ML20038C728: Difference between revisions

From kanterella
Jump to navigation Jump to search
(StriderTol Bot insert)
 
(StriderTol Bot change)
 
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:}}
{{#Wiki_filter:MRC FORM 366                                                                                                                                U, S. NUCLE AR REGUL ATORY COMMISSION (7-77) "
    -                                                                                  LICENSEE EVENT F EPORT CONTROL BLOCK: l 1
l    l        1        l    l 6
lh                (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo l1l l SlC lH lB lR l2 l@l0l0l-l0l0l0l0l0l-l0l0l@l4l1l1l1l1l@l 7      8 9              LICENSEE CODE                  14      15                          LICENSE NUMBEH                    25      26      LICENSE TYFE JO l
57 CAT 68 l@
CON'T 10111                3$0RcE              l L l@l          0] 5DOCKET l 0 l 0NUMBER  l 0 l 2 l 6 68l 1 @l        111    l 0 l 2 l 81174 l@l75 112REPORT        l 0 lD2ATEl 8 l 180 l@
7        8                        60            61                                                        69        EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10 l 2 l [ On November 2, 1981, a t 1906 hours, with the unit at 50% power, "B"                                                                                emergency diesel          l 90 ,3; l genera tor was declared inoperable when it failed to manually start during Periodic                                                                                                l 1 o l 4 l l Test PT-23.1.                          '1his resulted in a degraded mode of operation permitted by Technical                                                                  l
; o ; ,, ; l Specifica tion (T.S.) 3.7.2.d and is reported pursuant to T. S . 6. 9. 2. b . 2.                                                                            The                l l o Ic i Iredundant emergency diesel genera tor was demonstrated operable just prior to this                                                                                                l 10171 l event, therefore there was no threat to the public health and safety.                                                                                                              l Io18l l                                                                                                                                                                                    l 7      8 9                                                                                                                                                                              80 SYSTE"1                CAUSE                C AUS E                                                    COVP.          VAL %E CODE                  CODE              SU9 CODE                COYPONENT CCDE                    SUBCODE          SUBCODE yg                                    i El El@ l Xl@ l X l@ lE lN lG lI lN lE l@ l zl@ W @
9          10                                  12                                            18                          Vo 7        8                                                        11                                13                                        19 cEGLENTI AL                      OCCLA R E NCE          REPORT                    REVISION traq            EL ENT YE AR                                      REPORT NO.                            CODE                TYPE                        N O.
              @ Mg'' g                  18111                    1-1                1012151                1/1          10 13 I    '
Itl            I-I          10 I
_2t            22            23                  24            26      27            28        .)          30              Jt          32 ACTlON ruTURE                        EFFECT            SHUTDOWN                                      A TT ACHV E NT        NPR D-4      PRIME COVP.            COVPONENT TAKEN ACTION                      CN PLANT              ME THOD                      HOURS            SUBVITTED        FORM 5UB.        SUPP LIE R          MANUFACTURER IXl@lzl@ W@
JJ            34                    35 lzl@
2n 10 101010 I
                                                                                            ~.
Je                  40 LY 41 J@          IN 42 l@          l43A l@        {l0l1 l0l@
44            47 CAUSE DESCRIPTION AND CCRRECTIVE ACTIONS g g lThe cause of failure was loss of prime in the fuel oil system. This may have been due l
[i ;; j to debris in the ball check valve which allowed fuel oil to drain back to the day tank.1
, , , ,      [There was no actual debris found in the ball check valve or the piping.                                                                                'h e "B"              g
;, ;3; diesel generator was successfully tested and declared operable on November 2, 1981,                                                                                        l
    , g, g gat 2208 hours.                                                                                                                                                                  ;
7      ri    7                                                                                                                                                                          90 ST                      X PC/.E H                          CTHE R ST A TL3                sr                                    CiSCON EHV DESCRIPTION l1 l5l(E_j @ l0l510l@l                                                        NA                    l  lC B l@l                          Operator Observat ion                          l 1                to                12        13                                    44                46                                                                  80 ACTtVITY        CON TENT FELEASED GF HE LE AIE                            AYOU NT CF ACTl vlTY                                                            LOC A TION OF RE L E ASE '
NA                                                                          NA                                J li Is l I zl @ I z l@l
  /      a    #                10            tt                                                  44 I        I 45                                                                        80 PE RT s    '.E L f x % UU L'
                    ,  .9En TYPF          DE 5( O t f i t 'f a  -
NA I' I 7 I I 0101 Ol@l Zi@l                                13                                                                                                                              80 l
1      H <>                    11        12 PE P LGN N E L i'. J1i E 3 Pc. R[R              DESCRIPi!O*4 NA IiI1l01010l@l 1      4 3                    11        12                                                                                                                                            80 l
Lir .rJ ;.n L        '. A M T O F AC i L 17 Y m            w .'m.m l2 l9l lZ l@l 7      4    't            1;i NA go l
5W I          lY      ,
l':P T ; 79
              $..-(
I#
I"I "dd                                                                                                        NA                                l lllllllllllll[
                                                                                                                                                                                        " 3 N112140578811202                                            Howard T. Cox                                                          gggy g .    @D E4M                                2 PDR ADOCK 05000261 ra                                        EDR 3                                                                                                                                  o
 
