IR 05000202/2030004

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Integrated Inspection Report 052000250/2023004 and 05200026/2023004
ML24043A127
Person / Time
Site: Vogtle, 05000202  
Issue date: 02/13/2024
From: Bradley Davis
Division Reactor Projects II
To: Coleman J
Southern Nuclear Operating Co
References
IR 2023004
Download: ML24043A127 (23)


Text

SUBJECT:

VOGTLE ELECTRIC GENERATING PLANT, UNIT 3 & 4 - INTEGRATED INSPECTION REPORT 05200025/2023004 AND 05200026/2023004

Dear Jamie Coleman:

On December 31, 2023, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Vogtle Electric Generating Plant (VEGP), Unit 3 & 4 and discussed the results of this inspection with Mr. Patrick Martino, VEGP Units 3 & 4 Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Vogtle Electric Generating Plant, Unit 3 & 4.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at Vogtle Electric Generating Plant, Unit 3 & 4.

February 13, 2024 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Bradley J. Davis, Chief Construction Inspection Branch 2 Division of Construction Oversight Docket Nos. 05200025 and 05200026 License Nos. NPF-91 and NPF-92

Enclosure:

As stated

Inspection Report

Docket Numbers:

05200025 and 05200026

License Numbers:

NPF-91 and NPF-92

Report Numbers:

05200025/2023004 and 05200026/2023004

Enterprise Identifier:

I-2023-004-0073

Licensee:

Southern Nuclear Operating Company, Inc.

Facility:

Vogtle Electric Generating Plant, Unit 3 & 4

Location:

Waynesboro, GA

Inspection Dates:

October 01, 2023 to December 31, 2023

Inspectors:

B. Caballero, Senior Operations Engineer

J. Eargle, Senior Resident Inspector

S. Egli, Senior Construction Inspector

C. Even, Senior Reactor Inspector

B. Griman, Resident Inspector

B. Kemker, Senior Resident Inspector

J. Parent, Resident Inspector

J. Walker, Senior Emergency Preparedness Inspector

Approved By:

Bradley J. Davis, Chief

Construction Inspection Branch 2

Division of Construction Oversight

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Vogtle Electric Generating Plant, Unit 3

& 4, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Adequately Implement Containment Closeout Resulting in Loose Debris and Unanalyzed Materials Left in Unit 4 Containment Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05200026/2023004-01 Open/Closed

[H.2] - Field Presence 71111.20 The inspectors identified a finding of very low significance (Green) with an associated NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings for the licensee's failure to properly implement their containment cleanliness and material control closeout procedure prior to and after Unit 4 entering Mode 4.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05200025/2023-006-00 LER 2023-006-00 for Vogtle Electric Generating Plant,

Unit 3 Regarding Automatic Reactor Protection System Actuation During Startup Testing Due to Auto Reactive Power Regulator Being Active While In Island Mode Operation 71153 Closed

PLANT STATUS

Unit 3 Unit 3 was operated at or near 100% rated thermal power during the inspection period.

Unit 4

At the start of this inspection period, Unit 4 was in Mode 3 (Hot Standby) with the licensee investigating the cause for the 2A reactor coolant pump (RCP) trip on September 29.

On October 1, the licensee performed a plant cooldown and the unit entered Mode 4 (Safe Shutdown) to begin a maintenance outage for replacement of the 2A RCP pump motor prior to resumption of plant startup testing activities. The unit entered Mode 5 (Cold Shutdown) on October 3.

On December 23, the licensee completed its final maintenance outage activities and required testing, established conditions to begin plant heat up, and the unit entered Mode 4 (Safe Shutdown). On December 25, the licensee completed additional required testing and continued plant heat up for the unit to enter Mode 3 (Hot Standby). On December 30, the licensee performed a plant cooldown to Mode 4 (Safe Shutdown) and subsequently to Mode 5 (Cold Shutdown) on December 31 to address abnormal vibrations on trains B and D of ADS stage 4 piping.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal winter temperatures.

(1) Passive Containment Cooling System during the weeks of November 26 and December 10, 2023.

71111.04 - Equipment Alignment

Partial Walkdown Sample [AP1000] (IP Section 03.01) (1 Sample)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 3 passive containment cooling system during the week of October 29, 2023.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample [AP1000] (IP Section 03.01) (2 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Unit 3 Diesel Generator Building on October 19, 2023.
(2) Unit 4 PXS B and RNS Valve Room on October 26, 2023.

