Part 21 Rept Re Potential Util Failure to Comply W/Component Containment Isolation Licensing Commitment If Proposed Mods to Component Cooling Water Sys Instituted.Utils Advised to Evaluate Containment Isolation SysML17261A530 |
Person / Time |
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Site: |
Kewaunee, Point Beach, Turkey Point, Ginna, Robinson, 05000000 |
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Issue date: |
06/18/1987 |
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From: |
Johnson W WESTINGHOUSE ELECTRIC COMPANY, DIV OF CBS CORP. |
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To: |
Berlinger C Office of Nuclear Reactor Regulation |
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References |
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REF-PT21-87, REF-PT21-87-107-000 NS-NRC-87-3236, PT21-87-107, PT21-87-107-000, NUDOCS 8707020404 |
Download: ML17261A530 (5) |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A4151998-09-10010 September 1998 Part 21 Rept Re 980325 Discovery of Missing Tripper Bar Tabs During Troubleshooting of DB-75 Breaker Failure.Caused by Failure to Notify Technician of Revised Procedure to Reinstall Tabs.Inspected All DB-75 Breakers ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17265A4031998-08-12012 August 1998 Part 21 Rept Re W DB-75 Circuit Breakers W/Missing Tripper Bar Tabs.Caused by Intermittent Failure to Close in DB-75 B EDG Supply Circuit Breaker to Bus #16.Licensee Nuclear Engineering Personnel Are Performing Vendor Document Review ML20236J1051998-06-29029 June 1998 Part 21 30 Day Written Rept Re Refurbished DB-25 Circuit Breaker Returned W/Missing Pin in Operating Mechanism.Spare DB-25 Circuit Breaker Was Inspected,Tested & Installed to Restore B Service Water Pump to Service ML17265A3181998-06-0808 June 1998 Part 21 Rept Re Receipt of Refurbished DB-25 Circuit Breaker W/Missing Part from W Replacement Components Svcs on 980608. Spare DB-25 Circuit Breaker Was Inspected,Tested & Installed to Restore B Swp to Svc ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML17309A6241998-01-15015 January 1998 Deficiency Rept Re Failure of Shunt Trip Coil Plunger to Return to Deenergized Position Resulting in Breaker Tripper Bar Being Maintained in Trip Free Position,Preventing DB-75 Air Circuit Breaker from Closing.Failed Assembly Replaced ML17264B1401997-12-22022 December 1997 Part 21 Rept Re Binding Plunger of Assembly Shunt Trip Coil on 971114.Failed Shunt Trip Coil Was Replaced W/Spare from Stock ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML17309A6211997-09-29029 September 1997 Part 21 Rept Re Final Disposition of Masterflow 713 & Embeco 636 Grout Nonconformance Reported by Master Builders,Inc. Licensee Continuing to Monitor shelf-life of Masterflow 713 & Embeco 636 Grouts Produced at Rancho Cucamonga ML17264A9381997-07-10010 July 1997 Deficiency Rept Re Potential Safety Hazard Associated w/FM-Alco 251 Engin,High Pressure Fuel tube-catalog: 4401031-2 in Which Dual Failure Mode Exists.Caused by Incorrect Forming Process ML20210E3591997-03-27027 March 1997 Part 21 Rept Re Sorrento Electronics Inc Has Determined Operation & Maint Manual May Not Adequately Define Requirements for Performing Periodic Surveillance of SR Applications.Caused by Hardware Failures.Revised RM-23A ML20141K7711997-03-10010 March 1997 Preliminary Part 21 Rept Re Parsons Peebles/Electric Products Generators W/Modified Bearing Insulation.Util Implemented Mod to Add Insulation to Outer Spacer Ring ML20133E8001997-01-0808 January 1997 Deficiency Rept Re Nonconformance Related to Masterflow 713 Grout,Which Master Builders,Inc Has Supplied as Nuclear SR Product to 18 Npps.Cause Unknown.Requests That Listed Info Be Provided to Gain