IR 05000324/2024010

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Focused Engineering Inspection Commercial Grade Dedication Report 05000324-2024010 and 05000325-2024010
ML24248A206
Person / Time
Site: Brunswick  
Issue date: 09/10/2024
From: James Baptist
NRC/RGN-II/DRS/EB1
To: Krakuszeski J
Duke Energy Progress
References
IR 2024010
Download: ML24248A206 (1)


Text

SUBJECT:

BRUNSWICK UNITS 1 & 2 - FOCUSED ENGINEERING INSPECTION COMMERCIAL GRADE DEDICATION REPORT 05000324/2024010 AND 05000325/2024010

Dear John A. Krakuszeski:

On August 28, 2024, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Brunswick Units 1 & 2 and discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Brunswick Units 1 & 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at Brunswick Units 1 & 2.

September 10, 2024 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, James B. Baptist, Chief Engineering Branch 1 Division of Reactor Safety Docket Nos. 05000324 and 05000325 License Nos. DPR-62 and DPR-71

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000324 and 05000325

License Numbers:

DPR-62 and DPR-71

Report Numbers:

05000324/2024010 and 05000325/2024010

Enterprise Identifier:

I-2024-010-0047

Licensee:

Duke Energy Progress, LLC

Facility:

Brunswick Units 1 & 2

Location:

Southport, N.C.

Inspection Dates:

August 05, 2024 to August 28, 2024

Inspectors:

S. Egli, Sr. Construction Inspector

T. Fanelli, Senior Reactor Inspector

T. Su, Reactor Inspector

Approved By:

James B. Baptist, Chief

Engineering Branch 1

Division of Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a Focused Engineering Inspection Commercial Grade Dedication at Brunswick Units 1 & 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Maintain the Quality of Lubricants Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000325,05000324/2024010-01 Open/Closed

[H.3] - Change Management 71111.21N.

The NRC identified two examples of a Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion III for the failure to provide objective evidence of shelf life and ensure the quality assurance requirements for lubricants prior to their installation in their final locations.

Failure to Maintain Qualification of Relays Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000325,05000324/2024010-02 Open/Closed

[H.5] - Work Management 71111.21N.

The NRC identified a Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion III for the failure to install safety related relays in the configuration that maintained their qualification.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.21N.03 - Commercial Grade Dedication Commercial Grade Dedication

(1) Capacitors, CATID 9220128040
(2) Sealant (DC MCCB), CATID 51401651
(3) Current Transformer/Diode, CATID 9230036476
(4) Breakers: (MCCBs), CATID 73751653
(5) Relay Timing, CATID 9230032214
(6) Grout/Cement, CATID 9220093400
(7) Lubricants, Super-O-Lube CATID 73991622
(8) Lubricants, CATID 9220201439
(9) Gasket, CATID 69911352
(10) Thrust Bearing, CATID 73878852
(11) Pump, CATID

INSPECTION RESULTS

Failure to Maintain the Quality of Lubricants Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000325,05000324/2024010-01 Open/Closed

[H.3] - Change Management 71111.21N.0 The NRC identified two examples of a Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion III for the failure to provide objective evidence of shelf life and ensure the quality assurance requirements for lubricants prior to their installation in their final locations.

Description:

The inspection sampled two lubricants for which the manufacturer specified a five-year shelf life if stored at 68°F to 74°F & relative humidity 40-44% (MOV long life and Mobil grease XHP). Brunswick shelf life for lubricants (oils and greases) specified that shelf life was not applicable to any lubricants other than lube oil while stored in American National Standard Institute (ANSI) level B conditions (up to 140°F). The Brunswick Quality Assurance Program (QAP) is based on the criteria developed in ANSI N45.2, Quality Assurance Program Requirements for Nuclear Power Plants, and its criteria sub standards. For the control of purchase material equipment, and services, the QAP requires objective evidence of quality be furnished for purchased items. This required verifiable evidence, verifiable by the inspector. Standard N45.2.2, Packaging, Shipping, Receiving, Storage and Handling of Items for Nuclear Power Plants. The General requirements of section 6.1, stated, in part, that levels and methods of storage necessary are defined to minimize the possibility of damage or lowering of quality due to corrosion, contamination, deterioration or physical damage from the time an item is stored upon receipt until the time the item is removed from storage and placed in its final location.

