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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257
{{#Wiki_filter:UNITED STATES
    November 7, 2012  
                                        NUCLEAR REGULATORY COMMISSION
                                                      REGION II
Mr. Michael J. Annacone Vice President  
                                    245 PEACHTREE CENTER AVENUE NE, SUITE 1200
Brunswick Steam Electric Plant P.O. Box 10429 Southport, NC 28461-0429  
                                              ATLANTA, GEORGIA 30303-1257
SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2012004 AND 05000324/2012004  
                                          November 7, 2012
Dear Mr. Annacone:  
Mr. Michael J. Annacone
Vice President
On September 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an  
Brunswick Steam Electric Plant
inspection at your Brunswick Unit 1 and 2 facilities. The enclosed integrated inspection report  
P.O. Box 10429
documents the inspection findings, which were discussed on October 11, 2012, with you and other members of your staff.  
Southport, NC 28461-0429
SUBJECT:       BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.  
                REPORT NOS.: 05000325/2012004 AND 05000324/2012004
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
Dear Mr. Annacone:
personnel.  
On September 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an
One NRC-identified and one self-revealing finding of very low safety significance (Green) were  
inspection at your Brunswick Unit 1 and 2 facilities. The enclosed integrated inspection report
documents the inspection findings, which were discussed on October 11, 2012, with you and
other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
One NRC-identified and one self-revealing finding of very low safety significance (Green) were
identified during this inspection. These findings were determined to involve a violation of NRC
requirements. Further, two licensee-identified violations were determined to be of very low
safety significance and are listed in this report. The NRC is treating these findings as non-cited
violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violations or the significance of these NCVs, you should provide a response
within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear
Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with
copies to the Regional Administrator Region II; the Director, Office of Enforcement, United
States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident
Inspector at the Brunswick Steam Electric Plant.
If you disagree with the cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
Brunswick Steam Electric Plant.


identified during this inspection.
M. Annacone                                    2
  These findings were determ
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
ined to involve a violation of NRC requirements.  Further, two licensee-identified violations were determined to be of very low
enclosure, and your response (if any) will be available electronically for public inspection in the
safety significance and are listed in this report.  The NRC is treating these findings as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.  
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
If you contest the violations or the significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident
                                            Sincerely,
Inspector at the Brunswick Steam Electric Plant.
                                            /RA/
                                            Randall A. Musser, Chief
                                            Reactor Projects Branch 4
                                            Division of Reactor Projects
Docket Nos.: 50-325, 50-324
License Nos.: DPR-71, DPR-62
Enclosure:    Inspection Report 05000325, 324/2012004
              w/Attachment: Supplemental Information
cc w/encl:    (See page 3)


If you disagree with the cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
Brunswick Steam Electric Plant.
M. Annacone 2
  In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice", a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRC's document system (ADAMS).  ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,  /RA/  Randall A. Musser, Chief Reactor Projects Branch 4


Division of Reactor Projects
ML12312A082_________________                x SUNSI REVIEW COMPLETE x FORM 665 ATTACHED
   
  OFFICE            RII:DRP        RII:DRP      RII:DRP          RII:DRP          RII:DRP          RII:DRP        RII:DRP
Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62
SIGNATURE        JSD: /RA/      RAM RA for    Via e-mail      Via e-mail      Via e-mail      Via e-mail      JGW: /RA/
   
                                  MPS
Enclosure: Inspection Report 05000325, 324/2012004
NAME              JDodson        MCatts        MSchwieg        PNiebaum        LLake            MEndress        JWorosilo
   w/Attachment:  Supplemental Information
DATE                10/24/2012      11/07/2012    10/24/2012      10/29/2012      10/26/2012      10/25/2012      10/15/2012
E-MAIL COPY?        YES    NO    YES      NO  YES      NO      YES      NO    YES      NO    YES      NO    YES      NO
OFFICE            RII:DRP        RII:DRS
SIGNATURE        RAM: /RA/      Via e-mail
NAME              RMusser        MSpeck
DATE                  11/7/2012      11/06/2012
  E-MAIL COPY?        YES    NO    YES      NO
       
M. Annacone                          3
cc w/encl:                             Lee Grzeck
Plant General Manager                  Regulatory Affairs Manager
Brunswick Steam Electric Plant        Brunswick Steam Electric Plant
Progress Energy                        Progress Energy Carolinas, Inc.
Electronic Mail Distribution          Electronic Mail Distribution
Edward L. Wills, Jr.                  Randy C. Ivey
Director Site Operations              Manager, Nuclear Oversight
Brunswick Steam Electric Plant        Brunswick Steam Electric Plant
Electronic Mail Distribution          Progress Energy Carolinas, Inc.
                                      Electronic Mail Distribution
J. W. (Bill) Pitesa
Senior Vice President                  Paul E. Dubrouillet
Nuclear Operations                    Manager, Training
Duke Energy Corporation                Brunswick Steam Electric Plant
Electronic Mail Distribution          Electronic Mail Distribution
John A. Krakuszeski                    Joseph W. Donahue
Plant Manager                          Vice President
Brunswick Steam Electric Plant        Nuclear Oversight
Electronic Mail Distribution          Progress Energy
                                      Electronic Mail Distribution
Lara S. Nichols
Deputy General Counsel                Senior Resident Inspector
Duke Energy Corporation                U.S. Nuclear Regulatory Commission
Electronic Mail Distribution          Brunswick Steam Electric Plant
                                      U.S. NRC
M. Christopher Nolan                  8470 River Road, SE
Director - Regulatory Affairs          Southport, NC 28461
General Office
Duke Energy Corporation                John H. O'Neill, Jr.
Electronic Mail Distribution          Shaw, Pittman, Potts & Trowbridge
                                      2300 N. Street, NW
Michael J. Annacone                    Washington, DC 20037-1128
Vice President
Brunswick Steam Electric Plant        Peggy Force
Electronic Mail Distribution          Assistant Attorney General
                                      State of North Carolina
Annette H. Pope                        P.O. Box 629
Manager-Organizational Effectiveness   Raleigh, NC 27602
Brunswick Steam Electric Plant
Electronic Mail Distribution          (cc w/encl - continued)


  cc w/encl: (See page 3)
M. Annacone                              4
cc w/encl contd:
Chairman
North Carolina Utilities Commission
Electronic Mail Distribution
Robert P. Gruber
Executive Director
Public Staff - NCUC
4326 Mail Service Center
Raleigh, NC 27699-4326
Anthony Marzano
Director
Brunswick County Emergency Services
Electronic Mail Distribution
Public Service Commission
State of South Carolina
P.O. Box 11649
Columbia, SC 29211
W. Lee Cox, III
Section Chief
Radiation Protection Section
N.C. Department of Environmental Commerce & Natural Resources
Electronic Mail Distribution
Warren Lee
Emergency Management Director
New Hanover County
Department of Emergency Management
230 Government Center Drive
Suite 115
Wilmington, NC 28403


ML12312A082_________________  x SUNSI REVIEW COMPLETE x FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP SIGNATURE JSD: /RA/ RAM RA for
M. Annacone                                  5
MPS Via e-mail Via e-mail Via e-mail Via e-mail JGW: /RA/ NAME JDodson MCatts MSchwieg PNiebaum LLake MEndress JWorosilo DATE 10/24/2012 11/07/2012 10/24/2012 10/29/2012 10/26/2012 10/25/2012 10/15/2012 E-MAIL COPY?    YES NO      YES NO      YES NO      YES NO      YES NO      YES NO      YES NO    OFFICE RII:DRP RII:DRS SIGNATURE RAM: /RA/ Via e-mail NAME RMusser MSpeck DATE 11/7/2012 11/06/2012 E-MAIL COPY?    YES NO      YES NO     
Letter to Michael J. Annacone from Randall A. Musser dated November 7, 2012
M. Annacone 3
SUBJECT:       BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION
  cc w/encl:
                REPORT NOS.: 05000325/2012004 AND 05000324/2012004
Distribution w/encl:
J. Baptist, RII EICS
L. Douglas, RII EICS
OE Mail (email address if applicable)
RIDSNRRDIRS
PUBLIC
R. Pascarelli, NRR ((Regulatory Conferences Only))
RidsNrrPMBrunswick Resource


Plant General Manager
              U. S. NUCLEAR REGULATORY COMMISSION
Brunswick Steam Electric Plant  
                                  REGION II
Docket Nos.:  50-325, 50-324
License Nos.: DPR-71, DPR-62
Report Nos.:  05000325/2012004, 05000324/2012004
Licensee:    Carolina Power and Light (CP&L)
Facility:    Brunswick Steam Electric Plant, Units 1 & 2
Location:    8470 River Road, SE
              Southport, NC 28461
Dates:        July 1, 2012 through September 30, 2012
Inspectors:  M. Catts, Senior Resident Inspector
              M. Schwieg, Resident Inspector
              P. Niebaum, Acting Senior Resident Inspector
              J. Dodson, Senior Project Engineer (1R04, 1R05, 4OA2)
              L. Lake, Senior Reactor Inspector (4OA5)
              M. Endress, Reactor Inspector (1R07)
Approved by:  Randall A. Musser, Chief
              Reactor Projects Branch 4
              Division of Reactor Projects
                                                                    Enclosure


Progress Energy
                                    SUMMARY OF FINDINGS
Electronic Mail Distribution
IR 05000325/2012004, 05000324/2012004; 07/01/12 - 09/30/12; Brunswick Steam Electric
Edward L. Wills, Jr.  
Plant, Units 1 & 2; Refueling and Other Outage Activities, Identification and Resolution of
Problems
This report covers a three-month period of inspection by resident inspectors and announced
baseline inspections by regional inspectors. Two Green findings were identified by the
inspectors. The significance of most findings is indicated by their color (Green, White, Yellow,
Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process
(SDP). The cross-cutting aspects were determined using IMC 0310, Components Within the
Cross-Cutting Areas. Findings for which the SDP does not apply may be Green or be assigned
a severity level after NRC management review.
A.      NRC-Identified and Self-Revealing Findings
        Cornerstone: Barrier Integrity
        Green: The inspectors identified a Green non-cited violation (NCV) of TS 3.6.4.1,
        Secondary Containment because the licensee did not maintain secondary containment
        operable as required during a maintenance activity considered an operation with a
        potential for draining the reactor vessel (OPDRV). Once questioned by the inspectors,
        the licensee restored secondary containment, developed an Operation standing
        instruction (12-052) to treat the activity as an OPDRV and placed this issue into its
        corrective action program (CAP) as AR 562188.
        The failure to maintain secondary containment operable while Unit 1 was in Mode 4 with
        an OPDRV in progress was a performance deficiency. The finding was more than minor
        because it was associated with the configuration control attribute of the Barrier Integrity
        Cornerstone, and adversely affected the cornerstone objective to provide reasonable
        assurance that physical design barriers (fuel cladding, reactor coolant system, and
        containment) protect the public from radionuclide releases caused by accidents or
        events because the Unit 1 secondary containment boundary was not preserved or
        maintained. The inspectors evaluated the finding using Inspection Manual Chapter
        (IMC) 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,
        which required an analysis using IMC 0609 Appendix G since the reactor was in Mode 4
        (cold shutdown). The finding was determined to be of very low safety significance
        (Green) according to IMC 0609 Appendix G, Attachment 1, Checklist 6, since a
        quantitative assessment (Phase 2 or Phase 3 evaluation) was not required. Specifically,
        the inspectors determined that the licensee maintained adequate mitigation capability for
        reactor vessel water level inventory and an event did not occur that could be
        characterized as a loss of control. The cause of this finding was directly related to the
        cross-cutting aspect of Accurate Procedures in the Resources component of the Human
        Performance area, because the licensee did not consider the recirculation pump seal
        replacement activity to be OPDRV based on procedural guidance that contains
        exclusions to what are considered OPDRV activities. [H.2(c)] (Section 1R20)


