LER-1981-013, Determined Containment Isolation Valves Not Tested in Required Manner.Seven of Eight Valves Functioning as Designed.Eighth Valve Tested & Shown Operable.Test Undergoing Revision |
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U.S. NUCLEAR REGULATORY COMMISSION Update Report - Previous Report Date 5/15/81 NBC FORM 36G
' (17H LICENSEE EVENT REPORT.
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! 10121lon April 15. 1981. durinn a review of Periodic Test (PT) nrocedures_ ft unn lo13]lthat six containment isolation valves were not beinn tested in a manner which I
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On itav 10,_1_981. two additicnal l
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CODE TYPE NO.
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40 41 42 43 44 47 3J CAUSE DESCRIPTION AND CORRECTfVE ACTIONS h i o lRecent operating experience has verified that seven of the eight valves were func-l ltioning as designed. The eighth valve was tested and shown operable.
In order to I
i i recurrence, a PT is being revised to include provisions for fully testing l
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FOR LICENSEE EVENT REPORT 81-013, REV. 1 1.
Cause Description and Analysis On April 15, 1981, during a review of the H. B. Robinson Periodic Test isolation (PY) procedures, it was determined that six containment valves were not being tested in a manner which fully satisfied Tech-nical Specification 4.4.2.a.
On May 10, 1981, two additional valves were id entified.
'lhese valves are:
RMS-1, RMS-2, RMS-3, RMS-4, CVC-204A, CVC-?94B, PCV-1716 and SI-855.
These valves are tested for opcrability under the ISI Program.
The containment isolation function is verified by a number of periodic tests; however, these test procedures do notAs a require the above valves to be open prior to conducting the tests.
result a contact in each valve control circuit which is required to open to initiate the auto closure upon an isolation signal is not tested by Recent operating events have serified that each of these procedures.
these valves will close on the isolation signal, except SI-855 which was closed during the events.
SI-855 is the containment isolation valve for This valve which is operated the nitrogen supply to the SI accumulators.
from the control room is normally closed. In addition, there is one remotely operated valve downstream of SI-855 in each accumulator leg and manual valves upstream of the SI-855 valve which are also normally closed.
These valves are manually operated as necessary to add nitrogen to the SI These valves are only opened for very short time periods Accumulators.
Additionally, (2-5 minutes per week) and under direct operator control.
the safeguard position for SI-855 as well as the other seven containment isolation valves above is procedurally verified by a control room status panel following initiation of SI.
Therefore, there has been no undue risk to the public from this event.
This event is reportable pursuant to Technical Specification 6.9.2.b.3.
2..
Corrective Action
these Recent plant conditions and operating events have required that isolation valves respond to the Phase "A" isola tion signal containment I
which has verified the operability of all the valves except SI-855 (normally closed).
SI-855 was tested on June 5,1981, and verified operable. Therefore, no additional immediate actions are necessary.
3.
Corrective Action To Prevent Recurrence (PT-2.6) is being revised to include the above valves A periodic test in the pretest valve lineup to insure ' full compliance with the surveil-This revision will be completed prior to the next lance requirements.
refueling outage when the test is scheduled to be performed again.