Example 1: Duke Energy performed a corporate shelf-life evaluation. It is documented in Engineering Change (EC) 400765, Generic Shelf-Life Program, Revision 4. The EC specified that the quality of lubricants was not affected by degradation mechanisms prior to placement in its final location. The EC stated, DEPs historical practice of assigning lubricant shelf life per the guidance provided by Tables 1 and 2 below, combined with a lack of failures attributed to lubricant degradation in storage provides reasonable assurance that the current DEP practice is acceptable and shall continue as the acceptable practice for shelf life of lubricants. The table stated in part, No shelf life applicable (except as noted in TABLE 2 below). Table 2 excepted lube oil. The EC did not perform any technical evaluation of the degradation mechanisms (e.g., oxidation, moisture, temperature, and contaminants) to demonstrate that they are not in effect at Duke sites.

The inspectors observed that lubricants stored in the warehouse were degrading. For example, the oils in grease were leaching out and soaking into the containers they were stored in and onto the shelving. This degradation was contrary to the EC as stated above. In addition, the corrective action program (CAP) documented examples of degraded conditions that could be attributed to lubricant degradation and thus it could not be ruled out. Based on the inspector observations and CAP results the EC statement about lubricant degradation in storage was unsubstantiated. The inspectors determined that degraded lubricants could have been used for maintenance because the replacement frequencies were shorter than the specified life of the lubricants.

Example 2: The inspectors noted that, once lubricants were issued from the warehouse to the maintenance department, the quality of the storage conditions were not maintained to ensure the life of the lubricants were not degraded. The maintenance rooms did not have storage locations that were controlled by N45.2.2.

The manufactures of MOV long life and Mobil Grease specified that the established life was approximately five years dependent on if the containers were unopened and stored at around 68°F to 74°F. The inspectors noted that the storage and handling conditions in the maintenance areas were such that the lubricants could degrade further than allowed for by the lubricant specifications. The maintenance personnel did not have guidance to maintain the quality of the lubricants.

The Inspectors found the grease used for safety related components were checked out from the warehouse and stored in other areas of the plant unsealed without proper environmental controls before placement in their final locations i.e. in the components that required their application. Based on the observed degradation and recent degraded equipment examples in the CAP, the inspectors determined this was current licensee performance.

Corrective Actions: The licensee entered the issue into the corrective action program to restore compliance Corrective Action References: CR02526383

Performance Assessment:

Performance Deficiency: The failure to provide objective evidence of shelf life and ensure the quality assurance requirements for lubricants prior to their installation in their final locations was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Design Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the engineering changes that failed to evaluate objective evidence of the properties of lubricants (oils and greases) adversely affected the designed reliability of systems that respond to initiating events.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Exhibit 2, A.1, If the finding is a deficiency affecting the design or qualification of a mitigating SSC, does the SSC maintain its operability or PRA functionality? - YES --> GREEN Cross-Cutting Aspect: H.3 - Change Management: Leaders use a systematic process for evaluating and implementing change so that nuclear safety remains the overriding priority.

Leaders did not use a systematic process for evaluating the quality of lubricants over time with objective evidence and implementing that change so that nuclear safety remained the overriding priority.

Enforcement:

Violation: 10 CFR 50 Appendix B, to 10 CFR Part 50, Criterion III, Design Control, requires, in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in § 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions. These measures shall include provisions to assure that appropriate quality standards are specified and included in design documents and that deviations from such standards are controlled.

