation was entered into the licensee's corrective action
program as CR 787908. (NCV 05000424, 2014003-02, "Unauthorized Entry into a High
Radiation Area.")
2RS2 Occupational ALARA Planning and Controls
a. Inspection Scope
Work Planning and Exposure Tracking The inspectors reviewed planned work activities and their collective exposure estimates for the current 1R18 outage. The inspectors
reviewed ALARA planning packages for the following high collective exposure tasks:
install/remove scaffolding, thermocouple work, mechanical stress improvement project (MSIP) work in containment and interference removal work in Unit 1 containment
annulus. For the selected tasks, the inspectors reviewed established dose goals, discussed assumptions regarding the bases for the current estimates with responsible
ALARA planners and walked down a mock-up of the reactor cavity annulus. The
inspectors evaluated the incorporation of exposure reduction initiatives and operating
experience, including historical post-job reviews, into RWP requirements. Day-to-day
collective dose data for the selected tasks were compared with established dose
estimates and evaluated against procedural criteria (work-in-progress review limits) for
additional ALARA review. Where applicable, the inspectors discussed changes to
established estimates with ALARA planners and evaluated them against work scope
changes or unanticipated elevated dose rates.
Source Term Reduction and Control The inspectors reviewed the collective exposure three-year rolling average from 2010 - 2012 and reviewed historical collective exposure trends from 1988 - 2014. The inspectors evaluated historical dose rate trends for
reactor coolant system piping and compared them to current 1R18 data. The crud burst
evolution during the first week of the 1R18 outage and source term reduction initiatives
were reviewed and discussed with chemistry and HP staff.
Radiation Worker Performance The inspectors observed radiation worker performance for job evolutions such as the MSIP interference removal, installation of shielding and
work in and around the reactor cavity. The inspectors observed ALARA briefings for
multiple MSIP jobs and emerging jobs such as Unit 1 bullet nose repair and radiation
worker performance was also evaluated as part of IP 71124.01. While observing job
tasks, the inspectors evaluated the use of remote technologies to reduce dose including
teledosimetry and remote visual monitoring.
Problem Identification and Resolution The inspectors reviewed and discussed selected corrective action program documents associat ed with ALARA program implementation.
The inspectors evaluated the licensee's ability to identify and resolve the issues in
accordance with licensee procedure NMP-GM-002, "Corrective Action Program", Ver.
12.1. The inspectors also evaluated the scope and frequency of the licensee's self-
assessment program and reviewed recent assessment results. ALARA program activities were evaluated against the requirements of UFSAR Section 12, TS Section 5.4, 10 CFR Part 20, and approved licensee procedures. Records reviewed are listed in
the report Attachment.
b. Findings
No findings were identified.
2RS3 In-Plant Airborne Radioactivity Control and Mitigation
a. Inspection Scope
Engineering Controls The inspectors reviewed the use of temporary and permanent engineering controls to mitigate airborne radioactivity during the 1R18 refueling outage.
The inspectors observed the use of portable air filtration units for work in contaminated
areas of the containment building and reviewed filtration unit testing records. The
inspectors evaluated the effectiveness of continuous air monitors and air samplers placed
in work area "breathing zones" to provide indication of increasing airborne levels.
Respiratory Protection Equipment The inspectors reviewed the use of respiratory protection devices to limit the intake of radioactive material. This included review of
devices used for routine tasks and devices stored for use in emergency situations. The
inspectors reviewed ALARA evaluations for the use of respiratory protection devices during
work associated with steam generator (S/G) eddy current testing. Selected self-contained
breathing apparatus (SCBA) units and negative pressure respirators (NPR)s staged for
routine and emergency use in the main control room and other locations were inspected for
material condition, SCBA bottle air pressure, number of units, and number of spare masks
and air bottles available. The inspectors reviewed maintenance records for selected SCBA
units for the past two years and evaluated SCBA and NPR compliance with National
Institute for Occupational Safety and Health certification requirements. The inspectors also
reviewed records of air quality testing for supplied-air devices and SCBA bottles.
The inspectors observed the use of powered air-purifying hoods during work on the S/G
platforms and in the upper cavity. The inspectors discussed training for various types of
respiratory protection devices with HP staff and interviewed radworkers and control room
operators on use of the devices. The inspectors reviewed respirator qualification records (including medical qualifications) for several main control room operators and emergency
responder personnel in the maintenance department.
Problem Identification and Resolution The inspectors reviewed CRs associated with airborne radioactivity mitigation and respiratory protection. The inspectors evaluated the
licensee's ability to identify and resolve the issues in accordance with licensee procedures.
The inspectors also reviewed recent self-assessment results.
Licensee activities associated with the use of engineering controls and respiratory
protection equipment were reviewed against TS Section 5.4; 10 CFR Part 20; Regulatory
Guide 8.15, "Acceptable Programs for Respiratory Protection," and applicable licensee
procedures. Documents reviewed are listed in the report Attachment.
b. Findings
No findings were identified.
2RS4 Occupational Dose Assessment
a. Inspection Scope
External Dosimetry The inspectors reviewed the licensee's national voluntary accreditation program (NVLAP) certification data for accreditation for the current year for
ionizing radiation dosimetry. The inspectors reviewed program procedures for
processing EDs and onsite storage of optically stimulated luminescent dosimeters (OSLD)s. Comparisons between ED and OSLD results, including correction factors, were discussed in detail. The inspectors also reviewed dosimetry occurrence reports
regarding alarming dosimeters.
Internal Dosimetry Inspectors reviewed and discussed the in vivo bioassay program with the licensee. Inspectors reviewed procedures that addressed methods for
determining internal or external contamination, releasing contaminated individuals, the
assignment of dose, and the frequency of measurements depending on the nuclides.
Inspectors reviewed and evaluated a sample of whole body counter (WBC) records
selected from September 2012 through February 2014. There were no internal dose
assessments for internal exposure greater than 10 millirem committed effective dose equivalent to review.
The inspectors evaluated the licensee's program for in vitro monitoring, however, no dose assessments had been performed using this method since the last inspection.
Special Dosimetric Situations The inspectors reviewed records for declared pregnant workers (DPW)s from September 2012 through February 2014 and discussed guidance
for monitoring and instructing DPWs. Inspectors reviewed and witnessed the licensee's
practices for monitoring external dose in areas of expected dose rate gradients, including the use of multi-badging and extremity dosimetry. The inspectors evaluated
the licensee's neutron dosimetry program incl uding instrumentation which was evaluated under procedure 71124.05. In addition, the inspectors evaluated the adequacy of
procedures and processes for assessing shallow dose.
Problem Identification and Resolution The inspectors reviewed and discussed licensee corrective action program documents associated with occupational dose assessment.
Inspectors evaluated the licensee's ability to identify and resolve the identified issues in
accordance with procedure NPM-GM-002, "Corrective Action Program", Ver. 12.1. The
inspectors also discussed the scope of the licensee's internal audit program and
reviewed recent assessment results.
Health physics program occupational dose assessment activities were evaluated against
the requirements of UFSAR Section 12; TS Section 5.4; 10 CFR Parts 19 and 20; and
approved licensee procedures. Records reviewed are listed in Section 2RS01, 2RS02, and 2RS04 of the report Attachment.
b. Findings
No findings were identified.
2RS5 Radiation Monitoring Instrumentation
a. Inspection Scope
Radiation Monitoring Instrumentation
- During walk-downs of the auxiliary building, radwaste processing building, fuel handling building and the RCA exit points, the
inspectors observed installed and portable radiation detection equipment. These
included area radiation monitors (ARM)s, cont inuous air monitors (CAMs), PCMs, SAMs, PMs, and liquid and gaseous effluent monitors, a WBC, count room equipment, and
portable survey instruments. The inspecto rs observed the physical location of the components, noted the material condition, noted flow measurement devices, input and
output of flow to monitors and compared sensitivity ranges with UFSAR requirements.
In addition to equipment walkdowns, the inspectors observed source checks and alarm
setpoint testing of various portable and fixed detection instruments including ion
chambers, a telepole, GEM TM-5s, ARGOS TM-ABs, and SAMs. Material condition of source check devices, device operation, and establishment of source check acceptance
ranges were also discussed with calibration lab personnel.