Insight as to Scope & Possible Cause ML17264A7301996-11-0606 November 1996 Part 21 Rept Re Defective 350 HP,1800 RPM,460 VAC,3 Phase, 5006P Frame,1.15 Sf,Vertical Hollow Shaft Motor Used as Service Water Pump motor.Safety-Relayed Cgiee Revised to Enhance Steps for Exam of Windings & Workmanship ML17264A7331996-10-10010 October 1996 Part 21 Rept Re Defect in 350 HP,1800 RPM,460 VAC,3 Phase, 500GP frame,1.15 Sf Vertical Hollow Shaft Motor for Use as Svc Water Pump Motor.Motor Removed,Disassembled,Inspected, Refurbished,Reinstalled & Satisfactorily Tested ML20115J3981996-07-22022 July 1996 Interim Part 21 Rept Re 3/4 Schedule 80 Pipe Furnished to Consolidated Power Supply.Investigation Revealed Only One Nuclear Customer Involved in Sale of Matl ML20115F2471996-07-0303 July 1996 Part 21 Rept Re Piping (Small Portion of Unmelted Matl Drawn Lengthwise Into Bar During Drawing Process) Defect That Existed in Bar as Received from Mill.Addl Insp Procedure for Raw Matl Instituted ML17353A6141996-02-28028 February 1996 Part 21 Rept 10CFR21-0073 Re Defect W/Voltage Adjust Potentiometer Mfg by Chicago Telephone Supply Used on NEI Peebles (Portec) Voltage Regulators at Plant.Util Updating Voltage Regulators W/Maury Instrument Corp Potentiometer ML17264A1701995-09-28028 September 1995 Part 21 Rept Re Fuel Oil Booster Pump post-maint Testing Revealed Fuel Oil Sys Pressure Readings of 32 PSIG in Required Action Low Range.Plant Personnel Installed Rebuilt Fuel Oil Booster Pump on B EDG ML20095K0361995-08-28028 August 1995 Part 21 Rept Re Failure of Diesel Min Operating Fuel Oil Pressure Pump Mfg by Tuthill Corp.Safety Hazard May Be Created If Emergency DG B Not Able to Maintain Design Load Rating.Pump End Play Clearance Adjusted ML20086T1761995-07-19019 July 1995 Part 21 Rept Re Potential Problem W/Type 51's & 87T Relays. Potential Problem Identified as Defective Tap Block. Recommends That Users Identified on Attachment 1 Page Verify Testing Per Instruction Listed on Encl Product Advisory Ltr ML17264A1091995-07-14014 July 1995 Part 21 Rept Re 14 Inch air-operated Butterfly Valve,Used as SW Outlet Valve AOV-4561 Supplied by Fisher Controls Co.On 950418,found That Valve Actuated Opposite from Required Configuration.Actuator Lever Reinstalled ML17309A5801995-06-16016 June 1995 Initial Part 21 Rept Re air-operated Butterfly Valve Mfg by Fisher Controls Co.Actuator Lever Altered ML17352B1391995-04-28028 April 1995 Part 21 Rept Re Mechanical Defect in Shaft Length of Some HEA63 Lockout Relays Mfg Between 1990-94.Defect Identified Could Possibly Result in Binding of Front Shaft.Suspect Relays Checked for Date Codes & Replacements Ordered ML20083R7961995-04-24024 April 1995 Interim Part 21 Rept Re Contact Failure of Square D Type Kpd Relay Used in Diesel Generator Control Panel.Relays Replaced at Plant.Review of Matter Expected to Be Completed on 950508 ML20077C2801994-11-21021 November 1994 Deficiency Rept Re Defective Yokes P/N 342849 Mfg by Copes- Vulcan,Inc.Affected Utilities Notified & Defective Yokes Will Be replaced.Copes-Vulcan Also re-inspected All Yokes in Inventory & Verified Yokes Acceptability ML17352A8951994-11-15015 November 1994 Part 21 Rept Re Unit 3A Sequencers at Turkey Point Plant. Unless Contacted by FP&L to Perform Programming Changes & Subsequent V&V to Sequencer Software,United Controls Plans No Other Evaluation of Defect for Listed Reason ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML20057G1511993-10-0707 October 1993 Part 21 Rept Re Westronics Model 2100C Series Recorders. Informs That Over Several Tests,Observed That Recorder Would Reset During Peak Acceleration & Door Being Forced Off Recorder.Small Retaining Clips Added to Bottom of Door ML17263A3311993-07-20020 July 1993 Part 21 