Director Site Operations
                                              3
Brunswick Steam Electric Plant  
  Cornerstone: Emergency Preparedness
Electronic Mail Distribution
  Green: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the
J. W. (Bill) Pitesa
  licensees failure to properly evaluate or consider the impact to emergency response
Senior Vice President
  facilities of design change ESR98-00436 which was implemented in 1999. This resulted
  in the loss of Emergency Response Facility Information System (ERFIS), Emergency
  Response Data System (ERDS), Safety Parameter Display System (SPDS), and all
  displays including radiation monitors for the emergency response facilities. Specifically,
  the licensee failed to ensure that adequate emergency response facilities and equipment
  were available as required by the Brunswick Nuclear Plant Radiological Emergency
  Plan, Section 1.3.1.3 revision 80 and 10 CFR 50.47(b)(8). This issue was captured in the
  licensees CAP as AR 542704.
  The licensees failure to properly evaluate or consider the impact to emergency
  response facilities of design change ESR98-00436 which was implemented in 1999 was
  a performance deficiency. Specifically, the licensee introduced a single point failure
  mode which did not meet the design requirements specified in their Design Basis
  Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees failure
  to ensure that adequate emergency response facilities and equipment were available as
  delineated in the Updated Final Safety Analysis Report (UFSAR) Section 7.7.1.9, and
  required by the Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3,
  revision 80, and 10 CFR 50.47(b)(8). The finding was more than minor because it
  adversely affected the Emergency Preparedness Cornerstone objective of ensuring that
  the licensee was capable of implementing adequate measures to protect the health and
  safety of the public in the event of a radiological emergency. Specifically, the Facilities
  and Equipment attribute was affected during the time when the ERFIS, ERDS, SPDS,
  and all displays including radiation monitors for the emergency response facilities were
  degraded, and as a result did not meet 10 CFR 50.47(b)(8) Planning Standard program
  element, adequate emergency facilities and equipment to support the emergency
  response are provided and maintained. The finding was assessed for significance in
  accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance
  Determination Process. Attachment 2 of Appendix B, Failure to Comply Significance
  Logic is as follows: Failure to comply; Loss of Risk Significant Planning Standard
  Function (RSPS), No; RSPS Degraded Function, No; Loss of Planning Standard
  Function, No; the result is a Green finding. The inspectors determined that this resulted
  in a very low safety significance finding (Green). No cross-cutting aspect was assigned
  to this finding because the performance deficiency occurred more than three years ago
  and is not reflective of current plant performance. (Section 4OA2.2)
B. Licensee-Identified Violations
  Violations of very low safety significance that were identified by the licensee have been
  reviewed by inspectors. Corrective actions taken or planned by the licensee have been
  entered into the licensees CAP. These violations and corrective action tracking
  numbers are listed in Section 4OA7 of this report.


Nuclear Operations
                                        REPORT DETAILS
Duke Energy Corporation
Summary of Plant Status
Electronic Mail Distribution
Unit 1 began the inspection period at rated thermal power (RTP), and operated at or near full
John A. Krakuszeski
power until July 22, 2012 when reactor power was lowered to 52 percent to clear a fouled
circulating water debris filter and power was returned to RTP on July 23, 2012. On August 3,
2012, power was reduced to 70 percent for a rod sequence exchange and power was returned
to RTP on August 5, 2012. On August 5, 2012, power was reduced to 90 percent for control rod
improvement and power was returned to RTP on the same day. On August 8, 2012, power was
reduced to 65 percent for offsite transmission line work and power was returned to RTP on the
same day. On September 16, 2012, the reactor was shut down for forced outage to replace the
1A and 1B recirculation pump seal assemblies. Reactor startup commenced on September 27,
2012 and the main generator was synchronized to the grid on September 28, 2012. Reactor
power was raised to RTP on September 29, 2012. On September 30, 2012 reactor power was
reduced to 75 percent for a scheduled control rod improvement. Power ascension continued to
RTP for the remainder of the inspection period.
Unit 2 began the inspection period at RTP, and operated at or near full power until August 18,
2012, when power was reduced to 70 percent for a rod sequence exchange and power was
returned to RTP on August 19, 2012. On August 20, 2012, power was reduced to 86 percent
for control rod improvement and power was returned to RTP on August 21, 2012. On August
21, 2012, power was reduced to 94 percent for control rod improvement and power was
returned to RTP on August 21, 2012. On September 29, 2012, reactor power was reduced to
94 percent to support a scheduled rod improvement and returned to RTP later that day and
maintained RTP for the remainder of the inspection period.
1.      REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01 - 1 sample)
        External Flooding
  a.    Inspection Scope
        The inspectors evaluated the design, material condition, and procedures for coping with
        the design basis probable maximum flood. The inspectors reviewed the Updated Final
        Safety Analysis Report (UFSAR), which depicted the design flood levels and protection
        areas containing safety-related equipment, to identify areas that may be affected by
        external flooding. The inspectors conducted a site walk-down of the service water
        building, to ensure that erected flood protection measures were in accordance with
        design specifications. The inspectors reviewed the sealing of equipment below the flood
        line, adequacy of watertight doors, drain systems and sumps including check valves,
        and maintenance and calibration of flood protection equipment. The inspectors also
        reviewed operating procedures for mitigating external flooding during severe weather to


Plant Manager
                                                5
Brunswick Steam Electric Plant 
      determine if the licensee planned or established adequate measures to protect against
Electronic Mail Distribution
      external flooding events.
Lara S. Nichols
  b. Findings
Deputy General Counsel
      No findings were identified.
Duke Energy Corporation
1R04 Equipment Alignment
Electronic Mail Distribution
.1    Quarterly Partial System Walk-downs (71111.04Q - 3 samples)
M. Christopher Nolan
  a. Inspection Scope
      The inspectors performed partial system walk-downs of the following risk-significant
      systems:
      *    Unit 2 A train Core Spray (CS) system while B residual heat removal/service
          (RHR/SW) was inoperable for a system outage on July 11, 2012;
      *    Unit 1 Reactor Building Closed Cooling Water (RBCCW) on July 27, 2012; and
      *    Unit 1 B Standby Gas Treatment (SBGT) while the A SBGT was inoperable for a
          maintenance outage on September 19, 2012.
      The inspectors selected these systems based on their risk-significance relative to the
      reactor safety cornerstones at the time they were inspected. The inspectors attempted
      to identify any discrepancies that could impact the function of the system, and, therefore,
      potentially increase risk. The inspectors reviewed applicable operating procedures,
      system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work
      orders, condition reports, and the impact of ongoing work activities on redundant trains
      of equipment in order to identify conditions that could have rendered the systems
      incapable of performing their intended functions. The inspectors also walked down
      accessible portions of the systems to verify that system components and support
      equipment were aligned correctly and were operable. The inspectors examined the
      material condition of the components and observed operating parameters of equipment
      to verify that there were no obvious deficiencies. The inspectors also verified that the
      licensee had properly identified and resolved equipment alignment problems that could
      cause initiating events or impact the capability of mitigating systems or barriers and
      entered them into the CAP with the appropriate significance characterization.
  b. Findings
      No findings were identified.
.2    Semi-Annual Complete System Walk-down (71111.04S - 1 sample)
  a. Inspection Scope
      On September 5, 2012 the inspectors performed a complete system alignment
      inspection of the Unit 1 RHR system to verify the functional capability of the system.
      This system was selected because it was considered both safety-significant and risk-


Director - Regulatory Affairs
                                                6
    significant in the licensees probabilistic risk assessment. The inspectors walked down
    the system to review mechanical and electrical equipment line-ups, electrical power
    availability, system pressure and temperature indications, as appropriate, component
    labeling, component lubrication, component and equipment cooling, hangers and
    supports, operability of support systems, and to ensure that ancillary equipment or
    debris did not interfere with equipment operation. A review of a sample of past and
    outstanding work orders (WOs) was performed to determine whether any deficiencies
    significantly affected the system function. In addition, the inspectors reviewed the CAP
    to ensure that system equipment alignment problems were being identified and
    appropriately resolved.
b.  Findings
    No findings were identified.
1R05 Fire Protection (71111.05Q - 5 samples)
    Quarterly Resident Inspector Tours
a.  Inspection Scope
    The inspectors conducted fire protection walk-downs which were focused on availability,
    accessibility, and the condition of firefighting equipment in the following risk-significant
    plant areas:
    *    Unit 1 and 2 Control Buildings 23' Elevation 1PFP-CB-7;
    *    Unit 1 Reactor Building East 50 Elevation 1PFP-RB1-1h;
    *    Unit 1 Turbine Building South Area 38 Elevation 1PFP-TB1-1k;
    *    Unit 2 Reactor Building 50 Elevation 2PFP-RB2-1h; and
    *    Unit 2 Reactor Building North 2A Core Spray Room 2-PFP-RB2-1b.
    The inspectors reviewed areas to assess if the licensee had implemented a fire
    protection program that adequately controlled combustibles and ignition sources within
    the plant, effectively maintained fire detection and suppression capability, maintained
    passive fire protection features in good material condition, and had implemented
    adequate compensatory measures for out-of-service, degraded or inoperable fire
    protection equipment, systems, or features in accordance with the licensees fire plan.
    The inspectors selected fire areas based on their overall contribution to internal fire risk
    as documented in the plants Individual Plant Examination of External Events with later
    additional insights, their potential to impact equipment which could initiate or mitigate a
    plant transient, or their impact on the plants ability to respond to a security event. Using
    the documents listed in the attachment, the inspectors verified that fire hoses and
    extinguishers were in their designated locations and available for immediate use; that
    fire detectors and sprinklers were unobstructed, that transient material loading was
    within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
    be in satisfactory condition. The inspectors also verified that minor issues identified
    during the inspection were entered into the licensees CAP.


General Office
                                                7
Duke Energy Corporation
b.  Findings
Electronic Mail Distribution
    No findings were identified.
  Michael J. Annacone
1R06 Flood Protection Measures (71111.06 - 1 sample)
Vice President
    Annual Review of Cables Located in Underground Bunkers/Manholes
Brunswick Steam Electric Plant
  a.  Inspection Scope
Electronic Mail Distribution
    The inspectors conducted an inspection of underground bunkers/manholes subject to
  Annette H. Pope
    flooding that contain cables whose failure could disable risk-significant equipment. The
Manager-Organizational Effectiveness
    inspectors performed walk-downs of risk-significant areas, including manhole 2-MH-
Brunswick Steam Electric Plant  
    7SW, to verify that the cables were not submerged in water, that cables and/or splices
Electronic Mail Distribution
    appear intact and to observe the condition of cable support structures. When applicable,
Lee Grzeck
    the inspectors verified proper dewatering device (sump pump) operation and verified
    level alarm circuits are set appropriately to ensure that the cables will not be submerged.
    Where dewatering devices were not installed; the inspectors ensured that drainage was
    provided and was functioning properly.
b.  Findings
    No findings were identified.
1R07 Heat Sink Performance (71111.07T - 3 samples)
    Triennial Review of Heat Sink Performance
  a. Inspection Scope
    The inspectors selected the Residual Heat Removal (RHR) Heat Exchanger 2A, Diesel
    Generator (DG) 3 Jacket Water Cooler and the Core Spray (CS) Room Cooler 1A,
    based on their risk-significance in the licensees probabilistic safety analysis and their
    importance to safety-related mitigating system support functions in the NRCs model for
    Brunswick Nuclear Power Plant, Units 1 and 2.
    For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler
    1A, the inspectors reviewed the licensees inspection, maintenance, and monitoring of
    biotic fouling and macro-fouling programs, to determine if they were adequate to ensure
    proper heat transfer. This was accomplished by determining whether the methods used
    were consistent with accepted industry practices. The inspectors also reviewed the
    licensees inspection and cleaning activities had established acceptance criteria
    consistent with industry standards, and the as-found results were recorded, evaluated,
    and appropriately dispositioned to maintain structural integrity.
    For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler
    1A, the inspectors reviewed the methods and results of heat exchanger performance
    inspections. In addition, the inspectors reviewed the condition and operation of the RHR
    Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler 1A to


