ML12227A711: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(5 intermediate revisions by the same user not shown)
Line 3: Line 3:
| issue date = 08/14/2012
| issue date = 08/14/2012
| title = IR 05000259-12-003, 05000260-12-003, 05000296-12-003, 05000259/2012502, 05000260/2012502, 05000296/2012502; 04/01/2012 -06/30/2012; Browns Ferry Nuclear Plant, Units 1, 2 and 3; Operability Evaluations, Radioactive Solid Waste Processing an
| title = IR 05000259-12-003, 05000260-12-003, 05000296-12-003, 05000259/2012502, 05000260/2012502, 05000296/2012502; 04/01/2012 -06/30/2012; Browns Ferry Nuclear Plant, Units 1, 2 and 3; Operability Evaluations, Radioactive Solid Waste Processing an
| author name = Guthrie E F
| author name = Guthrie E
| author affiliation = NRC/RGN-II/DRP
| author affiliation = NRC/RGN-II/DRP
| addressee name = Shea J W
| addressee name = Shea J
| addressee affiliation = Tennessee Valley Authority
| addressee affiliation = Tennessee Valley Authority
| docket = 05000259, 05000260, 05000296
| docket = 05000259, 05000260, 05000296
Line 14: Line 14:
| page count = 72
| page count = 72
}}
}}
See also: [[followed by::IR 05000259/2012003]]
See also: [[see also::IR 05000259/2012003]]


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:UNITED STATES
[[Issue date::August 14, 2012]]
                                NUCLEAR REGULATORY COMMISSION
                                                REGION II
                            245 PEACHTREE CENTER AVENUE NE, SUITE 1200
                                      ATLANTA, GEORGIA 30303-1257
                                            August 14, 2012
Mr. Joseph W. Shea
Vice President, Nuclear Licensing
Tennessee Valley Authority
1101 Market Street, LP 4B-C
Chattanooga, TN 37402-2801
SUBJECT:         BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION
                REPORT 05000259/2012003, 05000260/2012003, 05000296/2012003,
                05000259/2012502, 05000260/2012502, AND 05000296/2012502
Dear Mr. Shea:
On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection report documents
the inspection results which were discussed on July 10, August 10 and 14th, 2012, with Mr.
Keith Polson and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations, orders, and with the conditions of your
license. The inspectors reviewed selected procedures and records, observed activities, and
interviewed personnel.
One NRC identified and 3 self revealing findings of very low safety significance (Green) were
identified during this inspection. Three of these findings were determined to involve violations of
NRC requirements. Further, a licensee-identified violation which was determined to be of very
low safety significance is listed in this report. The NRC is treating the violations as non-cited
violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy. If you contest these
non-cited violations, you should provide a response within 30 days of the date of this inspection
report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document
Control Desk, Washington DC 20555-0001, with copies to: (1) the Regional Administrator,
Region II; (2) the Director, Office of Enforcement, United States Nuclear Regulatory
Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Browns
Ferry Nuclear Plant.
In addition, if you disagree with any cross-cutting aspect assignment in the report, you should
provide a response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
Browns Ferry Nuclear Plant.


Mr. Joseph Vice President, Nuclear Licensing Tennessee Valley Authority 1101 Market Street, LP 4B-C Chattanooga, TN 37402-2801
J. Shea                                      2
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
enclosure, and your response (if any), will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                              Sincerely,
                                              /RA/
                                              Eugene F. Guthrie, Chief
                                              Special Project, Browns Ferry
                                              Division of Reactor Projects
Docket Nos.: 50-259, 50-260, 50-296
License Nos.: DPR-33, DPR-52, DPR-68
Enclosure: NRC Integrated Inspection Report 05000259/2012003,
            05000260/2012003, 05000296/2012003
cc w/encl. (See page 3)


SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000259/2012003, 05000260/2012003, 05000296/2012003, 05000259/2012502, 05000260/2012502, AND 05000296/2012502


==Dear Mr. Shea:==
_________________________                X SUNSI REVIEW COMPLETE
On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection report documents the inspection results which were discussed on July 10, August 10 and 14th, 2012, with Mr. Keith Polson and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations, orders, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. One NRC identified and 3 self revealing findings of very low safety significance (Green) were identified during this inspection. Three of these findings were determined to involve violations of NRC requirements. Further, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. The NRC is treating the violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy. If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with copies to: (1) the Regional Administrator, Region II; (2) the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Browns Ferry Nuclear Plant. In addition, if you disagree with any cross-cutting aspect assignment in the report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the Browns Ferry Nuclear Plant. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
OFFICE            RII:DRP        RII:DRP      RII:DRP        RII:DRP        RII:DRS          RII:DRS      RII:DRS
SIGNATURE          Via email      Via email    Via email      Via email      BRB /RA for/    BRB /RA for/  BRB /RA for/
NAME              DDumbacher    CStancil      PNiebaum        LPressley      MSpeck          RHamilton    CDykes
DATE                  08/14/2012    08/14/2012    08/14/2012      08/14/2012      08/14/2012      08/14/2012    08/14/2012
E-MAIL COPY?        YES    NO    YES      NO  YES      NO    YES      NO    YES      NO      YES      NO  YES      NO
OFFICE            RII:DRS        RII:DRS      RII:DRP        RII:DRP
SIGNATURE          Via email      Via email    Via email      EFG /RA/
NAME              RKellner      MCoursey      CKontz          EGuthrie
DATE                  07/26/2012    08/14/2012    08/14/2012      08/14/2012
E-MAIL COPY?        YES    NO    YES      NO  YES      NO    YES      NO    YES      NO      YES      NO  YES      NO
       
J. Shea                               3
cc w/encl:                               James L. McNees, CHP
K. J. Polson                            Director
Site Vice President                      Office of Radiation Control
Browns Ferry Nuclear Plant               Alabama Dept. of Public Health
Tennessee Valley Authority              P. O. Box 303017
Electronic Mail Distribution            Montgomery, AL 36130-3017
C.J. Gannon
General Manager
Browns Ferry Nuclear Plant
Tennessee Valley Authority
Electronic Mail Distribution
James E. Emens
Manager, Licensing
Browns Ferry Nuclear Plant
Tennessee Valley Authority
Electronic Mail Distribution
Manager, Corporate Nuclear Licensing -
BFN
Tennessee Valley Authority
Electronic Mail Distribution
Edward J. Vigluicci
Assistant General Counsel
Tennessee Valley Authority
Electronic Mail Distribution
T. A. Hess
Tennessee Valley Authority
Electronic Mail Distribution
Chairman
Limestone County Commission
310 West Washington Street
Athens, AL 35611
Donald E. Williamson
State Health Officer
Alabama Dept. of Public Health
RSA Tower - Administration
Suite 1552
P.O. Box 30317
Montgomery, AL 36130-3017


Sincerely,/RA/ Eugene F. Guthrie, Chief Special Project, Browns Ferry Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68
J. Shea                                4
Letter to Joseph W. Shea from Eugene Guthrie dated August 14, 2012
SUBJECT:      BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION
              REPORT 05000259/2012003, 05000260/2012003, 05000296/2012003,
              05000259/2012502, 05000260/2012502, AND 05000296/2012502
Distribution w/encl:
C. Evans, RII
L. Douglas, RII
OE Mail
RIDSNRRDIRS
PUBLIC
RidsNrrPMBrownsFerry Resource


===Enclosure:===
              U.S. NUCLEAR REGULATORY COMMISSION
NRC Integrated Inspection Report 05000259/2012003, 05000260/2012003, 05000296/2012003 cc w/encl. (See page 3)
                                REGION II
Docket Nos.:  50-259, 50-260, 50-296
License Nos.: DPR-33, DPR-52, DPR-68
Report No.:    05000259/2012003, 05000260/2012003, 05000296/2012003,
              05000259/2012502, 05000260/2012502, 05000296/2012502
Licensee:      Tennessee Valley Authority (TVA)
Facility:      Browns Ferry Nuclear Plant, Units 1, 2, and 3
Location:      Corner of Shaw and Nuclear Plant Roads
              Athens, AL 35611
Dates:        April 1, 2012, through June 30, 2012
Inspectors:    D. Dumbacher, Senior Resident Inspector
              C. Stancil, Senior Resident Inspector
              P. Niebaum, Resident Inspector
              L. Pressley, Resident Inspector
              M. Speck, Senior Emergency Preparedness Inspector (1EP2, 1EP3,
              1EP5, 4OA1)
              R. Hamilton, Senior Health Physicist (2RS1, 2RS2, 2RS6, 4OA1)
              C. Dykes, Health Physicist (2RS7)
              R. Kellner, Health Physicist (2RS8)
              M. Coursey, Reactor Inspector (1R08)
Approved by:  Eugene F. Guthrie, Chief
              Reactor Projects Special Branch
              Division of Reactor Projects
                                                                        Enclosure


=SUMMARY OF FINDINGS=
                                    SUMMARY OF FINDINGS
IR 05000259/2012003, 05000260/2012003, 05000296/2012003, 05000259/2012502, 05000260/2012502, 05000296/2012502; 04/01/2012 -06/30/2012; Browns Ferry Nuclear Plant, Units 1, 2 and 3; Operability Evaluations, Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation, and Event Follow-Up. The report covered a three month period of inspection by resident and regional inspectors. Four findings were identified. The significance of most findings is identified by their color (Green,  
IR 05000259/2012003, 05000260/2012003, 05000296/2012003, 05000259/2012502,
05000260/2012502, 05000296/2012502; 04/01/2012 -06/30/2012; Browns Ferry Nuclear Plant,
Units 1, 2 and 3; Operability Evaluations, Radioactive Solid Waste Processing and Radioactive
Material Handling, Storage, and Transportation, and Event Follow-Up.
The report covered a three month period of inspection by resident and regional inspectors. Four
findings were identified. The significance of most findings is identified by their color (Green,
White, Yellow, and Red) using Inspection Manual Chapter (IMC) 0609, Significance
Determination Process (SDP); and, the cross-cutting aspects were determined using IMC
0310, Components Within the Cross-Cutting Areas. Findings for which the SDP does not
apply may be Green or be assigned a severity level after NRC management review. The NRCs
program for overseeing the safe operation of commercial nuclear power reactors is described in
NUREG-1649, Reactor Oversight Process Revision 4, dated December 2006.
NRC Identified and Self-Revealing Findings
        Cornerstone: Initiating Events
        *  Green. A self-revealing finding (FIN) was identified for the licensees failure to
            perform preventive maintenance on the Unit 3 Main Control Room (MCR)
            annunciator power supplies. As a result, a power supply failed which led to a fire in
            annunciator panel 3-X-55-5A in the Unit 3 control room. The licensee initiated
            actions to extinguish the fire, replace the two affected power supplies and develop a
            preventive maintenance program to replace the power supplies every ten years.
            Additional corrective actions to replace all power supplies that have been installed for
            more than four years are pending. This was captured in the licensees corrective
            action program as problem event report (PER) 496592.
            The performance deficiency was determined to be more than minor because it was
            considered sufficiently similar to example 4.f of Inspection Manual Chapter (IMC)
            0612, Appendix E, for an issue that resulted in a fire hazard in a safety-related area
            of the plant. The finding was associated with the Initiating Events Cornerstone and
            required a phase 3 analysis in accordance with IMC 0609 because the finding
            increased the likelihood of, and actually caused, a fire in the Unit 3 control room.
            The phase 3 analysis determined that without an impact to additional plant
            equipment, or a major impact on human action failure rates, the finding was
            determined to be Green. The cause of this finding was related to the cross cutting
            aspect of Problem Identification in the Corrective Action Program component of the
            Problem Identification and Resolution area because the licensee should have
            recognized the electrolytic capacitors were installed beyond their recommended
            service life and scheduled replacement prior to their failure [P.1(a)]. (Section
            4OA3.6)
                                                                                            Enclosure


White, Yellow, and Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP); and, the cross-cutting aspects were determined using IMC 0310, "Components Within the Cross-Cutting Areas". Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process" Revision 4, dated December 2006.
                                      3
Cornerstone: Mitigating Systems
*  Green. An NRC-identified non-cited violation (NCV) of the Technical Specifications
  5.4.1.a was identified for the licensees failure to maintain an Emergency Equipment
  Cooling Water (EECW) pump flood barrier in accordance with written procedures
  which resulted in the inoperability of two other safety related pumps. The licensee
  immediately restored the flood protection configuration of the C Residual Heat
  Removal Service Water (RHRSW) pump room by properly re-installing the flood
  protection cover and permanently stenciled the aluminum plate with the required
  procedure for installation. The licensee entered this issue into their corrective action
  program as PER 532050.
  The finding was more than minor because it was associated with the Mitigating
  Systems cornerstone attribute of Protection Against External Events, and adversely
  affected the cornerstone objective to ensure the availability, reliability, and capability
  of RHRSW pumps to perform their intended safety function during a design basis
  flooding event. Specifically, the improper re-installation of an external flood
  protection cover resulted in the inoperability of two Residual Heat Removal Service
  Water (RHRSW) pumps. The significance of this finding was evaluated in
  accordance with the IMC 0609 Attachment 4, Phase 1- Initial Screening and
  Characterization of Findings, which required a Phase 3 analysis because the finding
  involved the degradation of equipment designed to mitigate a flooding event and it
  was risk significant due to external initiating event core damage sequences. The
  finding was determined to be Green because of the short exposure time, and the low
  likelihood of the flood. The cause of this finding was directly related to the cross
  cutting aspect of Supervisory Oversight in the Work Practices component of the
  Human Performance area, because of the foremans assumption that workers knew
  to restore the flood protection cover to meet procedural requirements without a
  formal pre-job brief [H.4(c)]. (Section 1R15)
Cornerstone: Public Radiation Safety
*  Green. A self-revealing non-cited violation (NCV) of 10 CFR 71.5, Transportation of
  Licensed Material, was identified by inspectors for the licensees failure to comply
  with Department of Transportation (DOT) regulations during shipment of radioactive
  materials. Specifically, the licensee failed to ensure proper packaging of two DOT 7A
  Type A packages as required by Department of Transportation (DOT) regulations in
  49 CFR 173.475, Quality Control Requirements Prior To Each Shipment Of Class 7
  (Radioactive) Materials. This issue has been entered into the licensees corrective
  action program as SR 570902.
  The finding was more than minor because it is associated with the Public Radiation
  Safety Cornerstone, Plant Facilities/Equipment and Instrumentation attribute,
  involving transportation packaging and adversely affected the cornerstone objective,
  to ensure adequate protection of public health and safety from exposure to
  radioactive materials released into the public domain as a result of routine civilian
  nuclear reactor operation. Specifically, the failure to correctly secure the package
                                                                                  Enclosure


===NRC Identified and Self-Revealing Findings===
                                      4
  contents to prevent movement could have resulted in damage or failure of the
  container during transportation. The finding was determined to be of very low safety
  significance (Green) because it did not involve radiation limits being exceeded, a
  package breach, a certificate of compliance issue, a low-level burial ground non-
  conformance, or a failure to make emergency notifications. The cause of this finding
  was directly related to the cross cutting aspect of Documents, Procedures and
  Component Labeling in the Resources component of the Human Performance area
  because the licensee did not effectively incorporate package design specifications
  into their transportation program to ensure that all internal restraining devices are
  correctly installed to secure the CRDM in place to prevent damage to the transport
  package. (H.2(c)) (Section 2RS8)
* Green. A self-revealing non-cited violation (NCV) of 10 CFR 71.5, Transportation of
  Licensed Material, was identified by inspectors for the licensees failure to comply
  with Department of Transportation (DOT) regulations during shipment of radioactive
  materials. Specifically, the licensee failed to ensure proper closure of a DOT 7A Type
  A package as required by Department of Transportation (DOT) regulations in 49
  CFR 173.475, Quality Control Requirements Prior To Each Shipment Of Class 7
  (Radioactive) Materials. This issue has been entered into the licensees corrective
  action program as SR 571151.
  The finding was more than minor because it is associated with the Public Radiation
  Safety Cornerstone, Plant Facilities/Equipment and Instrumentation attribute,
  involving transportation packaging and adversely affected the cornerstone objective,
  to ensure adequate protection of public health and safety from exposure to
  radioactive materials released into the public domain as a result of routine civilian
  nuclear reactor operation. Specifically, the failure to apply the correct torque to the
  package closure bolts could have resulted in incomplete sealing of the container or
  failure of the cover bolts during transportation. The finding was determined to be of
  very low safety significance (Green) because it did not involve radiation limits being
  exceeded, a package breach, a certificate of compliance issue, a low-level burial
  ground non-conformance, or a failure to make emergency notifications. The cause
  of this finding was directly related to the cross cutting aspect of Documents,
  Procedures and Component Labeling in the Resources component of the Human
  Performance area because the licensee did not effectively incorporate the vendor
  provided container loading and shipping instructions into their work package and
  transportation program to ensure correct torque values were used to close the
  shipping container. (H.2(c)) (Section 2RS8).
                                                                                Enclosure


===Cornerstone: Initiating Events===
                                          REPORT DETAILS
: '''Green.'''
Summary of Plant Status
A self-revealing finding (FIN) was identified for the licensee's failure to perform preventive maintenance on the Unit 3 Main Control Room (MCR) annunciator power supplies. As a result, a power supply failed which led to a fire in annunciator panel 3-X-55-5A in the Unit 3 control room. The licensee initiated actions to extinguish the fire, replace the two affected power supplies and develop a preventive maintenance program to replace the power supplies every ten years. Additional corrective actions to replace all power supplies that have been installed for more than four years are pending. This was captured in the licensee's corrective action program as problem event report (PER) 496592. The performance deficiency was determined to be more than minor because it was considered sufficiently similar to example 4.f of Inspection Manual Chapter (IMC)0612, Appendix E, for an issue that resulted in a fire hazard in a safety-related area of the plant. The finding was associated with the Initiating Events Cornerstone and required a phase 3 analysis in accordance with IMC 0609 because the finding increased the likelihood of, and actually caused, a fire in the Unit 3 control room. The phase 3 analysis determined that without an impact to additional plant equipment, or a major impact on human action failure rates, the finding was determined to be
Unit 1 operated at full power for most of the report period except for an unplanned downpower
: '''Green.'''
on June 29, 2012, to 75 percent power to reduce load on the B Phase Main Bank Transformer
The cause of this finding was related to the cross cutting aspect of Problem Identification in the Corrective Action Program component of the Problem Identification and Resolution area because the licensee should have recognized the electrolytic capacitors were installed beyond their recommended service life and scheduled replacement prior to their failure [P.1(a)].  (Section 4OA3.6) 
due to a lifting oil pressure relief. The unit returned to full power on June 30, 2012.
Unit 2 operated at full power for most of the report period except for one planned and one
unplanned downpower. On April 20, 2012, the unit performed a planned downpower to 66
percent power for rod pattern adjustment, scram time testing and turbine valve testing. The unit
returned to full power on April 22nd. On May 15, 2012, the unit performed an unplanned
downpower to 92 percent power to insert control rod 30-51 for scram outlet valve repair and
returned to full power the same day.
Unit 3 operated at full power for most of the report period except for one planned downpower,
one manual and two automatic scrams, and one unplanned downpower. On April 6, 2012, the
unit was shutdown for a scheduled refueling outage that lasted 49 days. The unit was restarted
on May 19th. On May 22nd, an automatic scram occurred from 19.5 percent power with the
main turbine generator offline due to a 3A Unit Station Service Transformer differential relay trip
caused by incorrect relay setting. On May 24, 2012, during reactor startup and heatup an
unplanned manual scram occurred as a result of a partial control rod insertion caused by a
combination of a signal spike and an inappropriate operator downrange on separate
intermediate power range monitors. The unit restarted the same day. On May 29, 2012, a main
generator current transformer manufactured and installed with reverse polarity caused an
automatic scram from 75 percent power. The unit restarted on June 2nd and returned to full
power on June 5th. On June 6th, the unit performed an unplanned downpower from 96 percent
power to 75 percent power to remove the 3B condensate booster pump with high moisture in its
oil system from service. The unit returned to full power on June 8, 2012.
1.      REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
  .1  Offsite and Alternate Alternating Current (AC) Power Systems Readiness
  a.  Inspection Scope
        Prior to the summer season, inspectors reviewed electrical power design features, onsite
        risk and work management procedures, and corporate transmission and power supply
        procedures to verify appropriate operational oversight and assurance of continued
        availability of offsite and alternate AC power systems. Inspectors verified that
        communications protocols existed between the transmission system operator and
        Browns Ferry Nuclear Plant for coordination of off-normal and emergency events
        affecting the plant, event details, estimates of return-to-service times, and notifications of
        grid status changes. Inspectors also verified that procedures included controls to
                                                                                            Enclosure


===Cornerstone: Mitigating Systems===
                                            6
: '''Green.'''
    adequately monitor both offsite AC power systems (including post-trip voltages) and
An NRC-identified non-cited violation (NCV) of the Technical Specifications 5.4.1.a was identified for the licensee's failure to maintain an Emergency Equipment Cooling Water (EECW) pump flood barrier in accordance with written procedures which resulted in the inoperability of two other safety related pumps. The licensee immediately restored the flood protection configuration of the C Residual Heat Removal Service Water (RHRSW) pump room by properly re-installing the flood protection cover and permanently stenciled the aluminum plate with the required procedure for installation. The licensee entered this issue into their corrective action program as PER 532050. The finding was more than minor because it was associated with the Mitigating Systems cornerstone attribute of Protection Against External Events, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of RHRSW pumps to perform their intended safety function during a design basis flooding event. Specifically, the improper re-installation of an external flood protection cover resulted in the inoperability of two Residual Heat Removal Service Water (RHRSW) pumps. The significance of this finding was evaluated in accordance with the IMC 0609 Attachment 4, Phase 1- Initial Screening and Characterization of Findings, which required a Phase 3 analysis because the finding involved the degradation of equipment designed to mitigate a flooding event and it was risk significant due to external initiating event core damage sequences. The finding was determined to be Green because of the short exposure time, and the low likelihood of the flood. The cause of this finding was directly related to the cross cutting aspect of Supervisory Oversight in the Work Practices component of the Human Performance area, because of the foreman's assumption that workers knew to restore the flood protection cover to meet procedural requirements without a formal pre-job brief [H.4(c)]. (Section 1R15) 
    onsite alternate AC power systems for availability and reliability. Furthermore,
    inspectors interviewed onsite licensed operators and offsite transmission personnel to
    determine their understanding and implementation of the power monitoring and
    assessment process. Inspectors reviewed the material condition of offsite AC power
    systems and onsite alternate AC power systems to the plant, including switchyard and
    transformers. This review included review of outstanding work orders affecting these
    systems and a walkdown of the switchyard with operations personnel to ensure the
    systems will continue to provide appropriate as designed capabilities. This activity
    constituted one Offsite and AC Readiness sample.
b.  Findings
    No findings were identified.
.2  Readiness for Seasonal Extreme Weather Conditions
a.  Inspection Scope
    Prior to and during the onset of hot weather conditions, the inspectors reviewed the
    licensees implementation of 0-GOI-200-3, Hot Weather Operations. The inspectors
    also reviewed the Hot Weather Discrepancy Log; and discussed implementation of
    0-GOI-200-3 with responsible Operations personnel and management. Furthermore, the
    inspectors conducted walkdowns of potentially affected risk significant equipment
    systems located in the Unit 1 and 2 Diesel Generator Building, and the Unit 3 Diesel
    Generator Building. The inspectors also performed a walkdown of the Standby Gas
    Treatment (SBGT) Building. This activity constituted one Readiness for Seasonal
    Extreme Weather sample.
b.  Findings
    No findings were identified.
1R04 Equipment Alignment
.1  Partial Walkdown
a.  Inspection Scope
    The inspectors conducted three partial equipment alignment walkdowns to evaluate the
    operability of selected redundant trains or backup systems, listed below, while the other
    train or subsystem was inoperable or out of service. The inspectors reviewed the
    functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system
    operating procedures, and Technical Specifications to determine correct system lineups
    for the current plant conditions. The inspectors performed walkdowns of the systems to
    verify that critical components were properly aligned and to identify any discrepancies
    which could affect operability of the redundant train or backup system. This activity
    constituted three Equipment Alignment inspection samples.
                                                                                      Enclosure


===Cornerstone: Public Radiation Safety===
                                            7
: '''Green.'''
    *    Unit 1&2 A Emergency Diesel Generator
A self-revealing non-cited violation (NCV) of 10 CFR 71.5, Transportation of Licensed Material, was identified by inspectors for the licensee's failure to comply with Department of Transportation (DOT) regulations during shipment of radioactive materials. Specifically, the licensee failed to ensure proper packaging of two DOT 7A Type A packages as required by Department of Transportation (DOT) regulations in 49 CFR 173.475, Quality Control Requirements Prior To Each Shipment Of Class 7 (Radioactive) Materials. This issue has been entered into the licensee's corrective action program as SR 570902. The finding was more than minor because it is associated with the Public Radiation Safety Cornerstone, Plant Facilities/Equipment and Instrumentation attribute, involving transportation packaging and adversely affected the cornerstone objective, to ensure adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. Specifically, the failure to correctly secure the package contents to prevent movement could have resulted in damage or failure of the container during transportation. The finding was determined to be of very low safety significance (Green) because it did not involve radiation limits being exceeded, a package breach, a certificate of compliance issue, a low-level burial ground non-conformance, or a failure to make emergency notifications. The cause of this finding was directly related to the cross cutting aspect of Documents, Procedures and Component Labeling in the Resources component of the Human Performance area because the licensee did not effectively incorporate package design specifications into their transportation program to ensure that all internal restraining devices are correctly installed to secure the CRDM in place to prevent damage to the transport package. (H.2(c)) (Section 2RS8)
    *    Unit 3 Residual Heat Removal System - Division II
: '''Green.'''
    *    Unit 1 Reactor Core Isolation Cooling (RCIC) System
A self-revealing non-cited violation (NCV) of 10 CFR 71.5, Transportation of Licensed Material, was identified by inspectors for the licensee's failure to comply with Department of Transportation (DOT) regulations during shipment of radioactive materials. Specifically, the licensee failed to ensure proper closure of a DOT 7A Type A package as required by Department of Transportation (DOT) regulations in 49 CFR 173.475, Quality Control Requirements Prior To Each Shipment Of Class 7 (Radioactive) Materials. This issue has been entered into the licensee's corrective action program as SR 571151. The finding was more than minor because it is associated with the Public Radiation Safety Cornerstone, Plant Facilities/Equipment and Instrumentation attribute, involving transportation packaging and adversely affected the cornerstone objective, to ensure adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. Specifically, the failure to apply the correct torque to the package closure bolts could have resulted in incomplete sealing of the container or failure of the cover bolts during transportation. The finding was determined to be of very low safety significance (Green) because it did not involve radiation limits being exceeded, a package breach, a certificate of compliance issue, a low-level burial ground non-conformance, or a failure to make emergency notifications. The cause of this finding was directly related to the cross cutting aspect of Documents,
b. Findings
Procedures and Component Labeling in the Resources component of the Human Performance area because the licensee did not effectively incorporate the vendor provided container loading and shipping instructions into their work package and transportation program to ensure correct torque values were used to close the shipping container. (H.2(c)) (Section 2RS8).
    No findings were identified.
1R05 Fire Protection
.1  Fire Protection Tours
a. Inspection Scope
    The inspectors reviewed licensee procedures, Nuclear Power Group Standard Programs
    and Processes NPG-SPP-18.4.7, Control of Transient Combustibles, and NPG-SPP-
    18.4.6, Control of Fire Protection Impairments, and conducted a walkdown of the four
    fire areas (FA) and fire zones (FZ) listed below. Selected FAs/FZs were examined in
    order to verify licensee control of transient combustibles and ignition sources; the
    material condition of fire protection equipment and fire barriers; and operational lineup
    and operational condition of fire protection features or measures. Furthermore, the
    inspectors reviewed applicable portions of the Fire Protection Report, Volumes 1 and 2,
    including the applicable Fire Hazards Analysis, and Pre-Fire Plan drawings, to verify that
    the necessary firefighting equipment, such as fire extinguishers, hose stations, ladders,
    and communications equipment, was in place. This activity constituted four Fire
    Protection inspection samples.
    *    Unit 2 Reactor Building Elevations 519, 541, and 565 west of column line R11 (FZ 2-
          1)
    *    Unit 3 Reactor Building, EL 593 and residual heat removal (RHR) heat exchanger
          rooms, EL 565, and 593 near column R15-S and R21-S (FZ 3-3)
    *    Unit 1, Control Building, EL 593 (FA 16)
    *    Unit 1,2, and 3 Turbine Building Deluge Sprinkler Control Stations Affecting Control
          Bay (FA 25)
b. Findings
    No findings were identified.
                                                                                      Enclosure


=REPORT DETAILS=
                                            8
Summary of Plant Status Unit 1 operated at full power for most of the report period except for an unplanned downpower on June 29, 2012, to 75 percent power to reduce load on the B Phase Main Bank Transformer due to a lifting oil pressure relief. The unit returned to full power on June 30, 2012. Unit 2 operated at full power for most of the report period except for one planned and one unplanned downpower. On April 20, 2012, the unit performed a planned downpower to 66 percent power for rod pattern adjustment, scram time testing and turbine valve testing. The unit returned to full power on April 22nd. On May 15, 2012, the unit performed an unplanned downpower to 92 percent power to insert control rod 30-51 for scram outlet valve repair and returned to full power the same day. Unit 3 operated at full power for most of the report period except for one planned downpower, one manual and two automatic scrams, and one unplanned downpower. On April 6, 2012, the unit was shutdown for a scheduled refueling outage that lasted 49 days. The unit was restarted on May 19th. On May 22nd, an automatic scram occurred from 19.5 percent power with the main turbine generator offline due to a 3A Unit Station Service Transformer differential relay trip caused by incorrect relay setting. On May 24, 2012, during reactor startup and heatup an unplanned manual scram occurred as a result of a partial control rod insertion caused by a combination of a signal spike and an inappropriate operator downrange on separate intermediate power range monitors. The unit restarted the same day. On May 29, 2012, a main generator current transformer manufactured and installed with reverse polarity caused an automatic scram from 75 percent power. The unit restarted on June 2nd and returned to full power on June 5th. On June 6th, the unit performed an unplanned downpower from 96 percent power to 75 percent power to remove the 3B condensate booster pump with high moisture in its oil system from service. The unit returned to full power on June 8,
1R07 Heat Sink Performance
.1  Annual Review
a.  Inspection Scope
    The inspectors examined activities associated with Unit 3 RHR Heat Exchangers. The
    inspectors also reviewed design basis documents, calculations, test procedures,
    maintenance procedures and preventive maintenance procedures and results to
    evaluate the licensees program for maintaining heat sinks in accordance with the
    licensing basis. Specifically inspectors reviewed modifications performed on the Unit 3
    RHR Heat Exchanger Flanges. Inspectors reviewed available performance testing
    documentation of the 3A and 3C RHR Heat Exchangers.
    In addition, the inspectors reviewed the licensees implementation of the GL 89-13
    program. Inspectors reviewed associated PERs and corrective actions to verify that the
    licensee was identifying issues and correcting them. The inspectors performed
    walkdowns of key components of the Unit 3 RHR system to verify material conditions
    were acceptable and physical arrangement matched procedures and drawings. This
    activity constituted one Annual Heat Sink sample.
b.  Findings
    No findings were identified.
1R08 Inservice Inspection (ISI) Activities (71111.08G, Unit 3)
a.  Inspection Scope
    Non-Destructive Examination (NDE) Activities and Welding Activities: From April 16 to
    April 20, 2012, the inspectors conducted an on-site review of the implementation of the
    licensees Inservice Inspection (ISI) Program for monitoring degradation of the reactor
    coolant system, emergency feedwater systems, risk-significant piping and components,
    and containment systems in Unit 3. The inspectors activities included a review of non-
    destructive examinations (NDEs) to evaluate compliance with the applicable edition of
    the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel
    Code (BPVC), Section XI (Code of record: 2001 Edition with 2003 Addenda), and to
    verify that indications and defects (if present) were appropriately evaluated and
    dispositioned in accordance with the requirements of the ASME Code, Section XI,
    acceptance standards.
    The inspectors directly observed the following NDE mandated by the ASME Code to
    evaluate compliance with the ASME Code Section XI and Section V requirements and, if
    any indications and defects were detected, to evaluate if they were dispositioned in
    accordance with the ASME Code or an NRC-approved alternative requirement.
                                                                                      Enclosure


==REACTOR SAFETY==
                                        9
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  1R01 Adverse Weather Protection
  *  UT Exam of Weld DRHR-03-03, 3-FCV-74-53, Low Pressure Coolant Injection
      (LPCI) Loop I Inlet
  *  UT Exam of Weld DSRHR-03-04, 3-HCV-74-55, 24 in. inlet for Recirculation Loop B
  The inspectors reviewed records of the following NDEs mandated by the ASME Code
  Section XI to evaluate compliance with the ASME Code Section XI and Section V
  requirements and, if any indications and defects were detected, to evaluate if they were
  dispositioned in accordance with the ASME Code or an NRC-approved alternative
  requirement.
  *  VT Exam of RPV-WASH-3-50, Reactor Pressure Vessel Stud Washer
  *  UT Exam of weld DRHR-03-12, 3-FCV-74-67, LPCI Loop II Inlet
  *  EVT of BFN-3-RPV-068-RA048 Standpipe in Unit 3 Steam Separator
  *  EVT of BFN-3-RPV-068-RA050 U3 Feedwater Sparger End Brackets
  The inspectors reviewed associated documents for the welding activities referenced
  below in order to evaluate compliance with procedures and the ASME Code. The
  inspectors reviewed the work order, repair and replacement plan, weld data sheets,
  welding procedures, procedure qualification records, welder performance qualification
  records, and NDE reports.
  *  Work Order 04-719493-003, 3-FCV-073-016 HPCI Turbine Steam Supply Valve
  *  Work Order 08-718716-004, Replace Strain Gauges on MS Lines
  During non-destructive surface and volumetric examinations performed since the
  previous refuelling outage, the licensee did not identify any relevant indications that were
  analytically evaluated and accepted for continued service. Therefore, no NRC review
  was completed for this inspection procedure attribute.
  Identification and Resolution of Problems: The inspectors performed a review of a
  sample of ISI-related problems which were identified by the licensee and entered into
  the corrective action program as Problem Evaluation Reports (PERs). The inspectors
  reviewed the PERs to confirm the licensee had appropriately described the scope of the
  problem, and had initiated corrective actions. The review also included the licensees
  consideration and assessment of operating experience events applicable to the plant.
  The inspectors performed this review to ensure compliance with 10 CFR Part 50,
  Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action
  documents reviewed by the inspectors are listed in the report attachment.
b. Findings
  No findings were identified.
                                                                                    Enclosure


===.1 Offsite and Alternate Alternating Current (AC) Power Systems Readiness===
                                              10
1R11 Licensed Operator Requalification
.1   Resident Inspector Quarterly Review
a.  Inspection Scope
      On June 11, 2012, the inspectors observed an as-found licensed operator requalification
      simulator examination according to Unit 2 Simulator Exercise Guide OPL173.S039. The
      scenario involved Partial Loss of Reactor Building Closed Cooling Water, Loss of I & C
      Bus B, Anticipated Transient without Scram (ATWS), Lower Water Level (C-5) for Power
      Control with Bypass Valves.
    The inspectors specifically evaluated the following attributes related to the operating
    crews performance:
    *    Clarity and formality of communication
    *    Ability to take timely action to safely control the unit
    *    Prioritization, interpretation, and verification of alarms
    *    Correct use and implementation of Abnormal Operating Instructions (AOIs), and
          Emergency Operating Instructions (EOIs)
    *    Timely and appropriate Emergency Action Level declarations per Emergency Plan
          Implementing Procedures (EPIP)
    *    Control board operation and manipulation, including high-risk operator actions
    *    Command and Control provided by the Unit Supervisor and Shift Manager
    The inspectors attended the post-examination critique to assess the effectiveness of the
    licensee evaluators and to verify that licensee-identified issues were comparable to
    issues identified by the inspector. The inspectors reviewed simulator physical fidelity
    (i.e., the degree of similarity between the simulator and the reference plant control room,
    such as physical location of panels, equipment, instruments, controls, labels, and related
    form and function). This activity counts for one Observation of Requalification Activity
    inspection sample.
b.  Findings
      No findings were identified.
.2  Control Room Observations
a.  Inspection Scope
      Inspectors observed and assessed licensed operator performance in the plant and main
      control room, particularly during periods of heightened activity or risk and where the
      activities could affect plant safety. Inspectors reviewed various licensee policies and
      procedures such as OPDP-1, Conduct of Operations, NPG-SPP-10.0, Plant Operations
      and GOI-100-12, Power Maneuvering.
                                                                                        Enclosure


====a. Inspection Scope====
                                            11
Prior to the summer season, inspectors reviewed electrical power design features, onsite risk and work management procedures, and corporate transmission and power supply procedures to verify appropriate operational oversight and assurance of continued availability of offsite and alternate AC power systems. Inspectors verified that communications protocols existed between the transmission system operator and Browns Ferry Nuclear Plant for coordination of off-normal and emergency events affecting the plant, event details, estimates of return-to-service times, and notifications of grid status changes. Inspectors also verified that procedures included controls to adequately monitor both offsite AC power systems (including post-trip voltages) and onsite alternate AC power systems for availability and reliability. Furthermore, inspectors interviewed onsite licensed operators and offsite transmission personnel to determine their understanding and implementation of the power monitoring and assessment process. Inspectors reviewed the material condition of offsite AC power systems and onsite alternate AC power systems to the plant, including switchyard and transformers. This review included review of outstanding work orders affecting these systems and a walkdown of the switchyard with operations personnel to ensure the systems will continue to provide appropriate "as designed" capabilities. This activity constituted one Offsite and AC Readiness sample.
    Inspectors utilized activities such as post maintenance testing, surveillance testing and
    refueling and other outage activities to focus on the following conduct of operations as
    appropriate;
    *    Operator compliance and use of procedures.
    *    Control board manipulations.
    *    Communication between crew members.
    *    Use and interpretation of plant instruments, indications and alarms.
    *    Use of human error prevention techniques.
    *    Documentation of activities, including initials and sign-offs in procedures.
    *    Supervision of activities, including risk and reactivity management.
    *    Pre-job briefs.
    This activity constituted one License Operator Requalification inspection sample and one
    Control Room Observation inspection sample.
b.  Findings
    No findings were identified.
1R12 Maintenance Effectiveness
.1  Routine
a.  Inspection Scope
    The inspectors reviewed three specific structures, systems and components (SSC)
    within the scope of the Maintenance Rule (MR) (10 CFR 50.65) with regard to some or
    all of the following attributes, as applicable: (1) Appropriate work practices; (2)
    Identifying and addressing common cause failures; (3) Scoping in accordance with 10
    CFR 50.65(b) of the MR; (4) Characterizing reliability issues for performance monitoring;
    (5) Tracking unavailability for performance monitoring; (6) Balancing reliability and
    unavailability; (7) Trending key parameters for condition monitoring; (8) System
    classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); (9)
    Appropriateness of performance criteria in accordance with 10 CFR 50.65(a)(2); and
    (10) Appropriateness and adequacy of 10 CFR 50.65 (a)(1) goals, monitoring and
    corrective actions (i.e., Ten Point Plan). The inspectors also compared the licensees
    performance against site procedure NPG-SPP-3.4, Maintenance Rule Performance
    Indicator Monitoring, Trending and Reporting; Technical Instruction 0-TI-346,
    Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; and NPG-
    SPP-03.1, Corrective Action Program. The inspectors also reviewed, as applicable,
    work orders, surveillance records, PERs, system health reports, engineering
    evaluations, and MR expert panel minutes; and attended MR expert panel meetings to
    verify that regulatory and procedural requirements were met. This activity constituted
    three Maintenance Effectiveness inspection samples.
                                                                                        Enclosure


====b. Findings====
                                          12
No findings were identified.
    *  FIN work process during U3R15 refueling outage, various Work Orders (WOs)
    *  Unit 1, 2 and 3 Intermediate Range Monitors - System 092
    *  Unit Common Residual Heat Removal Service Water (RHRSW) Pump Room
        Watertight Door Functional Failures
b. Findings
    No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation
.1  Risk Assessment and Management of Risk
a.  Inspection Scope
    For planned online work and/or emergent work that affected the combinations of risk
    significant systems listed below, the inspectors examined five on-line maintenance risk
    assessments, and actions taken to plan and/or control work activities to effectively
    manage and minimize risk. The inspectors verified that risk assessments and applicable
    risk management actions (RMAs) were conducted as required by 10 CFR 50.65(a)(4),
    applicable plant procedures, and BFN Equipment to Plant Risk Matrix. Furthermore, as
    applicable, the inspectors verified the actual in-plant configurations to ensure accuracy
    of the licensees risk assessments and adequacy of RMA implementation. This activity
    constituted five Maintenance Risk Assessment inspection samples.
    *  Planned refueling outage work on both loops of Unit 3 RHR, 3B Fuel Pool Cooling
        pump, Unit 3 500KV off-site power, 3C EDG, 1A Condenser Circulating Water Pump,
        1A Control Bay chiller and AHU, B Fire Pump, RCW Booster Pumps 2A and 3A, C3
        EECW Pump, and C RHRSW Common Header
    *  Emergent work on D Emergency Diesel Generator (EDG) for troubleshooting and
        corrective maintenance, Unit 2 C Residual Heat Removal (RHR) Heat Exchanger
        OOS for piping leak repair, Intake Pumping Station Vent Fan A and B work, and
        Common Switchyard Centered LOOP High Risk due to Unit 3 Transformer activities.
    *  Planned work and yellow risk on Unit 3, Div. I and Div. II RHR, CS Div II, 3C and 3D
        EDG, 3B Fuel Pool Cooling (FPC) Pump, 3C and 3D 4kV Shutdown Boards and
        Standby Gas Treatment (SBGT) Train C
    *  Planned Unit 3 refueling outage yellow risk associated with Div. I RHRand CS OOS.
        Unit 1/2 risk associated with RHR Heat Exchanger 2C and RHRSW Pump A3 OOS
        and, Common Switchyard Centered LOOP High Risk due to Unit 3 Transformer
        activities.
    *  Planned Unit 2 risk with High Pressure Coolant Injection pump and D EDG OOS
                                                                                      Enclosure


===.2 Readiness for Seasonal Extreme Weather Conditions===
                                            13
b.   Findings
      No findings were identified.
1R15 Operability Evaluations
a.  Inspection Scope
      The inspectors reviewed the six operability/functional evaluations listed below to verify
      technical adequacy and ensure that the licensee had adequately assessed TS
      operability. The inspectors also reviewed applicable sections of the UFSAR to verify that
      the system or component remained available to perform its intended function. In
      addition, where appropriate, the inspectors reviewed licensee procedure NEDP-22,
      Functional Evaluations, to ensure that the licensees evaluation met procedure
      requirements. Furthermore, where applicable, inspectors examined the implementation
      of compensatory measures to verify that they achieved the intended purpose and that
      the measures were adequately controlled. The inspectors also reviewed PERs on a
      daily basis to verify that the licensee was identifying and correcting any deficiencies
      associated with operability evaluations. This activity constituted six Operability
      Evaluation inspection samples.
      *    RHRSW Rooms Appendix R Fire Barrier Impacted by Tarpaulin (PER 492957)
      *    Emergency Equipment Cooling Water (EECW) check valve not fully closed (PER
          520497)
      *    RHRSW Pump Room Watertight Door BFN-0-DOOR-260-C-RHRSW Degraded
          (PER 469640)
      *    Past Operability for C3 Emergency Equipment Cooling Water (EECW) Pump
          Foundation Hole Flood Protection Cover Inadequate Installation (PER 532050)
      *    Units 1,2 and 3 EECW yard drain basins partially blocked, (PER 569282)
      *    Unit 1 HPCI Turbine Stop Valve, 1-FCV-073-0018, Failed to Trip (PER 539040)
b.  Findings
      Two findings were identified. One finding is documented as a licensee identified violation
      in Section 4OA7.
  1) Introduction: The NRC identified a Green non-cited violation (NCV) of Technical
      Specification 5.4.1.a for the licensees failure to maintain an Emergency Equipment
      Cooling Water (EECW) pump flood barrier in accordance with written procedures which
      resulted in the inoperability of two other safety related pumps.
      Description:
      The safety related Residual Heat Removal Service Water (RHRSW) pumps are housed
      in the A, B, C, and D rooms of the intake pumping station. UFSAR Section 12.2.7.1.1
      states, in part, that each room is designed to protect the RHRSW pumps from water and
      wave forces resulting from a probable maximum flood (PMF) scenario. During
                                                                                        Enclosure


====a. Inspection Scope====
                                      14
Prior to and during the onset of hot weather conditions, the inspectors reviewed the licensee's implementation of 0-GOI-200-3, Hot Weather Operations. The inspectors also reviewed the Hot Weather Discrepancy Log; and discussed implementation of       0-GOI-200-3 with responsible Operations personnel and management. Furthermore, the inspectors conducted walkdowns of potentially affected risk significant equipment systems located in the Unit 1 and 2 Diesel Generator Building, and the Unit 3 Diesel Generator Building. The inspectors also performed a walkdown of the Standby Gas Treatment (SBGT) Building. This activity constituted one Readiness for Seasonal Extreme Weather sample.
maintenance activities, the licensee maintained the design flood protection configuration
through implementation of properly written work instructions.
The C3 Emergency Equipment Cooling Water (EECW) pump is located in the C
RHRSW pump room with two similarly designed C1 and C2 RHRSW pumps. On March
26, 2012, the licensee had removed C3 pump from service for maintenance. The C3
pump and motor had been disassembled and the pump column removed from the intake
sump pit through the pump base plate and foundation leaving an approximate 22 inch
diameter hole. The hole was protected against flooding by a temporary 1/4 inch thick
aluminum cover plate, over a rubber gasket and secured with 8 foundation bolts. The
flood cover was prescribed by work order 112744581 and implemented by maintenance
procedures MCI-0-023-PMP002, Maintenance of EECW and RHRSW Pumps, and MCI-
0-023-PMP003, Emergency Equipment Cooling Water and Residual Heat Removal
Service Water Pump Removal and Installation.
On April 2, 2012, maintenance personnel removed the flood protection cover to facilitate
an inspection. Personnel re-installed the cover with only two bolts and nuts run down to
approximately one inch from being fully secured. On April 5, 2012, inspectors identified
and informed the licensee of the inadequate flood protection barrier. The licensee
immediately re-installed the flood protection cover in accordance with maintenance
procedures. As an added corrective action, the licensee permanently stenciled the
aluminum plate with the required procedure for installation. The licensee determined
that the workers had re-installed the flood protection cover following the inspection
assuming that it was only for foreign material exclusion. The licensee also determined
that the foreman did not direct an adequate pre-job brief and assumed the workers knew
of the procedural flood requirements. Furthermore, the licensee evaluated the
inadequate flood barrier for past operability and concluded that the C RHRSW pump
room would have flooded in the event of a PMF and that the other two RHRSW pumps
in the room, C1 and C2, would be made nonfunctional. The licensee credited the slow
progression of a PMF flood rise (four days and eight hours) to allow time to adequately
install the flood protection cover, and therefore, prevent the loss of the RHRSW pumps.
These actions were contained in licensee abnormal operating instruction 0-AOI-100-3,
Flood Above Elevation 558.
Analysis: The licensees failure to maintain an Emergency Equipment Cooling Water
(EECW) pump flood barrier in accordance with written procedures was a performance
deficiency. The finding was more than minor because it was associated with the
Mitigating Systems cornerstone attribute of Protection Against External Events, and
adversely affected the cornerstone objective to ensure the availability, reliability, and
capability of RHRSW pumps to perform their intended safety function during a design
basis flooding event. Specifically, the improper re-installation of an external flood
protection cover resulted in the inoperability of two RHRSW pumps. The significance of
this finding was evaluated in accordance with the IMC 0609 Attachment 4, Phase 1-
Initial Screening and Characterization of Findings, which required a Phase 3 analysis
because the finding involved the degradation of equipment designed to mitigate a
flooding event and was risk significant due to external initiating event core damage
sequences. A Phase 3 SDP analysis was performed by the regional Senior Reactor
Analyst using a modified NRC plant model. The model had been modified to calculate
                                                                                    Enclosure


====b. Findings====
                                          15
No findings were identified.
    the impact on the plant from external flooding due to the failure of the RHRSW flood
{{a|1R04}}
    doors. The plant model was solved for a loss of condenser heat sink, with the initiating
==1R04 Equipment Alignment==
    event frequency set to 5E-3 as a conservative estimate for the external flood. Also
    assumed was the unavailability of the power conversion system, since the circ water
    pumps, and their power supplies would be flooded. Condensate was assumed lost
    when the turbine building floods. RHRSW pumps and EECW pumps in the flooded
    RHRSW room were failed by model changes for different flood door failure basic events.
    This analysis failed only the C room door, which duplicated the impact of an unsecured
    flood barrier. For the 4 day exposure time, the result was several orders of magnitude
    below the CDF or LERF threshold for a finding of significance. The finding is Green
    because of the short exposure time, and the low likelihood of the flood.
    The cause of this finding was directly related to the cross cutting aspect of Supervisory
    Oversight in the Work Practices component of the Human Performance area, because of
    supervisions assumption that workers knew to restore the flood protection cover to meet
    procedural requirements without a formal pre-job brief [H.4(c)].
    Enforcement: TS 5.4.1.a. required that written procedures recommended in RG 1.33,
    Revision 2, Appendix A, shall be established, implemented, and maintained. Item 9.a of
    RG 1.33, Appendix A, stated, in part, that maintenance affecting the performance of
    safety-related equipment be properly performed in accordance with written procedures
    or documented instructions appropriate to the circumstances. Contrary to the above,
    between April 2, and April 5, 2012, the licensee failed to properly perform maintenance
    procedures MCI-0-023-PMP002 and MCI-0-023-PMP003, Section 5.0.K. Specifically,
    the licensee failed to maintain a flood barrier during maintenance on C3 EECW Pump
    which resulted in the inoperability of C1 and C2 RHRSW Pumps. Because this finding is
    of very low safety significance (Green) and because it was entered into the licensees
    corrective action program as PER 532050, this violation is being treated as a non-cited
    violation consistent with the NRC Enforcement Policy. This violation was applicable to
    U1, U2 and U3 and is identified as NCV 05000259, 260, 296/2012003-01, Failure to
    Maintain Flood Barrier Results in Inoperable Safety Related Pumps.
1R18 Plant Modifications
a.  Inspection Scope
    The inspectors reviewed the two modifications listed below to verify regulatory
    requirements were met, along with procedures, as applicable, such as NPG-SPP-9.3,
    Plant Modifications and Engineering Change Control; NPG-SPP-9.5, Temporary
    Alterations; and NPG-SPP-6.9.3, Post-Modification Testing. The inspectors also
    reviewed the associated 10 CFR 50.59 screenings and evaluations and compared each
    against the UFSAR and TS to verify that the modifications did not affect operability or
    availability of the affected systems. Furthermore, the inspectors walked down each
    modification to ensure that it was installed in accordance with the modification
    documents and reviewed post-installation and removal testing to verify that the actual
    impact on permanent systems was adequately verified by the tests. This activity
    constituted two Plant Modification inspection samples.
                                                                                      Enclosure


===.1 Partial Walkdown===
                                          16
    *  Temporary Alteration Control Form (TACF) 1-12-001-073, Removed Thermal
        Insulation Attached to BFN-1-FCV-073-0016, HPCI Steam Supply Valve
    *  Design Change Notice (DCN) 70549, Unit 3 Reactor Water Level Flood-Up
        Transmitter and Indication Loop Replacement
b.  Findings
    No findings were identified.
1R19 Post Maintenance Testing
a.  Inspection Scope
    The inspectors witnessed and reviewed the six post-maintenance tests (PMT) listed
    below to verify that procedures and test activities confirmed SSC operability and
    functional capability following the described maintenance. The inspectors reviewed the
    licensees completed test procedures to ensure any of the SSC safety function(s) that
    may have been affected were adequately tested, that the acceptance criteria were
    consistent with information in the applicable licensing basis and/or design basis
    documents, and that the procedure had been properly reviewed and approved. The
    inspectors also reviewed the test data, to verify that test results adequately
    demonstrated restoration of the affected safety function(s). The inspectors verified that
    PMT activities were conducted in accordance with applicable WO instructions, or
    licensee procedural requirements. Furthermore, the inspectors verified that problems
    associated with PMTs were identified and entered into the CAP. This activity constituted
    six Post Maintenance Test inspection samples.
    *  Unit 3: Reactor Vessel Head Tensioning and subsequent Pressure Test per MSI-0-
        001-VSL001, Reactor Vessel Head Disassembly and Reassembly; 3-SI-3.3.1.A,
        ASME Section XI System Leakage Test of the Reactor Pressure Vessel and
        Associated Piping; 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring;
        and 3-SR-3.4.9.1(2), Reactor Vessel Shell Temperature and Reactor Coolant
        Pressure Monitoring During In-Service Hydrostatic or Leak Testing
    *  Unit 1/2 Common: PMT for Replacement of Common D EDG Woodward Governor
        Speed Stop Micro Switches, OI-82, Standby Diesel Generator System and WO
        113480917
    *  Unit 1: PMT for Repair of HPCI Stop Valve, WO 113426235
    *  Unit 3: PMT for 3C EDG Generator Replacement per 3-SR-3.8.1.7(3C), Diesel
        Generator 3C 24-hour Run WO 112472092
    *  Unit 3: PMT for the 3-FCV-074-0048, RHR Shutdown Cooling Valve wedge
        replacement performed under WO 111044044
    *  Unit 3: PMT for the B outboard MSIV (3-FCV-001-0027) valve repack performed
        under WO 113394369
b.  Findings
    No findings were identified.
                                                                                      Enclosure


====a. Inspection Scope====
                                          17
The inspectors conducted three partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems, listed below, while the other train or subsystem was inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify that critical components were properly aligned and to identify any discrepancies which could affect operability of the redundant train or backup system. This activity constituted three Equipment Alignment inspection samples.
1R20 Refueling and Other Outage Activities
* Unit 1&2 'A' Emergency Diesel Generator
.1  Unit 3 Scheduled Refueling Outage (U3R15)
* Unit 3 Residual Heat Removal System - Division II
a. Inspection Scope
* Unit 1 Reactor Core Isolation Cooling (RCIC) System
    During April 7 to May 26, 2012, the inspectors examined critical outage activities to verify
    that they were conducted in accordance with technical specifications, applicable
    procedures, and the licensees outage risk assessment and management plans through
    the end of the reporting period. Some of the more significant inspection activities
    conducted by the inspectors were as follows:
    Outage Risk Assessment
    Prior to the Unit 3 scheduled 30 day U3C15 refueling outage that began on April 7, the
    inspectors attended outage risk assessment team meetings and reviewed the Outage
    Risk Assessment Report to verify that the licensee had appropriately considered risk,
    industry experience, and previous site-specific problems in developing and implementing
    an outage plan that assured defense-in-depth of safety functions were maintained. The
    inspectors also reviewed the daily U3C15 Refueling Outage Reports, including the
    Outage Risk Assessment Management (ORAM) Safety Function Status, and regularly
    attended the twice a day outage status meetings. These reviews were compared to the
    requirements in licensee procedure NPG-SPP-07.2, Outage Management, and technical
    specifications. These reviews were also done to verify that for identified high risk
    significant conditions, due to equipment availability and/or system configurations,
    contingency measures were identified and incorporated into the overall outage and
    contingency response plan. Furthermore, the inspectors frequently discussed risk
    conditions and designated protected equipment with Operations and outage
    management personnel to assess licensee awareness of actual risk conditions and
    mitigation strategies.
    Shutdown and Cooldown Process
    The inspectors witnessed the shutdown and cooldown of Unit 3 in accordance with
    licensee procedures OPDP-1, Conduct of Operations; 3-GOI-100-12A, Unit Shutdown
    from Power Operations to Cold Shutdown and Reduction in Power During Power
    Operations; and 3-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring.
    Decay Heat Removal
    The inspectors reviewed licensee procedures 3-OI-74, Residual Heat Removal System
    (RHR); 3-OI-78, Fuel Pool Cooling and Cleanup System; and Abnormal Operating
    Instruction 0-AOI-72-1, Alternate Decay Heat Removal System Failures; and conducted
    a main control room panel and in-plant walkdowns of system and components to verify
    correct system alignment. During planned evolutions that resulted in an increased
    outage risk condition of Yellow for shutdown cooling, inspectors verified that the plant
    conditions and systems identified in the risk mitigation strategy were available. In
    addition, the inspectors reviewed controls implemented to ensure that outage work was
                                                                                      Enclosure


====b. Findings====
                                        18
No findings were identified.
not impacting the ability of operators to operate spent fuel pool cooling, RHR shutdown
{{a|1R05}}
cooling, and/or Alternate Decay Heat Removal (ADHR) system. Furthermore, the
==1R05 Fire Protection==
inspectors conducted several walkdowns of the ADHR system during operation with the
fuel pool gates removed.
Critical Outage Activities
The inspectors examined outage activities to verify that they were conducted in
accordance with technical specifications, licensee procedures, and the licensees outage
risk control plan. Some of the more significant inspection activities accomplished by the
inspectors were as follows:
*  Walked down selected safety-related equipment clearance orders (i.e., tag orders)
*  Verified Reactor Coolant System (RCS) inventory controls, especially during
    evolutions involving operations with the potential to drain the reactor vessel
    (OPDRV)
*  Verified electrical systems availability and alignment
*  Monitored important control room plant parameters (e.g., RCS pressure, level, flow,
    and temperature) and technical specifications compliance during the various
    shutdown modes of operation, and mode transitions
*  Evaluated implementation of reactivity controls
*  Reviewed control of containment penetrations and overall integrity
*  Examined foreign material exclusion controls particularly in proximity to and around
    the reactor cavity, equipment pit, and spent fuel pool
*  Routine tours of the control room, reactor building including areas normally
    inaccessible during power operations, refueling floor, torus and drywell.
Reactor Vessel Disassembly and Refueling Activities
The inspectors witnessed selected activities associated with reactor vessel disassembly,
and reactor cavity flood-up and drain down in accordance with 3-GOI-100-3A, Refueling
Operations (Reactor Vessel Disassembly and Floodup). Also, on numerous occasions,
the inspectors witnessed fuel handling operations during the two Unit 3 reactor core fuel
shuffles performed in accordance with technical specifications and applicable operating
procedures. Inspectors also observed control rod unlatching and relatching for control
rod drive mechanism change-outs. In addition, the inspectors verified specific fuel
movements as delineated by the Fuel Assembly Transfer Sheets (FATF). Furthermore,
the inspectors also witnessed and performed a 100 percent core verification examination
of the video verification of the final completed reactor core.
Drywell Closeout
On May 17, 2012, the inspectors reviewed the licensees conduct of 3-GOI-200-2,
Section 5.3 Drywell Closeout, and performed an independent detailed closeout
inspection of the Unit 3 drywell.
                                                                                  Enclosure


===.1 Fire Protection Tours===
                                        19
  Torus Closeout
  On May 12, 2012, the inspectors reviewed the licensees conduct of procedure 3-GOI-
  200-2, Section 5.4 Torus Closeout, and performed an independent detailed closeout
  inspection of the Unit 3 torus (suppression pool and chamber). In addition inspectors
  reviewed the Foreign Material Exclusion (FME) log for any discrepancies.
  Restart Activities
  The inspectors specifically conducted the following:
  *  Witnessed Unit 2 reactor pressure vessel head tensioning in accordance with MSI-0-
      001-VSL001, Reactor Vessel Disassembly and Reassembly
  *  Witnessed heatup and pressurization of Unit 3 reactor pressure vessel in accordance
      with 3-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor pressure
      Vessel and Associated Piping, and reviewed reactor coolant heatup/pressurization
      data per 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, and 3-SR-
      3.4.9.1(2), Reactor Vessel Shell Temperature & Reactor Coolant Pressure
      Monitoring During In-Service Leak Testing
  *  Reviewed Reactor Coolant Heatup/Pressurization to Rated Temperature and
      Pressure per 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring
  *  Reviewed and verified completion of selected items of 0-TI-270, Refueling Test
      Program, Attachment 2, Startup Review Checklist
  *  Reviewed 2-SR-3.6.1.1.1(OPT-A) Primary Containment Total Leak Rate - Option A,
      Revision 11
  *  Witnessed Unit 3 approach to criticality and power ascension per 3-GOI-100-1A, Unit
      Startup, 3-SR-3.3.1.1.5, SRM and IRM Overlap Verification, and 3-GOI-100-12,
      Power Maneuvering
  Corrective Action Program
  The inspectors reviewed PERs generated during refueling outage U3C15 and
  periodically attended Corrective Action Review Board (CARB) and PER Screening
  Committee (PSC) meetings to verify that initiation thresholds, priorities, mode holds,
  operability concerns and significance levels were adequately addressed. Resolution and
  implementation of corrective actions of several PERs were also reviewed for
  completeness. This constitutes one Refueling Outage activity inspection sample.
b. Findings
  No findings were identified.
                                                                                    Enclosure


====a. Inspection Scope====
                                            20
The inspectors reviewed licensee procedures, Nuclear Power Group Standard Programs and Processes NPG-SPP-18.4.7, Control of Transient Combustibles, and NPG-SPP-18.4.6, Control of Fire Protection Impairments, and conducted a walkdown of the four fire areas (FA) and fire zones (FZ) listed below. Selected FAs/FZs were examined in order to verify licensee control of transient combustibles and ignition sources; the material condition of fire protection equipment and fire barriers; and operational lineup and operational condition of fire protection features or measures. Furthermore, the inspectors reviewed applicable portions of the Fire Protection Report, Volumes 1 and 2, including the applicable Fire Hazards Analysis, and Pre-Fire Plan drawings, to verify that the necessary firefighting equipment, such as fire extinguishers, hose stations, ladders, and communications equipment, was in place. This activity constituted four Fire Protection inspection samples.
1R22 Surveillance Testing
* Unit 2 Reactor Building Elevations 519, 541, and 565 west of column line R11 (FZ 2-1)
a.   Inspection Scope
* Unit 3 Reactor Building, EL 593' and residual heat removal (RHR) heat exchanger rooms, EL 565', and 593' near column R15-S and R21-S (FZ 3-3)
      The inspectors witnessed portions of, and/or reviewed completed test data for the
* Unit 1, Control Building, EL 593' (FA 16)
      following seven surveillance tests of risk-significant and/or safety-related systems to
* Unit 1,2, and 3 Turbine Building Deluge Sprinkler Control Stations Affecting Control Bay (FA 25)
      verify that the tests met technical specification surveillance requirements, UFSAR
      commitments, and in-service testing and licensee procedure requirements. The
      inspectors review confirmed whether the testing effectively demonstrated that the SSCs
      were operationally capable of performing their intended safety functions and fulfilled the
      intent of the associated surveillance requirement. This activity constituted seven
      Surveillance Testing inspection samples: one inservice test, three routine, two
      containment isolation valve and one reactor coolant system leak detection test. .
      In-Service Tests:
      *   2-SI-4.4.A.1, Standby Liquid Control Pump Functional Test
      Routine Surveillance Tests:
      *    3-SR-3.8.1.9(3D OL), Diesel Generator 3D Emergency Load Acceptance Test with
          Unit 3 Operating
      *   3-SR-3.5.1.8, HPCI Main and Booster Pump Set Developed Head and Flow Rate
          Test at 150 psig Reactor Pressure, Rev. 13 performed on May 16, 2012
      *    3-SI-4.7.A.2.g-3/74g, Unit 3 Primary Containment Local Leak Rate Test (LLRT) RHR
          Shutdown Cooling Suction: Penetration X-12
      Containment Isolation Valve Tests:
      * 3-SR-3.6.1.3.10(B), Primary Containment Local Leak Rate Test (LLRT) Main Steam
          Line B: Penetration X-7B
      * 3-SI-4.7.A.2.a-f, Primary Containment Integrated Leak Rate test (CILRT), Rev. 10
      Reactor Coolant System Leak Detection Tests:
      *   2-SI-4.2.E-1(B), Drywell Equipment Drain Sump Flow Integrator Calibration
  b. Findings
      No findings were identified.
                                                                                        Enclosure


====b. Findings====
                                          21
No findings were identified.
    Cornerstone: Emergency Preparedness
{{a|1R07}}
1EP2 Alert and Notification System Evaluation
==1R07 Heat Sink Performance==
a. Inspection Scope
 
    The inspectors evaluated the adequacy of the licensees methods for testing the alert
===.1 Annual Review===
    and notification system in accordance with NRC Inspection Procedure 71114,
 
    Attachment 02, Alert and Notification System (ANS) Evaluation. The applicable planning
====a. Inspection Scope====
    standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section
The inspectors examined activities associated with Unit 3 RHR Heat Exchangers. The inspectors also reviewed design basis documents, calculations, test procedures, maintenance procedures and preventive maintenance procedures and results to evaluate the licensee's program for maintaining heat sinks in accordance with the licensing basis. Specifically inspectors reviewed modifications performed on the Unit 3 RHR Heat Exchanger Flanges. Inspectors reviewed available performance testing documentation of the 3A and 3C RHR Heat Exchangers.
    IV.D requirements were used as reference criteria. The criteria contained in NUREG-
 
    0654, Criteria for Preparation and Evaluation of Radiological Emergency Response
In addition, the inspectors reviewed the licensee's implementation of the GL 89-13 program. Inspectors reviewed associated PERs and corrective actions to verify that the licensee was identifying issues and correcting them. The inspectors performed walkdowns of key components of the Unit 3 RHR system to verify material conditions were acceptable and physical arrangement matched procedures and drawings. This activity constituted one Annual Heat Sink sample.
    Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, were also
 
    used as a reference.
====b. Findings====
    The inspectors reviewed various documents which are listed in the Attachment. This
No findings were identified.
    inspection activity satisfied one inspection sample for the alert and notification system on
{{a|1R08}}
    a biennial basis.
==1R08 Inservice Inspection (ISI) Activities (71111.08G, Unit 3)==
b. Findings
 
    No findings were identified.
====a. Inspection Scope====
1EP3 Emergency Preparedness Organization Staffing and Augmentation System
Non-Destructive Examination (NDE) Activities and Welding Activities:  From April 16 to April 20, 2012, the inspectors conducted an on-site review of the implementation of the licensee's Inservice Inspection (ISI) Program for monitoring degradation of the reactor coolant system, emergency feedwater systems, risk-significant piping and components, and containment systems in Unit 3. The inspector's activities included a review of non-destructive examinations (NDEs) to evaluate compliance with the applicable edition of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (BPVC), Section XI (Code of record:  2001 Edition with 2003 Addenda), and to verify that indications and defects (if present) were appropriately evaluated and dispositioned in accordance with the requirements of the ASME Code, Section XI, acceptance standards. The inspectors directly observed the following NDE mandated by the ASME Code to evaluate compliance with the ASME Code Section XI and Section V requirements and, if any indications and defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement.
a. Inspection Scope
* UT Exam of Weld DRHR-03-03, 3-FCV-74-53, Low Pressure Coolant Injection (LPCI) Loop I Inlet
    The inspectors reviewed the licensees Emergency Response Organization (ERO)
* UT Exam of Weld DSRHR-03-04, 3-HCV-74-55, 24 in. inlet for Recirculation Loop B  The inspectors reviewed records of the following NDEs mandated by the ASME Code Section XI to evaluate compliance with the ASME Code Section XI and Section V requirements and, if any indications and defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement.
    augmentation staffing requirements and process for notifying the ERO to ensure the
* VT Exam of RPV-WASH-3-50, Reactor Pressure Vessel Stud Washer
    readiness of key staff for responding to an event and timely facility activation. The
* UT Exam of weld DRHR-03-12, 3-FCV-74-67, LPCI Loop II Inlet
    qualification records of key position ERO personnel were reviewed to ensure all ERO
* EVT of BFN-3-RPV-068-RA048 Standpipe in Unit 3 Steam Separator
    qualifications were current. A sample of problems identified from augmentation drills or
* EVT of BFN-3-RPV-068-RA050 U3 Feedwater Sparger End Brackets  The inspectors reviewed associated documents for the welding activities referenced below in order to evaluate compliance with procedures and the ASME Code. The inspectors reviewed the work order, repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports.
    system tests performed since the last inspection was reviewed to assess the
* Work Order 04-719493-003, 3-FCV-073-016 HPCI Turbine Steam Supply Valve
    effectiveness of corrective actions.
* Work Order 08-718716-004, Replace Strain Gauges on MS Lines  During non-destructive surface and volumetric examinations performed since the previous refuelling outage, the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service. Therefore, no NRC review was completed for this inspection procedure attribute. Identification and Resolution of Problems:  The inspectors performed a review of a sample of ISI-related problems which were identified by the licensee and entered into the corrective action program as Problem Evaluation Reports (PERs). The inspectors reviewed the PERs to confirm the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the licensee's consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements. The corrective action documents reviewed by the inspectors are listed in the report attachment.
    The inspection was conducted in accordance with NRC Inspection Procedure 71114,
 
    Attachment 03, Emergency Preparedness Organization Staffing and Augmentation
====b. Findings====
    System. The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR
No findings were identified.
    50, Appendix E requirements were used as reference criteria.
{{a|1R11}}
    The inspectors reviewed various documents which are listed in the Attachment. This
==1R11 Licensed Operator Requalification==
    inspection activity satisfied one inspection sample for the ERO staffing and
 
    augmentation system on a biennial basis.
===.1 Resident Inspector Quarterly Review===
b. Findings
 
    No findings were identified.
====a. Inspection Scope====
                                                                                        Enclosure
On June 11, 2012, the inspectors observed an as-found licensed operator requalification simulator examination according to Unit 2 Simulator Exercise Guide OPL173.S039. The scenario involved Partial Loss of Reactor Building Closed Cooling Water, Loss of I & C Bus B, Anticipated Transient without Scram (ATWS), Lower Water Level (C-5) for Power Control with Bypass Valves.
 