Contrary to the above, since 1995, the site did not provide design control measures to include provisions to assure that appropriate quality standards were specified and included in design documents for evaluating the quality of lubricants and that deviations from such standards for quality lubricants were controlled.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Maintain Qualification of Relays Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000325,05000324/2024010-02

[H.5] - Work Management 71111.21N.0

Open/Closed The NRC identified a Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion III for the failure to install safety related relays in the configuration that maintained their qualification.

Description:

The inspection sampled Allen Bradley 700-RTC relays that were commercial grade dedicated (CGD) by Nuclear Logistics Incorporated (NLI) for the site. The licensing basis required the relays to be qualified to the range of voltage, frequency, load, electromagnetic interference, and other electrical characteristics in accordance with IEEE 323-1974, IEEE Standard-for Qualifying Class 1E Equipment for Nuclear Power Generating Stations. To meet the electromagnetic interference requirement, the CGD used the tests and acceptance criteria in MIL-STD-461G, Requirements for The Control of Electromagnetic Interference Characteristics of Subsystems and Equipment.

Relay qualification report QR-700RTC-1, Rev. 1, identified electromagnetic interference (EMI)during MIL-STD-461G test for conducted susceptibility (test CS114) in the frequency range from 10 kHz - 30 MHz. Specifically, the degraded condition appeared in the range 2.6MHz to 20.3MHz and required the installation of a ferrite bead to mitigate the condition. This made the ferrite bead a required addition to the installed components in the emergency diesel generators (EDGs). The qualification report documents that the relay was successfully retested with input power lines wrapped three turns through a ferrite bead (Fair Rite P/N 0475176451).

Neither the ferrite beads or any other device to filter this noise was installed in the EDGs 700-RTC circuits. The 700-RTC relays are not installed in a qualified condition and are susceptible to failures due to conducted high frequency noise.

Corrective Actions: The licensee entered the issue into the corrective action program to restore compliance.

Corrective Action References: CR2526612

Performance Assessment:

Performance Deficiency: The failure to install safety related relays in the configuration that maintained their qualification was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Design Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to install the relays in the qualified condition exposed the EDGs to failures due to high frequency noise affecting the reliability.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Exhibit 2, A.1, If the finding is a deficiency affecting the design or qualification of a mitigating SSC, does the SSC maintain its operability or PRA functionality? - YES --> GREEN Cross-Cutting Aspect: H.5 - Work Management: The organization implements a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities.

The organization did not implement a process of planning, controlling, and executing work activities to install digital relay that were susceptible to high frequency interference such that nuclear safety is the overriding priority. The work process did not include the identification of different mitigation techniques for different kinds of interference and how that may be used to management the risk of using the relays commensurate with the work and the need for coordination with different groups or job activities

Enforcement:

Violation: 10 CFR 50 Appendix B, to 10 CFR Part 50, Criterion III, Design Control, requires, in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in § 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions.

Contrary to the above, since April 2016, the site failed to assure that applicable regulatory requirements and the design basis, for 700-RTC relay circuit installations were correctly translated into specifications, drawings, procedures, and instructions used to ensure the circuits were installed correctly.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On August 28, 2024, the inspectors presented the Focused Engineering Inspection Commercial Grade Dedication results to John A. Krakuszeski and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.21N.03