71111.06 - Flood Protection Measures

Flooding Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated internal flooding mitigation protection in the Unit 4 Auxiliary Building Elevation 66'6" on October 4, 2023.

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

The licensee completed the annual requalification operating examinations and biennial written examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), "Requalification Requirements," of the NRC's "Operator's Licenses." The inspector performed an in-office review of the overall pass/fail results of the individual operating examinations, the crew simulator operating examinations, and the biennial written examinations in accordance with Inspection Procedure (IP) 71111.11, "Licensed Operator Requalification Program and Licensed Operator Performance." These results were compared to the thresholds established in Section 3.03, "Requalification Examination Results," of IP 71111.11.

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates following the administration of the requalification annual operating tests and the biennial written examinations administered, which the facility licensee completed on 9/27/23 and 9/28/23, respectively.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Main Control Room during performance of 4-GOP-102, "Draining the Reactor Coolant System (RCS)" on October 5, 2023.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator requalification training in the simulator on October 31, 2023.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample [AP1000] (IP Section 03.01) (2 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Unit 4 risk mitigation activities with the RCS at reduced inventory during the week of October 15, 2023.
(2) Unit 3 online risk management of planned and emergent work activities during the week of November 26, 2023.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment [AP1000] (IP Section 03.01) (3 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) ODS-CR-11009833, Backleakage from RCS into CVS Makeup Line (2)

===11017912-Unit 3-ODS, Potential Use of Plywood in Unit 3 Containment Elevator Construction

(3) TE 1138793, Past Operability Review - Plywood in Unit 4 Containment Elevator

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01)===

(1) The inspectors evaluated the Unit 4 outage activities including the 2A reactor coolant pump replacement and the ADS stage 4 vibration issues from October 1 through December 31, 2023.

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) [AP1000] (IP Section 03.01) (2 Samples)

(1) Work Order # SNC1599740, Re-install 4-RCS-PL-L095 to Support 4-RCS-MP-02A Restoration on November 20, 2023.
(2) PCI Weld Process Traveler # 920484-005, Unit 4 / Pipe Support RCS-PH-11R2189 Reinstall on November 29, 2023.

Surveillance Testing [AP1000] (IP Section 03.01) (1 Sample)

(1)3-RLS-CSP-001, Hot Leg Grab Sample from RCS Train A on October 30, 2023.

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) Emergency Preparedness Training Evolution on November 1, 2023.

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Emergency Preparedness Drill on October 10,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

EP01: Drill/Exercise Performance (DEP) Sample [AP1000] (IP Section 02.12)===

(1) April 1, 2023 through December 31, 2023 EP02: Emergency Response Organization (ERO) Drill Participation [AP1000] (IP Section 02.13) (1 Sample)
(1) April 1, 2023 through December 31, 2023 EP03: Alert And Notification System (ANS) Reliability Sample [AP1000] (IP Section 02.14) (1 Sample)
(1) April 1, 2023 through December 31, 2023 BI01: Reactor Coolant System (RCS) Specific Activity Sample [AP1000] (IP Section 02.10) (1 Sample)
(1) Unit 3 (March 13, 2023 through September 25, 2023)

BI02: RCS Leak Rate Sample [AP1000] (IP Section 02.11) (1 Sample)

(1) Unit 3 (December 16, 2022 through October 30, 2023)

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) CAR 80000109, ADS Stage 4 Actuation Received during Maintenance Activity
(2) CAR 507319, Foreign Material in Core Makeup Line
(3) CAR 430119, Work Hour Rule Implementation Review

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)

The inspectors reviewed the licensees corrective action program and other licensee trending programs for potential adverse trends in its corrective action program (CAP) that might be indicative of a more significant safety issue.

(1) Assessment and Observations The inspectors determined the licensee's trending program was generally effective at identifying, monitoring, and correcting adverse performance trends before they could become more significant safety problems. The inspectors' evaluation did not reveal any new trends that would indicate a more significant safety issue. The inspectors determined, in most cases, issues were appropriately evaluated by the licensee's staff for potential trends at a low threshold and resolved within the scope of the CAP.

The inspectors observed a trend associated with an increase in CRs for personnel qualification standards (PQ&S) / fatigue/work hour waivers. The inspectors noted there were multiple CRs emphasizing the amount of fatigue/work hour waivers being processed. The inspectors also noted a trend with Level 2 CRs not being closed within 9 days in accordance with procedure ND-AD-002-028, Corrective Action Program Instructions.