Regulatory Affairs Manager
                                              8
Brunswick Steam Electric Plant
  determine if they were consistent with design assumptions in heat transfer calculations
Progress Energy Carolinas, Inc.  
  and as described in the USFAR. This included determining whether the number of
Electronic Mail Distribution
  plugged tubes was within pre-established limits based on capacity and heat transfer
Randy C. Ivey
  assumptions. The inspectors also determined whether the licensee evaluated the
Manager, Nuclear Oversight
  potential for water hammer and established adequate controls and operational limits to
Brunswick Steam Electric Plant
  prevent heat exchanger degradation due to excessive flow-induced vibration during
Progress Energy Carolinas, Inc. Electronic Mail Distribution
  operation.
  The inspectors determined whether the performance of the ultimate heat sink (UHS)-
Paul E. Dubrouillet
  Cape Fear River and its subcomponents such as piping, intake screens, pumps, valves,
Manager, Training
  etc. was appropriately evaluated by tests or other equivalent methods to ensure
Brunswick Steam Electric Plant
  availability and accessibility to the in-plant cooling water systems. The inspectors also
Electronic Mail Distribution
  reviewed design changes to the service water system and the UHS.
Joseph W. Donahue
  The inspectors reviewed the licensees operation of the service water system and UHS.
Vice President
  This included a review of licensees procedures for a loss of the service water system or
Nuclear Oversight
  UHS and the verification that instrumentation, which is relied upon for decision-making,
  was available and functional. The inspectors also performed a system walk-down on the
  service water system to determine whether the licensees assessment on structural
  integrity was adequate and interviewed the respective system engineer. For buried or
  inaccessible piping, the inspectors reviewed the licensees pipe testing, inspection, and
  monitoring program to determine whether structural integrity was ensured and that any
  leakage or degradation was appropriately identified and dispositioned by the licensee.
  The inspectors performed a system walk-down of the service water intake structure to
  determine whether the licensees assessment on structural integrity and component
  functionality was adequate. The inspectors also determined whether service water
  pump bay silt accumulation was monitored, trended, and maintained at an acceptable
  level by the licensee, and that water level instruments were functional and routinely
  monitored. The inspectors also determined whether the licensees ability to ensure
  functionality during adverse weather conditions was adequate.
  The inspectors reviewed condition reports related to the heat exchangers and heat sink
  performance issues to determine whether the licensee had an appropriate threshold for
  identifying issues and to evaluate the effectiveness of the corrective actions. Records
  were also reviewed to verify that the licensee actions were consistent with Generic Letter
  (GL) 89-13 licensee commitments, Electric Power Research Institute (EPRI) and other
  industry guidelines. These inspection activities constituted three heat sink inspection
  samples as defined in IP 71111.07-05.
b. Findings
  No findings were identified.


Progress Energy Electronic Mail Distribution
                                                  9
1R11 Licensed Operator Requalification Program (71111.11Q - 2 samples)
Senior Resident Inspector
.1    Quarterly Review of Licensed Operator Requalification Testing and Training
U.S. Nuclear Regulatory Commission
  a. Inspection Scope
Brunswick Steam Electric Plant U.S. NRC 8470 River Road, SE
      On August 13, 2012, the inspectors observed a crew of licensed operators in the plants
 
      simulator during licensed operator requalification examinations to verify that operator
Southport, NC  28461
      performance was adequate, evaluators were identifying and documenting crew
 
      performance problems, and to ensure that training was being conducted in accordance
      with licensee procedures. The inspectors evaluated the following areas:
John H. O'Neill, Jr.
      *   licensed operator performance;
 
      *  crews clarity and formality of communications;
Shaw, Pittman, Potts & Trowbridge
      *  ability to take timely actions in the conservative direction;
2300 N. Street, NW Washington, DC   20037-1128
      *  prioritization, interpretation, and verification of annunciator alarms;
 
      *  correct use and implementation of abnormal and emergency procedures;
      *  control board manipulations;
Peggy Force
      *   oversight and direction from supervisors; and
Assistant Attorney General
      *  ability to identify and implement appropriate TS actions and Emergency Plan actions
State of North Carolina P.O. Box 629
          and notifications.
 
      The crews performance in these areas was compared to pre-established operator action
Raleigh, NC   27602
      expectations and successful critical task completion requirements.
 
   b. Findings
      No findings were identified.
(cc w/encl - continued)
.2    Quarterly Review of Licensed Operator Performance in the Main Control Room
M. Annacone 4
  a. Inspection Scope
   cc w/encl cont'd:
      Inspectors observed and assessed licensed operator performance in the plant and main
Chairman
      control room, particularly during periods of heightened activity or risk and where the
North Carolina Utilities Commission
      activities could affect plant safety. Specifically, on September 16th, the inspectors
Electronic Mail Distribution
      observed the Unit 1 shutdown and cooldown evolutions leading up to the forced outage
 
      to repair the recirculation pump seals. The inspectors reviewed various licensee policies
Robert P. Gruber Executive Director
      and procedures listed in the Attachment.
Public Staff - NCUC
      *  Operator compliance and use of procedures.
 
      *  Control board manipulations.
4326 Mail Service Center
      *   Communication between crew members.
 
      *  Use and interpretation of plant instruments, indications and alarms.
Raleigh, NC   27699-4326
      *  Use of human error prevention techniques.
Anthony Marzano
      *  Documentation of activities, including initials and sign-offs in procedures.
 
      *  Supervision of activities, including risk and reactivity management.
Director
      *  Pre-job briefs and crew briefs
Brunswick County Emergency Services
Electronic Mail Distribution


  Public Service Commission
                                              10
State of South Carolina
    This activity constituted one License Operator Requalification inspection sample and one
P.O. Box 11649
    Control Room Observation inspection sample.
b.  Findings
    No findings were identified.
1R12 Maintenance Effectiveness (71111.12Q - 3 samples)
a. Inspection Scope
    The inspectors evaluated degraded performance issues involving the following risk-
    significant systems:
    *  1B Nuclear Service Water Pump smoking with vibration and strainer leakage on
        pump start on June 26, 2012;
    *  2A Standby Liquid Cooling accumulator failure before operability run on September
        10, 2012 (AR560026); and
    *  Performance (unavailability and unreliability) history of the Severe Accident
        Mitigation Alternatives (SAMA) diesels
    The inspectors reviewed events where ineffective equipment maintenance may have
    resulted in equipment failure or invalid automatic actuations of Engineered Safeguards
    Systems and independently verified the licensee's actions to address system
    performance or condition problems in terms of the following:
    *  implementing appropriate work practices;
    *  identifying and addressing common cause failures;
    *  scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
    *  characterizing system reliability issues for performance;
    *  charging unavailability for performance;
    *  trending key parameters for condition monitoring; and
    *  ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and verifying
        appropriate performance criteria for structures, systems and components
        (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and
        corrective actions for systems classified as (a)(1).
    The inspectors assessed performance issues with respect to the reliability, availability,
    and condition monitoring of the system. In addition, the inspectors verified maintenance
    effectiveness issues were entered into the corrective action program with the appropriate
    significance characterization.
b. Findings
    No findings were identified.


Columbia, SC   29211
                                                11
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples)
a.  Inspection Scope
    The inspectors reviewed the licensee's evaluation and management of plant risk for the
    maintenance and emergent work activities affecting risk-significant equipment listed
    below to verify that the appropriate risk assessments were performed prior to removing
    equipment for work:
    *  Unit 2 yellow risk during emergent work on 2-E21-F015A, 2A Core Spray Full Flow
        Test Bypass Valve, and scheduled maintenance on 2B RHR/residual heat removal
        service water (RHRSW) on July 11, 2012;
    *  Unit 1 yellow risk during 1B Recirculation Pump Variable Frequency Drive power
        recovery, and planned maintenance on 1A RHR/RHRSW on July 26, 2012;
    *  Unit 1 yellow risk during planned maintenance on 1B RHR/RHRSW September 4 to
        September 6, 2012;
    *   Unit 1 integrated risk during repair of 1B recirculation pump seal September 17 to
        September 25, 2012;
    These activities were selected based on their potential risk-significance relative to the
    reactor safety cornerstones. As applicable for each activity, the inspectors verified that
    risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
    and complete. When emergent work was performed, the inspectors verified that the
    plant risk was promptly reassessed and managed. The inspectors reviewed the scope
    of maintenance work, discussed the results of the assessment with the licensee's
    probabilistic risk analyst or shift technical advisor, and verified plant conditions were
    consistent with the risk assessment. The inspectors also reviewed TS requirements and
    walked down portions of redundant safety systems, when applicable, to verify risk
    analysis assumptions were valid and applicable requirements were met.
b.  Findings
    No findings were identified.
1R15 Operability Evaluations (71111.15 - 5 samples)
a.  Inspection Scope
    The inspectors reviewed the following five issues:
    *  Unit 2 High Pressure Coolant Injection (HPCI) elevated thrust bearing temperature
        on July 6, 2012 (AR548370);
    *  2D RHRSW Booster pump coupling grease specification evaluation on July 12, 2012
        (AR542025);
    *  Emergency Diesel Generator (EDG) #3 debris in bearing oil site glass on July 15,
        2012 (AR549420);
    *  Reactor Building Close Cooling Water (RBCCW) piping corrosion in rattle space on
        August 21, 2012 (AR557151); and


  W. Lee Cox, III Section Chief
                                              12
    *  EDG #4 alternate safe shutdown switch contact continuity indications on August 27,
        2012 (AR558810)
    The inspectors selected these potential operability issues based on the risk-significance
    of the associated components and systems. The inspectors evaluated the technical
    adequacy of the evaluations to ensure that TS operability was properly justified and the
    subject component or system remained available such that no unrecognized increase in
    risk occurred. The inspectors compared the operability and design criteria in the
    appropriate sections of the UFSAR and TS to the licensees evaluations, to determine
    whether the components or systems were operable. Where compensatory measures
    were required to maintain operability, the inspectors determined whether the measures
    in place would function as intended and were properly controlled. The inspectors
    determined, where appropriate, compliance with bounding limitations associated with the
    evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
    documents to verify that the licensee was identifying and correcting any deficiencies
    associated with operability evaluations.
b.  Findings
    No findings were identified.
1R18 Plant Modifications (71111.18 - 2 samples)
a. Inspection Scope
    The inspectors reviewed the two modifications listed below to determine whether the
    modifications affected the safety functions of systems that are important to safety. The
    inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results
    and conducted field walk-downs of the modifications to verify that the modifications did
    not degrade the design bases, licensing bases, and performance capability of the
    affected systems.
    *  Design leak tight barriers at reactor building rattle spaces (EC86304);
    *  Service water building drain hub baffle plate installation (EC 88431)
b.  Findings
    No findings were identified.
1R19 Post Maintenance Testing (71111.19 - 7 samples)
a.  Inspection Scope
    The inspectors reviewed the following seven post-maintenance activities to verify that
    procedures and test activities were adequate to ensure system operability and functional
    capability:
    *  0PT-12.2D, No. 4 Diesel Generator Monthly Load Test after replacement of the 60X
        relay on July 23, 2012;