Rept Re CCW HXs Mfg by Atlas Industrial Mfg Co.As Result of Eddy Current Exam Performed During 1993 Refueling Outage,Tubes W/Measurable Defects at Tube Plate Locations That Exceeded 70% of Tube Wall Thickness Removed from Svc ML20056D7071993-07-15015 July 1993 Part 21 Rept Re Reportable defect-75 PSIG Relief Check Valve 1 Npt,Emd 9521844,Kepner 416C-1-75 ML17263A3231993-06-22022 June 1993 Initial Part 21 Rept Re High Component Cooling Water Flow Results in flow-induced Vibration of HX Tubes Mfg by Atlas Industrial Mfg Co & Subsequent Tube Degradation.Tubes W/ Through Wall Indications Greater than 70% Plugged ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML17262A9821992-08-28028 August 1992 Interim Part 21 Rept Re Weld Overlap Area on body-to-bonnet Weld on 1/2-inch ASME Class II Valve Purchased from Henry Vogt Machine Co.Weld Will Be liquid-penetrant Tested Per ASME Class 2 Requirements.Completion Scheduled by 911215 ML20113H4871992-07-30030 July 1992 Part 21 Rept Re Surge Line Flooding Which May Occur When Large Pressurizer Vent Used to Support Reduced Rc Inventory Operations.Notification Received from Westinghouse on 920312.Item Not Reportable Per 10CFR21 ML17262A8341992-05-0404 May 1992 Interim Part 21 Rept Re 920313 Discovery of Potential Inaccuracies Associated W/Using Open Calibr Approach to Measure Closing Stem Thrust of Movs.Program for re- Evaluation of Previous Test Results in Progress 1999-09-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr NPL-99-0569, Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212D5961999-09-15015 September 1999 Safety Evaluation Supporting Licensee IPEEE Process.Plant Has Met Intent of Suppl 4 to GL 88-20 ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr NPL-99-0051, Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr NPL-99-0449, Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML20209D2691999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbnps,Units 1 & 2 ML20196J4251999-06-30030 June 1999 Safety Evaluation Authorizing Proposed Alternatives Described in Relief Requests VRR-01,ROJ-16,PRR-01 & VRR-02 ML20196F3341999-06-22022 June 1999 Safety Evaluation for Implementation of 422V+ Fuel Assemblies at Pbnp Units 1 & 2 ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML20195F9781999-06-10010 June 1999 Unit 2 Refueling 23 Inservice Insp Summary Rept for Form NIS-1 ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr NPL-99-0328, Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with ML20209D2751999-05-31031 May 1999 Revised MORs for May 1999 for Pbnps,Units 1 & 2 ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG NPL-99-0273, Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr 1999-09-30
[Table view] |
Text
REGULATORY RNATION DISTRIBUTION SYS (RIDS)
< 'ACCESSION NBR: 8707020404 DOC. DATE: 87/06/18 NOTARIZED: NO DOCKET 0 FAC IL: 50-000 Generic Docket 05000000 50-244 Robev t Emmet Qinna Nucleav Plant> Unit i. Rochestev Q 05000244 50-266 Point Beach Nucleav Plant> Unit ii Wisconsin Electric 0500026m 50-301 Point Beach Nuclear Planti Unit 2i Wisconsin Electric 05000301 50-250 Turkey Point Planti Unit 3i Florida Powev and Light C 05000250 50-251 Tuv keg Point Planti Unit 4i Florida Powev and Light C 05000251 50-261 H. B. Robinson Planti Unit 2i Carolina Powev Zc Light C 05000261 50-305 Kewaunee Nuclear Power Plant> Wisconsin Public Servic o5aoo3o5 AUTH. NANE AUTHOR AFFILIATION JOHNSON'. A. Westinghouse Electv ic Cov p.
RECIP. NANE RECIPIENT AFFILIATION BERLINQERn C. Generic Communi cat i ons Bv anc h
SUBJECT:
Pav t 21 rept e potential util fai luv e to comp lg w/component v
containment isolation licensing commitment if pv oposed mods Initially epov ted to component cooling watev sos instituted. v on 840713. Util notif i ed.