Calibration and Testing
- The inspectors reviewed the last two calibration records for selected ARMs, PCMs, PMs, SAMs, and containment high-range ARMs and the most
recent calibration record for a WBC. Inspectors reviewed records of survey instrument
function/source checks and observed and discussed performance of required checks
with calibration lab personnel. Calibration source documentation was reviewed for the
ARM high-range calibrator and the Cs-137 (J.L. Shepherd) source used for portable instrument checks. Calibration stickers on portable survey instruments were reviewed
and inspections of storage areas for 'ready-to-use' equipment were completed during
walkdowns. The inspectors reviewed alarm se tpoint values for selected ARMs, PCMs, PMs, SAMs, and effluent monitors. The inspectors also reviewed count room quality
control records for germanium detectors and liquid scintillator counters.
Problem Identification and Resolution:
The inspectors reviewed selected CAP reports in the area of radiological instrumentation. The inspectors evaluated the licensee's ability
to identify and resolve the issues in accordance with procedure NMP-GM-002-001, "Corrective Action Program Instructions", Ver. 31.1.
Effectiveness and reliability of selected radiation detection instruments were reviewed
against details documented in the following: 10 CFR Part 20; NUREG-0737, "Clarification of TMI Action Plan Requirements"; UFSAR Chapters 11 and 12; and
applicable licensee procedures. Documents reviewed during the inspection are listed in
the report Attachment.
b. Findings
No findings were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
a. Inspection Scope
The inspectors reviewed a sample of the performance indicator (PI) data, submitted by
the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant
records compiled between April 2013 and March 2014 to verify the accuracy and
completeness of the data reported for the station. The inspectors verified that the PI
data complied with guidance contained in Nuclear Energy Institute 99-02, "Regulatory
Assessment Performance Indicator Guideline," and licensee procedures. The inspectors
verified the accuracy of reported data that were used to calculate the value of each PI.
In addition, the inspectors reviewed a sample of related corrective action documents to
verify the licensee was identifying and correcting any deficiencies associated with PI
data. Documents reviewed are listed in the Attachment.
Cornerstone: Barrier Integrity
- reactor coolant system leak rate
- reactor coolant system specific activity
Cornerstone: Occupational Radiation Safety
The inspectors reviewed the occupational exposure control effectiveness PI results for
the occupational radiation safety cornerstone from January 2013 through December
2013. For the assessment period, the inspectors reviewed ED alarm logs and CRs
related to controls for exposure significant areas. Documents reviewed are listed in the
report Attachment.
Cornerstone: Public Radiation Safety:
The inspectors reviewed the radiological control effluent release occurrences PI results
for the public radiation safety cornerstone from January 2013 through December 2013.
The inspectors reviewed cumulative and projected doses to the public contained in liquid
and gaseous release permits and CRs related to radiological effluent technical
specifications/offsite dose calculation manual issues. The inspectors also reviewed
licensee procedural guidance for collecting and documenting PI data. Documents
reviewed are listed in the report Attachment.
b. Findings
No findings were identified.
4OA2 Identification and Resolution of Problems
.1 Routine Review
The inspectors screened items entered into the licensee's corrective action program in
order to identify repetitive equipment failures or specific human performance issues for
follow-up. The inspectors reviewed condition reports, attended screening meetings, or
accessed the licensee's computerized corrective action database.
.2 Semi-Annual Trend Review
a. Inspection Scope
The inspectors reviewed issues entered in the licensee's corrective action program and
associated documents to identify trends that could indicate the existence of a more
significant safety issue. The inspectors focused their review on equipment issues, but
also considered the results of inspector daily condition report screenings, licensee
trending efforts, and licensee human performance results. The review nominally
considered the 6-month period of January 2014 through June 2014 although some
examples extended beyond those dates when the scope of the trend warranted. The
inspectors compared their results with the licensee's analysis of trends. Additionally, the
inspectors reviewed the adequacy of corrective actions associated with a sample of the
issues identified in the licensee's trend reports. The inspectors also reviewed corrective
action documents that were processed by the licensee to identify potential adverse
trends in the condition of structures, sy stems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents
reviewed are listed in the Attachment.
b. Findings and Observations
No findings were identified.
.3 Annual Follow-up of Selected Samples
a. Inspection Scope
The inspectors conducted a detailed review of condition report CR 648248, "Calculation Error Affects Emergency Action Level (EAL) Setpoints."
The inspectors evaluated the following attributes of the licensee's actions:
- complete and accurate identification of the problem in a timely manner
- evaluation and disposition of operability/reportability issues
- consideration of extent of condition, generic implications, common cause, and previous occurrences
- classification and prioritization of the problem
- identification of root and contributing causes of the problem
- identification of any additional condition reports
- completion of corrective actions in a timely manner Documents reviewed are listed in the Attachment.
b. Findings
Introduction
- A White finding and associated violation of 10 CFR 50.54(q)(2) was identified by the licensee for the failure to follow and maintain the effectiveness of
emergency plans which meet the requirements of 10 CFR 50.47(b)(4). Specifically, the
licensee's emergency classification scheme action levels for Category R - Abnormal
Radiological General Emergency Action Level RG1 and Site Area Emergency Action
Level RS1 contained declaration threshold values which were significantly higher than
appropriate due to a calculation error.
Description:
In March 2005 Southern Co. corporate engineering calculation, X6CNA14, V3.0, was developed to estimate dose rates as a function of radiological releases
correlated to radiation monitor values. The calculation provided radiation monitor
threshold values for General Emergency (i.e. exceeding 1000 mrem TEDE/5000 mrem
thyroid CDE beyond the site boundary) and Site Area Emergency (i.e. exceeding 100
mR TEDE/500 mrem thyroid CDE beyond the site boundary). The calculation was a
manual calculation using a spreadsheet program; however, a unit conversion (Sieverts/second to mrem/hour) was made incorrectly and not detected during the
review process. The error resulted in threshold values sixty times greater than
appropriate. In 2005, Vogtle Electric Generating Plant submitted a license amendment
request to the NRC to change their EAL scheme to one based on NEI 99-01, "Development of Emergency Action Levels for Non-Passive Reactors," Rev. 4
guidelines. The request included EAL threshold values for RG1 and RS1 which were
based on the errant calculation. The NRC approved the amendment and the licensee
implemented the EAL scheme by issuing Revision 29 of Vogtle procedure 91001-C, "Emergency Classification and Implementing Instructions," on March 20, 2008. The non-
conservative threshold values were contained in this implementing procedure.
During an extent of condition review prompted by Southern Co. fleet operating experience, calculation X6CNA14, V3.0 was found to contain the calculation error. On
May 31, 2013, this issue was placed in the licensee's corrective action program as CR
648248. The licensee took immediate corrective actions, which included providing
corrected threshold values to appropriate management and decision-makers (shift
managers/emergency directors). In addition, the licensee performed an enhanced
apparent cause determination per the licensee's procedures, processed formal changes
to the station emergency plan and associated implementing procedures, and performed
additional extent of condition/cause reviews throughout the Southern Co. fleet. NRC
regional inspectors were advised of the issue and intended plan-of-action. Following
extensive review, the revised emergency plan and associated implementing procedure were provided to the NRC in September 2013.
These discrepant threshold values degraded the licensee's ability to make timely and accurate General Emergency and Site Area Emergency classifications based on the
abnormal radiological initiating condition, in that decision-makers would have to rely on
other means to classify the event (e.g.
dose assessments or field monitoring data) and that could delay such a declaration.
Analysis:
The inspectors concluded that the failure to maintain the effectiveness of an emergency plan to meet the requirements of 10 CFR 50.47(b)(4) and Part 50 Appendix
E to have a standardized EAL scheme in use based on facility system and effluent
parameters, was a performance deficiency. The performance deficiency was
determined to be more than minor because it was associated with the emergency
preparedness cornerstone attribute of procedure quality. It impacted the cornerstone
objective because it was associated with inappropriate EAL and emergency plan
changes and their adequacy to protect the health and safety of the public in the event of
a radiological emergency. Specifically, the licensee's ability to declare a Site Area
Emergency and General Emergency based on effluent radiation monitor values was
degraded in that event classification using these radiation monitors would be delayed.
The finding was assessed for significance in accordance with NRC Manual Chapter
0609, Appendix B, "Emergency Preparedness Significance Determination Process,"
which states, "Failure to comply means that a program is noncompliant with a
Regulatory requirement." The inspector determined the licensee was noncompliant with
10 CFR 50.54(q), 50.47(b)(4), and Appendix E,Section IV.B in that, due to a calculation
error, the abnormal radiological initiating conditions RG1(General Emergency) and RS1 (Site Area Emergency) emergency action levels contained classification threshold values sixty times greater than the appropriate value. This would require use of other means (dose assessment or actual field readings) to determine whether a Site Area Emergency
or General Emergency threshold had been exceeded which could delay the declaration.