Radiation Protection Section
                                              13
N.C. Department of Environmental Commerce & Natural Resources
    *    0PT-08.1.4B, Residual Heat Removal (RHR) Service Water (SW) System Operability
Electronic Mail Distribution
          Test - Unit 2 RHRSW Loop B after the maintenance outage on July 12, 2012;
Warren Lee
    *    0PT-08.2.2c, Low Pressure Coolant Injection/RHR System Operability Test - Unit 1
Emergency Management Director
          RHR Loop A after the maintenance outage on July 27, 2012;
New Hanover County 
    *    0PT-12.2C, EDG #3 Operability Test - Unit 2 after repair of jacket water pump on
Department of Emergency Management
          August 16, 2012;
230 Government Center Drive
    *    0PT-15.6, Standby Gas Treatment Operability Test, Unit 1 B after relay replacement
Suite 115
          on August 15, 2012;
Wilmington, NC  28403  
    *    0PT-10.1.1, Reactor Core Isolation Cooling System Operability Test, Unit 2 after
M. Annacone 5
          replacement of Electronic Governor - Magnetic (EGM) on August 23, 2012; and
  Letter to Michael J. Annacone from Randall A. Musser dated November 7, 2012
    *    0PT-80.5, Reactor Pressure Vessel Pressure Test - Unit 1 after repair of 1B
          recirculation pump seal on September 26, 2012
    These activities were selected based upon the structure, system, or component's ability
    to impact risk. The inspectors evaluated these activities for the following, as applicable:
    the effect of testing on the plant had been adequately addressed; testing was adequate
    for the maintenance performed; acceptance criteria were clear and demonstrated
    operational readiness; test instrumentation was appropriate; tests were performed as
    written in accordance with properly reviewed and approved procedures; equipment was
    returned to its operational status following testing, and test documentation was properly
    evaluated. The inspectors evaluated the activities against the UFSAR and TS to ensure
    that the test results adequately ensured that the equipment met the licensing basis and
    design requirements. In addition, the inspectors reviewed corrective action documents
    associated with post-maintenance tests to determine whether the licensee was
    identifying problems and entering them in the CAP and that the problems were being
    corrected commensurate with their importance to safety.
b. Findings
    No findings were identified.
1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)
    Other Outage Activities
  a. Inspection Scope
    The inspectors evaluated licensee outage activities for an unscheduled forced outage to
    replace the 1B recirculation pump seal assembly. During the outage, the licensee made
    the decision to replace the 1A recirculation pump seal assembly to address the potential
    extent of cause/condition. The outage began on September 16, 2012 and concluded on
    September 28, 2012. The inspectors reviewed activities to ensure that the licensee
    considered risk in developing, planning, and implementing the outage schedule.
    Additionally, the inspectors observed or reviewed the reactor shutdown and cool down,
    outage equipment configuration and risk management, electrical lineups, control and
    monitoring of decay heat removal, control of containment activities, performed a drywell
    close out inspection, observed reactor startup and heat up activities, and identification
    and resolution of problems associated with the outage. Documents reviewed are listed
    in the Attachment.


                                            14
SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.:  05000325/2012004 AND 05000324/2012004
b. Findings
Distribution w/encl:
  Introduction: The inspectors identified a Green NCV of TS 3.6.4.1, Secondary
J. Baptist, RII EICS 
  Containment because the licensee did not maintain secondary containment operable as
L. Douglas, RII EICS 
  required during an activity considered an operation with a potential for draining the
OE Mail (email address if applicable)  
  reactor vessel (OPDRV).
RIDSNRRDIRS PUBLIC R. Pascarelli, NRR ((Regulatory Conferences Only))
  Description: On September 19, 2012, the licensee was replacing the 1B recirculation
RidsNrrPMBrunswick Resource
  pump seal assembly while Unit 1 was in Mode 4 (cold shutdown). In an effort to properly
  Enclosure U. S. NUCLEAR REGULATORY COMMISSION
  isolate the work area, the recirculation suction and discharge isolation valves were
REGION II
  tagged closed. Due to seat leakage across the isolation valves, the 1B recirculation
  pump drain valve was uncapped and opened to maintain the pump body partially empty
Docket Nos.: 50-325, 50-324
  to prevent water from impacting the work area while the pump seal was removed. The
   License Nos.: DPR-71, DPR-62
  pump drain leakage was sent to the drywell floor drain system. The 1B recirculation
   Report Nos.: 05000325/2012004, 05000324/2012004
  pump seal replacement activity had the potential to drain the reactor vessel below the
   Licensee: Carolina Power and Light (CP&L)  
  top of the fuel because the recirculation loops penetrate the reactor vessel below the top
   Facility: Brunswick Steam Electric Plant, Units 1 & 2  
  of active fuel. An OPDRV is described in the licensees technical specifications as an
   Location: 8470 River Road, SE Southport, NC 28461
  operation with a potential for draining the reactor vessel. However, the licensee did not
   Dates: July 1, 2012 through September 30, 2012  
  recognize or consider this activity as an OPDRV due to inadequate procedural guidance
   Inspectors: M. Catts, Senior Resident Inspector M. Schwieg, Resident Inspector
   that was used to exclude this activity as an OPDRV. Specifically, the licensee adopted
P. Niebaum, Acting Senior Resident Inspector
   the definition of an OPDRV in procedure 0OI-01.01 as provided in Enforcement
J. Dodson, Senior Project Engineer (1R04, 1R05, 4OA2)  
   Guidance Memorandum (EGM) 11-003 as any activity that could potentially result in
L. Lake, Senior Reactor Inspector (4OA5)  
   draining or siphoning the RPV water level below the top of the fuel, without taking credit
  for mitigating measures. However, section 9.16.15.b.(2) of licensee procedure 0OI-
   01.01, BNP Conduct of Operations Supplement, stated leakage through mechanical
   joints (for example valve or flange packing leaks, seat leakage through an isolation
  valve, flange leakage, etc) is not considered an OPDRV. On September 19, 2012, the
   licensee relaxed Unit 1 secondary containment from 03:30 a.m. until 09:20 p.m. by
  opening the reactor building air lock doors on the 20-foot elevation to increase ventilation
  to the recirculation pump seal replacement work area in the Unit 1 drywell. This resulted
  in Secondary Containment inoperability while Unit 1 was in Mode 4 during an OPRDV
  activity. The inspectors questioned the licensees Operations staff on the decision to
  make secondary containment inoperable during an OPDRV activity. Following this, the
  licensee restored secondary containment, developed an Operation standing instruction
  12-052 to treat this activity as an OPDRV and placed this issue into its CAP as AR
  562188.
  Analysis: The inspectors determined that the failure to maintain secondary containment
  operable while Unit 1 was in Mode 4 with an OPDRV in progress was a performance
  deficiency. The performance deficiency was more than minor because it was associated
  with the configuration control attribute of the Barrier Integrity Cornerstone, and adversely
  affected the cornerstone objective to provide reasonable assurance that physical design
  barriers (fuel cladding, reactor coolant system, and containment) protect the public from
  radionuclide releases caused by accidents or events because the Unit 1 secondary
  containment boundary was not preserved or maintained. The inspectors evaluated the
  finding using Inspection Manual Chapter (IMC) 0609, Attachment 4, Phase 1 - Initial
  Screening and Characterization of Findings, which required an analysis using IMC 0609
  Appendix G since the reactor was in Mode 4 (cold shutdown). The finding was
  determined to be of very low safety significance (Green) according to IMC 0609


M. Endress, Reactor Inspector (1R07)
                                                15
    Approved by: Randall A. Musser, Chief Reactor Projects Branch 4
      Appendix G, Attachment 1, Checklist 6, since a quantitative assessment (Phase 2 or
Division of Reactor Projects
      Phase 3 evaluation) was not required. Specifically, the inspectors determined that the
 
      licensee maintained adequate mitigation capability for reactor vessel water level
  SUMMARY OF FINDINGS
      inventory and an event did not occur that could be characterized as a loss of control.
      The cause of this finding was directly related to the cross-cutting aspect of Accurate
IR 05000325/2012004, 05000324/2012004; 07/01/12 - 09/30/12; Brunswick Steam Electric
      Procedures in the Resources component of the Human Performance area, because the
Plant, Units 1 & 2; Refueling and Other Outage Activities, Identification and Resolution of
      licensee did not consider the recirculation pump seal replacement activity to be OPDRV
 
      based on procedural guidance that contains exclusions to what are considered OPDRV
Problems
      activities. [H.2(c)]
      Enforcement: Unit 1 TS 3.6.4.1, Secondary Containment, required secondary
This report covers a three-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors.  Two Green findings were identified by the inspectors.  The significance of most findings is indicated by their color (Green, White, Yellow,
      containment to be operable during modes one, two, three, during movement of recently
Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process"
      irradiated fuel assemblies in the secondary containment and during operations with a
(SDP).  The cross-cutting aspects were determined using IMC 0310, "Components Within the
      potential for draining the reactor vessel (OPDRVs). Contrary to the above, on
Cross-Cutting Areas".  Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. 
      September 19, 2012, Unit 1 secondary containment was not maintained operable during
      an OPDRV activity. The licensee entered this issue in its CAP as AR 562188, and
A. NRC-Identified and Self-Revealing Findings
      restored secondary containment during the OPDRV activity. Because the licensee
  Cornerstone:  Barrier Integrity
      entered the issue into its CAP and the finding is of very low safety significance (Green),
Green:  The inspectors identified a Green non-cited violation (NCV) of TS 3.6.4.1, Secondary Containment because the licensee did not maintain secondary containment
      this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRCs
operable as required during a maintenance activity considered an operation with a
      Enforcement Policy: NCV 05000325/2012004-01, Failure to Maintain Secondary
potential for draining the reactor vessel (OPDRV).  Once questioned by the inspectors,
      Containment Operable during an OPDRV activity.
the licensee restored secondary containment, developed an Operation standing instruction (12-052) to treat the activity as an OPDRV and placed this issue into its corrective action program (CAP) as AR 562188. The failure to maintain secondary containment operable while Unit 1 was in Mode 4 with an OPDRV in progress was a performance deficiency.  The finding was more than minor because it was associated with the configuration control attribute of the Barrier Integrity
1R22 Surveillance Testing
 
.1   Routine Surveillance Testing (71111.22 - 4 samples)
Cornerstone, and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding, reactor coolant system, and
containment) protect the public from radionuclide releases caused by accidents or
events because the Unit 1 secondary containment boundary was not preserved or maintained.  The inspectors evaluated the finding using Inspection Manual Chapter (IMC) 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,
which required an analysis using IMC 0609 Appendix G since the reactor was in Mode 4 (cold shutdown).  The finding was determined to be of very low safety significance
(Green) according to IMC 0609 Appendix G, Attachment 1, Checklist 6, since a quantitative assessment (Phase 2 or Phase 3 evaluation) was not required. Specifically, the inspectors determined that the licensee maintained adequate mitigation capability for  
reactor vessel water level inventory and an event did not occur that could be  
characterized as a loss of control. The cause of this finding was directly related to the  
cross-cutting aspect of Accurate Procedures in the Resources component of the Human  
Performance area, because the licensee did not consider the recirculation pump seal replacement activity to be OPDRV based on procedural guidance that contains exclusions to what are considered OPDRV activities. [H.2(c)] (Section 1R20)
 
 
3 Cornerstone:  Emergency Preparedness
Green:  A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the licensee's failure to properly evaluate or consider the impact to emergency response
facilities of design change ESR98-00436 which was implemented in 1999. This resulted
in the loss of Emergency Response Facility Information System (ERFIS), Emergency Response Data System (ERDS), Safety
Parameter Display System (SPDS), and all displays including radiation monitors for the emergency response facilities.  Specifically, the licensee failed to ensure that adequate emergency response facilities and equipment
were available as required by the Brunswick Nuclear Plant Radiological Emergency
Plan, Section 1.3.1.3 revision 80 and 10 CFR 50.47(b)(8). This issue was captured in the
licensee's CAP as AR 542704.
The licensee's failure to properly evaluate or consider the impact to emergency
response facilities of design change ESR98-00436 which was implemented in 1999 was
a performance deficiency.  Specifically, the licensee introduced a single point failure
mode which did not meet the design requirements specified in their Design Basis Document (DBD 60) sections 3.6.7.2 and 3.6.7.3.  This resulted in the licensee's failure to ensure that adequate emergency response facilities and equipment were available as
delineated in the Updated Final Safety Analysis Report (UFSAR) Section 7.7.1.9, and
required by the Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3,
revision 80, and 10 CFR 50.47(b)(8). The finding was more than minor because it
adversely affected the Emergency Preparedness Cornerstone objective of ensuring that the licensee was capable of implementing adequate measures to protect the health and safety of the public in the event of a radiological emergency.  Specifically, the Facilities and Equipment attribute was affected during the time when the ERFIS, ERDS, SPDS,
and all displays including radiation monitors for the emergency response facilities were degraded, and as a result did not meet 10 CFR 50.47(b)(8) Planning Standard program element, adequate emergency facilities and equipment to support the emergency response are provided and maintained.  The finding was assessed for significance in
accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance
Determination Process.  Attachment 2 of Appendix B, Failure to Comply Significance
Logic is as follows:  Failure to comply; Loss of Risk Significant Planning Standard
Function (RSPS), No; RSPS Degraded Function, No; Loss of Planning Standard Function, No; the result is a Green finding.  The inspectors determined that this resulted in a very low safety significance finding (Green).  No cross-cutting aspect was assigned
to this finding because the performance deficiency occurred more than three years ago and is not reflective of current plant performance. (Section 4OA2.2)
B. Licensee-Identified Violations
  Violations of very low safety significance that were identified by the licensee have been reviewed by inspectors.  Corrective actions taken or planned by the licensee have been
entered into the licensee's CAP.  These violations and corrective action tracking
numbers are listed in Section 4OA7 of this report.
 