The inspectors specifically evaluated the following attributes related to the operating crew's performance:
* Clarity and formality of communication
* Ability to take timely action to safely control the unit
* Prioritization, interpretation, and verification of alarms
* Correct use and implementation of Abnormal Operating Instructions (AOIs), and Emergency Operating Instructions (EOIs)
* Timely and appropriate Emergency Action Level declarations per Emergency Plan Implementing Procedures (EPIP)
* Control board operation and manipulation, including high-risk operator actions
* Command and Control provided by the Unit Supervisor and Shift Manager  The inspectors attended the post-examination critique to assess the effectiveness of the licensee evaluators and to verify that licensee-identified issues were comparable to issues identified by the inspector. The inspectors reviewed simulator physical fidelity (i.e., the degree of similarity between the simulator and the reference plant control room, such as physical location of panels, equipment, instruments, controls, labels, and related form and function). This activity counts for one Observation of Requalification Activity inspection sample.
 
====b. Findings====
No findings were identified.
 
===.2 Control Room Observations===
 
====a. Inspection Scope====
Inspectors observed and assessed licensed operator performance in the plant and main control room, particularly during periods of heightened activity or risk and where the activities could affect plant safety. Inspectors reviewed various licensee policies and procedures such as OPDP-1, Conduct of Operations, NPG-SPP-10.0, Plant Operations and GOI-100-12, Power Maneuvering.
 
Inspectors utilized activities such as post maintenance testing, surveillance testing and refueling and other outage activities to focus on the following conduct of operations as appropriate;
* Operator compliance and use of procedures.
* Control board manipulations.
* Communication between crew members.
* Use and interpretation of plant instruments, indications and alarms.
* Use of human error prevention techniques.
* Documentation of activities, including initials and sign-offs in procedures.
* Supervision of activities, including risk and reactivity management.
* Pre-job briefs.
 
This activity constituted one License Operator Requalification inspection sample and one Control Room Observation inspection sample.
 
====b. Findings====
No findings were identified.
{{a|1R12}}
==1R12 Maintenance Effectiveness==
 
===.1 Routine===
 
====a. Inspection Scope====
The inspectors reviewed three specific structures, systems and components (SSC) within the scope of the Maintenance Rule (MR) (10 CFR 50.65) with regard to some or all of the following attributes, as applicable:  (1) Appropriate work practices; (2) Identifying and addressing common cause failures; (3) Scoping in accordance with 10 CFR 50.65(b) of the MR; (4) Characterizing reliability issues for performance monitoring; (5) Tracking unavailability for performance monitoring; (6) Balancing reliability and unavailability; (7) Trending key parameters for condition monitoring; (8) System classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); (9) Appropriateness of performance criteria in accordance with 10 CFR 50.65(a)(2); and (10) Appropriateness and adequacy of 10 CFR 50.65 (a)(1) goals, monitoring and corrective actions (i.e., Ten Point Plan). The inspectors also compared the licensee's performance against site procedure NPG-SPP-3.4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; Technical Instruction 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; and NPG-SPP-03.1, Corrective Action Program. The inspectors also reviewed, as applicable, work orders, surveillance records, PERs, system health reports, engineering evaluations, and MR expert panel minutes; and attended MR expert panel meetings to verify that regulatory and procedural requirements were met. This activity constituted three Maintenance Effectiveness inspection samples.
* FIN work process during U3R15 refueling outage, various Work Orders (WO's)
* Unit 1, 2 and 3 Intermediate Range Monitors - System 092
* Unit Common Residual Heat Removal Service Water (RHRSW) Pump Room Watertight Door Functional Failures
 
====b. Findings====
No findings were identified.
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Evaluation==
 
===.1 Risk Assessment and Management of Risk===
 
====a. Inspection Scope====
For planned online work and/or emergent work that affected the combinations of risk significant systems listed below, the inspectors examined five on-line maintenance risk assessments, and actions taken to plan and/or control work activities to effectively manage and minimize risk. The inspectors verified that risk assessments and applicable risk management actions (RMAs) were conducted as required by 10 CFR 50.65(a)(4), applicable plant procedures, and BFN Equipment to Plant Risk Matrix. Furthermore, as applicable, the inspectors verified the actual in-plant configurations to ensure accuracy of the licensee's risk assessments and adequacy of RMA implementation. This activity constituted five Maintenance Risk Assessment inspection samples.
* Planned refueling outage work on both loops of Unit 3 RHR, 3B Fuel Pool Cooling pump, Unit 3 500KV off-site power, 3C EDG, 1A Condenser Circulating Water Pump,  1A Control Bay chiller and AHU, B Fire Pump, RCW Booster Pumps 2A and 3A, C3 EECW Pump, and C RHRSW Common Header
* Emergent work on 'D' Emergency Diesel Generator (EDG) for troubleshooting and corrective maintenance, Unit 2 'C' Residual Heat Removal (RHR) Heat Exchanger OOS for piping leak repair, Intake Pumping Station Vent Fan A and B work, and Common Switchyard Centered LOOP High Risk due to Unit 3 Transformer activities.
* Planned work and yellow risk on Unit 3, Div. I and Div. II RHR, CS Div II, 3C and 3D EDG, 3B Fuel Pool Cooling (FPC) Pump, 3C and 3D 4kV Shutdown Boards and Standby Gas Treatment (SBGT) Train C
* Planned Unit 3 refueling outage yellow risk associated with Div. I RHRand CS  OOS. Unit 1/2 risk associated with RHR Heat Exchanger 2C and RHRSW Pump A3 OOS and, Common Switchyard Centered LOOP High Risk due to Unit 3 Transformer activities.
* Planned Unit 2 risk with High Pressure Coolant Injection pump and D EDG OOS
 
====b. Findings====
No findings were identified.
{{a|1R15}}
==1R15 Operability Evaluations==
 
====a. Inspection Scope====
The inspectors reviewed the six operability/functional evaluations listed below to verify technical adequacy and ensure that the licensee had adequately assessed TS operability. The inspectors also reviewed applicable sections of the UFSAR to verify that the system or component remained available to perform its intended function. In addition, where appropriate, the inspectors reviewed licensee procedure NEDP-22, Functional Evaluations, to ensure that the licensee's evaluation met procedure requirements. Furthermore, where applicable, inspectors examined the implementation of compensatory measures to verify that they achieved the intended purpose and that the measures were adequately controlled. The inspectors also reviewed PERs on a daily basis to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. This activity constituted six Operability Evaluation inspection samples.
* RHRSW Rooms Appendix R Fire Barrier Impacted by Tarpaulin (PER 492957)
* Emergency Equipment Cooling Water (EECW) check valve not fully closed (PER 520497)
* RHRSW Pump Room Watertight Door BFN-0-DOOR-260-C-RHRSW Degraded (PER 469640)
* Past Operability for C3 Emergency Equipment Cooling Water (EECW) Pump Foundation Hole Flood Protection Cover Inadequate Installation (PER 532050)
* Units 1,2 and 3 EECW yard drain basins partially blocked, (PER 569282)
* Unit 1 HPCI Turbine Stop Valve, 1-FCV-073-0018, Failed to Trip (PER 539040)
 
====b. Findings====
Two findings were identified. One finding is documented as a licensee identified violation in Section 4OA7.
 
1)
 
=====Introduction:=====
The NRC identified a Green non-cited violation (NCV) of Technical Specification 5.4.1.a for the licensee's failure to maintain an Emergency Equipment Cooling Water (EECW) pump flood barrier in accordance with written procedures which resulted in the inoperability of two other safety related pumps.
 
=====Description:=====
The safety related Residual Heat Removal Service Water (RHRSW) pumps are housed in the A, B, C, and D rooms of the intake pumping station. UFSAR Section 12.2.7.1.1 states, in part, that each room is designed to protect the RHRSW pumps from water and wave forces resulting from a probable maximum flood (PMF) scenario. During maintenance activities, the licensee maintained the design flood protection configuration through implementation of properly written work instructions. The C3 Emergency Equipment Cooling Water (EECW) pump is located in the C RHRSW pump room with two similarly designed C1 and C2 RHRSW pumps. On March 26, 2012, the licensee had removed C3 pump from service for maintenance. The C3 pump and motor had been disassembled and the pump column removed from the intake sump pit through the pump base plate and foundation leaving an approximate 22 inch diameter hole. The hole was protected against flooding by a temporary 1/4 inch thick aluminum cover plate, over a rubber gasket and secured with 8 foundation bolts. The flood cover was prescribed by work order 112744581 and implemented by maintenance procedures MCI-0-023-PMP002, Maintenance of EECW and RHRSW Pumps, and MCI-0-023-PMP003, Emergency Equipment Cooling Water and Residual Heat Removal Service Water Pump Removal and Installation. On April 2, 2012, maintenance personnel removed the flood protection cover to facilitate an inspection. Personnel re-installed the cover with only two bolts and nuts run down to approximately one inch from being fully secured. On April 5, 2012, inspectors identified and informed the licensee of the inadequate flood protection barrier. The licensee immediately re-installed the flood protection cover in accordance with maintenance procedures. As an added corrective action, the licensee permanently stenciled the aluminum plate with the required procedure for installation. The licensee determined that the workers had re-installed the flood protection cover following the inspection assuming that it was only for foreign material exclusion. The licensee also determined that the foreman did not direct an adequate pre-job brief and assumed the workers knew of the procedural flood requirements. Furthermore, the licensee evaluated the inadequate flood barrier for past operability and concluded that the C RHRSW pump room would have flooded in the event of a PMF and that the other two RHRSW pumps in the room, C1 and C2, would be made nonfunctional. The licensee credited the slow progression of a PMF flood rise (four days and eight hours) to allow time to adequately install the flood protection cover, and therefore, prevent the loss of the RHRSW pumps.
 
These actions were contained in licensee abnormal operating instruction 0-AOI-100-3, Flood Above Elevation 558'.
 
=====Analysis:=====
The licensee's failure to maintain an Emergency Equipment Cooling Water (EECW) pump flood barrier in accordance with written procedures was a performance deficiency. The finding was more than minor because it was associated with the Mitigating Systems cornerstone attribute of Protection Against External Events, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of RHRSW pumps to perform their intended safety function during a design basis flooding event. Specifically, the improper re-installation of an external flood protection cover resulted in the inoperability of two RHRSW pumps. The significance of this finding was evaluated in accordance with the IMC 0609 Attachment 4, Phase 1-Initial Screening and Characterization of Findings, which required a Phase 3 analysis because the finding involved the degradation of equipment designed to mitigate a flooding event and was risk significant due to external initiating event core damage sequences. A Phase 3 SDP analysis was performed by the regional Senior Reactor Analyst using a modified NRC plant model. The model had been modified to calculate the impact on the plant from external flooding due to the failure of the RHRSW flood doors. The plant model was solved for a loss of condenser heat sink, with the initiating event frequency set to 5E-3 as a conservative estimate for the external flood. Also assumed was the unavailability of the power conversion system, since the circ water pumps, and their power supplies would be flooded. Condensate was assumed lost when the turbine building floods. RHRSW pumps and EECW pumps in the flooded RHRSW room were failed by model changes for different flood door failure basic events. This analysis failed only the C room door, which duplicated the impact of an unsecured flood barrier. For the 4 day exposure time, the result was several orders of magnitude below the CDF or LERF threshold for a finding of significance. The finding is Green because of the short exposure time, and the low likelihood of the flood.
 
The cause of this finding was directly related to the cross cutting aspect of Supervisory Oversight in the Work Practices component of the Human Performance area, because of supervision's assumption that workers knew to restore the flood protection cover to meet procedural requirements without a formal pre-job brief [H.4(c)].
 
=====Enforcement:=====
TS 5.4.1.a. required that written procedures recommended in RG 1.33, Revision 2, Appendix A, shall be established, implemented, and maintained. Item 9.a of RG 1.33, Appendix A, stated, in part, that maintenance affecting the performance of safety-related equipment be properly performed in accordance with written procedures or documented instructions appropriate to the circumstances. Contrary to the above, between April 2, and April 5, 2012, the licensee failed to properly perform maintenance procedures MCI-0-023-PMP002 and MCI-0-023-PMP003, Section 5.0.K. Specifically, the licensee failed to maintain a flood barrier during maintenance on C3 EECW Pump which resulted in the inoperability of C1 and C2 RHRSW Pumps. Because this finding is of very low safety significance (Green) and because it was entered into the licensee's corrective action program as PER 532050, this violation is being treated as a non-cited violation consistent with the NRC Enforcement Policy. This violation was applicable to U1, U2 and U3 and is identified as NCV 05000259, 260, 296/2012003-01, Failure to Maintain Flood Barrier Results in Inoperable Safety Related Pumps.
{{a|1R18}}
==1R18 Plant Modifications==
 
====a. Inspection Scope====
The inspectors reviewed the two modifications listed below to verify regulatory requirements were met, along with procedures, as applicable, such as NPG-SPP-9.3, Plant Modifications and Engineering Change Control; NPG-SPP-9.5, Temporary Alterations; and NPG-SPP-6.9.3, Post-Modification Testing. The inspectors also reviewed the associated 10 CFR 50.59 screenings and evaluations and compared each against the UFSAR and TS to verify that the modifications did not affect operability or availability of the affected systems. Furthermore, the inspectors walked down each modification to ensure that it was installed in accordance with the modification documents and reviewed post-installation and removal testing to verify that the actual impact on permanent systems was adequately verified by the tests. This activity constituted two Plant Modification inspection samples.
* Temporary Alteration Control Form (TACF) 1-12-001-073, Removed Thermal Insulation Attached to BFN-1-FCV-073-0016, HPCI Steam Supply Valve
* Design Change Notice (DCN) 70549, Unit 3 Reactor Water Level Flood-Up Transmitter and Indication Loop Replacement
 
====b. Findings====
No findings were identified.
{{a|1R19}}
==1R19 Post Maintenance Testing==
 
====a. Inspection Scope====
The inspectors witnessed and reviewed the six post-maintenance tests (PMT) listed below to verify that procedures and test activities confirmed SSC operability and functional capability following the described maintenance. The inspectors reviewed the licensee's completed test procedures to ensure any of the SSC safety function(s) that may have been affected were adequately tested, that the acceptance criteria were consistent with information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also reviewed the test data, to verify that test results adequately demonstrated restoration of the affected safety function(s). The inspectors verified that PMT activities were conducted in accordance with applicable WO instructions, or licensee procedural requirements. Furthermore, the inspectors verified that problems associated with PMTs were identified and entered into the CAP. This activity constituted six Post Maintenance Test inspection samples.
* Unit 3:  Reactor Vessel Head Tensioning and subsequent Pressure Test per MSI-0-001-VSL001, Reactor Vessel Head Disassembly and Reassembly; 3-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor Pressure Vessel and Associated Piping; 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring; and 3-SR-3.4.9.1(2), Reactor Vessel Shell Temperature and Reactor Coolant Pressure Monitoring During In-Service Hydrostatic or Leak Testing
* Unit 1/2 Common:  PMT for Replacement of Common 'D' EDG Woodward Governor Speed Stop Micro Switches, OI-82, Standby Diesel Generator System and WO 113480917
* Unit 1:  PMT for Repair of HPCI Stop Valve, WO 113426235
* Unit 3:  PMT for 3C EDG Generator Replacement per 3-SR-3.8.1.7(3C), Diesel Generator '3C' 24-hour Run WO 112472092
* Unit 3:  PMT for the 3-FCV-074-0048, RHR Shutdown Cooling Valve wedge replacement performed under WO 111044044
* Unit 3:  PMT for the 'B' outboard MSIV (3-FCV-001-0027) valve repack performed under WO 113394369
 
====b. Findings====
No findings were identified.
{{a|1R20}}
==1R20 Refueling and Other Outage Activities==
 
===.1 Unit 3 Scheduled Refueling Outage (U3R15)===
 
====a. Inspection Scope====
During April 7 to May 26, 2012, the inspectors examined critical outage activities to verify that they were conducted in accordance with technical specifications, applicable procedures, and the licensee's outage risk assessment and management plans through the end of the reporting period. Some of the more significant inspection activities conducted by the inspectors were as follows:  Outage Risk Assessment  Prior to the Unit 3 scheduled 30 day U3C15 refueling outage that began on April 7, the inspectors attended outage risk assessment team meetings and reviewed the Outage Risk Assessment Report to verify that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing an outage plan that assured defense-in-depth of safety functions were maintained. The inspectors also reviewed the daily U3C15 Refueling Outage Reports, including the Outage Risk Assessment Management (ORAM) Safety Function Status, and regularly attended the twice a day outage status meetings. These reviews were compared to the requirements in licensee procedure NPG-SPP-07.2, Outage Management, and technical specifications. These reviews were also done to verify that for identified high risk significant conditions, due to equipment availability and/or system configurations, contingency measures were identified and incorporated into the overall outage and contingency response plan. Furthermore, the inspectors frequently discussed risk conditions and designated protected equipment with Operations and outage management personnel to assess licensee awareness of actual risk conditions and mitigation strategies. Shutdown and Cooldown Process  The inspectors witnessed the shutdown and cooldown of Unit 3 in accordance with licensee procedures OPDP-1, Conduct of Operations; 3-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and Reduction in Power During Power Operations; and 3-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring. Decay Heat Removal  The inspectors reviewed licensee procedures 3-OI-74, Residual Heat Removal System (RHR); 3-OI-78, Fuel Pool Cooling and Cleanup System; and Abnormal Operating Instruction 0-AOI-72-1, Alternate Decay Heat Removal System Failures; and conducted a main control room panel and in-plant walkdowns of system and components to verify correct system alignment. During planned evolutions that resulted in an increased outage risk condition of "Yellow" for shutdown cooling, inspectors verified that the plant conditions and systems identified in the risk mitigation strategy were available. In addition, the inspectors reviewed controls implemented to ensure that outage work was not impacting the ability of operators to operate spent fuel pool cooling, RHR shutdown cooling, and/or Alternate Decay Heat Removal (ADHR) system. Furthermore, the inspectors conducted several walkdowns of the ADHR system during operation with the fuel pool gates removed.
 
Critical Outage Activities  The inspectors examined outage activities to verify that they were conducted in accordance with technical specifications, licensee procedures, and the licensee's outage risk control plan. Some of the more significant inspection activities accomplished by the inspectors were as follows:
* Walked down selected safety-related equipment clearance orders (i.e., tag orders)
* Verified Reactor Coolant System (RCS) inventory controls, especially during evolutions involving operations with the potential to drain the reactor vessel (OPDRV)
* Verified electrical systems availability and alignment
* Monitored important control room plant parameters (e.g., RCS pressure, level, flow, and temperature) and technical specifications compliance during the various shutdown modes of operation, and mode transitions
* Evaluated implementation of reactivity controls
* Reviewed control of containment penetrations and overall integrity
* Examined foreign material exclusion controls particularly in proximity to and around the reactor cavity, equipment pit, and spent fuel pool
* Routine tours of the control room, reactor building including areas normally inaccessible during power operations, refueling floor, torus and drywell.
 
Reactor Vessel Disassembly and Refueling Activities  The inspectors witnessed selected activities associated with reactor vessel disassembly, and reactor cavity flood-up and drain down in accordance with 3-GOI-100-3A, Refueling Operations (Reactor Vessel Disassembly and Floodup). Also, on numerous occasions, the inspectors witnessed fuel handling operations during the two Unit 3 reactor core fuel shuffles performed in accordance with technical specifications and applicable operating procedures. Inspectors also observed control rod unlatching and relatching for control rod drive mechanism change-outs. In addition, the inspectors verified specific fuel movements as delineated by the Fuel Assembly Transfer Sheets (FATF). Furthermore, the inspectors also witnessed and performed a 100 percent core verification examination of the video verification of the final completed reactor core. Drywell Closeout  On May 17, 2012, the inspectors reviewed the licensee's conduct of 3-GOI-200-2, Section 5.3 Drywell Closeout, and performed an independent detailed closeout inspection of the Unit 3 drywell.
 
Torus Closeout  On May 12, 2012, the inspectors reviewed the licensee's conduct of procedure 3-GOI-200-2, Section 5.4 Torus Closeout, and performed an independent detailed closeout inspection of the Unit 3 torus (suppression pool and chamber). In addition inspectors reviewed the Foreign Material Exclusion (FME) log for any discrepancies.
 
Restart Activities  The inspectors specifically conducted the following:
* Witnessed Unit 2 reactor pressure vessel head tensioning in accordance with MSI-0-001-VSL001, Reactor Vessel Disassembly and Reassembly
* Witnessed heatup and pressurization of Unit 3 reactor pressure vessel in accordance with 3-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor pressure Vessel and Associated Piping, and reviewed reactor coolant heatup/pressurization data per 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, and 3-SR-3.4.9.1(2), Reactor Vessel Shell Temperature & Reactor Coolant Pressure Monitoring During In-Service Leak Testing
* Reviewed Reactor Coolant Heatup/Pressurization to Rated Temperature and Pressure per 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring
* Reviewed and verified completion of selected items of 0-TI-270, Refueling Test Program, Attachment 2, Startup Review Checklist
* Reviewed 2-SR-3.6.1.1.1(OPT-A) Primary Containment Total Leak Rate - Option A, Revision 11
* Witnessed Unit 3 approach to criticality and power ascension per 3-GOI-100-1A, Unit Startup, 3-SR-3.3.1.1.5, SRM and IRM Overlap Verification, and 3-GOI-100-12, Power Maneuvering  Corrective Action Program  The inspectors reviewed PERs generated during refueling outage U3C15 and periodically attended Corrective Action Review Board (CARB) and PER Screening Committee (PSC) meetings to verify that initiation thresholds, priorities, mode holds, operability concerns and significance levels were adequately addressed. Resolution and implementation of corrective actions of several PERs were also reviewed for completeness. This constitutes one Refueling Outage activity inspection sample.
 
====b. Findings====
No findings were identified.
{{a|1R22}}
==1R22 Surveillance Testing==
 
====a. Inspection Scope====
The inspectors witnessed portions of, and/or reviewed completed test data for the following seven surveillance tests of risk-significant and/or safety-related systems to verify that the tests met technical specification surveillance requirements, UFSAR commitments, and in-service testing and licensee procedure requirements. The inspectors' review confirmed whether the testing effectively demonstrated that the SSCs were operationally capable of performing their intended safety functions and fulfilled the intent of the associated surveillance requirement. This activity constituted seven Surveillance Testing inspection samples:  one inservice test, three routine, two containment isolation valve and one reactor coolant system leak detection test. . In-Service Tests:
* 2-SI-4.4.A.1, Standby Liquid Control Pump Functional Test  Routine Surveillance Tests:
* 3-SR-3.8.1.9(3D OL), Diesel Generator 3D Emergency Load Acceptance Test with Unit 3 Operating
* 3-SR-3.5.1.8, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at 150 psig Reactor Pressure, Rev. 13 performed on May 16, 2012
* 3-SI-4.7.A.2.g-3/74g, Unit 3 Primary Containment Local Leak Rate Test (LLRT) RHR Shutdown Cooling Suction: Penetration X-12  Containment Isolation Valve Tests:
* 3-SR-3.6.1.3.10(B), Primary Containment Local Leak Rate Test (LLRT) Main Steam Line B: Penetration X-7B
* 3-SI-4.7.A.2.a-f, Primary Containment Integrated Leak Rate test (CILRT), Rev. 10  Reactor Coolant System Leak Detection Tests:
* 2-SI-4.2.E-1(B), Drywell Equipment Drain Sump Flow Integrator Calibration
 
====b. Findings====
No findings were identified.
 
===Cornerstone:===
Emergency Preparedness 1EP2 Alert and Notification System Evaluation
 
====a. Inspection Scope====
The inspectors evaluated the adequacy of the licensee's methods for testing the alert and notification system in accordance with NRC Inspection Procedure 71114, Attachment 02, Alert and Notification System (ANS) Evaluation. The applicable planning standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section IV.D requirements were used as reference criteria. The criteria contained in NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, were also used as a reference.
 
The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the alert and notification system on a biennial basis.
 
====b. Findings====
No findings were identified. 1EP3 Emergency Preparedness Organization Staffing and Augmentation System
 
====a. Inspection Scope====
The inspectors reviewed the licensee's Emergency Response Organization (ERO) augmentation staffing requirements and process for notifying the ERO to ensure the readiness of key staff for responding to an event and timely facility activation. The qualification records of key position ERO personnel were reviewed to ensure all ERO qualifications were current. A sample of problems identified from augmentation drills or system tests performed since the last inspection was reviewed to assess the effectiveness of corrective actions.
 
The inspection was conducted in accordance with NRC Inspection Procedure 71114, 03, Emergency Preparedness Organization Staffing and Augmentation System. The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR 50, Appendix E requirements were used as reference criteria.
 
The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the ERO staffing and augmentation system on a biennial basis.
 
====b. Findings====
No findings were identified.


                                          22
1EP5 Maintenance of Emergency Preparedness
1EP5 Maintenance of Emergency Preparedness
  a. Inspection Scope
    The inspectors reviewed the corrective actions identified through the Emergency
    Preparedness program to determine the significance of the issues, the completeness
    and effectiveness of corrective actions, and to determine if issues were recurring. The
    licensees post-event after action reports, self-assessments, and audits were reviewed to
    assess the licensees ability to be self-critical, thus avoiding complacency and
    degradation of their emergency preparedness program. The inspectors toured facilities
    and reviewed equipment and facility maintenance records to assess licensees
    adequacy in maintaining them. In addition, the inspectors reviewed licensee procedures
    and training for the evaluation of changes to the emergency plans.
    The inspection was conducted in accordance with NRC Inspection Procedure 71114,
    Attachment 05, Maintenance of Emergency Preparedness. The applicable 10 CFR
    50.47(b) planning standards and related 10 CFR 50, Appendix E requirements were
    used as reference criteria.
    The inspectors reviewed various documents which are listed in the Attachment. This
    inspection activity satisfied one inspection sample for the Maintenance of Emergency
    preparedness on a biennial basis.
  b. Findings
    No findings were identified.
1EP6 Drill Evaluation
  a. Inspection Scope
    During the report period, the inspectors observed an Emergency Preparedness (EP) drill
    that contributed to the licensees Drill/Exercise Performance (DEP) and Emergency
    Response Organization (ERO) performance indicator (PI) measures on June 13, 2012,
    to identify any weaknesses and deficiencies in classification, notification, dose
    assessment and protective action recommendation (PAR) development activities. The
    inspectors observed emergency response operations in the simulated control room and
    certain Emergency Response Facilities to verify that event classification and notifications
    were done in accordance with EPIP-1, Emergency Classification Procedure and other
    applicable Emergency Plan Implementing Procedures. The inspectors also attended the
    post-drill critique to compare any inspector-observed weakness with those identified by
    the licensee in order to verify whether the licensee was properly identifying weaknesses.
    This inspection activity satisfied one inspection sample for the Drill Evaluation of
    emergency preparedness
b.  Findings
    No findings were identified.
                                                                                        Enclosure


====a. Inspection Scope====
                                            23
The inspectors reviewed the corrective actions identified through the Emergency Preparedness program to determine the significance of the issues, the completeness and effectiveness of corrective actions, and to determine if issues were recurring. The licensee's post-event after action reports, self-assessments, and audits were reviewed to assess the licensee's ability to be self-critical, thus avoiding complacency and degradation of their emergency preparedness program. The inspectors toured facilities and reviewed equipment and facility maintenance records to assess licensee's adequacy in maintaining them. In addition, the inspectors reviewed licensee procedures and training for the evaluation of changes to the emergency plans.
2.    RADIATION SAFETY
 
      Cornerstone: Occupational Radiation Safety (OS)
The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment 05, Maintenance of Emergency Preparedness. The applicable 10 CFR 50.47(b) planning standards and related 10 CFR 50, Appendix E requirements were used as reference criteria.
2RS1 Radiological Hazard Assessment and Exposure Control
 
  a. Inspection Scope
The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the Maintenance of Emergency preparedness on a biennial basis.
      Radiological Hazard Assessment: The inspectors reviewed a number of radiological
 
      surveys, including those performed for airborne areas, of locations throughout the facility
====b. Findings====
      including the Unit 3 (U3) drywell, Unit 1 (U1), Unit 2 (U2), and U3 reactor buildings, the
No findings were identified. 1EP6 Drill Evaluation
      turbine building, and the independent spent fuel storage installation (ISFSI). The
 
      inspectors also walked down many of the same areas and select radioactive material
====a. Inspection Scope====
      storage locations with a survey instrument, evaluating material condition, postings, and
During the report period, the inspectors observed an Emergency Preparedness (EP) drill that contributed to the licensee's Drill/Exercise Performance (DEP) and Emergency Response Organization (ERO) performance indicator (PI) measures on June 13, 2012, to identify any weaknesses and deficiencies in classification, notification, dose assessment and protective action recommendation (PAR) development activities. The inspectors observed emergency response operations in the simulated control room and certain Emergency Response Facilities to verify that event classification and notifications were done in accordance with EPIP-1, Emergency Classification Procedure and other applicable Emergency Plan Implementing Procedures. The inspectors also attended the post-drill critique to compare any inspector-observed weakness with those identified by the licensee in order to verify whether the licensee was properly identifying weaknesses. This inspection activity satisfied one inspection sample for the Drill Evaluation of emergency preparedness
      radiological controls. Of specific interest was the Condensate Storage Tank area which
 
      due to a liquid radwaste processing problem created an actual radiation area outside the
====b. Findings====
      building, near on-going work. The inspectors observed jobs in radiologically risk-
No findings were identified.
      significant areas including high radiation areas and areas with, or with the potential for,
 
      airborne activity. The inspectors evaluated the surveys in relation to the identified
==RADIATION SAFETY==
      hazards for sufficient detail and frequency.
 
      Instructions to Workers: During plant walk downs, the inspectors observed labeling and
===Cornerstone:===
      radiological controls on containers of radioactive material. The inspectors also reviewed
Occupational Radiation Safety (OS)
      radiation work permits (RWP) used for accessing high radiation areas and airborne
{{a|2RS1}}
      areas, verifying that appropriate work control instructions and electronic dosimeter (ED)
==2RS1 Radiological Hazard Assessment and Exposure Control==
      setpoints had been provided and to assess the communication of radiological control
 
      requirements to workers. The inspectors reviewed selected ED dose and dose rate
====a. Inspection Scope====
      alarms, to verify workers properly responded to the alarms and that the licensees review
Radiological Hazard Assessment:  The inspectors reviewed a number of radiological surveys, including those performed for airborne areas, of locations throughout the facility including the Unit 3 (U3) drywell, Unit 1 (U1), Unit 2 (U2), and U3 reactor buildings, the turbine building, and the independent spent fuel storage installation (ISFSI). The inspectors also walked down many of the same areas and select radioactive material storage locations with a survey instrument, evaluating material condition, postings, and radiological controls. Of specific interest was the Condensate Storage Tank area which due to a liquid radwaste processing problem created an actual radiation area outside the building, near on-going work. The inspectors observed jobs in radiologically risk-significant areas including high radiation areas and areas with, or with the potential for, airborne activity. The inspectors evaluated the surveys in relation to the identified hazards for sufficient detail and frequency.
      of the events was appropriate. The inspectors observed pre-job RWP briefings and
 
      health physics technician coverage of workers. The inspectors reviewed the various
Instructions to Workers:  During plant walk downs, the inspectors observed labeling and radiological controls on containers of radioactive material. The inspectors also reviewed radiation work permits (RWP) used for accessing high radiation areas and airborne areas, verifying that appropriate work control instructions and electronic dosimeter (ED) setpoints had been provided and to assess the communication of radiological control requirements to workers. The inspectors reviewed selected ED dose and dose rate alarms, to verify workers properly responded to the alarms and that the licensee's review of the events was appropriate. The inspectors observed pre-job RWP briefings and health physics technician coverage of workers. The inspectors reviewed the various methods being used to notify workers of changing or changed radiological conditions.
      methods being used to notify workers of changing or changed radiological conditions.
 
      Contamination and Radioactive Material Control: The inspectors observed the release
Contamination and Radioactive Material Control:  The inspectors observed the release of potentially contaminated items from the radiologically controlled area (RCA) and from contaminated areas such as the drywell. The inspectors also reviewed the procedural requirements for, and equipment used to perform, the radiation surveys for release of personnel and material. During plant walk downs, the inspectors evaluated radioactive material storage areas and containers, including satellite RCAs and the low level radwaste facility, assessing material condition, posting/labeling, and control of materials/areas. In addition, the inspectors reviewed the sealed source inventory and verified labeling, storage conditions, and leak testing of selected sources. The inspectors verified if Category 1 and 2 sealed sources had been appropriately reported to the National Source Tracking System and physically verified the presence and controls of these sources. The sources were verified to be physically present and in proper working order.
      of potentially contaminated items from the radiologically controlled area (RCA) and from
 
      contaminated areas such as the drywell. The inspectors also reviewed the procedural
Radiological Hazards Control and Work Coverage:  The inspectors evaluated licensee performance in controlling worker access to radiologically significant areas and monitoring jobs in-progress associated with the Unit 3 refueling outage. Established radiological controls were evaluated for selected tasks including diver area setup for torus underwater coatings inspection and desludging activities, equipment staging for control rod drive work, reactor water cleanup sludge sampling, and work to support the extended power uprate for Unit 3. The inspectors evaluated the effectiveness of radiation exposure controls, including air sampling, barrier integrity, engineering controls, and postings through a review of both internal and external exposure results. The inspector followed up on two minor airborne radioactivity events.
      requirements for, and equipment used to perform, the radiation surveys for release of
 
      personnel and material. During plant walk downs, the inspectors evaluated radioactive
During walk downs with a radiation survey meter, the inspectors independently verified if ambient radiological conditions were consistent with licensee performed surveys, RWPs, and pre-job briefings; observed the adequacy of radiological controls; and observed controls for radioactive materials stored in the spent fuel pool. ED alarm set points and worker stay times were evaluated against area radiation survey results for drywell and refueling floor activities.
      material storage areas and containers, including satellite RCAs and the low level
 
      radwaste facility, assessing material condition, posting/labeling, and control of
Risk-Significant High Radiation Area and Very High Radiation Area Controls:  The inspectors discussed the controls and procedures for locked-high radiation areas (LHRAs) and very high radiation areas (VHRAs) with health physics supervisors and the radiation protection manager. During plant walk downs, the inspectors verified the posting/locking of LHRA/VHRA areas.
      materials/areas. In addition, the inspectors reviewed the sealed source inventory and
 
      verified labeling, storage conditions, and leak testing of selected sources. The
Radiation Worker Performance and Radiation Protection Technician Proficiency  The inspectors observed radiation worker performance through direct observation, via remote camera monitoring, and via telemetry. These jobs were performed in high radiation, airborne, and/or contaminated areas. The inspectors also observed health physics technicians providing field coverage of jobs and providing remote coverage.
      inspectors verified if Category 1 and 2 sealed sources had been appropriately reported
 
      to the National Source Tracking System and physically verified the presence and
Problem Identification & Resolution:  Licensee Corrective Action Program (CAP) documents associated with radiation monitoring and exposure control were reviewed and assessed. This included review of selected Problem Evaluation Reports (PERs) related to radworker and health physics technician performance. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve the identified issues in accordance with procedure NPG-SPP-3.1, Corrective Action Program, Rev. 2. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results. Licensee CAP documents reviewed are listed in Section
      controls of these sources. The sources were verified to be physically present and in
{{a|2RS1}}
      proper working order.
==2RS1 of the Attachment.==
                                                                                        Enclosure
Radiation protection activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12; Technical Specification  Sections 5.4 and 5.7; 10 Code of Federal Regulations (CFR) Parts 19 and 20; and approved licensee procedures. Radiological control activities for ISFSI areas were evaluated against 10 CFR Part 20, 10 CFR Part 72, and TS details. Records reviewed are listed in Section
{{a|2RS1}}
==2RS1 of the Attachment.==
 
The inspectors completed 1 sample, as described in Inspection Procedure (IP) 71124.01.
 
====b. Findings====
No findings were identified.
 
{{a|2RS6}}
==2RS6 Radioactive Gaseous and Liquid Effluent Treatment==
 
====a. Inspection Scope====
Program Reviews:  The inspectors reviewed the 2010 and 2011 Annual Radiological Effluent Release Report documents for consistency with the requirements in the Offsite Dose Calculation Manual (ODCM) and Technical Specifications. Unexpected results were followed up to determine the cause. Radioactive effluent monitor operability issues were discussed with plant staff. The inspectors reviewed the ODCM changes made since the last inspection against the guidance in NUREG-1301 and RG 1.109, RG 1.21, and RG 4.1.
 
Walk-Downs and Observations:  The inspectors walked-down selected components of the gaseous and liquid discharge systems to ascertain material condition, configuration and alignment. To the extent practical, the inspectors observed the material condition of abandoned in place liquid waste processing equipment for indications of degradation or leakage that could constitute a possible release pathway to the environment. The inspectors also observed the collection and analysis of gaseous effluent samples (noble gas, iodine, particulates) from the plant stack. The inspectors walked-down portions of the Standby Gas Treatment System, to ascertain material condition, configuration, and alignment. In addition, the inspectors reviewed the most recent HEPA and charcoal filtration surveillance testing results for each train of the standby gas treatment system.
 
Sampling and Analyses:  In addition to observing collection of gaseous effluent samples from the plant stack, the inspectors observed a chemistry technician verifying plant stack flow rates. The results of the chemistry count room's inter-laboratory comparison program were reviewed and discussed with cognizant licensee personnel. Dose Calculations:  The inspectors reviewed several gas release permits, and monthly gaseous/liquid effluent dose calculation summaries. The magnitudes of the releases were determined to be a small fraction of the applicable limits. The inspectors reviewed the contributions to public dose from the abnormal releases. The site's 10 CFR 61 analysis was reviewed for expected nuclide distribution from the aspects of quantifying effluents, the treatment of hard to detect nuclides, determining appropriate calibration nuclides for instruments and whole body counting libraries. The inspectors also reviewed the licensee's most recent Land Use Census results and changes in the ODCM since the last inspection. Ground Water Protection:  The licensee's implementation of the Industry Ground Water Protection Initiative was reviewed for changes since the last inspection as well. Groundwater sampling results obtained since the last inspection were reviewed.
 
Licensee response, evaluation, and follow-up to spills and leaks since the last inspection were reviewed in detail.
 
Problem Identification and Resolution:  Selected corrective action program documents associated with the effluent monitoring and control program, including problem evaluation reports (PERs) and audits, were reviewed and assessed. The inspectors verified that problems were being identified at an appropriate threshold and resolved in accordance with procedure NPG-SPP-3.1, Corrective Action Program, Rev. 2 and    Rev. 3.
 
Documents reviewed are listed in Section
{{a|2RS6}}
==2RS6 and 2RS7 of the report Attachment.==
The inspectors completed one sample as required by inspection procedure 71124.06.
 
====b. Findings====
No findings were identified.
{{a|2RS7}}
==2RS7 Radiological Environmental Monitoring Program (REMP)==
 
====a. Inspection Scope====
REMP Status and Results:  The inspectors discussed changes and reviewed the ODCM and the Annual Radiological Environmental Operating Report documents issued for calendar year (CY) 2010 and CY 2011. The inspectors also reviewed and evaluated REMP contract laboratory cross-check program results, and current procedural guidance for environmental sample collection and processing. Inspectors reviewed the Annual Radiological Effluent Release Report for CY 2010 & CY 2011 under section 2RS6. Equipment Walk-down:  The inspectors observed sample collection activities of selected air sampling stations as specified per procedure. The inspectors observed equipment material condition and verified operability, including verification of flow rates/total sample volume results, for the weekly airborne particulate filter and iodine cartridge change-outs at selected atmospheric sampling stations. The material condition and placement of environmental thermoluminescent dosimeters and water sampling stations were verified by direct observation at select ODCM locations. Land use census results actions for missed samples including compensatory measures and availability of replacement equipment were discussed with environmental technicians and knowledgeable licensee staff. Inspectors also reviewed calibration and maintenance surveillance records for the installed environmental air sampling stations. Procedural guidance, program implementation, quantitative analysis sensitivities, and environmental monitoring results were reviewed against 10 CFR Part 20; Appendix I to 10CFR Part 50; TS Sections 6.8 Procedures and Programs and 6.9, Reporting Requirements; ODCM, Rev. 15; RG 4.15, Quality Assurance for Radiological Monitoring Programs (Normal Operation) - Effluent Streams and the Environment; and the Branch Technical Position, An Acceptable Radiological Environmental Monitoring Program -1979. Documents reviewed are listed in Section
{{a|2RS7}}
==2RS7 of the Attachment.==
 
Meteorological Monitoring Program:  The inspectors walked-down the meteorological tower and observed local data collection equipment readouts. The physical condition of the tower and the instruments were observed and equipment operability, and maintenance history were discussed with responsible licensee staff. The transmission of locally generated meteorological data to the main control room operators was also verified. The inspectors reviewed applicable tower instrumentation calibration records for the meteorological measurements of wind speed, wind direction, and temperature, and evaluated measurement data recovery for CY 2010 and CY 2011.
 
Licensee procedures and activities related to meteorological monitoring were evaluated against: ODCM; FSAR; RG 1.23, Meteorological Monitoring Programs For Nuclear Power Plants, and ANSI/ANS-2.5-1984, Standard for Determining Meteorological Information at Nuclear Power Sites. Documents reviewed are listed in Section
{{a|2RS7}}
==2RS7 of the Attachment.==
Problem Identification and Resolution: The inspectors reviewed selected PERs in the areas of environmental monitoring and meteorological monitoring. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve the identified issues in accordance with NPG-SPP 3.1, Corrective Action Program, Rev. 2. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results. Documents reviewed are listed in Sections
{{a|2RS6}}
==2RS6 & 2RS7 in the Attachment.==
The inspectors completed one sample as required by inspection procedure 71124.07.
 
====b. Findings====
No findings were identified.
{{a|2RS8}}
==2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation==
 
====a. Inspection Scope====
Waste Processing and Characterization:  During inspector walk-downs, accessible sections of the liquid and solid radioactive waste (radwaste) processing systems were assessed for material condition and conformance with system design diagrams. Inspected equipment included floor drain tanks; phase separator tanks; resin and filter packaging components; and abandoned evaporator equipment. The inspectors discussed component function, processing system changes, and radwaste program implementation with licensee staff.
 
The 2010 and 2011 Annual Radiological Effluent Release Report and radionuclide characterizations for select waste streams from 2010, and each major waste stream from 2012 were reviewed and discussed with radwaste staff. For cleanup waste phase separator resin, reactor water cleanup resin, Thermex resin, and dry active waste (DAW) the inspectors evaluated analyses for hard-to-detect nuclides, reviewed the use of scaling factors, and examined quality assurance comparison results between licensee waste stream characterizations and outside laboratory data. Waste stream mixing and concentration averaging methodology for resins and filters was evaluated and discussed with radwaste staff. The inspectors also reviewed the licensee's procedural guidance for monitoring changes in waste stream isotopic mixtures. Radwaste processing activities and equipment configuration were reviewed for compliance with the licensee's Process Control Program (PCP) and UFSAR, Chapter 9. Waste stream characterization analyses were reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical Position on Waste Classification (1983). Reviewed documents are listed in Section
{{a|2RS8}}
==2RS8 of the Attachment.==
 
Radioactive Material Storage:  During walk-downs of radioactive material storage areas in the radwaste building and outdoor low-level storage yard, the inspectors observed the physical condition and labeling of storage containers and the posting of Radioactive Material Areas. The inspectors also reviewed licensee procedural guidance for storage and monitoring of radioactive material.
 
Radioactive material and waste storage activities were reviewed against the requirements of 10 CFR Part 20. Reviewed documents are listed in Section
{{a|2RS8}}
==2RS8 of the report Attachment.==
 
Transportation:  The inspectors directly observed preparation activities for shipment of a high integrity container (HIC) of resin. The inspectors noted package markings and placarding, performed independent dose rate measurements, and interviewed shipping technicians regarding Department of Transportation (DOT) regulations.
 
Selected shipping records were reviewed for consistency with licensee procedures and compliance with NRC and DOT regulations. The inspectors reviewed emergency response information, DOT shipping package classification, waste classification, radiation survey results, and evaluated whether receiving licensees were authorized to accept the packages. Licensee procedures for opening and closing Type A shipping containers were compared to manufacturer requirements. In addition, training records for selected individuals currently qualified to ship radioactive material were reviewed. Transportation program implementation was reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 71, 49 CFR Parts 172-178, as well as the guidance provided in NUREG-1608. Training activities were assessed against 49 CFR Part 172 Subpart H. Documents reviewed during the inspection are listed in Section
{{a|2RS8}}
==2RS8 of the Attachment.==
 
Problem Identification and Resolution:  The inspectors reviewed PERs in the area of radwaste/shipping. The inspectors evaluated the licensee's ability to identify and resolve the issues in accordance with procedure NPG-SPP-3.1, Corrective Action Program, Rev.
 
2 and Rev. 3. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results. Licensee corrective action program documents reviewed are listed in Section
{{a|2RS8}}
==2RS8 of the Attachment.==
 
The inspectors completed one sample as required by inspection procedure 71124.08.
 
====b. Findings====
===.1 Failure to adequately secure radioactive shipping container contents for transport===
 
=====Introduction:=====
A self-revealing Green Non-Cited Violation (NCV) of 10 CFR 71.5, Transportation of Licensed Material, was identified for the licensees failure to ensure proper packaging of two DOT 7A Type A packages as required by 49 CFR 173.475(e),
Quality Control Requirements Prior To Each Shipment Of Class 7 (Radioactive) Materials.
 
=====Description:=====
On March 22, 2010, the licensee shipped control rod drive mechanisms (CRDMs) to GE Hitachi Nuclear (GEH) for refurbishment in six Department of Transportation (DOT) approved Type A boxes. Each box contained four CRDMs. In a letter dated September 17, 2010, GEH informed the licensee that their receipt inspection of containers 1343-S and 966-S on April 23, 2010, identified that pig shield containment lid restraint bars designed to secure the CRDMs and pig shields in place were not installed and were laying loose in the bottom of the container. The licensee documented the issue in PER 236118. Licensee investigation determined that the radwaste packaging inspector failed to follow procedural requirements and verify that the CRDMs were properly secured within the container to prevent movement during shipping. The inspectors reviewed the Container Certification, container closure procedure for the CRDM boxes, licensee radioactive material shipment procedures, and engineering documents concerning the container meeting DOT 7A requirements. The inspectors noted that although the container closure procedure did not specifically address internal packaging and the restraint bars, the container certification states that "All contents must be securely positioned to prevent shifting during normal conditions of transport.", and that site procedural guidance requires verification that the contents of the package have been secured and satisfies the requirements of 10 CFR 71.87, prior to shipment.
 
=====Analysis:=====
The failure to properly secure, or adequately block or brace the material within  a Class 7 (radioactive) materials package to prevent movement during transport prior to shipment was determined to be a performance deficiency. Specifically, the licensee failed to follow established site procedures and applicable documents provided by the package vendor for package inspection and verification to ensure materials are secured within containers. The finding was more than minor because it is associated with the Public Radiation Safety Cornerstone, Plant Facilities/Equipment and Instrumentation attribute, involving transportation packaging and adversely affected the cornerstone objective to ensure adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. Specifically, the failure to correctly secure the package contents to prevent movement could have resulted in damage or failure of the container during transportation. The significance of the finding was evaluated using IMC 0612, Appendix D, "Public Radiation Safety Significance Determination Process". The issue was evaluated using the Public Radiation Safety flowchart because it involved radioactive material control, specifically, transportation. The finding was determined to be of very low safety significance (Green) because it did not involve radiation limits being exceeded, a package breach, a certificate of compliance issue, a low-level burial ground non-conformance, or a failure to make emergency notifications.
 
The cause of this finding was directly related to the cross cutting aspect of Documents, Procedures and Component Labeling in the Resources component of the Human Performance area because the licensee did not effectively incorporate package design specifications into their transportation program to ensure that all internal restraining devices are correctly installed to secure the CRDM in place to prevent damage to the transport package. [H.2(c)]
 
=====Enforcement:=====
10 CFR 71.5, Transportation of Licensed Material, required, in part, that each licensee who transports licensed material outside the site of usage, as specified in the NRC license, or where transport is on public highways, or who delivers licensed material to a carrier for transport, shall comply with the applicable requirements of the DOT regulations in 49 CFR Parts 107, 171 through 180, and 390 through 397, appropriate to the mode of transport. 49 CFR 173.475(e), Quality Control Requirements Prior To Each Shipment Of Class 7 (Radioactive) Materials, required, in part, that before each shipment of any Class 7 (radioactive) materials package, the offeror must ensure, by examination or appropriate tests, that each special instruction for filling, closing, and preparation of the packaging for shipment has been followed. Licensee procedure RWTP-100, "Radioactive Material/Waste Shipments", contains package inspection and verification requirements to ensure materials are secured within containers. Contrary to the above, on March 22, 2010, the licensee failed to comply with the applicable requirements of DOT regulation 49 CFR 173.475(e) for transport of licensed material. Specifically, the licensee failed to follow Container Certification guidance, in that the CRDMs were not properly packaged and secured inside two CRDM shipping containers as required by licensee procedure RWTP-100. Because this violation was of very low safety significance and it was entered into the licensee's CAP (SR 570902), this violation is being treated as an NCV, in accordance with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000259, 260, 296/2012003-02; Failure to Properly Prepare a DOT Type A Package for Transport)
 
===.2 Failure to Implement DOT Type A Package Closure Requirements===
 
=====Introduction:=====
A self-revealing Green Non-Cited Violation (NCV) of 10 CFR 71.5, Transportation of Licensed Material, was identified for the licensees failure to properly close a DOT 7A Type A packages as required by DOT 49 CFR 173.475(f) Quality Control Requirements Prior To Each Shipment Of Class 7 (Radioactive) Materials.
 
=====Description:=====
On September 7, 2011, the licensee shipped a DOT approved Type 'A' shipping container, containing an ISP surveillance capsule, to MP Machinery and Testing, LLC (MPM) for analysis of the contents. In a letter dated September 9, 2011, MPM informed the licensee that upon arrival at the MPM facility the closure bolts on the shipping container were found to be undertorqued at 30 ft-lbs torque, not 390 ft-lbs torque as specified in the DOT Package Certification provided by MPM. The licensee documented the issue in PER 431446. Licensee investigation determined that the ISP surveillance capsule shipping container closure bolts did not have the correct torque applied due to inadequate procedure guidance, unfamiliarity of the workers with the task, and a lack of procedure use and adherence. Preparation of the surveillance capsule for shipment occurred over several months, the Technical Instruction was revised during the period, and the container instructions provided by the vendor were not used during loading activities. The inspectors reviewed the DOT Package Certification, container loading and shipping instructions, Technical Instruction for obtaining and packaging the Reactor Vessel Test Specimens (both revisions), and the work order used to remove and package the ISP surveillance capsule for shipment. The inspectors noted that although detailed instructions for loading and closure of the container were provided by the vendor, the instructions and required container closure torque values were not included, or referenced, in the Technical Instruction or the work package.
 
=====Analysis:=====
The failure to properly close a Class 7 (radioactive) materials package was determined to be a performance deficiency. Specifically, the licensee failed to follow established site procedures and applicable vendor documents for closing the package resulting in inadequate torque of the shipping container closure bolts. The finding was more than minor because it is associated with the Public Radiation Safety Cornerstone, Plant Facilities/Equipment and Instrumentation attribute, involving transportation packaging and adversely affected the cornerstone objective to ensure adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. Specifically, the failure to apply the correct torque to the package closure bolts could have resulted in incomplete sealing of the container or failure of the cover bolts during transportation. The significance of the finding was evaluated using IMC 0612, Appendix D, "Public Radiation Safety Significance Determination Process". The issue was evaluated using the Public Radiation Safety flowchart because it involved radioactive material control, specifically, transportation. The finding was determined to be of very low safety significance (Green) because it did not involve radiation limits being exceeded, a package breach, a certificate of compliance issue, a low-level burial ground non-conformance, or a failure to make emergency notifications  The cause of this finding was directly related to the cross cutting aspect of Documents, Procedures and Component Labeling in the Resources component of the Human Performance area because the licensee did not effectively incorporate the vendor provided container loading and shipping instructions into their work package and transportation program to ensure correct torque values were used to close the shipping container. [H.2(c)]
 
=====Enforcement:=====
10 CFR 71.5, Transportation of Licensed Material, required, in part, that each licensee who transports licensed material outside the site of usage, as specified in the NRC license, or where transport is on public highways, or who delivers licensed material to a carrier for transport, shall comply with the applicable requirements of the DOT regulations in 49 CFR Parts 107, 171 through 180, and 390 through 397, appropriate to the mode of transport.
 
49 CFR 173.475(f) Quality Control Requirements Prior To Each Shipment Of Class 7 (Radioactive) Materials, required, in part, that each closure, valve, or other opening of the containment system through which the radioactive content might escape is properly closed and sealed.
 
Contrary to the above, on September 7, 2011, the licensee failed to comply with the applicable requirements of DOT regulation 49 CFR 173.475(f) for transport of licensed material. Specifically, the licensee failed to properly close an opening in the containment system of a Class 7 (radioactive) materials package. Because this violation was of very low safety significance and it was entered into the licensee's CAP (SR 571151), this violation is being treated as an NCV, in accordance with Section 2.3.2 of the NRC Enforcement Policy.  (NCV 05000259, 260, 296/2012003-03; Failure to Implement DOT Type A Package Closure Requirements)
 
==OTHER ACTIVITIES==
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness
{{a|4OA1}}
==4OA1 Performance Indicator (PI) Verification==
 
===Cornerstone:===
Mitigating Systems
 
===.1 Safety System Functional Failures; Mitigating Systems Performance Indicator- Heat===
Removal (Reactor Core Isolation Cooling)
 
====a. Inspection Scope====
The inspectors reviewed the licensee's procedures and methods for compiling and reporting the following Performance Indicators (PIs), including procedure NPG-SPP-02.2 Performance Indicator Program. The inspectors examined the licensee's PI data for the specific PIs listed below for the second quarter 2011 through first quarter of 2012. The inspectors reviewed the licensee's data and graphical representations as reported to the NRC to verify that the data was correctly reported. The inspectors also validated this data against relevant licensee records (e.g., PERs, Daily Operator Logs, Plan of the Day, Licensee Event Reports, etc.), and assessed any reported problems regarding implementation of the PI program. Furthermore, the inspectors met with responsible plant personnel to discuss and go over licensee records to verify that the PI data was appropriately captured, calculated correctly, and discrepancies resolved. The inspectors also used the Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, to ensure that industry reporting guidelines were appropriately applied. This activity constituted six mitigating systems performance indicator inspection samples.
* Unit 1 Safety System Functional Failures
* Unit 2 Safety System Functional Failures
* Unit 3 Safety System Functional Failures
* Unit 1 Mitigating Systems Performance Index - Reactor Core Isolation Cooling
* Unit 2 Mitigating Systems Performance Index - Reactor Core Isolation Cooling
* Unit 3 Mitigating Systems Performance Index - Reactor Core Isolation Cooling
{{a|4OA1}}
==4OA1 Performance Indicator (PI) Verification==
Cornerstone:  Barrier Integrity
 
====a. Inspection Scope====
The inspectors reviewed the licensee's procedures and methods for compiling and reporting the Performance Indicators (PI) listed below, including procedure SPP-3.4, Performance Indicator for NRC Reactor Oversight Process for Compiling and Reporting PIs to the NRC. The inspectors reviewed the raw data for the PITs listed below for the 1st through 4th quarters of 2006. The inspectors compared the licensee's raw data against graphical representations and specific values reported to the NRC in the 4th quarter 2006 PI report to verify that the data was correctly reflected in the report. The inspectors also reviewed the past history of PERs for any that might be relevant to problems with the PI program. Furthermore, the inspectors met with responsible chemistry and engineering personnel to discuss and go over licensee records to verify that the PI data was appropriately captured, calculated correctly, and discrepancies resolved. The inspectors reviewed Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, to verify that industry reporting guidelines were applied.
* RCS Activity for Units 2 and 3
* RCS Leakage for Units 2 and 3
 
====b. Findings====
No findings were identified.
 