Calculations

BNP-E-2.006

Unit 1 480V Vital MCC Calculations

Rev. 22

71111.21N.03

Corrective Action

Documents

AR 00210659

Diesel Generator #1 Fuel Injection Leakage

10/27/2006

71111.21N.03

Corrective Action

Documents

AR 00327572

2-B32-F023A, 2-B32-F031A, 2-B32-F031B Failed Motor

Inspect

03/26/2009

71111.21N.03

Corrective Action

Documents

AR 00418628

2C RHR SW Booster Pump Making Very Loud Noise

When Running

08/26/2010

71111.21N.03

Corrective Action

Documents

AR 00755161

2C RHRSW Booster Pump Motor Brg has Oil Weepage

06/18/2015

71111.21N.03

Corrective Action

Documents

AR 02373438

2C RHR SW Booster Pump Has a Small Packing Leak

03/10/2021

71111.21N.03

Corrective Action

Documents

AR 02398997

1-E41-F004-MO Operator Will Not Go Into Manual Mode

09/23/2021

71111.21N.03

Corrective Action

Documents

AR 02488552

Minimum Bend Radius Not Achieved for Some FO and LO

Flex Hoses on EDGs

09/28/2023

71111.21N.03

Corrective Action

Documents

Resulting from

Inspection

AR 02526383

Discrepancies in Shelf Life Evaluation and Application

08/22/2024

71111.21N.03

Corrective Action

Documents

Resulting from

Inspection

AR 02526612

Relay Installation Not in Conformance With Qualification

Report

08/26/2024

71111.21N.03

Drawings

0-FP-5859

Valve Assembly Con-C-Cap Explosive Actuated

Rev. A

71111.21N.03

Drawings

0-FP-84248

8XI3AD Pump Cross Sectional Dwg

Rev. A

71111.21N.03

Drawings

DW-59310109

Fuel Injection Pump

03/21/1972

71111.21N.03

Engineering

Changes

00000067954

B,EE,Q2,Various,Grease,MOBILGREASE XHP 220

Series, EXXON MOBIL, JH/FS

Rev. 0

71111.21N.03

Engineering

Changes

0000073996

C, EE, Various, Various, Bearing, SKF, JB/JT/LC SKF

Explorer Bearing

Rev. 2

71111.21N.03

Engineering

Changes

0000079457

C, EE, Q2, VARIOUS, GREASE, MOV LONG LIFE,

FORSYTHE/CROMPTON, JT/JB

Rev. 0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.21N.03

Engineering

Changes

0000081016

C, CGI, Q2, Various, Lubricants, EXXONMOBIL, WP/MS

Rev. 2

71111.21N.03

Engineering

Changes

0000098353

C, CGI, Various, Bearing, Various Types, MH/JB

Rev. 0

71111.21N.03

Engineering

Changes

400765

Generic Shelf Life Program

Rev. 4

71111.21N.03

Engineering

Changes

EC 288479

C,EE,Q1,9220093400,Masterflow 928 Grout, BASF,

RFH/FS Reduction in Quick Lime Contained in Product

Rev. 0

71111.21N.03

Engineering

Changes

EC 411104

Service Water Intake Structure (SWIS) Repair Project

Rev. 7

71111.21N.03

Engineering

Evaluations

0944 VA20082

Westinghouse Nuclear Parts Audit Package

01/19/2021

71111.21N.03

Engineering

Evaluations

DR-79 EQ

Westinghouse Electric Corporation Report No. 30103-

CCR-4 Environmental Qualification for Nuclear Safety

Related Class 1E Components devices for Replacing

Functionally Equivalent Equipment In the G. E. 7700 Motor

Control Centers,

Rev. 4

71111.21N.03

Engineering

Evaluations

EWR 13462

Use of Loctite PST #580 at Brunswick Nuclear Plant

4/25/1994

71111.21N.03

Engineering

Evaluations

Material

Evaluation

003850.00

Gasket, Ring, 1-1/2", SS

09/17/1998

71111.21N.03

Engineering

Evaluations

Material

Evaluation 07646

GREASE, MOV LONG LIFE, Grades 0, 1, 2

07/28/2010

71111.21N.03

Engineering

Evaluations

ME No;

