LER-1981-016, /03L-0:on 810611,during Startup,Motor Driven Auxiliary Feedwater Pump a Tripped Due to Low Discharge Pressure While Feeding Steam Generators.Event Reoccurred on 810716.Caused by Backleakage Through Discharge Valve AFW-40 |
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FORM 366 m S. NC6 EAR REGUMcTORY COMMIS$iGN 7
(7-77) #
LICENSEE EVENT REPORT e
CONTROL BLOCX: l l
l l
l l lh (PLEASE PRINT OA TYPE ALL REQUIRED INFORMATION) i 6
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7 8 9 LICENSEE CODE 14 15 eCENSE NUMBER 25 26 LICENSE Ty 30 57 CAT 50 CON'T
(.0 l I l 3$n"CE l L }@l 0 l 5 l 0 l 0 l 0 l 2 l 6 l 1 @l 0 l 6 l 1 l ' l 8 l 1 @l 0 17 l 1 l 0 l 8 l 1 l 7
8 60 61 DOCKET NUM8ER 68 69 EVENT DATE 74 75 REPORT D ATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h io l2l l On June 11, 1981, at 1145 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.356725e-4 months <br />, during plant startup, "A" Motor Driven A W Pump was l
Iol3l l noted to be tripped due to low discharge pressure while feeding the steam generators. I lol4l l On June 16, 1981, at 2115 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.047575e-4 months <br />, with unit at 93% power, "A" AW pump tripped durine I
lo Isl l performance of Periodic Test 22.1C.
The remaining operable AW pump provides 100%
l l 0 l6 l l feedwater capacity and so there was no threat to public health and safety.
Since the l l o l 7 l l Steam Driven AW Pump was inoperable, this resulted in operation in a degraded mode l
I o Is l l permitted by Tech. Spec. 3.4.3 which is reportable pursuant to 6.9.2.b.2.
I 80 7
8 9 SYSTEM
CAUSE
CAUSE COYP.
VALVE CODE CODE SU8 CODE CO*jPONENT CODE SUSCODE SU8 CODE l0l91 l Hj H]h Wh l B lh lP lU lM lP lX lX lh lBl@ lZlh 7
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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LE R RO EVENT YEAR R EPORT NO.
CODE TYPE N O.
@ REPORT l8 l1 l l-l l0 l1 l6 l
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_ 21 22 2J 24 26 27 28 29 30 31 32 TAKEN A TO ON PLANT T
HOURS S 8 i FO 1 8.
SUPPLIE MAN FACTURER l B l@l Z lh l35Zl@ l Z lh l70 l0 l010 l lY l@
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3J 34 36 3
40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i j o l l Af ter the fitst pump trip, the discharge valve was readjus ted.
Af ter the second l
li li j l pump trip, the cause of both trips was determined to be backleakage throuch motor 1
l operated discharge valve V2-16A and check valve AW-40 which created steam binding l
i,,,i lil3l l with u the pump casing.
These valves were reworked which reduced the backleakage.
l [i i4 ; j Additionally, as a precautionary measure, the pump casing is being vented hourly.
I 80 7
8 9 ST S
% POWER OTHER STATUS IS OV RY DISCOVERY DESCRIPTION NA l
l A l@l Operator Observation l
l1 l5 l dh l 0 l 0 l 0 lh' A TiVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE NA l
l NA l
li 161 I 21 @ l Z l@l 7
8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUV8ER TYPE
DESCRIPTION
l Ii I 7 I l 0l ol Ol@l Zl@l NA w
2 a
Pe RSONN E L,Nau'R,,,
NUv8ER
DESCRIPTION
l 11 1a 1 l 0l 0l Ol@l NA 80 7
8 9 11 12 LOSS OF OR DAVAGE TO FACILITY TYPE
DESCRIPTION
NA l
Q lZl@l 80 7
8 9 10
[ 8108030344 810710 NRc uSE ONLY PDR NA l llllllllll l l l :1 PDR ADOCK 05000261 68 69 80 5 i
7 iu (803) 383-4524
{
Howard T. Cox psoyg NAME OF PR3 PARER
?-__<
e Supplemental Information for Licensee Event Report 81-16 1.
Cause Description and Analysis:
On June 11, 1981, at 1143 hours0.0132 days <br />0.318 hours <br />0.00189 weeks <br />4.349115e-4 months <br />, during plant startup and the reactor critical, "A" Main Feedwater Pump was secured for repair of a drain valve leak on "6B" Feedwater Heater.