  REPORT DETAILS
Summary of Plant Status
 
Unit 1 began the inspection period at rated thermal power (RTP), and operated at or near full power until July 22, 2012 when reactor power was lowered to 52 percent to clear a fouled
circulating water debris filter and power was returned to RTP on July 23, 2012. On August 3,
2012, power was reduced to 70 percent for a rod sequence exchange and power was returned to RTP on August 5, 2012.  On August 5, 2012, power was reduced to 90 percent for control rod improvement and power was returned to RTP on the same day.  On August 8, 2012, power was
reduced to 65 percent for offsite transmission line work and power was returned to RTP on the
same day.  On September 16, 2012, the reactor was shut down for forced outage to replace the
1A and 1B recirculation pump seal assemblies.  Reactor startup commenced on September 27, 2012 and the main generator was synchronized to the grid on September 28, 2012.  Reactor power was raised to RTP on September 29, 2012.  On September 30, 2012 reactor power was
reduced to 75 percent for a scheduled control rod improvement.  Power ascension continued to
RTP for the remainder of the inspection period.  
 
Unit 2 began the inspection period at RTP, and operated at or near full power until August 18, 2012, when power was reduced to 70 percent for a rod sequence exchange and power was
returned to RTP on August 19, 2012.  On August 20, 2012, power was reduced to 86 percent
for control rod improvement and power was returned to RTP on August 21, 2012.  On August
21, 2012, power was reduced to 94 percent for control rod improvement and power was
returned to RTP on August 21, 2012.  On September 29, 2012, reactor power was reduced to 94 percent to support a scheduled rod improvement and returned to RTP later that day and maintained RTP for the remainder of the inspection period.
 
1. REACTOR SAFETY
  Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01 - 1 sample)
External Flooding
    a. Inspection Scope
  The inspectors evaluated the design, material condition, and procedures for coping with
the design basis probable maximum flood.  The inspectors reviewed the Updated Final
Safety Analysis Report (UFSAR), which depicted the design flood levels and protection areas containing safety-related equipment, to identify areas that may be affected by external flooding.  The inspectors conducted a site walk-down of the service water
building, to ensure that erected flood protection measures were in accordance with
design specifications.  The inspectors reviewed the sealing of equipment below the flood
line, adequacy of watertight doors, drain systems and sumps including check valves, and maintenance and calibration of flood protection equipment.  The inspectors also reviewed operating procedures for mitigating external flooding during severe weather to 
5  determine if the licensee planned or established adequate measures to protect against
external flooding events.  
    b. Findings
  No findings were identified.
1R04 Equipment Alignment
 
.1 Quarterly Partial System Walk-downs (71111.04Q - 3 samples)  
   a. Inspection Scope
   a. Inspection Scope
  The inspectors performed partial system walk-downs of the following risk-significant
      The inspectors either observed surveillance tests or reviewed the test results for the
systems:  * Unit 2 "A" train Core Spray (CS) system while "B" residual heat removal/service (RHR/SW) was inoperable for a system outage on July 11, 2012; * Unit 1 Reactor Building Closed Cooling Water (RBCCW) on July 27, 2012; and
      following activities to verify the tests met TS surveillance requirements, UFSAR
* Unit 1 "B" Standby Gas Treatment (SBGT) while the "A" SBGT was inoperable for a maintenance outage on September 19, 2012.
      commitments, in-service testing requirements, and licensee procedural requirements.
  The inspectors selected these systems based on their risk-significance relative to the  
      The inspectors assessed the effectiveness of the tests in demonstrating that the SSCs
reactor safety cornerstones at the time they were inspected.  The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk.  The inspectors reviewed applicable operating procedures,  
      were operationally capable of performing their intended safety functions.
system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down
      *    0PT-07.2.4A, Core Spray System Operability Test - Loop A on July 5, 2012;
accessible portions of the systems to verify that system components and support equipment were aligned correctly and were operable.  The inspectors examined the  
      *    0MST-RHR21Q, RHR-LPCI, CSS and HPCI Hi Drywell Pressure Trip Unit Inst Chan
material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly identified and resolv
          Cal on July 10, 2012;
ed equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization.
      *    0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional on July 24,
    b. Findings
          2012; and
  No findings were identified.  
      *    0PT-12.12D, No. 4 Diesel Generator Monthly Load Test on August 17, 2012;
.2 Semi-Annual Complete System Walk-down (71111.04S - 1 sample)
  b. Findings
    a. Inspection Scope
      No findings were identified.
  On September 5, 2012 the inspectors
performed a complete system alignment inspection of the Unit 1 RHR system
to verify the functional capability of the system.  This system was selected because it was considered both safety-significant and risk-
6  significant in the licensee's probabilistic risk assessment.  The inspectors walked down the system to review mechanical and electrical equipment line-ups, electrical power availability, system pressure and temperature indications, as appropriate, component labeling, component lubrication, component and equipment cooling, hangers and
supports, operability of support systems, and to ensure that ancillary equipment or
debris did not interfere with equipment operation. A review of a sample of past and
outstanding work orders (WOs) was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the CAP to ensure that system equipment alignment problems were being identified and
appropriately resolved. 
    b. Findings
  No findings were identified.  


                                                16
1R05 Fire Protection (71111.05Q - 5 samples)  
.2    In-Service Testing (IST) Surveillance (71111.22 - 1 sample)
  Quarterly Resident Inspector Tours
 
   a. Inspection Scope
   a. Inspection Scope
  The inspectors conducted fire protection walk-downs which were focused on availability,  
      The inspectors reviewed the performance of Unit 1 LPCI/RHR System Operability Test -
accessibility, and the condition of firefighting equipment in the following risk-significant plant areas: 
      Loop B on August 9, 2012 to evaluate the effectiveness of the licensees American
* Unit 1 and 2 Control Buildings 23'
      Society of Mechanical Engineers (ASME) Section XI testing program for determining
Elevation 1PFP-CB-7; * Unit 1 Reactor Building East 50' Elevation 1PFP-RB1-1h;
      equipment availability and reliability. The inspectors evaluated selected portions of the
* Unit 1 Turbine Building South Area 38' Elevation 1PFP-TB1-1k; * Unit 2 Reactor Building 50' Elevation 2PFP-RB2-1h; and * Unit 2 Reactor Building North 2A Core Spray Room 2-PFP-RB2-1b.  
      following areas: 1) testing procedures, 2) acceptance criteria, 3) testing methods, 4)
 
      compliance with the licensees IST program, TS, selected licensee commitments, and
      code requirements, 5) range and accuracy of test instruments, and 6) required corrective
The inspectors reviewed areas to assess if the licensee had implemented a fire
      actions.
protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out-of-service, degraded or inoperable fire
protection equipment, systems, or features in accordance with the licensee's fire plan. 
The inspectors selected fire areas based on their overall contribution to internal fire risk
as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event.  Using
the documents listed in the attachment, the inspectors verified that fire hoses and  
extinguishers were in their designated locations and available for immediate use; that
fire detectors and sprinklers were unobstructed, that transient material loading was
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP.
 
   b. Findings
   b. Findings
  No findings were identified.  
      No findings were identified.
.3    Reactor Coolant System Leak Detection Inspection Surveillance (71111.22 - 1 sample)
1R06 Flood Protection Measures (71111.06 - 1 sample)  
  a. Inspection Scope
      The inspectors observed and reviewed the test results for a reactor coolant system leak
Annual Review of Cables Located in Underground Bunkers/Manholes
      detection surveillance, 0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure
    a. Inspection Scope
      Vessel Pressure Test, on September 28, 2012. The inspectors observed in-plant
  The inspectors conducted an inspection of underground bunkers/manholes subject to
      activities and reviewed procedures and associated records to determine whether:
flooding that contain cables whose failure could disable risk-significant equipment. The inspectors performed walk-downs of risk-significant areas, including manhole 2-MH-7SW, to verify that the cables were not submerged in water, that cables and/or splices
      effects of the testing were adequately addressed by control room personnel or engineers
appear intact and to observe the condition of cable support structures.  When applicable,  
      prior to the commencement of the testing; acceptance criteria were clearly stated,
the inspectors verified proper dewatering device (sump pump) operation and verified
      demonstrated operational readiness, and were consistent with the system design basis;
level alarm circuits are set appropriately to ensure that the cables will not be submerged. Where dewatering devices were not installed; the inspectors ensured that drainage was provided and was functioning properly.
      plant equipment calibration was correct, accurate, and properly documented; and the
      calibration frequency was in accordance with TSs, the UFSAR, procedures, and
      applicable commitments; applicable prerequisites described in the test procedures were
      satisfied; test frequencies met TS requirements to demonstrate operability and reliability;
      tests were performed in accordance with the test procedures and other applicable
      procedures; and test data and results were accurate, complete, within limits, and valid.
      Inspectors verified that test results not meeting acceptance criteria were addressed with
      an adequate operability evaluation or the system or component was declared
      inoperable; equipment was returned to a position or status required to support the
      performance of its safety functions; and all problems identified during the testing were
      appropriately documented and dispositioned in the corrective action program.
   b. Findings
   b. Findings
  No findings were identified.  
      No findings were identified.
1R07 Heat Sink Performance
(71111.07T - 3 samples)
Triennial Review of Heat Sink Performance
    a. Inspection Scope
  The inspectors selected the Residual Heat Removal (RHR) Heat Exchanger 2A, Diesel
Generator (DG) 3 Jacket Water Cooler and the Core Spray (CS) Room Cooler 1A,
based on their risk-significance in the licensee's probabilistic safety analysis and their


importance to safety-related mitigating syst
                                                17
em support functions in the NRC's model for Brunswick Nuclear Power Plant, Units 1 and 2.
1EP6 Emergency Planning Drill Evaluation (71114.06 - 2 samples)
For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler
1A, the inspectors reviewed the licensee's inspection, maintenance, and monitoring of biotic fouling and macro-fouling programs, to determine if they were adequate to ensure proper heat transfer.  This was accomplished by determining whether the methods used were consistent with accepted industry practices.  The inspectors also reviewed the
licensee's inspection and cleaning activities had established acceptance criteria
consistent with industry standards, and the as-found results were recorded, evaluated,
and appropriately dispositioned to maintain structural integrity.
 