001203.00

Material Evaluation

07/07/1995

71111.21N.03

Engineering

Evaluations

QR-09314565-1

Qualification Report for Time Delay Relays Allen-Bradley

Rev. 1

71111.21N.03

Engineering

Evaluations

QR-700RTC-1

EMI-RFI Qualification Report for Allen-Bradley Relay Mod

Rev. 1

71111.21N.03

Engineering

Evaluations

VVR-700RTC-01

Commercial Grade Dedication Verification and Validation

Report

Rev. 0

71111.21N.03

Miscellaneous

00328626

QC Inspection Report for PO 03083136

2/05/2018

71111.21N.03

Miscellaneous

00333563

QC Inspection Report for PO 03092247

07/17/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.21N.03

Miscellaneous

00338666

QC Inspection Report for PO 03109526

04/07/2020

71111.21N.03

Miscellaneous

00344467

QC Inspection Report for PO 03125422

03/30/2021

71111.21N.03

Miscellaneous

00345522

QC Inspection Report for PO 03126732

05/18/2021

71111.21N.03

Miscellaneous

00346483

QC Inspection Report for PO 03120884

2/01/2021

71111.21N.03

Miscellaneous

238-011

Specification Horizontal Centrifugal Pumps for Service

Water Supply to Residual Heat Removal System

Rev. 7

71111.21N.03

Miscellaneous

27-01-201-1

Specification for Emergency Diesel Generator Sets

Rev. 4

71111.21N.03

Miscellaneous

DBD-39

Design Basis Document for Emergency Diesel Generator

and Supplemental Diesel Generator Systems

2/07/2024

71111.21N.03

Miscellaneous

DBDE-05

Design Basis Document: Standby Liquid Control System

Rev. 16

71111.21N.03

Miscellaneous

EPRI 1019518

Lubrication Guide

Rev. 4

71111.21N.03

Miscellaneous

EPRI NP-6408

Guidelines for Establishing, Maintaining, and Extending the

Shelf Life Capability of Limited Life Items.

Rev. 1

71111.21N.03

Miscellaneous

FP-50588

Technical Manual Valve, Explosive Actuated

Rev. 0

71111.21N.03

Miscellaneous

ME07922R00

Circuit Breakers & Supplementary Protectors Motor Circuit

Protectors

Rev. 0

71111.21N.03

Miscellaneous

Mobile Industrial

Lubricants

Technical Topic

Shelf Life Recommendations for Lubricating Oils and

Greases

2012

71111.21N.03

Miscellaneous

PO 03058272

Grout, Construction, Masterflow 928, Ref. BASF Product

Data Sht Form No 1019303

Rev. 1

71111.21N.03

Miscellaneous

PO 03083136

Lubricant, Grease, MOV Long Life, Grade 1, Tube, 14OZ

11/29/2018

71111.21N.03

Miscellaneous

PO 03092247

Bearing, Trust, 2.7559, 5.90550, 1.3780, Angular Contact,

Ball Bearing

05/09/2019

71111.21N.03

Miscellaneous

PO 03109526

Lubricant, Grease, Mobile Grease XHP 222, TU, 14 OZ

Tubes, 10 Tubes Per Cartoon

03/24/2020

71111.21N.03

Miscellaneous

PO 03110236

Relay, Timing, Solid State (RTC), 0.05-64 Minutes,

20VDC 110/120VAC, 5A, 4

Rev. 1

71111.21N.03

Miscellaneous

PO 03117513

GROUT, CONSTRUCTION, MASTERFLOW 928, REF.