The inspector determined that the situation constituted a degraded rather than lost risk-
significant planning standard (RSPS). The issue of concern was similar to the example
in Table 5.4.1 (Degraded RSPS) and was determined to be of low to moderate safety
significance (White). The licensee took immediate corrective actions providing corrected
threshold values to appropriate management and decision-makers (shift
managers/emergency directors). These and additional corrective actions were placed in
the licensee's corrective action program as CR 648248. A cross-cutting aspect was not
assigned based on the elapsed time since the performance deficiency occurred and
because the inspectors determined it was not reflective of current licensee performance.
Enforcement
- 10 CFR 50.54(q)(2), requires that a holder of a nuclear power reactor operating license under this part, shall follow and maintain the effectiveness of
emergency plans which meet the standards in 10 CFR 50.47(b), and the requirements in
Appendix E of this part.
10 CFR 50.47(b)(4), requires a standard emergency classification and action level
scheme, the bases of which include facility and system effluent parameters in use by the nuclear facility licensee, and state and local response calls for reliance on information by
facility licensees for determinations of mi nimum initial offsite response measures.
10 CFR Part 50, Appendix E, Section IV.B., "Assessment Actions," requires that means
to be used for determining the magnitude of, and for continuously assessing the impact of, the release of radioactive materials shall be described, including emergency action levels that are to be used as criteria for determining the need for notification and
participation of local and state agencies, the Commission, and other federal agencies.
The emergency action levels shall be based on in-plant conditions and instrumentation
in addition to onsite and offsite monitoring.
Contrary to the above, from March 2008 to May 2013, the licensee failed to maintain the
effectiveness of its emergency plan. The licensee failed to maintain a standard
emergency classification scheme which included facility effluent parameters.
Specifically, the emergency classificati ons RG1 (General Emergency) and RS1 (Site Area Emergency) contained effluent radiation monitor threshold values significantly
greater than appropriate. These monitors were being relied upon to determine the
magnitude and for continuously assessing the impact of the release of radioactive
materials, as well as providing criteria for determining the need for notification and
participation of local and state agencies. Following review by a Significance
Enforcement Review Panel and NRC management, the violation was determined to
meet IMC 0305, Section 11.05, criteria for discretion as an old design issue.
Specifically, the issue was licensee-identified through an extent-of-condition review of
internal operating experience, the issue was immediately corrected by the licensee, the
issue was not likely to be previously identified during normal operations, routine testing, or maintenance, and the issue is not reflective of current licensee performance. As
such, this finding will not be used as an input in the assessment process or NRC Action
Matrix. This finding has been identified as a cited violation 05000424, -425/2014003-03, "Calculation Error Results in Significantly non-Conservative EAL Threshold Values."
This is a violation of 10 CFR 50.54(q)(2) and a Notice of Violation is enclosed.
(Enclosure 2)
.4 Operator Work-Around Annual Review
a. Inspection Scope
The inspectors performed a detailed review of the licensee's operator work-around, operator burden, and control room deficiency lists for the station in effect on June 16, 2014 to verify that the licensee identified operator workarounds at an appropriate
threshold and entered them in the corrective action program. The inspectors verified
that the licensee identified the full extent of issues, performed appropriate evaluations, and planned appropriate corrective actions. The inspectors also reviewed compensatory
actions and their cumulative effects on plant operation. Documents reviewed are listed
in the Attachment.
b. Findings
No findings were identified.
4OA3 Event Follow-up
.1 (Closed) Licensee Event Report 05000425/2014-001-00:
Automatic Reactor Trip Due to Low Steam Generator Level
a. Inspection Scope
On April 08, 2014, with Unit 2 in Mode 1, 100 percent reactor power, at approximately
04:28, operators received unexpected annunciators, "Digital Feedwater Trouble Alarm"
for all four steam generators. Upon further investigation, operators noted loop 3 steam
generator water level was lowering at rapid rate. The operator at the controls (OATC)
took manual control of the loop 3 MFRV and attempted to raise water level. Water level
continued to decrease to the SG low-low level reactor trip setpoint and an automatic
reactor trip occurred as expected. The inspectors reviewed the licensee event report (LER), the associated condition report and root cause determination, and subsequent
action items for potential performance deficiencies and/or violations of regulatory
requirements. Additionally, discussions were held with operations, engineering and
licensing staff members to understand the details surrounding this issue. This condition
was documented in the licensee's corrective action program as CR 797929. This LER is
closed.
b. Findings
Introduction
- A Green, self-revealing non-cited violation (NCV) of 10 CFR 50 Appendix B Criterion V, "Instructions, Procedures, and Drawings," was identified for failure to
provide adequate work instructions as well as failure to follow the maintenance
procedure used to install flexible and rigid conduit. Specifically, the work instructions did
not provide adequate instructions and/or precautions to properly slope conduit during
installation to prevent water intrusion into a valve positioner. The work instructions
referenced maintenance procedure 25008-C, "Flexible and Rigid Conduit Installation."
The maintenance procedure referenced Vogtle design specification X3AR01 Section E-
8, "Raceway Systems," which provided sloping and tightness criteria for conduit installations.
Description
- On April 08, 2014, with Unit 2 in Mode 1, 100 percent reactor power, at approximately 04:28, operators received unex pected annunciators, "Digital Feedwater Trouble Alarm," for all four steam generators. Upon further investigation, operators
noted loop 3 steam generator water level was lowering at rapid rate. The operator at the
controls (OATC) took manual control of the loop 3 MFRV and attempted to raise water
level. Water level continued to decrease to the SG low-low level reactor trip setpoint and
an automatic reactor trip occurred as expected. The plant was stabilized in Mode 3 and
all safety related equipment responded as expected. Loop 3 SG water level was
restored using auxiliary feedwater. The licensee subsequently assembled an issue
response team (IRT) and a root cause team to investigate the cause of the automatic
reactor trip due to the failure of the loop 3 MFRV and to determine the required
corrective actions. Further investigation revealed water had entered the loop 3 MFRV
positioner junction box through a conduit penetration from a leaking valve located
approximately twenty feet above the junction box. The water had shorted out the valve positioner and caused the MFRV to go shut. The licensee had identified the leak one month before the incident and had entered it into their corrective action program, but had
not yet entered it into the work control process. The licensee determined the conduit connection was loose and not installed per design specification drawing AX2D94V077-3, "Digital Feedwater Flow Controller Instrument Support Details," Rev. 1.0. The
specification drawing shows the conduit being routed to the underside of the junction
versus the top where it was installed. A combination of the loose conduit connection
combined with improper conduit installation resulted in the leaking water entering the
positioner junction box shorting the MFRV positioner and causing the MFRV to close.
Further research by the root cause team revealed that during digital feedwater design
modification installation, the work instructions used by the maintenance technician to
install the flexible conduit was inadequate. Specifically, the work instructions did not
contain sufficient detail to properly slope the conduit to prevent water intrusion. The
work instructions referenced maintenance procedure 25008-C, "Flexible and Rigid
Conduit Installation." The maintenance procedure directed the use of specification X3AR01 Section E-8, "Raceway Systems," which contained proper sloping and tightness
criteria. The licensee replaced the positioner, revised the procedure, and rerouted the
conduit per design specification. The licensee entered this issue into their corrective
action program as CR 797929.
Analysis:
The failure to provide adequate work instructions as well as the failure to follow maintenance procedure 25008-C as required by 10 CFR 50 Appendix B Criterion
V was a performance deficiency. The inspectors determined that the finding was more
than minor because it was associated with the procedure quality and human
performance attributes of the initiating ev ents cornerstone and it adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and
challenge critical safety functions during shutdown as well as power operations.
Specifically, the failure to provide adequate work instructions resulted in a failure of the
loop 3 MFRV and a subsequent automatic reactor trip due to low-low SG water level.
Using IMC 0609, Attachment 4, "Initial Characterization of Findings" dated June 19, 2012, the inspectors determined that the finding affected the initiating events
cornerstone. The inspectors evaluated the finding using IMC 0609, Appendix A, "The
Significance Determination Process (SDP) for Findings At-Power," dated June 19, 2012.