For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler 1A, the inspectors reviewed the methods and results of heat exchanger performance inspections.  In addition, the inspectors
reviewed the condition and operation of the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler 1A to 
8  determine if they were consistent with design assumptions in heat transfer calculations and as described in the USFAR.  This included determining whether the number of plugged tubes was within pre-established limits based on capacity and heat transfer
assumptions.  The inspectors also determined whether the licensee evaluated the potential for water hammer and established adequate controls and operational limits to
prevent heat exchanger degradation due to excessive flow-induced vibration during operation.
The inspectors determined whether the performance of the ultimate heat sink (UHS)-
Cape Fear River and its subcomponents such as piping, intake screens, pumps, valves,
etc. was appropriately evaluated by tests or other equivalent methods to ensure availability and accessibility to the in-plant cooling water systems.  The inspectors also reviewed design changes to the service water system and the UHS.
The inspectors reviewed the licensee's operation of the service water system and UHS. 
This included a review of licensee's procedures for a loss of the service water system or UHS and the verification that instrumentation, which is relied upon for decision-making, was available and functional.  The inspectors also performed a system walk-down on the
service water system to determine whether the licensee's assessment on structural integrity was adequate and interviewed the respective system engineer.  For buried or
inaccessible piping, the inspectors reviewed the licensee's pipe testing, inspection, and
monitoring program to determine whether structural integrity was ensured and that any
leakage or degradation was appropriately identified and dispositioned by the licensee.
The inspectors performed a system walk-down of the service water intake structure to determine whether the licensee's assessment on structural integrity and component functionality was adequate.  The inspectors also determined whether service water pump bay silt accumulation was monitored, trended, and maintained at an acceptable level by the licensee, and that water level instruments were functional and routinely monitored.  The inspectors also determined whether the licensee's ability to ensure
functionality during adverse weather conditions was adequate.
 
The inspectors reviewed condition reports related to the heat exchangers and heat sink
performance issues to determine whether the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions.  Records were also reviewed to verify that the licensee actions were consistent with Generic Letter
(GL) 89-13 licensee commitments, Electric Power Research Institute (EPRI) and other
industry guidelines.  These inspection activities constituted three heat sink inspection
samples as defined in IP 71111.07-05.
    b. Findings
  No findings were identified.
 
 
 
1R11 Licensed Operator Requalification Program (71111.11Q - 2 samples)  
.1 Quarterly Review of Licensed Operator Requalification Testing and Training
 
   a. Inspection Scope
   a. Inspection Scope
  On August 13, 2012, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator
      The inspectors observed site emergency preparedness training drill/simulator scenarios
performance was adequate, evaluators we
      conducted on July 9, 2012 and July 25, 2012. The inspectors reviewed the drill scenario
re identifying and documenting crew performance problems, and to ensure that training was being conducted in accordance
      narrative to identify the timing and location of classifications, notifications, and protective
with licensee procedures. The inspectors evaluated the following areas:
      action recommendations development activities. During the drill, the inspectors
* licensed operator performance; * crew's clarity and formality of communications;
      assessed the adequacy of event classification and notification activities. The inspectors
* ability to take timely actions in the conservative direction;
      observed portions of the licensees post-drill. The inspectors verified that the licensee
* prioritization, interpretation, and verification of annunciator alarms;
      properly evaluated the drills performance with respect to performance indicators and
* correct use and implementation of abnormal and emergency procedures; * control board manipulations; * oversight and direction from supervisors; and
      assessed drill performance with respect to drill objectives.
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.
The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements.  
   b. Findings
   b. Findings
  No findings were identified.  
      No findings were identified.
.2 Quarterly Review of Licensed Operator Performance in the Main Control Room
4.   OTHER ACTIVITIES
 
4OA1 Performance Indicator (PI) Verification (71151 - 6 samples)
.1    Mitigating Systems Cornerstone
   a. Inspection Scope
   a. Inspection Scope
   Inspectors observed and assessed licensed operator performance in the plant and main control room, particularly during periods of heightened activity or risk and where the activities could affect plant safety. Specifically, on September 16
      *   Mitigating Systems Performance Index, Residual Heat Removal - Unit 1
th, the inspectors observed the Unit 1 shutdown and cooldown evolutions leading up to the forced outage
      *  Mitigating Systems Performance Index, Residual Heat Removal - Unit 2
to repair the recirculation pump seals. The inspectors reviewed various licensee policies
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
and procedures listed in the Attachment. 
      Index (MSPI) performance indicators listed above for the period from the third (3rd)
* Operator compliance and use of procedures.  
      quarter 2011 through the second (2nd) quarter 2012. The inspectors reviewed the
* Control board manipulations.  
      licensees operator narrative logs, issue reports, MSPI derivation reports, event reports
* Communication between crew members.  
      and NRC Integrated Inspection reports for the period to validate the accuracy of the
* Use and interpretation of plant instruments, indications and alarms.  
      submittals.
* Use of human error prevention techniques.  
  b. Findings
* Documentation of activities, including initials and sign-offs in procedures.
      No findings were identified.
* Supervision of activities, including risk and reactivity management.
.2    Barrier Integrity Cornerstone
* Pre-job briefs and crew briefs 
  a. Inspection Scope
10  This activity constituted one License Operator Requalification inspection sample and one Control Room Observation inspection sample.
      *   Reactor Coolant System (RCS) Specific Activity - Unit 1
    b. Findings
      *   Reactor Coolant System (RCS) Specific Activity - Unit 2
  No findings were identified.  
      The inspectors reviewed licensee submittals for the Reactor Coolant System Specific
      Activity performance indicator for the period from the third (3rd) quarter 2011 through the
      second (2nd) quarter 2012. The inspectors reviewed the licensees RCS chemistry


1R12 Maintenance Effectiveness (71111.12Q - 3 samples)  
                                                  18
      samples, TS requirements, issue reports, and event reports for the period to validate the
      accuracy of the submittals. In addition to record reviews, the inspectors observed a
      chemistry technician obtain and analyze a reactor coolant system sample.
      *  Reactor Coolant System Leakage - Unit 1
      *  Reactor Coolant System Leakage - Unit 2
      The inspectors sampled licensee submittals for the Reactor Coolant System Leakage
      performance indicator for the period from the third (3rd) quarter 2011 through the second
      (2nd) quarter 2012. The inspectors reviewed the licensees operator logs, RCS leakage
      tracking data, issue reports, and event reports for the period to validate the accuracy of
      the submittals.
  b. Findings
      No findings were identified.
4OA2 Identification and Resolution of Problems (71152 - 2 samples)
.1    Routine Review of Items Entered Into the Corrective Action Program
   a. Inspection Scope
   a. Inspection Scope
  The inspectors evaluated degraded performance
      To aid in the identification of repetitive equipment failures or specific human performance
issues involving the following risk-significant systems:
      issues for follow-up, the inspectors performed frequent screenings of items entered into
* 1B Nuclear Service Water Pump smoking with vibration and strainer leakage on pump start on June 26, 2012;
      the licensees corrective action program. The review was accomplished by reviewing
* 2A Standby Liquid Cooling accumulator failure before operability run on September
      daily action request reports.
10, 2012 (AR560026); and * Performance (unavailability and unreliability) history of the Severe Accident
Mitigation Alternatives (SAMA) diesels
  The inspectors reviewed events where ineffective equipment maintenance may have
resulted in equipment failure or invalid automatic actuations of Engineered Safeguards Systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
 
* implementing appropriate work practices;
* identifying and addressing common cause failures; * scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule; * characterizing system reliability issues for performance;
* charging unavailability for performance;
* trending key parameters for condition monitoring; and
* ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and verifying appropriate performance criteria for structures, systems and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1).
The inspectors assessed performance issues with respect to the reliability, availability,
and condition monitoring of the system.  In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization.  
  b. Findings
  No findings were identified.
 
 
11 
1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples)
    a. Inspection Scope
  The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant equipment listed
below to verify that the appropriate risk assessments were performed prior to removing
equipment for work:
* Unit 2 yellow risk during emergent work on 2-E21-F015A, 2A Core Spray Full Flow Test Bypass Valve, and scheduled maintenance on 2B RHR/residual heat removal
service water (RHRSW) on July 11, 2012; * Unit 1 yellow risk during 1B Recirculation Pump Variable Frequency Drive power recovery, and planned maintenance on 1A RHR/RHRSW on July 26, 2012; * Unit 1 yellow risk during planned maintenance on 1B RHR/RHRSW September 4 to September 6, 2012; * Unit 1 integrated risk during repair of 1B recirculation pump seal September 17 to September 25, 2012;
These activities were selected based on their potential risk-significance relative to the
reactor safety cornerstones.  As applicable for each activity, the inspectors verified that
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
and complete.  When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed.  The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's
probabilistic risk analyst or shift technical advisor, and verified plant conditions were
consistent with the risk assessment. The inspectors also reviewed TS requirements and
walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
   b. Findings
   b. Findings
  No findings were identified.  
      No findings were identified.
1R15 Operability Evaluations (71111.15 - 5 samples)  
.2    Assessments and Observations
      Selected Issue Follow-up Inspection: UPS-A Failure and Loss of Emergency Response
      Facility Information System (ERFIS), Plant Process Computer (PPC), Business Network
   a. Inspection Scope
   a. Inspection Scope
  The inspectors reviewed the following five issues:
      The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business
* Unit 2 High Pressure Coolant Injection (HPCI) elevated thrust bearing temperature
      Network, for detailed review. This AR identified that a single failure caused the loss of
on July 6, 2012 (AR548370); * 2D RHRSW Booster pump coupling grease specification evaluation on July 12, 2012 (AR542025); * Emergency Diesel Generator (EDG) #3 debris in bearing oil site glass on July 15, 2012 (AR549420); * Reactor Building Close Cooling Water (RBCCW) piping corrosion in rattle space on August 21, 2012 (AR557151); and
      ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors
12  * EDG #4 alternate safe shutdown switch contact continuity indications on August 27, 2012 (AR558810)  
      reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors
      reviewed these reports to verify that the licensee identified the full extent of the issue,
The inspectors selected these potential operability issues based on the risk-significance
      performed an appropriate evaluation, and specified and prioritized appropriate corrective
of the associated components and systems. The inspectors evaluated the technical
      actions. The inspectors evaluated the reports against the requirements of the licensees
adequacy of the evaluations to ensure that TS operability was properly justified and the
      CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action
subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the UFSAR and TS to the licensee's evaluations, to determine
      Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.
 
                                            19
b. Findings
  No findings were identified
a. Inspection Scope
  The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business
  Network, for detailed review. This AR identified that a single failure caused the loss of
  ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors
  reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors
  reviewed these reports to verify that the licensee identified the full extent of the issue,
  performed an appropriate evaluation, and specified and prioritized appropriate corrective
  actions. The inspectors evaluated the reports against the requirements of the licensees
  CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action
  Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.
b. Findings
  Introduction: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the
  licensees failure to properly evaluate or consider the impact to emergency response
  facilities of design change ESR98-00436 which was implemented in 1999. As a result,
  a number of temporary losses of ERFIS, Emergency Response Data System (ERDS),
  SPDS, and all displays including radiation monitors for the emergency response facilities
  occurred. Specifically, the licensee failed to ensure that adequate emergency response
  facilities and equipment were available as required by the Brunswick Nuclear Plant
  Radiological Emergency Plan, Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).
  This issue was captured in the licensees CAP as AR 542704.
  Description: In 1999, the licensee implemented design change ESR98-00436 for the
  power supply to the ERFIS, ERDS, SPDS, and all displays including RMS for the
  emergency response facilities. The licensee did not properly evaluate or consider the
  impact to emergency response facilities and equipment prior to implementation of this
  design change. As a result, the ERFIS, ERDS, and SPDS systems, and all radiation
  monitoring system (RMS) displays were susceptible to a single point power failure mode.
  The implementation of the design change introduced a single point failure mode which
  did not meet the design requirements specified in their Design Basis Document (DBD
  60) sections 3.6.7.2 and 3.6.7.3. Prior to the licensees implementation of design
  change ESR98-00436 in 1999, this single point vulnerability did not exist as the power
  supply system had automatic switching capability on loss of one power source. When
  the design change was implemented, the ERFIS, ERDS, and SPDS systems and RMS
  displays were degraded as demonstrated by the resulting failures of those systems on
  multiple occasions including July 17, 2004 and June 12, 2012. Additionally, all displays
  for those systems were lost in all of the emergency facilities including the radiation
  monitoring system.


