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{{#Wiki_filter:NRC FOHA4 366 'Jpdate Report - Previous Report Dste July 16, 1981                                                          U.!E NUCLEAR REGULATO3Y COMMISSION 0m.s LICENSEE EVENT REPORT CONTROu 9 LOCK: l              l      l    l    l  l      l                (PLEASE PRINT 03 TYPE ALL REQUtRED INFORMATION) 1                                  6 7
o i 8 9 l S l C l li j B l R l 2 l@l 0 l 0 l - l 0 l 0 l 0 l 0 l 0 l- l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@l67 CAT L?CENSEE CODE              14    15                    LICENSE NUMBER                    25      26      LICENSE TYPE Jo l
68 l@
CON'T o 1                                                                                                                                  l    l    l  l    l      'a,9) 7      8 Zn"c[ l60L l@l 0 l 5 l 0DOCKET 1
l 0 lNUMBER 0 l 2 l 6 l 168@l690 l 7EVENT      l 0 lDATE 2 l 8 l 0 74l@l76              REPORT DATE          80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l On July 2,1980, as a result of review of inf ormation obtained bY Carolina Power                                                                                  I o 3      l and Light Company from the manufacturer of Robinson Plant Containment electrical                                                                              l l o l4 l l penetrations, it was determined that no certification of qualification is available                                                                              1 o 3      l for the apparent PVC electric cable " pigtails" used on eight penetrations, Catalog                                                                          l 0 s      l No. 0100759, as required by IE Bulletin 79-01B.                                            No noncompliance with plant                                      l 0 7      l Technical Specifications is known to have resulted from this event. This finding                                                                            l
      ; o y g l is being reported consistent with NRC guidelines contained in IE Bulletin 79-01B.                                                                                l DE              CODE      S 8C E                  COMPONENT CODE                  SU8 CODE        SU      E Fd                                l1lB l@ {@ {@ l Pl El Nl El Tl Rl@ {@ y @'
7      8                        9        10'          11            12            13                            18          19              20
                                    ,_                                        SEQUENTIAL                      OCCURRENCE          REPORT                      REVISION LE R/RO      EVENT YEAR                              REPORT NO.                          CODE              TYPE                          N O.
                  @ ,RE                l8 l0 l              g            l0 l1 l4 l 24 y
l0l1l 28        29 g
30 g31 y32
_ 21          22          23                          26 N A                    ON        NT        ET D                  HOUMS          S8 li D          FOR      8. SU PLIE              MANUF CTUREl
[X 31__
jg[X 34_
j@            lZ lg 35 Q@
M l 0l 0l 0l 0l 31                  40 l41 Yl@          [_Y_j@
42 W@
43 l C l 7 l 2 l(:j@
44              '7 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g l The cable pigtails of these penetrations meet the design sp mii' cations for their                                                                                      l i ,      l cons truction,                  h addition, tests have been performed which certify that the                                                                  i
          , ,      gcable pigtails are qualifted to the accident conditions described in the                                                                                        l
        , ,      l H. B. Robinson FSAR.                                                                                                                                          l i 4      l                                                                                                                                                                1
- 7          8 9                                                                                                                                                                80 oTHER STATUS              DIS O RY                            DISCOVERY DESCRIPTION STA                % POWER 31 1)@ l 0l 9 l 3 l@l                                              NA                l    lDl@l                    Document Review - IEB 79-Oln                              l A TlVITY Co TENT AMOUNT OF ACTIVITY                                                    LOCATION OF RELEASE NA 7
1 6 RE'. EASE @D OF RELEASE l 8 9                to          el NA 44 l        l 45                                                                        80 l
PERSONrt'L EXPOSI 7 NUMBER                            DESCRIPTION '
NA l        1 7      l 0 l 0 l]QlTY 4l@l                                                                                                                                              l PERSONNELINJU IES
,                                          DESCRIPTION i a      l0 lNUb*BE Rl0 lgl                                                                      NA                                                                    l F      8 9                11      12                                                                                                                                    80 f
7 E        DE R PT ON 7
8 9 8 9 b hl        to 8110290361 211019 PDR ADOCK 05000261 "A
80 S                                                                                          NRC USE ONLY              '
PUBL IC1T,Y,
                                                @                                              PDR.
7 2 o 8 9 hhl        10 NA                                                          l 68 69 lllllllllllll1 80 E
                                                                                                                                                                ~
NAME OF PREPARER                                                                                PHONE:
 