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| 05000261/LER-1981-001, Updated LER 81-001/01T-1:on 810109,turbine Runback & Automatic Rod Withdrawal Block Protection Defeated W/Power Range Channel N41 Being Out of Svc.Caused by Improper Rod Drop Analysis.Administrative Controls Revised | Updated LER 81-001/01T-1:on 810109,turbine Runback & Automatic Rod Withdrawal Block Protection Defeated W/Power Range Channel N41 Being Out of Svc.Caused by Improper Rod Drop Analysis.Administrative Controls Revised | | | 05000261/LER-1981-002, Updated LER 81-002/01T-2:on 810113,review of Svc Water Sys Revealed Potential Unmonitored Release Path on Svc Water Return Lines from Containment for Hydrogen Vent Header Motor Coolers.Caused by Design Error.Sys Will Be Modifie | Updated LER 81-002/01T-2:on 810113,review of Svc Water Sys Revealed Potential Unmonitored Release Path on Svc Water Return Lines from Containment for Hydrogen Vent Header Motor Coolers.Caused by Design Error.Sys Will Be Modified | | | 05000261/LER-1981-002-01, /01T-3:on 810113,review of Svc Water Sys Revealed Potential Unmonitored Release Path to Environ.Caused by Lack of Radiation Monitoring on Svc Water Return Lines from Containment.Discharge Lines Modified | /01T-3:on 810113,review of Svc Water Sys Revealed Potential Unmonitored Release Path to Environ.Caused by Lack of Radiation Monitoring on Svc Water Return Lines from Containment.Discharge Lines Modified | | | 05000261/LER-1981-004, Forwards Updated LER 81-004/03L-1 | Forwards Updated LER 81-004/03L-1 | | | 05000261/LER-1981-004-03, Primary Coolant Sys Leak Found.Caused by Sample Cooler Tube Bundle Leakage Due to Normal Wear.Bundle Replaced.Review of Maint Records Revealed No Generic Problems | Primary Coolant Sys Leak Found.Caused by Sample Cooler Tube Bundle Leakage Due to Normal Wear.Bundle Replaced.Review of Maint Records Revealed No Generic Problems | | | 05000261/LER-1981-006-01, /01T-0:on 820715,motor Cooler Leak Found in Containment Fan Cooler HVH-2.HVH-2 Shut Down & Svc Water to Unit Isolated.Caused by Corrosion/Erosion of Cooler Tubing. Leak Repaired & Motor Coolers Will Be Replaced W/New Units | /01T-0:on 820715,motor Cooler Leak Found in Containment Fan Cooler HVH-2.HVH-2 Shut Down & Svc Water to Unit Isolated.Caused by Corrosion/Erosion of Cooler Tubing. Leak Repaired & Motor Coolers Will Be Replaced W/New Units | | | 05000261/LER-1981-007, Updated LER 81-007/01T-1:on 810122,potential Modeling Error in ECCS Model Used for LOCA Analysis Reported.Caused by Shift in Peak Clad Temp.New ECCS Analysis Performed in Aug 1981.No Impact on Public Health & Safety | Updated LER 81-007/01T-1:on 810122,potential Modeling Error in ECCS Model Used for LOCA Analysis Reported.Caused by Shift in Peak Clad Temp.New ECCS Analysis Performed in Aug 1981.No Impact on Public Health & Safety | | | 05000261/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000261/LER-1981-008-03, /03L-0:on 810225 While Performing Monthly Periodic Test CPL-PT-5.5,Hagan Signal Comparator Module Found Inoperable.Cause Not Stated.Comparator Replaced | /03L-0:on 810225 While Performing Monthly Periodic Test CPL-PT-5.5,Hagan Signal Comparator Module Found Inoperable.Cause Not Stated.Comparator Replaced | | | 05000261/LER-1981-013, Forwards Updated LER 81-013/03L-1 | Forwards Updated LER 81-013/03L-1 | | | 05000261/LER-1981-013-03, Determined Containment Isolation Valves Not Tested in Required Manner.Seven of Eight Valves Functioning as Designed.Eighth Valve Tested & Shown Operable.Test Undergoing Revision | Determined Containment Isolation Valves Not Tested in Required Manner.Seven of Eight Valves Functioning as Designed.Eighth Valve Tested & Shown Operable.Test Undergoing Revision | | | 05000261/LER-1981-014-03, /03L-0:on 810523,discovered That Hagan Summator PM-446B Had Shifted Nonconservatively Approx 3%.Caused by Failure of Filter Capacitor Due to Normal Wear.Faulty Capacitor Replaced | /03L-0:on 810523,discovered That Hagan Summator PM-446B Had Shifted Nonconservatively Approx 3%.Caused by Failure of Filter Capacitor Due to Normal Wear.Faulty Capacitor Replaced | | | 05000261/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000261/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000261/LER-1981-015-03, /03L-0:on 810525,computer Box FM-475 Found to Be Out of Acceptable Tolerances & Several Checkpoints Showed Erratic Readings During Loop a Steam Flow Channel Investigation.Caused by Two Worn Electronic Components | /03L-0:on 810525,computer Box FM-475 Found to Be Out of Acceptable Tolerances & Several Checkpoints Showed Erratic Readings During Loop a Steam Flow Channel Investigation.Caused by Two Worn Electronic Components | | | 05000261/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000261/LER-1981-016-03, /03L-0:on 810611,during Startup,Motor Driven Auxiliary Feedwater Pump a Tripped Due to Low Discharge Pressure While Feeding Steam Generators.Event Reoccurred on 810716.Caused by Backleakage Through Discharge Valve