Because the inspectors answered "No" to all the Exhibit 1, Section B, "Initiating Events
Screening Questions," the inspectors determined that the finding was of very low safety
significance (Green). The inspectors determined that the finding had a cross-cutting
aspect of "procedure adherence" in the human performance area because the
maintenance electricians did not follow Vogtle design specification procedures or
drawings resulting in the improper sloping of the MFRV flexible conduit. [H.8]
Enforcement
- 10 CFR 50 Appendix B Criterion V requires, in part, that procedures shall include appropriate quantitative or qualitative acceptance criteria for determining that
important activities have been satisfactorily accomplished. Contrary to the above, the maintenance procedure used to install the flexible conduit during the Unit 2 digital
feedwater design change modification installation did not provide appropriate
instructions for the sloping and tightening of the conduit thus preventing water intrusion
into the loop 3 MFRV positioner junction box. Specifically, maintenance procedure
25008-C, "Flexible and Rigid Conduit Installation," which is used to install conduit, did not provide adequate instructions and/or precautions to properly slope and tighten conduit such that water intrusion is avoided. To restore compliance, the licensee
replaced the positioner, revised the procedure, and rerouted the conduit per the design
specification. This violation is being treated as an NCV, consistent with Section 2.3.2 of
the NRC Enforcement Policy. The violation was entered into the licensee's corrective
action program as CR 797929. (NCV 05000425/2014003-04, "Inadequate Maintenance
Procedures and Usage Results in a Failed MFRV and an Automatic Reactor Trip")
.2 (Closed) Licensee Event Report 05000424/2014-002-00:
Manual Reactor Trip Due to Main Steam Isolation Valve Failure
a. Inspection Scope
On April 12, 2014 Unit 1 was in Mode 1 ascending in power after the 1R18 refueling
outage. At approximately 20:08, control room operators received an MSIV actuator
trouble alarm followed by the MSIV not fully open indication. Control room operators
identified lowering loop 1 steam generator (SG) #1 level and steam flow and manually
tripped Unit 1 at about 28 percent reactor power. The inspectors reviewed the LER, the
associated condition report and root cause determination, and subsequent action items.
This condition was documented in the licensee's corrective action program as CR
800018. This LER is closed.
b. Findings
The enforcement aspects associated with this event are discussed in Section 1R12 of
this integrated inspection report.
4OA5 Other Activities
.1 (Closed) Unresolved Item 05000425/2013007-02:
Failure to Identify and Correct Potential Emergency Diesel Generator "2B" Inoperability Following Failed Surveillance Testing
a. Inspection Scope
During the component design bases inspection documented in NRC Inspection Report
05000424, 425/2013007 (ADAMS ML13269A419), the team identified an unresolved
item (URI) regarding the discovery of a condition that could have potentially resulted in
an inoperable condition of the "2B" EDG due to an intermittently misaligned mechanically
operated cell (MOC) switch. Since the licensee had not recognized the potential
operability impact on the "2B" EDG during their investigations of EDG surveillance test
failures on December 13, 2011, and June 25, 2012, additional NRC inspection of the
specific alignment of the affected MOC switch contacts, and of the licensee's evaluation
of operability of the "2B" EDG, prior to the MOC switch being adjusted, was necessary to
determine if the issue of concern was minor or more than minor. On June 16, 2014, NRC inspection of the MOC switch contacts was performed to determine if the proper
functioning of the "2B" EDG, during emergency mode of operation, would have been
affected. Based on this additional review, this URI is now closed.
b. Findings
No findings were identified. However, the inspectors identified a minor performance deficiency and associated minor violation of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action." In accordance with IMC 0612, "Power Reactor Inspection Reports,"
dated January 24, 2013, minor violations are not routinely documented in inspection
reports. However, they may be documented to discuss inspection activities and
conclusions for closing a URI.
The inspectors determined that the licensee's failure to promptly identify and correct a
misaligned MOC switch associated with the "2B" EDG output breaker following a
surveillance test failure on December 13, 2011, was contrary to 10 CFR 50, Appendix B, Criterion XVI, and was a performance deficiency. This failure led to a small amount of
additional unavailability to troubleshoot the issue following an additional failure on June
25, 2012. Following additional NRC inspection on June 16, 2014, the inspectors
determined the actual radial alignment of the MOC switch contacts would have
supported the proper functioning of the EDG if it had been called upon during an event.
Using IMC 0612, Appendix B, "Issue Screening," dated September 7, 2012, the
inspectors determined the issue was of minor significance because, if left uncorrected, would not have led to a more significant safety concern. The licensee corrected the
condition of the misaligned MOC switch following the second failure on June 25, 2012.
Because this issue was entered into the licensee's corrective action program as CR
687752, and was of minor significance, the failure to comply with 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," constituted a minor violation that is not subject to
enforcement action in accordance with the NRC's Enforcement Policy.
4OA6 Meetings, Including Exit
.1 Exit Meeting
On July 25, 2014, the resident inspectors presented the inspection results to
Mr. T. Tynan and other members of the licensee's staff. The inspectors confirmed that
proprietary information was not provi ded or examined during the inspection.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- R. Barringer, Security Manager
- R. Collins, Chemistry Manager
- H. Cooper, Engineering Programs Supervisor
- J. Dixon, Corporate Fleet Area Manager, Health Physics
- G. Gunn, Licensing Supervisor
- R. Hons, Training Manager
- M. Johnson, Health Physics Manager
- K. Morrow, Licensing
- F. Pournia, Engineering Director
- J. Robinson, Engineering Programs Manager
- I. Sarygin, Sr. Engineer
- G. Saxon, Plant Manager
- J. Thomas, Work Management Director
- T. Thompson, Systems Engineering Manager
- T. Tynan, Site Vice-President
- K. Walden, Licensing Engineer
- S. Waldrup, Licensing Director
NRC personnel
- F. Ehrhardt, Chief, Region II Reactor Projects Branch 2
LIST OF ITEMS
OPENED AND CLOSED
Opened
- 05000424,425/2014003-03 VIO Calculation Error Results in Significantly Non-
Conservative EAL Threshold Values (Section
4OA2.3)
Open and
Closed
- 05000424/FIN-2014003-01 NCV Inadequate Maintenance Procedure Results in a
- Failed MSIV and a Manual Reactor Trip (Section
- 1R12)
- 05000424/FIN-2014003-02 NCV Unauthorized Entry into a High Radiation Area (Section 2RS1)
- 05000425/FIN-2014003-04 NCV Inadequate Maintenance Procedures and Usage
- Results in a Failed MFRV and an Automatic
- Reactor Trip (Section 4OA3.1)
- Attachment
Closed
- 05000424/FIN-2014003-01 NCV Inadequate Maintenance Procedure Results in a
- Failed MSIV and a Manual Reactor Trip (Section
- 1R12)
- 05000424/FIN-2014003-02 NCV Unauthorized Entry into a High Radiation Area (Section 2RS1)
- 05000425/FIN-2014003-04 NCV Inadequate Maintenance Procedures and Usage
- Results in a Failed MFRV and an Automatic
- Reactor Trip (Section 4OA3.1)
- Attachment
LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather Protection
Procedures
- 11889-C Rev. 21, Severe Weather Checklist
- VNP-CMS-710-00-PR-00001 Rev. 0, CB&I Heal th, Safety and Environmental Management System (Units 3&4)
- VNP-CMS-710-03-PR-00400 Rev. 0, CB&I Emergency Preparedness Plan (Units 3&4)
- 230-1, Rev. 23.0, Offsite AC Circuit Verification and Capacity/Capability Evaluation
- 230-2, Rev. 22.0, Offsite AC Circuit Verification and Capacity/Capability Evaluation
- 18017-C, Rev. 9.6, Abnormal Grid Disturbances/Loss of Grid
- 13830-1, Rev. 69.0, Main Generator Operation
- 13830-2, Rev. 55.0, Main Generator Operation
Section 1R04: Equipment Alignment
Procedures
- 11145-2 Rev. 12.2, Diesel Generator Alignment
- 11146-2 Rev. 7.1, Diesel Generator Fuel Oil Transfer System Alignment
- 11610-2 Rev. 21.3, Auxiliary Feedwater System Alignment
Drawings
- 2X4DB170-1 Rev. 42.0, P&I Diagram Diesel Generator System Train A - System No. 2403 2X4DB170-2 Rev. 47.0, P&I Diagram Diesel Generator System Train B - System No. 2403 2X4DB161-1, P&I Diagram Rev. 36.0, Aux iliary Feedwater System Condensate Storage &
- Degasifier System, System No. 1302
- 2X4DB161-2, P&I Diagram Rev. 24.0, Au xiliary Feedwater Syst em, System No. 1302 2X4DB161-3, P&I Diagram Rev. 38.0, Auxilia ry Feedwater Pump System, (Aux Feedwater Pump Turbine Driver) System No. 1302
- 2X4DB168-3, P&I Diagram Rev. 37.0, C
ondensate and Feedwater System, System No.