SUPPLEMENTAL INFORMATION FOR LICENSEE EVENT REPORT 81-025
: 1. Cause Description and Analysis:
On November 2, 1981, a t 1906 hours, "B" diesel genera tor '(DG) fa iled to manually start during the weekly Periodic Test of both DG's.      "A" DG was demonstrated operable just prior to "B" DG's failure to start.
Two additional unsuccessful starts were attempted. "B" DG fuel oil lines were then primed with the hand pump, which resulted in successfully starting the DG, The failure of "B" DG to start is believed to be the result of debris in the ball check valve which allowed fuel to drain back to the day tank.
It should be noted that during a manual DG start (used during the Periodic Test) the air start solenoids will open for only 10 seconds which may not have provided adequate time to prime the fuel oil lines.
However, during an automa tic start of a DG (safeguards actuation), the time the air start solenoids are open is not limited, and therefore the diesel would probably have started on an automatic signal.
        "B" DG's failure to sta rt, a degraded mode of operation as described in Technical Specification 3.7.2.d, is repot ted pursuant to 6.9.2.b.2.
: 2. Corrective Action:
The fuel oil lines and ball check valve were disassembled, inspected, reassembled and "B" DG returned to an operable condition at 2208 hours on November 2, 1981.
: 3. Co rrec t ive Ac t io n to Prevent Recurrence:
No further action is considered necessary.}}

Latest revision as of 23:45, 1 March 2020

LER 81-025/03L-0:on 811102,emergency Diesel Generator B Failed to Start Manually.Caused by Loss of Prime in Fuel Oil Sys,Possibly Due to Debris in Ball Check Valve.Generator Returned to Svc
ML20038C728
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 12/02/1981
From: Cox H
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20038C721 List:
References
LER-81-025-03L, LER-81-25-3L, NUDOCS 8112140078
Download: ML20038C728 (2)


Text

MRC FORM 366 U, S. NUCLE AR REGUL ATORY COMMISSION (7-77) "

- LICENSEE EVENT F EPORT CONTROL BLOCK: l 1

l l 1 l l 6

lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo l1l l SlC lH lB lR l2 l@l0l0l-l0l0l0l0l0l-l0l0l@l4l1l1l1l1l@l 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBEH 25 26 LICENSE TYFE JO l

57 CAT 68 l@

CON'T 10111 3$0RcE l L l@l 0] 5DOCKET l 0 l 0NUMBER l 0 l 2 l 6 68l 1 @l 111 l 0 l 2 l 81174 l@l75 112REPORT l 0 lD2ATEl 8 l 180 l@

7 8 60 61 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10 l 2 l [ On November 2, 1981, a t 1906 hours0.0221 days <br />0.529 hours <br />0.00315 weeks <br />7.25233e-4 months <br />, with the unit at 50% power, "B" emergency diesel l 90 ,3; l genera tor was declared inoperable when it failed to manually start during Periodic l 1 o l 4 l l Test PT-23.1. '1his resulted in a degraded mode of operation permitted by Technical l

o ; ,, ; l Specifica tion (T.S.) 3.7.2.d and is reported pursuant to T. S . 6. 9. 2. b . 2. The l l o Ic i Iredundant emergency diesel genera tor was demonstrated operable just prior to this l 10171 l event, therefore there was no threat to the public health and safety. l Io18l l l 7 8 9 80 SYSTE"1 CAUSE C AUS E COVP. VAL %E CODE CODE SU9 CODE COYPONENT CCDE SUBCODE SUBCODE yg i El El@ l Xl@ l X l@ lE lN lG lI lN lE l@ l zl@ W @

9 10 12 18 Vo 7 8 11 13 19 cEGLENTI AL OCCLA R E NCE REPORT REVISION traq EL ENT YE AR REPORT NO. CODE TYPE N O.