      -.  *b>
                                                          -$UPPLEMENTAL INFORMATION FOR .
LICENSEE EVENT REPORT 80-014, UPDATE REPORT
: 1.      Cause Description ~and Analysis:
On July 2,1980, as a res ult of taformation obtained by Carolina Power and Light Company from Crouse Hinds (manufacturer'of Robinson-2
,                              Containment Vessel (CV) electrica. penetrations) .it was determined l                              that no certification of qualification is available for the electric cable " pigtails" used in the manufacture of CV penetratio'ns (C.H.
Catalog No. 0100759).          This type penetration contains two (2) and four (4) conductor AWG No.16 shielded cable and is used for instrumentation on saf ety related equipment. The instruments involved .
which would be required in. the event of a design basis accident and their required operating times following the accident are as follows:
Pressurizer Pressure                                                                              30 Minutes Pressurizer Level' (No ESF Function)                                                              30 Minutes Steam Generator Level                                                                              24 Hours Steam Line Flow                                                                                    24 Hours
: 2.        Corrective Action:
A program was implemented to test and qualify samples of the
                              . penetration pigtails. These tests have certified that the cable pigtails are qualified to the accident conditions described in the H. B. Robinson FSAR.
In addition, information from Crouse Hinds revealed that material documentation could not be located uon one of two penetrations built '
for Robinson as Catalog No. 0100747. This type penetration has three conductor cables of AWG No. 9 and is used primarily to power small 480 volt motors.        One of these penetrations is in train A and the other in train B. One penetration is fully documented and qualified and the other penetration _ has been inspected to verify that it is of the same composition and construction.            There fore, the penetration is believed to be adequate and no further actions are required.
: 3.        Corrective Action'To ' Prevent Purther' Occurrence:
Since it was a thorough review of the environmental qualifications of electrical equipment at Robinson Plant which resulted in this report, further additional corrective action is not considered necessary at this time.
i....i.,.....            .i...- .    -
_ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _}}

Latest revision as of 02:59, 21 February 2020

Updated LER 80-014/01T-1:on 800702,vendor Info Indicated That No Certification of Qualification Was Available for PVC Electric Cable Pigtails Used on Eight Penetrations.Cable Pigtails Meet Design Specs & Accident Requirements
ML20011A731
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 10/19/1981
From: Starkey R
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20011A729 List:
References
IEB-79-01B, IEB-79-1B, LER-80-014-01T, LER-80-14-1T, NUDOCS 8110290361
Download: ML20011A731 (2)


Text

NRC FOHA4 366 'Jpdate Report - Previous Report Dste July 16, 1981 U.!E NUCLEAR REGULATO3Y COMMISSION 0m.s LICENSEE EVENT REPORT CONTROu 9 LOCK: l l l l l l l (PLEASE PRINT 03 TYPE ALL REQUtRED INFORMATION) 1 6 7

o i 8 9 l S l C l li j B l R l 2 l@l 0 l 0 l - l 0 l 0 l 0 l 0 l 0 l- l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@l67 CAT L?CENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE Jo l

68 l@

CON'T o 1 l l l l l 'a,9) 7 8 Zn"c[ l60L l@l 0 l 5 l 0DOCKET 1

l 0 lNUMBER 0 l 2 l 6 l 168@l690 l 7EVENT l 0 lDATE 2 l 8 l 0 74l@l76 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l On July 2,1980, as a result of review of inf ormation obtained bY Carolina Power I o 3 l and Light Company from the manufacturer of Robinson Plant Containment electrical l l o l4 l l penetrations, it was determined that no certification of qualification is available 1 o 3 l for the apparent PVC electric cable " pigtails" used on eight penetrations, Catalog l 0 s l No. 0100759, as required by IE Bulletin 79-01B. No noncompliance with plant l 0 7 l Technical Specifications is known to have resulted from this event. This finding l

o y g l is being reported consistent with NRC guidelines contained in IE Bulletin 79-01B. l DE CODE S 8C E COMPONENT CODE SU8 CODE SU E Fd l1lB l@ {@ {@ l Pl El Nl El Tl Rl@ {@ y @'

7 8 9 10' 11 12 13 18 19 20

,_ SEQUENTIAL OCCURRENCE REPORT REVISION LE R/RO EVENT YEAR REPORT NO. CODE TYPE N O.