- 1305
Section 1R05: Fire Protection
Procedures
- Preplan Attachment 92755-2 Rev. 0.2, Zone 55 - Auxiliary Building - Level 2 Train "B" CCW HX Fire Fighting Preplan
- 2848-2 Rev. 0.2, Zone 148 - Auxiliary Building - Level 2 Fire Fighting Preplan
- 2723-2 Rev. 2.1, Zone 23 - Auxiliary Building - Electrical Chase Rooms Fire Fighting Preplan
- 2872-2 Rev. 1.2, Zone 172 - Auxiliary Building - Level 2 Fire Fighting Preplan
- 2847-2 Rev. 1.2, Zone 147 - Auxiliary Building - Level 2 Fire Fighting Preplan
- 2714B-1 Rev. 2.2, Zone 14B - Auxiliary Building - Level C Fire Fighting Preplan
- 2719-1 Rev. 4.1, Zone 19 - Auxiliary Building - CVCS Centrifugal
- Charging Pump Rooms
- Fire Fighting Preplan
- 2720-1 Rev. 4.1, Zone 20 - Auxiliary Building - CVCS Pump Rm Train A Fire Fighting Preplan
- 2789-2 Rev. 3.1, Zone 89 - Control Building - Level A Fire Fighting Preplan
- 2790-2 Rev. 2.2, Zone 90 - Control Building - Level A Fire Fighting Preplan
- 2859-2 Rev. 1.2, Zone 159 - Control Building - Level A Fire Fighting Preplan
- 2787-2 Rev. 2.2, Zone 87 - Control Building - Level A Fire Fighting Preplan
- 2788-2 Rev. 2.2, Zone 88 - Control Building - Level A Fire Fighting Preplan
- 2793-2 Rev. 3.2, Zone 93 - Control Building - Level A Fire Fighting Preplan
- 2802-2 Rev. 2.2, Zone 102 - Control Building - Level A Fire Fighting Preplan
- 2858-2 Rev. 1.2, Zone 158 - Control Building - Level A Fire Fighting Preplan
- 2862-1 Rev. 2.2, Zone 162 - Diesel Generator Building Fire Fighting Preplan
- 2864-1 Rev. 2.2, Zone 164 - Diesel Generator Building - Train B DFO Tank Fire Fighting
- 2855-2, Rev. 0.2, Zone 155 - Auxiliary Feedwater Pumphouse - Train B Fire Fighting Preplan
- 2856-2, Rev. 0.2, Zone 156 - Auxiliary Feedwater Pumphouse Fire Fighting Preplan
- 2857A-2, Rev. 0.2, Zone 157A - Auxiliary Feedwater Pumphouse - Train C Fire Fighting
- Preplan
- 2857B-2, Rev. 0.2, Zone 157B - Auxiliary Feedwater Pumphouse - Train C Fire Fighting
- Preplan
Section 1R06: Internal Flooding
Procedures
- 219-1 Rev. 35, Auxiliary and Containment Buildings and Miscellaneous Drain Systems
- Other X6CXC-27 Rev.8, Flooding Analysis Auxiliary Building Level D
- AX1D94A56 Rev. 2.0, Auxiliary Building Units 1 & 2 Door Schedule Level D
- CCN-V-07-0011 Rev. 8.0, Flooding - Auxiliary Building Level D
Drawings
- AX1D08A02-2, Rev. 6.0, Auxiliary Building Floor Plan El. 119 Level D
Section 1R11: Licensed Operator Requalification Program
Procedures
- 2003-C Rev. 53, Reactor Startup Mode 3 to Mode 2
- 2004-C Rev.107.2, Power Operation Mode 1
- NMP-OS-007-001 Rev. 14.3, Conduct of Operations Standards and Expectations
- Attachment Other Simulator scenario V-RQ-SE-12702, Loss of Grid/Natural Circulation Cooldown
- Simulator scenario V-RQ-SE-14300, Pe rformance Improvement Exercise Simulator scenario V-RQ-SE-14301, Large Break LOCA Response
- Simulator scenario V-RQ-SE-14302, SGTL/SGTR/Recovery
- Simulator scenario V-RQ-SE-14303, Control Room Evacuation
Section 1R12: Maintenance Rule Effectiveness
Condition Reports
and Action Items
- 807906, MPFF documented for Unit 2, System 1305, 2HV5230
- 795933, Unexpected control room annunciator ALB16-D04, MFIV Loop 4 low hydraulic pressure
Section 1R15: Operability Evaluations
Condition Reports
- 776584, Unknown chemical buildup on top of upper motor windings
- 808990, 2B DG Jacket Water Leak
- 805473/CAR
- 210188, 1HV3036A MSIV control board 'red' light flickering
- 807567/CAR
- 210214, Unit 2 turbine driven auxiliary feedwater pump (TDAFW) controller output
reading low
- CR 607966, U1 CCW Pump 1A inboard bearing over 160F
- Other Records
- Power Services, PO# SNG10075822 dated 3/10/2014 initiative
- CAR 210245, IDO - 2B DG Jacket Water Leak
- MWO SNC572497, 2B DG Jacket Water Leak
- CAR 210188, IDO - 1HV3036A MSIV
- CAR 210214, IDO - Unit 2 turbine driven auxiliary feedwater pump (TDAFW) controller
- MWO SNC525698, Troubleshoot Unit 2 TDAFW controller output
- TE 767342, IDO revision for CR 607966
Section 1R18: Plant Modifications
Procedures
- NMP-AD-010 Rev. 13.0, 10
- CFR 50.59 Screening/Evaluation
- NMP-ES-054-001 Rev. 2.0, Temporary Modification Processing
Work Orders
- SNC417397, Temporary modification to install accelerometers and a pressure transducer on
- CVCS letdown lines, Unit 1
- 1081013501, Accelerometer Installation at the CVCS letdown flow orifices and line 1-1208-255-
- 3", 6/13/2008
- Processing Facility (RPF)
- Attachment
Drawings
- AX3D-CH-T01J, Wiring Diagram Alternate Radwaste Building and ABB Control Room Misc Devices
- AX3D-BC-G20C, Elementary Diagram Alternate R
adwaste Building Cabling Block Diagram Rad Monitors, HVAC, Bridge Crane
- AX3DH469-1, Wiring Diagram Alternate Radwaste Building Control Room Conduit and Lighting
and Communications Plans Sheet 001
- Corrective Action Documents
Condition Report (CR)
- 2008106194, Walk down of Unit 1 containment for increased leakage
discovered upstream of letdown orifice isolation valve 1HV8149A, 6/1/2008
- Technical Evaluation (TE) 34658, Corrective Action to establish a replacement interval for the
letdown flow orifices, 5/7/2009
connection orifice during the refueling outage 15, 9/11/2008
- Enhanced Apparent Cause Determination (EACD)
- 194554, Station personnel failed to
implement the corrective action program to resolve an uncontrolled change in which area radiation monitors were permanently removed fr om the Alternate Radwaste Building (ARB).
- Technical Evaluation (TE)
- 363628, Revise procedure
- NMP-GM-002-001 Attachment 1 to
provide guidance for screening CRs that include design document aspects and configuration
control issues.
- ARE-16851,
- ARE-16852,
- ARE-16853,
- ARE-16854 as being no longer in service.
- TE 366715, Complete and approve an ABN to update any associated documents to reflect the
- ARE-16851,
- ARE-16852,
- ARE-16853,
- ARE-16854 as being no longer in service.
monitor system that is no longer in use.
- Other
- VEGP-FSAR-11, Radioactive Waste Management
- VEGP-FSAR-12, Radiation Protection
- ABN-V03007, Incorporate PDMS changes per DEC
- DBN-V03007
- LDCR No.
- 2012017, Update the FSAR to reflect the
- ARE-16851,
- ARE-16852,
- ARE-16853 and
- ARE-16854 as being no longer is Service.