71153 - Follow Up of Events and Notices of Enforcement Discretion Event Report [AP1000] (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05200025/2023-006-00, "Automatic Reactor Protection System Actuation During Startup Testing Due to the Auto Reactive Power Regulator Being Active While in Island Mode Operation." (ADAMS Accession No. ML23262A958)

The inspectors determined the cause of the condition described in the LER was not reasonably within the licensee's ability to have foreseen and corrected and therefore was not reasonably preventable. No performance deficiency nor violation of NRC requirements was identified. This LER is closed.

INSPECTION RESULTS

Failure to Adequately Implement Containment Closeout Resulting in Loose Debris and Unanalyzed Materials Left in Unit 4 Containment Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05200026/2023004-01 Open/Closed

[H.2] - Field Presence 71111.20 The inspectors identified a finding of very low significance (Green) with an associated NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings for the licensee's failure to properly implement their containment cleanliness and material control closeout procedure prior to and after Unit 4 entering Mode 4.

Description:

After the licensee had completed containment cleanliness activities in accordance with procedure 4-CNS-SOP-001 Attachment 4, Containment Closeout Inspection, the inspectors identified loose debris and materials that were not allowed to be inside containment during operation without an evaluation by the licensee in accordance with its procedure. The primary purpose of this procedure was to ensure no loose debris/materials were left in containment prior to plant start up from an outage that could either contribute to recirculation sump screen blockage during a design basis accident or get transported into a direct vessel injection or a cold leg LOCA break that becomes submerged during a design basis accident.

On September 20, the inspectors completed their independent verification of containment cleanliness prior to the licensee entering Mode 4. The inspectors identified fibrous and latent debris consisting of items such as lanyards, pig matting, wire brushes, metal clamps, tubing, paper, cords, plastic bottles, tape, and tie wraps. After identification of the material by the inspectors, the licensee removed these items from containment prior to entering Mode 4 on September 21, and Mode 3 on September 25, during which time the containment debris limits affecting operability of safety systems became applicable. The licensee documented the issue in their corrective action program as CRs 11009227 and 11014122.

On October 1, the licensee transitioned the plant to Mode 4, and then transitioned the plant to Mode 5 on October 3. On October 10, the NRC inspectors entered containment and identified a 4ft x 6ft sheet of plywood in the containment elevator shaft. This sheet of plywood exceeded the design limits of 6.6lbs of fibrous material. The licensee entered this issue in their corrective action program as CR 11014112, and performed a past operability review because the fibrous material was inside containment while the plant was in Mode 4. Based on the location of the material being outside of the recirculation flowpath and the fact that the plant had never achieved initial criticality to produce latent heat, the licensee concluded that the plywood would not have affected the operability of the core heat removal function during a design basis accident. The plywood was removed from containment prior to the plant transitioning to Mode 4 on December 23.

Corrective Actions: The licensee entered this violation into its CAP as CRs 11009227, 11014122, and 11014112 to evaluate the cause and to identify appropriate corrective actions.

The licensee took immediate corrective actions to remove the debris found by the inspectors and evaluated the past operability of the core heat removal function during a design basis accident.

Corrective Action References: CR 11009227, Debris Found During NRC Mode 4 Inspection, 09/22/2023 CR 11014122, GSI-191 Containment Cleanliness Debris Limits Exceeded, 10/10/2023 CR 11014112, 4' X 6' Sheet Of Plywood Found In U4 Containment Elevator Shaft, 10/10/2023

Performance Assessment:

Performance Deficiency: The licensees failure to perform an adequate containment cleanliness and material control closeout prior to and after Unit 4 entering Mode 4 in accordance with procedure 4-CNS-SOP-0 was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, loose materials/debris in containment could result in the materials/debris being transported to the recirculation sump screens in the event of design basis accident and adversely affect the sump performance or get transported into a direct vessel injection or a cold leg LOCA break that becomes submerged during a design basis accident and collect in reactor core flow channels.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix G, Shutdown Safety SDP. The inspectors assessed the significance of the finding using IMC 0609 Appendix G, Shutdown Operations Significance Determination Process. The inspectors performed a Phase 1 SDP review of this finding using IMC 0609, Appendix G, Attachment 1, "Shutdown Operations Significance Determination Process Phase 1 Initial Screening and Characterization of Findings, and determined this finding was of very low safety significance (Green) based on No answers to all of the Exhibit 3 - Mitigating Systems Screening Questions.