AFW-40 | /03L-0:on 810611,during Startup,Motor Driven Auxiliary Feedwater Pump a Tripped Due to Low Discharge Pressure While Feeding Steam Generators.Event Reoccurred on 810716.Caused by Backleakage Through Discharge Valve AFW-40 | | | 05000261/LER-1981-017-03, /03L-0:on 810619,auxiliary Feedwater Pump a Tripped on Low Discharge Pressure.Caused by Improper Throttle Setting of Discharge Valve.Valve Repositioned | /03L-0:on 810619,auxiliary Feedwater Pump a Tripped on Low Discharge Pressure.Caused by Improper Throttle Setting of Discharge Valve.Valve Repositioned | | | 05000261/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000261/LER-1981-018-03, /03L-0:on 810701,Channel I (PI-474) of a Steam Generator Steam Line Pressure Indicated High Compared to Two Redundant Channels.Caused by Throttled Root Isolation Valve MSV-14.Valve Reopened | /03L-0:on 810701,Channel I (PI-474) of a Steam Generator Steam Line Pressure Indicated High Compared to Two Redundant Channels.Caused by Throttled Root Isolation Valve MSV-14.Valve Reopened | | | 05000261/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000261/LER-1981-019-03, /03L-0:on 810705,w/unit at 95% Power,Svc Water Booster Pump (Swbp) a Motor Tripped.On 810706,SWBP a Motor Tripped Again.Caused by Normal Wear of Motor Bearings & Possible Breaker Problem,Respectively | /03L-0:on 810705,w/unit at 95% Power,Svc Water Booster Pump (Swbp) a Motor Tripped.On 810706,SWBP a Motor Tripped Again.Caused by Normal Wear of Motor Bearings & Possible Breaker Problem,Respectively | | | 05000261/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000261/LER-1981-020-03, /03L-0:on 810902,containment Spray Check Valve SI-890B & Associated Flow Path Declared Inoperable.Caused by Failure to Perform Post Maint Testing Prior to Startup Due to Oversight.Valve Tested.Procedures Will Be Revised | /03L-0:on 810902,containment Spray Check Valve SI-890B & Associated Flow Path Declared Inoperable.Caused by Failure to Perform Post Maint Testing Prior to Startup Due to Oversight.Valve Tested.Procedures Will Be Revised | | | 05000261/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000261/LER-1981-021, Forwards LER 81-021/01T-0 | Forwards LER 81-021/01T-0 | | | 05000261/LER-1981-021-01, /01T-0:on 810925,w/unit at 50% Power,Group 2 Control Bank D Control Rods Were Inoperable & Reactor Shutdown Commenced.Caused by Faulty Input/Output Amplifier Printed Circuit Card in Control Rod Logic Cabinet | /01T-0:on 810925,w/unit at 50% Power,Group 2 Control Bank D Control Rods Were Inoperable & Reactor Shutdown Commenced.Caused by Faulty Input/Output Amplifier Printed Circuit Card in Control Rod Logic Cabinet | | | 05000261/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000261/LER-1981-022-03, /03L-0:on 811015,w/unit at 50% Power,Lower than Normal Temp Indication Noted on Strip Chart Recorder for Valves on Discharge Line of Boron Injection Tank.Caused by Broken Wire Splice in Heat Tracing Circuit 70 | /03L-0:on 811015,w/unit at 50% Power,Lower than Normal Temp Indication Noted on Strip Chart Recorder for Valves on Discharge Line of Boron Injection Tank.Caused by Broken Wire Splice in Heat Tracing Circuit 70 | | | 05000261/LER-1981-023-03, /03L-0:on 811022,at 50% Power,Safety Injection Pump Started from Control Room for Routine Filling of Accumulators & Circuit Breaker Tripped.Cause Unidentified. No Further Action Considered Necessary | /03L-0:on 811022,at 50% Power,Safety Injection Pump Started from Control Room for Routine Filling of Accumulators & Circuit Breaker Tripped.Cause Unidentified. No Further Action Considered Necessary | | | 05000261/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000261/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000261/LER-1981-024-03, /03L-0:on 811028,heat Tracing for Motor Operated Valves on Discharge Line of Boron Injection Tank Found Failed.Caused by Short to Ground Resulting from Insulation Repairs.Personnel Cautioned Re Insulation | /03L-0:on 811028,heat Tracing for Motor Operated Valves on Discharge Line of Boron Injection Tank Found Failed.Caused by Short to Ground Resulting from Insulation Repairs.Personnel Cautioned Re Insulation | | | 05000261/LER-1981-025-03, /03L-0:on 811102,emergency Diesel Generator B Failed to Start Manually.Caused by Loss of Prime in Fuel Oil Sys,Possibly Due to Debris in Ball Check Valve.Generator Returned to