Section 1R19: Post Maintenance Testing
Procedures
- 14825-2 Rev. 94, Quarterly Inservice Valve Test
- 14825-2 Rev. 95, Quarterly Inservice Valve Test
- 14430-1 Rev. 11.0, NSCW Cooling Tower Fans Monthly Test
- 24449-2 Rev. 9, Diesel Generator Power Out Train 2Q-2791 Channel Calibration
- 24812-1 Rev. 44, Unit 1 Delta T/Tavg loop 3 protection channel III 1T 431 operational test and
calibration
- 24810-2 Rev. 36, Unit 2 Delta T/Tavg loop 1 protection channel I 2T-411 operational test and
calibration
- Attachment
Work Orders
- SNC137725 - Replacement of 1E D26 Relays MCC21805S3ABE
- SNC413540 - 2PV3020 Replace A/B Solenoid
- SNC527135 - Quarterly Steam Generator Atmos pheric Relief Valve Inservice Valve Test
- SNC507135 - Manually stroke 2PV3020 from the loca
l control station and perform ARV fail safe test per 14825-2
- SNC408041 - (1A NSCW Fan 2) - Replace Agastat Relay
- SNC525486 - Unit 2A EDG Undervoltage Relay Calibration
- SNC516991 - Unit 1 Delta T/Tavg loop 3 protection channel operational test and calibration
- SNC488414 - Unit 2 Delta T/Tavg loop 1 protection channel I 2T-411 operational test and
calibration
- Other Records Unit 2 operator logs for 4/14/14
- Unit 2 operator logs for 4/26/14
- Unit 2
- ARV 3020 system outage fragnet
- Unit 1 operator logs for 5/12/14
- 1A NSCW Fan 2 system outage fragnet
Section 1R22: Surveillance Testing
Procedures
- 14802A-2 Rev. 5, Train A NSCW Pump / Check Valve IST and Response Time Test
- 24568-2 Rev. 38, RCP 1 Train A, Reactor Trip Relays Under Frequency (281-A), Under Voltage
(227-A), Timing (262R-A) Trip Actuating Device Operational Test and Channel Calibration
- 24565-2, Rev. 37, RCP 2 Train A, Reactor Trip Relays Under Frequency (281-A), Under
- Voltage (227-A), Timing (262R-A) Trip Actuating Device Operational Test and Channel
- Calibration
- 14804B-1 Rev. 5.0, Safety Injection Pump B Inservice and Response Time Tests
- 24449-2 Rev. 9, Diesel Generator Power Out Train 2Q-2791 Channel Calibration
- 21118-2 Rev. 3.2, Centrifugal Charging Pump (CCP) Train A Safety Grade Charging Flow Loop
- 2F-0138 Channel Calibration
- 14905-1 Rev. 69.0, RCS Leakage Calculation (Inventory Balance)
- 14905-2 Rev. 53.0, RCS Leakage Calculation (Inventory Balance)
Work Orders
- SNC523019 - Quarterly train A NSCW pump 21202P4005 discharge MOV and check valve
inservice test
- SNC523018 - Quarterly train A NSCW pump 21202P4003 discharge MOV and check valve
inservice test
- SNC523447- Quarterly train A NSCW pump 21202P4001 discharge MOV and check valve
inservice test
- SNC528899, Quarterly train A RCP #1 under voltage and under frequency relays TADOT
- SNC405763, 18-month train A RCP #2 under voltage and under frequency relays TADOT
- SNC457082, 18M staggered test basis (train B) safety injection pump response time test
- SNC520727, Quarterly (train B) safety injecti on pump and discharge check valve inservice test
- SNC525486, Unit 2A EDG Undervoltage Relay Calibration
- SNC412442, Centrifugal Charging Pump (CCP) Train A Safety Grade Charging Flow Loop 2F-
- Attachment
- 0138 Channel Calibration
Section 2RS1: Radiological Hazard Assessment and Exposure Controls
- Procedures, Guidance Documents, and Manuals
- 00008-C, Plant Lock and Key Control, Ver. 16.2
- 11882-1, Outside Area Rounds Sheets, Ver. 90.2
- 43014-C, Special Radiological Controls, Ver. 43.5
- 43021-C, Health Physics Central Monitoring Station Expectation and Guidelines, Rev. 4.4
- 43022-C, Health Physics Central Monitoring Station, Ver. 5.2
- 43032-C, Reactor Head and Upper Internals Movement, Ver. 3.2
- 46100-C, 10
- CFR 61 Waste Classification Sampling Program, Ver. 9
- 46111-C, Storage of Radwaste in Outdoor Process Shields, Ver. 6.1
- 47009-C, Operation and Use of Portable Ventilation Units, Ver. 22.3
- 93610-C, Conduct of Special Nuclear Material Control and Accountability, Ver. 11.1
- 93641-C, Development and Implementation of the Fuel Shuffle Sequence Plan, Ver, 21.1
- 93780-C,
- HI-TRAC Contamination Survey, Ver. 1.0
- 93781-C, HI -TRAC Surface Dose Rates, Ver. 1.0
- 93782-C,
- HI-STORM Surface Dose Rates, Ver. 1.0
- NMP-GM-002, Corrective Action Program, Ver. 12.1
- NMP-GM-002-001, Corrective Action Program Instructions, Ver. 31.1
- NMP-HP-109, Investigation, Evaluation and Management of Damaged, Lost, Malfunctioning or
- Alarming Dosimetry, Ver. 1.1
- NMP-HP-202, Radiological Controls for Highly Radioactive Objects, Ver. 1.0
- NMP-HP-206, Issuance, Use and Control of Radiation Work Permits, Ver. 3.0
- NMP-HP-207, Selection and Use of Protective Clothing, Ver. 1.0
- NMP-HP-218, Health Physics Stop Work Authority and Guidance on Response, Ver. 1.0
- NMP-HP-300, Radiation and Contamination Surveys, Ver. 2.1
- NMP-HP-301, Airborne Radioactivity Sampling and Evaluation, Ver. 2.2
- NMP-HP-302, Restricted Area Classification, Postings, and Access Control, Ver. 6.0
- NMP-HP-302-001, Radiological Key Control, Ver. 2.1
- NMP-HP-303, Personnel Decontamination, Ver. 2.2
- NMP-HP-304, Decontamination of Areas, Tools and Equipment, Ver. 1.0
- NMP-HP-305, Alpha Radiation Monitoring, Ver. 4.0
- NMP-HP-400, Control and Accountability of Radioactive Sources, Ver. 2.0
- NMP-HP-403, Control and Monitoring of Materials in Radiation Controlled Areas, Ver. 1.0
- NMP-HP-404, Release of Materials from the RCA and Protected Areas, Ver. 1.0
- Health Physics Work Plan, Rx Cavity Decon
- Records and Data
- 46100-C, 10
- CFR 61 Waste Classification Sampling Program, Ver. 9, Dated 06/12/12
- Air Sampler Calibration, Sheet 1 of 3, Data Sheet 1, Air Sampler Calibration Form, Instrument
- Nos.
- VEGP-HP-1368, Model No.
- RAS-1, Dated 03/13/14;
- VEGP-HP-1369, Model No.
- RAS-1, Dated 01/09/14; and
- VEGP-HP-1371, Model No.
- RAS-1, Dated 12/26/13
- Airborne Radioactivity Sampling and Evaluation, Data Sheet 1, Air Sample Record (Particulate and Iodine), Air Sample Nos.:
- 14-0132, U1 CTMT/220' (Pulling NI Covers in Upper RX Cavity), Dated 03/16/14; 14-0133, U1 EH (Equipment Hatch Routine), Dated 03/16/14; and 14-0157, U1
- CTMT/171' (Routine
- VEGP-HP-1368), Dated 03/20/14
- National Source Tracking System, Annual Inventory Reconciliation Report, Vogtle 1, Dated
- 01/17/14
- Attachment Plant Vogtle, Gamma Spectroscopy Results, Sample IDs:
- 86362, U1 RX Head Lift Level 220
(1L Gas sample in liquid marinelli), Dated 03/19/14; 86363, U1 RX Head Lift (1L Gas sample in liquid marinelli), Dated 03/19/14; 86375, U1 Polar Crane RX Head Lift (Particulate Shelf 0), Dated 03/19/14; 86376, U1 Polar Crane RX Head Lift (Breathing Zone Charcoal Shelf 0), Dated
- 03/19/14; 86406 and 86409, 1-CTMT 220'-South Cavity-Upper Internal Lift (Particulate Shelf 0), Dated 03/20/14; and 86407 and 86408, 1-CTMT 220'-South Cavity-Upper Internal Lift (Large
- Plastic Charcoal Shelf 0), Dated 03/20/14
- Plant Vogtle Radiological Information Survey Nos.