whether the components or systems were
                                        20
operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures
On June 13, 2012, the licensee made an event notification to the NRC Operations
in place would function as intended and were properly controlled. The inspectors
Center, 50.72(b)(3)(xiii) Loss of Emergency Assessment Capability, Offsite Response
determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.
Capability, or Offsite Communications Capability for the emergency response facilities.
    b. Findings
The report delineated that at 5:57 p.m. EDT on June 12, 2012, Brunswick Nuclear Plant
  No findings were identified.  
experienced a fault on the Emergency Response Facility Information System (ERFIS)
uninterruptible power supply (UPS) electrical bus A. This resulted in a loss of site
1R18 Plant Modifications (71111.18 - 2 samples)
Safety Parameter Display System (SPDS), Emergency Response Data System (ERDS)
    a. Inspection Scope
and Plant Process Computer (PPC) for both Unit 1 and Unit 2.
  The inspectors reviewed the two modifications listed below to determine whether the modifications affected the safety functions of
During the loss of SPDS, the emergency response capability of that system was lost to
systems that are important to safety. The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results and conducted field walk-downs of the modifications to verify that the modifications did not degrade the design bases, licensing bases, and performance capability of the  
the site. During the loss of ERDS, the automatic data transfer feature of that system
was lost for transmissions to the NRC, however manual data transfer was still available.
During the loss of the PPC, automatic core thermal power averaging and automatic core
thermal limit monitoring was lost. Manual calculations were available for these functions.
Unit 1 SPDS was restored to the Emergency Operations Facility (EOF) at 7:49 p.m. on
June 12, 2012. Unit 2 SPDS was restored to the EOF at 8:30 p.m. on June 12, 2012.
The inverter was restored to service on June 17, 2012 at 12:00 noon.
Inspectors determined that the licensee did not properly evaluate or consider the impact
to all emergency response facilities and equipment prior to implementation of the
ESR98-00436 design change. The inspectors concluded that the ERFIS, ERDS, and
SPDS systems required by the Brunswick Nuclear Plant Radiological Emergency Plan
were degraded from 1999 when the design change was installed to present.
Compensatory measures were put in place during the June 2012 event to manually
obtain and log the required data from the instrumentation in the control room and
transmit to the emergency response facilities, and after the June 2012 event, the
licensee initiated a design change to restore the power configuration to those systems
back to the original design which would remove this failure mechanism.
Analysis: The licensees failure to properly evaluate or consider the impact to
emergency response facilities of design change ESR98-00436 which was implemented
in 1999 was a performance deficiency. Specifically, the licensee introduced a single
point failure mode which did not meet the design requirements specified in their Design
Basis Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees
failure to ensure that adequate emergency response facilities and equipment were
available as delineated in the Updated Final Safety Analysis Report (UFSAR) Section
7.7.1.9, and required by the Brunswick Nuclear Plant Radiological Emergency Plan,
Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).
The finding was more than minor because it adversely affected the Emergency
Preparedness Cornerstone objective of ensuring that the licensee was capable of
implementing adequate measures to protect the health and safety of the public in the
event of a radiological emergency. Specifically, the Facilities and Equipment attribute
was affected during the time when the ERFIS, ERDS, SPDS, and all displays including
radiation monitors for the emergency response facilities were degraded, and as a result
did not meet 10 CFR 50.47(b)(8) Planning Standard program element, adequate
emergency facilities and equipment to support the emergency response are provided
and maintained. The finding was assessed for significance in accordance with NRC IMC
0609, Appendix B Emergency Preparedness Significance Determination Process.


affected systems.  
                                                21
* Design leak tight barriers at reactor building rattle spaces (EC86304); * Service water building drain hub baffle plate installation (EC 88431)  
      Attachment 2 of Appendix B, Failure to Comply Significance Logic is as follows: Failure
    b. Findings
      to comply; Loss of Risk Significant Planning Standard Function (RSPS), No; RSPS
  No findings were identified.  
      Degraded Function, No; Loss of Planning Standard Function, No; the result is a Green
1R19 Post Maintenance Testing (71111.19 - 7 samples)
      finding. The inspectors determined that this resulted in a low safety significance finding
      (Green). No cross-cutting aspect was assigned to this finding because the performance
      deficiency occurred more than three years ago and is not reflective of current plant
      performance.
      Enforcement: 10 CFR 50.54(q)(2) requires, in part, a licensee to follow and maintain the
      effectiveness of an emergency plan that meets the requirements in Appendix E to this
      part and, for nuclear power reactor licensee, the planning standards of 10 CFR 50.47(b).
      The Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3, revision 80,
      states in part that special provisions have been made to assure that ample space and
      proper equipment are available to effectively respond to a full range of possible
      emergencies. Contrary to the above, from 1999, when design change ESR98-00436
      was installed, until the compensatory measures were put in place in June 2012, the
      licensee failed to maintain adequate emergency facilities and equipment to support
      emergency response when the ERFIS, ERDS, SPDS, and all displays including radiation
      monitors for the emergency response facilities were degraded due to the implementation
      of the design change. This resulted in failures of those systems on July 17, 2004 and
      June 12, 2012. The licensee has compensatory measures in place, entered this issue
      their CAP as AR 542704, and initiated a design change to restore the power
      configuration back to the original design. Because the licensee entered the issue into its
      CAP and the finding is of very low safety significance (Green), this violation is being
      treated as an NCV, consistent with Section 2.3.2 of the NRCs Enforcement Policy: NCV
      05000325; 324/2012004-02, Failure to Maintain Reliability and Availability of Emergency
      Response Equipment for Emergency Response Facilities.
.3    Assessments and Observations
      Selected Issue Follow-up Inspection: EDG 2 wiring associated with Alternate Safe
      Shutdown (ASSD) Switch 2-DG-SS-A1
   a. Inspection Scope
   a. Inspection Scope
  The inspectors reviewed the following seven post-maintenance activities to verify that
      The inspectors performed a detailed review of AR 557897 associated with the wiring for
procedures and test activities were adequate to ensure system operability and functional capability:
      the EDG 2 Alternate Safe Shutdown (ASSD) Switch 2-DG-SS-A1. The issue was
      discovered during a planned system outage for EDG2 during the week of August 26.
* 0PT-12.2D, No. 4 Diesel Generator Monthly Load Test after replacement of the 60X relay on July 23, 2012; 
      The inspectors verified that the issue was captured completely and accurately in the
13  * 0PT-08.1.4B, Residual Heat Removal (RHR) Service Water (SW) System Operability Test - Unit 2 RHRSW Loop B after the maintenance outage on July 12, 2012;  * 0PT-08.2.2c, Low Pressure Coolant Injection/RHR System Operability Test - Unit 1 RHR Loop A after the maintenance outage on July 27, 2012; * 0PT-12.2C, EDG #3 Operability Test - Unit 2 after repair of jacket water pump on August 16, 2012; * 0PT-15.6, Standby Gas Treatment Operability Test, Unit 1 B after relay replacement on August 15, 2012; * 0PT-10.1.1, Reactor Core Isolation Cooling System Operability Test, Unit 2 after replacement of Electronic Governor - Magnetic (EGM) on August 23, 2012; and * 0PT-80.5, Reactor Pressure Vessel Pressure Test - Unit 1 after repair of 1B recirculation pump seal on September 26, 2012
      CAP. The inspectors evaluated the licensees operability determinations and performed
These activities were selected based upon the structure, system, or component's ability
      walk-downs with licensee staff of applicable fire areas as needed. The inspectors
to impact risk.  The inspectors evaluated these activities for the following, as applicable:
      followed the licensees actions to restore the wiring to its proper configuration and also
the effect of testing on the plant had been adequately addressed; testing was adequate
      verified the extent of condition inspections for the remaining EDGs 1, 3 and 4 were
for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing, and test documentation was properly
      completed in a timely manner. The inspectors reviewed the licensees reportability
evaluated. The inspectors evaluated the activities against the UFSAR and TS to ensure
      evaluation and subsequent 8-hour report made to the NRC in accordance with 10 CFR
that the test results adequately ensured that the equipment met the licensing basis and
      50.72(b)(3)(ii)(B). Additional documents reviewed are listed in the Attachment.
design requirements.  In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being
corrected commensurate with their importance to safety.  
  b. Findings
  No findings were identified.
1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)
Other Outage Activities
    a. Inspection Scope
  The inspectors evaluated licensee outage activities for an unscheduled forced outage to
replace the 1B recirculation pump seal assembly.  During the outage, the licensee made the decision to replace the 1A recirculation pump seal assembly to address the potential extent of cause/condition.  The outage began on September 16, 2012 and concluded on
September 28, 2012. The inspectors reviewed activities to ensure that the licensee
considered risk in developing, planning, and implementing the outage schedule.
Additionally, the inspectors observed or reviewed the reactor shutdown and cool down,
outage equipment configuration and risk management, electrical lineups, control and
monitoring of decay heat removal, control of containment activities, performed a drywell close out inspection, observed reactor startup and heat up activities, and identification and resolution of problems associated with the outage. Documents reviewed are listed  
in the Attachment.
14 
   b. Findings
   b. Findings
  Introduction:  The inspectors identified a Green NCV of TS 3.6.4.1, Secondary Containment because the licensee did not maintain secondary containment operable as
required during an activity considered an operation with a potential for draining the
reactor vessel (OPDRV).
Description:  On September 19, 2012, the licensee was replacing the 1B recirculation
pump seal assembly while Unit 1 was in Mode 4 (cold shutdown).  In an effort to properly isolate the work area, the recirculation suction and discharge isolation valves were
tagged closed.  Due to seat leakage across the isolation valves, the 1B recirculation pump drain valve was uncapped and opened to maintain the pump body partially empty to prevent water from impacting the work area while the pump seal was removed.  The
pump drain leakage was sent to the drywell floor drain system.  The 1B recirculation
pump seal replacement activity had the potential to drain the reactor vessel below the
top of the fuel because the recirculation loops penetrate the reactor vessel below the top
of active fuel.  An OPDRV is described in the licensee's technical specifications as an operation with a potential for draining the reactor vessel.  However, the licensee did not recognize or consider this activity as an OPDRV due to inadequate procedural guidance
that was used to exclude this activity as an OPDRV.  Specifically, the licensee adopted the definition of an OPDRV in procedure 0OI-01.01 as provided in Enforcement