@ Mg g 18111 1-1 1012151 1/1 10 13 I '

Itl I-I 10 I

_2t 22 23 24 26 27 28 .) 30 Jt 32 ACTlON ruTURE EFFECT SHUTDOWN A TT ACHV E NT NPR D-4 PRIME COVP. COVPONENT TAKEN ACTION CN PLANT ME THOD HOURS SUBVITTED FORM 5UB. SUPP LIE R MANUFACTURER IXl@lzl@ W@

JJ 34 35 lzl@

2n 10 101010 I

~.

Je 40 LY 41 J@ IN 42 l@ l43A l@ {l0l1 l0l@

44 47 CAUSE DESCRIPTION AND CCRRECTIVE ACTIONS g g lThe cause of failure was loss of prime in the fuel oil system. This may have been due l

[i ;; j to debris in the ball check valve which allowed fuel oil to drain back to the day tank.1

, , , , [There was no actual debris found in the ball check valve or the piping. 'h e "B" g

, ;3; diesel generator was successfully tested and declared operable on November 2, 1981, l

, g, g gat 2208 hours0.0256 days <br />0.613 hours <br />0.00365 weeks <br />8.40144e-4 months <br />.  ;

7 ri 7 90 ST X PC/.E H CTHE R ST A TL3 sr CiSCON EHV DESCRIPTION l1 l5l(E_j @ l0l510l@l NA l lC B l@l Operator Observat ion l 1 to 12 13 44 46 80 ACTtVITY CON TENT FELEASED GF HE LE AIE AYOU NT CF ACTl vlTY LOC A TION OF RE L E ASE '

NA NA J li Is l I zl @ I z l@l

/ a # 10 tt 44 I I 45 80 PE RT s '.E L f x % UU L'

, .9En TYPF DE 5( O t f i t 'f a -

NA I' I 7 I I 0101 Ol@l Zi@l 13 80 l

1 H <> 11 12 PE P LGN N E L i'. J1i E 3 Pc. R[R DESCRIPi!O*4 NA IiI1l01010l@l 1 4 3 11 12 80 l

Lir .rJ ;.n L '. A M T O F AC i L 17 Y m w .'m.m l2 l9l lZ l@l 7 4 't 1;i NA go l

5W I lY ,

l':P T ; 79

$..-(

I#

I"I "dd NA l lllllllllllll[

" 3 N112140578811202 Howard T. Cox gggy g . @D E4M 2 PDR ADOCK 05000261 ra EDR 3 o

SUPPLEMENTAL INFORMATION FOR LICENSEE EVENT REPORT 81-025

1. Cause Description and Analysis:

On November 2, 1981, a t 1906 hours0.0221 days <br />0.529 hours <br />0.00315 weeks <br />7.25233e-4 months <br />, "B" diesel genera tor '(DG) fa iled to manually start during the weekly Periodic Test of both DG's. "A" DG was demonstrated operable just prior to "B" DG's failure to start.

Two additional unsuccessful starts were attempted. "B" DG fuel oil lines were then primed with the hand pump, which resulted in successfully starting the DG, The failure of "B" DG to start is believed to be the result of debris in the ball check valve which allowed fuel to drain back to the day tank.

It should be noted that during a manual DG start (used during the Periodic Test) the air start solenoids will open for only 10 seconds which may not have provided adequate time to prime the fuel oil lines.

However, during an automa tic start of a DG (safeguards actuation), the time the air start solenoids are open is not limited, and therefore the diesel would probably have started on an automatic signal.

"B" DG's failure to sta rt, a degraded mode of operation as described in Technical Specification 3.7.2.d, is repot ted pursuant to 6.9.2.b.2.

2. Corrective Action:

The fuel oil lines and ball check valve were disassembled, inspected, reassembled and "B" DG returned to an operable condition at 2208 hours0.0256 days <br />0.613 hours <br />0.00365 weeks <br />8.40144e-4 months <br /> on November 2, 1981.

3. Co rrec t ive Ac t io n to Prevent Recurrence:

No further action is considered necessary.