Svc | /03L-0:on 811102,emergency Diesel Generator B Failed to Start Manually.Caused by Loss of Prime in Fuel Oil Sys,Possibly Due to Debris in Ball Check Valve.Generator Returned to Svc | | | 05000261/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | | | 05000261/LER-1981-026, Forwards LER 81-026/01T-0 | Forwards LER 81-026/01T-0 | | | 05000261/LER-1981-026-01, /01T-0:on 811120,primary to Secondary Leak of Approx 1.5 Gpm Found in Steam Generator A.Caused by Leaking Explosive Plug.Plant Shut Down,Plug Removed & Weld Repaired on 811127 | /01T-0:on 811120,primary to Secondary Leak of Approx 1.5 Gpm Found in Steam Generator A.Caused by Leaking Explosive Plug.Plant Shut Down,Plug Removed & Weld Repaired on 811127 | | | 05000261/LER-1981-028-03, /03L-0:on 811125,steam Generator low-low Level Trip & Alarm Bistables BS-494-A1 & BS-494-A2 Found to Be Inoperable During Periodic Test PT-5.5 W/Unit at Cold Shutdown.Caused by Failure of Instrument Channel LI-494 | /03L-0:on 811125,steam Generator low-low Level Trip & Alarm Bistables BS-494-A1 & BS-494-A2 Found to Be Inoperable During Periodic Test PT-5.5 W/Unit at Cold Shutdown.Caused by Failure of Instrument Channel LI-494 | | | 05000261/LER-1981-028, Forwards LER 81-028/03L-0 | Forwards LER 81-028/03L-0 | | | 05000261/LER-1981-029, Forwards LER 81-029/03L-0 | Forwards LER 81-029/03L-0 | | | 05000261/LER-1981-029-03, /03L-0:on 811130,w/unit at Hot Shutdown,Leak Was Discovered in Chemical & Vol Control Sys.Caused by Failed bonnet-to-body Gasket on Valve CVC-291.Gasket Replaced | /03L-0:on 811130,w/unit at Hot Shutdown,Leak Was Discovered in Chemical & Vol Control Sys.Caused by Failed bonnet-to-body Gasket on Valve CVC-291.Gasket Replaced | | | 05000261/LER-1981-030-03, /03L-0:on 811130,emergency Diesel Generator B Failed to Reach Rated Output Voltage Following Automatic Start Initiated by Safety Injection Signal.Caused by Faulty auto-voltage Adjust Reostat.Failure Due to Normal Wear | /03L-0:on 811130,emergency Diesel Generator B Failed to Reach Rated Output Voltage Following Automatic Start Initiated by Safety Injection Signal.Caused by Faulty auto-voltage Adjust Reostat.Failure Due to Normal Wear | | | 05000261/LER-1981-030, Forwards LER 81-030/03L-0 | Forwards LER 81-030/03L-0 | | | 05000261/LER-1981-031-01, /01T-0:on 811201,pressurizer Power Operated Relief Valve Block Valves Were Determined Not to Meet Design Specs. Valve Motor Operators Failed to Shut Valves Completely Following 811130 Transient.Block Valves Closed Manually | /01T-0:on 811201,pressurizer Power Operated Relief Valve Block Valves Were Determined Not to Meet Design Specs. Valve Motor Operators Failed to Shut Valves Completely Following 811130 Transient.Block Valves Closed Manually | | | 05000261/LER-1981-032-03, /03L-0:on 811205,boric Acid Transfer Pump a Tripped & Was Declared Inoperable.Caused by Error in Valve Lineup Procedure & Open Winding in Transfer Pump Motor. Procedure Revised & Motor Replaced | /03L-0:on 811205,boric Acid Transfer Pump a Tripped & Was Declared Inoperable.Caused by Error in Valve Lineup Procedure & Open Winding in Transfer Pump Motor. Procedure Revised & Motor Replaced | | | 05000261/LER-1981-032, Forwards LER 81-032/03L-0 | Forwards LER 81-032/03L-0 | | | 05000261/LER-1981-033, Forwards LER 81-033/01T-0 | Forwards LER 81-033/01T-0 | | | 05000261/LER-1981-033-01, /01T-0:on 811228,error in Tech Spec Heatup & Cooldown Curves Found to Be Not Reported to Nrc.Caused by Administrative Reporting Failure & Errors in Calculation. Info Will Be Reported as Tech Spec Change by 820131 | /01T-0:on 811228,error in Tech Spec Heatup & Cooldown Curves Found to Be Not Reported to Nrc.Caused by Administrative Reporting Failure & Errors in Calculation. Info Will Be Reported as Tech Spec Change by 820131 | | | 05000261/LER-1981-034-03, /03L-0:on 811211,loop 2 Steamline Pressure Channel Indicated Higher than Other Channels.Caused by Frozen Sensing Lines in Pressure Transmitter & Failure to Return Freeze Protection Circuit to Svc After Maint | /03L-0:on 811211,loop 2 Steamline Pressure Channel Indicated Higher than Other Channels.Caused by Frozen Sensing Lines in Pressure Transmitter & Failure to Return Freeze Protection Circuit to Svc After Maint | | | 05000261/LER-1981-034, Forwards LER 81-034/03L-0 | Forwards LER 81-034/03L-0 | |
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