Both Motor Driven Auxiliary Feedwater Pumps started automatically as a resu.:.
"B" Auxiliary Feedwater (AFW) pump was secured and "A" AFW Pump alone was used to feed the steam generators. At 1145 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.356725e-4 months <br />, it was noted that "A" AFW pump had tripped on low discharge pressure. The operators immediately went to the pump room, readjus ted ths cischarge valve throttled to prevent pump runout, and restarted the pump satisfactorily at 1215 hours0.0141 days <br />0.338 hours <br />0.00201 weeks <br />4.623075e-4 months <br />. The trip was thought to have been caused by an improperly positioned discharge valve. On June 16, 1981, at 2115 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.047575e-4 months <br />, with the unit at 93% power, "A" AFW pump tripped during the performance of Periodic Test 22.1C.
Since the pump was ho t (indicating possible backleakage and pump casing vapor binding) the casing was vented., the pump was restarted, and the test was satisfactorily completed at 2132 hours0.0247 days <br />0.592 hours <br />0.00353 weeks <br />8.11226e-4 months <br />. After a review, it was determined that both pump trips were due to cavitation caused by steam as a result of backleakage through motor operated discharge valve V2-16A and check valve AFW-40.
During both events, "B" AFW pump was operatienal and capable of supplying the necessary feedwater. For this reason there was no threat to the public health and safety.
Since the Steam Driven AW pump was inoperable during this time, the failure of "A" AFW pump resulted in cperation in a degraded mode permitted by Technical Specification 3.4.3 which is reportable pursuant to 6.9.2.b.2.
2.
Corrective Action
Af ter the first pump trip, the discharge valve was readjusted.
Af ter the second pump trip, th'e pump casing was vented.
In bo th cases, the pump was successfully restarted.
i 3.
Corrective Action to Prevent Recurrence:
The motor operated discharge valve (V2-16A) and check valve (AFW-40) were repaired in an ef fort to stop the backleakage.
The backleakage, as indicated by pump casing temperature, was reduced low enough to preclude steam binding of the pump.
However, as an added precaution, the auxiliary operators were instructed to vent the pump casing as necessary on an hourly basis. This will continue until the next outage of sufficient length for a thorough investigation and the resolution of the backleakage problem.
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| 05000261/LER-1981-001, Updated LER 81-001/01T-1:on 810109,turbine Runback & Automatic Rod Withdrawal Block Protection Defeated W/Power Range Channel N41 Being Out of Svc.Caused by Improper Rod Drop Analysis.Administrative Controls Revised | Updated LER 81-001/01T-1:on 810109,turbine Runback & Automatic Rod Withdrawal Block Protection Defeated W/Power Range Channel N41 Being Out of Svc.Caused by Improper Rod Drop Analysis.Administrative Controls Revised | | | 05000261/LER-1981-002, Updated LER 81-002/01T-2:on 810113,review of Svc Water Sys Revealed Potential Unmonitored Release Path on Svc Water Return Lines from Containment for Hydrogen Vent Header Motor Coolers.Caused by Design Error.Sys Will Be Modifie | Updated LER 81-002/01T-2:on 810113,review of Svc Water Sys Revealed Potential Unmonitored Release Path on Svc Water Return Lines from Containment for Hydrogen Vent Header Motor Coolers.Caused by Design Error.Sys Will Be Modified | | | 05000261/LER-1981-002-01, /01T-3:on 810113,review of Svc Water Sys Revealed Potential Unmonitored Release Path to Environ.Caused by Lack of Radiation Monitoring on Svc Water Return Lines from Containment.Discharge Lines Modified | /01T-3:on 810113,review of Svc Water Sys Revealed Potential Unmonitored Release Path to Environ.Caused by Lack of Radiation Monitoring on Svc Water Return Lines from Containment.Discharge Lines Modified | | | 05000261/LER-1981-004, Forwards Updated LER 81-004/03L-1 | Forwards Updated LER 81-004/03L-1 | | | 05000261/LER-1981-004-03, Primary