DIBTRIBUTION CODE: IEI9D COPIEB RECEIVED:LTR i ENCL 0 BIIE:
TITLE: Part 21 Rept (50 DKT)
NOTES: License Exp date in accov'dance with 10CFR2i 2. 109(9/19/72). osooa244 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAl'fE LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA PD3-3 LA PD2-2 LA PD2-1 L*
PD1-3 PD PD3-3 PD PD2-2 PD PD2-1 PD STAHLEi C WAGNER' NcDONALDe D ECCLESTONI K QUAY' INTERNAL: AEOD/DOA 1 *EOD/DSP/TPAB 1 ARN TECH ADV 1 NRR CRUTCHFIELD 1 NRR VARGAI 8 NRR/DEBT/ADE 1 NRR/DEST/ADS 1 NRR/DLPG/GAB NRR/DOEA/EAB 1 NRR/DOEA/GCB d~~
NRR/DRIS/VIB RES/DE/ElB Oi 1 NRR/PNAS/ILRB RES DEPY QI RGN1 1
1 RGN0 RGN3 RGN4 1 RGN5 1 EXTERNAL: INPO RECORD CTR LPDR NRC PDR NSIC SILVER> E TOTAL NUMBER OF COPIES REQUIRED: LTTR 41 ENCL
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Box 355 Westinghouse Power Systems Pittsburgh Pennsylvania 15230 0355 Electric Corporation June 18, 1987 NS-NRC-87-3236 Hr. Carl Berlinger, Chief Generic Communications Branch Division of Operational Events Assesement U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Dear Hr. Berlinger:
This is to confirm the telephone conversation on June 18 between Messrs.
Johnson and HcIntyre of Westinghouse and Hr. Carl Berlinger of the NRC. In that conversation, Westinghouse notified the NRC of a reportable item per 10CFR21 associated with a previously recommended modification to the component cooling water system of two operating plants: Point Beach 1 and 2. Had these recommended modifications been implemented by the utility, the above plants would have Failed to comply with the containment isolation licensing commitment. This item may also affect five other plants: Turkey Point 3 and 4, H. B. Robinson, Ginna and Kewaunee. However, we lack sufficient information to complete an evaluations Westinghouse has advised the owners of these plants of this issue.
The issue relates to an item that Westinghouse rep'orted earlier concerning a potential overpressure condition in the component cooling water systems designed by Westinghouse. This earlier issue was reported under 10CFR21 as a Substantial Safety Hazard For ll operating plants and 7 plants under construction in a July 13, 1984 letter to Hr. R. C. OeYoung, Division of Inspection and Enforcement, from Hr. E. P. Rahe, Jr., Westinghouse (NS-EPR-2938). Specifically, the overpressure condition could result from closure of the surge tank vent valve on a high radiation signal from the radiation detectors within the component cooling water system. This pressure increase (above the normal atmospheric pressure) in the surge tank results from a system inleakage and increases in system heat load. The pressure in the surge tank could increase to the set pressure of the surge tank relief valve. System overpressurization oF up to 1705 of the design pressure may occur downstream of the CCW pumps as a result of the pump developed head.
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Hr. Carl Berlinger June 18, 1987 NS-NRC-87-3236 Based on a generic review oF typical plant designs, Westinghouse determined that the potential for overpressuization could be reduced or eliminated by minor modifications to the component cooling water system. Each Utility was notified by letter of the potential overpressure condition and recommendations were made for plant modifications. Specifically, it was recommended that:
- 1. The circuitry which automatically closes the CCWS surge tank vent valve on a high radiation or surge tank level signal be disabled and, in the long term, the air operated, fail closed vent valve be converted to a normally open, locked open, local valve; and
- 2. The surge tank relieF valve be removed or the internals of the relief valve be removed.
These measures effectively achieve a low pressure drop overflow path from the surge tank which would be sufficient to ensure that the maximum pressure in the CCWS would not exceed 110 percent oF the design pressure in the event of operation with a water solid surge tank coincident with the maximum anticipated inleakage through a ruptured tube in one of the system heat exchangers. Additional review of these recommended changes indicates that implementation could have lead to a violation of containment isolation requirements for Point Beach Units 1 and 2 The design For these units depends on the CCWS outside of containment being a closed system which serves as an extension of the containment boundary. The above changes, if implemented, would make the CCWS outside of containment an open system.
The individual utilities mentioned in this letter have been advised to evaluate their respective containment isolation systems with regard to this potential item.
If you have any questions, please contact myself (412-374-4868) or Hike Shannon (412-374-5590) of my staff.
Very truly yours, WESTINGHOUSE ELECTRIC CORPORATION t
W J J hnson, Manager N Safety Oepartment HHS/bek/2908n