Cross-Cutting Aspect: H.2 - Field Presence: Leaders are commonly seen in the work areas of the plant observing, coaching, and reinforcing standards and expectations. Deviations from standards and expectations are corrected promptly. Senior managers ensure supervisory and management oversight of work activities, including contractors and supplemental personnel.

H.2 - Field Presence: Leaders are commonly seen in the work areas of the plant observing, coaching, and reinforcing standards and expectations. Deviations from standards and expectations are corrected promptly. Senior managers ensure supervisory and management oversight of work activities, including contractors and supplemental personnel.

The inspectors determined the finding had a cross-cutting aspect of Field Presence in the Human Performance area because the licensee failed to ensure adequate supervisory and management oversight of the containment closeout process was conducted to ensure proper performance of containment cleanliness and material control closeout procedures prior to and after Unit 4 entered Mode 4.

Enforcement:

Violation: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings states, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

3-CNS-SOP-001, Attachment 4, Step 4.5.a states: Locally check loose debris is NOT present in accessible areas of containment. IF loose debris is present in containment, THEN perform one of the following:

  • Remove debris OR
  • Document presence of debris per B-GEN-ENG-032-002, Control of Unattended Temporary Material in Containment in Modes 1-4.

Contrary to the above, from September 20, 2023, through October 10, 2023, NRC inspectors identified loose materials/debris, including fibrous materials, present in the Unit 4 containment without it having been documented or evaluated as acceptable to remain in containment in Modes 1 - 4.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 23, 2024, the inspectors presented the integrated inspection results to Mr.

Patrick Martino, VEGP 3&4 Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

3-PCS-SOP-001

Passive Containment Cooling System

Version 3.0

71111.01

Procedures

4-PCS-SOP-001

Passive Containment Cooling System

Version 1.0

71111.01

Procedures

B-GEN-OPS-009

Cold Weather Checklist

Version 4.0

71111.01

Procedures

NMP-OS-017

Severe Weather

Version 3.1

71111.04

Drawings

APP-PCS-M6-

001

Piping and Instrumentation Diagram Passive Containment

Cooling System

Revision 12

71111.04

Drawings

APP-PCS-M6-

2

Piping and Instrumentation Diagram Passive Containment

Cooling System

Revision 14

71111.04

Drawings

APP-PCS-M6-

003

Piping and Instrumentation Diagram Passive Containment

Cooling System

Revision 10

71111.04

Drawings

APP-PCS-M6-

004

Piping and Instrumentation Diagram Passive Containment

Cooling System

Revision 10

71111.04

Procedures

3-PCS-SOP-001

Passive Containment Cooling System

Version 3.0

71111.05

Corrective Action

Documents

Resulting from

Inspection

CR 11016977

NRC Identified Housekeeping Issues in Unit 3 Diesel

Building A & B

71111.05

Fire Plans

B-PFP-ENG-001-

F3101

Pre-Fire Plan - Containment Building EL 82'-6"

Version 2.0

71111.05

Fire Plans

B-PFP-ENG-001-

F3102

Pre-Fire Plan - Containment Building EL 92'-6"

Version 2.0

71111.05

Fire Plans

B-PFP-ENG-001-

F3600

Pre-Fire Plan - Diesel Generator Building

Version 4.0

71111.06

Corrective Action

Documents

CR 10977535

71111.06

Corrective Action

Documents

CR 50178817

71111.06

Miscellaneous

Vogtle 3&4 QA Monthly Report

August 2023

71111.06

Miscellaneous

VEGP 3&4 UFSAR

71111.06

Procedures

4-AOP-908

Internal Flooding Response

1.0

71111.06

Procedures

4-AOP-908-B

Background document for 4-AOP-908 Internal Flooding

Response

1.0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.11Q

Procedures

4-GOP-102

Draining the Reactor Coolant System (RCS)

Version 3.0

71111.13

Corrective Action

Documents

CR 11015501

Unexpected alarm on A Diesel Generator.