@ ,RE l8 l0 l g l0 l1 l4 l 24 y

l0l1l 28 29 g

30 g31 y32

_ 21 22 23 26 N A ON NT ET D HOUMS S8 li D FOR 8. SU PLIE MANUF CTUREl

[X 31__

jg[X 34_

j@ lZ lg 35 Q@

M l 0l 0l 0l 0l 31 40 l41 Yl@ [_Y_j@

42 W@

43 l C l 7 l 2 l(:j@

44 '7 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g l The cable pigtails of these penetrations meet the design sp mii' cations for their l i , l cons truction, h addition, tests have been performed which certify that the i

, , gcable pigtails are qualifted to the accident conditions described in the l

, , l H. B. Robinson FSAR. l i 4 l 1

- 7 8 9 80 oTHER STATUS DIS O RY DISCOVERY DESCRIPTION STA  % POWER 31 1)@ l 0l 9 l 3 l@l NA l lDl@l Document Review - IEB 79-Oln l A TlVITY Co TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE NA 7

1 6 RE'. EASE @D OF RELEASE l 8 9 to el NA 44 l l 45 80 l

PERSONrt'L EXPOSI 7 NUMBER DESCRIPTION '

NA l 1 7 l 0 l 0 l]QlTY 4l@l l PERSONNELINJU IES

, DESCRIPTION i a l0 lNUb*BE Rl0 lgl NA l F 8 9 11 12 80 f

7 E DE R PT ON 7

8 9 8 9 b hl to 8110290361 211019 PDR ADOCK 05000261 "A

80 S NRC USE ONLY '

PUBL IC1T,Y,

@ PDR.

7 2 o 8 9 hhl 10 NA l 68 69 lllllllllllll1 80 E

~

NAME OF PREPARER PHONE:

-. *b>

-$UPPLEMENTAL INFORMATION FOR .

LICENSEE EVENT REPORT 80-014, UPDATE REPORT

1. Cause Description ~and Analysis:

On July 2,1980, as a res ult of taformation obtained by Carolina Power and Light Company from Crouse Hinds (manufacturer'of Robinson-2

, Containment Vessel (CV) electrica. penetrations) .it was determined l that no certification of qualification is available for the electric cable " pigtails" used in the manufacture of CV penetratio'ns (C.H.

Catalog No. 0100759). This type penetration contains two (2) and four (4) conductor AWG No.16 shielded cable and is used for instrumentation on saf ety related equipment. The instruments involved .

which would be required in. the event of a design basis accident and their required operating times following the accident are as follows:

Pressurizer Pressure 30 Minutes Pressurizer Level' (No ESF Function) 30 Minutes Steam Generator Level 24 Hours Steam Line Flow 24 Hours

2. Corrective Action:

A program was implemented to test and qualify samples of the

. penetration pigtails. These tests have certified that the cable pigtails are qualified to the accident conditions described in the H. B. Robinson FSAR.

In addition, information from Crouse Hinds revealed that material documentation could not be located uon one of two penetrations built '

for Robinson as Catalog No. 0100747. This type penetration has three conductor cables of AWG No. 9 and is used primarily to power small 480 volt motors. One of these penetrations is in train A and the other in train B. One penetration is fully documented and qualified and the other penetration _ has been inspected to verify that it is of the same composition and construction. There fore, the penetration is believed to be adequate and no further actions are required.

3. Corrective Action'To ' Prevent Purther' Occurrence:

Since it was a thorough review of the environmental qualifications of electrical equipment at Robinson Plant which resulted in this report, further additional corrective action is not considered necessary at this time.

i....i.,..... .i...- . -

_ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _