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| {{#Wiki_filter:1)7121121)14Pnop IU.2S.04 I Nucearr Ro-oulatorv Commissin Onperations. Center Event Rennrt Pn"" IPart 21 (PAR) Event # 50291Rep Org: FISHER CONTROLS INTERNATIONAL Notification Date I Time: 07/21/2014 16:35 (EDT)Supplier: FISHER CONTROLS INTERNATIONAL Event Date / Time: 06/26/2014 (CDT)Last Modification: 07/21/2014Region: 3 Docket #:City: Marshalltown Agreement State: YesCounty: License #:State: IANRC Notified by: CHAD ENGLE Notifications: STEVE ORTH R3DOHQ Ops Officer: DONALD NORWOOD GERALD MCCOY R2DOEmergency Class: NON EMERGENCY PART 21 GROUP EMAIL10 CFR Section:21.21 (d)(3)(i) DEFECTS AND NONCOMPLIANCEPART 21 REPORT -INCORRECT VALVE SOLENOIDS PROVIDEDThe following is a synopsis of information received via facsimile:Brunswick Nuclear Plant ordered 10 (ten) 120VAC/6OHz valve solenoids on two purchase orders from FisherControls International LLC. In February, 2014, Fisher shipped six 125VDC solenoids to Brunswick. All six of thosesolenoids were identified as non-conforming prior to installation in the plant. The remaining 4 solenoids at Fisherare on a shipping hold. For technical questions or concerns contact: George Baitinger, Manager, Quality, FisherControls International. LLC, 301 South 1st Ave, Marshalltown, IA 50158, Fax: (641) 754--2854, Phone: (641) 754-2026.Fisher Information Notice: FIN 2014-02>61-Jul. 21. 2014 3:09PMNo. 0266 P. 1EMERSON.[FISHER]Facsimile301 South First AveMarshalltown, IA 50158T 641-754-3011F 641-754-2830To: NRC Operations Center -Alln:, Bill HUffmanFax: 301-815-5151From: Dennis Swanson, Emerson Process ManagementDate: 712112014Pages: 4(inc cover) | | {{#Wiki_filter:1)7121121)14 Pnop IU.2S.04 I Nucearr Ro-oulatorv Commissin Onperations. |
| | Center Event Rennrt Pn"" IPart 21 (PAR) Event # 50291Rep Org: FISHER CONTROLS INTERNATIONAL Notification Date I Time: 07/21/2014 16:35 (EDT)Supplier: |
| | FISHER CONTROLS INTERNATIONAL Event Date / Time: 06/26/2014 (CDT)Last Modification: |
| | 07/21/2014 Region: 3 Docket #:City: Marshalltown Agreement State: YesCounty: License #:State: IANRC Notified by: CHAD ENGLE Notifications: |
| | STEVE ORTH R3DOHQ Ops Officer: |
| | DONALD NORWOOD GERALD MCCOY R2DOEmergency Class: NON EMERGENCY PART 21 GROUP EMAIL10 CFR Section:21.21 (d)(3)(i) |
| | DEFECTS AND NONCOMPLIANCE PART 21 REPORT -INCORRECT VALVE SOLENOIDS PROVIDEDThe following is a synopsis of information received via facsimile: |
| | Brunswick Nuclear Plant ordered 10 (ten) 120VAC/6OHz valve solenoids on two purchase orders from FisherControls International LLC. In February, 2014, Fisher shipped six 125VDC solenoids to Brunswick. |
| | All six of thosesolenoids were identified as non-conforming prior to installation in the plant. The remaining 4 solenoids at Fisherare on a shipping hold. For technical questions or concerns contact: |
| | George Baitinger, |
| | : Manager, Quality, FisherControls International. |
| | LLC, 301 South 1st Ave, Marshalltown, IA 50158, Fax: (641) 754--2854, Phone: (641) 754-2026.Fisher Information Notice: FIN 2014-02>61-Jul. 21. 2014 3:09PMNo. 0266 P. 1EMERSON.[FISHER]Facsimile 301 South First AveMarshalltown, IA 50158T 641-754-3011 F 641-754-2830 To: NRC Operations Center -Alln:, Bill HUffmanFax: 301-815-5151 From: Dennis Swanson, Emerson Process Management Date: 712112014 Pages: 4(inc cover) |
|
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| ==Attachment:== | | ==Attachment:== |
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| Fisher Information Notice -(FIN) 2014-02For technical questions please contact Dennis Swanson at (641) 754-2381. | | Fisher Information Notice -(FIN) 2014-02For technical questions please contact Dennis Swanson at (641) 754-2381. |
| Ju,1- 21, 20143109MNo, 0266 P. 2EMERSON.Process ManagementFisher Controls International LLC301 South First Ave.P.O. Box 190Marshalltown, Iowa 50158-0190USAT (641) 754-3011F (641) 754-2830July 21, 2014To Whom It May Concern:Attached is a Fisher Information Notice, (FIN) 2014-02.Emerson Process Management -Fisher Valves complies with the reporting requirements of 10CFR Part 21 Section 21.21 (b) and 10 CFR Part 50.55 (e) by informing the U.S. NuclearRegulatory Commission Licensees or Purchaser of deviations or failures to comply.Please review the attached FIN notice for applicability to your facility.Dennis SwansonDirector, QualityValve Division -AmericasAttachments[FISHER | | Ju,1- 21, 20143109MNo, 0266 P. 2EMERSON.Process Management Fisher Controls International LLC301 South First Ave.P.O. Box 190Marshalltown, Iowa 50158-0190 USAT (641) 754-3011F (641) 754-2830July 21, 2014To Whom It May Concern:Attached is a Fisher Information Notice, (FIN) 2014-02.Emerson Process Management |
| ,Iul.21. 2014 3:10PMNo. 0266 P. 3EMERSON.. Fisher Controls International LLCProcess Management 301 South First Ava.P.O. Box 190Marshalitown, Iowa 501 5"-0190USAT (641) 754-3011F (641) 754-2830Fisher Information Notice: FIN 2014-02July 18, 2014Subiect: Fisher Orders: 033-F800216042 for Progress Energy -Brunswick033-F800200404 for Progress Energy -BrunswickFrom:Chad EngleDirector, Nuclear Business UnitFisher Controls International LLC301 South 1tAvenueMarshalltown, IA 50158Fax: (641) 754-2854Equipment Affected By This Information Notice:Items provided to Progress Energy -Brunswick per Fisher Order Number 033-F800216042, Items 0001, 0003, 0004, 0005, 0007, (Progress Energy PurchaseOrder 592286) and Fisher Order Number 033-F800200404, Item 0002 (ProgressEnergy Purchase Order 516573). This equipment included 125VDC Solenoids(quantity 6). The solenoids correspond to valves with Fisher Serial Numbers20659675, 20659677, 20659678, 20659679, 20659681, and 19875287.Purpose:The purpose of this Fisher Information Notice (FIN) is to alert Progress Energy-Brunswick that as of 26 June, 2014, Fisher Controls International LLC (Fisher) becameaware of the possibility of a situation which may affect the performance of the applicableequipment.We are informing you of this circumstance in accordance with Section 21.21 (b) of1OCFR21.Applicability:This notice applies only to the subject equipment supplied by Fisher, identified above,LFISRIERJ Page 1 of 2 Jul.21, 2014 3:10PMNo. 0266 P. 4Fisher Information Notice: FIN 2014-02that was provided to Progress Energy -Brunswick.DiscussionFisher has determined that the subject items did not meet the customer requestedconstruction per the Customer Purchase Orders.Specifically the discrepancies are:* Both Customer Purchase Orders specified 120VAC/6OHz solenoids. Fisherprovided solenoids that were 125VDC.A total of 10 items were ordered between the two Purchase Orders. A quantity of 6 wereshipped in February 2014 but all were identified as non-confon-ning prior to installationin the plant. The remaining 4 are on a shipping hold pending solenoid replacement.Action RequiredFisher will support Progress Energy -Brunswick in performing the replacement of thesolenoid valves at no cost to Progress Energy-In addition, a Corrective Action Request (CAR) is being initiated by Fisher to preventthis issue from reoccurring.10CFR21 Implications:Fisher requests that the recipient of this notice review it and take appropriate action inaccordance with 1 OCFR21.If there are any technical questions or concerns, please contact:George BaitingerManager, QualityFisher Controls International LLC301 South IMt AvenueMarshalltown, IA 50158Fax: (641) 754-2854Phone: (641) 754-2026GeorTce. BaitingerEmerson.com[FISHER] Page 2 of 2}} | | -Fisher Valves complies with the reporting requirements of 10CFR Part 21 Section 21.21 (b) and 10 CFR Part 50.55 (e) by informing the U.S. NuclearRegulatory Commission Licensees or Purchaser of deviations or failures to comply.Please review the attached FIN notice for applicability to your facility. |
| | Dennis SwansonDirector, QualityValve Division |
| | -AmericasAttachments |
| | [FISHER |
| | ,Iul.21. |
| | 2014 3:10PMNo. 0266 P. 3EMERSON.. |
| | Fisher Controls International LLCProcess Management 301 South First Ava.P.O. Box 190Marshalitown, Iowa 501 5"-0190USAT (641) 754-3011F (641) 754-2830Fisher Information Notice: FIN 2014-02July 18, 2014Subiect: |
| | Fisher Orders: 033-F800216042 for Progress Energy -Brunswick 033-F800200404 for Progress Energy -Brunswick From:Chad EngleDirector, Nuclear Business UnitFisher Controls International LLC301 South 1tAvenueMarshalltown, IA 50158Fax: (641) 754-2854Equipment Affected By This Information Notice:Items provided to Progress Energy -Brunswick per Fisher Order Number 033-F800216042, Items 0001, 0003, 0004, 0005, 0007, (Progress Energy PurchaseOrder 592286) and Fisher Order Number 033-F800200404, Item 0002 (Progress Energy Purchase Order 516573). |
| | This equipment included 125VDC Solenoids (quantity 6). The solenoids correspond to valves with Fisher Serial Numbers20659675, |
| | : 20659677, 20659678, |
| | : 20659679, 20659681, and 19875287. |
| | Purpose:The purpose of this Fisher Information Notice (FIN) is to alert Progress Energy-Brunswick that as of 26 June, 2014, Fisher Controls International LLC (Fisher) becameaware of the possibility of a situation which may affect the performance of the applicable equipment. |
| | We are informing you of this circumstance in accordance with Section 21.21 (b) of1OCFR21.Applicability: |
| | This notice applies only to the subject equipment supplied by Fisher, identified above,LFISRIERJ Page 1 of 2 Jul.21, 2014 3:10PMNo. 0266 P. 4Fisher Information Notice: FIN 2014-02that was provided to Progress Energy -Brunswick. |
| | Discussion Fisher has determined that the subject items did not meet the customer requested construction per the Customer Purchase Orders.Specifically the discrepancies are:* Both Customer Purchase Orders specified 120VAC/6OHz solenoids. |
| | Fisherprovided solenoids that were 125VDC.A total of 10 items were ordered between the two Purchase Orders. A quantity of 6 wereshipped in February 2014 but all were identified as non-confon-ning prior to installation in the plant. The remaining 4 are on a shipping hold pending solenoid replacement. |
| | Action RequiredFisher will support Progress Energy -Brunswick in performing the replacement of thesolenoid valves at no cost to Progress Energy-In addition, a Corrective Action Request (CAR) is being initiated by Fisher to preventthis issue from reoccurring. |
| | 10CFR21 Implications: |
| | Fisher requests that the recipient of this notice review it and take appropriate action inaccordance with 1 OCFR21.If there are any technical questions or concerns, please contact:George Baitinger |
| | : Manager, QualityFisher Controls International LLC301 South IMt AvenueMarshalltown, IA 50158Fax: (641) 754-2854Phone: (641) 754-2026GeorTce. |
| | BaitingerEmerson.com |
| | [FISHER] |
| | Page 2 of 2}} |
|
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Category:Deficiency Report (per 10CFR50.55e and Part 21)
MONTHYEARML24004A2092023-12-12012 December 2023 Flowline, Inc. - Interim Part 21 Report Notification Regarding Supply of 1 Sch. 80 (0.179 Wall) SB466 Uns C71500 Buttweld Long Radius 90 Degree Elbow; Manufacturer: Flowline; Heat No: 27668; 27 Pieces - Heat Code ML23352A2382023-12-0808 December 2023 56882-EN 56882 - Tioga Pipe, Inc Interim Part 21 Report Re Supply of 1 Inch Sch. 80 SB466 Uns C71500 Buttweld Long Radius 90 Degree Elbow ML23212A9502023-05-24024 May 2023 Engine Systems, Inc., Part 21 Report Re Woodward EGB-35P Governor/Actuator with Foreign Material ML21322A0512021-10-27027 October 2021 Paragon Energy Solutions, LLC, P21-09282021, Rev. 0, Final Notification of a Deviation with Inverter Assembly (Model NLI-072034-CSI-K-5-A) ML21295A2472021-10-18018 October 2021 Engine Systems, Inc., Part 21 Reportable Notification on a Pressure Regulator Valve ML21260A0072021-09-0909 September 2021 Ametek Solidstate Controls, Notification of Potential Defect - 10CFR Part 21 Report Re Omron Timer Relay ML19024A1642019-01-0707 January 2019 Ametek - Notification of Potential Defect - 10CFR Part 21 Re Solidstate Controls Safety-Related Operational Spare Parts Kits ML18102A5292018-04-0303 April 2018 10CFR21 Reporting of Defects and Non-Compliance - Engine Systems, Inc. Report No. 10CFR21-0121, Rev. 0, Refurbished Pressure Regulator Assembly, P/N 1776 506. ML18087A0032018-03-21021 March 2018 Crane Nuclear, Inc. - Part 21 Notification of Defect on Crane Nuclear Figure Number 83 1/2 Spl 10x8x10 and 6x4x6 Bolted Bonnet Gate Valve (Updated) ML18075A3552018-03-0606 March 2018 10 CFR Part 21 Notification of Defect on Crane Nuclear Figure Number 83 1/2 Spl 10x8x10 and 6x4x6 Bolted Bonnet Gate Valve ML18079A0142018-03-0606 March 2018 Crane Nuclear, Inc., 10 CFR Part 21 Notification of Defect on Crane Nuclear Figure Number 83 1/2 Spl I0x8x10 and 6x4x6 Bolted Bonnet Gate Valve ML17194A8252017-07-11011 July 2017 Part 21 Report Re Wedge Pin Failure in Anchor Darling Motor Operated Double Disc Gate Valves with Threaded Stem to Upper Wedge Connections ML17142A3232017-05-11011 May 2017 Interim Report Concerning Supply of Stainless Steel Tubing ML17081A4532017-03-20020 March 2017 Part 21 - Plastic Jar Dedication Sampling ML16281A2712016-09-30030 September 2016 Part 21 - Safety Related Component Welding by an Unqualified Welder ML16321A4502016-08-31031 August 2016 Part 21 Notification - Flowserve Swing Check Valves ML16243A4752016-08-26026 August 2016 Part 21 Safety Related Component Welding by an Unqualified Welder ML16188A3742016-06-30030 June 2016 Part 21 - Inadequate Swaging and Adherence of Silicone O-Ring and Silicone PAD Soft Seat Main Disc and Pilot Disc Assemblies ML16039A2692016-02-0303 February 2016 Nutherm International, Inc. - Potential Issue Regarding Incorrect Industrial Irradiation Dose, Per Cooper, Oconee, Fitzpatrick, Point Beach, Brunswick, and Susquehanna ML15265A4182015-09-21021 September 2015 Sor, Inc. - Part 21 Notification of Deviation - ML15251A212 Irradiation Certification with Insufficient Margin BSEP 15-0054, Part 21 Notification Regarding Allen Bradley Model 700RTC Relays2015-06-25025 June 2015 Part 21 Notification Regarding Allen Bradley Model 700RTC Relays ML15162A0232015-06-0909 June 2015 Part 21 - Incorrect Part Number Relay Shipped to Brunswick Nuclear Plant ML15173A0162015-06-0808 June 2015 Engine Systems, Inc. - 1OCFR21 Reporting of Defects and Non-Compliance - Report No. 10CFR21-0112, Rev. 0, Incorrect Relay Installed in Governor Control Panel, P/N 8002096-PANEL ML15155A5772015-05-28028 May 2015 Part 21 Notification Regarding Allen Bradley 700RTC Relay Configuration ML15103A2442015-04-0606 April 2015 Part 21 Report - Deviation of Hk Circuit Breaker Close Latch Spring ML14261A1502014-09-17017 September 2014 Interim Report to the NRC of 10 CFR 21 Event 50285, Reported by Itt 07/18/14 Concerning M1 Diaphragms, Customer Testing ML14210A0102014-07-23023 July 2014 Part 21 - Unseating of Valve Spring on Scram Solenoid Pilot Valve ML14204A7082014-07-23023 July 2014 Enclosure 2, Description of Closure Evaluation, Non-Proprietary Information - Class I (Public) ML14204A7072014-07-23023 July 2014 Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Unseating of Valve Spring on SSPV ML14210A0092014-07-21021 July 2014 Part 21 Report - Incorrect Valve Solenoids Provided ML14070A1832014-02-14014 February 2014 Part 21 Report - Failed Pressure Regulator During Post Installation EDG Pressure Testing ML13340A3822013-12-0505 December 2013 Part 21 Reportable Condition Notification: Failure of Relay Logic Card Modules in 2 Out of 4 Voters ML13165A3422013-06-12012 June 2013 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML13064A0122013-02-25025 February 2013 Notification of Potential Part 21 Report Re Wedge Pin Failure of an Anchor/Darling Double-Disc Gate Valve ML13044A0752013-02-0808 February 2013 Part 21 - Completed Evaluation for Potential Error in Main Steam Line High Flow Calculational Methodology ML12352A1232012-12-13013 December 2012 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML12348A1362012-12-13013 December 2012 Part 21 60-Day Interim Report Notification: Adequacy of Design Change in Am Magne-Blast Circuit Breakers ML12347A3082012-12-12012 December 2012 Part 21 60-Day Interim Report Notification: Error in Main Steam Line High Flow Calculational Methodology ML12318A0412012-11-0808 November 2012 Part 21 Report - Commercial Grade Dedication Not Properly Applied to Butterfly Valves ML12319A0122012-09-27027 September 2012 Error in Main Steam Line High Flow Calculational Methodology ML12177A0562012-06-21021 June 2012 Part 21 - Reliability Degradation of Resistors in Trip Units and Readout Assemblies ML12158A4472012-06-0606 June 2012 Part 21 60-Day Interim Report Notification - Closufailure of CRD Collet Retainer Tube/Outer Tube Weld ML12163A1302012-06-0606 June 2012 Part 21 Report - Failure of CRD Collet Retainer Tube/Outer Tube Weld ML12123A0892012-04-27027 April 2012 Abb, Inc., Notification of Potential Part 21 Report - Hk Circuit Breaker Studs Failed to Meet Specification ML12094A3712012-04-0202 April 2012 Part 21 Report - Rosemount Pressure Transmitters with Nonzero Based Calibrations ML12058A1412012-02-23023 February 2012 Part 21 Report - Rosemount Nuclear Instruments, Inc., Pressure Transmitter with Nonzero Based Calibrations ML12040A2832012-02-0707 February 2012 Notification of Potential Part 21 - Failure to Include Seismic Input in Reactor Control Blade Customer Guidance ML12038A0282012-02-0202 February 2012 Failure of CRD Collet Retainer Tube/Outer Tube Weld ML12032A2402012-02-0101 February 2012 Notification of Potential Part 21 - 60-Day Interim Report Notification: Failure of CRD Collet Retainer Tube/Outer Tube Weld ML11278A0762011-09-28028 September 2011 Abb, Inc. - 10 CFR Part 21 Notification of Potential Defect, Solid State Relays - Update of Previous Notification 2023-05-24
[Table view] Category:Facsimile
MONTHYEARML24037A0202024-02-0202 February 2024 LTR-NRC-2024-01 Mackson-Duke 10CFR Part 21 Final Notification and Closure 2.2.2024 ML21295A2472021-10-18018 October 2021 Engine Systems, Inc., Part 21 Reportable Notification on a Pressure Regulator Valve ML14210A0092014-07-21021 July 2014 Part 21 Report - Incorrect Valve Solenoids Provided 2024-02-02
[Table view] Category:Letter
MONTHYEARIR 05000324/20240102024-09-10010 September 2024 Focused Engineering Inspection Commercial Grade Dedication Report 05000324-2024010 and 05000325-2024010 ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 IR 05000324/20240052024-08-23023 August 2024 Updated Inspection Plan for Brunswick Steam Electric Plant, Units 1 and 2 (Report 05000324/2024005 and 05000325/2024005) IR 05000324/20240022024-08-0505 August 2024 Integrated Inspection Report 05000324/2024002 and 05000325/2024002 and 07200006/2024001 ML24206A1062024-07-30030 July 2024 2024 Brunswick Requal Inspection Corporate Notification Letter ML24183A0972024-07-12012 July 2024 ISFSI; Catawba 1, 2 & ISFSI; McGuire 1, 2 & ISFSI; Oconee 1, 2, 3 & ISFSI; Shearon Harris 1; H. B. Robinson 2 & ISFSI; and Radioactive Package Shipping Under 10 CFR 71 (71-266 & 71-345) – Review of QA Program Changes EPID L-2024-LLQ-0002 IR 05000324/20244202024-07-0202 July 2024 – Security Baseline Inspection Report 05000324/2024420 and 05000325/2024420 ML24108A0702024-06-0505 June 2024 – Issuance of License Amendments to Revise the 10 CFR 50.69 Categorization Process to Reflect an Alternative Seismic Approach IR 05000324/20244022024-05-17017 May 2024 Plan Material Control and Accounting Program Inspection Report 05000324/2024402 and 05000325/2024402 - Cover Letter IR 05000324/20240012024-05-0909 May 2024 Integrated Inspection Report 05000324/2024001 and 05000325/2024001 IR 05000324/20243012024-04-0303 April 2024 NRC Operator License Examination Report 05000325/2024301 and 05000324/2024301 ML24066A0132024-03-0505 March 2024 Bru 2024-002 Radiation Safety Baseline Inspection Information Request ML24026A0982024-03-0101 March 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0057 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) IR 05000324/20230062024-02-28028 February 2024 Annual Assessment Letter for Brunswick Steam Electric Plant, Units 1 and 2 – NRC Inspection Reports 05000324/2023006 and 05000325/2023006 IR 05000324/20244032024-02-14014 February 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perm Inspection 05000325/2024403; 05000324/2024403 ML24032A1392024-02-12012 February 2024 Correction of Errors within Authorized Alternative Request RA-22-0308 IR 05000324/20230042024-02-0606 February 2024 Integrated Inspection Report 05000324/2023004 and 05000325/2023004 IR 05000324/20230112023-12-26026 December 2023 NRC Fire Protection Team Inspection - FPTI Report 05000324/2023011 and 05000325/2023011 IR 05000324/20234022023-12-14014 December 2023 Security Baseline Inspection Report 05000324-2023402 and 05000325-2023402 ML23297A0262023-11-27027 November 2023 Proposed Alternatives to ASME Code Section XI Subsection IWE Requirements for Torus Metallic Liner Inspections ML23317A3462023-11-14014 November 2023 Duke Fleet - Correction Letter to License Amendment Nos. 312 & 340 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000324/20230032023-11-0101 November 2023 Integrated Inspection Report 05000324/2023003 and 05000325/2023003 IR 05000324/20230102023-10-17017 October 2023 Biennial Problem Identification and Resolution Inspection Report 05000324/2023010 and 05000325/2023010 IR 05000325/20234012023-10-16016 October 2023 Security Baseline Inspection Report 05000324 and 05000325 2023401 ML23346A1322023-10-0606 October 2023 Communication from C-10 Research & Education Foundation Regarding NextEra Common Emergency Fleet Plan License Amendment Request and Related Documents Subsequently Published ML23256A0882023-09-25025 September 2023 Issuance of Alternative to Steam Generator Welds ML23195A0782023-08-29029 August 2023 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000324/20230052023-08-23023 August 2023 Updated Inspection Plan for Brunswick Steam Electric Plant, Units 1 and 2 (Report 05000324/2023005 and 05000325/2023005) IR 05000324/20230022023-08-0404 August 2023 Integrated Inspection Report 05000324/2023002 and 05000325/2023002 ML23201A2042023-07-28028 July 2023 Summary of Regulatory Audit in Support of Alternative Request RA-22-0308 for Inservice Inspection of the Torus Metallic Liner ML23212B2682023-07-25025 July 2023 Notification of Licensed