Coolant Sys Leak Found.Caused by Sample Cooler Tube Bundle Leakage Due to Normal Wear.Bundle Replaced.Review of Maint Records Revealed No Generic Problems | Primary Coolant Sys Leak Found.Caused by Sample Cooler Tube Bundle Leakage Due to Normal Wear.Bundle Replaced.Review of Maint Records Revealed No Generic Problems | | | 05000261/LER-1981-006-01, /01T-0:on 820715,motor Cooler Leak Found in Containment Fan Cooler HVH-2.HVH-2 Shut Down & Svc Water to Unit Isolated.Caused by Corrosion/Erosion of Cooler Tubing. Leak Repaired & Motor Coolers Will Be Replaced W/New Units | /01T-0:on 820715,motor Cooler Leak Found in Containment Fan Cooler HVH-2.HVH-2 Shut Down & Svc Water to Unit Isolated.Caused by Corrosion/Erosion of Cooler Tubing. Leak Repaired & Motor Coolers Will Be Replaced W/New Units | | | 05000261/LER-1981-007, Updated LER 81-007/01T-1:on 810122,potential Modeling Error in ECCS Model Used for LOCA Analysis Reported.Caused by Shift in Peak Clad Temp.New ECCS Analysis Performed in Aug 1981.No Impact on Public Health & Safety | Updated LER 81-007/01T-1:on 810122,potential Modeling Error in ECCS Model Used for LOCA Analysis Reported.Caused by Shift in Peak Clad Temp.New ECCS Analysis Performed in Aug 1981.No Impact on Public Health & Safety | | | 05000261/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000261/LER-1981-008-03, /03L-0:on 810225 While Performing Monthly Periodic Test CPL-PT-5.5,Hagan Signal Comparator Module Found Inoperable.Cause Not Stated.Comparator Replaced | /03L-0:on 810225 While Performing Monthly Periodic Test CPL-PT-5.5,Hagan Signal Comparator Module Found Inoperable.Cause Not Stated.Comparator Replaced | | | 05000261/LER-1981-013, Forwards Updated LER 81-013/03L-1 | Forwards Updated LER 81-013/03L-1 | | | 05000261/LER-1981-013-03, Determined Containment Isolation Valves Not Tested in Required Manner.Seven of Eight Valves Functioning as Designed.Eighth Valve Tested & Shown Operable.Test Undergoing Revision | Determined Containment Isolation Valves Not Tested in Required Manner.Seven of Eight Valves Functioning as Designed.Eighth Valve Tested & Shown Operable.Test Undergoing Revision | | | 05000261/LER-1981-014-03, /03L-0:on 810523,discovered That Hagan Summator PM-446B Had Shifted Nonconservatively Approx 3%.Caused by Failure of Filter Capacitor Due to Normal Wear.Faulty Capacitor Replaced | /03L-0:on 810523,discovered That Hagan Summator PM-446B Had Shifted Nonconservatively Approx 3%.Caused by Failure of Filter Capacitor Due to Normal Wear.Faulty Capacitor Replaced | | | 05000261/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000261/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000261/LER-1981-015-03, /03L-0:on 810525,computer Box FM-475 Found to Be Out of Acceptable Tolerances & Several Checkpoints Showed Erratic Readings During Loop a Steam Flow Channel Investigation.Caused by Two Worn Electronic Components | /03L-0:on 810525,computer Box FM-475 Found to Be Out of Acceptable Tolerances & Several Checkpoints Showed Erratic Readings During Loop a Steam Flow Channel Investigation.Caused by Two Worn Electronic Components | | | 05000261/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000261/LER-1981-016-03, /03L-0:on 810611,during Startup,Motor Driven Auxiliary Feedwater Pump a Tripped Due to Low Discharge Pressure While Feeding Steam Generators.Event Reoccurred on 810716.Caused by Backleakage Through Discharge Valve AFW-40 | /03L-0:on 810611,during Startup,Motor Driven Auxiliary Feedwater Pump a Tripped Due to Low Discharge Pressure While Feeding Steam Generators.Event Reoccurred on 810716.Caused by Backleakage Through Discharge Valve AFW-40 | | | 05000261/LER-1981-017-03, /03L-0:on 810619,auxiliary Feedwater Pump a Tripped on Low Discharge Pressure.Caused by Improper Throttle Setting of Discharge Valve.Valve Repositioned | /03L-0:on 810619,auxiliary Feedwater Pump a Tripped on Low Discharge Pressure.Caused by Improper Throttle Setting of Discharge Valve.Valve Repositioned | | | 05000261/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000261/LER-1981-018-03, /03L-0:on 810701,Channel I (PI-474) of a Steam Generator Steam Line Pressure Indicated High Compared to Two Redundant Channels.Caused by Throttled Root Isolation Valve MSV-14.Valve Reopened | /03L-0:on 810701,Channel I (PI-474) of a Steam Generator Steam Line Pressure Indicated High Compared to Two Redundant Channels.Caused by Throttled Root Isolation Valve MSV-14.Valve Reopened | | | 05000261/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000261/LER-1981-019-03, /03L-0:on 810705,w/unit at 95% Power,Svc Water Booster Pump (Swbp) a Motor Tripped.On 810706,SWBP a Motor Tripped Again.Caused by Normal Wear of Motor Bearings & Possible Breaker Problem,Respectively | /03L-0:on 810705,w/unit at 95% Power,Svc Water Booster Pump (Swbp) a Motor Tripped.On 810706,SWBP a Motor Tripped Again.Caused by Normal Wear of Motor Bearings & Possible Breaker Problem,Respectively | | | 05000261/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000261/LER-1981-020-03, /03L-0:on 810902,containment Spray Check Valve SI-890B & Associated Flow Path Declared Inoperable.Caused by Failure to Perform Post Maint Testing Prior to Startup Due to Oversight.Valve Tested.Procedures Will Be Revised | /03L-0:on 810902,containment Spray Check Valve SI-890B & Associated Flow Path Declared Inoperable.Caused by Failure to Perform Post Maint Testing Prior to Startup Due to Oversight.Valve Tested.Procedures Will Be Revised | | | 05000261/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000261/LER-1981-021, Forwards LER 81-021/01T-0 | Forwards LER 81-021/01T-0 | | | 05000261/LER-1981-021-01, /01T-0:on 810925,w/unit at 50% Power,Group 2 Control Bank D Control Rods Were Inoperable & Reactor Shutdown Commenced.Caused by Faulty Input/Output Amplifier Printed Circuit Card in Control Rod Logic Cabinet | /01T-0:on 810925,w/unit at 50% Power,Group 2 Control Bank D Control Rods Were Inoperable & Reactor Shutdown Commenced.Caused by Faulty Input/Output Amplifier Printed Circuit Card in Control Rod Logic Cabinet | | | 05000261/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000261/LER-1981-022-03, /03L-0:on 811015,w/unit at 50% Power,Lower than Normal Temp Indication Noted on Strip Chart Recorder for Valves on Discharge Line of Boron Injection Tank.Caused by Broken Wire Splice in Heat Tracing Circuit 70 | /03L-0:on 811015,w/unit at 50% Power,Lower than Normal Temp Indication Noted on Strip Chart Recorder for Valves on Discharge Line of Boron Injection Tank.Caused by Broken Wire Splice in Heat Tracing Circuit 70 | | | 05000261/LER-1981-023-03, /03L-0:on 811022,at 50% Power,Safety Injection Pump Started from Control Room for Routine Filling of Accumulators & Circuit Breaker Tripped.Cause Unidentified. No Further Action Considered Necessary | /03L-0:on 811022,at 50% Power,Safety Injection Pump Started from Control Room for Routine Filling of Accumulators & Circuit Breaker Tripped.Cause Unidentified. No Further Action Considered Necessary | | | 05000261/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000261/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000261/LER-1981-024-03, /03L-0:on 811028,heat Tracing for Motor Operated Valves on Discharge Line of Boron Injection Tank Found Failed.Caused by Short to Ground Resulting from Insulation Repairs.Personnel Cautioned Re Insulation | /03L-0:on 811028,heat Tracing for Motor Operated Valves on Discharge Line of Boron Injection Tank Found Failed.Caused by Short to Ground Resulting from Insulation Repairs.Personnel Cautioned Re Insulation | | | 05000261/LER-1981-025-03, /03L-0:on 811102,emergency Diesel Generator B Failed to Start Manually.Caused by Loss of Prime in Fuel Oil Sys,Possibly Due to Debris in Ball Check Valve.Generator Returned to Svc | /03L-0:on 811102,emergency Diesel Generator B Failed to Start Manually.Caused by Loss of Prime in Fuel Oil Sys,Possibly Due to Debris in Ball Check Valve.Generator Returned to Svc | | | 05000261/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | | | 05000261/LER-1981-026, Forwards LER 81-026/01T-0 | Forwards LER 81-026/01T-0 | | | 05000261/LER-1981-026-01, /01T-0:on 811120,primary to Secondary Leak of Approx 1.5 Gpm Found in Steam Generator A.Caused by Leaking Explosive Plug.Plant Shut Down,Plug Removed & Weld Repaired on 811127 | /01T-0:on 811120,primary to Secondary Leak of Approx 1.5 Gpm Found in Steam Generator A.Caused by Leaking Explosive Plug.Plant Shut Down,Plug Removed & Weld Repaired on 811127 | | | 05000261/LER-1981-028-03, /03L-0:on 811125,steam Generator low-low Level Trip & Alarm Bistables BS-494-A1 & BS-494-A2 Found to Be Inoperable During Periodic Test PT-5.5 W/Unit at Cold Shutdown.Caused by Failure of Instrument Channel LI-494 | /03L-0:on 811125,steam Generator low-low Level Trip & Alarm Bistables BS-494-A1 & BS-494-A2 Found to Be Inoperable During Periodic Test PT-5.5 W/Unit at Cold Shutdown.Caused by Failure of Instrument Channel LI-494 | | | 05000261/LER-1981-028, Forwards LER 81-028/03L-0 | Forwards LER 81-028/03L-0 | | | 05000261/LER-1981-029, Forwards LER 81-029/03L-0 | Forwards LER 81-029/03L-0 | | | 05000261/LER-1981-029-03, /03L-0:on 811130,w/unit at Hot Shutdown,Leak Was Discovered in Chemical & Vol Control Sys.Caused by Failed bonnet-to-body Gasket on Valve CVC-291.Gasket Replaced | /03L-0:on 811130,w/unit at Hot Shutdown,Leak Was Discovered in Chemical & Vol Control Sys.Caused by Failed bonnet-to-body Gasket on Valve CVC-291.Gasket Replaced | | | 05000261/LER-1981-030-03, /03L-0:on 811130,emergency Diesel Generator B Failed to Reach Rated Output Voltage Following Automatic Start Initiated by Safety Injection Signal.Caused by Faulty auto-voltage Adjust Reostat.Failure Due to Normal Wear | /03L-0:on 811130,emergency Diesel Generator B Failed to Reach Rated Output Voltage Following Automatic Start Initiated by Safety Injection Signal.Caused by Faulty auto-voltage Adjust Reostat.Failure Due to Normal Wear | | | 05000261/LER-1981-030, Forwards LER 81-030/03L-0 | Forwards LER 81-030/03L-0 | | | 05000261/LER-1981-031-01, /01T-0:on 811201,pressurizer Power Operated Relief Valve Block Valves Were Determined Not to Meet Design Specs. Valve Motor Operators Failed to Shut Valves Completely Following 811130 Transient.Block Valves Closed Manually | /01T-0:on 811201,pressurizer Power Operated Relief Valve Block Valves Were Determined Not to Meet Design Specs. Valve Motor Operators Failed to Shut Valves Completely Following 811130 Transient.Block Valves Closed Manually | | | 05000261/LER-1981-032-03, /03L-0:on 811205,boric Acid Transfer Pump a Tripped & Was Declared Inoperable.Caused by Error in Valve Lineup Procedure & Open Winding in Transfer Pump Motor. Procedure Revised & Motor Replaced | /03L-0:on 811205,boric Acid Transfer Pump a Tripped & Was Declared Inoperable.Caused by Error in Valve Lineup Procedure & Open Winding in Transfer Pump Motor. Procedure Revised & Motor Replaced | | | 05000261/LER-1981-032, Forwards LER 81-032/03L-0 | Forwards LER 81-032/03L-0 | | | 05000261/LER-1981-033, Forwards LER 81-033/01T-0 | Forwards LER 81-033/01T-0 | | | 05000261/LER-1981-033-01, /01T-0:on 811228,error in Tech Spec Heatup & Cooldown Curves Found to Be Not Reported to Nrc.Caused by Administrative Reporting Failure & Errors in Calculation. Info Will Be Reported as Tech Spec Change by 820131 | /01T-0:on 811228,error in Tech Spec Heatup & Cooldown Curves Found to Be Not Reported to Nrc.Caused by Administrative Reporting Failure & Errors in Calculation. Info Will Be Reported as Tech Spec Change by 820131 | | | 05000261/LER-1981-034-03, /03L-0:on 811211,loop 2 Steamline Pressure Channel Indicated Higher than Other Channels.Caused by Frozen Sensing Lines in Pressure Transmitter & Failure to Return Freeze Protection Circuit to Svc After Maint | /03L-0:on 811211,loop 2 Steamline Pressure Channel Indicated Higher than Other Channels.Caused by Frozen Sensing Lines in Pressure Transmitter & Failure to Return Freeze Protection Circuit to Svc After Maint | | | 05000261/LER-1981-034, Forwards LER 81-034/03L-0 | Forwards LER 81-034/03L-0 | |
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