10/15/2023

71111.13

Miscellaneous

Work Logs Review

10/15/2023

71111.13

Procedures

B-ADM-OPS-018

Protected Division and Protected Equipment Program

Version 3.0

71111.13

Procedures

B-ADM-OPS-018

Protected Division and Protected Equipment Program

Version 3.0

71111.13

Procedures

NMP-DP-001

Operational Risk Awareness

Version 24.3

71111.13

Procedures

NMP-GM-031

On-Line Configuration Risk Management Program

Version 9.4

71111.13

Procedures

NMP-GM-031-

001

Online Maintenance Rule (a)(4) Risk Calculations

Version 8.0

71111.15

Corrective Action

Documents

CR 11014112

4' x 6' 3/4" Sheet Of Plywood Found In U4 Containment

Elevator Shaft

10/20/2023

71111.15

Corrective Action

Documents

CR 11009833

Back-leakage from RCS into CVS Makeup lines

09/25/2023

71111.15

Corrective Action

Documents

CR 11014122

GSI-191 Containment Cleanliness Limits Exceeded

10/11/2023

71111.15

Corrective Action

Documents

CR 11017912

Potential Use of Plywood in U3 Containment Elevator

Construction

10/23/2023

71111.15

Corrective Action

Documents

TE 1138793

Past Operability Review - Plywood in U4 Containment

Elevator

10/12/2023

71111.15

Miscellaneous

VEGP 3&4 IST Program Plant

3.0

71111.15

Miscellaneous

Vogtle Units 3

and 4 Technical

Specifications

and Basis

Technical specification 5.5.3 Inservice Testing Program

71111.15

Operability

Evaluations

11009833-U4-

ODS

Back-leakage from RCS into CVS Makeup lines

09/28/2023

71111.15

Operability

Evaluations

11017912-Unit3-

ODS

Potential Use of Plywood in U3 Containment Elevator

Construction

11/20/2023

71111.15

Procedures

4-CVS-OTS-10-

2

Chemical And Volume Control System Check Valve

Exercise Test

1.0

71111.15

Procedures

NMP-AD-012

Operability Determinations

16.1

71111.15

Procedures

NMP-AD-012-F01

Operability Determination Support bases

4.1

71111.20

Corrective Action

11007847

Permanent ADS 4 Sensors Out Of Line

09/18/2023

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

71111.20

Corrective Action

Documents

11017846

Unit 4 entry into TR 3.0.3 due to RCP 2A Replacement

Outage

10/23/2023

71111.20

Corrective Action

Documents

CR 11025404

Base Metal Repairs required for Electrical Supports in 11202

(Support RCP 2A replacement)

11/17/2023

71111.20

Corrective Action

Documents

CR 11025415

Base Metal Repair for 1120-1251618-C15-028 (Supports

RCP 2A Replacement)

11/17/2023

71111.20

Corrective Action

Documents

CR 11033385

Unit 4 ADS 4 Vibration Alarm in

2/21/2023

71111.20

Corrective Action

Documents

CR 11034094

High Vibrations on Stage 4 ADS B & D

2/26/2023

71111.20

Corrective Action

Documents

Resulting from

Inspection

CR 11008843

T&B "Ty-Rap and 3M Co. No. 35 Insulating/Color Coding

Tapes

09/21/2023

71111.20

Corrective Action

Documents

Resulting from

Inspection

CR 11009227

Debris Found During NRC Mode 4 Inspection

09/22/2023

71111.20

Corrective Action

Documents

Resulting from

Inspection

CR 11014112

4' X 6' Sheet Of Plywood Found In U4 Containment Elevator

Shaft

10/10/2023

71111.20

Corrective Action

Documents

Resulting from

Inspection

CR 11014122

GSI-191 Containment Cleanliness Debris Limits Exceeded

10/10/2023

71111.20

Engineering

Changes

SNC1643809

Impact damage to RCP 2A and 2B Flanges During

Installation

Rev. 0

71111.20

Engineering

Evaluations

1141432

Base Metal Repair for 1120-1251618-C15028 (Supports

RCP 2A Replacement)

11/18/2023

71111.20

Miscellaneous

APP-GW-GLR-

079

AP1000 Verification of Water Sources for Long-Term

Recirculation Cooling Following a LOCA

Rev. 9

71111.20

Miscellaneous

APP-MH17-VNM-

AP1000 RCP Installation Cart Technical Manual

Rev. 3

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

001

71111.20

Miscellaneous

SV4-MP01-MEW-

1016971

ASME III - Install RCP 2A Heat Exchanger SV4-RCS-MP-

2A_HX Including Associated Piping

Rev. 0

71111.20

Operability

Evaluations

TE 1138793

Past Operability Review - Plywood in U4 Containment

Elevator

10/12/2023

71111.20

Procedures

4-CNS-SOP-001

Containment System, Attachment 4, Containment Closeout

Inspection

Version 2.0

71111.20

Procedures

4-GEN-ITPS-606

Post-Fuel Loading Precritical Test Sequence Startup Test

Procedure

Version 2.0

71111.20

Procedures

4-GEN-ITPS-618

Power Ascension Test Sequence Startup Test Procedure

Version 3.0

71111.20

Procedures

4-GOP-205

Plant Cooldown Mode 3 to Mode 5

Version 1.0

71111.20

Procedures

4-GOP-301

Mode Change Checklists

Version 1.1

71111.20

Procedures

4-GOP-303

Plant Heatup Mode 5 to Normal Operating Temperature

Version 3.0

71111.20

Procedures

4-RNS-SOP-001

Normal Residual Heat Removal System

Version

E=0.4

71111.20

Procedures

B-GEN-ENG-032

Containment Cleanliness and Sampling Program

Version 1.0

71111.20

Procedures

B-GEN-ENG-032-

001

Containment Debris Sampling

Version

A=0.0

71111.20

Procedures

B-GEN-ENG-032-

2

Control of Temporary Unattended Material in Containment in

Modes 1-4

Version 1.1

71111.20

Procedures

B-GEN-OPS-006

Containment Entry

Version 3.1

71111.20

Work Orders

SNC1588324

RCP 2A - Reinstall RCP Heat Exchanger

Rev. 0

71111.20

Work Orders

SNC1599802

Assemble / Disassemble / Reconfigure RCP Installation Cart

For 4-RCS-MP-02A Replacement

Rev. 0

71111.20

Work Orders

SNC1607533

Perform post work testing on ADS stage 4 vib sensors 4-

RCS-YE341D (ADS Stage 4 V014D X Vib).

Rev. 0

71111.24

Miscellaneous

PCI Traveler

Number 920484-

005

Unit 4 / Pipe Support RCS-PH-11R2189 Reinstall

71111.24

Procedures

3-RLS-CSP-001

Primary System Sampling Using the RSI Primary Sampling

Panel

Version 5.0

71111.24

Procedures

B-GEN-CRC-002

Guidelines for Radiochemistry Data Review Using APEX

Version 1.0

71111.24

Work Orders

SNC1599740

Re-install 4-RCS-PL-L095 to support 4-RCS-MP-02A

Restoration

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71114.06

Corrective Action

Documents

CR 11014269

VEGP 3&4 ERO Training Drill (Simulator EDS Issues)

10/11/2023

71114.06

Corrective Action

Documents

CR 11014278

VEGP 3&4 ERO Training Drill (TSC EPBX Phone Plant

Page Issue)

10/11/2023

71114.06

Miscellaneous

Drill Packet for the October 10, 2023 Emergency

Preparedness Drill.