- 165158,
- HI-TRAC Surface Dose (C), Dated
- 11/22/13;
- 165176, HI Storm Surface Dose Rates (C), Dated 11/22/13;
- 165177, HI Storm Duct
- Survey C, Dated 11/22/13;
- 165641,
- HI-TRAC Surface Dose (C), Dated 12/11/13;
- 165655, HI
- Storm Duct Survey C, Dated 12/11/13;
- 168234, Upper Cavity (1RXA16), Dated 03/16/14;
- 168472, Reactor Cavity Area (1RXA2), Dated 03/19/14;
- 168526, Quadrant 3 (1RXC), Dated
- 03/20/14;
- 168528, Reactor Cavity Area (1RXA2), Dated 03/19/14;
- 168538, Reactor Cavity Area
(1RXA2), Dated 03/20/14;165662, ISFSI Pad (C), Dated 12/11/13,
- 169489, U1 Upper Cavity,
- 4/4/14,
- 169524, U1 Upper Cavity, 4/4/14 and
- 169517, U1 Upper Cavity, 4/4/14
- RWP No. 14-1006, Installation and Removal of Insulation in Unit 1 Containment, Revision
(Rev.) 0
- RWP No. 14-1403, Decon of Upper and Lower Cavity, Rev. 0
- RWP No. 14-1406, Reactor Head and Upper Internals Lift and Set, Rev. 0
- Unit 1 and U2 Spent Fuel Pool Inventory Log, Non Fuel Radioactive Material Stored in Unit 1
and U2 Spent Fuel Pool, Dated 02/18/14
- Type:
- Portable, HEPA S/Ns:
- HU2000, Dated 03/06/14; HU200002, Dated 03/06/14; and HU
- 35015, Dated 03/06/14
- CAP Documents
- CR 603893
- CR 604563
- CR 610824
- CR 615028
- CR 624795
- CR 663674
- CR 679060
- CR 697578
- CR 787908
- CR 795074
- Health Physics Fleet Performance Summary Report,
- NOSCPA-HP-2013-13, Dated 12/04/13
- Nuclear Oversight Audit of Health Physics, Fleet-HP-2013, Dated July 15, 2013
Section 2RS2: Occupational
- ALARA Planning and Controls Procedures, Guidance Documents, and Manuals
- 16035-1, "Chemistry Operations Interface for RCS Chemistry Control During Scheduled Plant
- Shutdowns", Ver. 15.2
- NMP-AD-035, "ALARA Program", Ver. 1.3
- NMP-HP-204, "ALARA Planning and Job Review", Ver. 3.3
- Attachment
- 41006-C, Temporary Shielding, Ver 29.2
- NMP-HP-202, Radiological Controls for Highly Radioactive Objects, Ver. 1.0
- NMP-HP-206, Issuance, Use and Control of Radiation Work Permits, Ver 3.0
- Records and Data
- U-1 Containment 1R18 Outage Turnover, dated 03/20/2014
- 1R18 Outage Dose Summary Report, dated 03/20/2014
- HP Duty Foreman's Checklist - Daily Report Items, dated 03/19/2014
- 1R18 Temporary Shielding Worksheet, dated 11/21/2013
- Plant Vogtle Radiological Information Survey Nos.
- 168301, Under Vessel Annulus Area (Pre-
- Shielding), Dated 03/17/2014,
- 168313, Under Vessel Annulus Area (Pre-Shielding), Dated
- 03/18/2014,
- 168345, Under Vessel Annulus Area (Post Shielding), Dated 03/18/2014,
- 168362, Under Vessel Annulus Area (Post Shielding), dated 03/17/2014,
- 169356, Reactor Cavity Area
for Core Exit Thermocouple Bullet Nose Manual Alignment, dated 04/02/2014,
- 169077, Lower
- Reactor Cavity Area for Core Exit Thermocouple Bullet Nose Manual Alignment, dated
- 03/29/2014, Plant Vogtle EPRI Radiological Survey Nos.
- 168339, EPRI Survey Map Loop 1, dated
- 03/18/2014,
- 168477, EPRI Survey Map Loop 1, dated 03/20/2014,
- 168339, EPRI Survey Map Loop 2, dated 03/18/2014,
- 168488, EPRI Survey Map Loop 2, dated 03/20/2014,
- 168341, EPRI
- Survey Map Loop 3, dated 03/18/2014,
- 168491, EPRI Survey Map Loop 3, dated 03/20/2014,
- 168337, EPRI Survey Map Loop 4, dated 03/18/
- 2014,
- 168478, EPRI Survey Map Loop 4, dated
- 03/20/2014,
- Work in Progress (WIP) Reviews,
- RWP 14-1004, Installation and Removal of Scaffolding in U1
- Containment (50%), dated 03/23/2014,
- RWP 14-1408, Theermocouple Work in U1
- Containment, dated 03/28/2014,
- 03/26/2014,
- Interference Removal (80%), dated 03/31/2014
- ALARA Briefing Records,
- RWP 14-1408, Thermcouple Work in Containment,
- Interference Work
- ALARA Post Job Reviews,
- RWP 13-2302, Eddy Current Testing on S/G 1&2 and All Associated Work,
- RWP 13-2400, Rx Head Disassembly/Assembly
- Shutdown Chemistry Review: Vogtle Unit 1 Fuel Cycle 17, dated 11/27/2012
- U1 EPRI Shutdown Survey Points Trend Graph for Refueling Outages 1R1 - 1R17
- U1 S/G Channel Head Dose Rate Trend Graph for Refueling Outages 1R1 - 1R17
- U2 EPRI Shutdown Survey Points Trend Graph for Refueling Outages 2R1 - 2R16
- U2 S/G Channel Head Dose Rate Trend Graph for Refueling Outages 2R1 - 2R16
- EPRI Sponsored Source Term Assessment for Vogtle Units 1 and 2, Final Report, Dec 2013
- NOSCPA-HP-2012-04, Health Physics Fleet Performance Summary Report, dated 11/26/2012
- VNP - Health Physics Focused Self Assessment for Dose Controls, dated 01/02/2013
- NOSCPA-HP-2013-13, Health Physics Fleet Performance Summary Report, dated 12/04/2013
- ALARA Committee Meeting Minutes Fourth Quarter 2013
- 2012 Annual ALARA Report, 09/25/2013
- 1R17 ALARA Report Attachment
- PARC "Called Monthly Meeting," dated 03/05/14
- RWP Dose Totals Year to Date (YTD), dated 04/03/14
- CAP Documents
- CR 610495
- CR 643120
- CR 650993
- CR 651612
- CR 762528
- CR 763764
Section 2RS3: In-Plant Airborne Radioactivity Control and Mitigation Adam 4/9/14
- Procedures, Guidance Documents, and Manuals
- 47004-C, Breathing Air Analysis, Rev. 16
- 47001-C, Selection and Use of Respiratory Protection Equipment Used for Radiological
- Purposes, Ver. 19.2
- 47005-C, Inspection, Repair, and Storage of Respiratory Protection Equipment, Rev. 15
- NMP-GM-002-001, Corrective Action Program, Ver. 31.1
- Records and Data Reviewed
- SCBA Maintenance Records, Kit 58 and
- HP-0060, January 2012 - December 2013
- Respirator Use Evaluation Worksheets, 10/9/13
- DOP Test Log Sheets, 3/10/14, 3/20/14, 3/24/14
- Breathing Air Analysis Results, Scott Revolve 5016 Compressor, 6/1/13, 8/26/13, 12/6/13,
- 2/18/14
- Breathing Air Analysis Results, U2 Containment Breathing Air, 3/14/13
- Breathing Air Analysis Results, U2 Service Air Compressor 1, 12/6/13
- Breathing Air Analysis Results, U2 Service Air Compressor 2, 6/1/13
- Breathing Air Analysis Results, Hypress FTB Compressor, 6/1/13, 8/26/13, 12/6/13, 2/18/14
- Breathing Air Analysis Results, U1 Service Air Compressors 2 & 3, 2/18/14
- Breathing Air Analysis Results, U1 Service Air, 8/26/13
- Breathing Air Analysis Results, U1 Equipment Hatch Compressor, 3/21/14
- Laboratory Report Compressed Air/Gas Quality Testing, Scott Revolve 5016 Compressor,
- 2/12/13
- Laboratory Report Compressed Air/Gas Quality Testing, Hypress FTB Compressor, 2/12/13
- List of Maintenance Personnel with SCBA Qualification Assigned, 2/28/14
- List of Operations Personnel with SCBA Qualification Assigned, 2/28/14
- CAP Documents Fleet-HP-2013, Nuclear Oversight Audit of Health Physics, 7/15/13
- CR 617112
- CR 647987
- CR 695027
- Attachment
Section 2RS4: Occupational Dose Assessment
- Procedures, Guidance Documents, and Manuals
- NMP-HP-107-001, "Instructions for Retrieving, Printing and Updating Individual Radiation
- Exposure Records", Ver.1.0
- NMP-HP-106, "Investigating of Exposures Exceedi ng Fleet Administrative Limits", Ver. 1.0
- NMP-HP-103, "Skin Dose Assessment", Ver. 1.1
- NMP-HP-100, "Bioassay Program", Ver. 1.1
- NMP-HP-101, "In-Vivo Bioassay and Internal Dose Assessment", Ver. 3.0
- NMP-HP-102, "In-Vitro Bioassay," Ver. 1.1
- NMP-HP-201, "Personnel Dosimetry Program," Ver. 1.1
- NMP-HP-204, "Use and Calibration of Whole Body Counters," Ver. 1.3
- Records and Data
- NVLAP Certification of Accreditation to ISO/IEC 17025:2005, for Lab Code:100551-0, dated
- 2/13/2013.
- Vogtle Alpha Plant Characterization Study 2011 Update
- Canberra Report of Performance Testing Results for Nuclear Enterprises (NE) Model SPM
- 904B/906 Personnel Portal Monitor, May 18, 2012
- Personnel Contamination Events/Personnel Contamination Reports (PCE/PCR) Logs, 2/2012 -
- 3/2014
- EDE & NRC Form 5 Calculations for Steam Generator Multibadging Jobs entry made on
- 3/25/14; Multibadge RCA Authorization/Worksheets
- NMP-HP-109 Data Sheets, Investigation of Lost, Damaged or Malfunctioning Personnel
- Dosimetry, for occurrence on 3/18/2014
- NMP-HP-109 Data Sheet 2, Investigation of Lost, Damaged or Malfunctioning Personnel
- Dosimetry, for occurrence on 6/12/2013
- CAP Documents
- CR 541097
- CR 585435
- CR 610472
- CR 746418
- CR 748897
Section 2RS5: Radiation Monitoring Instrumentation
- Procedures, Guidance Documents, and Manuals
- 43802-C, "Calibration of Gamma Standards", Ver. 12.4
- NMP-HP-700, "Radiation Protection Instrumentation Program," Ver. 1.0
- NMP-HP-701, "Daily Instrumentation Source Checks," Ver. 1.3
- NMP-HP-719, "Operation and Calibration of the CANBERRA
- ARGOS-5AB Exit Monitor",
- Ver. 2.0
- NMP-HP-718, "Operation and Calibration of the CANBERRA
- GEM-5 Gamma Exit Monitor",
- Ver. 1.0
- NMP-HP-709, "Calibration of the Small Article Monitor (SAM-12)", Ver. 1.0
- NMP-HP-708, "Operation and Calibration of the MGPI Telepole Instrument", Ver. 3.0
- 43693-C, "Operation and Use of the JL Shepard Model 89-400 Calibrator", Ver. 2.2
- Attachment Records and Data Work Order SNC551063, RMSOOS 1-RE003 Out of Service
- Work Order SNC405890, Plant Vent Post Accident COT 1RE12444C-18M, 8/20/12
- System Health Report, Unit 1 1609-R
ad Monitoring System, 7/1/2013-9/30/2013
- Fleet-HP-2013, Nuclear Oversight Audit of Health Physics, July 15, 2013
- 43689-C Data Sheet 1, Calibration of the Small Article Monitor, Rev 7, for
- SAM-11 VEGP
- 1151, 5/23/2012 & 5/22/2014
- NMP-HP-708 Data Sheet1, Telepole Gamma Calibration, SN#
- VEG-HP-1511 3/04/14
- 43635-C Data Sheet 2, AMS High Voltage and Flow Calibration, SN#
- VEGP-1450, 3-13-14 & 3-
- 6-13
- NMP-HP-703 Data Sheet 1, Calibration Sheet,
- RO-20 SN#
- VEGP-HP-1017 03-4-14 & 03-5-13
- 43658-C Data Sheet 1, Air Sampler Calibration Sheet, SN#
- VEGP-HP-1372 11-26-13 & 11-28-
- NMP-HP-719, "Operation and Calibration of the CANBERRA
- ARGOS-5AB Exit Monitor" Data
- Sheet 1, ARGOS 5AB Calibration Certificate, 12-3-13
- CAP Documents
- TE 710894
- CR 713514
- CR 745425
- CR 765241
- CR 779661
- CR 785178
Section 4OA1: Performance Indicator (PI) Verification
- Procedures, Guidance Documents, and Manuals
- 00163-C, NRC Performance Indicator and Monthly Operating Report Preparation and Submittal, Ver. 14.6
- Records and Data Liquid Effluent Release Permits L-20131221-239-B and L-20140227-035-B
- Gaseous Effluent Release Permits G-20131231-002-B and G-20140222-045-B
- CAP Documents
- CR 617317
- CR 654735
- CR 700923
- CR 723420
Section 4OA2: Identification and Resolution of Problems
Condition Reports
- CR 648248; Calculation Error Affects EAL Setpoints for AS1 and AG1
- CR 648345; Revise Emergency Plan and EPIP to correct EAL RS1 and RG1 error
- CR 650353; Perform Apparent Cause Determination on Calculation Error
- Attachment Documents: Southern Co. letter
- NL-13-1979 to NRC, Emergency Plan Revision 60, dated September 24,
- 2013
- Apparent Cause Determination Report, Calculation Errors Resulted in Incorrect EAL Setpoints, July 1, 2013
- Documentation of Engineering Judgment
- DOEJ-VXSNC648248-M001, Corrected Emergency
- Action Level Set Points for RS1 and RG1 for Plant Vogtle, 5/31/2013
Procedures
- 91001-C, Emergency Classification and Implementing Instructions, Rev. 29
- NMP-GM-002-001, Corrective Action Program Instructions, Ver. 31.1
- NMP-GM-002-007, Apparent Cause Determination Instruction, Ver. 10
Section 4OA5: Other Activities
Condition Reports
- CR 687752, 2B EDG Operability Assessment -
- NOTICE OF VIOLATION
- Southern Nuclear Operating Company, Inc
- Docket No. 50-424, 50-425
- Vogtle Electric Generating Plant
- License No.
- NFP-81
- During an NRC inspection completed on June 30, 2014, one violation of NRC requirements was
identified.
- In accordance with the NRC Enforcement Policy, the violation is listed below:
- CFR Part 50.54(q)(2), requires that a holder of a nuclear power reactor operating
license under this part, shall follow and maintain the effectiveness of emergency plans
which meet the requirements in Appendix E of this part and the standards in 10 CFR
- 50.47(b)
- CFR 50.47(b)(4), requires a standard emergency classification and action level scheme, the bases of which include facility and system effluent parameters, is in use by the nuclear
facility licensee, and State and local response plans call for reliance on information
provided by facility licensees for determinations of minimum initial offsite response
measures.
- CFR Part 50, Appendix E, Section
- IV.B., Assessment Actions, requires the means to be
used for determining the magnitude of, and for continuously assessing the impact of, the
release of radioactive materials shall be described, including emergency action levels that
are to be used as criteria for determining the need for notification and participation of local
and State agencies, and the Commission.
- The emergency action levels shall be based on
in-plant conditions and instrumentation in addition to onsite and offsite monitoring.
- Contrary to the above, from March 20, 2008, until May 31, 2013, the licensee failed to
maintain the effectiveness of their emergency plan.
- Specifically, the licensee failed to
maintain a standard emergency classification scheme which included facility effluent
parameters in that effluent parameter classification threshold values for RG1 (General
- Emergency) and RS1 (Site Area Emergency) were significantly non-conservative.
- These
monitors were being relied upon to continuously assess the impact of the release of
radioactive materials as well as provide criteria for determining the need for notification and
participation of local and State agencies.
- This violation is associated with a White SDP finding.
- The NRC has concluded that information regarding:
- 1) the reason for the violation; 2) the
actions planned or already taken to correct the violation and prevent recurrence; and, 3) the
date when full compliance was achieved, is already adequately addressed on the docket in
- Inspection Report No. 05000424/2014003 and 05000425/2014003.
- However, you are required
to submit a written statement or explanation pursuant to 10 CFR 2.201 if the description therein
does not accurately reflect your corrective actions or your position.
- In that case, or if you choose to respond, clearly mark your response as a "Reply to a Notice of Violation,
and send it to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,
- DC 20555-0001 with a copy to the Regional Administrator, Region II, and a copy to
the NRC Resident Inspector, within 30 days of the date of the letter transmitting this Notice.
- If you choose to respond, your response will be made available electronically for public inspection in the NRC Public Document Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html.
- Therefore, to
the extent possible, the response should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the Public without redaction.
- In accordance with 10
- CFR 19.11, you may be required to post this Notice within two working
days of receipt.
- Dated this 6
th day of August, 2014.