05000261/LER-1981-004-03, Primary Coolant Sys Leak Found.Caused by Sample Cooler Tube Bundle Leakage Due to Normal Wear.Bundle Replaced.Review of Maint Records Revealed No Generic Problems

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Primary Coolant Sys Leak Found.Caused by Sample Cooler Tube Bundle Leakage Due to Normal Wear.Bundle Replaced.Review of Maint Records Revealed No Generic Problems
ML20009H358
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 07/30/1981
From: Paine E
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009H356 List:
References
LER-81-004-03L, LER-81-4-3L, NUDOCS 8108100008
Download: ML20009H358 (2)


LER-1981-004, Primary Coolant Sys Leak Found.Caused by Sample Cooler Tube Bundle Leakage Due to Normal Wear.Bundle Replaced.Review of Maint Records Revealed No Generic Problems
Event date:
Report date:
2611981004R03 - NRC Website

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NRC Ff)RM 36h Update Report - Previous Report Date 2/13/81 ' S. NUCLEAR REGULATORY CoMMISSloN 1

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l o l 2 I lAt 1228 hours0.0142 days <br />0.341 hours <br />0.00203 weeks <br />4.67254e-4 months <br /> during normal operation on 1-16-81, indication of leakage to the CCW l

I o l a i ISystem prompted a RCS leak rate test which verified a 2.37 gpm leak rate.

Inves tiga-l 10 l 4 l l tion revealed that the leak path was from the pressurizer through the pressurizer i

tolsl l liquid space sample cooler to the CCW System via a leaking tube bundle in the sample l

I o 16 l l cooler. The lenkage experienced is contrary to the requirements of T.S. 3.1.5.2 and j

l o l 7 l lis reportable per T.S. 6.9.2.b(2). All leakage was contained within a closed plant l

l o is l l radioactive system and there was no threat to plant or public health or safetv.

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33 34 35 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i l o l [Ihe sample line isolation valves were closed as immediate corrective action. The root l l3 lij lcause of the event was the failure of the sample cooler tube bundle. The tube bundle l

l3 l7; [was replaced to prevent recurrence. Failure was attributed to normal operational l

lil3l l wear. Review of maintenance records revealed no generic implications with the reportedl L g [ failure. Therefore, a further action is necessary.

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Cause Description and Analysis On 1-16-81 at 1228 hours0.0142 days <br />0.341 hours <br />0.00203 weeks <br />4.67254e-4 months <br />, the combination of a volume control tank

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makeup signal, an increasing component cooling water- (CCW) surge tank level and an increasing radiation reading from the CCW System radiation monitor alerted the operators to the possibility.of a Primary Coolant-1 System leak. A RCS leak test was initiated and, at 1244 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.73342e-4 months <br />, RCS leakage was verified and. determined to be 2.37 gpm.-

At 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br />;the pressurizer liquid sample line isolation valves, which are normally opened during day shift operations for sampling, were.promptly closed.-

A second RCS leak test was performed and, at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br />, the RCS leak ~

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rate was-determined to'be essentially zero. No further increase in CCW surge tank level or CCW radiation monitor readings occurred follow-ing the closure of the sample line isolation valves. The leak path i

was subsequently identified as being'from the pressurizer liquid space throup the sample line into the sample cooler and into the CCW System via a leaking tube bundle in the cooler. The leakage experienced was in excess of the limits allowed by Technical Specification Section 3.1.5.2 and is reportable in accordance with Technical Specification-6.9.2.b(2).

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The cause of the event was the sampic cooler tube bundle. leakage. The tube bundle leakage is attributed to normal wear.

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- Since the RCS leakage ^was totally contained within the CCW System,_

which is a closed radioactive system, there.was no threat to either.

the plant or to the public health or safety.

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Corrective Action

The sample line isolation valves were closed ~to eliminate further leakage as immediate corrective action.

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Corrective Action to Prevent Further Occurrence The sample cooler tube bundle was removed and replaced. A review of' maintenance records on this~and other similar sample coolers was performed to' determine if any generic. problems could.be identified which would indicate a need for further corrective' action..This i

review revealed that all sample coolers.have operated'in a reliable manner and no generic problems were identified Specifically,'since the beginning of operation, only three cooler tube bundle _ftilures have occurred for six sample coolers (i.e.,:three separate failures in approximately 60 tube bundle years of operation) and ru) cooler l-tube bundles have failed more than once.

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Therefore, the sample cooler operation is' considered to be sufficiently-j reliable'and no further corrective action is deemed necessary, i

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