Operator Initial Examination 05000325/2024301 and 05000324/2024301 ML23146A0012023-05-24024 May 2023 EN 56538 - Engine Systems Inc and Brunswick ML23212A9502023-05-24024 May 2023 Engine Systems, Inc., Part 21 Report Re Woodward EGB-35P Governor/Actuator with Foreign Material ML23130A3902023-05-12012 May 2023 Regulatory Audit Plan in Support of Alternative Request RA 22-0308 for Inservice Inspection of the Torus Metallic Liner IR 05000324/20230012023-05-10010 May 2023 Integrated Inspection Report 05000324 2023001 and 05000325 2023001 ML23118A0762023-05-0101 May 2023 Approval for Use of Specific Provision of a Later Edition of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI IR 05000324/20220042023-04-0404 April 2023 Reissue - Brunswick Steam Electric Plant - Integrated Inspection Report 05000324/2022004 and 05000325/022004 ML22332A4932023-03-10010 March 2023 William States Lee III 1 and 2 - Issuance of Amendments Regarding the Relocation of the Emergency Operations Facility IR 05000324/20220062023-03-0101 March 2023 Annual Assessment Letter for Brunswick Steam Electric Plant, Units 1 and 2 NRC Inspection Reports 05000324/2022006 and 05000325/2022006 ML23033A5252023-02-0808 February 2023 Integrated Inspection Report 05000324/2022004 and 05000325/2022004 IR 05000324/20223012023-02-0303 February 2023 NRC Operator License Examination Report 05000325/2022301 and 05000324/2022301 ML22332A0132022-11-23023 November 2022 Operator Licensing Written Examination Approval 05000325/2022301 and 05000324/2022301 IR 05000324/20224022022-11-23023 November 2022 Security Baseline Inspection Report 05000324 2022402 and 05000325 2022402 ML22096A0032022-11-18018 November 2022 McGuire Nuclear Station and Shearon Harris Nuclear Power Plant Authorization of RA-19-0352 Regarding Use of Alternative for RPV Head Closure Stud Examinations ML22256A2532022-11-14014 November 2022 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-541, Rev. 2 IR 05000324/20224032022-11-10010 November 2022 Cyber Security Inspection Report 05000324/2022403 and 05000325/2022403 ML22307A1762022-11-0707 November 2022 Notification of an NRC Fire Protection Team Inspection (FPTI) IR 05000324/20220032022-11-0707 November 2022 Integrated Inspection Report 05000324/2022003 and 05000325/2022003 ML22258A0302022-09-15015 September 2022 Evacuation Time Estimate Reports IR 05000324/20220052022-08-24024 August 2022 Updated Inspection Plan for Brunswick Steam Electric Plant (Report 05000324/2022005 and 05000325/2022005) 2024-09-04
[Table view] |
Text
1)7121121)14 Pnop IU.2S.04 I Nucearr Ro-oulatorv Commissin Onperations.
Center Event Rennrt Pn"" IPart 21 (PAR) Event # 50291Rep Org: FISHER CONTROLS INTERNATIONAL Notification Date I Time: 07/21/2014 16:35 (EDT)Supplier:
FISHER CONTROLS INTERNATIONAL Event Date / Time: 06/26/2014 (CDT)Last Modification:
07/21/2014 Region: 3 Docket #:City: Marshalltown Agreement State: YesCounty: License #:State: IANRC Notified by: CHAD ENGLE Notifications:
STEVE ORTH R3DOHQ Ops Officer:
DONALD NORWOOD GERALD MCCOY R2DOEmergency Class: NON EMERGENCY PART 21 GROUP EMAIL10 CFR Section:21.21 (d)(3)(i)
DEFECTS AND NONCOMPLIANCE PART 21 REPORT -INCORRECT VALVE SOLENOIDS PROVIDEDThe following is a synopsis of information received via facsimile:
Brunswick Nuclear Plant ordered 10 (ten) 120VAC/6OHz valve solenoids on two purchase orders from FisherControls International LLC. In February, 2014, Fisher shipped six 125VDC solenoids to Brunswick.
All six of thosesolenoids were identified as non-conforming prior to installation in the plant. The remaining 4 solenoids at Fisherare on a shipping hold. For technical questions or concerns contact:
George Baitinger,
- Manager, Quality, FisherControls International.