10/10/2023

71114.06

Miscellaneous

AP-LT-C-SG-

241B

LOCT 24-1 Integrated Training Scenario 241B

Revision 1.2

71114.06

Procedures

NMP-EP-146-F01

CR Emergency Director

Revision 6

71114.06

Procedures

NMP-EP-303-F02

Drill and Exercise Comment and Feedback Form

2.0

71114.06

Procedures

NMP-EP-303-F03

Drill & Exercise Observation Form

1.0

71151

Miscellaneous

eSOMS Narrative / Unit Logs

71151

Procedures

SNC Standard Emergency Plan

Rev. 7

71151

Procedures

3-RLS-CSP-001

Primary System Sampling Using the RSI Primary Sampling

Panel

Version 5.0

71151

Procedures

B-GEN-CRC-002

Guidelines for Radiochemistry Data Review Using APEX

Version 1.0

71151

Procedures

NMP-AD-029

Preparation and Reporting of Regulatory Assessment

Performance Indicator Data and the Monthly Operating

Report

Rev. 3.2

71151

Procedures

NMP-EP-308

SNC Emergency Alert Siren Operation, Testing and

Maintenance

Rev. 4.1

71152A

Corrective Action

Documents

CAR 507319

Foreign Material Found in Core Makeup

71152A

Corrective Action

Documents

CAR 80000109

ATV-CAR-80008714 Perform O&P IAW ND-AD-006

Requirement ADS Stage 4 Actuation Received during

Maintenance Activity

71152A

Corrective Action

Documents

CR 1090022

April PQS review

05/08/2023

71152A

Corrective Action

Documents

CR 10957063

Work hour waiver

03/16/2023

71152A

Corrective Action

Documents

CR 10957305

Work hour waiver

03/17/2023

71152A

Corrective Action

Documents

CR 10957416

Work hour waiver

03/18/2023

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152A

Corrective Action

Documents

CR 10957543

Work hour waiver

03/18/2023

71152A

Corrective Action

Documents

CR 10961421

Work hour waiver

03/31/2023

71152A

Corrective Action

Documents

CR 10961650

Work hour waiver

04/02/2023

71152A

Corrective Action

Documents

CR 10961747

Work hour waiver

04/03/2023

71152A

Corrective Action

Documents

CR 10961863

Work hour waiver

04/03/2023

71152A

Corrective Action

Documents

CR 10962231

Work hour waiver

04/04/2023

71152A

Corrective Action

Documents

CR 10962272

Work hour waiver

04/04/2023

71152A

Corrective Action

Documents

CR 10962577

Work hour waiver

04/05/2023

71152A

Corrective Action

Documents

CR 10962869

Work hour waiver

04/06/2023

71152A

Corrective Action

Documents

CR 10963509

Work hour waiver

06/27/2023

71152A

Corrective Action

Documents

CR 10963719

Work hour waiver

04/11/2023

71152A

Corrective Action

Documents

CR 10964151

Work hour waiver

04/12/2023

71152A

Corrective Action

Documents

CR 10964165

Work hour waiver

04/12/2023

71152A

Corrective Action

Documents

CR 10965908

Work hour waiver

04/12/2023

71152A

Corrective Action

Documents

CR 10966124

Work hour waiver

04/20/2023

71152A

Corrective Action

Documents

CR 10966251

Work hour waiver

04/21/2023

71152A

Corrective Action

Documents

CR 10966278

Work hour waiver

04/21/2023

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152A

Corrective Action

Documents

CR 10967156

Work hour waiver

04/26/2023

71152A

Corrective Action

Documents

CR 10967892

Work hour waiver

04/28/2023

71152A

Corrective Action

Documents

CR 10968034

Work hour waiver

04/30/2023

71152A

Corrective Action

Documents

CR 10968844

Work hour waiver

05/03/2023

71152A

Corrective Action

Documents

CR 10969257

Work hour waiver

05/04/2023

71152A

Corrective Action

Documents

CR 1096941

Work hour waiver

05/03/2023

71152A

Corrective Action

Documents

CR 10969412

Work hour waiver

05/05/2023

71152A

Corrective Action

Documents

CR 10969763

Work hour waiver

05/07/2023

71152A

Corrective Action

Documents

CR 10969952

Work hour waiver

05/08/2023

71152A

Corrective Action

Documents

CR 10970939

Work hour waiver

05/11/2023

71152A

Corrective Action

Documents

CR 10971265

April PQS validations

05/12/2023

71152A

Corrective Action

Documents

CR 10977804

Late validations

06/07/2023

71152A

Corrective Action

Documents

CR 10978349

Operations PQS validations

06/08/2023

71152A

Corrective Action

Documents

CR 10979104

May PQS review

06/12/2023

71152A

Corrective Action

Documents

CR 10981610

Ops schedule change not updated in PQS

06/20/2023

71152A

Corrective Action

Documents

CR 10982070

PQS timeliness

06/22/2023

71152A

Corrective Action

Documents

CR 10983575

Discrepancy between time worked and PQS

06/27/2023

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152A

Corrective Action

Documents

CR 10983737

Identified work hour waiver deficiencies

06/28/2023

71152A

Corrective Action

Documents

CR 10983899

Work performed without PQS being updated

06/28/2023

71152A

Corrective Action

Documents

CR 10985348

Late PQS validation

07/05/2023

71152A

Corrective Action

Documents

CR 10985348

PQS not updated before work occurred

07/05/2023

71152A

Corrective Action

Documents

CR 10985724

PQS not updated before work occurred

07/06/2023

71152A

Corrective Action

Documents

CR 10985959

June PQS review

07/07/2023

71152A

Corrective Action

Documents

CR 1098601

Potential work hour violation not flagged by PQS

07/10/2023

71152A

Corrective Action

Documents

CR 10986620

PQS not configured to calculate min day off during outage

07/10/2023

71152A

Corrective Action

Documents

CR 10986632

Fatigue assessment

07/10/2023

71152A

Corrective Action

Documents

CR 10987476

Mid-year Part 26 review

07/13/2023

71152A

Corrective Action

Documents

CR 10987655

Work hour rule violation not recognized

07/13/2023

71152A

Corrective Action

Documents

CR 10987664

June PQS revalidations

07/13/2023

71152A

Corrective Action

Documents

CR 10987751

Unrecognized work hour rule violation

07/13/2023

71152A

Corrective Action

Documents

CR 10987845

Work hour rule not recognized

07/14/2023

71152A

Corrective Action

Documents

CR 50179773

ADS Stage 4 Actuation Received during Maintenance

Activity

71152A

Corrective Action

Documents

CR 90000368

CR 50179773 ADS Stage 4 Actuation during Maintenance

Activity

71152A

Corrective Action

Documents

TE 1137826

Ensure CIM Audit Was Performed Nightly until Configuration

Control Was Established

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152A

Corrective Action

Documents

TE 1137828

Ensure 7 Risk-Based Questions Are Being Asked at Work

Controls by Each WCC SRO or Every Work Group

71152A

Corrective Action

Documents

TE 1138943

Ensure Proper Oversight for All Vendors

71152A

Miscellaneous

EN 56779

60-Day Optional 10 CFR 50.73(a)(1) Report of Invalid

Specified System Actuation

71152S

Corrective Action

Documents

CAR 430119

PQ&S Waivers/Violations Adverse Trend

71152S

Corrective Action

Documents

CAR 527372

Perform CCA for Adverse Trend in Unit 3 CAP CRs not

closed within 9 Days

71152S

Corrective Action

Documents

CR 10967156

PQ&S Waivers/Violations Adverse Trend

71152S

Corrective Action

Documents

CR 11010437

Adverse Trend in Unit 3 CAP CRs Not Closed Within 9 Days

- MRC Identified

71152S

Corrective Action

Documents

CR 11017115

NDQA Identified - Basis For Fatigue Management Waiver

Did Not Meet Procedure Requirements

71152S

Corrective Action

Documents

CR 11017120

NDQA Identified - Fatigue Management Waiver Form -

Section 3 Was Incomplete Per Procedure Requirements

71152S

Corrective Action

Documents

CR 11017146

WEC CAP IR 2023-6889 - Communication Of Westinghouse

CAP Items (SVP_SV0_230248) PIN 02822

71152S

Corrective Action

Documents

CR 11018220

Weekly Review of PQ&S Data 9/3-9/9/2023 - Operations

71152S

Corrective Action

Documents

TE 1129429

Add Work Hour Rule Software Training To SRO Continuing

Training (SRO LOCT)

71152S

Corrective Action

Documents

TE 1129430

Scheduling: Complete Business Case To Evaluate Better

Software To Track Work Hour Rules And Schedule

71152S

Corrective Action

Documents

TE 1129663

Raise Licensed and Non-licensed Operations Staffing

71152S

Corrective Action

Documents

TE 1140428

Evaluate CR Closure Timeliness

71152S

Miscellaneous

Unit 3 & 4 Weekly Management Review Committee Packet

71152S

Miscellaneous

Audit Report #

23-S&W-2

ASME QAI-1 Audit

07/24/2023

71152S

Procedures

NMP-GM-003

Self-Assessment and Benchmark Procedure

Version 35.0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71153

Corrective Action

Documents

CAR 479744

Unplanned Reactor Trip During 3-GEN-ITPS-633, 100%

Load Rejection Startup Test Procedure

71153

Engineering

Changes

E&DCR SV3-

ZAS-GEF-034

MSU Relay RY1 V/Hz Trip

Revision 0

71153

Engineering

Changes

SNC 1520848

Change to PLS Logic to Disable AQR Mode When Plant

Enters Island Mode

Revision 0

71153

Miscellaneous

LER 2023-006-00

Automatic Reactor Protection System Actuation During

Startup Testing Due to the Auto Reactive Power Regulator

Being Active While in Island Mode Operation

09/19/2023

71153

Procedures

3-GEN-ITPS-633

100% Load Rejection Startup Test Procedure

Version 5.0

71153

Procedures

3-GOP-101

Power Operations Above 25% Power

Version 2.0