===Cornerstone:===
Emergency Preparedness
 
====a. Inspection Scope====
The inspectors sampled licensee submittals relative to the PIs listed below for the period October 1, 2011, and March 31, 2012. To verify the accuracy of the PI data reported during that period, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, were used to confirm the reporting basis for each data element.
* Emergency Response Organization (ERO) Drill/Exercise Performance
* ERO Drill Participation
* Alert and Notification System Reliability For the specified review period, the inspector examined data reported to the NRC, procedural guidance for reporting PI information, and records used by the licensee to identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO drill and exercise performance through review of a sample of drill and event records.
 
The inspectors reviewed selected training records to verify the accuracy of the PI for ERO drill participation for personnel assigned to key positions in the ERO. The inspectors verified the accuracy of the PI for alert and notification system reliability through review of a sample of the licensee's records of periodic system tests. The inspectors also interviewed the licensee personnel who were responsible for collecting and evaluating the PI data. Licensee procedures, records, and other documents reviewed within this inspection area are listed in the Attachment. This inspection satisfied three Emergency Preparedness inspection samples for PI verification on an annual basis.
 
====b. Findings====
No findings were identified.
 
===Cornerstone:===
Occupational Radiation Safety    a Inspection Scope  The inspectors reviewed Performance Indicator (PI) data collected from January 1, 2011, through March 31, 2012, for the Occupational Exposure Control Effectiveness PI. For the reviewed period, the inspectors assessed CAP records to determine whether high radiation area, VHRA, or unplanned exposures, resulting in TS or 10 CFR 20 non-conformances, had occurred during the review period. In addition, the inspectors reviewed selected personnel contamination event data, internal dose assessment results, and ED alarms for cumulative doses and/or dose rates exceeding established set-points. The reviewed data were assessed against guidance contained in Nuclear Energy Institute 99-02, "Regulatory Assessment Indicator Guideline," Rev. 6. The reviewed documents relative to these PI reviews are listed in Sections
{{a|2RS1}}
==2RS1 and 4OA1 of the Attachment.==
 
====b. Findings====
No findings were identified.
 
Public Radiation Safety (PS) Cornerstone  The inspectors reviewed the Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences PI results from June 18, 2010 through May 2012. The inspectors reviewed PERs, liquid and gaseous effluent release permits, effluent dose data, and licensee procedural guidance for classifying and reporting PI events. Reviewed documents are listed in Sections
{{a|2RS6}}
==2RS6 of the Attachment.==
The inspectors completed 1 of the required samples for IP 71151.
 
====b. Findings====
No findings were identified.
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
 
===.1 Review of items entered into the Corrective Action Program:===
As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"
and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP. This review was accomplished by reviewing daily PER and Service Request (SR) reports, and periodically attending Corrective Action Review Board (CARB) and PER Screening Committee (PSC) meetings.
 
===.2 Annual Follow-up of Selected Issues - Operations with a Potential for Draining the Reactor Vessel (OPDRVs)===
 
====a. Inspection Scope====
The inspectors reviewed the licensee's response to the NRC's EMG-11-03, Enforcement Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel (OPDRVs). The inspectors focused on the changes made to licensee procedure 3-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity and discussed OPDRVs with Operations staff. The inspectors reviewed the Main Control Room (MCR) operating logs to verify OPDRVs were identified by the MCR operating crew and appropriate action taken were necessary. The inspectors also walked down portions of the alternate reactor water level control make-up and let-down line line-ups to verify they were established in accordance with the licensee's procedures. Documents reviewed are listed in the Attachment. This activity constituted one in-depth selected issue.
 
b. Assessment and Observations  No findings were identified.
 
===.3 Semiannual Review to Identify Trends===
 
====a. Inspection Scope====
As required by Inspection Procedure 71152, the inspectors performed a review of the licensee's CAP implementation and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors' review included the results from daily screening of individual PERs (see Section 4OA2.1 above), licensee trend reports and trending efforts, and independent searches of the PER database and WO history. The inspectors' review nominally considered the six-month period of January 2012 through June 2012, although some searches expanded beyond these dates. Additionally, the inspectors' review also included the Integrated Trend Reports (ITR) from the first and second quarters of fiscal year 2012. The licensee reports covered the period of October 1, 2011, to March 31, 2012. Furthermore, the inspectors verified that adverse or negative trends identified in the licensee's PERs, periodic reports and trending efforts were entered into the CAP. Inspectors interviewed the appropriate licensee staff and also reviewed procedures, NPG-SPP-02.8, Integrated Trend Review and NPG-SPP-02.7, PER Trending. The purpose of the licensee's integrated trend reviews was to identify the top site and departmental issues (gaps to excellence) requiring management attention. Other objectives were to provide status of the top issues and their progress to resolution, identify continuing issues, emerging trends and issues to be monitored, review progress towards resolving past top issues, review issues identified by external organizations such as the NRC, INPO, Nuclear Safety Review Board (NSRB), QA, etc., and determine why they were not identified by line organizations. This activity constituted one semiannual trend review inspection sample.
 
====b. Findings and Observations====
No findings were identified, but the inspectors identified a number of observations as discussed below.
 
Inspectors observed licensee-identified issues and trends in both the first and second quarter ITRs that were identical or similar in nature. Inspectors reviewed the repeat issues to assess the licensee's progress of corrective actions associated with the issues and trends identified. Some of the more notable site/departmental issues were as follows:
* Corrective Action Program (CAP):  The CAP has not been considered as a core business function by the station. Improvement is needed with problem identification, cause evaluations and timely completion of corrective actions. This issue was documented in PERs 346645 and 471366.
* Human Performance/Standards:  Human performance practices resulted in consequential events, specifically:  procedure use and adherence, procedure quality, accountability, human performance fundamentals, and the observation program.
 
This issue was documented in PERs 410308 and 491985.
* Procedure Use and Adherence:  The first quarter 2012 ITR included this in the Human Performance area (Issue #2) and developed actions to drive rigorous use of procedures throughout all organization. The second quarter 2012 ITR included this with the Procedure/Work Order Quality/Procedure Use and Adherence area (Issue #2). This issue was documented in PERs 410308 and 491985. The second quarter ITR contained fifteen fundamental problem statements that were developed as a result of the 95003 supplemental inspection. The process is intended to determine the root organizational and/or cultural causes of these issues. Corrective actions were under development for these fifteen problem areas at the end of the reporting period.
 
The inspectors conducted an independent review of the licensee's CAP to identify potential adverse trends. The inspectors identified a potential adverse trend with the licensee's control of transient combustible materials in plant areas. A review of PERs from January 2012 to June 2012 revealed twelve PERs associated with transient and excessive combustible materials in plant areas however, a PER that identified this as a trend was not identified by the licensee staff. The inspectors discussed this issue with the appropriate licensee staff and PER 577382 was initiated to document this as an adverse trend.
{{a|4OA3}}
==4OA3 Event Follow-up==
 
===.1 Unit 3 Automatic Reactor Scram Following Refueling Outage===
 
====a. Inspection Scope====
On May 22, 2012, while recovering from a refueling outage with control rod and main turbine generator off-line testing in progress, Unit 3 automatically scrammed from 19.5 percent power. Unit 3 scrammed due to a loss of offsite power when an inadvertent actuation of 3A Unit Station Service Transformer (USST) differential relay 387SA resulted from an incorrect relay setting. Inspectors promptly responded to the control room and verified that the unit was stable in Mode 3 (Hot Shutdown), and confirmed that all safety-related mitigating systems had operated properly. Inspectors evaluated safety equipment and operator performance before and after the event by examining existing plant parameters, strip charts, plant computer historical data displays, operator logs, and the critical parameter trend charts used for the post-trip report. Inspectors also interviewed responsible on-shift operations personnel, examined the implementation of the applicable annunciator response procedures and abnormal operating instructions, including 3-AOI-100-1, Reactor Scram, and reviewed the written notification made in accordance with 10 CFR 50.72. Inspectors discussed the preliminary cause of the incorrect relay setting with responsible Operations and Engineering personnel and monitored Plant Oversight Review Committee (PORC) event review and restart meetings. This review included only initial event follow-up.
 
====b. Findings====
No findings were identified.
 
===.2 Unit 3 Manual Reactor Scram Following Refueling Outage===
 
====a. Inspection Scope====
On May 24, 2012, Unit 3 was manually scrammed from Mode 2 (less than 1% rated power) when operators ranged down the Intermediate Range Monitor (IRM) 'H' instrument, instead of up, resulting in half scram on Reactor Protection System (RPS) 'B' trip system. The half scram was being reset after IRM 'H' was properly ranged. As the operator adjusted the reset scram switch, a spike on IRM 'A' was received on the RPS 'A' trip system, resulting in a partial rod insertion. When the operator identified multiple rods inserting, the actions of the Reactor Scram Procedure, 3-AOI-l00-1, were followed and a manual scram was inserted. The inspectors evaluated safety equipment and operator performance before and after the event by examining existing plant parameters, strip charts, plant computer historical data displays, operator logs, the alarm typewriter Sequence of Events printout, and the critical parameter trend charts in the post-trip report. The inspectors interviewed responsible on-shift Operations personnel, examined the implementation of annunciator response and abnormal operating procedures, (including 3-AOI-100-1, Reactor Scram) and reviewed the written notification made in accordance with 10 CFR 50.72. This review included only initial event follow up.
 
====b. Findings====
No findings were identified
 
===.3 Unit 3 Automatic Reactor Scram and Forced Outage===
 
====a. Inspection Scope====
On May 29, 2012, Unit 3 automatically scrammed from 78 percent power due to a power to load unbalance (i.e., main generator load reject) automatic trip of the main turbine generator from an A-B phase trip of the main transformer differential relay 387T. The licensee identified the cause of the differential relay trip to be a B phase current transformer manufactured and installed with opposite polarity. Preliminarily, the licensee revealed that factory acceptance and field testing failed to detect the manufacturing defect of reverse polarity. Inspectors promptly responded to the control room and verified that the unit was stable in Mode 3 (Hot Shutdown), and confirmed that all safety-related mitigating systems had operated properly. Inspectors evaluated safety equipment and operator performance before and after the event by examining existing plant parameters, strip charts, plant computer historical data displays, operator logs, and the critical parameter trend charts used for the post-trip report. Inspectors also interviewed responsible on-shift operations personnel, examined the implementation of the applicable annunciator response procedures and abnormal operating instructions, including 3-AOI-100-1, Reactor Scram, and reviewed the written notification made in accordance with 10 CFR 50.72. Inspectors discussed the preliminary cause of the failed acceptance and installation testing with responsible Operations and Engineering personnel. This review included only initial event follow-up.
 
Operators commenced restart of Unit 3 (i.e., entered Mode 2) on June 2 and achieved full power on June 6, 2011. During this short forced outage the inspectors examined the conduct of critical outage activities pursuant to technical specifications, applicable procedures, and the licensee's risk assessment and maintenance plans. Some of the more significant outage activities monitored, examined and/or reviewed by the inspectors were as follows:
* Plant Oversight Review Committee (PORC) event review and restart meetings.
* Reactor startup and power ascension activities per 3-GOI-100-1A, Unit Startup
* Reactor vessel and coolant heatup per 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring
* Outage risk assessment and management
* Control and management of forced outage and emergent work activities  Corrective Action Program  The inspectors reviewed PERs generated during the Unit 3 forced outage and attended management review committee meetings to verify that initiation thresholds, priorities, mode holds, and significance levels were assigned as required.
 
====b. Findings====
No findings were identified
 
===.4 (Closed) Licensee Event Report (LER) 05000296/2011-003-00, Automatic Reactor Scram Due to a Main Turbine Generator Load Reject.===
 
====a. Inspection Scope====
On September 28, 2011, Unit 3 automatically scrammed from 100 percent power due to a power to load unbalance (i.e., main generator load reject) automatic trip of the main turbine generator (MTG) caused by a broken debris screen. The initial follow-up of this event by the inspectors was documented in Section 4OA3.10 of IR 05000296/2011004. The inspectors reviewed the applicable LER that was issued on November 28, 2011, and it's associated PER 440539, which included the root cause analysis (RCA) and corrective actions. The licensee concluded that the direct cause of the Unit 3 turbine trip and scram was the isolated-phase bus C debris screen failure.
 
====b. Findings====
No findings were identified
 
===.5 (Closed) Licensee Event Report (LER) 05000259,296 /2011-009-02, As-Found Undervoltage Trip for the Reactor Protection System 1A1 Relay that Did Not Meet Acceptance Criteria During Several Surveillances===
 
====a. Inspection Scope====
The inspectors reviewed Revision 2 of LER 05000259/2011-009 dated April 25, 2012, PER 486780, and the associated operability determination, and corrective action plans.
 
This revised LER was submitted to provide the results of the licensee's completed investigation and evaluation of a second Reactor Protection System (RPS) relay that did not meet its acceptance criteria during previous surveillance testing for the same reason. The original LER 05000259/2011-009-00 dated December 5, 2011, the revised LER 05000259/2011-009-01 dated January 31, 2012, applicable PERs 413140 and 442914, including root cause analysis, operability determination and corrective action plans, were reviewed by the inspectors and documented in Sections 4OA3.1 and
{{a|4OA7}}
==4OA7 of NRC IR==
 
05000259/2012002. As a result of this prior review, the licensee had identified one violation of NRC requirements associated with Unit 1 RPS 1A1 relay. On January 6, 2012, while performing an operability determination for the Unit 3 reactor protection system (RPS) 3C1 relay undervoltage trips, the licensee determined that the as-found undervoltage trip setpoint for the Unit 3 relay was less than the required acceptance criteria during several technical specification surveillances. Seven of the last thirteen surveillance test results were below the technical specification acceptance criteria. Therefore, based on performance history, the RPS 3C1 relay was determined to be inoperable from June 9, 2006, to February 2, 2012, when the relay was replaced. The licensee determined the previous root cause and corrective actions were applicable in that the surveillance test program did not require past operability reviews when out of calibration technical specification conditions were corrected during surveillances. The inspectors reviewed the second LER revision and verified that the supplemental information provided in the LER was complete and accurate and that the information was not of a significant nature to warrant any change to the original LER finding. This licensee identified violation constitutes an additional example as documented in NRC IR 05000259/2012002 and is not an individual non-cited violation. Further corrective actions for this additional example are expected to be taken in conjunction with corrective actions for the previous violation.


====b. Findings====
                                      24
One finding for the original and Revision 1 of the LER was previously identified in Section
Radiological Hazards Control and Work Coverage: The inspectors evaluated licensee
{{a|4OA7}}
performance in controlling worker access to radiologically significant areas and
==4OA7 of NRC IR 05000259/2012002.==
monitoring jobs in-progress associated with the Unit 3 refueling outage. Established
No additional findings were identified. The revised LER is considered closed.
radiological controls were evaluated for selected tasks including diver area setup for
torus underwater coatings inspection and desludging activities, equipment staging for
control rod drive work, reactor water cleanup sludge sampling, and work to support the
extended power uprate for Unit 3. The inspectors evaluated the effectiveness of
radiation exposure controls, including air sampling, barrier integrity, engineering controls,
and postings through a review of both internal and external exposure results. The
inspector followed up on two minor airborne radioactivity events.
During walk downs with a radiation survey meter, the inspectors independently verified if
ambient radiological conditions were consistent with licensee performed surveys, RWPs,
and pre-job briefings; observed the adequacy of radiological controls; and observed
controls for radioactive materials stored in the spent fuel pool. ED alarm set points and
worker stay times were evaluated against area radiation survey results for drywell and
refueling floor activities.
Risk-Significant High Radiation Area and Very High Radiation Area Controls: The
inspectors discussed the controls and procedures for locked-high radiation areas
(LHRAs) and very high radiation areas (VHRAs) with health physics supervisors and the
radiation protection manager. During plant walk downs, the inspectors verified the
posting/locking of LHRA/VHRA areas.
Radiation Worker Performance and Radiation Protection Technician Proficiency The
inspectors observed radiation worker performance through direct observation, via
remote camera monitoring, and via telemetry. These jobs were performed in high
radiation, airborne, and/or contaminated areas. The inspectors also observed health
physics technicians providing field coverage of jobs and providing remote coverage.
Problem Identification & Resolution: Licensee Corrective Action Program (CAP)
documents associated with radiation monitoring and exposure control were reviewed
and assessed. This included review of selected Problem Evaluation Reports (PERs)
related to radworker and health physics technician performance. The inspectors
evaluated the licensees ability to identify, characterize, prioritize, and resolve the
identified issues in accordance with procedure NPG-SPP-3.1, Corrective Action
Program, Rev. 2. The inspectors also evaluated the scope of the licensees internal
audit program and reviewed recent assessment results. Licensee CAP documents
reviewed are listed in Section 2RS1 of the Attachment.
Radiation protection activities were evaluated against the requirements of Updated Final
Safety Analysis Report (UFSAR) Section 12; Technical Specification Sections 5.4 and
5.7; 10 Code of Federal Regulations (CFR) Parts 19 and 20; and approved licensee
procedures. Radiological control activities for ISFSI areas were evaluated against 10
CFR Part 20, 10 CFR Part 72, and TS details. Records reviewed are listed in Section
2RS1 of the Attachment.
                                                                                    Enclosure


===.6 (Closed) Licensee Event Report (LER) 05000296/2012-001-00, Annunciator Panel Power Supply Fire in Unit 3 Control Room===
                                            25
    The inspectors completed 1 sample, as described in Inspection Procedure (IP)
    71124.01.
b.  Findings
    No findings were identified.
2RS6 Radioactive Gaseous and Liquid Effluent Treatment
a.  Inspection Scope
    Program Reviews: The inspectors reviewed the 2010 and 2011 Annual Radiological
    Effluent Release Report documents for consistency with the requirements in the Offsite
    Dose Calculation Manual (ODCM) and Technical Specifications. Unexpected results
    were followed up to determine the cause. Radioactive effluent monitor operability issues
    were discussed with plant staff. The inspectors reviewed the ODCM changes made
    since the last inspection against the guidance in NUREG-1301 and RG 1.109, RG 1.21,
    and RG 4.1.
    Walk-Downs and Observations: The inspectors walked-down selected components of
    the gaseous and liquid discharge systems to ascertain material condition, configuration
    and alignment. To the extent practical, the inspectors observed the material condition of
    abandoned in place liquid waste processing equipment for indications of degradation or
    leakage that could constitute a possible release pathway to the environment. The
    inspectors also observed the collection and analysis of gaseous effluent samples (noble
    gas, iodine, particulates) from the plant stack. The inspectors walked-down portions of
    the Standby Gas Treatment System, to ascertain material condition, configuration, and
    alignment. In addition, the inspectors reviewed the most recent HEPA and charcoal
    filtration surveillance testing results for each train of the standby gas treatment system.
    Sampling and Analyses: In addition to observing collection of gaseous effluent samples
    from the plant stack, the inspectors observed a chemistry technician verifying plant stack
    flow rates. The results of the chemistry count rooms inter-laboratory comparison
    program were reviewed and discussed with cognizant licensee personnel.
    Dose Calculations: The inspectors reviewed several gas release permits, and monthly
    gaseous/liquid effluent dose calculation summaries. The magnitudes of the releases
    were determined to be a small fraction of the applicable limits. The inspectors reviewed
    the contributions to public dose from the abnormal releases. The sites 10 CFR 61
    analysis was reviewed for expected nuclide distribution from the aspects of quantifying
    effluents, the treatment of hard to detect nuclides, determining appropriate calibration
    nuclides for instruments and whole body counting libraries. The inspectors also
    reviewed the licensees most recent Land Use Census results and changes in the
    ODCM since the last inspection.
    Ground Water Protection: The licensees implementation of the Industry Ground Water
    Protection Initiative was reviewed for changes since the last inspection as well.
    Groundwater sampling results obtained since the last inspection were reviewed.
                                                                                        Enclosure


====a. Inspection Scope====
                                          26
On January 26, 2012, Unit 3 main control room operators smelled smoke and observed a flame coming from the bottom of an annunciator panel 3-XA-55-5A power supply. Fire Operations personnel arrived on the scene within five minutes. The affected circuit breaker was opened and fire extinguished within ten minutes. Operations personnel increased plant monitoring to compensate for indications that lost their alarming functions when the circuit breaker was opened. The fire damage was limited to the failed annunciator power supply and the power supply directly above it. The inspectors reviewed the details surrounding this event, interviewed operations and engineering personnel involved with this issue and reviewed the licensee's apparent cause determination report. This was captured in the licensee's corrective action program as problem event report (PER) 496592. This LER is closed.
    Licensee response, evaluation, and follow-up to spills and leaks since the last inspection
    were reviewed in detail.
    Problem Identification and Resolution: Selected corrective action program documents
    associated with the effluent monitoring and control program, including problem
    evaluation reports (PERs) and audits, were reviewed and assessed. The inspectors
    verified that problems were being identified at an appropriate threshold and resolved in
    accordance with procedure NPG-SPP-3.1, Corrective Action Program, Rev. 2 and
    Rev. 3.
    Documents reviewed are listed in Section 2RS6 and 2RS7 of the report Attachment.
    The inspectors completed one sample as required by inspection procedure 71124.06.
b.  Findings
    No findings were identified.
2RS7 Radiological Environmental Monitoring Program (REMP)
a. Inspection Scope
    REMP Status and Results: The inspectors discussed changes and reviewed the ODCM
    and the Annual Radiological Environmental Operating Report documents issued for
    calendar year (CY) 2010 and CY 2011. The inspectors also reviewed and evaluated
    REMP contract laboratory cross-check program results, and current procedural guidance
    for environmental sample collection and processing. Inspectors reviewed the Annual
    Radiological Effluent Release Report for CY 2010 & CY 2011 under section 2RS6.
    Equipment Walk-down: The inspectors observed sample collection activities of selected
    air sampling stations as specified per procedure. The inspectors observed equipment
    material condition and verified operability, including verification of flow rates/total sample
    volume results, for the weekly airborne particulate filter and iodine cartridge change-outs
    at selected atmospheric sampling stations. The material condition and placement of
    environmental thermoluminescent dosimeters and water sampling stations were verified
    by direct observation at select ODCM locations. Land use census results actions for
    missed samples including compensatory measures and availability of replacement
    equipment were discussed with environmental technicians and knowledgeable licensee
    staff. Inspectors also reviewed calibration and maintenance surveillance records for the
    installed environmental air sampling stations.
    Procedural guidance, program implementation, quantitative analysis sensitivities, and
    environmental monitoring results were reviewed against 10 CFR Part 20; Appendix I to
    10CFR Part 50; TS Sections 6.8 Procedures and Programs and 6.9, Reporting
    Requirements; ODCM, Rev. 15; RG 4.15, Quality Assurance for Radiological Monitoring
    Programs (Normal Operation) - Effluent Streams and the Environment; and the Branch
    Technical Position, An Acceptable Radiological Environmental Monitoring Program -
    1979. Documents reviewed are listed in Section 2RS7 of the Attachment.
                                                                                          Enclosure


====b. Findings====
                                          27
    Meteorological Monitoring Program: The inspectors walked-down the meteorological
    tower and observed local data collection equipment readouts. The physical condition of
    the tower and the instruments were observed and equipment operability, and
    maintenance history were discussed with responsible licensee staff. The transmission of
    locally generated meteorological data to the main control room operators was also
    verified. The inspectors reviewed applicable tower instrumentation calibration records
    for the meteorological measurements of wind speed, wind direction, and temperature,
    and evaluated measurement data recovery for CY 2010 and CY 2011.
    Licensee procedures and activities related to meteorological monitoring were evaluated
    against: ODCM; FSAR; RG 1.23, Meteorological Monitoring Programs For Nuclear
    Power Plants, and ANSI/ANS-2.5-1984, Standard for Determining Meteorological
    Information at Nuclear Power Sites. Documents reviewed are listed in Section 2RS7 of
    the Attachment.
    Problem Identification and Resolution: The inspectors reviewed selected PERs in the
    areas of environmental monitoring and meteorological monitoring. The inspectors
    evaluated the licensees ability to identify, characterize, prioritize, and resolve the
    identified issues in accordance with NPG-SPP 3.1, Corrective Action Program, Rev. 2.
    The inspectors also evaluated the scope of the licensees internal audit program and
    reviewed recent assessment results. Documents reviewed are listed in Sections 2RS6
    & 2RS7 in the Attachment.
    The inspectors completed one sample as required by inspection procedure 71124.07.
b. Findings
    No findings were identified.
2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and
    Transportation
a.  Inspection Scope
    Waste Processing and Characterization: During inspector walk-downs, accessible
    sections of the liquid and solid radioactive waste (radwaste) processing systems were
    assessed for material condition and conformance with system design diagrams.
    Inspected equipment included floor drain tanks; phase separator tanks; resin and filter
    packaging components; and abandoned evaporator equipment. The inspectors
    discussed component function, processing system changes, and radwaste program
    implementation with licensee staff.
    The 2010 and 2011 Annual Radiological Effluent Release Report and radionuclide
    characterizations for select waste streams from 2010, and each major waste stream
    from 2012 were reviewed and discussed with radwaste staff. For cleanup waste phase
    separator resin, reactor water cleanup resin, Thermex resin, and dry active waste (DAW)
    the inspectors evaluated analyses for hard-to-detect nuclides, reviewed the use of
    scaling factors, and examined quality assurance comparison results between licensee
                                                                                          Enclosure


=====Introduction:=====
                                      28
A self-revealing Green finding (FIN) was identified for the licensee's failure to perform preventive maintenance on the Unit 3 Main Control Room (MCR) annunciator power supplies. As a result, a power supply failed which led to a fire in annunciator panel 3-XA-55-5A in the Unit 3 MCR.  
waste stream characterizations and outside laboratory data. Waste stream mixing and
concentration averaging methodology for resins and filters was evaluated and discussed
with radwaste staff. The inspectors also reviewed the licensees procedural guidance for
monitoring changes in waste stream isotopic mixtures.
Radwaste processing activities and equipment configuration were reviewed for
compliance with the licensees Process Control Program (PCP) and UFSAR, Chapter 9.
Waste stream characterization analyses were reviewed against regulations detailed in
10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical
Position on Waste Classification (1983). Reviewed documents are listed in Section
2RS8 of the Attachment.
Radioactive Material Storage: During walk-downs of radioactive material storage areas
in the radwaste building and outdoor low-level storage yard, the inspectors observed the
physical condition and labeling of storage containers and the posting of Radioactive
Material Areas. The inspectors also reviewed licensee procedural guidance for storage
and monitoring of radioactive material.
Radioactive material and waste storage activities were reviewed against the
requirements of 10 CFR Part 20. Reviewed documents are listed in Section 2RS8 of the
report Attachment.
Transportation: The inspectors directly observed preparation activities for shipment of a
high integrity container (HIC) of resin. The inspectors noted package markings and
placarding, performed independent dose rate measurements, and interviewed shipping
technicians regarding Department of Transportation (DOT) regulations.
Selected shipping records were reviewed for consistency with licensee procedures and
compliance with NRC and DOT regulations. The inspectors reviewed emergency
response information, DOT shipping package classification, waste classification,
radiation survey results, and evaluated whether receiving licensees were authorized to
accept the packages. Licensee procedures for opening and closing Type A shipping
containers were compared to manufacturer requirements. In addition, training records
for selected individuals currently qualified to ship radioactive material were reviewed.
Transportation program implementation was reviewed against regulations detailed in 10
CFR Part 20, 10 CFR Part 71, 49 CFR Parts 172-178, as well as the guidance provided
in NUREG-1608. Training activities were assessed against 49 CFR Part 172 Subpart H.
Documents reviewed during the inspection are listed in Section 2RS8 of the Attachment.
Problem Identification and Resolution: The inspectors reviewed PERs in the area of
radwaste/shipping. The inspectors evaluated the licensees ability to identify and resolve
the issues in accordance with procedure NPG-SPP-3.1, Corrective Action Program, Rev.
2 and Rev. 3. The inspectors also evaluated the scope of the licensees internal audit
program and reviewed recent assessment results. Licensee corrective action program
documents reviewed are listed in Section 2RS8 of the Attachment.
                                                                                  Enclosure


=====Description:=====
                                        29
On January 26, 2012, Unit 3 main control room operators smelled smoke and observed a flame coming from the bottom of an annunciator panel power supply.
  The inspectors completed one sample as required by inspection procedure 71124.08.
b. Findings
.1 Failure to adequately secure radioactive shipping container contents for transport
  Introduction: A self-revealing Green Non-Cited Violation (NCV) of 10 CFR 71.5,
  Transportation of Licensed Material, was identified for the licensees failure to ensure
  proper packaging of two DOT 7A Type A packages as required by 49 CFR 173.475(e),
  Quality Control Requirements Prior To Each Shipment Of Class 7 (Radioactive)
  Materials.
  Description: On March 22, 2010, the licensee shipped control rod drive mechanisms
  (CRDMs) to GE Hitachi Nuclear (GEH) for refurbishment in six Department of
  Transportation (DOT) approved Type A boxes. Each box contained four CRDMs. In a
  letter dated September 17, 2010, GEH informed the licensee that their receipt inspection
  of containers 1343-S and 966-S on April 23, 2010, identified that pig shield containment
  lid restraint bars designed to secure the CRDMs and pig shields in place were not
  installed and were laying loose in the bottom of the container. The licensee documented
  the issue in PER 236118. Licensee investigation determined that the radwaste
  packaging inspector failed to follow procedural requirements and verify that the CRDMs
  were properly secured within the container to prevent movement during shipping. The
  inspectors reviewed the Container Certification, container closure procedure for the
  CRDM boxes, licensee radioactive material shipment procedures, and engineering
  documents concerning the container meeting DOT 7A requirements. The inspectors
  noted that although the container closure procedure did not specifically address internal
  packaging and the restraint bars, the container certification states that All contents must
  be securely positioned to prevent shifting during normal conditions of transport., and
  that site procedural guidance requires verification that the contents of the package have
  been secured and satisfies the requirements of 10 CFR 71.87, prior to shipment.
  Analysis: The failure to properly secure, or adequately block or brace the material within
  a Class 7 (radioactive) materials package to prevent movement during transport prior to
  shipment was determined to be a performance deficiency. Specifically, the licensee
  failed to follow established site procedures and applicable documents provided by the
  package vendor for package inspection and verification to ensure materials are secured
  within containers. The finding was more than minor because it is associated with the
  Public Radiation Safety Cornerstone, Plant Facilities/Equipment and Instrumentation
  attribute, involving transportation packaging and adversely affected the cornerstone
  objective to ensure adequate protection of public health and safety from exposure to
  radioactive materials released into the public domain as a result of routine civilian
  nuclear reactor operation. Specifically, the failure to correctly secure the package
  contents to prevent movement could have resulted in damage or failure of the container
  during transportation. The significance of the finding was evaluated using IMC 0612,
  Appendix D, Public Radiation Safety Significance Determination Process. The issue
  was evaluated using the Public Radiation Safety flowchart because it involved
  radioactive material control, specifically, transportation. The finding was determined to
  be of very low safety significance (Green) because it did not involve radiation limits being
                                                                                      Enclosure


Within ten minutes, the Fire Brigade responded to the MCR and the circuit breaker was opened for the affected power supply which extinguished the fire. Damage was confined to two power supplies in annunciator panel 3-XA-55-5A. The damaged power supplies were replaced on January 27, 2012 in accordance with Work Order (WO) 113155456. Corrective action document PER 496592 identified the direct cause of the annunciator power supply failure as an overcurrent condition caused by a failed electrolytic capacitor. This PER referenced EPRI recommendations to change out components with electrolytic capacitors on a time based frequency. TVA's apparent cause concluded the power supply (capacitor), installed for thirty four (34) years, experienced an age related failure due to a lack of preventive maintenance. Age-related failures of electrolytic capacitors have been documented in the industry.
                                          30
  exceeded, a package breach, a certificate of compliance issue, a low-level burial ground
  non-conformance, or a failure to make emergency notifications.
  The cause of this finding was directly related to the cross cutting aspect of Documents,
  Procedures and Component Labeling in the Resources component of the Human
  Performance area because the licensee did not effectively incorporate package design
  specifications into their transportation program to ensure that all internal restraining
  devices are correctly installed to secure the CRDM in place to prevent damage to the
  transport package. [H.2(c)]
  Enforcement: 10 CFR 71.5, Transportation of Licensed Material, required, in part, that
  each licensee who transports licensed material outside the site of usage, as specified in
  the NRC license, or where transport is on public highways, or who delivers licensed
  material to a carrier for transport, shall comply with the applicable requirements of the
  DOT regulations in 49 CFR Parts 107, 171 through 180, and 390 through 397,
  appropriate to the mode of transport.
  49 CFR 173.475(e), Quality Control Requirements Prior To Each Shipment Of Class 7
  (Radioactive) Materials, required, in part, that before each shipment of any Class 7
  (radioactive) materials package, the offeror must ensure, by examination or appropriate
  tests, that each special instruction for filling, closing, and preparation of the packaging
  for shipment has been followed. Licensee procedure RWTP-100, Radioactive
  Material/Waste Shipments, contains package inspection and verification requirements
  to ensure materials are secured within containers.
  Contrary to the above, on March 22, 2010, the licensee failed to comply with the
  applicable requirements of DOT regulation 49 CFR 173.475(e) for transport of licensed
  material. Specifically, the licensee failed to follow Container Certification guidance, in
  that the CRDMs were not properly packaged and secured inside two CRDM shipping
  containers as required by licensee procedure RWTP-100. Because this violation was of
  very low safety significance and it was entered into the licensees CAP (SR 570902), this
  violation is being treated as an NCV, in accordance with Section 2.3.2 of the NRC
  Enforcement Policy. (NCV 05000259, 260, 296/2012003-02; Failure to Properly Prepare
  a DOT Type A Package for Transport)
.2 Failure to Implement DOT Type A Package Closure Requirements
  Introduction: A self-revealing Green Non-Cited Violation (NCV) of 10 CFR 71.5,
  Transportation of Licensed Material, was identified for the licensees failure to properly
  close a DOT 7A Type A packages as required by DOT 49 CFR 173.475(f) Quality
  Control Requirements Prior To Each Shipment Of Class 7 (Radioactive) Materials.
  Description: On September 7, 2011, the licensee shipped a DOT approved Type A
  shipping container, containing an ISP surveillance capsule, to MP Machinery and
  Testing, LLC (MPM) for analysis of the contents. In a letter dated September 9, 2011,
  MPM informed the licensee that upon arrival at the MPM facility the closure bolts on the
  shipping container were found to be undertorqued at 30 ft-lbs torque, not 390 ft-lbs
  torque as specified in the DOT Package Certification provided by MPM. The licensee
                                                                                        Enclosure


Electric Power Research Institute (EPRI) document, TR-112175, Capacitor Application and Maintenance Guide, dated August 1999, stated that capacitor change outs are performed between 7 and 15 years depending on vendor recommendations and plant operating experience. Another EPRI document, Power Supply Maintenance and Application Guide (1003096), dated December 2001, stated that many of the power supplies that failed had been in service greater than 15 years on average. Since 2008 three PERs have been entered in TVA's CAP that document similar failures of these annunciator power supplies on both Unit 2 and 3 main control room panels. PER 391479 was initiated in June 2011 to evaluate the equipment reliability classification of these power supplies. Corrective actions to evaluate the annunciator power supply preventive maintenance strategy were in progress when the fire occurred. These power supplies were classified as Quality-Related, Non-Critical, Low Duty-Cycle, Mild Service Condition in accordance with licensee procedure NPG-SPP-09.18.2, Equipment Reliability Classification. Licensee procedure TVA-NQA-PLN89-A, Nuclear Quality Assurance Plan stated that the nuclear maintenance program including corrective and preventive maintenance shall ensure that quality-related structures, systems and components are maintained at a level sufficient to perform their intended functions.
                                      31
documented the issue in PER 431446. Licensee investigation determined that the ISP
surveillance capsule shipping container closure bolts did not have the correct torque
applied due to inadequate procedure guidance, unfamiliarity of the workers with the task,
and a lack of procedure use and adherence. Preparation of the surveillance capsule for
shipment occurred over several months, the Technical Instruction was revised during the
period, and the container instructions provided by the vendor were not used during
loading activities. The inspectors reviewed the DOT Package Certification, container
loading and shipping instructions, Technical Instruction for obtaining and packaging the
Reactor Vessel Test Specimens (both revisions), and the work order used to remove
and package the ISP surveillance capsule for shipment. The inspectors noted that
although detailed instructions for loading and closure of the container were provided by
the vendor, the instructions and required container closure torque values were not
included, or referenced, in the Technical Instruction or the work package.
Analysis: The failure to properly close a Class 7 (radioactive) materials package was
determined to be a performance deficiency. Specifically, the licensee failed to follow
established site procedures and applicable vendor documents for closing the package
resulting in inadequate torque of the shipping container closure bolts. The finding was
more than minor because it is associated with the Public Radiation Safety Cornerstone,
Plant Facilities/Equipment and Instrumentation attribute, involving transportation
packaging and adversely affected the cornerstone objective to ensure adequate
protection of public health and safety from exposure to radioactive materials released
into the public domain as a result of routine civilian nuclear reactor operation.
Specifically, the failure to apply the correct torque to the package closure bolts could
have resulted in incomplete sealing of the container or failure of the cover bolts during
transportation. The significance of the finding was evaluated using IMC 0612, Appendix
D, Public Radiation Safety Significance Determination Process. The issue was
evaluated using the Public Radiation Safety flowchart because it involved radioactive
material control, specifically, transportation. The finding was determined to be of very
low safety significance (Green) because it did not involve radiation limits being
exceeded, a package breach, a certificate of compliance issue, a low-level burial ground
non-conformance, or a failure to make emergency notifications
The cause of this finding was directly related to the cross cutting aspect of Documents,
Procedures and Component Labeling in the Resources component of the Human
Performance area because the licensee did not effectively incorporate the vendor
provided container loading and shipping instructions into their work package and
transportation program to ensure correct torque values were used to close the shipping
container. [H.2(c)]
Enforcement: 10 CFR 71.5, Transportation of Licensed Material, required, in part, that
each licensee who transports licensed material outside the site of usage, as specified in
the NRC license, or where transport is on public highways, or who delivers licensed
material to a carrier for transport, shall comply with the applicable requirements of the
DOT regulations in 49 CFR Parts 107, 171 through 180, and 390 through 397,
appropriate to the mode of transport.
                                                                                  Enclosure


=====Analysis:=====
                                            32
The failure to perform preventive maintenance on the Unit 3 annunciator power supplies prior to their age related failure was a performance deficiency.
      49 CFR 173.475(f) Quality Control Requirements Prior To Each Shipment Of Class 7
      (Radioactive) Materials, required, in part, that each closure, valve, or other opening of
      the containment system through which the radioactive content might escape is properly
      closed and sealed.
      Contrary to the above, on September 7, 2011, the licensee failed to comply with the
      applicable requirements of DOT regulation 49 CFR 173.475(f) for transport of licensed
      material. Specifically, the licensee failed to properly close an opening in the containment
      system of a Class 7 (radioactive) materials package. Because this violation was of very
      low safety significance and it was entered into the licensees CAP (SR 571151), this
      violation is being treated as an NCV, in accordance with Section 2.3.2 of the NRC
      Enforcement Policy. (NCV 05000259, 260, 296/2012003-03; Failure to Implement DOT
      Type A Package Closure Requirements)
4.    OTHER ACTIVITIES
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
      Preparedness
4OA1 Performance Indicator (PI) Verification
      Cornerstone: Mitigating Systems
  .1 Safety System Functional Failures; Mitigating Systems Performance Indicator- Heat
      Removal (Reactor Core Isolation Cooling)
  a. Inspection Scope
      The inspectors reviewed the licensees procedures and methods for compiling and
      reporting the following Performance Indicators (PIs), including procedure NPG-SPP-02.2
      Performance Indicator Program. The inspectors examined the licensees PI data for the
      specific PIs listed below for the second quarter 2011 through first quarter of 2012. The
      inspectors reviewed the licensees data and graphical representations as reported to the
      NRC to verify that the data was correctly reported. The inspectors also validated this
      data against relevant licensee records (e.g., PERs, Daily Operator Logs, Plan of the
      Day, Licensee Event Reports, etc.), and assessed any reported problems regarding
      implementation of the PI program. Furthermore, the inspectors met with responsible
      plant personnel to discuss and go over licensee records to verify that the PI data was
      appropriately captured, calculated correctly, and discrepancies resolved. The inspectors
      also used the Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment
      Performance Indicator Guideline, to ensure that industry reporting guidelines were
      appropriately applied. This activity constituted six mitigating systems performance
      indicator inspection samples.
      *  Unit 1 Safety System Functional Failures
      *  Unit 2 Safety System Functional Failures
      *  Unit 3 Safety System Functional Failures
                                                                                        Enclosure


Specifically, TVA procedure TVA-NQA-PLN89-A, Nuclear Quality Assurance Plan stated that the nuclear maintenance program including corrective and preventive maintenance shall ensure that quality-related structures, systems and components are maintained at a level sufficient to perform their intended functions. These power supplies were classified as Quality-Related according to TVA procedure NPG-SPP-09.18.2, Equipment Reliability Classification. As a result of the performance deficiency, a Unit 3 MCR annunciator power supply was left in service for 34 years, failed due to an aged electrolytic capacitor and resulted in an over-current related fire. The performance deficiency was determined to be more than minor because it was considered sufficiently similar to example 4.f of Inspection Manual Chapter (IMC) 0612, Appendix E, for an issue that resulted in a fire hazard in a safety-related area of the plant. The finding was associated with the Initiating Events Cornerstone and initially characterized according to IMC 0609, Significance Determination Process (SDP), Attachment 4, Phase 1 - Initial Screening and Characterization of Findings. The results of this analysis required a phase 3 evaluation in accordance with IMC 0609 because the finding increased the likelihood of and actually caused a fire in the Unit 3 MCR. The regional Senior Reactor Analyst performed a Phase 3 analysis for the issue. Pictures were provided to an NRC contractor who provides expertise in fire damage for the agency. It was determined that the configuration of the fire would not likely result in damage to anything of significance because the metal box that the annunciator's power supplies are located in, would prevent propagation of the fire beyond the box. It is also unlikely that enough heat or smoke could be created to require control room evacuation, which would impact the human actions that would be performed to shut down the plant. Without an impact to additional plant equipment, or a major impact on human action failure rates, the finding was determined to be Green. The cause of this finding was related to the cross cutting aspect of Problem Identification in the Corrective Action Program component of the Problem Identification and Resolution area, because the licensee was aware of three previous failures of these power supplies in July 2009 and should have recognized that the electrolytic capacitors, installed beyond their recommended service life, required replacement prior to failure [P.1(a)]. 
                                          33
    *    Unit 1 Mitigating Systems Performance Index - Reactor Core Isolation Cooling
    *    Unit 2 Mitigating Systems Performance Index - Reactor Core Isolation Cooling
    *    Unit 3 Mitigating Systems Performance Index - Reactor Core Isolation Cooling
4OA1 Performance Indicator (PI) Verification
    Cornerstone: Barrier Integrity
a. Inspection Scope
    The inspectors reviewed the licensees procedures and methods for compiling and
    reporting the Performance Indicators (PI) listed below, including procedure SPP-3.4,
    Performance Indicator for NRC Reactor Oversight Process for Compiling and Reporting
    PIs to the NRC. The inspectors reviewed the raw data for the PITs listed below for the
    1st through 4th quarters of 2006. The inspectors compared the licensees raw data
    against graphical representations and specific values reported to the NRC in the 4th
    quarter 2006 PI report to verify that the data was correctly reflected in the report. The
    inspectors also reviewed the past history of PERs for any that might be relevant to
    problems with the PI program. Furthermore, the inspectors met with responsible
    chemistry and engineering personnel to discuss and go over licensee records to verify
    that the PI data was appropriately captured, calculated correctly, and discrepancies
    resolved. The inspectors reviewed Nuclear Energy Institute 99-02, Regulatory
    Assessment Performance Indicator Guideline, to verify that industry reporting guidelines
    were applied.
    *    RCS Activity for Units 2 and 3
    *    RCS Leakage for Units 2 and 3
b.  Findings
    No findings were identified.
    Cornerstone: Emergency Preparedness
a. Inspection Scope
    The inspectors sampled licensee submittals relative to the PIs listed below for the period
    October 1, 2011, and March 31, 2012. To verify the accuracy of the PI data reported
    during that period, PI definitions and guidance contained in NEI 99-02, Regulatory
    Assessment Performance Indicator Guideline, Revision 6, were used to confirm the
    reporting basis for each data element.
    *    Emergency Response Organization (ERO) Drill/Exercise Performance
    *    ERO Drill Participation
    *    Alert and Notification System Reliability
                                                                                        Enclosure


=====Enforcement:=====
                                        34
Enforcement action does not apply because the performance deficiency did not involve a violation of regulatory requirements since the main control room annunciator power supplies were not safety-related. Because the finding does not involve a violation, was entered into the licensee's corrective action program as PER 496592, and has very low safety significance, it is identified as FIN 05000296/2012003-04, Failure to Perform Preventive Maintenance on the Unit 3 Main Control Room Annunciator Power Supplies.  
  For the specified review period, the inspector examined data reported to the NRC,
{{a|4OA6}}
  procedural guidance for reporting PI information, and records used by the licensee to
==4OA6 Meetings, Including Exit==
  identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO
  drill and exercise performance through review of a sample of drill and event records.
  The inspectors reviewed selected training records to verify the accuracy of the PI for
  ERO drill participation for personnel assigned to key positions in the ERO. The
  inspectors verified the accuracy of the PI for alert and notification system reliability
  through review of a sample of the licensees records of periodic system tests. The
  inspectors also interviewed the licensee personnel who were responsible for collecting
  and evaluating the PI data. Licensee procedures, records, and other documents
  reviewed within this inspection area are listed in the Attachment. This inspection
  satisfied three Emergency Preparedness inspection samples for PI verification on an
  annual basis.
b. Findings
  No findings were identified.
  Cornerstone: Occupational Radiation Safety
a Inspection Scope
  The inspectors reviewed Performance Indicator (PI) data collected from January 1,
  2011, through March 31, 2012, for the Occupational Exposure Control Effectiveness PI.
  For the reviewed period, the inspectors assessed CAP records to determine whether
  high radiation area, VHRA, or unplanned exposures, resulting in TS or 10 CFR 20 non-
  conformances, had occurred during the review period. In addition, the inspectors
  reviewed selected personnel contamination event data, internal dose assessment
  results, and ED alarms for cumulative doses and/or dose rates exceeding established
  set-points. The reviewed data were assessed against guidance contained in Nuclear
  Energy Institute 99-02, "Regulatory Assessment Indicator Guideline," Rev. 6. The
  reviewed documents relative to these PI reviews are listed in Sections 2RS1 and 4OA1
  of the Attachment.
b. Findings
  No findings were identified.
  Public Radiation Safety (PS) Cornerstone
  The inspectors reviewed the Radiological Effluent Technical Specification/Offsite Dose
  Calculation Manual Radiological Effluent Occurrences PI results from June 18, 2010
  through May 2012. The inspectors reviewed PERs, liquid and gaseous effluent release
  permits, effluent dose data, and licensee procedural guidance for classifying and
  reporting PI events. Reviewed documents are listed in Sections 2RS6 of the
  Attachment.
  The inspectors completed 1 of the required samples for IP 71151.
                                                                                      Enclosure


===.1 Exit Meeting Summary===
                                            35
On April 13, 2012, regional inspectors presented the results of the Occupational Radiation Safety inspection to Mr. P. Summers, Director Safety and Licensing, and other members of the licensee's staff. On April 20, 2012, regional inspectors presented the results of the Unit 3 Inservice Inspection to members of the licensee's staff. On June 22, 2012, regional inspectors presented the results of the Public Radiation Safety inspection to Mr. K. Polson, Site Vice President, and other members of the licensee's staff, who acknowledged the findings. On July 03, 2012, regional inspectors presented changes to the inspection results via telephone to Mr. S. Bono, General Manager Site Operations, and other members of the licensee's staff, who acknowledged the changes.
b.  Findings
    No findings were identified.
4OA2 Identification and Resolution of Problems
.1 Review of items entered into the Corrective Action Program:
    As required by Inspection Procedure 71152, Identification and Resolution of Problems,
    and in order to help identify repetitive equipment failures or specific human performance
    issues for follow-up, the inspectors performed a daily screening of items entered into the
    licensees CAP. This review was accomplished by reviewing daily PER and Service
    Request (SR) reports, and periodically attending Corrective Action Review Board
    (CARB) and PER Screening Committee (PSC) meetings.
.2  Annual Follow-up of Selected Issues - Operations with a Potential for Draining the
    Reactor Vessel (OPDRVs)
a. Inspection Scope
    The inspectors reviewed the licensees response to the NRCs EMG-11-03, Enforcement
    Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee
    Noncompliance with Technical Specification Containment Requirements During
    Operations with a Potential for Draining the Reactor Vessel (OPDRVs). The inspectors
    focused on the changes made to licensee procedure 3-POI-200.5, Operations with
    Potential for Draining the Reactor Vessel/Cavity and discussed OPDRVs with
    Operations staff. The inspectors reviewed the Main Control Room (MCR) operating logs
    to verify OPDRVs were identified by the MCR operating crew and appropriate action
    taken were necessary. The inspectors also walked down portions of the alternate
    reactor water level control make-up and let-down line line-ups to verify they were
    established in accordance with the licensees procedures. Documents reviewed are
    listed in the Attachment. This activity constituted one in-depth selected issue.
b.  Assessment and Observations
    No findings were identified.
.3  Semiannual Review to Identify Trends
a.  Inspection Scope
    As required by Inspection Procedure 71152, the inspectors performed a review of the
    licensees CAP implementation and associated documents to identify trends that could
    indicate the existence of a more significant safety issue. The inspectors review included
    the results from daily screening of individual PERs (see Section 4OA2.1 above),
    licensee trend reports and trending efforts, and independent searches of the PER
    database and WO history. The inspectors review nominally considered the six-month
    period of January 2012 through June 2012, although some searches expanded beyond
                                                                                      Enclosure


On June 29, 2012, regional inspectors presented the results of the Emergency Preparedness inspection to Mr. S. Bono, General Manager Site Operations, and other members of the licensee's staff. On July 10, August 10 and 14th, 2012, the resident inspectors presented the results of the quarterly integrated onsite inspection to Mr. K. Polson, Site Vice President, and other members of the licensee's staff, who acknowledged the findings. All proprietary information reviewed by the inspectors as part of routine inspection activities were properly controlled, and subsequently returned to the licensee or disposed of appropriately.
                                        36
  these dates. Additionally, the inspectors review also included the Integrated Trend
  Reports (ITR) from the first and second quarters of fiscal year 2012. The licensee
  reports covered the period of October 1, 2011, to March 31, 2012. Furthermore, the
  inspectors verified that adverse or negative trends identified in the licensees PERs,
  periodic reports and trending efforts were entered into the CAP. Inspectors interviewed
  the appropriate licensee staff and also reviewed procedures, NPG-SPP-02.8, Integrated
  Trend Review and NPG-SPP-02.7, PER Trending.
  The purpose of the licensees integrated trend reviews was to identify the top site and
  departmental issues (gaps to excellence) requiring management attention. Other
  objectives were to provide status of the top issues and their progress to resolution,
  identify continuing issues, emerging trends and issues to be monitored, review progress
  towards resolving past top issues, review issues identified by external organizations
  such as the NRC, INPO, Nuclear Safety Review Board (NSRB), QA, etc., and determine
  why they were not identified by line organizations. This activity constituted one
  semiannual trend review inspection sample.
b. Findings and Observations
  No findings were identified, but the inspectors identified a number of observations as
  discussed below.
  Inspectors observed licensee-identified issues and trends in both the first and second
  quarter ITRs that were identical or similar in nature. Inspectors reviewed the repeat
  issues to assess the licensees progress of corrective actions associated with the issues
  and trends identified. Some of the more notable site/departmental issues were as
  follows:
  *    Corrective Action Program (CAP): The CAP has not been considered as a core
        business function by the station. Improvement is needed with problem identification,
        cause evaluations and timely completion of corrective actions. This issue was
        documented in PERs 346645 and 471366.
  *    Human Performance/Standards: Human performance practices resulted in
        consequential events, specifically: procedure use and adherence, procedure quality,
        accountability, human performance fundamentals, and the observation program.
        This issue was documented in PERs 410308 and 491985.
  *    Procedure Use and Adherence: The first quarter 2012 ITR included this in the
        Human Performance area (Issue #2) and developed actions to drive rigorous use of
        procedures throughout all organization. The second quarter 2012 ITR included this
        with the Procedure/Work Order Quality/Procedure Use and Adherence area (Issue
        #2). This issue was documented in PERs 410308 and 491985.
  The second quarter ITR contained fifteen fundamental problem statements that were
  developed as a result of the 95003 supplemental inspection. The process is intended to
  determine the root organizational and/or cultural causes of these issues. Corrective
  actions were under development for these fifteen problem areas at the end of the
  reporting period.
                                                                                    Enclosure


{{a|4OA7}}
                                            37
==4OA7 Licensee-Identified Violations==
    The inspectors conducted an independent review of the licensees CAP to identify
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which met the criteria of the NRC Enforcement Policy, for being dispositioned as a Non-Cited Violation:
    potential adverse trends. The inspectors identified a potential adverse trend with the
* A violation of Technical Specification 5.4.1.a was identified by the licensee for the failure to establish adequate work instructions to ensure proper installation of the gap setting between the actuator stem and valve stem of Unit 1 HPCI, (High Pressure Coolant Injection), turbine stop valve, 1-FCV-073-0018. On April 19, 2012, during the performance of a quarterly surveillance test the turbine stop valve, 1-FCV-073-0018, failed to close upon repeated demands. A Phase 3 analysis determined the significance of the finding was very low safety significance (Green) The regional Senior Reactor Analyst performed a Phase 3 SDP analysis on the finding. The risk was dominated by the unavailability of the HPCI during the repair time after discovery of the Stop Valve issue. The finding was determined to be GREEN in the SDP, primarily due to the short period of time it was fully non-functional. The licensee initiated PER 539040 to enter the issue into their corrective action program.
    licensees control of transient combustible materials in plant areas. A review of PERs
    from January 2012 to June 2012 revealed twelve PERs associated with transient and
    excessive combustible materials in plant areas however, a PER that identified this as a
    trend was not identified by the licensee staff. The inspectors discussed this issue with
    the appropriate licensee staff and PER 577382 was initiated to document this as an
    adverse trend.
4OA3 Event Follow-up
.1  Unit 3 Automatic Reactor Scram Following Refueling Outage
a.  Inspection Scope
    On May 22, 2012, while recovering from a refueling outage with control rod and main
    turbine generator off-line testing in progress, Unit 3 automatically scrammed from 19.5
    percent power. Unit 3 scrammed due to a loss of offsite power when an inadvertent
    actuation of 3A Unit Station Service Transformer (USST) differential relay 387SA
    resulted from an incorrect relay setting. Inspectors promptly responded to the control
    room and verified that the unit was stable in Mode 3 (Hot Shutdown), and confirmed that
    all safety-related mitigating systems had operated properly. Inspectors evaluated safety
    equipment and operator performance before and after the event by examining existing
    plant parameters, strip charts, plant computer historical data displays, operator logs, and
    the critical parameter trend charts used for the post-trip report. Inspectors also
    interviewed responsible on-shift operations personnel, examined the implementation of
    the applicable annunciator response procedures and abnormal operating instructions,
    including 3-AOI-100-1, Reactor Scram, and reviewed the written notification made in
    accordance with 10 CFR 50.72. Inspectors discussed the preliminary cause of the
    incorrect relay setting with responsible Operations and Engineering personnel and
    monitored Plant Oversight Review Committee (PORC) event review and restart
    meetings. This review included only initial event follow-up.
b.  Findings
    No findings were identified.
.2  Unit 3 Manual Reactor Scram Following Refueling Outage
a.  Inspection Scope
    On May 24, 2012, Unit 3 was manually scrammed from Mode 2 (less than 1% rated
    power) when operators ranged down the Intermediate Range Monitor (IRM) 'H'
    instrument, instead of up, resulting in half scram on Reactor Protection System (RPS) 'B'
    trip system. The half scram was being reset after IRM 'H' was properly ranged. As the
    operator adjusted the reset scram switch, a spike on IRM 'A' was received on the RPS
    'A' trip system, resulting in a partial rod insertion. When the operator identified multiple
                                                                                        Enclosure


=SUPPLEMENTAL INFORMATION=
                                          38
  rods inserting, the actions of the Reactor Scram Procedure, 3-AOI-l00-1, were followed
  and a manual scram was inserted. The inspectors evaluated safety equipment and
  operator performance before and after the event by examining existing plant parameters,
  strip charts, plant computer historical data displays, operator logs, the alarm typewriter
  Sequence of Events printout, and the critical parameter trend charts in the post-trip
  report. The inspectors interviewed responsible on-shift Operations personnel, examined
  the implementation of annunciator response and abnormal operating procedures,
  (including 3-AOI-100-1, Reactor Scram) and reviewed the written notification made in
  accordance with 10 CFR 50.72. This review included only initial event follow up.
b. Findings
  No findings were identified
.3 Unit 3 Automatic Reactor Scram and Forced Outage
a. Inspection Scope
  On May 29, 2012, Unit 3 automatically scrammed from 78 percent power due to a power
  to load unbalance (i.e., main generator load reject) automatic trip of the main turbine
  generator from an A-B phase trip of the main transformer differential relay 387T. The
  licensee identified the cause of the differential relay trip to be a B phase current
  transformer manufactured and installed with opposite polarity. Preliminarily, the licensee
  revealed that factory acceptance and field testing failed to detect the manufacturing
  defect of reverse polarity. Inspectors promptly responded to the control room and
  verified that the unit was stable in Mode 3 (Hot Shutdown), and confirmed that all safety-
  related mitigating systems had operated properly. Inspectors evaluated safety
  equipment and operator performance before and after the event by examining existing
  plant parameters, strip charts, plant computer historical data displays, operator logs, and
  the critical parameter trend charts used for the post-trip report. Inspectors also
  interviewed responsible on-shift operations personnel, examined the implementation of
  the applicable annunciator response procedures and abnormal operating instructions,
  including 3-AOI-100-1, Reactor Scram, and reviewed the written notification made in
  accordance with 10 CFR 50.72. Inspectors discussed the preliminary cause of the failed
  acceptance and installation testing with responsible Operations and Engineering
  personnel. This review included only initial event follow-up.
  Operators commenced restart of Unit 3 (i.e., entered Mode 2) on June 2 and achieved
  full power on June 6, 2011. During this short forced outage the inspectors examined the
  conduct of critical outage activities pursuant to technical specifications, applicable
  procedures, and the licensees risk assessment and maintenance plans. Some of the
  more significant outage activities monitored, examined and/or reviewed by the
  inspectors were as follows:
  *    Plant Oversight Review Committee (PORC) event review and restart meetings.
  *    Reactor startup and power ascension activities per 3-GOI-100-1A, Unit Startup
  *    Reactor vessel and coolant heatup per 3-SR-3.4.9.1(1), Reactor Heatup and
        Cooldown Rate Monitoring
                                                                                      Enclosure


==KEY POINTS OF CONTACT==
                                        39
Licensee
  *  Outage risk assessment and management
: [[contact::T. Adkins]], Manager EP Systems
  *  Control and management of forced outage and emergent work activities
: [[contact::S. Bono]], Plant General Manager Site Operations
  Corrective Action Program
: [[contact::C. Boschet]], QA Manager
  The inspectors reviewed PERs generated during the Unit 3 forced outage and attended
: [[contact::J. Boyer]], Acting Assistant Director of Engineering
  management review committee meetings to verify that initiation thresholds, priorities,
: [[contact::B. Bruce]], Acting Systems Engineering Manager
  mode holds, and significance levels were assigned as required.
: [[contact::D. Campbell]], SM 
b. Findings
: [[contact::S. Clement]], Operations Fire Protection
  No findings were identified
: [[contact::M. Durr]], Director of Engineering
.4 (Closed) Licensee Event Report (LER) 05000296/2011-003-00, Automatic Reactor
: [[contact::M. Ellet]], Maintenance Rule Coordinator
  Scram Due to a Main Turbine Generator Load Reject.
: [[contact::J. Emens]], Nuclear Site Licensing Manager
a. Inspection Scope
: [[contact::A. Feltman]], Emergency Preparedness Manager
  On September 28, 2011, Unit 3 automatically scrammed from 100 percent power due to
: [[contact::J. Ferguson]], Radiation Protection Support Superintendent
  a power to load unbalance (i.e., main generator load reject) automatic trip of the main
: [[contact::C. Gannon]], Plant Manager
  turbine generator (MTG) caused by a broken debris screen. The initial follow-up of this
: [[contact::H. Higgins]], Acting Licensed Operator Requalification Supervisor
  event by the inspectors was documented in Section 4OA3.10 of IR 05000296/2011004.
: [[contact::D. Hughes]], Operations Manager
  The inspectors reviewed the applicable LER that was issued on November 28, 2011,
: [[contact::S. Kelly]], Work Control Manager
  and its associated PER 440539, which included the root cause analysis (RCA) and
: [[contact::D. Kettering]], Electrical Systems Engineering Manager
  corrective actions. The licensee concluded that the direct cause of the Unit 3 turbine trip
: [[contact::J. Kimberlin]], FIN Manager
  and scram was the isolated-phase bus C debris screen failure.
: [[contact::R. King]], Design Engineering Manager
b. Findings
: [[contact::W. Lee]], Corporate EP Manager
  No findings were identified
: [[contact::R. Norris]], Radiation Protection Manager
.5 (Closed) Licensee Event Report (LER) 05000259,296 /2011-009-02, As-Found
: [[contact::S. Norris]], Engineering Supervisor
  Undervoltage Trip for the Reactor Protection System 1A1 Relay that Did Not Meet
: [[contact::P. Parker]], Site Security Manager
  Acceptance Criteria During Several Surveillances
: [[contact::J. Parshall]], Manager, EP Program Planning and Implementation
a. Inspection Scope
: [[contact::K. Polson]], Site Vice President
  The inspectors reviewed Revision 2 of LER 05000259/2011-009 dated April 25, 2012,
: [[contact::E. Quidley]], EDG Project Manager
  PER 486780, and the associated operability determination, and corrective action plans.
: [[contact::M. Rasmussen]], Operations Superintendent
  This revised LER was submitted to provide the results of the licensees completed
: [[contact::H. Smith]], Fire Protection Supervisor
  investigation and evaluation of a second Reactor Protection System (RPS) relay that did
: [[contact::R. Stowe]], Equipment Reliability Manager
  not meet its acceptance criteria during previous surveillance testing for the same reason.
: [[contact::P. Summers]], Director of Safety and Licensing
  The original LER 05000259/2011-009-00 dated December 5, 2011, the revised LER
: [[contact::J. Underwood]], Chemistry Manager
  05000259/2011-009-01 dated January 31, 2012, applicable PERs 413140 and 442914,
: [[contact::C. Vaughn]], Operations Superintendent
  including root cause analysis, operability determination and corrective action plans, were
: [[contact::S. Walton]], Electrical Maintenance Superintendent
  reviewed by the inspectors and documented in Sections 4OA3.1 and 4OA7 of NRC IR
: [[contact::M. Wilson]], Director of Training
                                                                                    Enclosure
: [[contact::A. Yarbrough]], BOP System Engineering Supervisor 


==LIST OF ITEMS==
                                          40
  05000259/2012002. As a result of this prior review, the licensee had identified one
  violation of NRC requirements associated with Unit 1 RPS 1A1 relay.
  On January 6, 2012, while performing an operability determination for the Unit 3 reactor
  protection system (RPS) 3C1 relay undervoltage trips, the licensee determined that the
  as-found undervoltage trip setpoint for the Unit 3 relay was less than the required
  acceptance criteria during several technical specification surveillances. Seven of the
  last thirteen surveillance test results were below the technical specification acceptance
  criteria. Therefore, based on performance history, the RPS 3C1 relay was determined to
  be inoperable from June 9, 2006, to February 2, 2012, when the relay was replaced.
  The licensee determined the previous root cause and corrective actions were applicable
  in that the surveillance test program did not require past operability reviews when out of
  calibration technical specification conditions were corrected during surveillances.
  The inspectors reviewed the second LER revision and verified that the supplemental
  information provided in the LER was complete and accurate and that the information
  was not of a significant nature to warrant any change to the original LER finding.
  This licensee identified violation constitutes an additional example as documented in
  NRC IR 05000259/2012002 and is not an individual non-cited violation. Further
  corrective actions for this additional example are expected to be taken in conjunction
  with corrective actions for the previous violation.
b. Findings
  One finding for the original and Revision 1 of the LER was previously identified in
  Section 4OA7 of NRC IR 05000259/2012002. No additional findings were identified.
  The revised LER is considered closed.
.6 (Closed) Licensee Event Report (LER) 05000296/2012-001-00, Annunciator Panel
  Power Supply Fire in Unit 3 Control Room
a. Inspection Scope
  On January 26, 2012, Unit 3 main control room operators smelled smoke and observed
  a flame coming from the bottom of an annunciator panel 3-XA-55-5A power supply. Fire
  Operations personnel arrived on the scene within five minutes. The affected circuit
  breaker was opened and fire extinguished within ten minutes. Operations personnel
  increased plant monitoring to compensate for indications that lost their alarming
  functions when the circuit breaker was opened. The fire damage was limited to the
  failed annunciator power supply and the power supply directly above it. The inspectors
  reviewed the details surrounding this event, interviewed operations and engineering
  personnel involved with this issue and reviewed the licensees apparent cause
  determination report. This was captured in the licensees corrective action program as
  problem event report (PER) 496592. This LER is closed.
                                                                                    Enclosure


===OPENED, CLOSED AND DISCUSSED===
                                          41
b. Findings
  Introduction: A self-revealing Green finding (FIN) was identified for the licensees failure
  to perform preventive maintenance on the Unit 3 Main Control Room (MCR) annunciator
  power supplies. As a result, a power supply failed which led to a fire in annunciator
  panel 3-XA-55-5A in the Unit 3 MCR.
  Description: On January 26, 2012, Unit 3 main control room operators smelled smoke
  and observed a flame coming from the bottom of an annunciator panel power supply.
  Within ten minutes, the Fire Brigade responded to the MCR and the circuit breaker was
  opened for the affected power supply which extinguished the fire. Damage was confined
  to two power supplies in annunciator panel 3-XA-55-5A. The damaged power supplies
  were replaced on January 27, 2012 in accordance with Work Order (WO) 113155456.
  Corrective action document PER 496592 identified the direct cause of the annunciator
  power supply failure as an overcurrent condition caused by a failed electrolytic capacitor.
  This PER referenced EPRI recommendations to change out components with electrolytic
  capacitors on a time based frequency. TVAs apparent cause concluded the power
  supply (capacitor), installed for thirty four (34) years, experienced an age related failure
  due to a lack of preventive maintenance.
  Age-related failures of electrolytic capacitors have been documented in the industry.
  Electric Power Research Institute (EPRI) document, TR-112175, Capacitor Application
  and Maintenance Guide, dated August 1999, stated that capacitor change outs are
  performed between 7 and 15 years depending on vendor recommendations and plant
  operating experience. Another EPRI document, Power Supply Maintenance and
  Application Guide (1003096), dated December 2001, stated that many of the power
  supplies that failed had been in service greater than 15 years on average. Since 2008
  three PERs have been entered in TVAs CAP that document similar failures of these
  annunciator power supplies on both Unit 2 and 3 main control room panels. PER
  391479 was initiated in June 2011 to evaluate the equipment reliability classification of
  these power supplies. Corrective actions to evaluate the annunciator power supply
  preventive maintenance strategy were in progress when the fire occurred.
  These power supplies were classified as Quality-Related, Non-Critical, Low Duty-Cycle,
  Mild Service Condition in accordance with licensee procedure NPG-SPP-09.18.2,
  Equipment Reliability Classification. Licensee procedure TVA-NQA-PLN89-A, Nuclear
  Quality Assurance Plan stated that the nuclear maintenance program including
  corrective and preventive maintenance shall ensure that quality-related structures,
  systems and components are maintained at a level sufficient to perform their intended
  functions.
  Analysis: The failure to perform preventive maintenance on the Unit 3 annunciator
  power supplies prior to their age related failure was a performance deficiency.
  Specifically, TVA procedure TVA-NQA-PLN89-A, Nuclear Quality Assurance Plan stated
  that the nuclear maintenance program including corrective and preventive maintenance
  shall ensure that quality-related structures, systems and components are maintained at
  a level sufficient to perform their intended functions. These power supplies were
  classified as Quality-Related according to TVA procedure NPG-SPP-09.18.2, Equipment
                                                                                      Enclosure


===Opened and Closed===
                                            42
: 05000259,260,296/2012-003-01 NCV Failure to Maintain Flood Barrier Results in Inoperable Safety Related Pumps (Section 1R15.
    Reliability Classification. As a result of the performance deficiency, a Unit 3 MCR
: 05000259,260,296/2012003-02 NCV Failure to Properly Prepare a DOT Type A Package for Transport) (Section 2RS8) 
    annunciator power supply was left in service for 34 years, failed due to an aged
: 05000259,260,296/2012003-03;  NCV Failure to Implement DOT Type A Package Closure Requirements) (Section 2RS8)
    electrolytic capacitor and resulted in an over-current related fire. The performance
: 05000260,296/2012003-04 FIN Failure to Establish Preventive Maintenance for Unit 2 and 3 Main Control Room Annunciator Power Supplies (Section 4OA3.6)  
    deficiency was determined to be more than minor because it was considered sufficiently
    similar to example 4.f of Inspection Manual Chapter (IMC) 0612, Appendix E, for an
    issue that resulted in a fire hazard in a safety-related area of the plant. The finding was
    associated with the Initiating Events Cornerstone and initially characterized according to
    IMC 0609, Significance Determination Process (SDP), Attachment 4, Phase 1 - Initial
    Screening and Characterization of Findings. The results of this analysis required a
    phase 3 evaluation in accordance with IMC 0609 because the finding increased the
    likelihood of and actually caused a fire in the Unit 3 MCR. The regional Senior Reactor
    Analyst performed a Phase 3 analysis for the issue. Pictures were provided to an NRC
    contractor who provides expertise in fire damage for the agency. It was determined that
    the configuration of the fire would not likely result in damage to anything of significance
    because the metal box that the annunciators power supplies are located in, would
    prevent propagation of the fire beyond the box. It is also unlikely that enough heat or
    smoke could be created to require control room evacuation, which would impact the
    human actions that would be performed to shut down the plant. Without an impact to
    additional plant equipment, or a major impact on human action failure rates, the finding
    was determined to be Green. The cause of this finding was related to the cross cutting
    aspect of Problem Identification in the Corrective Action Program component of the
    Problem Identification and Resolution area, because the licensee was aware of three
    previous failures of these power supplies in July 2009 and should have recognized that
    the electrolytic capacitors, installed beyond their recommended service life, required
    replacement prior to failure [P.1(a)].
    Enforcement: Enforcement action does not apply because the performance deficiency
    did not involve a violation of regulatory requirements since the main control room
    annunciator power supplies were not safety-related. Because the finding does not
    involve a violation, was entered into the licensees corrective action program as PER
    496592, and has very low safety significance, it is identified as FIN 05000296/2012003-
    04, Failure to Perform Preventive Maintenance on the Unit 3 Main Control Room
    Annunciator Power Supplies.
4OA6 Meetings, Including Exit
.1 Exit Meeting Summary
    On April 13, 2012, regional inspectors presented the results of the Occupational
    Radiation Safety inspection to Mr. P. Summers, Director Safety and Licensing, and other
    members of the licensees staff.
    On April 20, 2012, regional inspectors presented the results of the Unit 3 Inservice
    Inspection to members of the licensees staff.
    On June 22, 2012, regional inspectors presented the results of the Public Radiation
    Safety inspection to Mr. K. Polson, Site Vice President, and other members of the
    licensees staff, who acknowledged the findings. On July 03, 2012, regional inspectors
                                                                                        Enclosure


===Closed===
                                          43
: [[Closes LER::05000296/LER-2011-003]]-00  LER Automatic Reactor Scram Due to a Main Turbine Generator Load Reject (Section 4OA3.4)
    presented changes to the inspection results via telephone to Mr. S. Bono, General
: 05000259,296/2011-009-02  LER As-Found Undervoltage Trip for the Reactor Protection System 1A1 Relay that Did Not Meet Acceptance Criteria During Several Surveillances (Section 4OA3.5)
    Manager Site Operations, and other members of the licensees staff, who acknowledged
: [[Closes LER::05000296/LER-2012-001]]-00  LER Annunciator Panel Power Supply Fire in Unit 3 Control Room (Section 4OA3.6) 
    the changes.
===Discussed===
    On June 29, 2012, regional inspectors presented the results of the Emergency
None
    Preparedness inspection to Mr. S. Bono, General Manager Site Operations, and other
    members of the licensees staff.
    On July 10, August 10 and 14th, 2012, the resident inspectors presented the results of
    the quarterly integrated onsite inspection to Mr. K. Polson, Site Vice President, and other
    members of the licensees staff, who acknowledged the findings.
    All proprietary information reviewed by the inspectors as part of routine inspection
    activities were properly controlled, and subsequently returned to the licensee or
    disposed of appropriately.
4OA7 Licensee-Identified Violations
    The following violation of very low safety significance (Green) was identified by the
    licensee and is a violation of NRC requirements which met the criteria of the NRC
    Enforcement Policy, for being dispositioned as a Non-Cited Violation:
    *  A violation of Technical Specification 5.4.1.a was identified by the licensee for the
        failure to establish adequate work instructions to ensure proper installation of the gap
        setting between the actuator stem and valve stem of Unit 1 HPCI, (High Pressure
        Coolant Injection), turbine stop valve, 1-FCV-073-0018. On April 19, 2012, during
        the performance of a quarterly surveillance test the turbine stop valve, 1-FCV-073-
        0018, failed to close upon repeated demands. A Phase 3 analysis determined the
        significance of the finding was very low safety significance (Green) The regional
        Senior Reactor Analyst performed a Phase 3 SDP analysis on the finding. The risk
        was dominated by the unavailability of the HPCI during the repair time after
        discovery of the Stop Valve issue. The finding was determined to be GREEN in the
        SDP, primarily due to the short period of time it was fully non-functional. The
        licensee initiated PER 539040 to enter the issue into their corrective action program.
                                                                                      Enclosure


==LIST OF DOCUMENTS REVIEWED==
                                SUPPLEMENTAL INFORMATION
==Section 1R01: Adverse Weather Protection==
                                  KEY POINTS OF CONTACT
: 0-GOI-300-4, Switchyard Manual, Rev. 85 0-OI-30F, Common DG Building Ventilation, Rev. 30 0-OI-30F/ATT-1, Attachment 1 Valve Lineup Checklist, Rev. 28 0-OI-30F/ATT-1A, Attachment 1A Valve Lineup Checklist Unit 3, Rev. 28 0-OI-30F/ATT-2, Attachment 2 Panel Lineup Checklist, Rev. 29
Licensee
: LCEI-CI-C9, Procedure for Walkdown of Structures for Maintenance Rule, Rev. 5
T. Adkins, Manager EP Systems
: NPG-SPP-10.2, Clearance Procedure to Safely Control Energy, Rev. 3
S. Bono, Plant General Manager Site Operations
: OPDP-2, Switchyard Access and Switching Order Execution, Rev. 6
C. Boschet, QA Manager
: PER 390201, Concrete Piers in Switchyard Showing Signs of Degradation
J. Boyer, Acting Assistant Director of Engineering
: PER 534276, Conflicting information on 161-kv grid status during U3R15 outage
B. Bruce, Acting Systems Engineering Manager
: PER 536136, U3 Transformer Project Material Storage Area Poses U2 Concern
D. Campbell, SM
: PER 538016, Intake has no working ventilation fans
S. Clement, Operations Fire Protection
: PER 539365, Switchyard Deficiencies
M. Durr, Director of Engineering
: PER 539371, 500kV and 161kV Concrete Pedestals
M. Ellet, Maintenance Rule Coordinator
: PER 539580, Transformer Yard Discrepancies
J. Emens, Nuclear Site Licensing Manager
: PER 539581, Ground Soft in Transformer Yard
A. Feltman, Emergency Preparedness Manager
: PER 539582, Concrete Pedestal Degraded in Transformer Yard
J. Ferguson, Radiation Protection Support Superintendent
: PER 539583, Transformer Yard 500kV Tower Damaged
C. Gannon, Plant Manager
: PER 546871, Hot Weather procedure
H. Higgins, Acting Licensed Operator Requalification Supervisor
: PER 566119, Freeze protection heater still in place
D. Hughes, Operations Manager
: PER 568461, Hot weather procedure PSO
S. Kelly, Work Control Manager
: PER 546093, Transformer Yard 500 kV P.O. Structure Damage
D. Kettering, Electrical Systems Engineering Manager
: TRO-TO-SPP-30-128, Browns Ferry Nuclear Plant Grid Operating Guide, Rev. 13
J. Kimberlin, FIN Manager
: TVA-SPP-10.010, NERC Standard Compliance Processes Shared by TVA's Nuclear Power and Energy Delivery Organizations, Rev. 0
R. King, Design Engineering Manager
: UFSAR-8.4, Normal auxiliary Power System, Amendment 23
W. Lee, Corporate EP Manager
: WO 113419591, Hand switch stuck in slow position
R. Norris, Radiation Protection Manager
: WO110926526, Plant air wash pump
S. Norris, Engineering Supervisor
P. Parker, Site Security Manager
J. Parshall, Manager, EP Program Planning and Implementation
K. Polson, Site Vice President
E. Quidley, EDG Project Manager
M. Rasmussen, Operations Superintendent
H. Smith, Fire Protection Supervisor
R. Stowe, Equipment Reliability Manager
P. Summers, Director of Safety and Licensing
J. Underwood, Chemistry Manager
C. Vaughn, Operations Superintendent
S. Walton, Electrical Maintenance Superintendent
M. Wilson, Director of Training
A. Yarbrough, BOP System Engineering Supervisor
                                                                Attachment


==Section 1R04: Equipment Alignment==
                LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
: 0-47E861-1, Flow & Control Diagram Diesel Starting Air System Diesel Generator A, Rev. 17
Opened and Closed
: 0-OI-82/ATT-1A, Standby Diesel Generator A, Valve Lineup Checklist, Rev. 100 0-OI-82/ATT-2A, Standby Diesel Generator A, Panel Lineup Checklist, Rev. 100
05000259,260,296/2012-003-01  NCV  Failure to Maintain Flood Barrier Results in
: 0-OI-82/ATT-3A, Standby Diesel Generator A, Electrical Lineup Checklist, Rev. 100 0-OI-82/ATT-4A, Standby Diesel Generator A, Instrument Inspection Checklist, Rev. 101 1-OI-71, Reactor Core Isolation Cooling System, Rev. 14 1-OI-71/ATT-1, RCIC System, Valve Lineup Checklist, Rev. 13 1-OI-71/ATT-2, RCIC System, Panel Lineup Checklist, Rev. 13 1-OI-71/ATT-3, RCIC System, Electrical Lineup Checklist, Rev. 13 3-OI-74, Residual Heat Removal System, Revision 0104
                                    Inoperable Safety Related Pumps (Section 1R15.)
: 3-OI-74/ATT-1, Valve Lineup Checklist Unit 3, Revision 0086 3-OI-74/ATT-2, Panel Lineup Checklist, Revision 0086 3-OI-74/ATT-3, Electrical Lineup Checklist, Revision 0087 DWG 1-47E813-1, Flow Diagram RCIC System, Rev. 33
05000259,260,296/2012003-02    NCV  Failure to Properly Prepare a DOT Type A Package
: Attachment Technical Requirements Manual Section 3.5.3, Equipment Area Coolers Technical Requirements Manual Section 3.5.4, Maintenance of Filled Discharge Piping Updated Final Safety Report Section 4.8, Residual Heat Removal System
                                    for Transport) (Section 2RS8)
05000259,260,296/2012003-03;  NCV  Failure to Implement DOT Type A Package Closure
                                    Requirements) (Section 2RS8)
05000260,296/2012003-04        FIN  Failure to Establish Preventive Maintenance for
                                    Unit 2 and 3 Main Control Room Annunciator
                                    Power Supplies (Section 4OA3.6)
Closed
05000296/2011-003-00          LER  Automatic Reactor Scram Due to a Main Turbine
                                    Generator Load Reject (Section 4OA3.4)
05000259,296/2011-009-02      LER  As-Found Undervoltage Trip for the Reactor
                                    Protection System 1A1 Relay that Did Not Meet
                                    Acceptance Criteria During Several Surveillances
                                    (Section 4OA3.5)
05000296/2012-001-00          LER  Annunciator Panel Power Supply Fire in Unit 3
                                    Control Room (Section 4OA3.6)
Discussed
None
                                                                            Attachment


==Section 1R05: Fire Protection==
                              LIST OF DOCUMENTS REVIEWED
: 0-SI-4.11.E.1.B(2), Safety Related Fire Hose Replacement, Rev 08 0-SI-4.11.E.1.B(2)/ATT-1, Attachment 1 Fire Hose Replacement Data Sheet, Rev. 08 0-TI-470, Temporary Wiring And Electrical Equipment (600 Volt Or Less), Rev. 1 Active FPIP's dated 5/1/2012
Section 1R01: Adverse Weather Protection
: Active FPIP's List, 06/01/2012 DWG 0-47W216-51, Fire Protection - 10
0-GOI-300-4, Switchyard Manual, Rev. 85
: CFR 50 Appendix R, Fire Area Compartmentation and Zone Drawings, Rev. 7 DWG 0-47W216-56, Fire Protection - 10
0-OI-30F, Common DG Building Ventilation, Rev. 30
: CFR 50 Appendix R, Fire Area Compartmentation and Zone Drawings, Plan
0-OI-30F/ATT-1, Attachment 1 Valve Lineup Checklist, Rev. 28
: EL 593.0 & 586.0, Rev. 7 Fire Hazard Analysis Fire Zone 3-3 Fire Protection Report Vol. 1, Fire Hazards Analysis, Rev. 11
0-OI-30F/ATT-1A, Attachment 1A Valve Lineup Checklist Unit 3, Rev. 28
: Fire Protection Report Vol. 2, Rev. 48 Fire Protection Report, Volume 1, Section 2, Fire Hazards Analysis, Rev. 11 Fire Protection Report, Volume 2, Section IV, Pre-Plan No.
0-OI-30F/ATT-2, Attachment 2 Panel Lineup Checklist, Rev. 29
: RX2-519 Torus Area and HPCI Room Fire Protection Report, Volume 2, Section IV, Pre-Plan No.
LCEI-CI-C9, Procedure for Walkdown of Structures for Maintenance Rule, Rev. 5
: RX2-519 NW
NPG-SPP-10.2, Clearance Procedure to Safely Control Energy, Rev. 3
: Fire Protection Report, Volume 2, Section IV, Pre-Plan No.
OPDP-2, Switchyard Access and Switching Order Execution, Rev. 6
: RX2-519 SW Fire Protection Report, Volume 2, Section IV, Pre-Plan No.
PER 390201, Concrete Piers in Switchyard Showing Signs of Degradation
: RX2-565
PER 534276, Conflicting information on 161-kv grid status during U3R15 outage
: FP-0-000-INS001(A), Inspection of Portable and Wheel Type Fire Extinguisher Stations (Reactor Building), Rev. 17
PER 536136, U3 Transformer Project Material Storage Area Poses U2 Concern
: FP-0-000-INS001(A)/ATT-2, Attachment 2 Inspection Check/Data Sheet Dry Chemical (12 yrs) Co2 (5 yrs) Halon (12 yrs) Charging Cylinder (5 yrs), Rev. 17
PER 538016, Intake has no working ventilation fans
: FP-0-000-INS012, Fire Watch Expectations, Rev. 1
PER 539365, Switchyard Deficiencies
: FP-0-000-INS019, Fire Protection Weekly Inspection, Rev. 13
PER 539371, 500kV and 161kV Concrete Pedestals
: NPG-SPP-09.17, Temporary Equipment Control, Rev. 1
PER 539580, Transformer Yard Discrepancies
: NPG-SPP-18.4.6, Control of Fire Protection Impairments, Rev. 0
PER 539581, Ground Soft in Transformer Yard
: PER 545547, Room on 1C Hallway Contain Excessive Combustibles
PER 539582, Concrete Pedestal Degraded in Transformer Yard
: PER 546065, Multiple Extension Cords Plugged Into One Another on 1C Hallway
PER 539583, Transformer Yard 500kV Tower Damaged
: PER 546188, Roving Fire Watch Route Sheet Pre-Fire Plan for Browns Ferry Nuclear Plant - Reactor Building Unit 3, pre-plan No.
PER 546871, Hot Weather procedure
: RX3-593 Pre-Fire Plan for Browns Ferry Nuclear Plant - Reactor Building Unit 3, pre-plan No.
PER 566119, Freeze protection heater still in place
: RX3-565
PER 568461, Hot weather procedure
: TVA Safety Manual Chapter 2, Procedure 1004, Extension Cords and Attachments, Rev. 4
PSO PER 546093, Transformer Yard 500 kV P.O. Structure Damage
TRO-TO-SPP-30-128, Browns Ferry Nuclear Plant Grid Operating Guide, Rev. 13
TVA-SPP-10.010, NERC Standard Compliance Processes Shared by TVA's Nuclear Power and
  Energy Delivery Organizations, Rev. 0
UFSAR-8.4, Normal auxiliary Power System, Amendment 23
WO 113419591, Hand switch stuck in slow position
WO110926526, Plant air wash pump
Section 1R04: Equipment Alignment
0-47E861-1, Flow & Control Diagram Diesel Starting Air System Diesel Generator A, Rev. 17
0-OI-82/ATT-1A, Standby Diesel Generator A, Valve Lineup Checklist, Rev. 100
0-OI-82/ATT-2A, Standby Diesel Generator A, Panel Lineup Checklist, Rev. 100
0-OI-82/ATT-3A, Standby Diesel Generator A, Electrical Lineup Checklist, Rev. 100
0-OI-82/ATT-4A, Standby Diesel Generator A, Instrument Inspection Checklist, Rev. 101
1-OI-71, Reactor Core Isolation Cooling System, Rev. 14
1-OI-71/ATT-1, RCIC System, Valve Lineup Checklist, Rev. 13
1-OI-71/ATT-2, RCIC System, Panel Lineup Checklist, Rev. 13
1-OI-71/ATT-3, RCIC System, Electrical Lineup Checklist, Rev. 13
3-OI-74, Residual Heat Removal System, Revision 0104
3-OI-74/ATT-1, Valve Lineup Checklist Unit 3, Revision 0086
3-OI-74/ATT-2, Panel Lineup Checklist, Revision 0086
3-OI-74/ATT-3, Electrical Lineup Checklist, Revision 0087
DWG 1-47E813-1, Flow Diagram RCIC System, Rev. 33
                                                                                  Attachment


==Section 1R07: Annual Heat Sink Performance==
                                            4
: 0-TI-322, RHR Heat Exchanger Performance Testing, Rev. 0 0-TI-364, ASME Section XI System Pressure Tests, Rev. 6 0-TI-389, Raw Water Fouling and Corrosion Control, Rev. 16 0-TI-522, Program for Implementing NRC Generic Letter 89-13, Rev. 1
Technical Requirements Manual Section 3.5.3, Equipment Area Coolers
: 0-TI-63, RHRSW Flow Blockage Monitoring, Rev. 25 DCN T38580A, Repair 3A and 3C RHR Heat Exchanger Flange Leaks Using Furmanite Sealing Compound, Rev. A DWG 0-47E452-1, Mechanical Residual Heat Removal System, Rev. 15 DWG 3-47W452-10, Mechanical Residual Heat Removal System, Rev. 15 
Technical Requirements Manual Section 3.5.4, Maintenance of Filled Discharge Piping
: Attachment
Updated Final Safety Report Section 4.8, Residual Heat Removal System
: DWG 69-D-160-03, Tube Sheet Details, Rev. 6
Section 1R05: Fire Protection
: EDC 69311A, Repair of 3B and 3D RHR Heat Exchanger Flange Leaks, Rev. A EPRI
0-SI-4.11.E.1.B(2), Safety Related Fire Hose Replacement, Rev 08
: NP-7552, Heat Exchanger Performance Monitoring Guidelines, Dec. 1991 Evaluation of Temporary Sealing Compound used as a replacement gasket, Dated 5/8/2012
0-SI-4.11.E.1.B(2)/ATT-1, Attachment 1 Fire Hose Replacement Data Sheet, Rev. 08
: MCI-0-000-LKS001, On-Line leak Sealing, Rev. 15
0-TI-470, Temporary Wiring And Electrical Equipment (600 Volt Or Less), Rev. 1
: MCI-0-074-HEX001, Maintenance of RHR Heat Exchangers, Rev. 23
Active FPIPs dated 5/1/2012
: NPG-SPP-09.7, Corrosion Control Program, Rev. 2 N-VT-4, System Pressure Test Visual Examination Procedure, Rev. 23 P.S. 4.M.4.3 (R4), General Engineering Specification, G-29B, Online Leak Sealing, Rev. 4
Active FPIPs List, 06/01/2012
: PER 543035, Temporary Furmanite repairs on RHR HX 3A, 3C, and 3D are not being tracked
DWG 0-47W216-51, Fire Protection - 10 CFR 50 Appendix R, Fire Area Compartmentation and
: PM 500103065, Inspect / Clean RHRSW Pump Pit
    Zone Drawings, Rev. 7
: PM 500108601, PM Performance of 0-TI-63, RHRSW Flow Blockage Monitoring, for
DWG 0-47W216-56, Fire Protection - 10 CFR 50 Appendix R, Fire Area Compartmentation and
: 1-HEX-74-900A & C.
    Zone Drawings, Plan EL 593.0 & 586.0, Rev. 7
: PM 500116540, PM Performance of 0-TI-63 for 2-HEX-74-900A and 2-HEX-74-900C
Fire Hazard Analysis Fire Zone 3-3
: PM 500116541, PM Performance of
Fire Protection Report Vol. 1, Fire Hazards Analysis, Rev. 11
: TI-63 for 2-HEX-74-900B and 2-HEX-74-900D
Fire Protection Report Vol. 2, Rev. 48
: PM 500126928, Clean
Fire Protection Report, Volume 1, Section 2, Fire Hazards Analysis, Rev. 11
: BFN-3-HEX -074-0900A Heat Exchanger
Fire Protection Report, Volume 2, Section IV, Pre-Plan No. RX2-519 Torus Area and HPCI
: PM 500126929, PM Performance of 0-TI-63, RHRSW Flow Blockage Monitoring, for
    Room
: 3-HEX-74-900A & C
Fire Protection Report, Volume 2, Section IV, Pre-Plan No. RX2-519 NW
: PM 500126931, Clean
Fire Protection Report, Volume 2, Section IV, Pre-Plan No. RX2-519 SW
: BFN-3-HEX -074-0900B Heat Exchanger
Fire Protection Report, Volume 2, Section IV, Pre-Plan No. RX2-565
: PM 500126932, PM Performance of 0-TI-63 for 3-HEX-74-900B and 3-HEX-74-900D.
FP-0-000-INS001(A), Inspection of Portable and Wheel Type Fire Extinguisher Stations
: PM 500126933, Disassemble, Clean, Inspect
    (Reactor Building), Rev. 17
: BFN-3-HEX -074-0900C
FP-0-000-INS001(A)/ATT-2, Attachment 2 Inspection Check/Data Sheet Dry Chemical (12 yrs)
: PM 500126935, Disassemble, Clean, Inspect
    Co2 (5 yrs) Halon (12 yrs) Charging Cylinder (5 yrs), Rev. 17
: BFN-3-HEX -074-0900D.
FP-0-000-INS012, Fire Watch Expectations, Rev. 1
: PM 500133228, PM Perform
FP-0-000-INS019, Fire Protection Weekly Inspection, Rev. 13
: TI-63 for 1-HEX-74-0900B and D
NPG-SPP-09.17, Temporary Equipment Control, Rev. 1
: WO 08-712116, Repair Leak, 3D RHR Heat Exchanger
NPG-SPP-18.4.6, Control of Fire Protection Impairments, Rev. 0
: WO 112857671, Test RHR Heat Exchanger 3A and 3C
PER 545547, Room on 1C Hallway Contain Excessive Combustibles
: WO 95-20541-000 (3A and 3C)
PER 546065, Multiple Extension Cords Plugged Into One Another on 1C Hallway
PER 546188, Roving Fire Watch Route Sheet
Pre-Fire Plan for Browns Ferry Nuclear Plant - Reactor Building Unit 3, pre-plan No. RX3-593
Pre-Fire Plan for Browns Ferry Nuclear Plant - Reactor Building Unit 3, pre-plan No. RX3-565
TVA Safety Manual Chapter 2, Procedure 1004, Extension Cords and Attachments, Rev. 4
Section 1R07: Annual Heat Sink Performance
0-TI-322, RHR Heat Exchanger Performance Testing, Rev. 0
0-TI-364, ASME Section XI System Pressure Tests, Rev. 6
0-TI-389, Raw Water Fouling and Corrosion Control, Rev. 16
0-TI-522, Program for Implementing NRC Generic Letter 89-13, Rev. 1
0-TI-63, RHRSW Flow Blockage Monitoring, Rev. 25
DCN T38580A, Repair 3A and 3C RHR Heat Exchanger Flange Leaks Using Furmanite Sealing
    Compound, Rev. A
DWG 0-47E452-1, Mechanical Residual Heat Removal System, Rev. 15
DWG 3-47W452-10, Mechanical Residual Heat Removal System, Rev. 15
                                                                                    Attachment


==Section 1R11: Licensed Operator Requalification==
                                          5
: 2-AOI-57-5B, Loss of Instrument & Control Bus 2-AOI-70-1, Loss of Reactor Building Closed Cooling Water 2-C-5, Level/Power Control 2-EOI-1, Reactor Pressure Vessel Control
DWG 69-D-160-03, Tube Sheet Details, Rev. 6
EDC 69311A, Repair of 3B and 3D RHR Heat Exchanger Flange Leaks, Rev. A
EPRI NP-7552, Heat Exchanger Performance Monitoring Guidelines, Dec. 1991
Evaluation of Temporary Sealing Compound used as a replacement gasket, Dated 5/8/2012
MCI-0-000-LKS001, On-Line leak Sealing, Rev. 15
MCI-0-074-HEX001, Maintenance of RHR Heat Exchangers, Rev. 23
NPG-SPP-09.7, Corrosion Control Program, Rev. 2
N-VT-4, System Pressure Test Visual Examination Procedure, Rev. 23
P.S. 4.M.4.3 (R4), General Engineering Specification, G-29B, Online Leak Sealing, Rev. 4
PER 543035, Temporary Furmanite repairs on RHR HX 3A, 3C, and 3D are not being tracked
PM 500103065, Inspect / Clean RHRSW Pump Pit
PM 500108601, PM Performance of 0-TI-63, RHRSW Flow Blockage Monitoring, for
  1-HEX-74-900A & C.
PM 500116540, PM Performance of 0-TI-63 for 2-HEX-74-900A and 2-HEX-74-900C
PM 500116541, PM Performance of TI-63 for 2-HEX-74-900B and 2-HEX-74-900D
PM 500126928, Clean BFN-3-HEX -074-0900A Heat Exchanger
PM 500126929, PM Performance of 0-TI-63, RHRSW Flow Blockage Monitoring, for
  3-HEX-74-900A & C
PM 500126931, Clean BFN-3-HEX -074-0900B Heat Exchanger
PM 500126932, PM Performance of 0-TI-63 for 3-HEX-74-900B and 3-HEX-74-900D.
PM 500126933, Disassemble, Clean, Inspect BFN-3-HEX -074-0900C
PM 500126935, Disassemble, Clean, Inspect BFN-3-HEX -074-0900D.
PM 500133228, PM Perform TI-63 for 1-HEX-74-0900B and D
WO 08-712116, Repair Leak, 3D RHR Heat Exchanger
WO 112857671, Test RHR Heat Exchanger 3A and 3C
WO 95-20541-000 (3A and 3C)
Section 1R11: Licensed Operator Requalification
2-AOI-57-5B, Loss of Instrument & Control Bus
2-AOI-70-1, Loss of Reactor Building Closed Cooling Water
2-C-5, Level/Power Control
2-EOI-1, Reactor Pressure Vessel Control
Section 1R12: Maintenance Effectiveness
0-AOI-100-3, Flood Above Elevation 558, Rev. 35
0-AOI-100-3, Flood Above Elevation 558, Rev. 35
0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting -
  10CFR50.65, Rev. 37
0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -
      10CFR50.65, Rev. 37
Cause Determination Evaluation 1041, May 31, 2011
Design Criteria BFN-50-7023, Residual Heat Removal Service Water (RHRSW) System
Design Criteria BFN-50-7067, Emergency Equipment Cooling Water (EECW) System
Design Criteria BFN-50-C-7101, Protection from Wind, Tornado Wind, Tornado
      Depressurization, Tornado Generated Missiles, and External Flooding
FSAR Section 10.10, Emergency Equipment Cooling Water (EECW) System, BFN-24
FSAR Section 10.9, RHR Service Water System, BFN-24
FSAR Section 10.9, RHR Service Water System, BFN-24
                                                                                  Attachment


==Section 1R12: Maintenance Effectiveness==
                                          6
: 0-AOI-100-3, Flood Above Elevation 558', Rev. 35
FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,
: 0-AOI-100-3, Flood Above Elevation 558', Rev. 35 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting - 10CFR50.65, Rev. 37 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting - 10CFR50.65, Rev. 37 Cause Determination Evaluation 1041, May 31, 2011 Design Criteria
        BFN-24
: BFN-50-7023, Residual Heat Removal Service Water (RHRSW) System Design Criteria
FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,
: BFN-50-7067, Emergency Equipment Cooling Water (EECW) System Design Criteria
        BFN-24
: BFN-50-C-7101, Protection from Wind, Tornado Wind, Tornado Depressurization, Tornado Generated Missiles, and External Flooding FSAR Section 10.10, Emergency Equipment Cooling Water (EECW) System,
FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology, BFN-24
: BFN-24 FSAR Section 10.9, RHR Service Water System,
FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology, BFN-24
: BFN-24
MCI-0-023-PMP002, Maintenance of EECW and RHRSW Pumps, Rev. 52
: FSAR Section 10.9, RHR Service Water System,
MCI-0-023-PMP003, Emergency Equipment Cooling Water and Residual Heat Removal Service
: BFN-24 
        Water Pump Removal and Installation, Rev. 12
: Attachment FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,
MCI-0-023-PMP004, EECW and RHRSW Pump Impeller Adjustment, Rev. 05 and 06
: BFN-24 FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,
MPI-0-260-DRS001, Inspection and Maintenance of Doors
: BFN-24 FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology,
NPG-SPP-03.4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting -
: BFN-24 FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology,
  10CFR50.65, Rev. 0
: BFN-24
NPG-SPP-06.10, NPG Fix It Now (FIN) Team Process, Rev. 0
: MCI-0-023-PMP002, Maintenance of EECW and RHRSW Pumps, Rev. 52
NPG-SPP-07.1, On-Line Work Management, Rev. 05
: MCI-0-023-PMP003, Emergency Equipment Cooling Water and Residual Heat Removal Service Water Pump Removal and Installation, Rev. 12
PER 234151, Unit 2 IRM scram signal
: MCI-0-023-PMP004, EECW and RHRSW Pump Impeller Adjustment, Rev. 05 and 06
PER 310544, Gaps in A and D RHRSW Pump Room Flood Doors
: MPI-0-260-DRS001, Inspection and Maintenance of Doors
PER 383975, Reliability of RHRSW Pump Room Door Seals
: NPG-SPP-03.4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting - 10CFR50.65, Rev. 0
PER 402414, IRM (a)(1) plan
: NPG-SPP-06.10, NPG Fix It Now (FIN) Team Process, Rev. 0
PER 469640, BFN-0-DOOR-260-C-RHRSW, Aggregate Impact of RHRSW Pump Room Doors
: NPG-SPP-07.1, On-Line Work Management, Rev. 05
PER 470350, BFN-0-DOOR-260-C-RHRSW May Not Seal
: PER 234151, Unit 2 IRM scram signal
PER 481145, B and D RHRSW Pump Room Watertight Doors Were Found Closed and Locked,
: PER 310544, Gaps in A and D RHRSW Pump Room Flood Doors
        But Not Mechanically Restrained
: PER 383975, Reliability of RHRSW Pump Room Door Seals
PER 482838, RHRSW B Pump Room Door Failed Chalk Test
: PER 402414, IRM (a)(1) plan
PER 482867, RHRSW D Pump Room Door Failed Chalk Test
: PER 469640,
PER 524957, Review past 48 months of IRM data for MR failures.
: BFN-0-DOOR-260-C-RHRSW, Aggregate Impact of RHRSW Pump Room Doors
PER 532050, NRC Identified C3 EECW Pump Foundation Hole Flood Protection Cover
: PER 470350,
        Inadequately Installed
: BFN-0-DOOR-260-C-RHRSW May Not Seal
PER 546734, Lack of specified torque value for pump coupling bolts
: PER 481145, B and D RHRSW Pump Room Watertight Doors Were Found Closed and Locked, But Not Mechanically Restrained
PER 561666, NRC Walkdown Identified RHRSW Door Issues
: PER 482838, RHRSW B Pump Room Door Failed Chalk Test
PER 563567, Site Tolerance of Degraded/Nonconforming Issue
: PER 482867, RHRSW D Pump Room Door Failed Chalk Test
PER 563727, RHRSW Intake Structure Doors Have Not Been Evaluated for MR (a)(1)
: PER 524957, Review past 48 months of IRM data for MR failures.
PER 566123, Document Former NRC Senior Resident Observation
: PER 532050, NRC Identified C3 EECW Pump Foundation Hole Flood Protection Cover Inadequately Installed
Plant Level Event Data from Mar. 2010 to Feb. 2012
: PER 546734, Lack of specified torque value for pump coupling bolts
SR 565020, Inaccurate Past Operability Due to CAP Input
: PER 561666, NRC Walkdown Identified RHRSW Door Issues
SR 568840, NRC Identified - Failure to Accurately Document NRC Observations in CAP
: PER 563567, Site Tolerance of Degraded/Nonconforming Issue
SR 569912, Inconsistency in Flood Cover Description Between Maintenance Procedures
: PER 563727, RHRSW Intake Structure Doors Have Not Been Evaluated for MR (a)(1)
Technical Specification and Basis 3.7.1 Residual Heat Removal Service Water (RHRSW)
: PER 566123, Document Former NRC Senior Resident Observation Plant Level Event Data from Mar. 2010 to Feb. 2012
        System, Amendment 234
: SR 565020, Inaccurate Past Operability Due to CAP Input
Technical Specification and Basis 3.7.2 Emergency Equipment Cooling Water (EECW) System
: SR 568840, NRC Identified - Failure to Accurately Document NRC Observations in CAP
        and Ultimate Heat Sink (UHS), Amendment 234
: SR 569912, Inconsistency in Flood Cover Description Between Maintenance Procedures Technical Specification and Basis 3.7.1 Residual Heat Removal Service Water (RHRSW) System, Amendment 234 Technical Specification and Basis 3.7.2 Emergency Equipment Cooling Water (EECW) System and Ultimate Heat Sink (UHS), Amendment 234 U1,2,3 Maintenance Rule Data from Nov. 2009 to Feb. 2012 Units 1,2,3 System 092 (IRMs) Health Reports from 10/1/2011 to 1/31/2012  
U1,2,3 Maintenance Rule Data from Nov. 2009 to Feb. 2012
: Unplanned Scram Data from Mar. 2010 to Feb. 2012
Units 1,2,3 System 092 (IRMs) Health Reports from 10/1/2011 to 1/31/2012
: WO 111457995, Repair
Unplanned Scram Data from Mar. 2010 to Feb. 2012
: BFN-0-DOOR-260-C-RHRSW
WO 111457995, Repair BFN-0-DOOR-260-C-RHRSW
: WO 111835839, D RHRSW Upper Dog Catching and Missing Dog
WO 111835839, D RHRSW Upper Dog Catching and Missing Dog
: WO 111926930, B RHRSW Dogs Lower Linkage Disconnected
WO 111926930, B RHRSW Dogs Lower Linkage Disconnected
: WO 112744581, C3 EECW Pump Vibes in Alert, Troubleshoot and Repair Attachment
WO 112744581, C3 EECW Pump Vibes in Alert, Troubleshoot and Repair
: WO 112972845, Impeller gap adjustment of A3 EECW pump
                                                                                Attachment
: WO 113062982, Repair
: BFN-0-DOOR-260-B-RHRSW
: WO 113062984, Repair
: BFN-0-DOOR-260-D-RHRSW
: WO 113228273, Why is A RHRSW Door Locked - Door Doesn't Fully Close
: WO 113348314, C RHRSW Lower Left Dragging and Scraping Metal
: WO 113446620, Performance of 3-SI-4.5.C.1(2) - EECW Pump Operation
: WO 113456059, Raw Cooling Water Leak on 3B CRD Pump
: WO 113474206, Performance of 3-SI-4.5.C.1(2) - EECW Pump Operation
: WO 113475937, 'D' Diesel Generator came up to 500 rpm
: WO 113483626, Troubleshoot
: BFN-0-RLY-082-D/ALM
: WO 113486500, Diesel Generator 'D' Air Pressure Alarm Relay


==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
                                          7
: 1-OI-73, High Pressure Coolant Injection System, Rev. 22  
WO 112972845, Impeller gap adjustment of A3 EECW pump
: 1-SR-3.3.3.1.4(G), Verification of Remote Position Indicators for HPCI System Valves, Rev. 2 1-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated Reactor Pressure, Rev. 21 BFN Unit 3 Defense in Depth Assessment May 4, 2012 BFN Unit 3 Defense in Depth Assessment, April 15, 16, 17, 18, 2012
WO 113062982, Repair BFN-0-DOOR-260-B-RHRSW
: BFN-ODM-4.18, Protected Equipment, Rev. 6 Browns Ferry Nuclear Plant Outage Risk Assessment Report, Unit 3 Cycle R15, Rev. 1 DWG 1-47E812-1, Rev. 34
WO 113062984, Repair BFN-0-DOOR-260-D-RHRSW
: DWG 68-XC-71, Schutte & Koerting Co. Manufacturing Drawing  
WO 113228273, Why is A RHRSW Door Locked - Door Doesnt Fully Close
: EOOS Report, Unit 2, dated May 7, 2012
WO 113348314, C RHRSW Lower Left Dragging and Scraping Metal
: MCI-0-073-VLV001, HPCI Turbine Stop Valve -
WO 113446620, Performance of 3-SI-4.5.C.1(2) - EECW Pump Operation
: FCV 73-18 Disassembly, Inspection, Rework and Reassembly, Revs. 12, 13
WO 113456059, Raw Cooling Water Leak on 3B CRD Pump
: MSI-1-073-GOV001, HPCI Turbine Overspeed Trip Test, Rev. 7
WO 113474206, Performance of 3-SI-4.5.C.1(2) - EECW Pump Operation
: NPG-SPP-7.0, Work Management
WO 113475937, D Diesel Generator came up to 500 rpm
: NPG-SPP-07.1, On Line Work Management, Rev. 5
WO 113483626, Troubleshoot BFN-0-RLY-082-D/ALM
: NPG-SPP-07.2, Outage Management, Rev. 2
WO 113486500, Diesel Generator D Air Pressure Alarm Relay
: NPG-SPP-07.2.11, Shutdown Risk Management, Rev. 2
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
: NPG-SPP-07.2.11, Shutdown Risk Management, Rev. 2
1-OI-73, High Pressure Coolant Injection System, Rev. 22
: NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 07
1-SR-3.3.3.1.4(G), Verification of Remote Position Indicators for HPCI System Valves, Rev. 2
: NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 7
1-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated
: NPG-SPP-09.11, Probabilistic Risk Assessment (PRA) Program, Rev. 01
  Reactor Pressure, Rev. 21
: NPG-SPP-09.11.1, Equipment Out of Service (EOOS) Management, Rev. 04
BFN Unit 3 Defense in Depth Assessment May 4, 2012
: NPG-SPP-7.2.11, Shutdown Risk Management, Rev. 2 ORAM Model Change Form, April 18, 2012 ORAM Sentinel Outage Safety Assessment, April 18, 2012  
BFN Unit 3 Defense in Depth Assessment, April 15, 16, 17, 18, 2012
: O-TI-367 Outage Risk Assessment Report, U3 Cycle R15, Rev. 1
BFN-ODM-4.18, Protected Equipment, Rev. 6
: PER 539040, HPCI Turbine Stop Valve Failed to Trip
Browns Ferry Nuclear Plant Outage Risk Assessment Report, Unit 3 Cycle R15, Rev. 1
: PER 539556, HPCI Turbine Main Pump Vibration
DWG 1-47E812-1, Rev. 34
: PER 541156, HPCI Oil Tank Level Low
DWG 68-XC-71, Schutte & Koerting Co. Manufacturing Drawing
: PER 541727, HPCI Gland Exhauster Pump Breaker
EOOS Report, Unit 2, dated May 7, 2012
: PER 547134, Shutdown Risk Management, Filling out DID Checklist Once per 24 Hours
MCI-0-073-VLV001, HPCI Turbine Stop Valve - FCV 73-18 Disassembly, Inspection, Rework
: PMT-0-000-MEC001, Leak Checks on Tube Fitting, Threaded, Flanged, Bolted or Welded Connections, Rev. 7
  and Reassembly, Revs. 12, 13
: Attachment
MSI-1-073-GOV001, HPCI Turbine Overspeed Trip Test, Rev. 7
: SR 541069, Adjust Sensitivity on Incipient Fire Detector U3 ORAM Safety Function Status Report, dated May 5, 2012
NPG-SPP-7.0, Work Management
: WO 113426235, HPCI Turbine Stop Valve Failed to Trip
NPG-SPP-07.1, On Line Work Management, Rev. 5
: WO 113426235, HPCI Turbine Stop Valve PMT Step Text
NPG-SPP-07.2, Outage Management, Rev. 2
: WO 113429679, Task 10: 1-FCV-073-0018, Rev. 0
NPG-SPP-07.2.11, Shutdown Risk Management, Rev. 2
: WO 113435872, HPCI Main & Booster Pump Head & Flow Rate Test
NPG-SPP-07.2.11, Shutdown Risk Management, Rev. 2
: WO 113440357, HPCI Oil Tank Level Low
NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 07
: WO 113441055, Verification of Remote Position Indicators
NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 7
: WO 113445422, Adjust Sensitivity on Incipient Fire Detector
NPG-SPP-09.11, Probabilistic Risk Assessment (PRA) Program, Rev. 01
NPG-SPP-09.11.1, Equipment Out of Service (EOOS) Management, Rev. 04
NPG-SPP-7.2.11, Shutdown Risk Management, Rev. 2
ORAM Model Change Form, April 18, 2012
ORAM Sentinel Outage Safety Assessment, April 18, 2012
O-TI-367
Outage Risk Assessment Report, U3 Cycle R15, Rev. 1
PER 539040, HPCI Turbine Stop Valve Failed to Trip
PER 539556, HPCI Turbine Main Pump Vibration
PER 541156, HPCI Oil Tank Level Low
PER 541727, HPCI Gland Exhauster Pump Breaker
PER 547134, Shutdown Risk Management, Filling out DID Checklist Once per 24 Hours
PMT-0-000-MEC001, Leak Checks on Tube Fitting, Threaded, Flanged, Bolted or Welded
  Connections, Rev. 7
                                                                                  Attachment


==Section 1R15: Operability Evaluations==
                                            8
: 0-17W300-9, Mechanical Isometric drawing for EECW drains, Rev. 0  
SR 541069, Adjust Sensitivity on Incipient Fire Detector
: 0-GOI-200-1, Freeze Protection Inspection, Rev. 69 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting - 10CFR50.65, Rev. 37 1-47E859-1, Flow Diagram Emergency Equipment Cooling Water, Rev. 81  
U3 ORAM Safety Function Status Report, dated May 5, 2012
: 1-47E859-1, Flow Diagram for EECW system Unit 1, Rev. 82 2-47E859-1, Flow Diagram for EECW system Unit 2, Rev. 31 3-47E859-1, Flow Diagram for EECW system Unit 1, Rev. 38 3-SI-4.5.C.1(2), EECW Pump Operation, Rev. 119
WO 113426235, HPCI Turbine Stop Valve Failed to Trip
: BFN-50-7067, General Design Criteria Document for the EECW system, Rev. 18
WO 113426235, HPCI Turbine Stop Valve PMT Step Text
: BFN-50-C-7067, EECW System Design Criteria, Rev. 18 Calculation MDN0026910163, Combustible Load Table, Rev. 42
WO 113429679, Task 10: 1-FCV-073-0018, Rev. 0
: DCN 69957, Appendix R Pump House Tunnel Fire Barrier, Rev. A DWG 2-47E600-53A, Mechanical Instruments and Controls, Rev. 3
WO 113435872, HPCI Main & Booster Pump Head & Flow Rate Test
: EPI-0-000-FRZ001, Freeze Protection Program for RHRSW Pump Rooms and Diesel Generator Building, Rev. 19 Fire Protection Report Volume 1, Fire Hazards Analysis for Fire Area 25, Rev. 11  
WO 113440357, HPCI Oil Tank Level Low
: FSAR Section 10.9, RHR Service Water System,
WO 113441055, Verification of Remote Position Indicators
: BFN-24 FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,
WO 113445422, Adjust Sensitivity on Incipient Fire Detector
: BFN-24 FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology,
Section 1R15: Operability Evaluations
: BFN-24
0-17W300-9, Mechanical Isometric drawing for EECW drains, Rev. 0
: MPI-0-260-DRS001, Inspection and Maintenance of Doors
0-GOI-200-1, Freeze Protection Inspection, Rev. 69
: NPG-SPP-09.0, Engineering, Rev. 1
0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -
: NPG-SPP-09.3, Plant Modifications and Engineering Change Control, Rev. 6 Past Operability Form for
      10CFR50.65, Rev. 37
: PER 492957, Tarps on RHRSW Rooms
1-47E859-1, Flow Diagram Emergency Equipment Cooling Water, Rev. 81
: PER 310544, Gaps in A and D RHRSW Pump Room Flood Doors
1-47E859-1, Flow Diagram for EECW system Unit 1, Rev. 82
: PER 372194, FPR Justification on Intake Pumping Station Fire Barriers
2-47E859-1, Flow Diagram for EECW system Unit 2, Rev. 31
: PER 469640,
3-47E859-1, Flow Diagram for EECW system Unit 1, Rev. 38
: BFN-0-DOOR-260-C-RHRSW, Aggregate Impact of RHRSW Pump Room Doors
3-SI-4.5.C.1(2), EECW Pump Operation, Rev. 119
: PER 470350,
BFN-50-7067, General Design Criteria Document for the EECW system, Rev. 18
: BFN-0-DOOR-260-C-RHRSW May Not Seal
BFN-50-C-7067, EECW System Design Criteria, Rev. 18
: PER 481145, B and D RHRSW Pump Room Watertight Doors Were Found Closed and Locked, But Not Mechanically Restrained
Calculation MDN0026910163, Combustible Load Table, Rev. 42
: PER 492957, Tarps on RHRSW Rooms
DCN 69957, Appendix R Pump House Tunnel Fire Barrier, Rev. A
: PER 500804, Immediate Actions Taken for
DWG 2-47E600-53A, Mechanical Instruments and Controls, Rev. 3
: PER 492957 Not Documented
EPI-0-000-FRZ001, Freeze Protection Program for RHRSW Pump Rooms and Diesel
: PER 520497, EECW check valve appears to be seeping and repressurizing pipe
    Generator Building, Rev. 19
: PIC 70445, System 26,
Fire Protection Report Volume 1, Fire Hazards Analysis for Fire Area 25, Rev. 11
: PER 372194 Corrective Action - IPS Fire Seals, Rev. 0 Prompt Determination of Operability (PDO) for 0-CKV-067-0502, Rev. 0 Prompt Determination of Operability for
FSAR Section 10.9, RHR Service Water System, BFN-24
: PER 569282
FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,
: Attachment
    BFN-24
: SR 482359, RHRSW B Pump Room Door Failed Chalk Test
FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology, BFN-24
: SR 482401, RHRSW D Pump Room Door Failed Chalk Test
MPI-0-260-DRS001, Inspection and Maintenance of Doors
: SR 560210, NRC Walkdown Identified RHRSW Door Issues
NPG-SPP-09.0, Engineering, Rev. 1
: SR 563000, Site Tolerance of Degraded/Nonconforming Issue
NPG-SPP-09.3, Plant Modifications and Engineering Change Control, Rev. 6
: SR 563507, RHRSW Intake Structure Doors Have Not Been Evaluated for MR (a)(1)
Past Operability Form for PER 492957, Tarps on RHRSW Rooms
: SR 565020, Document Former NRC Senior Resident Observation
PER 310544, Gaps in A and D RHRSW Pump Room Flood Doors
: WO 111457995, Repair BFN-0-DOOR-260-C-RHRSW
PER 372194, FPR Justification on Intake Pumping Station Fire Barriers
PER 469640, BFN-0-DOOR-260-C-RHRSW, Aggregate Impact of RHRSW Pump Room Doors
PER 470350, BFN-0-DOOR-260-C-RHRSW May Not Seal
PER 481145, B and D RHRSW Pump Room Watertight Doors Were Found Closed and Locked,
    But Not Mechanically Restrained
PER 492957, Tarps on RHRSW Rooms
PER 500804, Immediate Actions Taken for PER 492957 Not Documented
PER 520497, EECW check valve appears to be seeping and repressurizing pipe
PIC 70445, System 26, PER 372194 Corrective Action - IPS Fire Seals, Rev. 0
Prompt Determination of Operability (PDO) for 0-CKV-067-0502, Rev. 0
Prompt Determination of Operability for PER 569282
                                                                                Attachment


==Section 1R18: Plant Modifications==
                                          9
: 3-ARP-9-3E, Panel 9-3, 3XA-55-3E, Rev. 26  
SR 482359, RHRSW B Pump Room Door Failed Chalk Test
: 3-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 56 3-GOI-100-3B, Refueling Operations (RX Cavity Letdown and Vessel Re-Assembly), Rev. 50 3-SIMI-3A, Reactor Feedwater System Index, Rev. 32 ACE
SR 482401, RHRSW D Pump Room Door Failed Chalk Test
: PER 427252(330400) Initial Cavity Flood-up Overflow into Ventilation Ducts
SR 560210, NRC Walkdown Identified RHRSW Door Issues
: LCL-3-L-03-055, Reactor Water level Flood-Up Calibration, Rev. 5 Minor Mod
SR 563000, Site Tolerance of Degraded/Nonconforming Issue
: DCN 70549, Reactor Water Level Flood-Up Transmitter and Indication Loop Replacement, Rev. A
SR 563507, RHRSW Intake Structure Doors Have Not Been Evaluated for MR (a)(1)
: NPG-SPP-09.4, 10
SR 565020, Document Former NRC Senior Resident Observation
: CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 5
WO 111457995, Repair BFN-0-DOOR-260-C-RHRSW
: NPG-SPP-09.5, Temporary Alterations, Rev. 2
Section 1R18: Plant Modifications
: NPG-SPP-9.3, Plant Modifications and Engineering Change Control, Rev. 6
3-ARP-9-3E, Panel 9-3, 3XA-55-3E, Rev. 26
: NPG-SPP-9.4, 10
3-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 56
: CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 5
3-GOI-100-3B, Refueling Operations (RX Cavity Letdown and Vessel Re-Assembly), Rev. 50
: ODMI-2012-0004,
3-SIMI-3A, Reactor Feedwater System Index, Rev. 32
: FCV-73-16 Leakage
ACE PER 427252(330400) Initial Cavity Flood-up Overflow into Ventilation Ducts
: PER 427252, Initial Cavity Flood-up Overflow into Ventilation Ducts, (PER 330400)
LCL-3-L-03-055, Reactor Water level Flood-Up Calibration, Rev. 5
: PER 565572, U1 HPCI Steam Admission Valve Leakage
Minor Mod DCN 70549, Reactor Water Level Flood-Up Transmitter and Indication Loop
: PER 565577, U1 HPCI Steam Admission Valve Leakage
    Replacement, Rev. A
: PER 569927, Opportunity for Operations Turnover Improvement
NPG-SPP-09.4, 10 CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 5
: PER 571068, Potential Grease Degradation
NPG-SPP-09.5, Temporary Alterations, Rev. 2
: SII-3-L-03-055, 500" Reactor Water Level A Refuel Range
NPG-SPP-9.3, Plant Modifications and Engineering Change Control, Rev. 6
: LT-3-55 Special Calibration for Vented Vessel and Fuel Pool Flood-Up, Rev. 2 TACF 1-12-001-073, Thermal Insulation Attached to
NPG-SPP-9.4, 10 CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 5
: BFN-1-FCV-073-0016, HPCI Steam Supply Valve, Rev. 0 TACF 2-12-001-073, Thermal Insulation Attached to
ODMI-2012-0004, FCV-73-16 Leakage
: BFN-2-FCV-073-0016, HPCI Steam Supply Valve, Rev. 0
PER 427252, Initial Cavity Flood-up Overflow into Ventilation Ducts, (PER 330400)
: VTD-OT01-0020, OTEK Corp. Ops Manual for
PER 565572, U1 HPCI Steam Admission Valve Leakage
: HI-Q Programmable Controllers, Rev. 3
PER 565577, U1 HPCI Steam Admission Valve Leakage
: WO 112971110, WO Request for
PER 569927, Opportunity for Operations Turnover Improvement
: DCN 70549 to Implement 3-55 Loop Modification on U3
PER 571068, Potential Grease Degradation
: WO 113275768, Implement TACF 1-12-001-073 to remove insulation from
SII-3-L-03-055, 500 Reactor Water Level A Refuel Range LT-3-55 Special Calibration for
: BFN-1-FCV-073-0016
    Vented Vessel and Fuel Pool Flood-Up, Rev. 2
: WO 113322598, Implement TACF 2-12-001-073 to remove insulation from BFN-2-FCV-073-0016
TACF 1-12-001-073, Thermal Insulation Attached to BFN-1-FCV-073-0016, HPCI Steam Supply
    Valve, Rev. 0
TACF 2-12-001-073, Thermal Insulation Attached to BFN-2-FCV-073-0016, HPCI Steam Supply
    Valve, Rev. 0
VTD-OT01-0020, OTEK Corp. Ops Manual for HI-Q Programmable Controllers, Rev. 3
WO 112971110, WO Request for DCN 70549 to Implement 3-55 Loop Modification on U3
WO 113275768, Implement TACF 1-12-001-073 to remove insulation from BFN-1-FCV-073-
    0016
WO 113322598, Implement TACF 2-12-001-073 to remove insulation from BFN-2-FCV-073-
    0016
Section 1R19: Post-Maintenance Testing
0-OI-82, Standby Diesel Generator System, Rev. 129
0-SR-3.8.1.1(D), Diesel Generator D Monthly Operability Test, Rev. 39
0-TI-106, General Leak Rate Test Procedure, Rev. 14, performed on April 9, 2012
0-TI-360, Containment Leak Rate Programs, Rev. 33
0-TI-362, Inservice Testing of Pumps and Valves, Rev. 29
3-45E779-41, Wiring Diagram, 480V Shutdown Auxiliary Power Schematic Diagram, Rev. 19
3-45E779-51, Wiring Diagram, 480V Load Shed Div II Schematic Diagram, Rev. 19
                                                                                  Attachment


==Section 1R19: Post-Maintenance Testing==
                                          10
: 0-OI-82, Standby Diesel Generator System, Rev. 129 0-SR-3.8.1.1(D), Diesel Generator D Monthly Operability Test, Rev. 39
3-47E801-1-ISI, ASME Section XI, Flow Diagram Main Steam Code Class Boundaries, Rev. 19
: 0-TI-106, General Leak Rate Test Procedure, Rev. 14, performed on April 9, 2012 0-TI-360, Containment Leak Rate Programs, Rev. 33 0-TI-362, Inservice Testing of Pumps and Valves, Rev. 29 3-45E779-41, Wiring Diagram, 480V Shutdown Auxiliary Power Schematic Diagram, Rev. 19 3-45E779-51, Wiring Diagram, 480V Load Shed Div II Schematic Diagram, Rev. 19 
3-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor Pressure Vessel and
: Attachment 3-47E801-1-ISI, ASME Section XI, Flow Diagram Main Steam Code Class Boundaries, Rev. 19 3-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor Pressure Vessel and Associated Piping, Rev. 21 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, Rev. 21  
  Associated Piping, Rev. 21
: 3-SR-3.4.9.1(2), Reactor Vessel Shell Temperature and Reactor Coolant Pressure Monitoring During In-Service Hydrostatic or Leak Testing, Rev. 15 3-SR-3.6.1.3.10(B) Primary Containment Local Leak Rate Test Main Steam Line B: Penetration X-7B 3-SR-3.6.1.3.10(B-OUTBD), Primary Containment Local Leak Rate Test Main Steam Line B Outboard Penetration X-7B, Rev. 06, performed on April 8, 2012 3-SR-3.8.1.1(3C) Diesel Generator '3C' Monthly Operability Test, Rev. 42, performed on May 15, 2012 3-SR-3.8.1.7(3C), Diesel Generator '3C' 24 Hour Run, Rev. 21, performed on April 24, 2012
3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, Rev. 21
: ECI-0-000-RLY003, Replacement of Relays, Rev. 21
3-SR-3.4.9.1(2), Reactor Vessel Shell Temperature and Reactor Coolant Pressure Monitoring
: EII-0-000-TCC106, Troubleshooting, Doc. and Config. Control of Elect. Activities, Rev. 62
        During In-Service Hydrostatic or Leak Testing, Rev. 15
: MCI-0-000-PCK001, Generic Maintenance Instructions for Valve Packing, Rev. 26
3-SR-3.6.1.3.10(B) Primary Containment Local Leak Rate Test Main Steam Line B: Penetration
: MCI-0-074-VLV002, Residual Heat Removal Motor Operated Valves,
  X-7B
: FCV-74-47, 48, 53 and 67 Disassembly, Inspection, Rework and Reassembly
3-SR-3.6.1.3.10(B-OUTBD), Primary Containment Local Leak Rate Test Main Steam Line B
: MCI-0-082-GOV001, Standby Diesel Engine Governor Removal and Installation, Rev. 9 MCR logs
  Outboard Penetration X-7B, Rev. 06, performed on April 8, 2012
: MMDP-1, Maintenance Management System
3-SR-3.8.1.1(3C) Diesel Generator 3C Monthly Operability Test, Rev. 42, performed on May
: MSI-0-001-VSL001, Reactor Vessel Disassembly and Reassembly, Rev. 100
  15, 2012
: NPG-SPP-06.3, Pre-/Post-Maintenance Testing
3-SR-3.8.1.7(3C), Diesel Generator 3C 24 Hour Run, Rev. 21, performed on April 24, 2012
: PER 143225, High Vibration on Generator end bearing on 3D DG
ECI-0-000-RLY003, Replacement of Relays, Rev. 21
: PER 538810, Restart NOI U3RF15-002: RPV Head Deformation due to Foreign Object
EII-0-000-TCC106, Troubleshooting, Doc. and Config. Control of Elect. Activities, Rev. 62
: PER 541788, High Vibrations on 3C DG
MCI-0-000-PCK001, Generic Maintenance Instructions for Valve Packing, Rev. 26
: PER 548753, Extent of Condition for D DG, (3A)
MCI-0-074-VLV002, Residual Heat Removal Motor Operated Valves, FCV-74-47, 48, 53 and 67
: PER 548755, Extent of Condition for D DG, (3B)
Disassembly, Inspection, Rework and Reassembly
: PER 548756, Extent of Condition for D DG, (3C)
MCI-0-082-GOV001, Standby Diesel Engine Governor Removal and Installation, Rev. 9
: PER 548757, Extent of Condition for D DG, (3D)
MCR logs
: PER 553585, Hydro Procedure Discrepancy
MMDP-1, Maintenance Management System
: SR 532953, 3-FCV-1-27 failed as-found LLRT
MSI-0-001-VSL001, Reactor Vessel Disassembly and Reassembly, Rev. 100
: SR 542421, Smooth Indication Noted on the Top Surface of RPV Flange During U3R15
NPG-SPP-06.3, Pre-/Post-Maintenance Testing
: SR 546885, Address 3C DG axial vibration
PER 143225, High Vibration on Generator end bearing on 3D DG
: SR 547405, As-found LLRT rotameter did not meet required accuracy
PER 538810, Restart NOI U3RF15-002: RPV Head Deformation due to Foreign Object
: SR 548237, Four Studs Not Pulled While Tensioning the U3 RPV Head
PER 541788, High Vibrations on 3C DG
: VTD-W290-0050, Instruction Manual for Woodward
PER 548753, Extent of Condition for D DG, (3A)
: EG-B10C Governor Actuator, Rev. 2
PER 548755, Extent of Condition for D DG, (3B)
: WO 112472092, Generator Replacement Testing for 3C EDG
PER 548756, Extent of Condition for D DG, (3C)
: WO 112505164, Perform as-left LLRT for B outboard MSIV, Penetration X-7B
PER 548757, Extent of Condition for D DG, (3D)
: WO 113324169, Reassemble Generator for 3C EDG
PER 553585, Hydro Procedure Discrepancy
: WO 113394336, Re-torque Valve Packing on 3-FCV-001-0027 (B Outboard MSIV)
SR 532953, 3-FCV-1-27 failed as-found LLRT
: WO 113429130, 3-BKR-231-0003B/3C needs cell switch adjustment
SR 542421, Smooth Indication Noted on the Top Surface of RPV Flange During U3R15
: WO 113475937, D D/G Came Up To 500 RPM When Started During 0-SR-3.8.1.1(D)
SR 546885, Address 3C DG axial vibration
: WO 113480500, D/G 'D' Monthly Operability Test
SR 547405, As-found LLRT rotameter did not meet required accuracy
: WO 113480917, Replace D D/G Governor Speed Stop Micro Switches
SR 548237, Four Studs Not Pulled While Tensioning the U3 RPV Head
: WO 113483626, Troubleshoot/Repair/Replace
VTD-W290-0050, Instruction Manual for Woodward EG-B10C Governor Actuator, Rev. 2
: BFN-0-RLY-082-D/ALM
WO 112472092, Generator Replacement Testing for 3C EDG
: WO 113483967, D D/G Dryer Assembly High DP Causing Excessive Blow Down
WO 112505164, Perform as-left LLRT for B outboard MSIV, Penetration X-7B
: WO 113484062, D D/G Dryer Assembly High DP Causing Excessive Blow Down Attachment
WO 113324169, Reassemble Generator for 3C EDG
: WO 113484918, Lost Terminating Screw
WO 113394336, Re-torque Valve Packing on 3-FCV-001-0027 (B Outboard MSIV)
: WO 113484954, Extent of Condition for D DG, (3A)
WO 113429130, 3-BKR-231-0003B/3C needs cell switch adjustment
: WO 113484954, Extent of Condition for D DG, (3B)
WO 113475937, D D/G Came Up To 500 RPM When Started During 0-SR-3.8.1.1(D)
: WO 113484957, Extent of Condition for D DG, (3C)
WO 113480500, D/G D Monthly Operability Test
: WO 113484958, Extent of Condition for D DG, (3D)
WO 113480917, Replace D D/G Governor Speed Stop Micro Switches
: WO 113486500, Troubleshoot/Repair/Replace DG D Air Pressure Alarm Relay WO Instructions PMT for
WO 113483626, Troubleshoot/Repair/Replace BFN-0-RLY-082-D/ALM
: 113480917, Rev. 0
WO 113483967, D D/G Dryer Assembly High DP Causing Excessive Blow Down
WO 113484062, D D/G Dryer Assembly High DP Causing Excessive Blow Down
                                                                                    Attachment


==Section 1R20: Refueling and Other Outage Activities==
                                          11
: 0-47E820-1, Flow Diagram Control Rod Drive Hydraulic System, Rev. 32  
WO 113484918, Lost Terminating Screw
: 0-OI-2B, Condensate Storage and Transfer System, Rev. 76 0-GOI-100-3A, Refueling Operations (In-Vessel Operations) 0-GOI-100-3B, Operations in Spent Fuel Pool Only 0-GOI-100-3C, Fuel Movement Operations During Refueling 0-GOI-100-3C, Fuel Movement Operations During Refueling, Attachment 6, Core Verification 3-47E804-1, Flow Diagram Condensate, Rev. 45  
WO 113484954, Extent of Condition for D DG, (3A)
: 3-47E818-1, Flow Diagram Condensate Storage and Supply, Rev. 27 3-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 19 3-47E855-1, Flow Diagram Fuel Pool Cooling System, Rev. 24 3-AOI-100-1, Reactor Scram, Scram Reports, Rev. 58 3-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and Reduction in Power During Power Operations 3-GOI-100-1A, Unit Startup, Rev. 99 3-GOI-200-2, Primary Containment Initial Entry and Closeout, Rev. 34 3-OI-78, Fuel Pool Cooling and Cleanup System, Rev. 60 3-OI-85, Control Rod Drive System, Rev. 75  
WO 113484954, Extent of Condition for D DG, (3B)
: 3-POI-78, Reactor Water Letdown During Refueling Outages Using Submersible Pump/Filter, Rev. 06 3-SR-3.1.1.5(A), Control Rod Coupling Integrity Check, Att. 5, Startup Sequence, Rev. 25 3-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring 3-TI-179, CILRT Data Acquisition System Setup, Rev. 8  
WO 113484957, Extent of Condition for D DG, (3C)
: 3-TO-2012-0003; Clearance 3-001-0009B 3-TO-2012-0003; Clearance 3-068-0023A 3-TO-2012-0003; Clearance 3-071-0010 3-TO-2012-0003; Clearance 3-075-0009 3-TO-2012-0003; Clearance 3-075-0013  
WO 113484958, Extent of Condition for D DG, (3D)
: Browns Ferry Nuclear U3R15 Core Verification for BOC16 dated 4/10/2012
WO 113486500, Troubleshoot/Repair/Replace DG D Air Pressure Alarm Relay
: MMDP-11, Erection of Scaffolds / Temporary Wolf Platforms and Ladders, Rev. 3
WO Instructions PMT for 113480917, Rev. 0
: MMTP-102, Erection of Scaffolds / Temporary Work Platforms and Ladders, Revs. 2 & 7
Section 1R20: Refueling and Other Outage Activities
: NPG-SPP-09.17, Temporary Equipment Control, Rev. 1
0-47E820-1, Flow Diagram Control Rod Drive Hydraulic System, Rev. 32
: OPDP-1, Conduct of Operations, Rev. 23
0-OI-2B, Condensate Storage and Transfer System, Rev. 76
: PER 542193, Lock High Radiation Area Key
0-GOI-100-3A, Refueling Operations (In-Vessel Operations)
: PER 542874, Unacceptable Housekeeping Practices in U3 RWCU HX Room
0-GOI-100-3B, Operations in Spent Fuel Pool Only
: PER 543083, Housekeeping Inspection of 3B Reactor Water Cleanup Pump Room
0-GOI-100-3C, Fuel Movement Operations During Refueling
: PER 547169, U3 RWCU Equipment Drain Screens
0-GOI-100-3C, Fuel Movement Operations During Refueling, Attachment 6, Core Verification
: PER 547172, U3 RWCU Pump Room Equipment Drain Screen
3-47E804-1, Flow Diagram Condensate, Rev. 45
: PER 549286, 3D Diesel Generator 7-Day Tank Leaking From Inspection Port
3-47E818-1, Flow Diagram Condensate Storage and Supply, Rev. 27
: PER 554943, Pipe Support 3-47B458-564 - Core Spray Attachment
3-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 19
: PER 555573, Unit 3 Reactor Scram
3-47E855-1, Flow Diagram Fuel Pool Cooling System, Rev. 24
: PER 556790, Design Error with U3 3A USST
3-AOI-100-1, Reactor Scram, Scram Reports, Rev. 58
: Scaffold Request # 03-1453-3, RWCU HX Room Scaffold Request # 10-239-3, RWCU HX Room
3-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and Reduction in
: SR 556367, GOI Step Not Fully Signed Off and Dated 3-TO-2012-004, sections 3-002-0001 and 3-078-0001 for Unit 3 Alternate Reactor Water Level Control; 3-TO-2012-0003, Section 3-001-0008, for work on Main Steam Line Drain Inboard Isolation Valve, 1-FCV-001-055; 3-TO-2012-0003; Clearance 3-001-0009B, for maintenance on 3-FCV-1-56; Clearance 3-068-
  Power During Power Operations
: 23A, for maintenance of Recirculation Pump 3B; Clearance 3-071-0010, for maintenance on RCIC Barometric Condenser Condensate Pump Motor; Clearance 3-075-0009, for 3A Core Spray Motor Replacement; and Clearance 3-075-0013, for 3C Core Spray Motor Replacement. 3-POI-200.5
3-GOI-100-1A, Unit Startup, Rev. 99
: 0-GOI-100-3A, Refueling Operations (In-Vessel Operations), 0-GOI-100-3B, Operations in the Spent Fuel Pool Only, and 0-GOI-100-3C, Fuel Movement Operations During Refueling. Attachment 6, of 0-GOI-100-3C.
3-GOI-200-2, Primary Containment Initial Entry and Closeout, Rev. 34
3-OI-78, Fuel Pool Cooling and Cleanup System, Rev. 60
3-OI-85, Control Rod Drive System, Rev. 75
3-POI-78, Reactor Water Letdown During Refueling Outages Using Submersible Pump/Filter,
  Rev. 06
3-SR-3.1.1.5(A), Control Rod Coupling Integrity Check, Att. 5, Startup Sequence, Rev. 25
3-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring
3-TI-179, CILRT Data Acquisition System Setup, Rev. 8
3-TO-2012-0003; Clearance 3-001-0009B
3-TO-2012-0003; Clearance 3-068-0023A
3-TO-2012-0003; Clearance 3-071-0010
3-TO-2012-0003; Clearance 3-075-0009
3-TO-2012-0003; Clearance 3-075-0013
Browns Ferry Nuclear U3R15 Core Verification for BOC16 dated 4/10/2012
MMDP-11, Erection of Scaffolds / Temporary Wolf Platforms and Ladders, Rev. 3
MMTP-102, Erection of Scaffolds / Temporary Work Platforms and Ladders, Revs. 2 & 7
NPG-SPP-09.17, Temporary Equipment Control, Rev. 1
OPDP-1, Conduct of Operations, Rev. 23
PER 542193, Lock High Radiation Area Key
PER 542874, Unacceptable Housekeeping Practices in U3 RWCU HX Room
PER 543083, Housekeeping Inspection of 3B Reactor Water Cleanup Pump Room
PER 547169, U3 RWCU Equipment Drain Screens
PER 547172, U3 RWCU Pump Room Equipment Drain Screen
PER 549286, 3D Diesel Generator 7-Day Tank Leaking From Inspection Port
PER 554943, Pipe Support 3-47B458-564 - Core Spray
                                                                                  Attachment


==Section 1R22: Surveillance Testing==
                                          12
: 0-TI-360, Containment Leak Rate Programs, Rev. 33  
PER 555573, Unit 3 Reactor Scram
: 0-TI-360, Containment Leak Rate Programs, Rev. 33 0-TI-362, Inservice Testing of Pumps and Valves, Rev. 30  
PER 556790, Design Error with U3 3A USST
: 0-TI-362, Inservice Testing of Pumps and Valves, Rev. 30 2-SI-4.2.E-1(B), Drywell Equipment Drain Sump Flow Integrator Calibration, Rev. 22 2-SI-4.4.A.1, Standby Liquid Control Pump Functional Test, Rev. 66 3-47E811-1, Flow Diagram Residual Heat Removal System, Rev. 65 3D EDG LAT RA Recorder Chart A Test 1 and 2 Data, dated 4/03/12  
Scaffold Request # 03-1453-3, RWCU HX Room
: 3-SR-3.6.1.1.1(OPT-A), Primary Containment Total Leak Rate - Option A, Rev. 11 3-SR-3.6.1.3.10(B), Primary Containment Local Leak Rate Test Main Steam Line B: Penetration X-7B, Rev. 07 performed on April 29, 2012 3-SR-3.8.1.9(3D OL), Diesel Generator 3D Emergency Load Acceptance Test with Unit 3 Operating, Rev. 14 3-TI-173, Primary Containment Inspection, Rev. 10 and Rev.11 3-TI-179, CILRT Data Acquisition System Setup, Rev. 08 ANSI/ANS-56.8-1994, Containment System Leakage Testing Requirements Design Criteria
Scaffold Request # 10-239-3, RWCU HX Room
: BFN-50-7082, Standby Diesel Generator, Rev. 16 DWG 2-47E852-2, Flow Diagram Clean Radwaste & Decontamination Drainage, Rev. 33  
SR 556367, GOI Step Not Fully Signed Off and Dated
: FSAR Section 10.10, Emergency Equipment Cooling Water (EECW) System,
3-TO-2012-004, sections 3-002-0001 and 3-078-0001 for Unit 3 Alternate Reactor Water Level
: BFN-24
Control; 3-TO-2012-0003, Section 3-001-0008, for work on Main Steam Line Drain Inboard
: FSAR Section 8.5, Standby AC Power Supply and Distribution,
Isolation Valve, 1-FCV-001-055;
: BFN-24 Main Control Room Logs
3-TO-2012-0003; Clearance 3-001-0009B, for maintenance on 3-FCV-1-56; Clearance 3-068-
: NEDP-14, Containment Leak Rate Programs, Rev. 09
0023A, for maintenance of Recirculation Pump 3B; Clearance 3-071-0010, for maintenance on
: NEDP-27, Past Operability Evaluations, Rev. 0
RCIC Barometric Condenser Condensate Pump Motor; Clearance 3-075-0009, for 3A Core
: PER 533052, 3-FCV-1-27 failed as-found LLRT
Spray Motor Replacement; and Clearance 3-075-0013, for 3C Core Spray Motor Replacement.
: PER 549232, As Found Integrator Indication Found Out Of Tolerance Low
3-POI-200.5
: PER 551019, Torus site glass readings were taken while isolated during CILRT
0-GOI-100-3A, Refueling Operations (In-Vessel Operations), 0-GOI-100-3B, Operations in the
: PER 554996, Evaluate potential HPCI preconditioning
Spent Fuel Pool Only, and 0-GOI-100-3C, Fuel Movement Operations During Refueling.
: PER 568095, 2-SI-4.4.A.1 SLC TEST, Schrader valve
Attachment 6, of 0-GOI-100-3C.
: PER 568705, Issue During SLC Pump Functional Test
Section 1R22: Surveillance Testing
: PER 569867, HIgh vibration on 2A SLC pump Attachment
0-TI-360, Containment Leak Rate Programs, Rev. 33
: PER 569895, HIgh vibration on 2B SLC pump
0-TI-360, Containment Leak Rate Programs, Rev. 33
: PER 569965, 4 AUO's Not Present for Surveillance
0-TI-362, Inservice Testing of Pumps and Valves, Rev. 30
: PER 570625,
0-TI-362, Inservice Testing of Pumps and Valves, Rev. 30
: BFN-2-PMP-063-0006A, 2A SLC PUMP (GE-11-2A) Flowrate high
2-SI-4.2.E-1(B), Drywell Equipment Drain Sump Flow Integrator Calibration, Rev. 22
: PER 570710,U2 SLC Storage Tank Decreasing Level Trend
2-SI-4.4.A.1, Standby Liquid Control Pump Functional Test, Rev. 66
: PER 571768, Unit 2 SLC Storage Tank decreasing level trend.
3-47E811-1, Flow Diagram Residual Heat Removal System, Rev. 65
: SR 531728, Failure to Check Large Load Start
3D EDG LAT RA Recorder Chart A Test 1 and 2 Data, dated 4/03/12
: SR 531819, Failure to Send AUOs Locally for Large Load Start
3-SR-3.6.1.1.1(OPT-A), Primary Containment Total Leak Rate - Option A, Rev. 11
: SR 569401, 2-DRV-063-0530 leaking by its seat.
3-SR-3.6.1.3.10(B), Primary Containment Local Leak Rate Test Main Steam Line B: Penetration
: Needed excess force to seat valve Technical Specifications and Bases 3.3.8.1, Loss of Power (LOP) Instrumentation, Amendment 215 Technical Specifications and Bases 3.7.2, Emergency Equipment Cooling Water (EECW) System and Ultimate Heat Sink (UHS), Amendment 215 Technical Specifications and Bases 3.8.1, AC Sources - Operating, Amendment 266 U2 Bases B 3.4.5 RCS Leakage Detection Instrumentation, Rev. 0 U2 Tech Spec 3.4.5, RCS Leakage Detection Instrumentation, Amendment 253 UFSAR, 4.10 Nuclear System Leakage Rate Limits, Amendment 22
  X-7B, Rev. 07 performed on April 29, 2012
: WO 112511675, As Left - 3-SI-4.7.A.2.g-3/74g - PC LLRT - RHR Shutdown Cooling Suction
3-SR-3.8.1.9(3D OL), Diesel Generator 3D Emergency Load Acceptance Test with Unit 3
: WO 112816329, Drywell Equipment Drain Sump Flow Integrator Calibration
        Operating, Rev. 14
: WO 113145425, 2-SI-4.4.A.1, SLC Pump Functional Test
3-TI-173, Primary Containment Inspection, Rev. 10 and Rev.11
: WO 113614430, Replace the Schrader valve on the bladder for the 2A SLC Pump
3-TI-179, CILRT Data Acquisition System Setup, Rev. 08
: WO 113620697, 2-SI-4.4.A.1, SLC Pump Functional Test
ANSI/ANS-56.8-1994, Containment System Leakage Testing Requirements
: WO 113625610, 2-DRV-063-0530 leaking by its seat, Needed excess force to seat valve
Design Criteria BFN-50-7082, Standby Diesel Generator, Rev. 16
DWG 2-47E852-2, Flow Diagram Clean Radwaste & Decontamination Drainage, Rev. 33
FSAR Section 10.10, Emergency Equipment Cooling Water (EECW) System, BFN-24
FSAR Section 8.5, Standby AC Power Supply and Distribution, BFN-24
Main Control Room Logs
NEDP-14, Containment Leak Rate Programs, Rev. 09
NEDP-27, Past Operability Evaluations, Rev. 0
PER 533052, 3-FCV-1-27 failed as-found LLRT
PER 549232, As Found Integrator Indication Found Out Of Tolerance Low
PER 551019, Torus site glass readings were taken while isolated during CILRT
PER 554996, Evaluate potential HPCI preconditioning
PER 568095, 2-SI-4.4.A.1 SLC TEST, Schrader valve
PER 568705, Issue During SLC Pump Functional Test
PER 569867, HIgh vibration on 2A SLC pump
                                                                                  Attachment


==Section 1EP2: Alert and Notification System Evaluation 2012 Browns Ferry Emergency Planning Calendar mailer to members of the public in the 10-mile==
                                            13
: EPZ Documentation of bi-weekly siren tests and maintenance for 4th quarter 2011 and 1st quarter 2012 Documentation of Quarterly siren maintenance for 4th quarter 2011 and 1st quarter 2012
PER 569895, HIgh vibration on 2B SLC pump
: EPDP-10, Facilitation of the Alert and Notification System and Notification Tests, Rev. 4
PER 569965, 4 AUOs Not Present for Surveillance
: EPDP-14, Evaluation of Changes to Alert and Notification Systems (ANS), Rev. 0
PER 570625, BFN-2-PMP-063-0006A, 2A SLC PUMP (GE-11-2A) Flowrate high
: EPDP-16, Designated Emergency Response Equipment (DERE), Rev. 0
PER 570710,U2 SLC Storage Tank Decreasing Level Trend
: EPDP-17, NPG Emergency Plan Effectiveness Review (10
PER 571768, Unit 2 SLC Storage Tank decreasing level trend.
: CFR 50.54(q))
SR 531728, Failure to Check Large Load Start
: EPDP-8, Emergency Preparedness Quality Related Programs, Rev. 1
SR 531819, Failure to Send AUOs Locally for Large Load Start
: EPFS-9, Inspection, Service, and Maintenance of the Prompt Notification System (PNS) at Browns Ferry, Sequoyah, and Watts Bar Nuclear Plants, Rev. 6 and 7  
SR 569401, 2-DRV-063-0530 leaking by its seat. Needed excess force to seat valve
: Federal Signal 508 Electro-Mechanical Siren Installation and Operating Instructions, Rev. 12/11 Siren Annual Maintenance records: 2011 and 1st quarter 2012
Technical Specifications and Bases 3.3.8.1, Loss of Power (LOP) Instrumentation, Amendment
: SR 572389; admin requirements not met in implementing new ANS system
      215
Technical Specifications and Bases 3.7.2, Emergency Equipment Cooling Water (EECW)
      System and Ultimate Heat Sink (UHS), Amendment 215
Technical Specifications and Bases 3.8.1, AC Sources - Operating, Amendment 266
U2 Bases B 3.4.5 RCS Leakage Detection Instrumentation, Rev. 0
U2 Tech Spec 3.4.5, RCS Leakage Detection Instrumentation, Amendment 253
UFSAR, 4.10 Nuclear System Leakage Rate Limits, Amendment 22
WO 112511675, As Left - 3-SI-4.7.A.2.g-3/74g - PC LLRT - RHR Shutdown Cooling Suction
WO 112816329, Drywell Equipment Drain Sump Flow Integrator Calibration
WO 113145425, 2-SI-4.4.A.1, SLC Pump Functional Test
WO 113614430, Replace the Schrader valve on the bladder for the 2A SLC Pump
WO 113620697, 2-SI-4.4.A.1, SLC Pump Functional Test
WO 113625610, 2-DRV-063-0530 leaking by its seat, Needed excess force to seat valve
Section 1EP2: Alert and Notification System Evaluation
2012 Browns Ferry Emergency Planning Calendar mailer to members of the public in the 10-
mile EPZ
Documentation of bi-weekly siren tests and maintenance for 4th quarter 2011 and 1st quarter
2012
Documentation of Quarterly siren maintenance for 4th quarter 2011 and 1st quarter 2012
EPDP-10, Facilitation of the Alert and Notification System and Notification Tests, Rev. 4
EPDP-14, Evaluation of Changes to Alert and Notification Systems (ANS), Rev. 0
EPDP-16, Designated Emergency Response Equipment (DERE), Rev. 0
EPDP-17, NPG Emergency Plan Effectiveness Review (10 CFR 50.54(q))
EPDP-8, Emergency Preparedness Quality Related Programs, Rev. 1
EPFS-9, Inspection, Service, and Maintenance of the Prompt Notification System (PNS) at
Browns Ferry, Sequoyah, and Watts Bar Nuclear Plants, Rev. 6 and 7
Federal Signal 508 Electro-Mechanical Siren Installation and Operating Instructions, Rev. 12/11
Siren Annual Maintenance records: 2011 and 1st quarter 2012
SR 572389; admin requirements not met in implementing new ANS system
Section 1EP3: Emergency Preparedness Organization Staffing and Augmentation
System
2010, 2011, 2012 quarterly drill reports
2010, 2011, 2012 Unannounced pager test results
2012 Unannounced staffing drill report
239363 OSC Status Board Writer #1 failed to respond to Weekly Pager Test
243962 Operations Representative failed to respond to Weekly Pager Test
246558 Plant Assessment Team Leader failed to respond to Weekly Pager Test
                                                                                      Attachment


==Section 1EP3: Emergency Preparedness Organization Staffing and Augmentation System 2010, 2011, 2012 quarterly drill reports 2010, 2011, 2012 Unannounced pager test results 2012 Unannounced staffing drill report 239363==
                                            14
: OSC Status Board Writer #1 failed to respond to Weekly Pager Test
246569 OSC Status Board Writer #1 failed to respond to Weekly Pager Test
: 243962 Operations Representative failed to respond to Weekly Pager Test
248540 OSC I/C Supervisor failed to respond to Weekly Pager Test
: 246558 Plant Assessment Team Leader failed to respond to Weekly Pager Test Attachment
258558 Radiation Protection Manager failed to respond to Weekly Pager Test
: 246569 OSC Status Board Writer #1 failed to respond to Weekly Pager Test
266020 OSC I/C Engineer failed to respond to Weekly Pager Test
: 248540 OSC I/C Supervisor failed to respond to Weekly Pager Test
294582 OSC Mechanical Engineer failed to respond to Weekly Pager Test
: 258558 Radiation Protection Manager failed to respond to Weekly Pager Test
327650 Site Vice President failed to respond to Weekly Pager Test
: 266020 OSC I/C Engineer failed to respond to Weekly Pager Test
328191 OSC Director failed to respond to Weekly Pager Test
: 294582 OSC Mechanical Engineer failed to respond to Weekly Pager Test
362821 Confused communication on the need to send B5b blackout fire pump to BFN
: 327650 Site Vice President failed to respond to Weekly Pager Test
408093 Assistant OSC Director failed to respond to Weekly Pager Test
: 328191 OSC Director failed to respond to Weekly Pager Test
423217 CECC Plant Assessment Team member preparation for actual emergencies
: 362821 Confused communication on the need to send B5b blackout fire pump to
475726 2011 Graded Exercise Corrective Actions
: BFN 408093 Assistant OSC Director failed to respond to Weekly Pager Test  
541288 QA SSA1203 - EP qualifications not in Qualification Matrix
: 23217 CECC Plant Assessment Team member preparation for actual emergencies
542221 SAMG Decision Maker training requirements do not exclude Shift Managers as Site
: 475726 2011 Graded Exercise Corrective Actions
Emergency Director
: 541288 QA SSA1203 - EP qualifications not in Qualification Matrix
569374 Simulator issues during the BFN Off Year Exercise
: 542221 SAMG Decision Maker training requirements do not exclude Shift Managers as Site Emergency Director
CECC EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 41
: 569374 Simulator issues during the BFN Off Year Exercise CECC
CECC EPIP-4, Operations Duty Specialist Procedure for Site Area Emergency, Rev. 42
: EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 41  
Emergency Response Organization Teams listing dated 6/22/2012
: CECC
EPDP-3, Emergency Plan Exercises and Preparedness Drills, Rev. 5
: EPIP-4, Operations Duty Specialist Procedure for Site Area Emergency, Rev. 42 Emergency Response Organization Teams listing dated 6/22/2012
EPIP-6, Activation and Operation of the Technical Support Center (TSC), Rev. 34
: EPDP-3, Emergency Plan Exercises and Preparedness Drills, Rev. 5
EPIP-7, Activation and Operation of the Operations Support Center (OSC), Rev. 29
: EPIP-6, Activation and Operation of the Technical Support Center (TSC), Rev. 34
EPT500A, 2012 EP Staff Orientation Course Description
: EPIP-7, Activation and Operation of the Operations Support Center (OSC), Rev. 29  
TRN 30, Radiological Emergency Preparedness Training, Rev. 19
: EPT500A, 2012 EP Staff Orientation Course Description
Various EP staff and ERO member training records
: TRN 30, Radiological Emergency Preparedness Training, Rev. 19 Various EP staff and ERO member training records
Section 1EP5: Maintenance of Emergency Preparedness
10CFR50.54(q) Evaluation of TEENS augmentation hardware addition
10CFR50.54(q) Evaluation of TSC Renovation
362854; NOUE declared - Tornado
364318; Tornado event
364674; Extensive loss of ANS due to tornadoes
453700; PAR training requirement
456771; RP ERO staffing PER not closed correctly
571878; admin error on 50.54q eval of TEENS implementation
572826; EPDP-17 enhancement to add subject matter experts in 50.54q screening
95003-005, BFN NRC Column 4 Response Project and Administrative Controls - Appendix H,
Rev. 1: ERO Readiness Performance Area Report
BFN Quality Assurance - Emergency Preparedness Drill Assessment - QA-11-007 dated April
21, 2011
BFN Quality Assurance - Emergency Preparedness Equipment and Facility Readiness, QA-BF-
11-008 dated June 30, 2011
BFN Self-assessment BFN-EP-S-10-001, B5B Commitments
BFN Self-assessment BFN-EP-S-11-001, Effectiveness Reviews
Drill and exercise reports, 2010, 2011, and 2012
EPDP-1, Procedures, Maps, and Drawings, Rev. 3
EPDP-16, Designated Emergency Response Equipment (DERE), Rev. 0
EPDP-17, NPG Emergency Plan Effectiveness Review, Rev. 0
Event records of NOUE declared on 4/27/2011 - Tornado with Extended Loss of Off-site Power
                                                                                Attachment


==Section 1EP5: Maintenance of Emergency Preparedness 10CFR50.54(q) Evaluation of==
                                            15
: TEENS augmentation hardware addition
NPG-SPP-18.3, Emergency Preparedness, Rev. 1
: 10CFR50.54(q) Evaluation of TSC Renovation
REP, Radiological Emergency Plan, (Appendix A - BFN), Rev. 97
: 362854; NOUE declared - Tornado
REP, Radiological Emergency Plan, (Generic Part), Rev. 97
: 364318; Tornado event
Self-assessment CRP-EP-S-11-03, Site Tornado Procedure, BP-128, dated September 28,2011
: 364674; Extensive loss of ANS due to tornadoes
Self-assessment CRP-EP-S-12-005; Training Program comparison
: 453700; PAR training requirement
Self-assessment CRP-EP-S-12-006, REP drill
: 456771; RP ERO staffing PER not closed correctly
Self-assessment CRP-EP-S-12-020; EP Records
: 571878; admin error on 50.54q eval of TEENS implementation
SPP-3.1, Corrective Action Program, Rev. 4
: 572826;
TVA Quality Assurance - Emergency Preparedness Audit Report SSA1003 dated May 20, 2010
: EPDP-17 enhancement to add subject matter experts in 50.54q screening 95003-005, BFN NRC Column 4 Response Project and Administrative Controls - Appendix H, Rev. 1:
TVA Quality Assurance - Emergency Preparedness Audit Report SSA1203 dated April 24, 2012
: ERO Readiness Performance Area Report BFN Quality Assurance - Emergency Preparedness Drill Assessment -
Section 1EP6: Drill Evaluation
: QA-11-007 dated April 21, 2011 BFN Quality Assurance - Emergency Preparedness Equipment and Facility Readiness,
Browns Ferry, Off Year Exercise Report
: QA-BF-11-008 dated June 30, 2011 BFN Self-assessment
CECC-EPIP-1, Emergency Classification Procedure, REV. 53
: BFN-EP-S-10-001, B5B Commitments BFN Self-assessment
EPIP-1, Emergency Classification Procedure, REV. 47
: BFN-EP-S-11-001, Effectiveness Reviews Drill and exercise reports, 2010, 2011, and 2012
NP-REP, Radiological Emergency Plan, (Generic Part), Rev. 97
: EPDP-1, Procedures, Maps, and Drawings, Rev. 3
NP-REP, Radiological Emergency Plan, Appendix A, Rev. 97
: EPDP-16, Designated Emergency Response Equipment (DERE), Rev. 0
PER 567663, Accountability report inaccuracy during EP drill
: EPDP-17, NPG Emergency Plan Effectiveness Review, Rev. 0 Event records of NOUE declared on 4/27/2011 - Tornado with Extended Loss of Off-site Power Attachment
PER 568729, Revise EPIP-7, App. B to Indicate OSC Minimum Staffing
: NPG-SPP-18.3, Emergency Preparedness, Rev. 1 REP, Radiological Emergency Plan, (Appendix A - BFN), Rev. 97 REP, Radiological Emergency Plan, (Generic Part), Rev. 97 Self-assessment
PER 569310, CECC ERO member failed to respond to CECC activation
: CRP-EP-S-11-03, Site Tornado Procedure,
PER 569374, Simulator Issues during the BFN Off Year Exercise
: BP-128, dated September 28,2011
PER 570670, During the Unannounced Staffing Drill, TEENS System Delay
: Self-assessment
PER 571025, During EP OYE Simulator Stack Rad Simulation did not operate as expected
: CRP-EP-S-12-005; Training Program comparison Self-assessment
PER 571053, During the EP Unannounced Staffing Drill issues were observed
: CRP-EP-S-12-006, REP drill Self-assessment
PER 571382, During the 2012 EP Off Year Exercise Stack Monitor Simulation was an issue
: CRP-EP-S-12-020; EP Records
PER 572271, Focus areas found in the June 13th BFN REP OYE
: SPP-3.1, Corrective Action Program, Rev. 4 TVA Quality Assurance - Emergency Preparedness Audit Report SSA1003 dated May 20, 2010  
Performance Indicator Data from June 2012
: TVA Quality Assurance - Emergency Preparedness Audit Report SSA1203 dated April 24, 2012
Section 2RS1: Radiological Hazard Assessment and Exposure Control
(Annual Inventory Of Non-Fuel SNM and Other Items (Trash) In Unit 1, 2 And 3 Spent Fuel
Pools Performed 8/10-25/2011.)
0-TI-540, Storage of Material in the spent Fuel Storage Pool (SFSP) and Transfer Canal
(U1/U2), Rev. 2
Browns Ferry Technical Specification 5.7 Administrative Controls-High Radiation Area
NPG-SPP-05.0, Radiological and Chemistry Control, Rev. 1
NPG-SPP-05.1, Radiological Controls, Rev. 2
NSTS Confirmation Form 2012 Annual Inventory Reconciliation [Browns Ferry 1 AmBe Source],
Dated 1/18/2012
NSTS Confirmation Form 2012 Annual Inventory Reconciliation [Browns Ferry 3 Cs-137
Sources], Dated 1/18/2012
PER 334211 Track and trend radworker practices in drywell U2R16
PER 334244 Radworker practices in drywell U2R16
PER 439979 RP posted area incorrectly
PER 475108 U1R9 Drywell access room improperly posted
PER 512565 worker put tie wrap in mouth in RCA
PER 512567 building scaffold in unsurveyed area
RCDP-1, Conduct of Radiological Controls, Rev. 3
RCI-1.1, Radiation Operations Program Implementation, Revision 149
                                                                                  Attachment


==Section 1EP6: Drill Evaluation Browns Ferry, Off Year Exercise Report==
                                            16
: CECC-EPIP-1, Emergency Classification Procedure, REV. 53
RCI-1.2, Radiation, Contamination and Airborne Surveys, Revision 16
: EPIP-1, Emergency Classification Procedure, REV. 47
RCI-17, Control of High Radiation Areas and Very High Radiation Areas, Revision 71
: NP-REP, Radiological Emergency Plan, (Generic Part), Rev. 97
RCI-26, Radiation Protection Department Standards and Expectations, Revision 19
: NP-REP, Radiological Emergency Plan, Appendix A, Rev. 97
RCI-33, Diving Operations on the Refuel Floor, Rev. 9
: PER 567663, Accountability report inaccuracy during EP drill
RCI-34, Remote Monitoring, Revision 12
: PER 568729, Revise
RCI-40.0, RP Actions for Operation's Unit 0 (Common) Procedural Hold Points, Revision 17
: EPIP-7, App. B to Indicate OSC Minimum Staffing
RCI-47, Diving Operations in the Radiologically Controlled Area, Rev. 1
: PER 569310, CECC ERO member failed to respond to CECC activation
RCI-9.1, Radiation Work Permits, Revision 70
: PER 569374, Simulator Issues during the BFN Off Year Exercise
RWP 1238-0001, Unit-3R15 Refueling Outage Drywell Outside Support
: PER 570670, During the Unannounced Staffing Drill, TEENS System Delay
RWP 1238-0002, Unit-3R15 Refueling Outage Drywell Outside Support [High Rad]
: PER 571025, During EP OYE Simulator Stack Rad Simulation did not operate as expected
RWP 1238-0003, Unit-3R15 Outage Drywell Miscellaneous System Support [Locked High Rad]
: PER 571053, During the EP Unannounced Staffing Drill issues were observed
RWP 1238-0012, Unit-3R15 Outage Drywell Main Steam System Maintenance [High Rad]
: PER 571382, During the 2012 EP Off Year Exercise Stack Monitor Simulation was an issue
RWP 1238-0033, Unit-3R15, Outage Drywell Feedwater System Maintenance [Locked High
: PER 572271, Focus areas found in the June 13th BFN REP OYE
Rad]
: Performance Indicator Data from June 2012
RWP 1238-0683, Unit-3R15, Outage, Drywell Reactor Water Recirculation System [Continuous
Coverage- Locked High Radiation Area]
RWP 1238-0693, Unit-3R15, Outage, Drywell Reactor Water Cleanup System Maintenance
[Locked High Rad]
SR 532617 Worker got separated from escort
SR 532875 Inaccurate rad tag on a box
SR 532981 Small air activity excursion on RFF during Rx disassembly
SR 534873 Coordination issues obtaining RWCU sludge sample.
SR 534880 Deterioration of padding on Knee anchors U1 593
Survey M-010612-2, Unit 3 RXB 593' RWCU BW Transfer Pump Room, 01/06/2012
Survey M-020712-13, Unit 2 RXB 519' Under Torus, 02/07/2012
Survey M-021012-10, 0-CASK-079-0100/1 (MPC SN-0237), 02/10/2012
Survey M-102411-11, Unit 2 TB 586' 2A SJAE Room, 10/24/2011
Survey M-20120306-26, ISFSI Pad, 03/06/2012
Section 2RS6: Radioactive Gases and Liquid Effluent Treatment
Procedures, Guidance Documents, and Manuals
0-ODCM-001, Offsite Dose Calculation Manual, Rev. 21
NPG-SPP-05.14, Guide for Communicating Inadvertent Radiological Spills/Leaks to Outside
      Agencies, Rev. 0
NPG-SPP-05.15, Fleet Ground Water Protection Program, Rev.2
0-TI-15, Radioactive Gaseous Effluent Engineering Calculations and Measurements, Rev. 15
0-SI-4.8.A.1-1, Liquid Effluent Permit, Rev. 74
0-SI-4.8.B.1.a.2, Airborne Effluent Release Rate by Manual Sampling When a Gaseous Effluent
      Monitor is Inoperable, Rev. 31
0-SI-4.8.B.2-1, Airborne Effluent Analysis - Particulate and Charcoal Filter Analysis, Rev. 37
0-SI-4.8.B.2-5, Airborne Effluent Analysis - Monthly Tritium, Rev. 30
0-SI-4.8.B.2-8, Airborne Effluent Analysis - Stack Noble Gas, Rev. 12
0-SI-4.8.B.2-4, Airborne Effluent Analysis - Monthly Gamma Isotopic, Rev. 30
CI-714, Particulate and Charcoal Filter Sampling and Analysis, Rev. 30
CI-738, Sampling Effluent Monitors (CAMS) for Tritium and Gamma Isotopics, Rev. 31
0-SI-2.1-2, Airborne Effluent Radiation Monitor Source Checks, Rev. 45
1-SIMI-90B, Radiation Monitoring System Scaling and Setpoint Documents, Rev. 41
2010 Radiological Effluent Release Report
                                                                                      Attachment


==Section 2RS1: Radiological Hazard Assessment and Exposure Control (Annual Inventory Of Non-Fuel==
                                          17
: SNM and Other Items (Trash) In Unit 1, 2 And 3 Spent Fuel Pools Performed 8/10-25/2011.)
2011 Radiological Effluent Release Report
: 0-TI-540, Storage of Material in the spent Fuel Storage Pool (SFSP) and Transfer Canal (U1/U2), Rev. 2 Browns Ferry Technical Specification 5.7 Administrative Controls-High Radiation Area
2002 Radiological Effluent Release Report - Abnormal Release Addendum
: NPG-SPP-05.0, Radiological and Chemistry Control, Rev. 1
Records and Data Reviewed
: NPG-SPP-05.1, Radiological Controls, Rev. 2  
Browns Ferry UFSAR Chapter 9
: NSTS Confirmation Form 2012 Annual Inventory Reconciliation [Browns Ferry 1 AmBe Source], Dated 1/18/2012 NSTS Confirmation Form 2012 Annual Inventory Reconciliation [Browns Ferry 3 Cs-137 Sources], Dated 1/18/2012
0-SR-3.6.4.3.2(A)-SBGTS Iodine Removal Efficiency (Train-A), 8/23/2010
: PER 334211 Track and trend radworker practices in drywell U2R16
0-SR-3.6.4.3.2(A)-SBGTS Iodine Removal Efficiency (Train-A), 7/13/2011
: PER 334244 Radworker practices in drywell U2R16
Gaseous Release Permits: 120323.030.020.G, 120315.037.020.G, 120350.030.021.G,
: PER 439979 RP posted area incorrectly
        20328.032.020.G, 120333.043.019.G, 120340.046.020.G, 120330.040.025.G
: PER 475108 U1R9 Drywell access room improperly posted
Surveillance Task Sheet: 0-SI-4.8.B.2-1- Airborne Effluent Analysis- Particulate & Charcoal
: PER 512565 worker put tie wrap in mouth in RCA
        Filter Analysis, 5/1/2012
: PER 512567 building scaffold in unsurveyed area
System Health Reports, Each Unit System 66 - Off-Gas, 2/1/2011-1/31/2012
: RCDP-1, Conduct of Radiological Controls, Rev. 3
System Health Report, System 77 -Radwaste, 10/1/2011-1/31/2012
: RCI-1.1, Radiation Operations Program Implementation, Revision 149 
System Health Report, Each Unit System 90- Radiation Monitoring, 10/1/2011-1/31/2012
: Attachment
Cross-Check Analysis Data: 1st Quarter 2010 through 2nd Quarter 2011
: RCI-1.2, Radiation, Contamination and Airborne Surveys, Revision 16
Chemistry Focused Self Assessment Report - BFN-CEM-F-11-001, Performed 6/6-17/2011
: RCI-17, Control of High Radiation Areas and Very High Radiation Areas, Revision 71
White paper documenting Ground Water Monitoring in 2010 and 2011 with results
: RCI-26, Radiation Protection Department Standards and Expectations, Revision 19
CAP Documents
: RCI-33, Diving Operations on the Refuel Floor, Rev. 9
PER 257903 2-RM-090-013D, RCW Effluent Offline Rad Monitor alarmed on Hi Rad Setpoint
: RCI-34, Remote Monitoring, Revision 12
PER 313929 1Q FY11 Radwaste water processing and effluents continues to be problem areas.
: RCI-40.0, RP Actions for Operation's Unit 0 (Common) Procedural Hold Points, Revision 17
PER 324700 Unit 3 Station Sump tritium results from the sample obtained 1/18/2011
: RCI-47, Diving Operations in the Radiologically Controlled Area, Rev. 1
PER359503 Unmonitored release at the gas stack
: RCI-9.1, Radiation Work Permits, Revision 70
PER 367604, Insufficient sample equipment for inop Effluent CAM monitors
: RWP 1238-0001, Unit-3R15 Refueling Outage Drywell Outside Support
PER 532416, Possible release path to Waters of the US
: RWP 1238-0002, Unit-3R15 Refueling Outage Drywell Outside Support [High Rad]
Section 2RS7: Radiological Environmental Monitoring Program (REMP)
: RWP 1238-0003, Unit-3R15 Outage Drywell Miscellaneous System Support [Locked High Rad]
Procedures and Guidance Documents
: RWP 1238-0012, Unit-3R15 Outage Drywell Main Steam System Maintenance [High Rad]
Cl-420, Collection of Radiological Environmental Monitoring Samples, Revision 03
: RWP 1238-0033, Unit-3R15, Outage Drywell Feedwater System Maintenance [Locked High Rad]
EPFS-8, Servicing of Radiological Water Samplers, Revision 2
: RWP 1238-0683, Unit-3R15, Outage, Drywell Reactor Water Recirculation System [Continuous Coverage- Locked High Radiation Area]
EPFS-12, Repair and Preventative Maintenance Procedure for Radiological
: RWP 1238-0693, Unit-3R15, Outage, Drywell Reactor Water Cleanup System Maintenance [Locked High Rad]
EPFS-03, Servicing of Meteorological Equipment at Environmental Data Stations, Rev 15
: SR 532617 Worker got separated from escort
EPFS-07, Radio and Meteorological Tower Inspection, Rev 4
: SR 532875 Inaccurate rad tag on a box
EPFS-06, Calibration of Environmental Data Station Data Logger and Sonic Channels, Rev 16
: SR 532981 Small air activity excursion on RFF during Rx disassembly
Environmental Monitoring Air Sampling System, Rev 01
: SR 534873 Coordination issues obtaining RWCU sludge sample.
EMSTD-01, Environmental Radiological Monitoring Program, R25
: SR 534880 Deterioration of padding on Knee anchors U1 593 Survey M-010612-2, Unit 3
Records and Data Reviewed
: RXB 593' RWCU BW Transfer Pump Room, 01/06/2012 Survey M-020712-13, Unit 2
Annual Radiological Environmental Operating Report 2010 & 2011
: RXB 519' Under Torus, 02/07/2012 Survey M-021012-10, 0-CASK-079-0100/1 (MPC
Field Collection Sheets for June 4, 2012 Environmental Run
: SN-0237), 02/10/2012
EPFS-6 Data sheet 1 for Cal dates 3/21/12; 10/04/11; 04/13/11; 10/14/10; 08/24/10
: Survey M-102411-11, Unit 2
EPFS-6 Data sheet 6 for dates 03/21/12; 10/31/11; 10/04/11; 04/12/11; 10/14/10
: TB 586' 2A SJAE Room, 10/24/2011 Survey M-20120306-26, ISFSI Pad, 03/06/2012
EPFS-6 Data sheet 5 for dates 03/22/12; 04/12/11; 10/04/11; 10/20/10
EPFS-6 Data sheet 4 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10
EPFS-6 Data sheet 3 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10
EPFS-6 Data sheet 2 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10
Calibration Data Sheets for REMP Air Sampler Gas meter 2010 & 2011
                                                                                    Attachment


==Section 2RS6: Radioactive Gases and Liquid Effluent Treatment==
                                            18
: Procedures, Guidance Documents, and Manuals 0-ODCM-001, Offsite Dose Calculation Manual, Rev. 21
EPFS 1 Attachment 2 Trouble Report: 10BFN538, 10BFN536, 10BFN560, 10BFN561,
: NPG-SPP-05.14, Guide for Communicating Inadvertent Radiological Spills/Leaks to Outside Agencies, Rev. 0
10BFN557, 10BFN549, 10BFN506
: NPG-SPP-05.15, Fleet Ground Water Protection Program, Rev.2 0-TI-15, Radioactive Gaseous Effluent Engineering Calculations and Measurements, Rev. 15
QA Record L17111221800, TVA Quality Assurance- Nuclear Power Group- Fleet Comparative
: 0-SI-4.8.A.1-1, Liquid Effluent Permit, Rev. 74 0-SI-4.8.B.1.a.2, Airborne Effluent Release Rate by Manual Sampling When a Gaseous Effluent Monitor is Inoperable, Rev. 31 0-SI-4.8.B.2-1, Airborne Effluent Analysis - Particulate and Charcoal Filter Analysis, Rev. 37 0-SI-4.8.B.2-5, Airborne Effluent Analysis - Monthly Tritium, Rev. 30 0-SI-4.8.B.2-8, Airborne Effluent Analysis - Stack Noble Gas, Rev. 12 0-SI-4.8.B.2-4, Airborne Effluent Analysis - Monthly Gamma Isotopic, Rev. 30
Report SSA1107, 12/20/11
: CI-714, Particulate and Charcoal Filter Sampling and Analysis, Rev. 30
CAP Documents
: CI-738, Sampling Effluent Monitors (CAMS) for Tritium and Gamma Isotopics, Rev. 31 0-SI-2.1-2, Airborne Effluent Radiation Monitor Source Checks, Rev. 45 1-SIMI-90B, Radiation Monitoring System Scaling and Setpoint Documents, Rev. 41 2010 Radiological Effluent Release Report Attachment 2011 Radiological Effluent Release Report 2002 Radiological Effluent Release Report - Abnormal Release Addendum
PER 259776- The BFN REMP air filter and charcoal cartridge samples invalid
: Records and Data Reviewed
PER 366333- Loss of power to REMP air samplers
: Browns Ferry UFSAR Chapter 9 0-SR-3.6.4.3.2(A)-SBGTS Iodine Removal Efficiency (Train-A),
PER 411549- REMP TLDs
: 8/23/2010 0-SR-3.6.4.3.2(A)-SBGTS Iodine Removal Efficiency (Train-A),
PER 450297- REMP sample not analyzed and not recorded in PER
: 7/13/2011
PER 515446- REMP sample
: Gaseous Release Permits:
Section 2RS8: Radioactive Material Processing and Transportation
: 120323.030.020.G, 120315.037.020.G, 120350.030.021.G, 20328.032.020.G, 120333.043.019.G, 120340.046.020.G, 120330.040.025.G Surveillance Task Sheet: 0-SI-4.8.B.2-1- Airborne Effluent Analysis- Particulate & Charcoal Filter Analysis, 5/1/2012 System Health Reports, Each Unit System 66 - Off-Gas,
Procedures, Manuals, and Guides
: 2/1/2011-1/31/2012 System Health Report, System 77 -Radwaste, 10/1/2011-1/31/2012 System Health Report, Each Unit System 90- Radiation Monitoring, 10/1/2011-1/31/2012 Cross-Check Analysis Data:
Energy Solutions Procedure, FO-OP-022, Ecodex Precoat/Powdex/Solka-Floc/Diatomaceous
: 1st Quarter 2010 through 2nd Quarter 2011 Chemistry Focused Self Assessment Report -
    Earth/Zeolite Dewatering Procedure for Energy Solutions 14-215 or Smaller Liners, Rev. 23
: BFN-CEM-F-11-001, Performed 6/6-17/2011
Radioactive Material Shipment Manual (RMSM), Volume I, Rev. 40
: White paper documenting Ground Water Monitoring in 2010 and 2011 with results
Radioactive Material Shipment Manual (RMSM), Volume II, Rev. 42
: CAP Documents
Radioactive Material Shipment Manual (RMSM), Volume III, Rev. 39
: PER 257903 2-RM-090-013D, RCW Effluent Offline Rad Monitor alarmed on Hi Rad Setpoint
RWI-001, Administration of the Radioactive Material and Radwaste Packaging and
: PER 313929 1Q FY11 Radwaste water processing and effluents continues to be problem areas.
    Transportation Program, Rev 9
: PER 324700 Unit 3 Station Sump tritium results from the sample obtained 1/18/2011
RWTP-102, Use of Casks, Rev. 2
: PER359503 Unmonitored release at the gas stack
RWI-111, Storage of Radioactive Waste and Materials, Rev. 18
: PER 367604, Insufficient sample equipment for inop Effluent CAM monitors
RWI-112, Container Markings, Rev. 2
: PER 532416, Possible release path to Waters of the US
0-OI-77G, Duratek Procedure FO-OP-32, Set Up and Operating Procedure for the RDS-1000
    Unit at TVA Browns Ferry, Rev. 2
0-PCP-001, Process Control Program Manual (PCP), Rev. 4
NPG-SPP-3.1, Corrective Action Program, Rev. 2 and Rev. 3
Shipping Records and Radwaste Data
Certificate of Compliance No. 9168 for the Model No. 8-120B, 5/25/12
Certificate of Compliance No. 9204 for the Model No. 10-160B, 5/25/12
Gamma Isotopic Analysis Results - ID # 20120227-29 [For survey 022712-29, trash dumpster],
    2/27/12
Gamma Isotopic Analysis Results - ID # 20100607-23 [NCDM Coupon 101], 6/7/10
Gamma Isotopic Analysis Results - ID # 20100607-25 [NCDM Coupon 103], 6/7/10
Gamma Isotopic Analysis Results - ID # 20100607-27RC [NCDM Coupon 047], 6/7/10
Gamma Isotopic Analysis Results - ID # 20100607-26 [NCDM Coupon 192], 6/7/10
Letter to File, Browns Ferry Nuclear Plant - Personnel Qualified to Ship Radioactive
    Material/Waste, 3/19/12
List of Radioactive Material Storage Areas [Spreadsheet]
List of Red System 077 Issues
List of Outstanding Work Orders for System 077 [Radwaste]
Liquid Radwaste System (System 077) Health Report (2/1/12 - 5/31/12), 6/19/12
Liquid Radwaste System (System 077) Health Report (10/1/2011 - 1/31/2012), 5/17/12
Project Plan, BFN Radwaste Legacy Project, Project ID: 100533, Rev. 1, 2/1/12
Qualification Matrix Report for selected individuals to verify Subpart H training
Radioactive Material Shipping logs for the period 7/10/10 to 5/17/12
                                                                                      Attachment


==Section 2RS7: Radiological Environmental Monitoring Program (REMP)==
                                          19
Radiological Survey M-20120517-23, Pre-Shipment Survey on HIC# CL40524-9
Radiological Survey M-20120620-17, Down Post, HIC transfer complete.
Radiological Survey M-20120620-19, Pre-Shipment on cask # 14-170-35
Radiological Survey M-022412-4, Other - Trash Dumpster
Radiological Survey M-022712-29, Job Coverage [Trash Dumpster]
Radiological Survey M-20120312-12, Trash Dumpster from PA
RWP12040086, Legacy Radwaste Project (LHRA), Rev. 0
Shipment 100618, Corrosion coupons in a DOT 7A container, Type A
Shipment 120401, Liquid tanker, Low Specific Activity (LSA-I)
Shipment 120455, Control Rod Drives (2 boxes), Type A
Shipment 110804, Empty 8-120A cask, Excepted package-empty
Shipment 110318, DAW (2 sealand containers), Low Specific Activity (LSA-II)
Shipment 101111, DAW (1 sealand container), Low Specific Activity (LSA-II)
Shipment 110902, Surveillance Capsule, Type A
Shipment 100326, Control Rod Drives (2 boxes), Type A
Shipment 100327, Control Rod Drives (2 boxes), Type A
Shipment 100328, Control Rod Drives (2 boxes), Type A
Shipment 120616, Dewatered Resin, Low Specific Activity (LSA-II)
10 CFR Part 61 Analyses, DAW 2012; CWPS 2012; RWCU 2010 and 2012 Preliminary;
  Thermex 2010 and 2012 Preliminary,
CAP Documents
PER 513962, Non-RCA Trash dumpster alarms truck monitor
PER 520927, Non-RCA Trash dumpster alarms truck monitor
PER 409367, Equipment Sump over flowed contaminating RW 546
PER 425240, Radwaste El. 546 posted CA due to flooding from floor drains
PER 433904, RW 546 C-zone due to Equipment Sump overflow
PER 429803, Trend of flooding RW 546 elevation
PER 451830, Entire 546 elevation of the Rad waste building flooded
PER 456136, RW elevation 546 was flooded again spreading more contamination
PER 533414, 10CFR61 samples do not include a RWCU Sample
PER 441666, Intruder brakin at Low Level Radwaste yard
PER 254001, ATIS Radwaste Shipping Task tracking problem
PER 343736, Radioactive Material stored for years without disposition determination
PER 431466, Received notification that torque values were incorrect upon receipt of ISP
  capsule
PER 236118, Two boxes of Used Control Rod Drives Shipped to GEH Improperly
PER 453834, Adverse Trend of flooding RW 546 elevation
Apparent Cause Evaluation Report, PER 453834, 10/28/11
PERs written by licensee during inspection activities:
SR 568025, O-OI-77E needs to be revised to correct references to procedures that are no
  longer in existence.
SR 570902, PER 236118 needs to be revisited. Upon review, the corrective actions were
  inadequate.
SR 571151, PER 431466 needs to be revisited. Upon review, the corrective actions were
  inadequate.
                                                                                    Attachment


===Procedures===
                                          20
and Guidance Documents Cl-420, Collection of Radiological Environmental Monitoring Samples, Revision 03
Section 4OA1: Performance Indicator Verification
: EPFS-8, Servicing of Radiological Water Samplers, Revision 2
3-47E812-1, Flow Diagram for HPCI, Rev. 64
: EPFS-12, Repair and Preventative Maintenance Procedure for Radiological
3-OI-73, High Pressure Coolant Injection System, Rev. 52
: EPFS-03, Servicing of Meteorological Equipment at Environmental Data Stations, Rev 15
571936; improve DEP PI advance scheduling
: EPFS-07, Radio and Meteorological Tower Inspection, Rev 4
572831; PAR development in licensed operator training PI opportunities
: EPFS-06, Calibration of Environmental Data Station Data Logger and Sonic Channels, Rev 16 Environmental Monitoring Air Sampling System, Rev 01
BFN-50-7073, Design Criteria Document for the HPCI system, Rev. 22
: EMSTD-01, Environmental Radiological Monitoring Program, R25
CECC EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 41
: Records and Data Reviewed
Consolidated Date Entry Sheets for Units 1, 2 and 3 for the Safety System Functional Failures
: Annual Radiological Environmental Operating Report 2010 & 2011 Field Collection Sheets for June 4, 2012 Environmental Run
  (SSFF) PI
: EPFS-6 Data sheet 1 for Cal dates 3/21/12; 10/04/11; 04/13/11; 10/14/10; 08/24/10
Documentation of ANS tests for 4th quarter 2011 - 1st quarter 2012
: EPFS-6 Data sheet 6 for dates 03/21/12; 10/31/11; 10/04/11; 04/12/11; 10/14/10
Documentation of DEP opportunities for 4th quarter 2011 - 1st quarter 2012
: EPFS-6 Data sheet 5 for dates 03/22/12; 04/12/11; 10/04/11; 10/20/10
EPDP-11, Emergency Preparedness Performance Indicators, Rev. 3
: EPFS-6 Data sheet 4 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10
EPIP-2, Notification of Unusual Event, Rev. 31
: EPFS-6 Data sheet 3 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10
EPIP-3, Alert, Rev. 34
: EPFS-6 Data sheet 2 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10 Calibration Data Sheets for REMP Air Sampler Gas meter 2010 & 2011 
EPIP-4, Site Area Emergency, Rev. 33
: Attachment EPFS 1 Attachment 2 Trouble Report: 10BFN538, 10BFN536, 10BFN560, 10BFN561, 10BFN557, 10BFN549, 10BFN506 QA Record L17111221800, TVA Quality Assurance- Nuclear Power Group- Fleet Comparative Report SSA1107, 12/20/11  
LER 259/2011-006-00, Loss of Safety Function (HPCI) Due to Primary Containment Isolation.
: CAP Documents
Licensed Operator Training Scenarios 04, 17, 06, 18, 30, and 05 from 4th quarter 2011
: PER 259776- The BFN REMP air filter and charcoal cartridge samples invalid
Maintenance Rule Function Failure Report from April 1, 2011 to March 31, 2012
: PER 366333- Loss of power to REMP air samplers
NPG-SPP-02.2, Performance Indicator Program, Rev. 3
: PER 411549- REMP TLDs
NPG-SPP-03.4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting
: PER 450297- REMP sample not analyzed and not recorded in PER
  10 CFR 50.65, Rev. 01
: PER 515446- REMP sample
PER 439338 RP tech posted an area incorrectly
PER 533834 Contractor receives uptake during hydrolaze activities
PER 534086 Laborer contaminated while working in an area near where CRD header was
    being hydrolased.
RCI-39, Radiation Protection Cornerstones, Rev. 9
SR 532755, Dosimetry alarms due to being run through x-ray machine
Section 4OA2: Identification and Resolution of Problems
0-47E820-1, Flow Diagram Control Rod Drive Hydraulic System, Rev. 32
0-OI-2B, Condensate Storage and Transfer System, Rev. 76
1-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 04
2-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 14
3-47E804-1, Flow Diagram Condensate, Rev. 45
3-47E818-1, Flow Diagram Condensate Storage and Supply System, Rev. 27
3-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 19
3-47E855-1, Flow Diagram Fuel Pool Cooling System, Rev. 24
3-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 53
3-OI-78, Fuel Pool Cooling and Cleanup System, Rev. 60
3-OI-85, Control Rod Drive System, Rev. 75
3-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 11
3-POI-78, Reactor Water Letdown During Refueling Outages Using Submersible Pump/Filter,
  Rev. 06
Engineering trend report data from January 1, 2011 to December 1, 2011
Integrated Trend Report, Q1FY12, October 1  December 31, 2012
Integrated Trend Report, Q2FY12, January 1  March 31, 2011
PE-P4461A, Recirculation System Suction Plug Installation/Removal Procedure for Browns
  Ferry Nuclear Station under Project PE 00-829/1299 & 09-1614, Rev. 4
                                                                                    Attachment


==Section 2RS8: Radioactive Material Processing and Transportation Procedures, Manuals, and Guides Energy Solutions Procedure,==
                                            21
: FO-OP-022, "Ecodex
PE-P4462A, Jet Pump Plug Procedure for Browns Ferry Nuclear Station under Project PE 00-
: Precoat/Powdex/Solka-Floc/Diatomaceous Earth/Zeolite Dewatering Procedure for Energy Solutions 14-215 or Smaller Liners", Rev. 23
  829, Rev. 0
: Radioactive Material Shipment Manual (RMSM), Volume I, Rev. 40 Radioactive Material Shipment Manual (RMSM), Volume II, Rev. 42 Radioactive Material Shipment Manual (RMSM), Volume III, Rev. 39
PE-P4850, Operating and Maintenance Instructions for the Main Steam Line Plugs and
: RWI-001, "Administration of the Radioactive Material and Radwaste Packaging and Transportation Program", Rev 9
  Installation/Removal Tools for Browns Ferry Station - Project PE 998, Rev. 2
: RWTP-102, "Use of Casks", Rev. 2
PER 471366, CAP gaps to excellence plan
: RWI-111, "Storage of Radioactive Waste and Materials", Rev. 18
PER 491985, Human Performance gaps to excellence plan
: RWI-112, "Container Markings", Rev. 2 0-OI-77G, "Duratek Procedure
PER 512589, Cross-functional issue on outage-related worker practices
: FO-OP-32, Set Up and Operating Procedure for the
PER 539854, Engineering has documented several inappropriate action closures
: RDS-1000 Unit at TVA Browns Ferry", Rev. 2 0-PCP-001, "Process Control Program Manual (PCP)", Rev. 4
PER 563559, QA identified trend on BFN Fire Operations Training
: NPG-SPP-3.1, "Corrective Action Program", Rev. 2 and Rev. 3
RPT-CAP011, Gognos PER Word Search report from Jan 1, 2012 to June 29, 2012
: Shipping Records and Radwaste Data Certificate of Compliance No. 9168 for the Model No. 8-120B, 5/25/12
Section 4OA3: Event Follow-up
: Certificate of Compliance No. 9204 for the Model No. 10-160B, 5/25/12 Gamma Isotopic Analysis Results - ID #
0-TI-230V, Vibration Program, Rev. 10
: 20120227-29 [For survey
0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -
: 022712-29, trash dumpster], 2/27/12 Gamma Isotopic Analysis Results - ID #
  10CFR50.65, Rev. 38
: 20100607-23 [NCDM Coupon 101], 6/7/10 Gamma Isotopic Analysis Results - ID #
1-SR-3.3.8.2.1(A), RPS Circuit Protector Calibration/Functional Test For 1A1 and 1A2, Rev. 6
: 20100607-25 [NCDM Coupon 103], 6/7/10
3-AOI-100-1, Reactor Scram, Rev. 58
: Gamma Isotopic Analysis Results - ID # 20100607-27RC [NCDM Coupon 047], 6/7/10 Gamma Isotopic Analysis Results - ID #
Browns Ferry - Emergency Diesel Generator System Vulnerability to Functional Failure
: 20100607-26 [NCDM Coupon 192], 6/7/10 Letter to File, "Browns Ferry Nuclear Plant - Personnel Qualified to Ship Radioactive Material/Waste", 3/19/12 List of Radioactive Material Storage Areas [Spreadsheet] List of Red System 077 Issues List of Outstanding Work Orders for System 077 [Radwaste]
    Assessment, dated May 7, 2009
: Liquid Radwaste System (System 077) Health Report (2/1/12 - 5/31/12), 6/19/12 Liquid Radwaste System (System 077) Health Report (10/1/2011 - 1/31/2012), 5/17/12 Project Plan, BFN Radwaste Legacy Project, Project ID:
Design Criteria BFN-50-7082, Standby Diesel Generator, Rev. 16
: 100533, Rev. 1, 2/1/12 Qualification Matrix Report for selected individuals to verify Subpart H training Radioactive Material Shipping logs for the period 7/10/10 to 5/17/12 
Drawing 1-45E641-3, Instr & Controls Power Sys Schematic Diagram SH-3, Rev. 5
: Attachment Radiological Survey M-20120517-23, Pre-Shipment Survey on HIC# CL40524-9 Radiological Survey M-20120620-17, Down Post, HIC transfer complete. Radiological Survey M-20120620-19, Pre-Shipment on cask # 14-170-35 Radiological Survey M-022412-4, Other - Trash Dumpster Radiological Survey M-022712-29, Job Coverage [Trash Dumpster] Radiological Survey M-20120312-12, Trash Dumpster from PA RWP12040086, Legacy Radwaste Project (LHRA), Rev. 0 Shipment
Drawing, 0104D3695-1, Isolated Phase Bus Return Air Duct, dated 1/20/12
: 100618, Corrosion coupons in a DOT 7A container, Type A Shipment
Electro-Motive Vibration Guidelines Industrial Power Units, letter dated October 29, 1982
: 120401, Liquid tanker, Low Specific Activity (LSA-I)
EMD Power Systems Owners Group Meeting, Diesel Generator Vibration Acceptable Criteria,
: Shipment
    dated June 26-28, 1991
: 120455, Control Rod Drives (2 boxes), Type A Shipment
FSAR Section 11, Power Conversion Systems, BFN-24
: 110804, Empty 8-120A cask, Excepted package-empty Shipment
FSAR Section 8.4, Normal Auxiliary Power System, BFN-24
: 110318, DAW (2 sealand containers), Low Specific Activity (LSA-II) Shipment
FSAR Section 8.5, Standby AC Power Supply and Distribution, BFN-24
: 101111, DAW (1 sealand container), Low Specific Activity (LSA-II) Shipment
Main Control Room Logs
: 110902, Surveillance Capsule, Type A Shipment
NPG-SPP-06.2, Preventive Maintenance, Rev.0
: 100326, Control Rod Drives (2 boxes), Type A Shipment
NPG-SPP-06.2, Preventive Maintenance, Rev.04
: 100327, Control Rod Drives (2 boxes), Type A
NPG-SPP-09.18, Integrated Equipment Reliability Program, Rev. 02
: Shipment
NPG-SPP-09.18.1, System Vulnerability Review Process (MCIP Reviews), Rev. 4
: 100328, Control Rod Drives (2 boxes), Type A Shipment
NPG-SPP-09.18.2, Equipment Reliability Classification, Rev. 0
: 120616, Dewatered Resin, Low Specific Activity (LSA-II) 10 CFR Part 61 Analyses,
NPG-SPP-09.18.2, Equipment Reliability Classification, Rev. 01
: DAW 2012; CWPS 2012; RWCU 2010 and 2012 Preliminary; Thermex 2010 and 2012 Preliminary, 
NPG-SPP-2.3, Operating Experience Program, Rev. 3
: CAP Documents
OE25284 - Emergency Diesel Generator Governor Drive Oil Supply Line Sheared, North Anna
: PER 513962, Non-RCA Trash dumpster alarms truck monitor
    1 and 2
: PER 520927, Non-RCA Trash dumpster alarms truck monitor
Operations Standing Order 174, Rev. 1, To establish Operations Department expectation when
: PER 409367, Equipment Sump over flowed contaminating
    as-found data is outside of acceptable regulatory or programmatic requirements
: RW 546'
PER 131365, Out of Tolerance Time Delay Relay
: PER 425240, Radwaste El. 546' posted CA due to flooding from floor drains
PER 151812, RPS Circuit Protector Failed Acceptance Criteria
: PER 433904,
PER 178286, Acceptance Criteria Failed
: RW 546' C-zone due to Equipment Sump overflow
PER 248513, Failed Acceptance Criteria Step 7.2 (28)
: PER 429803, Trend of flooding
PER 362395, Oil Leak Resulting in Emergency Shutdown of C DG
: RW 546' elevation
PER 391479, Classification of System 55 Power Supplies
: PER 451830, Entire 546' elevation of the Rad waste building flooded
PER 413140, 1A1 RPS Circuit Protector Undervoltage Trips
: PER 456136, RW elevation 546' was flooded again spreading more contamination
PER 438808, Unknown Object Found in U3 Phase Bus Duct
: PER 533414, 10CFR61 samples do not include a RWCU Sample
                                                                                      Attachment
: PER 441666, Intruder brakin at Low Level Radwaste yard
: PER 254001, ATIS Radwaste Shipping Task tracking problem
: PER 343736, Radioactive Material stored for years without disposition determination
: PER 431466, Received notification that torque values were incorrect upon receipt of ISP capsule
: PER 236118, Two boxes of Used Control Rod Drives Shipped to GEH Improperly
: PER 453834, Adverse Trend of flooding
: RW 546 elevation Apparent Cause Evaluation Report,
: PER 453834, 10/28/11
: PERs written by licensee during inspection activities:
: SR 568025, O-OI-77E needs to be revised to correct references to procedures that are no longer in existence.
: SR 570902,
: PER 236118 needs to be revisited.
: Upon review, the corrective actions were inadequate.
: SR 571151,
: PER 431466 needs to be revisited.
: Upon review, the corrective actions were inadequate.
: Attachment


==Section 4OA1: Performance Indicator Verification==
                                          22
: 3-47E812-1, Flow Diagram for HPCI, Rev. 64
PER 440359, U3 Scrammed on September 28, 2011 at 0414
: 3-OI-73, High Pressure Coolant Injection System, Rev. 52
PER 442914, Evaluation of Surveillance Data from Past Performances
: 571936; improve DEP PI advance scheduling
PER 486780, 3C1 Relay Results Below Acceptance Criteria
: 2831; PAR development in licensed operator training PI opportunities
PER 496592, Fire in Annunciator Panel 3-XA-55-5A
: BFN-50-7073, Design Criteria Document for the HPCI system, Rev. 22 CECC
SPP-3.9, Operating Experience Program, Revs. 4 and 5
: EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 41 Consolidated Date Entry Sheets for Units 1, 2 and 3 for the Safety System Functional Failures (SSFF) PI Documentation of ANS tests for 4th quarter 2011 - 1st quarter 2012 Documentation of DEP opportunities for 4th quarter 2011 - 1st quarter 2012
SPP-6.2, Preventive Maintenance, Rev.09
: EPDP-11, Emergency Preparedness Performance Indicators, Rev. 3
SPP-9.18.2, Equipment Reliability Classification, Rev. 00
: EPIP-2, Notification of Unusual Event, Rev. 31
SR 496007, U-3 Annunciator Panel 9-5A Fire and AOI entry
: EPIP-3, Alert, Rev. 34
Technical Specification and Bases 3.3.8.2, Reactor Protection System (RPS) Electric Power
: EPIP-4, Site Area Emergency, Rev. 33
  Monitoring, Amendment 263 and Rev. 43, respectively
: LER 259/2011-006-00, Loss of Safety Function (HPCI) Due to Primary Containment Isolation. Licensed Operator Training Scenarios 04, 17, 06, 18, 30, and 05 from 4th quarter 2011 Maintenance Rule Function Failure Report from April 1, 2011 to March 31, 2012
Technical Specifications and Bases 3.8, Electrical Power System, Amendment 266
: NPG-SPP-02.2, Performance Indicator Program, Rev. 3
Technical Specifications and Bases Section 3.8, Electrical Power Systems, Amendment 280
: NPG-SPP-03.4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting
  and Rev. 52 respectively
: 10
TVA-NQA-PLN89-A, Nuclear Quality Assurance Plan (NQAP), Rev. 23, 24, 25 and 26
: CFR 50.65, Rev. 01
                                                                                  Attachment
: PER 439338 RP tech posted an area incorrectly
: PER 533834 Contractor receives uptake during hydrolaze activities
: PER 534086 Laborer contaminated while working in an area near where CRD header was being hydrolased.
: RCI-39, Radiation Protection Cornerstones, Rev. 9
: SR 532755, Dosimetry alarms due to being run through x-ray machine


==Section 4OA2: Identification and Resolution of Problems==
                              LIST OF ACRONYMS
: 0-47E820-1, Flow Diagram Control Rod Drive Hydraulic System, Rev. 32 0-OI-2B, Condensate Storage and Transfer System, Rev. 76
ADAMS - Agencywide Document Access and Management System
: 1-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 04 2-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 14 3-47E804-1, Flow Diagram Condensate, Rev. 45 3-47E818-1, Flow Diagram Condensate Storage and Supply System, Rev. 27 3-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 19
ADS  - Automatic Depressurization System
: 3-47E855-1, Flow Diagram Fuel Pool Cooling System, Rev. 24 3-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 53 3-OI-78, Fuel Pool Cooling and Cleanup System, Rev. 60 3-OI-85, Control Rod Drive System, Rev. 75 3-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 11 3-POI-78, Reactor Water Letdown During Refueling Outages Using Submersible Pump/Filter, Rev. 06 Engineering trend report data from January 1, 2011 to December 1, 2011 Integrated Trend Report, Q1FY12, October 1
ALARA  As Low As Reasonably Achievable
: December 31, 2012 Integrated Trend Report, Q2FY12, January 1
ARM  - area radiation monitor
: March 31, 2011
CAD  - containment air dilution
: PE-P4461A, Recirculation System Suction Plug Installation/Removal Procedure for Browns Ferry Nuclear Station under Project
CAP  - corrective action program
: PE 00-829/1299 & 09-1614, Rev. 4 
CCW  - condenser circulating water
: Attachment
CFR  - Code of Federal Regulations
: PE-P4462A, Jet Pump Plug Procedure for Browns Ferry Nuclear Station under Project
CoC  - certificate of compliance
: PE 00-829, Rev. 0
CRD  - control rod drive
: PE-P4850, Operating and Maintenance Instructions for the Main Steam Line Plugs and Installation/Removal Tools for Browns Ferry Station - Project
CS    - core spray
: PE 998, Rev. 2
DAC    Derived Air Concentration
: PER 471366, CAP gaps to excellence plan
DCN  - design change notice
: PER 491985, Human Performance gaps to excellence plan
ED      Electronic Dosimeter
: PER 512589, Cross-functional issue on outage-related worker practices
EDG  - emergency diesel generator
: PER 539854, Engineering has documented several inappropriate action closures
EECW  - emergency equipment cooling water
: PER 563559, QA identified trend on BFN Fire Operations Training
FE    - functional evaluation
: RPT-CAP011, Gognos PER Word Search report from Jan 1, 2012 to June 29, 2012
FPR  - Fire Protection Report
FSAR  - Final Safety Analysis Report
HP      Health Physics
HRA    High Radiation Area
IMC  - Inspection Manual Chapter
JOG    Joint Owners Group
LER  - licensee event report
LHRA    Locked High Radiation Area
NCV  - non-cited violation
NRC  - U.S. Nuclear Regulatory Commission
NSTS    National Source Tracking System
OA      Other Activity
ODCM  - Off-Site Dose Calculation Manual
PER  - problem evaluation report
PCIV  - primary containment isolation valve
PI    - performance indicator
RCE  - Root Cause Evaluation
RCW  - Raw Cooling Water
RG    - Regulatory Guide
RHR  - residual heat removal
RHRSW - residual heat removal service water
RS      Radiation Safety
RTP  - rated thermal power
RPS  - reactor protection system
RWP  - radiation work permit
SDP  - significance determination process
SBGT  - standby gas treatment
SLC  - standby liquid control
SNM  - special nuclear material
                                                        Attachment


==Section 4OA3: Event Follow-up==
                                    24
: 0-TI-230V, Vibration Program, Rev. 10 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting - 10CFR50.65, Rev. 38 1-SR-3.3.8.2.1(A), RPS Circuit Protector Calibration/Functional Test For 1A1 and 1A2, Rev. 6
SRV  -  safety relief valve
: 3-AOI-100-1, Reactor Scram, Rev. 58 Browns Ferry - Emergency Diesel Generator System Vulnerability to Functional Failure Assessment, dated May 7, 2009 Design Criteria
SSC   - structure, system, or component
: BFN-50-7082, Standby Diesel Generator, Rev. 16 Drawing 1-45E641-3, Instr & Controls Power Sys Schematic Diagram
TI   - Temporary Instruction
: SH-3, Rev. 5
TIP   - transverse in-core probe
: Drawing, 0104D3695-1, Isolated Phase Bus Return Air Duct, dated 1/20/12 Electro-Motive Vibration Guidelines Industrial Power Units, letter dated October 29, 1982 EMD Power Systems Owners Group Meeting, Diesel Generator Vibration Acceptable Criteria, dated June 26-28, 1991 FSAR Section 11, Power Conversion Systems,
TLD     Thermoluminescent Dosimeter
: BFN-24  
TRM   - Technical Requirements Manual
: FSAR Section 8.4, Normal Auxiliary Power System,
TS   - Technical Specification(s)
: BFN-24 FSAR Section 8.5, Standby AC Power Supply and Distribution,
U1       Unit 1
: BFN-24 Main Control Room Logs
U2       Unit 2
: NPG-SPP-06.2, Preventive Maintenance, Rev.0
U3       Unit 3
: NPG-SPP-06.2, Preventive Maintenance, Rev.04
UFSAR - Updated Final Safety Analysis Report
: NPG-SPP-09.18, Integrated Equipment Reliability Program, Rev. 02
URI   - unresolved item
: NPG-SPP-09.18.1, System Vulnerability Review Process (MCIP Reviews), Rev. 4
VHRA Very High Radiation Area
: NPG-SPP-09.18.2, Equipment Reliability Classification, Rev. 0
WO   - work order
: NPG-SPP-09.18.2, Equipment Reliability Classification, Rev. 01
                                            Attachment
: NPG-SPP-2.3, Operating Experience Program, Rev. 3
: OE25284 - Emergency Diesel Generator Governor Drive Oil Supply Line Sheared, North Anna 1 and 2 Operations Standing Order 174, Rev. 1, To establish Operations Department expectation when as-found data is outside of acceptable regulatory or programmatic requirements
: PER 131365, Out of Tolerance Time Delay Relay
: PER 151812, RPS Circuit Protector Failed Acceptance Criteria
: PER 178286, Acceptance Criteria Failed
: PER 248513, Failed Acceptance Criteria Step 7.2 (28)
: PER 362395, Oil Leak Resulting in Emergency Shutdown of C DG
: PER 391479, Classification of System 55 Power Supplies
: PER 413140, 1A1 RPS Circuit Protector Undervoltage Trips
: PER 438808, Unknown Object Found in U3 Phase Bus Duct Attachment
: PER 440359, U3 Scrammed on September 28, 2011 at 0414
: PER 442914, Evaluation of Surveillance Data from Past Performances
: PER 486780, 3C1 Relay Results Below Acceptance Criteria
: PER 496592, Fire in Annunciator Panel 3-XA-55-5A
: SPP-3.9, Operating Experience Program, Revs. 4 and 5
: SPP-6.2, Preventive Maintenance, Rev.09
: SPP-9.18.2, Equipment Reliability Classification, Rev. 00
: SR 496007, U-3 Annunciator Panel 9-5A Fire and AOI entry Technical Specification and Bases 3.3.8.2, Reactor Protection System (RPS) Electric Power Monitoring, Amendment 263 and Rev. 43, respectively Technical Specifications and Bases 3.8, Electrical Power System, Amendment 266 Technical Specifications and Bases Section 3.8, Electrical Power Systems, Amendment 280 and Rev. 52 respectively
: TVA-NQA-PLN89-A, Nuclear Quality Assurance Plan (NQAP), Rev. 23, 24, 25 and 26
==LIST OF ACRONYMS==
: [[ADAMS]] [[- Agencywide Document Access and Management System]]
: [[ADS]] [[- Automatic Depressurization System]]
: [[ALARA]] [[As Low As Reasonably Achievable]]
: [[ARM]] [[- area radiation monitor]]
: [[CAD]] [[- containment air dilution]]
: [[CAP]] [[- corrective action program]]
: [[CCW]] [[- condenser circulating water]]
CFR - Code of Federal Regulations
CoC  - certificate of compliance
: [[CRD]] [[- control rod drive]]
: [[CS]] [[- core spray]]
: [[DAC]] [[Derived Air Concentration]]
: [[DCN]] [[- design change notice]]
: [[ED]] [[Electronic Dosimeter]]
: [[EDG]] [[- emergency diesel generator]]
: [[EECW]] [[- emergency equipment cooling water]]
: [[FE]] [[- functional evaluation]]
: [[FPR]] [[- Fire Protection Report]]
: [[FSAR]] [[- Final Safety Analysis Report]]
: [[HP]] [[Health Physics]]
: [[HRA]] [[High Radiation Area]]
: [[IMC]] [[- Inspection Manual Chapter]]
: [[JOG]] [[Joint Owners Group]]
: [[LER]] [[- licensee event report]]
: [[LHRA]] [[Locked High Radiation Area]]
: [[NCV]] [[- non-cited violation]]
: [[NRC]] [[-]]
: [[U.S.]] [[Nuclear Regulatory Commission]]
: [[NSTS]] [[National Source Tracking System]]
: [[OA]] [[Other Activity]]
: [[ODCM]] [[- Off-Site Dose Calculation Manual]]
: [[PER]] [[- problem evaluation report]]
: [[PCIV]] [[- primary containment isolation valve]]
: [[PI]] [[- performance indicator]]
: [[RCE]] [[- Root Cause Evaluation]]
: [[RCW]] [[- Raw Cooling Water]]
: [[RG]] [[- Regulatory Guide]]
: [[RHR]] [[- residual heat removal]]
: [[RHRSW]] [[- residual heat removal service water]]
: [[RS]] [[Radiation Safety]]
: [[RTP]] [[- rated thermal power]]
: [[RPS]] [[- reactor protection system]]
: [[RWP]] [[- radiation work permit]]
: [[SDP]] [[- significance determination process]]
: [[SBGT]] [[- standby gas treatment]]
: [[SLC]] [[- standby liquid control]]
SNM  - special nuclear material
Attachment
: [[SRV]] [[- safety relief valve]]
: [[SSC]] [[- structure, system, or component]]
: [[TI]] [[- Temporary Instruction]]
: [[TIP]] [[- transverse in-core probe]]
: [[TLD]] [[Thermoluminescent Dosimeter]]
TRM - Technical Requirements Manual TS - Technical Specification(s) U1 Unit 1 U2 Unit 2
U3 Unit
: [[3 UFSAR]] [[- Updated Final Safety Analysis Report]]
: [[URI]] [[- unresolved item]]
: [[VHRA]] [[Very High Radiation Area]]
: [[WO]] [[- work order]]
}}
}}

Latest revision as of 23:45, 11 November 2019

IR 05000259-12-003, 05000260-12-003, 05000296-12-003, 05000259/2012502, 05000260/2012502, 05000296/2012502; 04/01/2012 -06/30/2012; Browns Ferry Nuclear Plant, Units 1, 2 and 3; Operability Evaluations, Radioactive Solid Waste Processing an
ML12227A711
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 08/14/2012
From: Eugene Guthrie
Division Reactor Projects II
To: James Shea
Tennessee Valley Authority
References
IR-12-003, IR-12-502
Download: ML12227A711 (72)


See also: IR 05000259/2012003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

August 14, 2012

Mr. Joseph W. Shea

Vice President, Nuclear Licensing

Tennessee Valley Authority

1101 Market Street, LP 4B-C

Chattanooga, TN 37402-2801

SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION

REPORT 05000259/2012003, 05000260/2012003, 05000296/2012003,

05000259/2012502, 05000260/2012502, AND 05000296/2012502

Dear Mr. Shea:

On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection report documents

the inspection results which were discussed on July 10, August 10 and 14th, 2012, with Mr.

Keith Polson and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations, orders, and with the conditions of your

license. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

One NRC identified and 3 self revealing findings of very low safety significance (Green) were

identified during this inspection. Three of these findings were determined to involve violations of

NRC requirements. Further, a licensee-identified violation which was determined to be of very

low safety significance is listed in this report. The NRC is treating the violations as non-cited

violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy. If you contest these

non-cited violations, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington DC 20555-0001, with copies to: (1) the Regional Administrator,

Region II; (2) the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Browns

Ferry Nuclear Plant.

In addition, if you disagree with any cross-cutting aspect assignment in the report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the

Browns Ferry Nuclear Plant.

J. Shea 2

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any), will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Eugene F. Guthrie, Chief

Special Project, Browns Ferry

Division of Reactor Projects

Docket Nos.: 50-259, 50-260, 50-296

License Nos.: DPR-33, DPR-52, DPR-68

Enclosure: NRC Integrated Inspection Report 05000259/2012003,

05000260/2012003, 05000296/2012003

cc w/encl. (See page 3)

_________________________ X SUNSI REVIEW COMPLETE

OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS

SIGNATURE Via email Via email Via email Via email BRB /RA for/ BRB /RA for/ BRB /RA for/

NAME DDumbacher CStancil PNiebaum LPressley MSpeck RHamilton CDykes

DATE 08/14/2012 08/14/2012 08/14/2012 08/14/2012 08/14/2012 08/14/2012 08/14/2012

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

OFFICE RII:DRS RII:DRS RII:DRP RII:DRP

SIGNATURE Via email Via email Via email EFG /RA/

NAME RKellner MCoursey CKontz EGuthrie

DATE 07/26/2012 08/14/2012 08/14/2012 08/14/2012

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

J. Shea 3

cc w/encl: James L. McNees, CHP

K. J. Polson Director

Site Vice President Office of Radiation Control

Browns Ferry Nuclear Plant Alabama Dept. of Public Health

Tennessee Valley Authority P. O. Box 303017

Electronic Mail Distribution Montgomery, AL 36130-3017

C.J. Gannon

General Manager

Browns Ferry Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

James E. Emens

Manager, Licensing

Browns Ferry Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

Manager, Corporate Nuclear Licensing -

BFN

Tennessee Valley Authority

Electronic Mail Distribution

Edward J. Vigluicci

Assistant General Counsel

Tennessee Valley Authority

Electronic Mail Distribution

T. A. Hess

Tennessee Valley Authority

Electronic Mail Distribution

Chairman

Limestone County Commission

310 West Washington Street

Athens, AL 35611

Donald E. Williamson

State Health Officer

Alabama Dept. of Public Health

RSA Tower - Administration

Suite 1552

P.O. Box 30317

Montgomery, AL 36130-3017

J. Shea 4

Letter to Joseph W. Shea from Eugene Guthrie dated August 14, 2012

SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION

REPORT 05000259/2012003, 05000260/2012003, 05000296/2012003,

05000259/2012502, 05000260/2012502, AND 05000296/2012502

Distribution w/encl:

C. Evans, RII

L. Douglas, RII

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMBrownsFerry Resource

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-259, 50-260, 50-296

License Nos.: DPR-33, DPR-52, DPR-68

Report No.: 05000259/2012003, 05000260/2012003, 05000296/2012003,

05000259/2012502, 05000260/2012502, 05000296/2012502

Licensee: Tennessee Valley Authority (TVA)

Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3

Location: Corner of Shaw and Nuclear Plant Roads

Athens, AL 35611

Dates: April 1, 2012, through June 30, 2012

Inspectors: D. Dumbacher, Senior Resident Inspector

C. Stancil, Senior Resident Inspector

P. Niebaum, Resident Inspector

L. Pressley, Resident Inspector

M. Speck, Senior Emergency Preparedness Inspector (1EP2, 1EP3,

1EP5, 4OA1)

R. Hamilton, Senior Health Physicist (2RS1, 2RS2, 2RS6, 4OA1)

C. Dykes, Health Physicist (2RS7)

R. Kellner, Health Physicist (2RS8)

M. Coursey, Reactor Inspector (1R08)

Approved by: Eugene F. Guthrie, Chief

Reactor Projects Special Branch

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000259/2012003, 05000260/2012003, 05000296/2012003, 05000259/2012502,

05000260/2012502, 05000296/2012502; 04/01/2012 -06/30/2012; Browns Ferry Nuclear Plant,

Units 1, 2 and 3; Operability Evaluations, Radioactive Solid Waste Processing and Radioactive

Material Handling, Storage, and Transportation, and Event Follow-Up.

The report covered a three month period of inspection by resident and regional inspectors. Four

findings were identified. The significance of most findings is identified by their color (Green,

White, Yellow, and Red) using Inspection Manual Chapter (IMC) 0609, Significance

Determination Process (SDP); and, the cross-cutting aspects were determined using IMC

0310, Components Within the Cross-Cutting Areas. Findings for which the SDP does not

apply may be Green or be assigned a severity level after NRC management review. The NRCs

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process Revision 4, dated December 2006.

NRC Identified and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. A self-revealing finding (FIN) was identified for the licensees failure to

perform preventive maintenance on the Unit 3 Main Control Room (MCR)

annunciator power supplies. As a result, a power supply failed which led to a fire in

annunciator panel 3-X-55-5A in the Unit 3 control room. The licensee initiated

actions to extinguish the fire, replace the two affected power supplies and develop a

preventive maintenance program to replace the power supplies every ten years.

Additional corrective actions to replace all power supplies that have been installed for

more than four years are pending. This was captured in the licensees corrective

action program as problem event report (PER) 496592.

The performance deficiency was determined to be more than minor because it was

considered sufficiently similar to example 4.f of Inspection Manual Chapter (IMC)

0612, Appendix E, for an issue that resulted in a fire hazard in a safety-related area

of the plant. The finding was associated with the Initiating Events Cornerstone and

required a phase 3 analysis in accordance with IMC 0609 because the finding

increased the likelihood of, and actually caused, a fire in the Unit 3 control room.

The phase 3 analysis determined that without an impact to additional plant

equipment, or a major impact on human action failure rates, the finding was

determined to be Green. The cause of this finding was related to the cross cutting

aspect of Problem Identification in the Corrective Action Program component of the

Problem Identification and Resolution area because the licensee should have

recognized the electrolytic capacitors were installed beyond their recommended

service life and scheduled replacement prior to their failure P.1(a). (Section

4OA3.6)

Enclosure

3

Cornerstone: Mitigating Systems

5.4.1.a was identified for the licensees failure to maintain an Emergency Equipment

Cooling Water (EECW) pump flood barrier in accordance with written procedures

which resulted in the inoperability of two other safety related pumps. The licensee

immediately restored the flood protection configuration of the C Residual Heat

Removal Service Water (RHRSW) pump room by properly re-installing the flood

protection cover and permanently stenciled the aluminum plate with the required

procedure for installation. The licensee entered this issue into their corrective action

program as PER 532050.

The finding was more than minor because it was associated with the Mitigating

Systems cornerstone attribute of Protection Against External Events, and adversely

affected the cornerstone objective to ensure the availability, reliability, and capability

of RHRSW pumps to perform their intended safety function during a design basis

flooding event. Specifically, the improper re-installation of an external flood

protection cover resulted in the inoperability of two Residual Heat Removal Service

Water (RHRSW) pumps. The significance of this finding was evaluated in

accordance with the IMC 0609 Attachment 4, Phase 1- Initial Screening and

Characterization of Findings, which required a Phase 3 analysis because the finding

involved the degradation of equipment designed to mitigate a flooding event and it

was risk significant due to external initiating event core damage sequences. The

finding was determined to be Green because of the short exposure time, and the low

likelihood of the flood. The cause of this finding was directly related to the cross

cutting aspect of Supervisory Oversight in the Work Practices component of the

Human Performance area, because of the foremans assumption that workers knew

to restore the flood protection cover to meet procedural requirements without a

formal pre-job brief H.4(c). (Section 1R15)

Cornerstone: Public Radiation Safety

  • Green. A self-revealing non-cited violation (NCV) of 10 CFR 71.5, Transportation of

Licensed Material, was identified by inspectors for the licensees failure to comply

with Department of Transportation (DOT) regulations during shipment of radioactive

materials. Specifically, the licensee failed to ensure proper packaging of two DOT 7A

Type A packages as required by Department of Transportation (DOT) regulations in

49 CFR 173.475, Quality Control Requirements Prior To Each Shipment Of Class 7

(Radioactive) Materials. This issue has been entered into the licensees corrective

action program as SR 570902.

The finding was more than minor because it is associated with the Public Radiation

Safety Cornerstone, Plant Facilities/Equipment and Instrumentation attribute,

involving transportation packaging and adversely affected the cornerstone objective,

to ensure adequate protection of public health and safety from exposure to

radioactive materials released into the public domain as a result of routine civilian

nuclear reactor operation. Specifically, the failure to correctly secure the package

Enclosure

4

contents to prevent movement could have resulted in damage or failure of the

container during transportation. The finding was determined to be of very low safety

significance (Green) because it did not involve radiation limits being exceeded, a

package breach, a certificate of compliance issue, a low-level burial ground non-

conformance, or a failure to make emergency notifications. The cause of this finding

was directly related to the cross cutting aspect of Documents, Procedures and

Component Labeling in the Resources component of the Human Performance area

because the licensee did not effectively incorporate package design specifications

into their transportation program to ensure that all internal restraining devices are

correctly installed to secure the CRDM in place to prevent damage to the transport

package. (H.2(c)) (Section 2RS8)

  • Green. A self-revealing non-cited violation (NCV) of 10 CFR 71.5, Transportation of

Licensed Material, was identified by inspectors for the licensees failure to comply

with Department of Transportation (DOT) regulations during shipment of radioactive

materials. Specifically, the licensee failed to ensure proper closure of a DOT 7A Type

A package as required by Department of Transportation (DOT) regulations in 49

CFR 173.475, Quality Control Requirements Prior To Each Shipment Of Class 7

(Radioactive) Materials. This issue has been entered into the licensees corrective

action program as SR 571151.

The finding was more than minor because it is associated with the Public Radiation

Safety Cornerstone, Plant Facilities/Equipment and Instrumentation attribute,

involving transportation packaging and adversely affected the cornerstone objective,

to ensure adequate protection of public health and safety from exposure to

radioactive materials released into the public domain as a result of routine civilian

nuclear reactor operation. Specifically, the failure to apply the correct torque to the

package closure bolts could have resulted in incomplete sealing of the container or

failure of the cover bolts during transportation. The finding was determined to be of

very low safety significance (Green) because it did not involve radiation limits being

exceeded, a package breach, a certificate of compliance issue, a low-level burial

ground non-conformance, or a failure to make emergency notifications. The cause

of this finding was directly related to the cross cutting aspect of Documents,

Procedures and Component Labeling in the Resources component of the Human

Performance area because the licensee did not effectively incorporate the vendor

provided container loading and shipping instructions into their work package and

transportation program to ensure correct torque values were used to close the

shipping container. (H.2(c)) (Section 2RS8).

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at full power for most of the report period except for an unplanned downpower

on June 29, 2012, to 75 percent power to reduce load on the B Phase Main Bank Transformer

due to a lifting oil pressure relief. The unit returned to full power on June 30, 2012.

Unit 2 operated at full power for most of the report period except for one planned and one

unplanned downpower. On April 20, 2012, the unit performed a planned downpower to 66

percent power for rod pattern adjustment, scram time testing and turbine valve testing. The unit

returned to full power on April 22nd. On May 15, 2012, the unit performed an unplanned

downpower to 92 percent power to insert control rod 30-51 for scram outlet valve repair and

returned to full power the same day.

Unit 3 operated at full power for most of the report period except for one planned downpower,

one manual and two automatic scrams, and one unplanned downpower. On April 6, 2012, the

unit was shutdown for a scheduled refueling outage that lasted 49 days. The unit was restarted

on May 19th. On May 22nd, an automatic scram occurred from 19.5 percent power with the

main turbine generator offline due to a 3A Unit Station Service Transformer differential relay trip

caused by incorrect relay setting. On May 24, 2012, during reactor startup and heatup an

unplanned manual scram occurred as a result of a partial control rod insertion caused by a

combination of a signal spike and an inappropriate operator downrange on separate

intermediate power range monitors. The unit restarted the same day. On May 29, 2012, a main

generator current transformer manufactured and installed with reverse polarity caused an

automatic scram from 75 percent power. The unit restarted on June 2nd and returned to full

power on June 5th. On June 6th, the unit performed an unplanned downpower from 96 percent

power to 75 percent power to remove the 3B condensate booster pump with high moisture in its

oil system from service. The unit returned to full power on June 8, 2012.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Offsite and Alternate Alternating Current (AC) Power Systems Readiness

a. Inspection Scope

Prior to the summer season, inspectors reviewed electrical power design features, onsite

risk and work management procedures, and corporate transmission and power supply

procedures to verify appropriate operational oversight and assurance of continued

availability of offsite and alternate AC power systems. Inspectors verified that

communications protocols existed between the transmission system operator and

Browns Ferry Nuclear Plant for coordination of off-normal and emergency events

affecting the plant, event details, estimates of return-to-service times, and notifications of

grid status changes. Inspectors also verified that procedures included controls to

Enclosure

6

adequately monitor both offsite AC power systems (including post-trip voltages) and

onsite alternate AC power systems for availability and reliability. Furthermore,

inspectors interviewed onsite licensed operators and offsite transmission personnel to

determine their understanding and implementation of the power monitoring and

assessment process. Inspectors reviewed the material condition of offsite AC power

systems and onsite alternate AC power systems to the plant, including switchyard and

transformers. This review included review of outstanding work orders affecting these

systems and a walkdown of the switchyard with operations personnel to ensure the

systems will continue to provide appropriate as designed capabilities. This activity

constituted one Offsite and AC Readiness sample.

b. Findings

No findings were identified.

.2 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

Prior to and during the onset of hot weather conditions, the inspectors reviewed the

licensees implementation of 0-GOI-200-3, Hot Weather Operations. The inspectors

also reviewed the Hot Weather Discrepancy Log; and discussed implementation of

0-GOI-200-3 with responsible Operations personnel and management. Furthermore, the

inspectors conducted walkdowns of potentially affected risk significant equipment

systems located in the Unit 1 and 2 Diesel Generator Building, and the Unit 3 Diesel

Generator Building. The inspectors also performed a walkdown of the Standby Gas

Treatment (SBGT) Building. This activity constituted one Readiness for Seasonal

Extreme Weather sample.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted three partial equipment alignment walkdowns to evaluate the

operability of selected redundant trains or backup systems, listed below, while the other

train or subsystem was inoperable or out of service. The inspectors reviewed the

functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system

operating procedures, and Technical Specifications to determine correct system lineups

for the current plant conditions. The inspectors performed walkdowns of the systems to

verify that critical components were properly aligned and to identify any discrepancies

which could affect operability of the redundant train or backup system. This activity

constituted three Equipment Alignment inspection samples.

Enclosure

7

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Fire Protection Tours

a. Inspection Scope

The inspectors reviewed licensee procedures, Nuclear Power Group Standard Programs

and Processes NPG-SPP-18.4.7, Control of Transient Combustibles, and NPG-SPP-

18.4.6, Control of Fire Protection Impairments, and conducted a walkdown of the four

fire areas (FA) and fire zones (FZ) listed below. Selected FAs/FZs were examined in

order to verify licensee control of transient combustibles and ignition sources; the

material condition of fire protection equipment and fire barriers; and operational lineup

and operational condition of fire protection features or measures. Furthermore, the

inspectors reviewed applicable portions of the Fire Protection Report, Volumes 1 and 2,

including the applicable Fire Hazards Analysis, and Pre-Fire Plan drawings, to verify that

the necessary firefighting equipment, such as fire extinguishers, hose stations, ladders,

and communications equipment, was in place. This activity constituted four Fire

Protection inspection samples.

  • Unit 2 Reactor Building Elevations 519, 541, and 565 west of column line R11 (FZ 2-

1)

rooms, EL 565, and 593 near column R15-S and R21-S (FZ 3-3)

  • Unit 1, Control Building, EL 593 (FA 16)
  • Unit 1,2, and 3 Turbine Building Deluge Sprinkler Control Stations Affecting Control

Bay (FA 25)

b. Findings

No findings were identified.

Enclosure

8

1R07 Heat Sink Performance

.1 Annual Review

a. Inspection Scope

The inspectors examined activities associated with Unit 3 RHR Heat Exchangers. The

inspectors also reviewed design basis documents, calculations, test procedures,

maintenance procedures and preventive maintenance procedures and results to

evaluate the licensees program for maintaining heat sinks in accordance with the

licensing basis. Specifically inspectors reviewed modifications performed on the Unit 3

RHR Heat Exchanger Flanges. Inspectors reviewed available performance testing

documentation of the 3A and 3C RHR Heat Exchangers.

In addition, the inspectors reviewed the licensees implementation of the GL 89-13

program. Inspectors reviewed associated PERs and corrective actions to verify that the

licensee was identifying issues and correcting them. The inspectors performed

walkdowns of key components of the Unit 3 RHR system to verify material conditions

were acceptable and physical arrangement matched procedures and drawings. This

activity constituted one Annual Heat Sink sample.

b. Findings

No findings were identified.

1R08 Inservice Inspection (ISI) Activities (71111.08G, Unit 3)

a. Inspection Scope

Non-Destructive Examination (NDE) Activities and Welding Activities: From April 16 to

April 20, 2012, the inspectors conducted an on-site review of the implementation of the

licensees Inservice Inspection (ISI) Program for monitoring degradation of the reactor

coolant system, emergency feedwater systems, risk-significant piping and components,

and containment systems in Unit 3. The inspectors activities included a review of non-

destructive examinations (NDEs) to evaluate compliance with the applicable edition of

the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel

Code (BPVC),Section XI (Code of record: 2001 Edition with 2003 Addenda), and to

verify that indications and defects (if present) were appropriately evaluated and

dispositioned in accordance with the requirements of the ASME Code,Section XI,

acceptance standards.

The inspectors directly observed the following NDE mandated by the ASME Code to

evaluate compliance with the ASME Code Section XI and Section V requirements and, if

any indications and defects were detected, to evaluate if they were dispositioned in

accordance with the ASME Code or an NRC-approved alternative requirement.

Enclosure

9

(LPCI) Loop I Inlet

  • UT Exam of Weld DSRHR-03-04, 3-HCV-74-55, 24 in. inlet for Recirculation Loop B

The inspectors reviewed records of the following NDEs mandated by the ASME Code

Section XI to evaluate compliance with the ASME Code Section XI and Section V

requirements and, if any indications and defects were detected, to evaluate if they were

dispositioned in accordance with the ASME Code or an NRC-approved alternative

requirement.

  • UT Exam of weld DRHR-03-12, 3-FCV-74-67, LPCI Loop II Inlet
  • EVT of BFN-3-RPV-068-RA048 Standpipe in Unit 3 Steam Separator
  • EVT of BFN-3-RPV-068-RA050 U3 Feedwater Sparger End Brackets

The inspectors reviewed associated documents for the welding activities referenced

below in order to evaluate compliance with procedures and the ASME Code. The

inspectors reviewed the work order, repair and replacement plan, weld data sheets,

welding procedures, procedure qualification records, welder performance qualification

records, and NDE reports.

  • Work Order 04-719493-003, 3-FCV-073-016 HPCI Turbine Steam Supply Valve
  • Work Order 08-718716-004, Replace Strain Gauges on MS Lines

During non-destructive surface and volumetric examinations performed since the

previous refuelling outage, the licensee did not identify any relevant indications that were

analytically evaluated and accepted for continued service. Therefore, no NRC review

was completed for this inspection procedure attribute.

Identification and Resolution of Problems: The inspectors performed a review of a

sample of ISI-related problems which were identified by the licensee and entered into

the corrective action program as Problem Evaluation Reports (PERs). The inspectors

reviewed the PERs to confirm the licensee had appropriately described the scope of the

problem, and had initiated corrective actions. The review also included the licensees

consideration and assessment of operating experience events applicable to the plant.

The inspectors performed this review to ensure compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the report attachment.

b. Findings

No findings were identified.

Enclosure

10

1R11 Licensed Operator Requalification

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On June 11, 2012, the inspectors observed an as-found licensed operator requalification

simulator examination according to Unit 2 Simulator Exercise Guide OPL173.S039. The

scenario involved Partial Loss of Reactor Building Closed Cooling Water, Loss of I & C

Bus B, Anticipated Transient without Scram (ATWS), Lower Water Level (C-5) for Power

Control with Bypass Valves.

The inspectors specifically evaluated the following attributes related to the operating

crews performance:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of Abnormal Operating Instructions (AOIs), and

Emergency Operating Instructions (EOIs)

  • Timely and appropriate Emergency Action Level declarations per Emergency Plan

Implementing Procedures (EPIP)

  • Control board operation and manipulation, including high-risk operator actions
  • Command and Control provided by the Unit Supervisor and Shift Manager

The inspectors attended the post-examination critique to assess the effectiveness of the

licensee evaluators and to verify that licensee-identified issues were comparable to

issues identified by the inspector. The inspectors reviewed simulator physical fidelity

(i.e., the degree of similarity between the simulator and the reference plant control room,

such as physical location of panels, equipment, instruments, controls, labels, and related

form and function). This activity counts for one Observation of Requalification Activity

inspection sample.

b. Findings

No findings were identified.

.2 Control Room Observations

a. Inspection Scope

Inspectors observed and assessed licensed operator performance in the plant and main

control room, particularly during periods of heightened activity or risk and where the

activities could affect plant safety. Inspectors reviewed various licensee policies and

procedures such as OPDP-1, Conduct of Operations, NPG-SPP-10.0, Plant Operations

and GOI-100-12, Power Maneuvering.

Enclosure

11

Inspectors utilized activities such as post maintenance testing, surveillance testing and

refueling and other outage activities to focus on the following conduct of operations as

appropriate;

  • Operator compliance and use of procedures.
  • Control board manipulations.
  • Communication between crew members.
  • Use and interpretation of plant instruments, indications and alarms.
  • Use of human error prevention techniques.
  • Documentation of activities, including initials and sign-offs in procedures.
  • Supervision of activities, including risk and reactivity management.
  • Pre-job briefs.

This activity constituted one License Operator Requalification inspection sample and one

Control Room Observation inspection sample.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

.1 Routine

a. Inspection Scope

The inspectors reviewed three specific structures, systems and components (SSC)

within the scope of the Maintenance Rule (MR) (10 CFR 50.65) with regard to some or

all of the following attributes, as applicable: (1) Appropriate work practices; (2)

Identifying and addressing common cause failures; (3) Scoping in accordance with 10

CFR 50.65(b) of the MR; (4) Characterizing reliability issues for performance monitoring;

(5) Tracking unavailability for performance monitoring; (6) Balancing reliability and

unavailability; (7) Trending key parameters for condition monitoring; (8) System

classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); (9)

Appropriateness of performance criteria in accordance with 10 CFR 50.65(a)(2); and

(10) Appropriateness and adequacy of 10 CFR 50.65 (a)(1) goals, monitoring and

corrective actions (i.e., Ten Point Plan). The inspectors also compared the licensees

performance against site procedure NPG-SPP-3.4, Maintenance Rule Performance

Indicator Monitoring, Trending and Reporting; Technical Instruction 0-TI-346,

Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; and NPG-

SPP-03.1, Corrective Action Program. The inspectors also reviewed, as applicable,

work orders, surveillance records, PERs, system health reports, engineering

evaluations, and MR expert panel minutes; and attended MR expert panel meetings to

verify that regulatory and procedural requirements were met. This activity constituted

three Maintenance Effectiveness inspection samples.

Enclosure

12

  • FIN work process during U3R15 refueling outage, various Work Orders (WOs)

Watertight Door Functional Failures

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

.1 Risk Assessment and Management of Risk

a. Inspection Scope

For planned online work and/or emergent work that affected the combinations of risk

significant systems listed below, the inspectors examined five on-line maintenance risk

assessments, and actions taken to plan and/or control work activities to effectively

manage and minimize risk. The inspectors verified that risk assessments and applicable

risk management actions (RMAs) were conducted as required by 10 CFR 50.65(a)(4),

applicable plant procedures, and BFN Equipment to Plant Risk Matrix. Furthermore, as

applicable, the inspectors verified the actual in-plant configurations to ensure accuracy

of the licensees risk assessments and adequacy of RMA implementation. This activity

constituted five Maintenance Risk Assessment inspection samples.

  • Planned refueling outage work on both loops of Unit 3 RHR, 3B Fuel Pool Cooling

pump, Unit 3 500KV off-site power, 3C EDG, 1A Condenser Circulating Water Pump,

1A Control Bay chiller and AHU, B Fire Pump, RCW Booster Pumps 2A and 3A, C3

EECW Pump, and C RHRSW Common Header

corrective maintenance, Unit 2 C Residual Heat Removal (RHR) Heat Exchanger

OOS for piping leak repair, Intake Pumping Station Vent Fan A and B work, and

Common Switchyard Centered LOOP High Risk due to Unit 3 Transformer activities.

  • Planned work and yellow risk on Unit 3, Div. I and Div. II RHR, CS Div II, 3C and 3D

EDG, 3B Fuel Pool Cooling (FPC) Pump, 3C and 3D 4kV Shutdown Boards and

Standby Gas Treatment (SBGT) Train C

  • Planned Unit 3 refueling outage yellow risk associated with Div. I RHRand CS OOS.

Unit 1/2 risk associated with RHR Heat Exchanger 2C and RHRSW Pump A3 OOS

and, Common Switchyard Centered LOOP High Risk due to Unit 3 Transformer

activities.

Enclosure

13

b. Findings

No findings were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the six operability/functional evaluations listed below to verify

technical adequacy and ensure that the licensee had adequately assessed TS

operability. The inspectors also reviewed applicable sections of the UFSAR to verify that

the system or component remained available to perform its intended function. In

addition, where appropriate, the inspectors reviewed licensee procedure NEDP-22,

Functional Evaluations, to ensure that the licensees evaluation met procedure

requirements. Furthermore, where applicable, inspectors examined the implementation

of compensatory measures to verify that they achieved the intended purpose and that

the measures were adequately controlled. The inspectors also reviewed PERs on a

daily basis to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. This activity constituted six Operability

Evaluation inspection samples.

520497)

  • RHRSW Pump Room Watertight Door BFN-0-DOOR-260-C-RHRSW Degraded

(PER 469640)

Foundation Hole Flood Protection Cover Inadequate Installation (PER 532050)

  • Units 1,2 and 3 EECW yard drain basins partially blocked, (PER 569282)
  • Unit 1 HPCI Turbine Stop Valve, 1-FCV-073-0018, Failed to Trip (PER 539040)

b. Findings

Two findings were identified. One finding is documented as a licensee identified violation

in Section 4OA7.

1) Introduction: The NRC identified a Green non-cited violation (NCV) of Technical

Specification 5.4.1.a for the licensees failure to maintain an Emergency Equipment

Cooling Water (EECW) pump flood barrier in accordance with written procedures which

resulted in the inoperability of two other safety related pumps.

Description:

The safety related Residual Heat Removal Service Water (RHRSW) pumps are housed

in the A, B, C, and D rooms of the intake pumping station. UFSAR Section 12.2.7.1.1

states, in part, that each room is designed to protect the RHRSW pumps from water and

wave forces resulting from a probable maximum flood (PMF) scenario. During

Enclosure

14

maintenance activities, the licensee maintained the design flood protection configuration

through implementation of properly written work instructions.

The C3 Emergency Equipment Cooling Water (EECW) pump is located in the C

RHRSW pump room with two similarly designed C1 and C2 RHRSW pumps. On March

26, 2012, the licensee had removed C3 pump from service for maintenance. The C3

pump and motor had been disassembled and the pump column removed from the intake

sump pit through the pump base plate and foundation leaving an approximate 22 inch

diameter hole. The hole was protected against flooding by a temporary 1/4 inch thick

aluminum cover plate, over a rubber gasket and secured with 8 foundation bolts. The

flood cover was prescribed by work order 112744581 and implemented by maintenance

procedures MCI-0-023-PMP002, Maintenance of EECW and RHRSW Pumps, and MCI-

0-023-PMP003, Emergency Equipment Cooling Water and Residual Heat Removal

Service Water Pump Removal and Installation.

On April 2, 2012, maintenance personnel removed the flood protection cover to facilitate

an inspection. Personnel re-installed the cover with only two bolts and nuts run down to

approximately one inch from being fully secured. On April 5, 2012, inspectors identified

and informed the licensee of the inadequate flood protection barrier. The licensee

immediately re-installed the flood protection cover in accordance with maintenance

procedures. As an added corrective action, the licensee permanently stenciled the

aluminum plate with the required procedure for installation. The licensee determined

that the workers had re-installed the flood protection cover following the inspection

assuming that it was only for foreign material exclusion. The licensee also determined

that the foreman did not direct an adequate pre-job brief and assumed the workers knew

of the procedural flood requirements. Furthermore, the licensee evaluated the

inadequate flood barrier for past operability and concluded that the C RHRSW pump

room would have flooded in the event of a PMF and that the other two RHRSW pumps

in the room, C1 and C2, would be made nonfunctional. The licensee credited the slow

progression of a PMF flood rise (four days and eight hours) to allow time to adequately

install the flood protection cover, and therefore, prevent the loss of the RHRSW pumps.

These actions were contained in licensee abnormal operating instruction 0-AOI-100-3,

Flood Above Elevation 558.

Analysis: The licensees failure to maintain an Emergency Equipment Cooling Water

(EECW) pump flood barrier in accordance with written procedures was a performance

deficiency. The finding was more than minor because it was associated with the

Mitigating Systems cornerstone attribute of Protection Against External Events, and

adversely affected the cornerstone objective to ensure the availability, reliability, and

capability of RHRSW pumps to perform their intended safety function during a design

basis flooding event. Specifically, the improper re-installation of an external flood

protection cover resulted in the inoperability of two RHRSW pumps. The significance of

this finding was evaluated in accordance with the IMC 0609 Attachment 4, Phase 1-

Initial Screening and Characterization of Findings, which required a Phase 3 analysis

because the finding involved the degradation of equipment designed to mitigate a

flooding event and was risk significant due to external initiating event core damage

sequences. A Phase 3 SDP analysis was performed by the regional Senior Reactor

Analyst using a modified NRC plant model. The model had been modified to calculate

Enclosure

15

the impact on the plant from external flooding due to the failure of the RHRSW flood

doors. The plant model was solved for a loss of condenser heat sink, with the initiating

event frequency set to 5E-3 as a conservative estimate for the external flood. Also

assumed was the unavailability of the power conversion system, since the circ water

pumps, and their power supplies would be flooded. Condensate was assumed lost

when the turbine building floods. RHRSW pumps and EECW pumps in the flooded

RHRSW room were failed by model changes for different flood door failure basic events.

This analysis failed only the C room door, which duplicated the impact of an unsecured

flood barrier. For the 4 day exposure time, the result was several orders of magnitude

below the CDF or LERF threshold for a finding of significance. The finding is Green

because of the short exposure time, and the low likelihood of the flood.

The cause of this finding was directly related to the cross cutting aspect of Supervisory

Oversight in the Work Practices component of the Human Performance area, because of

supervisions assumption that workers knew to restore the flood protection cover to meet

procedural requirements without a formal pre-job brief H.4(c).

Enforcement: TS 5.4.1.a. required that written procedures recommended in RG 1.33,

Revision 2, Appendix A, shall be established, implemented, and maintained. Item 9.a of

RG 1.33, Appendix A, stated, in part, that maintenance affecting the performance of

safety-related equipment be properly performed in accordance with written procedures

or documented instructions appropriate to the circumstances. Contrary to the above,

between April 2, and April 5, 2012, the licensee failed to properly perform maintenance

procedures MCI-0-023-PMP002 and MCI-0-023-PMP003, Section 5.0.K. Specifically,

the licensee failed to maintain a flood barrier during maintenance on C3 EECW Pump

which resulted in the inoperability of C1 and C2 RHRSW Pumps. Because this finding is

of very low safety significance (Green) and because it was entered into the licensees

corrective action program as PER 532050, this violation is being treated as a non-cited

violation consistent with the NRC Enforcement Policy. This violation was applicable to

U1, U2 and U3 and is identified as NCV 05000259, 260, 296/2012003-01, Failure to

Maintain Flood Barrier Results in Inoperable Safety Related Pumps.

1R18 Plant Modifications

a. Inspection Scope

The inspectors reviewed the two modifications listed below to verify regulatory

requirements were met, along with procedures, as applicable, such as NPG-SPP-9.3,

Plant Modifications and Engineering Change Control; NPG-SPP-9.5, Temporary

Alterations; and NPG-SPP-6.9.3, Post-Modification Testing. The inspectors also

reviewed the associated 10 CFR 50.59 screenings and evaluations and compared each

against the UFSAR and TS to verify that the modifications did not affect operability or

availability of the affected systems. Furthermore, the inspectors walked down each

modification to ensure that it was installed in accordance with the modification

documents and reviewed post-installation and removal testing to verify that the actual

impact on permanent systems was adequately verified by the tests. This activity

constituted two Plant Modification inspection samples.

Enclosure

16

  • Temporary Alteration Control Form (TACF) 1-12-001-073, Removed Thermal

Insulation Attached to BFN-1-FCV-073-0016, HPCI Steam Supply Valve

  • Design Change Notice (DCN) 70549, Unit 3 Reactor Water Level Flood-Up

Transmitter and Indication Loop Replacement

b. Findings

No findings were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors witnessed and reviewed the six post-maintenance tests (PMT) listed

below to verify that procedures and test activities confirmed SSC operability and

functional capability following the described maintenance. The inspectors reviewed the

licensees completed test procedures to ensure any of the SSC safety function(s) that

may have been affected were adequately tested, that the acceptance criteria were

consistent with information in the applicable licensing basis and/or design basis

documents, and that the procedure had been properly reviewed and approved. The

inspectors also reviewed the test data, to verify that test results adequately

demonstrated restoration of the affected safety function(s). The inspectors verified that

PMT activities were conducted in accordance with applicable WO instructions, or

licensee procedural requirements. Furthermore, the inspectors verified that problems

associated with PMTs were identified and entered into the CAP. This activity constituted

six Post Maintenance Test inspection samples.

  • Unit 3: Reactor Vessel Head Tensioning and subsequent Pressure Test per MSI-0-

001-VSL001, Reactor Vessel Head Disassembly and Reassembly; 3-SI-3.3.1.A,

ASME Section XI System Leakage Test of the Reactor Pressure Vessel and

Associated Piping; 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring;

and 3-SR-3.4.9.1(2), Reactor Vessel Shell Temperature and Reactor Coolant

Pressure Monitoring During In-Service Hydrostatic or Leak Testing

  • Unit 1/2 Common: PMT for Replacement of Common D EDG Woodward Governor

Speed Stop Micro Switches, OI-82, Standby Diesel Generator System and WO

113480917

  • Unit 3: PMT for 3C EDG Generator Replacement per 3-SR-3.8.1.7(3C), Diesel

Generator 3C 24-hour Run WO 112472092

replacement performed under WO 111044044

  • Unit 3: PMT for the B outboard MSIV (3-FCV-001-0027) valve repack performed

under WO 113394369

b. Findings

No findings were identified.

Enclosure

17

1R20 Refueling and Other Outage Activities

.1 Unit 3 Scheduled Refueling Outage (U3R15)

a. Inspection Scope

During April 7 to May 26, 2012, the inspectors examined critical outage activities to verify

that they were conducted in accordance with technical specifications, applicable

procedures, and the licensees outage risk assessment and management plans through

the end of the reporting period. Some of the more significant inspection activities

conducted by the inspectors were as follows:

Outage Risk Assessment

Prior to the Unit 3 scheduled 30 day U3C15 refueling outage that began on April 7, the

inspectors attended outage risk assessment team meetings and reviewed the Outage

Risk Assessment Report to verify that the licensee had appropriately considered risk,

industry experience, and previous site-specific problems in developing and implementing

an outage plan that assured defense-in-depth of safety functions were maintained. The

inspectors also reviewed the daily U3C15 Refueling Outage Reports, including the

Outage Risk Assessment Management (ORAM) Safety Function Status, and regularly

attended the twice a day outage status meetings. These reviews were compared to the

requirements in licensee procedure NPG-SPP-07.2, Outage Management, and technical

specifications. These reviews were also done to verify that for identified high risk

significant conditions, due to equipment availability and/or system configurations,

contingency measures were identified and incorporated into the overall outage and

contingency response plan. Furthermore, the inspectors frequently discussed risk

conditions and designated protected equipment with Operations and outage

management personnel to assess licensee awareness of actual risk conditions and

mitigation strategies.

Shutdown and Cooldown Process

The inspectors witnessed the shutdown and cooldown of Unit 3 in accordance with

licensee procedures OPDP-1, Conduct of Operations; 3-GOI-100-12A, Unit Shutdown

from Power Operations to Cold Shutdown and Reduction in Power During Power

Operations; and 3-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring.

Decay Heat Removal

The inspectors reviewed licensee procedures 3-OI-74, Residual Heat Removal System

(RHR); 3-OI-78, Fuel Pool Cooling and Cleanup System; and Abnormal Operating

Instruction 0-AOI-72-1, Alternate Decay Heat Removal System Failures; and conducted

a main control room panel and in-plant walkdowns of system and components to verify

correct system alignment. During planned evolutions that resulted in an increased

outage risk condition of Yellow for shutdown cooling, inspectors verified that the plant

conditions and systems identified in the risk mitigation strategy were available. In

addition, the inspectors reviewed controls implemented to ensure that outage work was

Enclosure

18

not impacting the ability of operators to operate spent fuel pool cooling, RHR shutdown

cooling, and/or Alternate Decay Heat Removal (ADHR) system. Furthermore, the

inspectors conducted several walkdowns of the ADHR system during operation with the

fuel pool gates removed.

Critical Outage Activities

The inspectors examined outage activities to verify that they were conducted in

accordance with technical specifications, licensee procedures, and the licensees outage

risk control plan. Some of the more significant inspection activities accomplished by the

inspectors were as follows:

  • Walked down selected safety-related equipment clearance orders (i.e., tag orders)

evolutions involving operations with the potential to drain the reactor vessel

(OPDRV)

  • Verified electrical systems availability and alignment
  • Monitored important control room plant parameters (e.g., RCS pressure, level, flow,

and temperature) and technical specifications compliance during the various

shutdown modes of operation, and mode transitions

  • Evaluated implementation of reactivity controls
  • Reviewed control of containment penetrations and overall integrity

the reactor cavity, equipment pit, and spent fuel pool

  • Routine tours of the control room, reactor building including areas normally

inaccessible during power operations, refueling floor, torus and drywell.

Reactor Vessel Disassembly and Refueling Activities

The inspectors witnessed selected activities associated with reactor vessel disassembly,

and reactor cavity flood-up and drain down in accordance with 3-GOI-100-3A, Refueling

Operations (Reactor Vessel Disassembly and Floodup). Also, on numerous occasions,

the inspectors witnessed fuel handling operations during the two Unit 3 reactor core fuel

shuffles performed in accordance with technical specifications and applicable operating

procedures. Inspectors also observed control rod unlatching and relatching for control

rod drive mechanism change-outs. In addition, the inspectors verified specific fuel

movements as delineated by the Fuel Assembly Transfer Sheets (FATF). Furthermore,

the inspectors also witnessed and performed a 100 percent core verification examination

of the video verification of the final completed reactor core.

Drywell Closeout

On May 17, 2012, the inspectors reviewed the licensees conduct of 3-GOI-200-2,

Section 5.3 Drywell Closeout, and performed an independent detailed closeout

inspection of the Unit 3 drywell.

Enclosure

19

Torus Closeout

On May 12, 2012, the inspectors reviewed the licensees conduct of procedure 3-GOI-

200-2, Section 5.4 Torus Closeout, and performed an independent detailed closeout

inspection of the Unit 3 torus (suppression pool and chamber). In addition inspectors

reviewed the Foreign Material Exclusion (FME) log for any discrepancies.

Restart Activities

The inspectors specifically conducted the following:

001-VSL001, Reactor Vessel Disassembly and Reassembly

with 3-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor pressure

Vessel and Associated Piping, and reviewed reactor coolant heatup/pressurization

data per 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, and 3-SR-

3.4.9.1(2), Reactor Vessel Shell Temperature & Reactor Coolant Pressure

Monitoring During In-Service Leak Testing

Pressure per 3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring

  • Reviewed and verified completion of selected items of 0-TI-270, Refueling Test

Program, Attachment 2, Startup Review Checklist

Revision 11

  • Witnessed Unit 3 approach to criticality and power ascension per 3-GOI-100-1A, Unit

Startup, 3-SR-3.3.1.1.5, SRM and IRM Overlap Verification, and 3-GOI-100-12,

Power Maneuvering

Corrective Action Program

The inspectors reviewed PERs generated during refueling outage U3C15 and

periodically attended Corrective Action Review Board (CARB) and PER Screening

Committee (PSC) meetings to verify that initiation thresholds, priorities, mode holds,

operability concerns and significance levels were adequately addressed. Resolution and

implementation of corrective actions of several PERs were also reviewed for

completeness. This constitutes one Refueling Outage activity inspection sample.

b. Findings

No findings were identified.

Enclosure

20

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed portions of, and/or reviewed completed test data for the

following seven surveillance tests of risk-significant and/or safety-related systems to

verify that the tests met technical specification surveillance requirements, UFSAR

commitments, and in-service testing and licensee procedure requirements. The

inspectors review confirmed whether the testing effectively demonstrated that the SSCs

were operationally capable of performing their intended safety functions and fulfilled the

intent of the associated surveillance requirement. This activity constituted seven

Surveillance Testing inspection samples: one inservice test, three routine, two

containment isolation valve and one reactor coolant system leak detection test. .

In-Service Tests:

Routine Surveillance Tests:

  • 3-SR-3.8.1.9(3D OL), Diesel Generator 3D Emergency Load Acceptance Test with

Unit 3 Operating

  • 3-SR-3.5.1.8, HPCI Main and Booster Pump Set Developed Head and Flow Rate

Test at 150 psig Reactor Pressure, Rev. 13 performed on May 16, 2012

Shutdown Cooling Suction: Penetration X-12

Containment Isolation Valve Tests:

Line B: Penetration X-7B

Reactor Coolant System Leak Detection Tests:

  • 2-SI-4.2.E-1(B), Drywell Equipment Drain Sump Flow Integrator Calibration

b. Findings

No findings were identified.

Enclosure

21

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Evaluation

a. Inspection Scope

The inspectors evaluated the adequacy of the licensees methods for testing the alert

and notification system in accordance with NRC Inspection Procedure 71114,

Attachment 02, Alert and Notification System (ANS) Evaluation. The applicable planning

standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section

IV.D requirements were used as reference criteria. The criteria contained in NUREG-

0654, Criteria for Preparation and Evaluation of Radiological Emergency Response

Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, were also

used as a reference.

The inspectors reviewed various documents which are listed in the Attachment. This

inspection activity satisfied one inspection sample for the alert and notification system on

a biennial basis.

b. Findings

No findings were identified.

1EP3 Emergency Preparedness Organization Staffing and Augmentation System

a. Inspection Scope

The inspectors reviewed the licensees Emergency Response Organization (ERO)

augmentation staffing requirements and process for notifying the ERO to ensure the

readiness of key staff for responding to an event and timely facility activation. The

qualification records of key position ERO personnel were reviewed to ensure all ERO

qualifications were current. A sample of problems identified from augmentation drills or

system tests performed since the last inspection was reviewed to assess the

effectiveness of corrective actions.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 03, Emergency Preparedness Organization Staffing and Augmentation

System. The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR

50, Appendix E requirements were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment. This

inspection activity satisfied one inspection sample for the ERO staffing and

augmentation system on a biennial basis.

b. Findings

No findings were identified.

Enclosure

22

1EP5 Maintenance of Emergency Preparedness

a. Inspection Scope

The inspectors reviewed the corrective actions identified through the Emergency

Preparedness program to determine the significance of the issues, the completeness

and effectiveness of corrective actions, and to determine if issues were recurring. The

licensees post-event after action reports, self-assessments, and audits were reviewed to

assess the licensees ability to be self-critical, thus avoiding complacency and

degradation of their emergency preparedness program. The inspectors toured facilities

and reviewed equipment and facility maintenance records to assess licensees

adequacy in maintaining them. In addition, the inspectors reviewed licensee procedures

and training for the evaluation of changes to the emergency plans.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 05, Maintenance of Emergency Preparedness. The applicable 10 CFR

50.47(b) planning standards and related 10 CFR 50, Appendix E requirements were

used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment. This

inspection activity satisfied one inspection sample for the Maintenance of Emergency

preparedness on a biennial basis.

b. Findings

No findings were identified.

1EP6 Drill Evaluation

a. Inspection Scope

During the report period, the inspectors observed an Emergency Preparedness (EP) drill

that contributed to the licensees Drill/Exercise Performance (DEP) and Emergency

Response Organization (ERO) performance indicator (PI) measures on June 13, 2012,

to identify any weaknesses and deficiencies in classification, notification, dose

assessment and protective action recommendation (PAR) development activities. The

inspectors observed emergency response operations in the simulated control room and

certain Emergency Response Facilities to verify that event classification and notifications

were done in accordance with EPIP-1, Emergency Classification Procedure and other

applicable Emergency Plan Implementing Procedures. The inspectors also attended the

post-drill critique to compare any inspector-observed weakness with those identified by

the licensee in order to verify whether the licensee was properly identifying weaknesses.

This inspection activity satisfied one inspection sample for the Drill Evaluation of

emergency preparedness

b. Findings

No findings were identified.

Enclosure

23

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety (OS)

2RS1 Radiological Hazard Assessment and Exposure Control

a. Inspection Scope

Radiological Hazard Assessment: The inspectors reviewed a number of radiological

surveys, including those performed for airborne areas, of locations throughout the facility

including the Unit 3 (U3) drywell, Unit 1 (U1), Unit 2 (U2), and U3 reactor buildings, the

turbine building, and the independent spent fuel storage installation (ISFSI). The

inspectors also walked down many of the same areas and select radioactive material

storage locations with a survey instrument, evaluating material condition, postings, and

radiological controls. Of specific interest was the Condensate Storage Tank area which

due to a liquid radwaste processing problem created an actual radiation area outside the

building, near on-going work. The inspectors observed jobs in radiologically risk-

significant areas including high radiation areas and areas with, or with the potential for,

airborne activity. The inspectors evaluated the surveys in relation to the identified

hazards for sufficient detail and frequency.

Instructions to Workers: During plant walk downs, the inspectors observed labeling and

radiological controls on containers of radioactive material. The inspectors also reviewed

radiation work permits (RWP) used for accessing high radiation areas and airborne

areas, verifying that appropriate work control instructions and electronic dosimeter (ED)

setpoints had been provided and to assess the communication of radiological control

requirements to workers. The inspectors reviewed selected ED dose and dose rate

alarms, to verify workers properly responded to the alarms and that the licensees review

of the events was appropriate. The inspectors observed pre-job RWP briefings and

health physics technician coverage of workers. The inspectors reviewed the various

methods being used to notify workers of changing or changed radiological conditions.

Contamination and Radioactive Material Control: The inspectors observed the release

of potentially contaminated items from the radiologically controlled area (RCA) and from

contaminated areas such as the drywell. The inspectors also reviewed the procedural

requirements for, and equipment used to perform, the radiation surveys for release of

personnel and material. During plant walk downs, the inspectors evaluated radioactive

material storage areas and containers, including satellite RCAs and the low level

radwaste facility, assessing material condition, posting/labeling, and control of

materials/areas. In addition, the inspectors reviewed the sealed source inventory and

verified labeling, storage conditions, and leak testing of selected sources. The

inspectors verified if Category 1 and 2 sealed sources had been appropriately reported

to the National Source Tracking System and physically verified the presence and

controls of these sources. The sources were verified to be physically present and in

proper working order.

Enclosure

24

Radiological Hazards Control and Work Coverage: The inspectors evaluated licensee

performance in controlling worker access to radiologically significant areas and

monitoring jobs in-progress associated with the Unit 3 refueling outage. Established

radiological controls were evaluated for selected tasks including diver area setup for

torus underwater coatings inspection and desludging activities, equipment staging for

control rod drive work, reactor water cleanup sludge sampling, and work to support the

extended power uprate for Unit 3. The inspectors evaluated the effectiveness of

radiation exposure controls, including air sampling, barrier integrity, engineering controls,

and postings through a review of both internal and external exposure results. The

inspector followed up on two minor airborne radioactivity events.

During walk downs with a radiation survey meter, the inspectors independently verified if

ambient radiological conditions were consistent with licensee performed surveys, RWPs,

and pre-job briefings; observed the adequacy of radiological controls; and observed

controls for radioactive materials stored in the spent fuel pool. ED alarm set points and

worker stay times were evaluated against area radiation survey results for drywell and

refueling floor activities.

Risk-Significant High Radiation Area and Very High Radiation Area Controls: The

inspectors discussed the controls and procedures for locked-high radiation areas

(LHRAs) and very high radiation areas (VHRAs) with health physics supervisors and the

radiation protection manager. During plant walk downs, the inspectors verified the

posting/locking of LHRA/VHRA areas.

Radiation Worker Performance and Radiation Protection Technician Proficiency The

inspectors observed radiation worker performance through direct observation, via

remote camera monitoring, and via telemetry. These jobs were performed in high

radiation, airborne, and/or contaminated areas. The inspectors also observed health

physics technicians providing field coverage of jobs and providing remote coverage.

Problem Identification & Resolution: Licensee Corrective Action Program (CAP)

documents associated with radiation monitoring and exposure control were reviewed

and assessed. This included review of selected Problem Evaluation Reports (PERs)

related to radworker and health physics technician performance. The inspectors

evaluated the licensees ability to identify, characterize, prioritize, and resolve the

identified issues in accordance with procedure NPG-SPP-3.1, Corrective Action

Program, Rev. 2. The inspectors also evaluated the scope of the licensees internal

audit program and reviewed recent assessment results. Licensee CAP documents

reviewed are listed in Section 2RS1 of the Attachment.

Radiation protection activities were evaluated against the requirements of Updated Final

Safety Analysis Report (UFSAR) Section 12; Technical Specification Sections 5.4 and

5.7; 10 Code of Federal Regulations (CFR) Parts 19 and 20; and approved licensee

procedures. Radiological control activities for ISFSI areas were evaluated against 10

CFR Part 20, 10 CFR Part 72, and TS details. Records reviewed are listed in Section

2RS1 of the Attachment.

Enclosure

25

The inspectors completed 1 sample, as described in Inspection Procedure (IP)

71124.01.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment

a. Inspection Scope

Program Reviews: The inspectors reviewed the 2010 and 2011 Annual Radiological

Effluent Release Report documents for consistency with the requirements in the Offsite

Dose Calculation Manual (ODCM) and Technical Specifications. Unexpected results

were followed up to determine the cause. Radioactive effluent monitor operability issues

were discussed with plant staff. The inspectors reviewed the ODCM changes made

since the last inspection against the guidance in NUREG-1301 and RG 1.109, RG 1.21,

and RG 4.1.

Walk-Downs and Observations: The inspectors walked-down selected components of

the gaseous and liquid discharge systems to ascertain material condition, configuration

and alignment. To the extent practical, the inspectors observed the material condition of

abandoned in place liquid waste processing equipment for indications of degradation or

leakage that could constitute a possible release pathway to the environment. The

inspectors also observed the collection and analysis of gaseous effluent samples (noble

gas, iodine, particulates) from the plant stack. The inspectors walked-down portions of

the Standby Gas Treatment System, to ascertain material condition, configuration, and

alignment. In addition, the inspectors reviewed the most recent HEPA and charcoal

filtration surveillance testing results for each train of the standby gas treatment system.

Sampling and Analyses: In addition to observing collection of gaseous effluent samples

from the plant stack, the inspectors observed a chemistry technician verifying plant stack

flow rates. The results of the chemistry count rooms inter-laboratory comparison

program were reviewed and discussed with cognizant licensee personnel.

Dose Calculations: The inspectors reviewed several gas release permits, and monthly

gaseous/liquid effluent dose calculation summaries. The magnitudes of the releases

were determined to be a small fraction of the applicable limits. The inspectors reviewed

the contributions to public dose from the abnormal releases. The sites 10 CFR 61

analysis was reviewed for expected nuclide distribution from the aspects of quantifying

effluents, the treatment of hard to detect nuclides, determining appropriate calibration

nuclides for instruments and whole body counting libraries. The inspectors also

reviewed the licensees most recent Land Use Census results and changes in the

ODCM since the last inspection.

Ground Water Protection: The licensees implementation of the Industry Ground Water

Protection Initiative was reviewed for changes since the last inspection as well.

Groundwater sampling results obtained since the last inspection were reviewed.

Enclosure

26

Licensee response, evaluation, and follow-up to spills and leaks since the last inspection

were reviewed in detail.

Problem Identification and Resolution: Selected corrective action program documents

associated with the effluent monitoring and control program, including problem

evaluation reports (PERs) and audits, were reviewed and assessed. The inspectors

verified that problems were being identified at an appropriate threshold and resolved in

accordance with procedure NPG-SPP-3.1, Corrective Action Program, Rev. 2 and

Rev. 3.

Documents reviewed are listed in Section 2RS6 and 2RS7 of the report Attachment.

The inspectors completed one sample as required by inspection procedure 71124.06.

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program (REMP)

a. Inspection Scope

REMP Status and Results: The inspectors discussed changes and reviewed the ODCM

and the Annual Radiological Environmental Operating Report documents issued for

calendar year (CY) 2010 and CY 2011. The inspectors also reviewed and evaluated

REMP contract laboratory cross-check program results, and current procedural guidance

for environmental sample collection and processing. Inspectors reviewed the Annual

Radiological Effluent Release Report for CY 2010 & CY 2011 under section 2RS6.

Equipment Walk-down: The inspectors observed sample collection activities of selected

air sampling stations as specified per procedure. The inspectors observed equipment

material condition and verified operability, including verification of flow rates/total sample

volume results, for the weekly airborne particulate filter and iodine cartridge change-outs

at selected atmospheric sampling stations. The material condition and placement of

environmental thermoluminescent dosimeters and water sampling stations were verified

by direct observation at select ODCM locations. Land use census results actions for

missed samples including compensatory measures and availability of replacement

equipment were discussed with environmental technicians and knowledgeable licensee

staff. Inspectors also reviewed calibration and maintenance surveillance records for the

installed environmental air sampling stations.

Procedural guidance, program implementation, quantitative analysis sensitivities, and

environmental monitoring results were reviewed against 10 CFR Part 20; Appendix I to

10CFR Part 50; TS Sections 6.8 Procedures and Programs and 6.9, Reporting

Requirements; ODCM, Rev. 15; RG 4.15, Quality Assurance for Radiological Monitoring

Programs (Normal Operation) - Effluent Streams and the Environment; and the Branch

Technical Position, An Acceptable Radiological Environmental Monitoring Program -

1979. Documents reviewed are listed in Section 2RS7 of the Attachment.

Enclosure

27

Meteorological Monitoring Program: The inspectors walked-down the meteorological

tower and observed local data collection equipment readouts. The physical condition of

the tower and the instruments were observed and equipment operability, and

maintenance history were discussed with responsible licensee staff. The transmission of

locally generated meteorological data to the main control room operators was also

verified. The inspectors reviewed applicable tower instrumentation calibration records

for the meteorological measurements of wind speed, wind direction, and temperature,

and evaluated measurement data recovery for CY 2010 and CY 2011.

Licensee procedures and activities related to meteorological monitoring were evaluated

against: ODCM; FSAR; RG 1.23, Meteorological Monitoring Programs For Nuclear

Power Plants, and ANSI/ANS-2.5-1984, Standard for Determining Meteorological

Information at Nuclear Power Sites. Documents reviewed are listed in Section 2RS7 of

the Attachment.

Problem Identification and Resolution: The inspectors reviewed selected PERs in the

areas of environmental monitoring and meteorological monitoring. The inspectors

evaluated the licensees ability to identify, characterize, prioritize, and resolve the

identified issues in accordance with NPG-SPP 3.1, Corrective Action Program, Rev. 2.

The inspectors also evaluated the scope of the licensees internal audit program and

reviewed recent assessment results. Documents reviewed are listed in Sections 2RS6

& 2RS7 in the Attachment.

The inspectors completed one sample as required by inspection procedure 71124.07.

b. Findings

No findings were identified.

2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and

Transportation

a. Inspection Scope

Waste Processing and Characterization: During inspector walk-downs, accessible

sections of the liquid and solid radioactive waste (radwaste) processing systems were

assessed for material condition and conformance with system design diagrams.

Inspected equipment included floor drain tanks; phase separator tanks; resin and filter

packaging components; and abandoned evaporator equipment. The inspectors

discussed component function, processing system changes, and radwaste program

implementation with licensee staff.

The 2010 and 2011 Annual Radiological Effluent Release Report and radionuclide

characterizations for select waste streams from 2010, and each major waste stream

from 2012 were reviewed and discussed with radwaste staff. For cleanup waste phase

separator resin, reactor water cleanup resin, Thermex resin, and dry active waste (DAW)

the inspectors evaluated analyses for hard-to-detect nuclides, reviewed the use of

scaling factors, and examined quality assurance comparison results between licensee

Enclosure

28

waste stream characterizations and outside laboratory data. Waste stream mixing and

concentration averaging methodology for resins and filters was evaluated and discussed

with radwaste staff. The inspectors also reviewed the licensees procedural guidance for

monitoring changes in waste stream isotopic mixtures.

Radwaste processing activities and equipment configuration were reviewed for

compliance with the licensees Process Control Program (PCP) and UFSAR, Chapter 9.

Waste stream characterization analyses were reviewed against regulations detailed in

10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical

Position on Waste Classification (1983). Reviewed documents are listed in Section

2RS8 of the Attachment.

Radioactive Material Storage: During walk-downs of radioactive material storage areas

in the radwaste building and outdoor low-level storage yard, the inspectors observed the

physical condition and labeling of storage containers and the posting of Radioactive

Material Areas. The inspectors also reviewed licensee procedural guidance for storage

and monitoring of radioactive material.

Radioactive material and waste storage activities were reviewed against the

requirements of 10 CFR Part 20. Reviewed documents are listed in Section 2RS8 of the

report Attachment.

Transportation: The inspectors directly observed preparation activities for shipment of a

high integrity container (HIC) of resin. The inspectors noted package markings and

placarding, performed independent dose rate measurements, and interviewed shipping

technicians regarding Department of Transportation (DOT) regulations.

Selected shipping records were reviewed for consistency with licensee procedures and

compliance with NRC and DOT regulations. The inspectors reviewed emergency

response information, DOT shipping package classification, waste classification,

radiation survey results, and evaluated whether receiving licensees were authorized to

accept the packages. Licensee procedures for opening and closing Type A shipping

containers were compared to manufacturer requirements. In addition, training records

for selected individuals currently qualified to ship radioactive material were reviewed.

Transportation program implementation was reviewed against regulations detailed in 10

CFR Part 20, 10 CFR Part 71, 49 CFR Parts 172-178, as well as the guidance provided

in NUREG-1608. Training activities were assessed against 49 CFR Part 172 Subpart H.

Documents reviewed during the inspection are listed in Section 2RS8 of the Attachment.

Problem Identification and Resolution: The inspectors reviewed PERs in the area of

radwaste/shipping. The inspectors evaluated the licensees ability to identify and resolve

the issues in accordance with procedure NPG-SPP-3.1, Corrective Action Program, Rev.

2 and Rev. 3. The inspectors also evaluated the scope of the licensees internal audit

program and reviewed recent assessment results. Licensee corrective action program

documents reviewed are listed in Section 2RS8 of the Attachment.

Enclosure

29

The inspectors completed one sample as required by inspection procedure 71124.08.

b. Findings

.1 Failure to adequately secure radioactive shipping container contents for transport

Introduction: A self-revealing Green Non-Cited Violation (NCV) of 10 CFR 71.5,

Transportation of Licensed Material, was identified for the licensees failure to ensure

proper packaging of two DOT 7A Type A packages as required by 49 CFR 173.475(e),

Quality Control Requirements Prior To Each Shipment Of Class 7 (Radioactive)

Materials.

Description: On March 22, 2010, the licensee shipped control rod drive mechanisms

(CRDMs) to GE Hitachi Nuclear (GEH) for refurbishment in six Department of

Transportation (DOT) approved Type A boxes. Each box contained four CRDMs. In a

letter dated September 17, 2010, GEH informed the licensee that their receipt inspection

of containers 1343-S and 966-S on April 23, 2010, identified that pig shield containment

lid restraint bars designed to secure the CRDMs and pig shields in place were not

installed and were laying loose in the bottom of the container. The licensee documented

the issue in PER 236118. Licensee investigation determined that the radwaste

packaging inspector failed to follow procedural requirements and verify that the CRDMs

were properly secured within the container to prevent movement during shipping. The

inspectors reviewed the Container Certification, container closure procedure for the

CRDM boxes, licensee radioactive material shipment procedures, and engineering

documents concerning the container meeting DOT 7A requirements. The inspectors

noted that although the container closure procedure did not specifically address internal

packaging and the restraint bars, the container certification states that All contents must

be securely positioned to prevent shifting during normal conditions of transport., and

that site procedural guidance requires verification that the contents of the package have

been secured and satisfies the requirements of 10 CFR 71.87, prior to shipment.

Analysis: The failure to properly secure, or adequately block or brace the material within

a Class 7 (radioactive) materials package to prevent movement during transport prior to

shipment was determined to be a performance deficiency. Specifically, the licensee

failed to follow established site procedures and applicable documents provided by the

package vendor for package inspection and verification to ensure materials are secured

within containers. The finding was more than minor because it is associated with the

Public Radiation Safety Cornerstone, Plant Facilities/Equipment and Instrumentation

attribute, involving transportation packaging and adversely affected the cornerstone

objective to ensure adequate protection of public health and safety from exposure to

radioactive materials released into the public domain as a result of routine civilian

nuclear reactor operation. Specifically, the failure to correctly secure the package

contents to prevent movement could have resulted in damage or failure of the container

during transportation. The significance of the finding was evaluated using IMC 0612,

Appendix D, Public Radiation Safety Significance Determination Process. The issue

was evaluated using the Public Radiation Safety flowchart because it involved

radioactive material control, specifically, transportation. The finding was determined to

be of very low safety significance (Green) because it did not involve radiation limits being

Enclosure

30

exceeded, a package breach, a certificate of compliance issue, a low-level burial ground

non-conformance, or a failure to make emergency notifications.

The cause of this finding was directly related to the cross cutting aspect of Documents,

Procedures and Component Labeling in the Resources component of the Human

Performance area because the licensee did not effectively incorporate package design

specifications into their transportation program to ensure that all internal restraining

devices are correctly installed to secure the CRDM in place to prevent damage to the

transport package. H.2(c)

Enforcement: 10 CFR 71.5, Transportation of Licensed Material, required, in part, that

each licensee who transports licensed material outside the site of usage, as specified in

the NRC license, or where transport is on public highways, or who delivers licensed

material to a carrier for transport, shall comply with the applicable requirements of the

DOT regulations in 49 CFR Parts 107, 171 through 180, and 390 through 397,

appropriate to the mode of transport.

49 CFR 173.475(e), Quality Control Requirements Prior To Each Shipment Of Class 7

(Radioactive) Materials, required, in part, that before each shipment of any Class 7

(radioactive) materials package, the offeror must ensure, by examination or appropriate

tests, that each special instruction for filling, closing, and preparation of the packaging

for shipment has been followed. Licensee procedure RWTP-100, Radioactive

Material/Waste Shipments, contains package inspection and verification requirements

to ensure materials are secured within containers.

Contrary to the above, on March 22, 2010, the licensee failed to comply with the

applicable requirements of DOT regulation 49 CFR 173.475(e) for transport of licensed

material. Specifically, the licensee failed to follow Container Certification guidance, in

that the CRDMs were not properly packaged and secured inside two CRDM shipping

containers as required by licensee procedure RWTP-100. Because this violation was of

very low safety significance and it was entered into the licensees CAP (SR 570902), this

violation is being treated as an NCV, in accordance with Section 2.3.2 of the NRC

Enforcement Policy. (NCV 05000259, 260, 296/2012003-02; Failure to Properly Prepare

a DOT Type A Package for Transport)

.2 Failure to Implement DOT Type A Package Closure Requirements

Introduction: A self-revealing Green Non-Cited Violation (NCV) of 10 CFR 71.5,

Transportation of Licensed Material, was identified for the licensees failure to properly

close a DOT 7A Type A packages as required by DOT 49 CFR 173.475(f) Quality

Control Requirements Prior To Each Shipment Of Class 7 (Radioactive) Materials.

Description: On September 7, 2011, the licensee shipped a DOT approved Type A

shipping container, containing an ISP surveillance capsule, to MP Machinery and

Testing, LLC (MPM) for analysis of the contents. In a letter dated September 9, 2011,

MPM informed the licensee that upon arrival at the MPM facility the closure bolts on the

shipping container were found to be undertorqued at 30 ft-lbs torque, not 390 ft-lbs

torque as specified in the DOT Package Certification provided by MPM. The licensee

Enclosure

31

documented the issue in PER 431446. Licensee investigation determined that the ISP

surveillance capsule shipping container closure bolts did not have the correct torque

applied due to inadequate procedure guidance, unfamiliarity of the workers with the task,

and a lack of procedure use and adherence. Preparation of the surveillance capsule for

shipment occurred over several months, the Technical Instruction was revised during the

period, and the container instructions provided by the vendor were not used during

loading activities. The inspectors reviewed the DOT Package Certification, container

loading and shipping instructions, Technical Instruction for obtaining and packaging the

Reactor Vessel Test Specimens (both revisions), and the work order used to remove

and package the ISP surveillance capsule for shipment. The inspectors noted that

although detailed instructions for loading and closure of the container were provided by

the vendor, the instructions and required container closure torque values were not

included, or referenced, in the Technical Instruction or the work package.

Analysis: The failure to properly close a Class 7 (radioactive) materials package was

determined to be a performance deficiency. Specifically, the licensee failed to follow

established site procedures and applicable vendor documents for closing the package

resulting in inadequate torque of the shipping container closure bolts. The finding was

more than minor because it is associated with the Public Radiation Safety Cornerstone,

Plant Facilities/Equipment and Instrumentation attribute, involving transportation

packaging and adversely affected the cornerstone objective to ensure adequate

protection of public health and safety from exposure to radioactive materials released

into the public domain as a result of routine civilian nuclear reactor operation.

Specifically, the failure to apply the correct torque to the package closure bolts could

have resulted in incomplete sealing of the container or failure of the cover bolts during

transportation. The significance of the finding was evaluated using IMC 0612, Appendix

D, Public Radiation Safety Significance Determination Process. The issue was

evaluated using the Public Radiation Safety flowchart because it involved radioactive

material control, specifically, transportation. The finding was determined to be of very

low safety significance (Green) because it did not involve radiation limits being

exceeded, a package breach, a certificate of compliance issue, a low-level burial ground

non-conformance, or a failure to make emergency notifications

The cause of this finding was directly related to the cross cutting aspect of Documents,

Procedures and Component Labeling in the Resources component of the Human

Performance area because the licensee did not effectively incorporate the vendor

provided container loading and shipping instructions into their work package and

transportation program to ensure correct torque values were used to close the shipping

container. H.2(c)

Enforcement: 10 CFR 71.5, Transportation of Licensed Material, required, in part, that

each licensee who transports licensed material outside the site of usage, as specified in

the NRC license, or where transport is on public highways, or who delivers licensed

material to a carrier for transport, shall comply with the applicable requirements of the

DOT regulations in 49 CFR Parts 107, 171 through 180, and 390 through 397,

appropriate to the mode of transport.

Enclosure

32

49 CFR 173.475(f) Quality Control Requirements Prior To Each Shipment Of Class 7

(Radioactive) Materials, required, in part, that each closure, valve, or other opening of

the containment system through which the radioactive content might escape is properly

closed and sealed.

Contrary to the above, on September 7, 2011, the licensee failed to comply with the

applicable requirements of DOT regulation 49 CFR 173.475(f) for transport of licensed

material. Specifically, the licensee failed to properly close an opening in the containment

system of a Class 7 (radioactive) materials package. Because this violation was of very

low safety significance and it was entered into the licensees CAP (SR 571151), this

violation is being treated as an NCV, in accordance with Section 2.3.2 of the NRC

Enforcement Policy. (NCV 05000259, 260, 296/2012003-03; Failure to Implement DOT

Type A Package Closure Requirements)

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness

4OA1 Performance Indicator (PI) Verification

Cornerstone: Mitigating Systems

.1 Safety System Functional Failures; Mitigating Systems Performance Indicator- Heat

Removal (Reactor Core Isolation Cooling)

a. Inspection Scope

The inspectors reviewed the licensees procedures and methods for compiling and

reporting the following Performance Indicators (PIs), including procedure NPG-SPP-02.2

Performance Indicator Program. The inspectors examined the licensees PI data for the

specific PIs listed below for the second quarter 2011 through first quarter of 2012. The

inspectors reviewed the licensees data and graphical representations as reported to the

NRC to verify that the data was correctly reported. The inspectors also validated this

data against relevant licensee records (e.g., PERs, Daily Operator Logs, Plan of the

Day, Licensee Event Reports, etc.), and assessed any reported problems regarding

implementation of the PI program. Furthermore, the inspectors met with responsible

plant personnel to discuss and go over licensee records to verify that the PI data was

appropriately captured, calculated correctly, and discrepancies resolved. The inspectors

also used the Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment

Performance Indicator Guideline, to ensure that industry reporting guidelines were

appropriately applied. This activity constituted six mitigating systems performance

indicator inspection samples.

  • Unit 1 Safety System Functional Failures
  • Unit 2 Safety System Functional Failures
  • Unit 3 Safety System Functional Failures

Enclosure

33

4OA1 Performance Indicator (PI) Verification

Cornerstone: Barrier Integrity

a. Inspection Scope

The inspectors reviewed the licensees procedures and methods for compiling and

reporting the Performance Indicators (PI) listed below, including procedure SPP-3.4,

Performance Indicator for NRC Reactor Oversight Process for Compiling and Reporting

PIs to the NRC. The inspectors reviewed the raw data for the PITs listed below for the

1st through 4th quarters of 2006. The inspectors compared the licensees raw data

against graphical representations and specific values reported to the NRC in the 4th

quarter 2006 PI report to verify that the data was correctly reflected in the report. The

inspectors also reviewed the past history of PERs for any that might be relevant to

problems with the PI program. Furthermore, the inspectors met with responsible

chemistry and engineering personnel to discuss and go over licensee records to verify

that the PI data was appropriately captured, calculated correctly, and discrepancies

resolved. The inspectors reviewed Nuclear Energy Institute 99-02, Regulatory

Assessment Performance Indicator Guideline, to verify that industry reporting guidelines

were applied.

  • RCS Activity for Units 2 and 3
  • RCS Leakage for Units 2 and 3

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

a. Inspection Scope

The inspectors sampled licensee submittals relative to the PIs listed below for the period

October 1, 2011, and March 31, 2012. To verify the accuracy of the PI data reported

during that period, PI definitions and guidance contained in NEI 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 6, were used to confirm the

reporting basis for each data element.

  • Emergency Response Organization (ERO) Drill/Exercise Performance
  • ERO Drill Participation
  • Alert and Notification System Reliability

Enclosure

34

For the specified review period, the inspector examined data reported to the NRC,

procedural guidance for reporting PI information, and records used by the licensee to

identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO

drill and exercise performance through review of a sample of drill and event records.

The inspectors reviewed selected training records to verify the accuracy of the PI for

ERO drill participation for personnel assigned to key positions in the ERO. The

inspectors verified the accuracy of the PI for alert and notification system reliability

through review of a sample of the licensees records of periodic system tests. The

inspectors also interviewed the licensee personnel who were responsible for collecting

and evaluating the PI data. Licensee procedures, records, and other documents

reviewed within this inspection area are listed in the Attachment. This inspection

satisfied three Emergency Preparedness inspection samples for PI verification on an

annual basis.

b. Findings

No findings were identified.

Cornerstone: Occupational Radiation Safety

a Inspection Scope

The inspectors reviewed Performance Indicator (PI) data collected from January 1,

2011, through March 31, 2012, for the Occupational Exposure Control Effectiveness PI.

For the reviewed period, the inspectors assessed CAP records to determine whether

high radiation area, VHRA, or unplanned exposures, resulting in TS or 10 CFR 20 non-

conformances, had occurred during the review period. In addition, the inspectors

reviewed selected personnel contamination event data, internal dose assessment

results, and ED alarms for cumulative doses and/or dose rates exceeding established

set-points. The reviewed data were assessed against guidance contained in Nuclear

Energy Institute 99-02, "Regulatory Assessment Indicator Guideline," Rev. 6. The

reviewed documents relative to these PI reviews are listed in Sections 2RS1 and 4OA1

of the Attachment.

b. Findings

No findings were identified.

Public Radiation Safety (PS) Cornerstone

The inspectors reviewed the Radiological Effluent Technical Specification/Offsite Dose

Calculation Manual Radiological Effluent Occurrences PI results from June 18, 2010

through May 2012. The inspectors reviewed PERs, liquid and gaseous effluent release

permits, effluent dose data, and licensee procedural guidance for classifying and

reporting PI events. Reviewed documents are listed in Sections 2RS6 of the

Attachment.

The inspectors completed 1 of the required samples for IP 71151.

Enclosure

35

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

.1 Review of items entered into the Corrective Action Program:

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into the

licensees CAP. This review was accomplished by reviewing daily PER and Service

Request (SR) reports, and periodically attending Corrective Action Review Board

(CARB) and PER Screening Committee (PSC) meetings.

.2 Annual Follow-up of Selected Issues - Operations with a Potential for Draining the

Reactor Vessel (OPDRVs)

a. Inspection Scope

The inspectors reviewed the licensees response to the NRCs EMG-11-03, Enforcement

Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee

Noncompliance with Technical Specification Containment Requirements During

Operations with a Potential for Draining the Reactor Vessel (OPDRVs). The inspectors

focused on the changes made to licensee procedure 3-POI-200.5, Operations with

Potential for Draining the Reactor Vessel/Cavity and discussed OPDRVs with

Operations staff. The inspectors reviewed the Main Control Room (MCR) operating logs

to verify OPDRVs were identified by the MCR operating crew and appropriate action

taken were necessary. The inspectors also walked down portions of the alternate

reactor water level control make-up and let-down line line-ups to verify they were

established in accordance with the licensees procedures. Documents reviewed are

listed in the Attachment. This activity constituted one in-depth selected issue.

b. Assessment and Observations

No findings were identified.

.3 Semiannual Review to Identify Trends

a. Inspection Scope

As required by Inspection Procedure 71152, the inspectors performed a review of the

licensees CAP implementation and associated documents to identify trends that could

indicate the existence of a more significant safety issue. The inspectors review included

the results from daily screening of individual PERs (see Section 4OA2.1 above),

licensee trend reports and trending efforts, and independent searches of the PER

database and WO history. The inspectors review nominally considered the six-month

period of January 2012 through June 2012, although some searches expanded beyond

Enclosure

36

these dates. Additionally, the inspectors review also included the Integrated Trend

Reports (ITR) from the first and second quarters of fiscal year 2012. The licensee

reports covered the period of October 1, 2011, to March 31, 2012. Furthermore, the

inspectors verified that adverse or negative trends identified in the licensees PERs,

periodic reports and trending efforts were entered into the CAP. Inspectors interviewed

the appropriate licensee staff and also reviewed procedures, NPG-SPP-02.8, Integrated

Trend Review and NPG-SPP-02.7, PER Trending.

The purpose of the licensees integrated trend reviews was to identify the top site and

departmental issues (gaps to excellence) requiring management attention. Other

objectives were to provide status of the top issues and their progress to resolution,

identify continuing issues, emerging trends and issues to be monitored, review progress

towards resolving past top issues, review issues identified by external organizations

such as the NRC, INPO, Nuclear Safety Review Board (NSRB), QA, etc., and determine

why they were not identified by line organizations. This activity constituted one

semiannual trend review inspection sample.

b. Findings and Observations

No findings were identified, but the inspectors identified a number of observations as

discussed below.

Inspectors observed licensee-identified issues and trends in both the first and second

quarter ITRs that were identical or similar in nature. Inspectors reviewed the repeat

issues to assess the licensees progress of corrective actions associated with the issues

and trends identified. Some of the more notable site/departmental issues were as

follows:

  • Corrective Action Program (CAP): The CAP has not been considered as a core

business function by the station. Improvement is needed with problem identification,

cause evaluations and timely completion of corrective actions. This issue was

documented in PERs 346645 and 471366.

  • Human Performance/Standards: Human performance practices resulted in

consequential events, specifically: procedure use and adherence, procedure quality,

accountability, human performance fundamentals, and the observation program.

This issue was documented in PERs 410308 and 491985.

  • Procedure Use and Adherence: The first quarter 2012 ITR included this in the

Human Performance area (Issue #2) and developed actions to drive rigorous use of

procedures throughout all organization. The second quarter 2012 ITR included this

with the Procedure/Work Order Quality/Procedure Use and Adherence area (Issue

  1. 2). This issue was documented in PERs 410308 and 491985.

The second quarter ITR contained fifteen fundamental problem statements that were

developed as a result of the 95003 supplemental inspection. The process is intended to

determine the root organizational and/or cultural causes of these issues. Corrective

actions were under development for these fifteen problem areas at the end of the

reporting period.

Enclosure

37

The inspectors conducted an independent review of the licensees CAP to identify

potential adverse trends. The inspectors identified a potential adverse trend with the

licensees control of transient combustible materials in plant areas. A review of PERs

from January 2012 to June 2012 revealed twelve PERs associated with transient and

excessive combustible materials in plant areas however, a PER that identified this as a

trend was not identified by the licensee staff. The inspectors discussed this issue with

the appropriate licensee staff and PER 577382 was initiated to document this as an

adverse trend.

4OA3 Event Follow-up

.1 Unit 3 Automatic Reactor Scram Following Refueling Outage

a. Inspection Scope

On May 22, 2012, while recovering from a refueling outage with control rod and main

turbine generator off-line testing in progress, Unit 3 automatically scrammed from 19.5

percent power. Unit 3 scrammed due to a loss of offsite power when an inadvertent

actuation of 3A Unit Station Service Transformer (USST) differential relay 387SA

resulted from an incorrect relay setting. Inspectors promptly responded to the control

room and verified that the unit was stable in Mode 3 (Hot Shutdown), and confirmed that

all safety-related mitigating systems had operated properly. Inspectors evaluated safety

equipment and operator performance before and after the event by examining existing

plant parameters, strip charts, plant computer historical data displays, operator logs, and

the critical parameter trend charts used for the post-trip report. Inspectors also

interviewed responsible on-shift operations personnel, examined the implementation of

the applicable annunciator response procedures and abnormal operating instructions,

including 3-AOI-100-1, Reactor Scram, and reviewed the written notification made in

accordance with 10 CFR 50.72. Inspectors discussed the preliminary cause of the

incorrect relay setting with responsible Operations and Engineering personnel and

monitored Plant Oversight Review Committee (PORC) event review and restart

meetings. This review included only initial event follow-up.

b. Findings

No findings were identified.

.2 Unit 3 Manual Reactor Scram Following Refueling Outage

a. Inspection Scope

On May 24, 2012, Unit 3 was manually scrammed from Mode 2 (less than 1% rated

power) when operators ranged down the Intermediate Range Monitor (IRM) 'H'

instrument, instead of up, resulting in half scram on Reactor Protection System (RPS) 'B'

trip system. The half scram was being reset after IRM 'H' was properly ranged. As the

operator adjusted the reset scram switch, a spike on IRM 'A' was received on the RPS

'A' trip system, resulting in a partial rod insertion. When the operator identified multiple

Enclosure

38

rods inserting, the actions of the Reactor Scram Procedure, 3-AOI-l00-1, were followed

and a manual scram was inserted. The inspectors evaluated safety equipment and

operator performance before and after the event by examining existing plant parameters,

strip charts, plant computer historical data displays, operator logs, the alarm typewriter

Sequence of Events printout, and the critical parameter trend charts in the post-trip

report. The inspectors interviewed responsible on-shift Operations personnel, examined

the implementation of annunciator response and abnormal operating procedures,

(including 3-AOI-100-1, Reactor Scram) and reviewed the written notification made in

accordance with 10 CFR 50.72. This review included only initial event follow up.

b. Findings

No findings were identified

.3 Unit 3 Automatic Reactor Scram and Forced Outage

a. Inspection Scope

On May 29, 2012, Unit 3 automatically scrammed from 78 percent power due to a power

to load unbalance (i.e., main generator load reject) automatic trip of the main turbine

generator from an A-B phase trip of the main transformer differential relay 387T. The

licensee identified the cause of the differential relay trip to be a B phase current

transformer manufactured and installed with opposite polarity. Preliminarily, the licensee

revealed that factory acceptance and field testing failed to detect the manufacturing

defect of reverse polarity. Inspectors promptly responded to the control room and

verified that the unit was stable in Mode 3 (Hot Shutdown), and confirmed that all safety-

related mitigating systems had operated properly. Inspectors evaluated safety

equipment and operator performance before and after the event by examining existing

plant parameters, strip charts, plant computer historical data displays, operator logs, and

the critical parameter trend charts used for the post-trip report. Inspectors also

interviewed responsible on-shift operations personnel, examined the implementation of

the applicable annunciator response procedures and abnormal operating instructions,

including 3-AOI-100-1, Reactor Scram, and reviewed the written notification made in

accordance with 10 CFR 50.72. Inspectors discussed the preliminary cause of the failed

acceptance and installation testing with responsible Operations and Engineering

personnel. This review included only initial event follow-up.

Operators commenced restart of Unit 3 (i.e., entered Mode 2) on June 2 and achieved

full power on June 6, 2011. During this short forced outage the inspectors examined the

conduct of critical outage activities pursuant to technical specifications, applicable

procedures, and the licensees risk assessment and maintenance plans. Some of the

more significant outage activities monitored, examined and/or reviewed by the

inspectors were as follows:

  • Plant Oversight Review Committee (PORC) event review and restart meetings.
  • Reactor startup and power ascension activities per 3-GOI-100-1A, Unit Startup
  • Reactor vessel and coolant heatup per 3-SR-3.4.9.1(1), Reactor Heatup and

Cooldown Rate Monitoring

Enclosure

39

  • Outage risk assessment and management
  • Control and management of forced outage and emergent work activities

Corrective Action Program

The inspectors reviewed PERs generated during the Unit 3 forced outage and attended

management review committee meetings to verify that initiation thresholds, priorities,

mode holds, and significance levels were assigned as required.

b. Findings

No findings were identified

.4 (Closed) Licensee Event Report (LER) 05000296/2011-003-00, Automatic Reactor

Scram Due to a Main Turbine Generator Load Reject.

a. Inspection Scope

On September 28, 2011, Unit 3 automatically scrammed from 100 percent power due to

a power to load unbalance (i.e., main generator load reject) automatic trip of the main

turbine generator (MTG) caused by a broken debris screen. The initial follow-up of this

event by the inspectors was documented in Section 4OA3.10 of IR 05000296/2011004.

The inspectors reviewed the applicable LER that was issued on November 28, 2011,

and its associated PER 440539, which included the root cause analysis (RCA) and

corrective actions. The licensee concluded that the direct cause of the Unit 3 turbine trip

and scram was the isolated-phase bus C debris screen failure.

b. Findings

No findings were identified

.5 (Closed) Licensee Event Report (LER) 05000259,296 /2011-009-02, As-Found

Undervoltage Trip for the Reactor Protection System 1A1 Relay that Did Not Meet

Acceptance Criteria During Several Surveillances

a. Inspection Scope

The inspectors reviewed Revision 2 of LER 05000259/2011-009 dated April 25, 2012,

PER 486780, and the associated operability determination, and corrective action plans.

This revised LER was submitted to provide the results of the licensees completed

investigation and evaluation of a second Reactor Protection System (RPS) relay that did

not meet its acceptance criteria during previous surveillance testing for the same reason.

The original LER 05000259/2011-009-00 dated December 5, 2011, the revised LER

05000259/2011-009-01 dated January 31, 2012, applicable PERs 413140 and 442914,

including root cause analysis, operability determination and corrective action plans, were

reviewed by the inspectors and documented in Sections 4OA3.1 and 4OA7 of NRC IR

Enclosure

40

05000259/2012002. As a result of this prior review, the licensee had identified one

violation of NRC requirements associated with Unit 1 RPS 1A1 relay.

On January 6, 2012, while performing an operability determination for the Unit 3 reactor

protection system (RPS) 3C1 relay undervoltage trips, the licensee determined that the

as-found undervoltage trip setpoint for the Unit 3 relay was less than the required

acceptance criteria during several technical specification surveillances. Seven of the

last thirteen surveillance test results were below the technical specification acceptance

criteria. Therefore, based on performance history, the RPS 3C1 relay was determined to

be inoperable from June 9, 2006, to February 2, 2012, when the relay was replaced.

The licensee determined the previous root cause and corrective actions were applicable

in that the surveillance test program did not require past operability reviews when out of

calibration technical specification conditions were corrected during surveillances.

The inspectors reviewed the second LER revision and verified that the supplemental

information provided in the LER was complete and accurate and that the information

was not of a significant nature to warrant any change to the original LER finding.

This licensee identified violation constitutes an additional example as documented in

NRC IR 05000259/2012002 and is not an individual non-cited violation. Further

corrective actions for this additional example are expected to be taken in conjunction

with corrective actions for the previous violation.

b. Findings

One finding for the original and Revision 1 of the LER was previously identified in

Section 4OA7 of NRC IR 05000259/2012002. No additional findings were identified.

The revised LER is considered closed.

.6 (Closed) Licensee Event Report (LER) 05000296/2012-001-00, Annunciator Panel

Power Supply Fire in Unit 3 Control Room

a. Inspection Scope

On January 26, 2012, Unit 3 main control room operators smelled smoke and observed

a flame coming from the bottom of an annunciator panel 3-XA-55-5A power supply. Fire

Operations personnel arrived on the scene within five minutes. The affected circuit

breaker was opened and fire extinguished within ten minutes. Operations personnel

increased plant monitoring to compensate for indications that lost their alarming

functions when the circuit breaker was opened. The fire damage was limited to the

failed annunciator power supply and the power supply directly above it. The inspectors

reviewed the details surrounding this event, interviewed operations and engineering

personnel involved with this issue and reviewed the licensees apparent cause

determination report. This was captured in the licensees corrective action program as

problem event report (PER) 496592. This LER is closed.

Enclosure

41

b. Findings

Introduction: A self-revealing Green finding (FIN) was identified for the licensees failure

to perform preventive maintenance on the Unit 3 Main Control Room (MCR) annunciator

power supplies. As a result, a power supply failed which led to a fire in annunciator

panel 3-XA-55-5A in the Unit 3 MCR.

Description: On January 26, 2012, Unit 3 main control room operators smelled smoke

and observed a flame coming from the bottom of an annunciator panel power supply.

Within ten minutes, the Fire Brigade responded to the MCR and the circuit breaker was

opened for the affected power supply which extinguished the fire. Damage was confined

to two power supplies in annunciator panel 3-XA-55-5A. The damaged power supplies

were replaced on January 27, 2012 in accordance with Work Order (WO) 113155456.

Corrective action document PER 496592 identified the direct cause of the annunciator

power supply failure as an overcurrent condition caused by a failed electrolytic capacitor.

This PER referenced EPRI recommendations to change out components with electrolytic

capacitors on a time based frequency. TVAs apparent cause concluded the power

supply (capacitor), installed for thirty four (34) years, experienced an age related failure

due to a lack of preventive maintenance.

Age-related failures of electrolytic capacitors have been documented in the industry.

Electric Power Research Institute (EPRI) document, TR-112175, Capacitor Application

and Maintenance Guide, dated August 1999, stated that capacitor change outs are

performed between 7 and 15 years depending on vendor recommendations and plant

operating experience. Another EPRI document, Power Supply Maintenance and

Application Guide (1003096), dated December 2001, stated that many of the power

supplies that failed had been in service greater than 15 years on average. Since 2008

three PERs have been entered in TVAs CAP that document similar failures of these

annunciator power supplies on both Unit 2 and 3 main control room panels. PER

391479 was initiated in June 2011 to evaluate the equipment reliability classification of

these power supplies. Corrective actions to evaluate the annunciator power supply

preventive maintenance strategy were in progress when the fire occurred.

These power supplies were classified as Quality-Related, Non-Critical, Low Duty-Cycle,

Mild Service Condition in accordance with licensee procedure NPG-SPP-09.18.2,

Equipment Reliability Classification. Licensee procedure TVA-NQA-PLN89-A, Nuclear

Quality Assurance Plan stated that the nuclear maintenance program including

corrective and preventive maintenance shall ensure that quality-related structures,

systems and components are maintained at a level sufficient to perform their intended

functions.

Analysis: The failure to perform preventive maintenance on the Unit 3 annunciator

power supplies prior to their age related failure was a performance deficiency.

Specifically, TVA procedure TVA-NQA-PLN89-A, Nuclear Quality Assurance Plan stated

that the nuclear maintenance program including corrective and preventive maintenance

shall ensure that quality-related structures, systems and components are maintained at

a level sufficient to perform their intended functions. These power supplies were

classified as Quality-Related according to TVA procedure NPG-SPP-09.18.2, Equipment

Enclosure

42

Reliability Classification. As a result of the performance deficiency, a Unit 3 MCR

annunciator power supply was left in service for 34 years, failed due to an aged

electrolytic capacitor and resulted in an over-current related fire. The performance

deficiency was determined to be more than minor because it was considered sufficiently

similar to example 4.f of Inspection Manual Chapter (IMC) 0612, Appendix E, for an

issue that resulted in a fire hazard in a safety-related area of the plant. The finding was

associated with the Initiating Events Cornerstone and initially characterized according to

IMC 0609, Significance Determination Process (SDP), Attachment 4, Phase 1 - Initial

Screening and Characterization of Findings. The results of this analysis required a

phase 3 evaluation in accordance with IMC 0609 because the finding increased the

likelihood of and actually caused a fire in the Unit 3 MCR. The regional Senior Reactor

Analyst performed a Phase 3 analysis for the issue. Pictures were provided to an NRC

contractor who provides expertise in fire damage for the agency. It was determined that

the configuration of the fire would not likely result in damage to anything of significance

because the metal box that the annunciators power supplies are located in, would

prevent propagation of the fire beyond the box. It is also unlikely that enough heat or

smoke could be created to require control room evacuation, which would impact the

human actions that would be performed to shut down the plant. Without an impact to

additional plant equipment, or a major impact on human action failure rates, the finding

was determined to be Green. The cause of this finding was related to the cross cutting

aspect of Problem Identification in the Corrective Action Program component of the

Problem Identification and Resolution area, because the licensee was aware of three

previous failures of these power supplies in July 2009 and should have recognized that

the electrolytic capacitors, installed beyond their recommended service life, required

replacement prior to failure P.1(a).

Enforcement: Enforcement action does not apply because the performance deficiency

did not involve a violation of regulatory requirements since the main control room

annunciator power supplies were not safety-related. Because the finding does not

involve a violation, was entered into the licensees corrective action program as PER

496592, and has very low safety significance, it is identified as FIN 05000296/2012003-

04, Failure to Perform Preventive Maintenance on the Unit 3 Main Control Room

Annunciator Power Supplies.

4OA6 Meetings, Including Exit

.1 Exit Meeting Summary

On April 13, 2012, regional inspectors presented the results of the Occupational

Radiation Safety inspection to Mr. P. Summers, Director Safety and Licensing, and other

members of the licensees staff.

On April 20, 2012, regional inspectors presented the results of the Unit 3 Inservice

Inspection to members of the licensees staff.

On June 22, 2012, regional inspectors presented the results of the Public Radiation

Safety inspection to Mr. K. Polson, Site Vice President, and other members of the

licensees staff, who acknowledged the findings. On July 03, 2012, regional inspectors

Enclosure

43

presented changes to the inspection results via telephone to Mr. S. Bono, General

Manager Site Operations, and other members of the licensees staff, who acknowledged

the changes.

On June 29, 2012, regional inspectors presented the results of the Emergency

Preparedness inspection to Mr. S. Bono, General Manager Site Operations, and other

members of the licensees staff.

On July 10, August 10 and 14th, 2012, the resident inspectors presented the results of

the quarterly integrated onsite inspection to Mr. K. Polson, Site Vice President, and other

members of the licensees staff, who acknowledged the findings.

All proprietary information reviewed by the inspectors as part of routine inspection

activities were properly controlled, and subsequently returned to the licensee or

disposed of appropriately.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which met the criteria of the NRC

Enforcement Policy, for being dispositioned as a Non-Cited Violation:

failure to establish adequate work instructions to ensure proper installation of the gap

setting between the actuator stem and valve stem of Unit 1 HPCI, (High Pressure

Coolant Injection), turbine stop valve, 1-FCV-073-0018. On April 19, 2012, during

the performance of a quarterly surveillance test the turbine stop valve, 1-FCV-073-

0018, failed to close upon repeated demands. A Phase 3 analysis determined the

significance of the finding was very low safety significance (Green) The regional

Senior Reactor Analyst performed a Phase 3 SDP analysis on the finding. The risk

was dominated by the unavailability of the HPCI during the repair time after

discovery of the Stop Valve issue. The finding was determined to be GREEN in the

SDP, primarily due to the short period of time it was fully non-functional. The

licensee initiated PER 539040 to enter the issue into their corrective action program.

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Adkins, Manager EP Systems

S. Bono, Plant General Manager Site Operations

C. Boschet, QA Manager

J. Boyer, Acting Assistant Director of Engineering

B. Bruce, Acting Systems Engineering Manager

D. Campbell, SM

S. Clement, Operations Fire Protection

M. Durr, Director of Engineering

M. Ellet, Maintenance Rule Coordinator

J. Emens, Nuclear Site Licensing Manager

A. Feltman, Emergency Preparedness Manager

J. Ferguson, Radiation Protection Support Superintendent

C. Gannon, Plant Manager

H. Higgins, Acting Licensed Operator Requalification Supervisor

D. Hughes, Operations Manager

S. Kelly, Work Control Manager

D. Kettering, Electrical Systems Engineering Manager

J. Kimberlin, FIN Manager

R. King, Design Engineering Manager

W. Lee, Corporate EP Manager

R. Norris, Radiation Protection Manager

S. Norris, Engineering Supervisor

P. Parker, Site Security Manager

J. Parshall, Manager, EP Program Planning and Implementation

K. Polson, Site Vice President

E. Quidley, EDG Project Manager

M. Rasmussen, Operations Superintendent

H. Smith, Fire Protection Supervisor

R. Stowe, Equipment Reliability Manager

P. Summers, Director of Safety and Licensing

J. Underwood, Chemistry Manager

C. Vaughn, Operations Superintendent

S. Walton, Electrical Maintenance Superintendent

M. Wilson, Director of Training

A. Yarbrough, BOP System Engineering Supervisor

Attachment

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000259,260,296/2012-003-01 NCV Failure to Maintain Flood Barrier Results in

Inoperable Safety Related Pumps (Section 1R15.)