LLC, 301 South 1st Ave, Marshalltown, IA 50158, Fax: (641) 754--2854, Phone: (641) 754-2026.Fisher Information Notice: FIN 2014-02>61-Jul. 21. 2014 3:09PMNo. 0266 P. 1EMERSON.[FISHER]Facsimile 301 South First AveMarshalltown, IA 50158T 641-754-3011 F 641-754-2830 To: NRC Operations Center -Alln:, Bill HUffmanFax: 301-815-5151 From: Dennis Swanson, Emerson Process Management Date: 712112014 Pages: 4(inc cover)
Attachment:
Fisher Information Notice -(FIN) 2014-02For technical questions please contact Dennis Swanson at (641) 754-2381.
Ju,1- 21, 20143109MNo, 0266 P. 2EMERSON.Process Management Fisher Controls International LLC301 South First Ave.P.O. Box 190Marshalltown, Iowa 50158-0190 USAT (641) 754-3011F (641) 754-2830July 21, 2014To Whom It May Concern:Attached is a Fisher Information Notice, (FIN) 2014-02.Emerson Process Management
-Fisher Valves complies with the reporting requirements of 10CFR Part 21 Section 21.21 (b) and 10 CFR Part 50.55 (e) by informing the U.S. NuclearRegulatory Commission Licensees or Purchaser of deviations or failures to comply.Please review the attached FIN notice for applicability to your facility.
Dennis SwansonDirector, QualityValve Division
-AmericasAttachments
[FISHER
,Iul.21.
2014 3:10PMNo. 0266 P. 3EMERSON..
Fisher Controls International LLCProcess Management 301 South First Ava.P.O. Box 190Marshalitown, Iowa 501 5"-0190USAT (641) 754-3011F (641) 754-2830Fisher Information Notice: FIN 2014-02July 18, 2014Subiect:
Fisher Orders: 033-F800216042 for Progress Energy -Brunswick 033-F800200404 for Progress Energy -Brunswick From:Chad EngleDirector, Nuclear Business UnitFisher Controls International LLC301 South 1tAvenueMarshalltown, IA 50158Fax: (641) 754-2854Equipment Affected By This Information Notice:Items provided to Progress Energy -Brunswick per Fisher Order Number 033-F800216042, Items 0001, 0003, 0004, 0005, 0007, (Progress Energy PurchaseOrder 592286) and Fisher Order Number 033-F800200404, Item 0002 (Progress Energy Purchase Order 516573).
This equipment included 125VDC Solenoids (quantity 6). The solenoids correspond to valves with Fisher Serial Numbers20659675,
- 20659677, 20659678,
- 20659679, 20659681, and 19875287.
Purpose:The purpose of this Fisher Information Notice (FIN) is to alert Progress Energy-Brunswick that as of 26 June, 2014, Fisher Controls International LLC (Fisher) becameaware of the possibility of a situation which may affect the performance of the applicable equipment.
We are informing you of this circumstance in accordance with Section 21.21 (b) of1OCFR21.Applicability:
This notice applies only to the subject equipment supplied by Fisher, identified above,LFISRIERJ Page 1 of 2 Jul.21, 2014 3:10PMNo. 0266 P. 4Fisher Information Notice: FIN 2014-02that was provided to Progress Energy -Brunswick.
Discussion Fisher has determined that the subject items did not meet the customer requested construction per the Customer Purchase Orders.Specifically the discrepancies are:* Both Customer Purchase Orders specified 120VAC/6OHz solenoids.
Fisherprovided solenoids that were 125VDC.A total of 10 items were ordered between the two Purchase Orders. A quantity of 6 wereshipped in February 2014 but all were identified as non-confon-ning prior to installation in the plant. The remaining 4 are on a shipping hold pending solenoid replacement.
Action RequiredFisher will support Progress Energy -Brunswick in performing the replacement of thesolenoid valves at no cost to Progress Energy-In addition, a Corrective Action Request (CAR) is being initiated by Fisher to preventthis issue from reoccurring.
10CFR21 Implications:
Fisher requests that the recipient of this notice review it and take appropriate action inaccordance with 1 OCFR21.If there are any technical questions or concerns, please contact:George Baitinger
- Manager, QualityFisher Controls International LLC301 South IMt AvenueMarshalltown, IA 50158Fax: (641) 754-2854Phone: (641) 754-2026GeorTce.
BaitingerEmerson.com
[FISHER]
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