BASF PRODUCT DATA SHT FORM NO 1019303

Rev. 0

71111.21N.03

Miscellaneous

PO 03118288

Sealant, Pipe, Thread, PST-580,

10/07/2020

71111.21N.03

Miscellaneous

PO 03118457

Transformer, Current, 0.333V Output, Input 5A, Split Core

Rev. 1

71111.21N.03

Miscellaneous

PO 03120884

Pump, Injection, Fuel, Diesel, Repairable

04/20/2021

71111.21N.03

Miscellaneous

PO 03125422

Lubricant, Grease, MOV Long Life, Grade 1, Tube, 14OZ

03/15/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.21N.03

Miscellaneous

PO 03126732

Gasket, Ring, 1-1/2 IN, 304SS

04/20/2021

71111.21N.03

Miscellaneous

PO 03167763

CAPACITOR,.., 7300MFD,150VDC

08/26/2023

71111.21N.03

Miscellaneous

PO 3110236

Receipt Inspection Report

08/21/2020

71111.21N.03

Miscellaneous

PO 3110236

Receipt Inspection Report

08/21/2020

71111.21N.03

Miscellaneous

PO

3114719_UTC

30192602

Receipt Inspection Report

01/13/2021

71111.21N.03

Miscellaneous

PO

3114719_UTC

30198086

Receipt Inspection Report

07/07/2021

71111.21N.03

Miscellaneous

PO03114719

Breaker, Motor Circuit Protector, 3 Amp Continuous

Rating, 9-30 Amp Magnetic Trip Range, 600VAC Max,

65,000 Amp Interrupting Current Rating at 480 VAC

Rev. 2

71111.21N.03

Miscellaneous

Purchase Order

(PO) 03114719

Breaker, Circuit, Thermal Magnetic, 600V, 3A,

65KAIC@480V, Non-Aluminum Terminals, 3P

Rev. 0

71111.21N.03

Procedures

0MMM-053

Equipment Lubrication Application Guidance and

Lubrication Listing

Rev. 133

71111.21N.03

Procedures

0PM-MO009

AC and DC Limitorque Motor Operated Valve Preventive

Maintenance Procedure

Rev. 22

71111.21N.03

Procedures

0PM-MO504

Mechanical Inspection and Lubrication of Limitorque

Operators

Rev. 48

71111.21N.03

Procedures

AD-EG-ALL-1103

Procurement Engineering Products

Rev. 7

71111.21N.03

Procedures

AD-PI-ALL-0400

Operating Experience Program

Rev. 13

71111.21N.03

Procedures

DUKE-QAPD-

001 -A-

Quality Assurance Program Description Operating Fleet

Amendment

71111.21N.03

Procedures

FP-20243

Valve Operators

05/14/2020

71111.21N.03

Procedures

NSCD-282

Shelf Life

Rev. 6

71111.21N.03

Procedures

NSCD-284

Contract and Acceptance of Services

Rev. 15

71111.21N.03

Procedures

NSCD-285

Procurement Process

Rev. 13

71111.21N.03

Procedures

NSCD-285A

Nuclear Sourcing Purchase Order PSG

Rev. 5

71111.21N.03

Procedures

NSCD-410

Receiving

Rev. 10

71111.21N.03

Procedures

NSCG-R-010

Fraud Detection

Rev. 0

71111.21N.03

Procedures

OE 127237

Degraded equipment voltage setpoints will not ensure ESF

operability

07/24/1992

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.21N.03

Procedures

OPT-06.1

Standby Liquid Control System Operability Test

Rev. 90

71111.21N.03

Procedures

OPT-12.2A

No. 1 Diesel Generator Monthly Load Test

Rev. 124

71111.21N.03

Work Orders

11771487 01

2-DG1-ENG: Replace Fuel Injection Pumps

08/23/2022

71111.21N.03

Work Orders

20397473 02

Unit 2A-1 Battery Removal and Replacement

04/08/2021

71111.21N.03

Work Orders

20409476 32

Reassemble Reactor Vessel and The Associated

Components

2/10/2021

71111.21N.03

Work Orders

20410923 01

2-B32-F031A-MO: OPM-0504 Mechanical and Lube

Inspection

03/21/2021

71111.21N.03

Work Orders

20482448 01

1-C41-F004B, Squib Valve Functional

Testing

03/29/2022

71111.21N.03

Work Orders

20568184 01

1-E41-F004-MO, OPM-O504 Mech. and Lube Inspection

06/26/2023

71111.21N.03

Work Orders

20644838 01

1-E11-F004A-MO Perform OPM-MO009 RHR 1A Supp

Pool Suc

07/25/2024