05000259,260,296/2012003-02 NCV Failure to Properly Prepare a DOT Type A Package

for Transport) (Section 2RS8)

05000259,260,296/2012003-03; NCV Failure to Implement DOT Type A Package Closure

Requirements) (Section 2RS8)

05000260,296/2012003-04 FIN Failure to Establish Preventive Maintenance for

Unit 2 and 3 Main Control Room Annunciator

Power Supplies (Section 4OA3.6)

Closed

05000296/2011-003-00 LER Automatic Reactor Scram Due to a Main Turbine

Generator Load Reject (Section 4OA3.4)

05000259,296/2011-009-02 LER As-Found Undervoltage Trip for the Reactor

Protection System 1A1 Relay that Did Not Meet

Acceptance Criteria During Several Surveillances

(Section 4OA3.5)

05000296/2012-001-00 LER Annunciator Panel Power Supply Fire in Unit 3

Control Room (Section 4OA3.6)

Discussed

None

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

0-GOI-300-4, Switchyard Manual, Rev. 85

0-OI-30F, Common DG Building Ventilation, Rev. 30

0-OI-30F/ATT-1, Attachment 1 Valve Lineup Checklist, Rev. 28

0-OI-30F/ATT-1A, Attachment 1A Valve Lineup Checklist Unit 3, Rev. 28

0-OI-30F/ATT-2, Attachment 2 Panel Lineup Checklist, Rev. 29

LCEI-CI-C9, Procedure for Walkdown of Structures for Maintenance Rule, Rev. 5

NPG-SPP-10.2, Clearance Procedure to Safely Control Energy, Rev. 3

OPDP-2, Switchyard Access and Switching Order Execution, Rev. 6

PER 390201, Concrete Piers in Switchyard Showing Signs of Degradation

PER 534276, Conflicting information on 161-kv grid status during U3R15 outage

PER 536136, U3 Transformer Project Material Storage Area Poses U2 Concern

PER 538016, Intake has no working ventilation fans

PER 539365, Switchyard Deficiencies

PER 539371, 500kV and 161kV Concrete Pedestals

PER 539580, Transformer Yard Discrepancies

PER 539581, Ground Soft in Transformer Yard

PER 539582, Concrete Pedestal Degraded in Transformer Yard

PER 539583, Transformer Yard 500kV Tower Damaged

PER 546871, Hot Weather procedure

PER 566119, Freeze protection heater still in place

PER 568461, Hot weather procedure

PSO PER 546093, Transformer Yard 500 kV P.O. Structure Damage

TRO-TO-SPP-30-128, Browns Ferry Nuclear Plant Grid Operating Guide, Rev. 13

TVA-SPP-10.010, NERC Standard Compliance Processes Shared by TVA's Nuclear Power and

Energy Delivery Organizations, Rev. 0

UFSAR-8.4, Normal auxiliary Power System, Amendment 23

WO 113419591, Hand switch stuck in slow position

WO110926526, Plant air wash pump

Section 1R04: Equipment Alignment

0-47E861-1, Flow & Control Diagram Diesel Starting Air System Diesel Generator A, Rev. 17

0-OI-82/ATT-1A, Standby Diesel Generator A, Valve Lineup Checklist, Rev. 100

0-OI-82/ATT-2A, Standby Diesel Generator A, Panel Lineup Checklist, Rev. 100

0-OI-82/ATT-3A, Standby Diesel Generator A, Electrical Lineup Checklist, Rev. 100

0-OI-82/ATT-4A, Standby Diesel Generator A, Instrument Inspection Checklist, Rev. 101

1-OI-71, Reactor Core Isolation Cooling System, Rev. 14

1-OI-71/ATT-1, RCIC System, Valve Lineup Checklist, Rev. 13

1-OI-71/ATT-2, RCIC System, Panel Lineup Checklist, Rev. 13

1-OI-71/ATT-3, RCIC System, Electrical Lineup Checklist, Rev. 13

3-OI-74, Residual Heat Removal System, Revision 0104

3-OI-74/ATT-1, Valve Lineup Checklist Unit 3, Revision 0086

3-OI-74/ATT-2, Panel Lineup Checklist, Revision 0086

3-OI-74/ATT-3, Electrical Lineup Checklist, Revision 0087

DWG 1-47E813-1, Flow Diagram RCIC System, Rev. 33

Attachment

4

Technical Requirements Manual Section 3.5.3, Equipment Area Coolers

Technical Requirements Manual Section 3.5.4, Maintenance of Filled Discharge Piping

Updated Final Safety Report Section 4.8, Residual Heat Removal System

Section 1R05: Fire Protection

0-SI-4.11.E.1.B(2), Safety Related Fire Hose Replacement, Rev 08

0-SI-4.11.E.1.B(2)/ATT-1, Attachment 1 Fire Hose Replacement Data Sheet, Rev. 08

0-TI-470, Temporary Wiring And Electrical Equipment (600 Volt Or Less), Rev. 1

Active FPIPs dated 5/1/2012

Active FPIPs List, 06/01/2012

DWG 0-47W216-51, Fire Protection - 10 CFR 50 Appendix R, Fire Area Compartmentation and

Zone Drawings, Rev. 7

DWG 0-47W216-56, Fire Protection - 10 CFR 50 Appendix R, Fire Area Compartmentation and

Zone Drawings, Plan EL 593.0 & 586.0, Rev. 7

Fire Hazard Analysis Fire Zone 3-3

Fire Protection Report Vol. 1, Fire Hazards Analysis, Rev. 11

Fire Protection Report Vol. 2, Rev. 48

Fire Protection Report, Volume 1, Section 2, Fire Hazards Analysis, Rev. 11

Fire Protection Report, Volume 2,Section IV, Pre-Plan No. RX2-519 Torus Area and HPCI

Room

Fire Protection Report, Volume 2,Section IV, Pre-Plan No. RX2-519 NW

Fire Protection Report, Volume 2,Section IV, Pre-Plan No. RX2-519 SW

Fire Protection Report, Volume 2,Section IV, Pre-Plan No. RX2-565

FP-0-000-INS001(A), Inspection of Portable and Wheel Type Fire Extinguisher Stations

(Reactor Building), Rev. 17

FP-0-000-INS001(A)/ATT-2, Attachment 2 Inspection Check/Data Sheet Dry Chemical (12 yrs)

Co2 (5 yrs) Halon (12 yrs) Charging Cylinder (5 yrs), Rev. 17

FP-0-000-INS012, Fire Watch Expectations, Rev. 1

FP-0-000-INS019, Fire Protection Weekly Inspection, Rev. 13

NPG-SPP-09.17, Temporary Equipment Control, Rev. 1

NPG-SPP-18.4.6, Control of Fire Protection Impairments, Rev. 0

PER 545547, Room on 1C Hallway Contain Excessive Combustibles

PER 546065, Multiple Extension Cords Plugged Into One Another on 1C Hallway

PER 546188, Roving Fire Watch Route Sheet

Pre-Fire Plan for Browns Ferry Nuclear Plant - Reactor Building Unit 3, pre-plan No. RX3-593

Pre-Fire Plan for Browns Ferry Nuclear Plant - Reactor Building Unit 3, pre-plan No. RX3-565

TVA Safety Manual Chapter 2, Procedure 1004, Extension Cords and Attachments, Rev. 4

Section 1R07: Annual Heat Sink Performance

0-TI-322, RHR Heat Exchanger Performance Testing, Rev. 0

0-TI-364, ASME Section XI System Pressure Tests, Rev. 6

0-TI-389, Raw Water Fouling and Corrosion Control, Rev. 16

0-TI-522, Program for Implementing NRC Generic Letter 89-13, Rev. 1

0-TI-63, RHRSW Flow Blockage Monitoring, Rev. 25

DCN T38580A, Repair 3A and 3C RHR Heat Exchanger Flange Leaks Using Furmanite Sealing

Compound, Rev. A

DWG 0-47E452-1, Mechanical Residual Heat Removal System, Rev. 15

DWG 3-47W452-10, Mechanical Residual Heat Removal System, Rev. 15

Attachment

5

DWG 69-D-160-03, Tube Sheet Details, Rev. 6

EDC 69311A, Repair of 3B and 3D RHR Heat Exchanger Flange Leaks, Rev. A

EPRI NP-7552, Heat Exchanger Performance Monitoring Guidelines, Dec. 1991

Evaluation of Temporary Sealing Compound used as a replacement gasket, Dated 5/8/2012

MCI-0-000-LKS001, On-Line leak Sealing, Rev. 15

MCI-0-074-HEX001, Maintenance of RHR Heat Exchangers, Rev. 23

NPG-SPP-09.7, Corrosion Control Program, Rev. 2

N-VT-4, System Pressure Test Visual Examination Procedure, Rev. 23

P.S. 4.M.4.3 (R4), General Engineering Specification, G-29B, Online Leak Sealing, Rev. 4

PER 543035, Temporary Furmanite repairs on RHR HX 3A, 3C, and 3D are not being tracked

PM 500103065, Inspect / Clean RHRSW Pump Pit

PM 500108601, PM Performance of 0-TI-63, RHRSW Flow Blockage Monitoring, for

1-HEX-74-900A & C.

PM 500116540, PM Performance of 0-TI-63 for 2-HEX-74-900A and 2-HEX-74-900C

PM 500116541, PM Performance of TI-63 for 2-HEX-74-900B and 2-HEX-74-900D

PM 500126928, Clean BFN-3-HEX -074-0900A Heat Exchanger

PM 500126929, PM Performance of 0-TI-63, RHRSW Flow Blockage Monitoring, for

3-HEX-74-900A & C

PM 500126931, Clean BFN-3-HEX -074-0900B Heat Exchanger

PM 500126932, PM Performance of 0-TI-63 for 3-HEX-74-900B and 3-HEX-74-900D.

PM 500126933, Disassemble, Clean, Inspect BFN-3-HEX -074-0900C

PM 500126935, Disassemble, Clean, Inspect BFN-3-HEX -074-0900D.

PM 500133228, PM Perform TI-63 for 1-HEX-74-0900B and D

WO 08-712116, Repair Leak, 3D RHR Heat Exchanger

WO 112857671, Test RHR Heat Exchanger 3A and 3C

WO 95-20541-000 (3A and 3C)

Section 1R11: Licensed Operator Requalification

2-AOI-57-5B, Loss of Instrument & Control Bus

2-AOI-70-1, Loss of Reactor Building Closed Cooling Water

2-C-5, Level/Power Control

2-EOI-1, Reactor Pressure Vessel Control

Section 1R12: Maintenance Effectiveness

0-AOI-100-3, Flood Above Elevation 558, Rev. 35

0-AOI-100-3, Flood Above Elevation 558, Rev. 35

0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting -

10CFR50.65, Rev. 37

0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -

10CFR50.65, Rev. 37

Cause Determination Evaluation 1041, May 31, 2011

Design Criteria BFN-50-7023, Residual Heat Removal Service Water (RHRSW) System

Design Criteria BFN-50-7067, Emergency Equipment Cooling Water (EECW) System

Design Criteria BFN-50-C-7101, Protection from Wind, Tornado Wind, Tornado

Depressurization, Tornado Generated Missiles, and External Flooding

FSAR Section 10.10, Emergency Equipment Cooling Water (EECW) System, BFN-24

FSAR Section 10.9, RHR Service Water System, BFN-24

FSAR Section 10.9, RHR Service Water System, BFN-24

Attachment

6

FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,

BFN-24

FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,

BFN-24

FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology, BFN-24

FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology, BFN-24

MCI-0-023-PMP002, Maintenance of EECW and RHRSW Pumps, Rev. 52

MCI-0-023-PMP003, Emergency Equipment Cooling Water and Residual Heat Removal Service

Water Pump Removal and Installation, Rev. 12

MCI-0-023-PMP004, EECW and RHRSW Pump Impeller Adjustment, Rev. 05 and 06

MPI-0-260-DRS001, Inspection and Maintenance of Doors

NPG-SPP-03.4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting -

10CFR50.65, Rev. 0

NPG-SPP-06.10, NPG Fix It Now (FIN) Team Process, Rev. 0

NPG-SPP-07.1, On-Line Work Management, Rev. 05

PER 234151, Unit 2 IRM scram signal

PER 310544, Gaps in A and D RHRSW Pump Room Flood Doors

PER 383975, Reliability of RHRSW Pump Room Door Seals

PER 402414, IRM (a)(1) plan

PER 469640, BFN-0-DOOR-260-C-RHRSW, Aggregate Impact of RHRSW Pump Room Doors

PER 470350, BFN-0-DOOR-260-C-RHRSW May Not Seal

PER 481145, B and D RHRSW Pump Room Watertight Doors Were Found Closed and Locked,

But Not Mechanically Restrained

PER 482838, RHRSW B Pump Room Door Failed Chalk Test

PER 482867, RHRSW D Pump Room Door Failed Chalk Test

PER 524957, Review past 48 months of IRM data for MR failures.

PER 532050, NRC Identified C3 EECW Pump Foundation Hole Flood Protection Cover

Inadequately Installed

PER 546734, Lack of specified torque value for pump coupling bolts

PER 561666, NRC Walkdown Identified RHRSW Door Issues

PER 563567, Site Tolerance of Degraded/Nonconforming Issue

PER 563727, RHRSW Intake Structure Doors Have Not Been Evaluated for MR (a)(1)

PER 566123, Document Former NRC Senior Resident Observation

Plant Level Event Data from Mar. 2010 to Feb. 2012

SR 565020, Inaccurate Past Operability Due to CAP Input

SR 568840, NRC Identified - Failure to Accurately Document NRC Observations in CAP

SR 569912, Inconsistency in Flood Cover Description Between Maintenance Procedures

Technical Specification and Basis 3.7.1 Residual Heat Removal Service Water (RHRSW)

System, Amendment 234

Technical Specification and Basis 3.7.2 Emergency Equipment Cooling Water (EECW) System

and Ultimate Heat Sink (UHS), Amendment 234

U1,2,3 Maintenance Rule Data from Nov. 2009 to Feb. 2012

Units 1,2,3 System 092 (IRMs) Health Reports from 10/1/2011 to 1/31/2012

Unplanned Scram Data from Mar. 2010 to Feb. 2012

WO 111457995, Repair BFN-0-DOOR-260-C-RHRSW

WO 111835839, D RHRSW Upper Dog Catching and Missing Dog

WO 111926930, B RHRSW Dogs Lower Linkage Disconnected

WO 112744581, C3 EECW Pump Vibes in Alert, Troubleshoot and Repair

Attachment

7

WO 112972845, Impeller gap adjustment of A3 EECW pump

WO 113062982, Repair BFN-0-DOOR-260-B-RHRSW

WO 113062984, Repair BFN-0-DOOR-260-D-RHRSW

WO 113228273, Why is A RHRSW Door Locked - Door Doesnt Fully Close

WO 113348314, C RHRSW Lower Left Dragging and Scraping Metal

WO 113446620, Performance of 3-SI-4.5.C.1(2) - EECW Pump Operation

WO 113456059, Raw Cooling Water Leak on 3B CRD Pump

WO 113474206, Performance of 3-SI-4.5.C.1(2) - EECW Pump Operation

WO 113475937, D Diesel Generator came up to 500 rpm

WO 113483626, Troubleshoot BFN-0-RLY-082-D/ALM

WO 113486500, Diesel Generator D Air Pressure Alarm Relay

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

1-OI-73, High Pressure Coolant Injection System, Rev. 22

1-SR-3.3.3.1.4(G), Verification of Remote Position Indicators for HPCI System Valves, Rev. 2

1-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated

Reactor Pressure, Rev. 21

BFN Unit 3 Defense in Depth Assessment May 4, 2012

BFN Unit 3 Defense in Depth Assessment, April 15, 16, 17, 18, 2012

BFN-ODM-4.18, Protected Equipment, Rev. 6

Browns Ferry Nuclear Plant Outage Risk Assessment Report, Unit 3 Cycle R15, Rev. 1

DWG 1-47E812-1, Rev. 34

DWG 68-XC-71, Schutte & Koerting Co. Manufacturing Drawing

EOOS Report, Unit 2, dated May 7, 2012

MCI-0-073-VLV001, HPCI Turbine Stop Valve - FCV 73-18 Disassembly, Inspection, Rework

and Reassembly, Revs. 12, 13

MSI-1-073-GOV001, HPCI Turbine Overspeed Trip Test, Rev. 7

NPG-SPP-7.0, Work Management

NPG-SPP-07.1, On Line Work Management, Rev. 5

NPG-SPP-07.2, Outage Management, Rev. 2

NPG-SPP-07.2.11, Shutdown Risk Management, Rev. 2

NPG-SPP-07.2.11, Shutdown Risk Management, Rev. 2

NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 07

NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 7

NPG-SPP-09.11, Probabilistic Risk Assessment (PRA) Program, Rev. 01

NPG-SPP-09.11.1, Equipment Out of Service (EOOS) Management, Rev. 04

NPG-SPP-7.2.11, Shutdown Risk Management, Rev. 2

ORAM Model Change Form, April 18, 2012

ORAM Sentinel Outage Safety Assessment, April 18, 2012

O-TI-367

Outage Risk Assessment Report, U3 Cycle R15, Rev. 1

PER 539040, HPCI Turbine Stop Valve Failed to Trip

PER 539556, HPCI Turbine Main Pump Vibration

PER 541156, HPCI Oil Tank Level Low

PER 541727, HPCI Gland Exhauster Pump Breaker

PER 547134, Shutdown Risk Management, Filling out DID Checklist Once per 24 Hours

PMT-0-000-MEC001, Leak Checks on Tube Fitting, Threaded, Flanged, Bolted or Welded

Connections, Rev. 7

Attachment

8

SR 541069, Adjust Sensitivity on Incipient Fire Detector

U3 ORAM Safety Function Status Report, dated May 5, 2012

WO 113426235, HPCI Turbine Stop Valve Failed to Trip

WO 113426235, HPCI Turbine Stop Valve PMT Step Text

WO 113429679, Task 10: 1-FCV-073-0018, Rev. 0

WO 113435872, HPCI Main & Booster Pump Head & Flow Rate Test

WO 113440357, HPCI Oil Tank Level Low

WO 113441055, Verification of Remote Position Indicators

WO 113445422, Adjust Sensitivity on Incipient Fire Detector

Section 1R15: Operability Evaluations

0-17W300-9, Mechanical Isometric drawing for EECW drains, Rev. 0

0-GOI-200-1, Freeze Protection Inspection, Rev. 69

0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -

10CFR50.65, Rev. 37

1-47E859-1, Flow Diagram Emergency Equipment Cooling Water, Rev. 81

1-47E859-1, Flow Diagram for EECW system Unit 1, Rev. 82

2-47E859-1, Flow Diagram for EECW system Unit 2, Rev. 31

3-47E859-1, Flow Diagram for EECW system Unit 1, Rev. 38

3-SI-4.5.C.1(2), EECW Pump Operation, Rev. 119

BFN-50-7067, General Design Criteria Document for the EECW system, Rev. 18

BFN-50-C-7067, EECW System Design Criteria, Rev. 18

Calculation MDN0026910163, Combustible Load Table, Rev. 42

DCN 69957, Appendix R Pump House Tunnel Fire Barrier, Rev. A

DWG 2-47E600-53A, Mechanical Instruments and Controls, Rev. 3

EPI-0-000-FRZ001, Freeze Protection Program for RHRSW Pump Rooms and Diesel

Generator Building, Rev. 19

Fire Protection Report Volume 1, Fire Hazards Analysis for Fire Area 25, Rev. 11

FSAR Section 10.9, RHR Service Water System, BFN-24

FSAR Section 12.2.7.1.2, Principle Structures and Foundations, Personnel Access Doors,

BFN-24

FSAR Section 2.4, Hydrology, Water Quality, and Aquatic Biology, BFN-24

MPI-0-260-DRS001, Inspection and Maintenance of Doors

NPG-SPP-09.0, Engineering, Rev. 1

NPG-SPP-09.3, Plant Modifications and Engineering Change Control, Rev. 6

Past Operability Form for PER 492957, Tarps on RHRSW Rooms

PER 310544, Gaps in A and D RHRSW Pump Room Flood Doors

PER 372194, FPR Justification on Intake Pumping Station Fire Barriers

PER 469640, BFN-0-DOOR-260-C-RHRSW, Aggregate Impact of RHRSW Pump Room Doors

PER 470350, BFN-0-DOOR-260-C-RHRSW May Not Seal

PER 481145, B and D RHRSW Pump Room Watertight Doors Were Found Closed and Locked,

But Not Mechanically Restrained

PER 492957, Tarps on RHRSW Rooms

PER 500804, Immediate Actions Taken for PER 492957 Not Documented

PER 520497, EECW check valve appears to be seeping and repressurizing pipe

PIC 70445, System 26, PER 372194 Corrective Action - IPS Fire Seals, Rev. 0

Prompt Determination of Operability (PDO) for 0-CKV-067-0502, Rev. 0

Prompt Determination of Operability for PER 569282

Attachment

9

SR 482359, RHRSW B Pump Room Door Failed Chalk Test

SR 482401, RHRSW D Pump Room Door Failed Chalk Test

SR 560210, NRC Walkdown Identified RHRSW Door Issues

SR 563000, Site Tolerance of Degraded/Nonconforming Issue

SR 563507, RHRSW Intake Structure Doors Have Not Been Evaluated for MR (a)(1)

SR 565020, Document Former NRC Senior Resident Observation

WO 111457995, Repair BFN-0-DOOR-260-C-RHRSW

Section 1R18: Plant Modifications

3-ARP-9-3E, Panel 9-3, 3XA-55-3E, Rev. 26

3-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 56

3-GOI-100-3B, Refueling Operations (RX Cavity Letdown and Vessel Re-Assembly), Rev. 50

3-SIMI-3A, Reactor Feedwater System Index, Rev. 32

ACE PER 427252(330400) Initial Cavity Flood-up Overflow into Ventilation Ducts

LCL-3-L-03-055, Reactor Water level Flood-Up Calibration, Rev. 5

Minor Mod DCN 70549, Reactor Water Level Flood-Up Transmitter and Indication Loop

Replacement, Rev. A

NPG-SPP-09.4, 10 CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 5

NPG-SPP-09.5, Temporary Alterations, Rev. 2

NPG-SPP-9.3, Plant Modifications and Engineering Change Control, Rev. 6

NPG-SPP-9.4, 10 CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 5

ODMI-2012-0004, FCV-73-16 Leakage

PER 427252, Initial Cavity Flood-up Overflow into Ventilation Ducts, (PER 330400)

PER 565572, U1 HPCI Steam Admission Valve Leakage

PER 565577, U1 HPCI Steam Admission Valve Leakage

PER 569927, Opportunity for Operations Turnover Improvement

PER 571068, Potential Grease Degradation

SII-3-L-03-055, 500 Reactor Water Level A Refuel Range LT-3-55 Special Calibration for

Vented Vessel and Fuel Pool Flood-Up, Rev. 2

TACF 1-12-001-073, Thermal Insulation Attached to BFN-1-FCV-073-0016, HPCI Steam Supply

Valve, Rev. 0

TACF 2-12-001-073, Thermal Insulation Attached to BFN-2-FCV-073-0016, HPCI Steam Supply

Valve, Rev. 0

VTD-OT01-0020, OTEK Corp. Ops Manual for HI-Q Programmable Controllers, Rev. 3

WO 112971110, WO Request for DCN 70549 to Implement 3-55 Loop Modification on U3

WO 113275768, Implement TACF 1-12-001-073 to remove insulation from BFN-1-FCV-073-

0016

WO 113322598, Implement TACF 2-12-001-073 to remove insulation from BFN-2-FCV-073-

0016

Section 1R19: Post-Maintenance Testing

0-OI-82, Standby Diesel Generator System, Rev. 129

0-SR-3.8.1.1(D), Diesel Generator D Monthly Operability Test, Rev. 39

0-TI-106, General Leak Rate Test Procedure, Rev. 14, performed on April 9, 2012

0-TI-360, Containment Leak Rate Programs, Rev. 33

0-TI-362, Inservice Testing of Pumps and Valves, Rev. 29

3-45E779-41, Wiring Diagram, 480V Shutdown Auxiliary Power Schematic Diagram, Rev. 19

3-45E779-51, Wiring Diagram, 480V Load Shed Div II Schematic Diagram, Rev. 19

Attachment

10

3-47E801-1-ISI, ASME Section XI, Flow Diagram Main Steam Code Class Boundaries, Rev. 19

3-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor Pressure Vessel and

Associated Piping, Rev. 21

3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, Rev. 21

3-SR-3.4.9.1(2), Reactor Vessel Shell Temperature and Reactor Coolant Pressure Monitoring

During In-Service Hydrostatic or Leak Testing, Rev. 15

3-SR-3.6.1.3.10(B) Primary Containment Local Leak Rate Test Main Steam Line B: Penetration

X-7B

3-SR-3.6.1.3.10(B-OUTBD), Primary Containment Local Leak Rate Test Main Steam Line B

Outboard Penetration X-7B, Rev. 06, performed on April 8, 2012

3-SR-3.8.1.1(3C) Diesel Generator 3C Monthly Operability Test, Rev. 42, performed on May

15, 2012

3-SR-3.8.1.7(3C), Diesel Generator 3C 24 Hour Run, Rev. 21, performed on April 24, 2012

ECI-0-000-RLY003, Replacement of Relays, Rev. 21

EII-0-000-TCC106, Troubleshooting, Doc. and Config. Control of Elect. Activities, Rev. 62

MCI-0-000-PCK001, Generic Maintenance Instructions for Valve Packing, Rev. 26

MCI-0-074-VLV002, Residual Heat Removal Motor Operated Valves, FCV-74-47, 48, 53 and 67

Disassembly, Inspection, Rework and Reassembly

MCI-0-082-GOV001, Standby Diesel Engine Governor Removal and Installation, Rev. 9

MCR logs

MMDP-1, Maintenance Management System

MSI-0-001-VSL001, Reactor Vessel Disassembly and Reassembly, Rev. 100

NPG-SPP-06.3, Pre-/Post-Maintenance Testing

PER 143225, High Vibration on Generator end bearing on 3D DG

PER 538810, Restart NOI U3RF15-002: RPV Head Deformation due to Foreign Object

PER 541788, High Vibrations on 3C DG

PER 548753, Extent of Condition for D DG, (3A)

PER 548755, Extent of Condition for D DG, (3B)

PER 548756, Extent of Condition for D DG, (3C)

PER 548757, Extent of Condition for D DG, (3D)

PER 553585, Hydro Procedure Discrepancy

SR 532953, 3-FCV-1-27 failed as-found LLRT

SR 542421, Smooth Indication Noted on the Top Surface of RPV Flange During U3R15

SR 546885, Address 3C DG axial vibration

SR 547405, As-found LLRT rotameter did not meet required accuracy

SR 548237, Four Studs Not Pulled While Tensioning the U3 RPV Head

VTD-W290-0050, Instruction Manual for Woodward EG-B10C Governor Actuator, Rev. 2

WO 112472092, Generator Replacement Testing for 3C EDG

WO 112505164, Perform as-left LLRT for B outboard MSIV, Penetration X-7B

WO 113324169, Reassemble Generator for 3C EDG

WO 113394336, Re-torque Valve Packing on 3-FCV-001-0027 (B Outboard MSIV)

WO 113429130, 3-BKR-231-0003B/3C needs cell switch adjustment

WO 113475937, D D/G Came Up To 500 RPM When Started During 0-SR-3.8.1.1(D)

WO 113480500, D/G D Monthly Operability Test

WO 113480917, Replace D D/G Governor Speed Stop Micro Switches

WO 113483626, Troubleshoot/Repair/Replace BFN-0-RLY-082-D/ALM

WO 113483967, D D/G Dryer Assembly High DP Causing Excessive Blow Down

WO 113484062, D D/G Dryer Assembly High DP Causing Excessive Blow Down

Attachment

11

WO 113484918, Lost Terminating Screw

WO 113484954, Extent of Condition for D DG, (3A)

WO 113484954, Extent of Condition for D DG, (3B)

WO 113484957, Extent of Condition for D DG, (3C)

WO 113484958, Extent of Condition for D DG, (3D)

WO 113486500, Troubleshoot/Repair/Replace DG D Air Pressure Alarm Relay

WO Instructions PMT for 113480917, Rev. 0

Section 1R20: Refueling and Other Outage Activities

0-47E820-1, Flow Diagram Control Rod Drive Hydraulic System, Rev. 32

0-OI-2B, Condensate Storage and Transfer System, Rev. 76

0-GOI-100-3A, Refueling Operations (In-Vessel Operations)

0-GOI-100-3B, Operations in Spent Fuel Pool Only

0-GOI-100-3C, Fuel Movement Operations During Refueling

0-GOI-100-3C, Fuel Movement Operations During Refueling, Attachment 6, Core Verification

3-47E804-1, Flow Diagram Condensate, Rev. 45

3-47E818-1, Flow Diagram Condensate Storage and Supply, Rev. 27

3-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 19

3-47E855-1, Flow Diagram Fuel Pool Cooling System, Rev. 24

3-AOI-100-1, Reactor Scram, Scram Reports, Rev. 58

3-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and Reduction in

Power During Power Operations

3-GOI-100-1A, Unit Startup, Rev. 99

3-GOI-200-2, Primary Containment Initial Entry and Closeout, Rev. 34

3-OI-78, Fuel Pool Cooling and Cleanup System, Rev. 60

3-OI-85, Control Rod Drive System, Rev. 75

3-POI-78, Reactor Water Letdown During Refueling Outages Using Submersible Pump/Filter,

Rev. 06

3-SR-3.1.1.5(A), Control Rod Coupling Integrity Check, Att. 5, Startup Sequence, Rev. 25

3-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring

3-TI-179, CILRT Data Acquisition System Setup, Rev. 8

3-TO-2012-0003; Clearance 3-001-0009B

3-TO-2012-0003; Clearance 3-068-0023A

3-TO-2012-0003; Clearance 3-071-0010

3-TO-2012-0003; Clearance 3-075-0009

3-TO-2012-0003; Clearance 3-075-0013

Browns Ferry Nuclear U3R15 Core Verification for BOC16 dated 4/10/2012

MMDP-11, Erection of Scaffolds / Temporary Wolf Platforms and Ladders, Rev. 3

MMTP-102, Erection of Scaffolds / Temporary Work Platforms and Ladders, Revs. 2 & 7

NPG-SPP-09.17, Temporary Equipment Control, Rev. 1

OPDP-1, Conduct of Operations, Rev. 23

PER 542193, Lock High Radiation Area Key

PER 542874, Unacceptable Housekeeping Practices in U3 RWCU HX Room

PER 543083, Housekeeping Inspection of 3B Reactor Water Cleanup Pump Room

PER 547169, U3 RWCU Equipment Drain Screens

PER 547172, U3 RWCU Pump Room Equipment Drain Screen

PER 549286, 3D Diesel Generator 7-Day Tank Leaking From Inspection Port

PER 554943, Pipe Support 3-47B458-564 - Core Spray

Attachment

12

PER 555573, Unit 3 Reactor Scram

PER 556790, Design Error with U3 3A USST

Scaffold Request # 03-1453-3, RWCU HX Room

Scaffold Request # 10-239-3, RWCU HX Room

SR 556367, GOI Step Not Fully Signed Off and Dated

3-TO-2012-004, sections 3-002-0001 and 3-078-0001 for Unit 3 Alternate Reactor Water Level

Control; 3-TO-2012-0003, Section 3-001-0008, for work on Main Steam Line Drain Inboard

Isolation Valve, 1-FCV-001-055;

3-TO-2012-0003; Clearance 3-001-0009B, for maintenance on 3-FCV-1-56; Clearance 3-068-

0023A, for maintenance of Recirculation Pump 3B; Clearance 3-071-0010, for maintenance on

RCIC Barometric Condenser Condensate Pump Motor; Clearance 3-075-0009, for 3A Core

Spray Motor Replacement; and Clearance 3-075-0013, for 3C Core Spray Motor Replacement.

3-POI-200.5

0-GOI-100-3A, Refueling Operations (In-Vessel Operations), 0-GOI-100-3B, Operations in the

Spent Fuel Pool Only, and 0-GOI-100-3C, Fuel Movement Operations During Refueling.

Attachment 6, of 0-GOI-100-3C.

Section 1R22: Surveillance Testing

0-TI-360, Containment Leak Rate Programs, Rev. 33

0-TI-360, Containment Leak Rate Programs, Rev. 33

0-TI-362, Inservice Testing of Pumps and Valves, Rev. 30

0-TI-362, Inservice Testing of Pumps and Valves, Rev. 30

2-SI-4.2.E-1(B), Drywell Equipment Drain Sump Flow Integrator Calibration, Rev. 22

2-SI-4.4.A.1, Standby Liquid Control Pump Functional Test, Rev. 66

3-47E811-1, Flow Diagram Residual Heat Removal System, Rev. 65

3D EDG LAT RA Recorder Chart A Test 1 and 2 Data, dated 4/03/12

3-SR-3.6.1.1.1(OPT-A), Primary Containment Total Leak Rate - Option A, Rev. 11

3-SR-3.6.1.3.10(B), Primary Containment Local Leak Rate Test Main Steam Line B: Penetration

X-7B, Rev. 07 performed on April 29, 2012

3-SR-3.8.1.9(3D OL), Diesel Generator 3D Emergency Load Acceptance Test with Unit 3

Operating, Rev. 14

3-TI-173, Primary Containment Inspection, Rev. 10 and Rev.11

3-TI-179, CILRT Data Acquisition System Setup, Rev. 08

ANSI/ANS-56.8-1994, Containment System Leakage Testing Requirements

Design Criteria BFN-50-7082, Standby Diesel Generator, Rev. 16

DWG 2-47E852-2, Flow Diagram Clean Radwaste & Decontamination Drainage, Rev. 33

FSAR Section 10.10, Emergency Equipment Cooling Water (EECW) System, BFN-24

FSAR Section 8.5, Standby AC Power Supply and Distribution, BFN-24

Main Control Room Logs

NEDP-14, Containment Leak Rate Programs, Rev. 09

NEDP-27, Past Operability Evaluations, Rev. 0

PER 533052, 3-FCV-1-27 failed as-found LLRT

PER 549232, As Found Integrator Indication Found Out Of Tolerance Low

PER 551019, Torus site glass readings were taken while isolated during CILRT

PER 554996, Evaluate potential HPCI preconditioning

PER 568095, 2-SI-4.4.A.1 SLC TEST, Schrader valve

PER 568705, Issue During SLC Pump Functional Test

PER 569867, HIgh vibration on 2A SLC pump

Attachment

13

PER 569895, HIgh vibration on 2B SLC pump

PER 569965, 4 AUOs Not Present for Surveillance

PER 570625, BFN-2-PMP-063-0006A, 2A SLC PUMP (GE-11-2A) Flowrate high

PER 570710,U2 SLC Storage Tank Decreasing Level Trend

PER 571768, Unit 2 SLC Storage Tank decreasing level trend.

SR 531728, Failure to Check Large Load Start

SR 531819, Failure to Send AUOs Locally for Large Load Start

SR 569401, 2-DRV-063-0530 leaking by its seat. Needed excess force to seat valve

Technical Specifications and Bases 3.3.8.1, Loss of Power (LOP) Instrumentation, Amendment

215

Technical Specifications and Bases 3.7.2, Emergency Equipment Cooling Water (EECW)

System and Ultimate Heat Sink (UHS), Amendment 215

Technical Specifications and Bases 3.8.1, AC Sources - Operating, Amendment 266

U2 Bases B 3.4.5 RCS Leakage Detection Instrumentation, Rev. 0

U2 Tech Spec 3.4.5, RCS Leakage Detection Instrumentation, Amendment 253

UFSAR, 4.10 Nuclear System Leakage Rate Limits, Amendment 22

WO 112511675, As Left - 3-SI-4.7.A.2.g-3/74g - PC LLRT - RHR Shutdown Cooling Suction

WO 112816329, Drywell Equipment Drain Sump Flow Integrator Calibration

WO 113145425, 2-SI-4.4.A.1, SLC Pump Functional Test

WO 113614430, Replace the Schrader valve on the bladder for the 2A SLC Pump

WO 113620697, 2-SI-4.4.A.1, SLC Pump Functional Test

WO 113625610, 2-DRV-063-0530 leaking by its seat, Needed excess force to seat valve

Section 1EP2: Alert and Notification System Evaluation

2012 Browns Ferry Emergency Planning Calendar mailer to members of the public in the 10-

mile EPZ

Documentation of bi-weekly siren tests and maintenance for 4th quarter 2011 and 1st quarter

2012

Documentation of Quarterly siren maintenance for 4th quarter 2011 and 1st quarter 2012

EPDP-10, Facilitation of the Alert and Notification System and Notification Tests, Rev. 4

EPDP-14, Evaluation of Changes to Alert and Notification Systems (ANS), Rev. 0

EPDP-16, Designated Emergency Response Equipment (DERE), Rev. 0

EPDP-17, NPG Emergency Plan Effectiveness Review (10 CFR 50.54(q))

EPDP-8, Emergency Preparedness Quality Related Programs, Rev. 1

EPFS-9, Inspection, Service, and Maintenance of the Prompt Notification System (PNS) at

Browns Ferry, Sequoyah, and Watts Bar Nuclear Plants, Rev. 6 and 7

Federal Signal 508 Electro-Mechanical Siren Installation and Operating Instructions, Rev. 12/11

Siren Annual Maintenance records: 2011 and 1st quarter 2012

SR 572389; admin requirements not met in implementing new ANS system

Section 1EP3: Emergency Preparedness Organization Staffing and Augmentation

System

2010, 2011, 2012 quarterly drill reports

2010, 2011, 2012 Unannounced pager test results

2012 Unannounced staffing drill report

239363 OSC Status Board Writer #1 failed to respond to Weekly Pager Test

243962 Operations Representative failed to respond to Weekly Pager Test

246558 Plant Assessment Team Leader failed to respond to Weekly Pager Test

Attachment

14

246569 OSC Status Board Writer #1 failed to respond to Weekly Pager Test

248540 OSC I/C Supervisor failed to respond to Weekly Pager Test

258558 Radiation Protection Manager failed to respond to Weekly Pager Test

266020 OSC I/C Engineer failed to respond to Weekly Pager Test

294582 OSC Mechanical Engineer failed to respond to Weekly Pager Test

327650 Site Vice President failed to respond to Weekly Pager Test

328191 OSC Director failed to respond to Weekly Pager Test

362821 Confused communication on the need to send B5b blackout fire pump to BFN

408093 Assistant OSC Director failed to respond to Weekly Pager Test

423217 CECC Plant Assessment Team member preparation for actual emergencies

475726 2011 Graded Exercise Corrective Actions

541288 QA SSA1203 - EP qualifications not in Qualification Matrix

542221 SAMG Decision Maker training requirements do not exclude Shift Managers as Site

Emergency Director

569374 Simulator issues during the BFN Off Year Exercise

CECC EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 41

CECC EPIP-4, Operations Duty Specialist Procedure for Site Area Emergency, Rev. 42

Emergency Response Organization Teams listing dated 6/22/2012

EPDP-3, Emergency Plan Exercises and Preparedness Drills, Rev. 5

EPIP-6, Activation and Operation of the Technical Support Center (TSC), Rev. 34

EPIP-7, Activation and Operation of the Operations Support Center (OSC), Rev. 29

EPT500A, 2012 EP Staff Orientation Course Description

TRN 30, Radiological Emergency Preparedness Training, Rev. 19

Various EP staff and ERO member training records

Section 1EP5: Maintenance of Emergency Preparedness

10CFR50.54(q) Evaluation of TEENS augmentation hardware addition

10CFR50.54(q) Evaluation of TSC Renovation

362854; NOUE declared - Tornado

364318; Tornado event

364674; Extensive loss of ANS due to tornadoes

453700; PAR training requirement

456771; RP ERO staffing PER not closed correctly

571878; admin error on 50.54q eval of TEENS implementation

572826; EPDP-17 enhancement to add subject matter experts in 50.54q screening

95003-005, BFN NRC Column 4 Response Project and Administrative Controls - Appendix H,

Rev. 1: ERO Readiness Performance Area Report

BFN Quality Assurance - Emergency Preparedness Drill Assessment - QA-11-007 dated April

21, 2011

BFN Quality Assurance - Emergency Preparedness Equipment and Facility Readiness, QA-BF-

11-008 dated June 30, 2011

BFN Self-assessment BFN-EP-S-10-001, B5B Commitments

BFN Self-assessment BFN-EP-S-11-001, Effectiveness Reviews

Drill and exercise reports, 2010, 2011, and 2012

EPDP-1, Procedures, Maps, and Drawings, Rev. 3

EPDP-16, Designated Emergency Response Equipment (DERE), Rev. 0

EPDP-17, NPG Emergency Plan Effectiveness Review, Rev. 0

Event records of NOUE declared on 4/27/2011 - Tornado with Extended Loss of Off-site Power

Attachment

15

NPG-SPP-18.3, Emergency Preparedness, Rev. 1

REP, Radiological Emergency Plan, (Appendix A - BFN), Rev. 97

REP, Radiological Emergency Plan, (Generic Part), Rev. 97

Self-assessment CRP-EP-S-11-03, Site Tornado Procedure, BP-128, dated September 28,2011

Self-assessment CRP-EP-S-12-005; Training Program comparison

Self-assessment CRP-EP-S-12-006, REP drill

Self-assessment CRP-EP-S-12-020; EP Records

SPP-3.1, Corrective Action Program, Rev. 4

TVA Quality Assurance - Emergency Preparedness Audit Report SSA1003 dated May 20, 2010

TVA Quality Assurance - Emergency Preparedness Audit Report SSA1203 dated April 24, 2012

Section 1EP6: Drill Evaluation

Browns Ferry, Off Year Exercise Report

CECC-EPIP-1, Emergency Classification Procedure, REV. 53

EPIP-1, Emergency Classification Procedure, REV. 47

NP-REP, Radiological Emergency Plan, (Generic Part), Rev. 97

NP-REP, Radiological Emergency Plan, Appendix A, Rev. 97

PER 567663, Accountability report inaccuracy during EP drill

PER 568729, Revise EPIP-7, App. B to Indicate OSC Minimum Staffing

PER 569310, CECC ERO member failed to respond to CECC activation

PER 569374, Simulator Issues during the BFN Off Year Exercise

PER 570670, During the Unannounced Staffing Drill, TEENS System Delay

PER 571025, During EP OYE Simulator Stack Rad Simulation did not operate as expected

PER 571053, During the EP Unannounced Staffing Drill issues were observed

PER 571382, During the 2012 EP Off Year Exercise Stack Monitor Simulation was an issue

PER 572271, Focus areas found in the June 13th BFN REP OYE

Performance Indicator Data from June 2012

Section 2RS1: Radiological Hazard Assessment and Exposure Control

(Annual Inventory Of Non-Fuel SNM and Other Items (Trash) In Unit 1, 2 And 3 Spent Fuel

Pools Performed 8/10-25/2011.)

0-TI-540, Storage of Material in the spent Fuel Storage Pool (SFSP) and Transfer Canal

(U1/U2), Rev. 2

Browns Ferry Technical Specification 5.7 Administrative Controls-High Radiation Area

NPG-SPP-05.0, Radiological and Chemistry Control, Rev. 1

NPG-SPP-05.1, Radiological Controls, Rev. 2

NSTS Confirmation Form 2012 Annual Inventory Reconciliation [Browns Ferry 1 AmBe Source],

Dated 1/18/2012

NSTS Confirmation Form 2012 Annual Inventory Reconciliation [Browns Ferry 3 Cs-137

Sources], Dated 1/18/2012

PER 334211 Track and trend radworker practices in drywell U2R16

PER 334244 Radworker practices in drywell U2R16

PER 439979 RP posted area incorrectly

PER 475108 U1R9 Drywell access room improperly posted

PER 512565 worker put tie wrap in mouth in RCA

PER 512567 building scaffold in unsurveyed area

RCDP-1, Conduct of Radiological Controls, Rev. 3

RCI-1.1, Radiation Operations Program Implementation, Revision 149

Attachment

16

RCI-1.2, Radiation, Contamination and Airborne Surveys, Revision 16

RCI-17, Control of High Radiation Areas and Very High Radiation Areas, Revision 71

RCI-26, Radiation Protection Department Standards and Expectations, Revision 19

RCI-33, Diving Operations on the Refuel Floor, Rev. 9

RCI-34, Remote Monitoring, Revision 12

RCI-40.0, RP Actions for Operation's Unit 0 (Common) Procedural Hold Points, Revision 17

RCI-47, Diving Operations in the Radiologically Controlled Area, Rev. 1

RCI-9.1, Radiation Work Permits, Revision 70

RWP 1238-0001, Unit-3R15 Refueling Outage Drywell Outside Support

RWP 1238-0002, Unit-3R15 Refueling Outage Drywell Outside Support [High Rad]

RWP 1238-0003, Unit-3R15 Outage Drywell Miscellaneous System Support [Locked High Rad]

RWP 1238-0012, Unit-3R15 Outage Drywell Main Steam System Maintenance [High Rad]

RWP 1238-0033, Unit-3R15, Outage Drywell Feedwater System Maintenance [Locked High

Rad]

RWP 1238-0683, Unit-3R15, Outage, Drywell Reactor Water Recirculation System [Continuous

Coverage- Locked High Radiation Area]

RWP 1238-0693, Unit-3R15, Outage, Drywell Reactor Water Cleanup System Maintenance

[Locked High Rad]

SR 532617 Worker got separated from escort

SR 532875 Inaccurate rad tag on a box

SR 532981 Small air activity excursion on RFF during Rx disassembly

SR 534873 Coordination issues obtaining RWCU sludge sample.

SR 534880 Deterioration of padding on Knee anchors U1 593

Survey M-010612-2, Unit 3 RXB 593' RWCU BW Transfer Pump Room, 01/06/2012

Survey M-020712-13, Unit 2 RXB 519' Under Torus, 02/07/2012

Survey M-021012-10, 0-CASK-079-0100/1 (MPC SN-0237), 02/10/2012

Survey M-102411-11, Unit 2 TB 586' 2A SJAE Room, 10/24/2011

Survey M-20120306-26, ISFSI Pad, 03/06/2012

Section 2RS6: Radioactive Gases and Liquid Effluent Treatment

Procedures, Guidance Documents, and Manuals

0-ODCM-001, Offsite Dose Calculation Manual, Rev. 21

NPG-SPP-05.14, Guide for Communicating Inadvertent Radiological Spills/Leaks to Outside

Agencies, Rev. 0

NPG-SPP-05.15, Fleet Ground Water Protection Program, Rev.2

0-TI-15, Radioactive Gaseous Effluent Engineering Calculations and Measurements, Rev. 15

0-SI-4.8.A.1-1, Liquid Effluent Permit, Rev. 74

0-SI-4.8.B.1.a.2, Airborne Effluent Release Rate by Manual Sampling When a Gaseous Effluent

Monitor is Inoperable, Rev. 31

0-SI-4.8.B.2-1, Airborne Effluent Analysis - Particulate and Charcoal Filter Analysis, Rev. 37

0-SI-4.8.B.2-5, Airborne Effluent Analysis - Monthly Tritium, Rev. 30

0-SI-4.8.B.2-8, Airborne Effluent Analysis - Stack Noble Gas, Rev. 12

0-SI-4.8.B.2-4, Airborne Effluent Analysis - Monthly Gamma Isotopic, Rev. 30

CI-714, Particulate and Charcoal Filter Sampling and Analysis, Rev. 30

CI-738, Sampling Effluent Monitors (CAMS) for Tritium and Gamma Isotopics, Rev. 31

0-SI-2.1-2, Airborne Effluent Radiation Monitor Source Checks, Rev. 45

1-SIMI-90B, Radiation Monitoring System Scaling and Setpoint Documents, Rev. 41

2010 Radiological Effluent Release Report

Attachment

17

2011 Radiological Effluent Release Report

2002 Radiological Effluent Release Report - Abnormal Release Addendum

Records and Data Reviewed

Browns Ferry UFSAR Chapter 9

0-SR-3.6.4.3.2(A)-SBGTS Iodine Removal Efficiency (Train-A), 8/23/2010

0-SR-3.6.4.3.2(A)-SBGTS Iodine Removal Efficiency (Train-A), 7/13/2011

Gaseous Release Permits: 120323.030.020.G, 120315.037.020.G, 120350.030.021.G,

20328.032.020.G, 120333.043.019.G, 120340.046.020.G, 120330.040.025.G

Surveillance Task Sheet: 0-SI-4.8.B.2-1- Airborne Effluent Analysis- Particulate & Charcoal

Filter Analysis, 5/1/2012

System Health Reports, Each Unit System 66 - Off-Gas, 2/1/2011-1/31/2012

System Health Report, System 77 -Radwaste, 10/1/2011-1/31/2012

System Health Report, Each Unit System 90- Radiation Monitoring, 10/1/2011-1/31/2012

Cross-Check Analysis Data: 1st Quarter 2010 through 2nd Quarter 2011

Chemistry Focused Self Assessment Report - BFN-CEM-F-11-001, Performed 6/6-17/2011

White paper documenting Ground Water Monitoring in 2010 and 2011 with results

CAP Documents

PER 257903 2-RM-090-013D, RCW Effluent Offline Rad Monitor alarmed on Hi Rad Setpoint

PER 313929 1Q FY11 Radwaste water processing and effluents continues to be problem areas.

PER 324700 Unit 3 Station Sump tritium results from the sample obtained 1/18/2011

PER359503 Unmonitored release at the gas stack

PER 367604, Insufficient sample equipment for inop Effluent CAM monitors

PER 532416, Possible release path to Waters of the US

Section 2RS7: Radiological Environmental Monitoring Program (REMP)

Procedures and Guidance Documents

Cl-420, Collection of Radiological Environmental Monitoring Samples, Revision 03

EPFS-8, Servicing of Radiological Water Samplers, Revision 2

EPFS-12, Repair and Preventative Maintenance Procedure for Radiological

EPFS-03, Servicing of Meteorological Equipment at Environmental Data Stations, Rev 15

EPFS-07, Radio and Meteorological Tower Inspection, Rev 4

EPFS-06, Calibration of Environmental Data Station Data Logger and Sonic Channels, Rev 16

Environmental Monitoring Air Sampling System, Rev 01

EMSTD-01, Environmental Radiological Monitoring Program, R25

Records and Data Reviewed

Annual Radiological Environmental Operating Report 2010 & 2011

Field Collection Sheets for June 4, 2012 Environmental Run

EPFS-6 Data sheet 1 for Cal dates 3/21/12; 10/04/11; 04/13/11; 10/14/10; 08/24/10

EPFS-6 Data sheet 6 for dates 03/21/12; 10/31/11; 10/04/11; 04/12/11; 10/14/10

EPFS-6 Data sheet 5 for dates 03/22/12; 04/12/11; 10/04/11; 10/20/10

EPFS-6 Data sheet 4 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10

EPFS-6 Data sheet 3 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10

EPFS-6 Data sheet 2 for dates 03/21/12; 10/04/11; 04/13/11; 10/14/10

Calibration Data Sheets for REMP Air Sampler Gas meter 2010 & 2011

Attachment

18

EPFS 1 Attachment 2 Trouble Report: 10BFN538, 10BFN536, 10BFN560, 10BFN561,

10BFN557, 10BFN549, 10BFN506

QA Record L17111221800, TVA Quality Assurance- Nuclear Power Group- Fleet Comparative

Report SSA1107, 12/20/11

CAP Documents

PER 259776- The BFN REMP air filter and charcoal cartridge samples invalid

PER 366333- Loss of power to REMP air samplers

PER 411549- REMP TLDs

PER 450297- REMP sample not analyzed and not recorded in PER

PER 515446- REMP sample

Section 2RS8: Radioactive Material Processing and Transportation

Procedures, Manuals, and Guides

Energy Solutions Procedure, FO-OP-022, Ecodex Precoat/Powdex/Solka-Floc/Diatomaceous

Earth/Zeolite Dewatering Procedure for Energy Solutions14-215 or Smaller Liners, Rev. 23

Radioactive Material Shipment Manual (RMSM), Volume I, Rev. 40

Radioactive Material Shipment Manual (RMSM), Volume II, Rev. 42

Radioactive Material Shipment Manual (RMSM), Volume III, Rev. 39

RWI-001, Administration of the Radioactive Material and Radwaste Packaging and

Transportation Program, Rev 9

RWTP-102, Use of Casks, Rev. 2

RWI-111, Storage of Radioactive Waste and Materials, Rev. 18

RWI-112, Container Markings, Rev. 2

0-OI-77G, Duratek Procedure FO-OP-32, Set Up and Operating Procedure for the RDS-1000

Unit at TVA Browns Ferry, Rev. 2

0-PCP-001, Process Control Program Manual (PCP), Rev. 4

NPG-SPP-3.1, Corrective Action Program, Rev. 2 and Rev. 3

Shipping Records and Radwaste Data

Certificate of Compliance No. 9168 for the Model No. 8-120B, 5/25/12

Certificate of Compliance No. 9204 for the Model No. 10-160B, 5/25/12

Gamma Isotopic Analysis Results - ID # 20120227-29 [For survey 022712-29, trash dumpster],

2/27/12

Gamma Isotopic Analysis Results - ID # 20100607-23 [NCDM Coupon 101], 6/7/10

Gamma Isotopic Analysis Results - ID # 20100607-25 [NCDM Coupon 103], 6/7/10

Gamma Isotopic Analysis Results - ID # 20100607-27RC [NCDM Coupon 047], 6/7/10

Gamma Isotopic Analysis Results - ID # 20100607-26 [NCDM Coupon 192], 6/7/10

Letter to File, Browns Ferry Nuclear Plant - Personnel Qualified to Ship Radioactive

Material/Waste, 3/19/12

List of Radioactive Material Storage Areas [Spreadsheet]

List of Red System 077 Issues

List of Outstanding Work Orders for System 077 [Radwaste]

Liquid Radwaste System (System 077) Health Report (2/1/12 - 5/31/12), 6/19/12

Liquid Radwaste System (System 077) Health Report (10/1/2011 - 1/31/2012), 5/17/12

Project Plan, BFN Radwaste Legacy Project, Project ID: 100533, Rev. 1, 2/1/12

Qualification Matrix Report for selected individuals to verify Subpart H training

Radioactive Material Shipping logs for the period 7/10/10 to 5/17/12

Attachment

19

Radiological Survey M-20120517-23, Pre-Shipment Survey on HIC# CL40524-9

Radiological Survey M-20120620-17, Down Post, HIC transfer complete.

Radiological Survey M-20120620-19, Pre-Shipment on cask # 14-170-35

Radiological Survey M-022412-4, Other - Trash Dumpster

Radiological Survey M-022712-29, Job Coverage [Trash Dumpster]

Radiological Survey M-20120312-12, Trash Dumpster from PA

RWP12040086, Legacy Radwaste Project (LHRA), Rev. 0

Shipment 100618, Corrosion coupons in a DOT 7A container, Type A

Shipment 120401, Liquid tanker, Low Specific Activity (LSA-I)

Shipment 120455, Control Rod Drives (2 boxes), Type A

Shipment 110804, Empty 8-120A cask, Excepted package-empty

Shipment 110318, DAW (2 sealand containers), Low Specific Activity (LSA-II)

Shipment 101111, DAW (1 sealand container), Low Specific Activity (LSA-II)

Shipment 110902, Surveillance Capsule, Type A

Shipment 100326, Control Rod Drives (2 boxes), Type A

Shipment 100327, Control Rod Drives (2 boxes), Type A

Shipment 100328, Control Rod Drives (2 boxes), Type A

Shipment 120616, Dewatered Resin, Low Specific Activity (LSA-II)

10 CFR Part 61 Analyses, DAW 2012; CWPS 2012; RWCU 2010 and 2012 Preliminary;

Thermex 2010 and 2012 Preliminary,

CAP Documents

PER 513962, Non-RCA Trash dumpster alarms truck monitor

PER 520927, Non-RCA Trash dumpster alarms truck monitor

PER 409367, Equipment Sump over flowed contaminating RW 546

PER 425240, Radwaste El. 546 posted CA due to flooding from floor drains

PER 433904, RW 546 C-zone due to Equipment Sump overflow

PER 429803, Trend of flooding RW 546 elevation

PER 451830, Entire 546 elevation of the Rad waste building flooded

PER 456136, RW elevation 546 was flooded again spreading more contamination

PER 533414, 10CFR61 samples do not include a RWCU Sample

PER 441666, Intruder brakin at Low Level Radwaste yard

PER 254001, ATIS Radwaste Shipping Task tracking problem

PER 343736, Radioactive Material stored for years without disposition determination

PER 431466, Received notification that torque values were incorrect upon receipt of ISP

capsule

PER 236118, Two boxes of Used Control Rod Drives Shipped to GEH Improperly

PER 453834, Adverse Trend of flooding RW 546 elevation

Apparent Cause Evaluation Report, PER 453834, 10/28/11

PERs written by licensee during inspection activities:

SR 568025, O-OI-77E needs to be revised to correct references to procedures that are no

longer in existence.

SR 570902, PER 236118 needs to be revisited. Upon review, the corrective actions were

inadequate.

SR 571151, PER 431466 needs to be revisited. Upon review, the corrective actions were

inadequate.

Attachment

20

Section 4OA1: Performance Indicator Verification

3-47E812-1, Flow Diagram for HPCI, Rev. 64

3-OI-73, High Pressure Coolant Injection System, Rev. 52

571936; improve DEP PI advance scheduling

572831; PAR development in licensed operator training PI opportunities

BFN-50-7073, Design Criteria Document for the HPCI system, Rev. 22

CECC EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 41

Consolidated Date Entry Sheets for Units 1, 2 and 3 for the Safety System Functional Failures

(SSFF) PI

Documentation of ANS tests for 4th quarter 2011 - 1st quarter 2012

Documentation of DEP opportunities for 4th quarter 2011 - 1st quarter 2012

EPDP-11, Emergency Preparedness Performance Indicators, Rev. 3

EPIP-2, Notification of Unusual Event, Rev. 31

EPIP-3, Alert, Rev. 34

EPIP-4, Site Area Emergency, Rev. 33

LER 259/2011-006-00, Loss of Safety Function (HPCI) Due to Primary Containment Isolation.

Licensed Operator Training Scenarios 04, 17, 06, 18, 30, and 05 from 4th quarter 2011

Maintenance Rule Function Failure Report from April 1, 2011 to March 31, 2012

NPG-SPP-02.2, Performance Indicator Program, Rev. 3

NPG-SPP-03.4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting

10 CFR 50.65, Rev. 01

PER 439338 RP tech posted an area incorrectly

PER 533834 Contractor receives uptake during hydrolaze activities

PER 534086 Laborer contaminated while working in an area near where CRD header was

being hydrolased.

RCI-39, Radiation Protection Cornerstones, Rev. 9

SR 532755, Dosimetry alarms due to being run through x-ray machine

Section 4OA2: Identification and Resolution of Problems

0-47E820-1, Flow Diagram Control Rod Drive Hydraulic System, Rev. 32

0-OI-2B, Condensate Storage and Transfer System, Rev. 76

1-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 04

2-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 14

3-47E804-1, Flow Diagram Condensate, Rev. 45

3-47E818-1, Flow Diagram Condensate Storage and Supply System, Rev. 27

3-47E820-2, Flow Diagram Control Rod Drive Hydraulic System, Rev. 19

3-47E855-1, Flow Diagram Fuel Pool Cooling System, Rev. 24

3-GOI-100-3A, Refueling Operations (RX Vessel Disassembly and Floodup), Rev. 53

3-OI-78, Fuel Pool Cooling and Cleanup System, Rev. 60

3-OI-85, Control Rod Drive System, Rev. 75

3-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Rev. 11

3-POI-78, Reactor Water Letdown During Refueling Outages Using Submersible Pump/Filter,

Rev. 06

Engineering trend report data from January 1, 2011 to December 1, 2011

Integrated Trend Report, Q1FY12, October 1 December 31, 2012

Integrated Trend Report, Q2FY12, January 1 March 31, 2011

PE-P4461A, Recirculation System Suction Plug Installation/Removal Procedure for Browns

Ferry Nuclear Station under Project PE 00-829/1299 & 09-1614, Rev. 4

Attachment

21

PE-P4462A, Jet Pump Plug Procedure for Browns Ferry Nuclear Station under Project PE 00-

829, Rev. 0

PE-P4850, Operating and Maintenance Instructions for the Main Steam Line Plugs and

Installation/Removal Tools for Browns Ferry Station - Project PE 998, Rev. 2

PER 471366, CAP gaps to excellence plan

PER 491985, Human Performance gaps to excellence plan

PER 512589, Cross-functional issue on outage-related worker practices

PER 539854, Engineering has documented several inappropriate action closures

PER 563559, QA identified trend on BFN Fire Operations Training

RPT-CAP011, Gognos PER Word Search report from Jan 1, 2012 to June 29, 2012

Section 4OA3: Event Follow-up

0-TI-230V, Vibration Program, Rev. 10

0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -

10CFR50.65, Rev. 38

1-SR-3.3.8.2.1(A), RPS Circuit Protector Calibration/Functional Test For 1A1 and 1A2, Rev. 6

3-AOI-100-1, Reactor Scram, Rev. 58

Browns Ferry - Emergency Diesel Generator System Vulnerability to Functional Failure

Assessment, dated May 7, 2009

Design Criteria BFN-50-7082, Standby Diesel Generator, Rev. 16

Drawing 1-45E641-3, Instr & Controls Power Sys Schematic Diagram SH-3, Rev. 5

Drawing, 0104D3695-1, Isolated Phase Bus Return Air Duct, dated 1/20/12

Electro-Motive Vibration Guidelines Industrial Power Units, letter dated October 29, 1982

EMD Power Systems Owners Group Meeting, Diesel Generator Vibration Acceptable Criteria,

dated June 26-28, 1991

FSAR Section 11, Power Conversion Systems, BFN-24

FSAR Section 8.4, Normal Auxiliary Power System, BFN-24

FSAR Section 8.5, Standby AC Power Supply and Distribution, BFN-24

Main Control Room Logs

NPG-SPP-06.2, Preventive Maintenance, Rev.0

NPG-SPP-06.2, Preventive Maintenance, Rev.04

NPG-SPP-09.18, Integrated Equipment Reliability Program, Rev. 02

NPG-SPP-09.18.1, System Vulnerability Review Process (MCIP Reviews), Rev. 4

NPG-SPP-09.18.2, Equipment Reliability Classification, Rev. 0

NPG-SPP-09.18.2, Equipment Reliability Classification, Rev. 01

NPG-SPP-2.3, Operating Experience Program, Rev. 3

OE25284 - Emergency Diesel Generator Governor Drive Oil Supply Line Sheared, North Anna

1 and 2

Operations Standing Order 174, Rev. 1, To establish Operations Department expectation when

as-found data is outside of acceptable regulatory or programmatic requirements

PER 131365, Out of Tolerance Time Delay Relay

PER 151812, RPS Circuit Protector Failed Acceptance Criteria

PER 178286, Acceptance Criteria Failed

PER 248513, Failed Acceptance Criteria Step 7.2 (28)

PER 362395, Oil Leak Resulting in Emergency Shutdown of C DG

PER 391479, Classification of System 55 Power Supplies

PER 413140, 1A1 RPS Circuit Protector Undervoltage Trips

PER 438808, Unknown Object Found in U3 Phase Bus Duct

Attachment

22

PER 440359, U3 Scrammed on September 28, 2011 at 0414

PER 442914, Evaluation of Surveillance Data from Past Performances

PER 486780, 3C1 Relay Results Below Acceptance Criteria

PER 496592, Fire in Annunciator Panel 3-XA-55-5A

SPP-3.9, Operating Experience Program, Revs. 4 and 5

SPP-6.2, Preventive Maintenance, Rev.09

SPP-9.18.2, Equipment Reliability Classification, Rev. 00

SR 496007, U-3 Annunciator Panel 9-5A Fire and AOI entry

Technical Specification and Bases 3.3.8.2, Reactor Protection System (RPS) Electric Power

Monitoring, Amendment 263 and Rev. 43, respectively

Technical Specifications and Bases 3.8, Electrical Power System, Amendment 266

Technical Specifications and Bases Section 3.8, Electrical Power Systems, Amendment 280

and Rev. 52 respectively

TVA-NQA-PLN89-A, Nuclear Quality Assurance Plan (NQAP), Rev. 23, 24, 25 and 26

Attachment

LIST OF ACRONYMS

ADAMS - Agencywide Document Access and Management System

ADS - Automatic Depressurization System

ALARA As Low As Reasonably Achievable

ARM - area radiation monitor

CAD - containment air dilution

CAP - corrective action program

CCW - condenser circulating water

CFR - Code of Federal Regulations

CoC - certificate of compliance

CRD - control rod drive

CS - core spray

DAC Derived Air Concentration

DCN - design change notice

ED Electronic Dosimeter

EDG - emergency diesel generator

EECW - emergency equipment cooling water

FE - functional evaluation

FPR - Fire Protection Report

FSAR - Final Safety Analysis Report

HP Health Physics

HRA High Radiation Area

IMC - Inspection Manual Chapter

JOG Joint Owners Group

LER - licensee event report

LHRA Locked High Radiation Area

NCV - non-cited violation

NRC - U.S. Nuclear Regulatory Commission

NSTS National Source Tracking System

OA Other Activity

ODCM - Off-Site Dose Calculation Manual

PER - problem evaluation report

PCIV - primary containment isolation valve

PI - performance indicator

RCE - Root Cause Evaluation

RCW - Raw Cooling Water

RG - Regulatory Guide

RHR - residual heat removal

RHRSW - residual heat removal service water

RS Radiation Safety

RTP - rated thermal power

RPS - reactor protection system

RWP - radiation work permit

SDP - significance determination process

SBGT - standby gas treatment

SLC - standby liquid control

SNM - special nuclear material

Attachment

24

SRV - safety relief valve

SSC - structure, system, or component

TI - Temporary Instruction

TIP - transverse in-core probe

TLD Thermoluminescent Dosimeter

TRM - Technical Requirements Manual

TS - Technical Specification(s)

U1 Unit 1

U2 Unit 2

U3 Unit 3

UFSAR - Updated Final Safety Analysis Report

URI - unresolved item

VHRA Very High Radiation Area

WO - work order

Attachment