Guidance Memorandum (EGM) 11-003 as any activity that could potentially result in draining or siphoning the RPV water level below the top of the fuel, without taking credit for mitigating measures.  However, section 9.16.15.b.(2) of licensee procedure 0OI-
                                                22
01.01, BNP Conduct of Operations Supplement, stated leakage through mechanical
      Introduction: The inspectors opened an unresolved item (URI) for this issue of concern
joints (for example valve or flange packing leaks, seat leakage through an isolation
      to determine if a performance deficiency existed.
valve, flange leakage, etc) is not considered an OPDRV.  On September 19, 2012, the licensee relaxed Unit 1 secondary containment
      Description: A wiring discrepancy was identified during inspection of the EDG 2 ASSD
from 03:30 a.m. until 09:20 p.m. by opening the reactor building air lock doors on the 20-foot elevation to increase ventilation to the recirculation pump seal replacement work area in the Unit 1 drywell.  This resulted in Secondary Containment inoperability while Unit 1 was in Mode 4 during an OPRDV
      switch 2-DG-SS-A1. A contact in the circuit was determined to be bypassed that would
activity.  The inspectors questioned the licensee's Operations staff on the decision to
      have the potential to prevent proper isolation of the EDG2 control circuits from the Main
make secondary containment inoperable during an OPDRV activity.  Following this, the licensee restored secondary containment, developed an Operation standing instruction 12-052 to treat this activity as an OPDRV and placed this issue into its CAP as AR
      Control Room (MCR) during an Appendix R fire event. The inspectors plan to review the
 
      licensees cause evaluation for this event and determine if a performance deficiency
562188. Analysis:  The inspectors determined that the failure to maintain secondary containment operable while Unit 1 was in Mode 4 with an OPDRV in progress was a performance deficiency. The performance deficiency was more than minor because it was associated
      existed. This issue is being tracked as URI 05000325; 324/2012004-03, EDG2 wiring on
with the configuration control attribute of the Barrier Integrity Cornerstone, and adversely
      ASSD switch.
affected the cornerstone objective to provide reasonable assurance that physical design
4OA3 Follow-up of Events (71153 - 2 samples)
barriers (fuel cladding, reactor coolant system, and containment) protect the public from radionuclide releases caused by accidents or events because the Unit 1 secondary containment boundary was not preserved or maintained. The inspectors evaluated the
.1    Notice of Unusual Event for Fire in the Protected Area
finding using Inspection Manual Chapter (IMC) 0609, Attachment 4, Phase 1 - Initial
Screening and Characterization of Findings, which required an analysis using IMC 0609
Appendix G since the reactor was in Mode 4 (cold shutdown).  The finding was determined to be of very low safety significance (Green) according to IMC 0609 
15  Appendix G, Attachment 1, Checklist 6, since a quantitative assessment (Phase 2 or Phase 3 evaluation) was not required.  Specifically, the inspectors determined that the licensee maintained adequate mitigation capability for reactor vessel water level
inventory and an event did not occur that could be characterized as a loss of control. 
The cause of this finding was directly related to the cross-cutting aspect of Accurate
Procedures in the Resources component of the Human Performance area, because the  
licensee did not consider the recirculation pump seal replacement activity to be OPDRV based on procedural guidance that contains exclusions to what are considered OPDRV activities. [H.2(c)]
 
Enforcement:  Unit 1 TS 3.6.4.1, Secondary Containment, required secondary containment to be operable during modes one, two, three, during movement of recently irradiated fuel assemblies in the secondary containment and during operations with a potential for draining the reactor vessel (OPD
RVs). Contrary to the above, on September 19, 2012, Unit 1 secondary containment was not maintained operable during
an OPDRV activity.  The licensee entered this issue in its CAP as AR 562188, and  
restored secondary containment during the OPDRV activity. Because the licensee entered the issue into its CAP and the finding is of very low safety significance (Green), this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC's
Enforcement Policy:  NCV 05000325/2012004-01, Failure to Maintain Secondary
Containment Operable during an OPDRV activity. 1R22 Surveillance Testing
 
.1 Routine Surveillance Testing (71111.22 - 4 samples)  
   a. Inspection Scope
   a. Inspection Scope
  The inspectors either observed surveillance tests or reviewed the test results for the
      For the plant event listed below, the inspectors reviewed plant parameters, reviewed
following activities to verify the tests met TS surveillance requirements, UFSAR
      personnel performance, and evaluated performance of mitigating systems. The
commitments, in-service testing requirements, and licensee procedural requirements. The inspectors assessed the effectiveness of the tests in demonstrating that the SSCs
      inspectors communicated the plant events to appropriate regional NRC personnel, and
were operationally capable of performing their intended safety functions.  
      compared the event details with criteria contained in IMC 0309, Reactive Inspection
 
      Decision Basis for Reactors, for consideration of potential reactive inspection activities.
* 0PT-07.2.4A, Core Spray System Operability Test - Loop A on July 5, 2012; * 0MST-RHR21Q, RHR-LPCI, CSS and HPCI Hi Drywell Pressure Trip Unit Inst Chan
      As applicable, the inspectors verified that the licensee made appropriate emergency
Cal on July 10, 2012; * 0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional on July 24, 2012; and * 0PT-12.12D, No. 4 Diesel Generator Monthly Load Test on August 17, 2012;
      classification assessments and properly reported the event in accordance with 10 CFR
 
      50.72. The inspectors reviewed the licensees follow-up actions related to the events to
    b. Findings
      assure that the licensee implemented appropriate corrective actions commensurate with
  No findings were identified.
      their safety significance.
 
      *    On August 2, 2012, a fire existed in the protected area on the Units 1 and 2 turbine
          building roof for approximately two hours, meeting the criteria for a Notice of Unusual
 
          Event declaration.
16 
  b. Findings
.2 In-Service Testing (IST) Surveillance (71111.22 - 1 sample)
      One licensee identified violation is documented in Section 4OA7 of this report.
    a. Inspection Scope
.2    (Closed) LER 05000325/2012-004-00, High Pressure Coolant Injection (HPCI)
  The inspectors reviewed the performance of Unit 1 LPCI/RHR System Operability Test - Loop B on August 9, 2012 to evaluate the effectiveness of the licensee's American
      Inoperable Due to Erratic Governor Operation
Society of Mechanical Engineers (ASME) Section XI testing program for determining equipment availability and reliability. The inspectors evaluated selected portions of the following areas: 1) testing procedures, 2) acceptance criteria, 3) testing methods, 4)
compliance with the licensee's IST program, TS, selected licensee commitments, and  
code requirements, 5) range and accuracy of test instruments, and 6) required corrective actions.     b. Findings
  No findings were identified.  
.3 Reactor Coolant System Leak Detection Inspection Surveillance (71111.22 - 1 sample)  
   a. Inspection Scope
   a. Inspection Scope
  The inspectors observed and reviewed the test results for a reactor coolant system leak detection surveillance, 0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure
      On May 2, 2012, Unit 1 HPCI was declared inoperable due to erratic governor operation
Vessel Pressure Test
      during Surveillance Test 0PT-09.2, HPCI System Operability Test. The erratic governor
, on September 28, 2012
      operation was due to the failure of the Ramp Generator Signal Convertor (RGSC). The
. The inspectors observed in-plant activities and reviewed procedures and associated records to determine whether: 
      licensee determined that the root cause of the RGSC failure was due to a lack of a
effects of the testing were adequately addressed by control room personnel or engineers
      replacement preventative maintenance (PM) for the RGSC, which had been installed for
prior to the commencement of the testing; acceptance criteria were clearly stated,
      at least 22 years. The corrective actions included replacing the RGSC and creating a
demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; and the calibration frequency was in accordance with TSs, the UFSAR, procedures, and
      PM task to replace the RGSCs. The licensee documented the root cause evaluation in
applicable commitments; applicable prerequisites described in the test procedures were
satisfied; test frequencies met TS requirements to demonstrate operability and reliability;
tests were performed in accordance with the test procedures and other applicable
procedures; and test data and results were accurate, complete, within limits, and valid. Inspectors verified that test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared
inoperable; equipment was returned to a position or status required to support the  
performance of its safety functions; and all problems identified during the testing were
appropriately documented and dispositioned in the corrective action program.
    b. Findings
  No findings were identified.


                                                23
 
      NCR 534364. The inspectors reviewed the LER, the NCR, and corrective actions to
 
      determine whether the station adequately evaluated the condition.
17 
1EP6 Emergency Planning Drill Evaluation (71114.06 - 2 samples)
    a. Inspection Scope
  The inspectors observed site emergency preparedness training drill/simulator scenarios
conducted on July 9, 2012 and July 25, 2012.  The inspectors reviewed the drill scenario
narrative to identify the timing and location of classifications, notifications, and protective action recommendations development activities.  During the drill, the inspectors assessed the adequacy of event classification and notification activities.  The inspectors
observed portions of the licensee's post-drill.  The inspectors verified that the licensee
properly evaluated the drill's performance with respect to performance indicators and
assessed drill performance with respect to drill objectives.
    b. Findings
  No findings were identified.
 
4. OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification (71151 - 6 samples)
.1 Mitigating Systems Cornerstone
    a. Inspection Scope
  * Mitigating Systems Performance Index, Residual Heat Removal - Unit 1 * Mitigating Systems Performance Index, Residual Heat Removal - Unit 2
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) performance indicators listed above for the period from the third (3
rd) quarter 2011 through the second (2
nd) quarter 2012.  The inspectors reviewed the licensee's operator narrative logs, issue reports, MSPI derivation reports, event reports and NRC Integrated Inspection reports for the
period to validate the accuracy of the submittals. 
    b.  Findings
  No findings were identified.
.2 Barrier Integrity Cornerstone
 
  a. Inspection Scope
  * Reactor Coolant System (RCS) Specific Activity - Unit 1
* Reactor Coolant System (RCS) Specific Activity - Unit 2
The inspectors reviewed licensee submittals for the Reactor Coolant System Specific Activity performance indicator for the period from the third (3
rd) quarter 2011 through the
second (2 nd) quarter 2012.  The inspectors reviewed the licensee's RCS chemistry 
18  samples, TS requirements, issue reports, and event reports for the period to validate the accuracy of the submittals.  In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample.
* Reactor Coolant System Leakage - Unit 1
* Reactor Coolant System Leakage - Unit 2
The inspectors sampled licensee submittals for the Reactor Coolant System Leakage performance indicator for the period from the third (3
rd) quarter 2011 through the second
(2 nd) quarter 2012.
  The inspectors reviewed the licensee's operator logs, RCS leakage tracking data, issue reports, and event reports for the period to validate the accuracy of
the submittals.
    b. Findings
  No findings were identified.
4OA2 Identification and Resolution of Problems (71152 - 2 samples)
.1 Routine Review of Items Entered Into the Corrective Action Program
 
  a. Inspection Scope
  To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into
the licensee's corrective action program.  The review was accomplished by reviewing daily action request reports.
    b. Findings
  No findings were identified.
.2 Assessments and Observations
  Selected Issue Follow-up Inspection
: UPS-A Failure and Loss of Emergency Response Facility Information System (ERFIS), Plant Process Computer (PPC), Business Network
  a. Inspection Scope
  The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business Network, for detailed review.  This AR identified that a single failure caused the loss of
ERFIS and Safety Parameter Display System (SPDS) on both units.  The inspectors
reviewed the licensee's CAP for ERFIS and SPDS failures in the past.  The inspectors
reviewed these reports to verify that the licensee identified the full extent of the issue, performed an appropriate evaluation, and specified and prioritized appropriate corrective actions.  The inspectors evaluated the reports against the requirements of the licensee's CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action
Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.
 
19 
   b. Findings
   b. Findings
  No findings were identified
      One licensee identified violation is documented in Section 4OA7 of this report. This LER
 
      is closed.
    a. Inspection Scope
4OA5 Other Activities
  The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business Network, for detailed review.  This AR identified that a single failure caused the loss of ERFIS and Safety Parameter Display System (SPDS) on both units.  The inspectors
.1   (Discussed) NRC Temporary Instruction (TI) 2515/187, Inspection of Near-Term Task
reviewed the licensee's CAP for ERFIS and SPDS failures in the past.  The inspectors
      Force Recommendation 2.3 Flooding Walk-downs, and NRC TI 2515/188, Inspection of
reviewed these reports to verify that the licensee identified the full extent of the issue, performed an appropriate evaluation, and specified and prioritized appropriate corrective actions.  The inspectors evaluated the reports against the requirements of the licensee's CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action
      Near-Term Task Force Recommendation 2.3 Seismic Walk-downs
Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.
        b. Findings
 
Introduction:  A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the licensee's failure to properly evaluate or consider the impact to emergency response facilities of design change ESR98-00436 which was implemented in 1999.  As a result, 
a number of temporary losses of ERFIS, Emergency Response Data System (ERDS),
SPDS, and all displays including radiation monitors for the emergency response facilities
occurred.  Specifically, the licensee failed to ensure that adequate emergency response facilities and equipment were available as required by the Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8). 
This issue was captured in the licensee's CAP as AR 542704.
Description:  In 1999, the licensee implemented design change ESR98-00436 for the power supply to the ERFIS, ERDS, SPDS, and all displays including RMS for the emergency response facilities.  The licensee did not properly evaluate or consider the impact to emergency response facilities and equipment prior to implementation of this design change.  As a result, the ERFIS, ERDS, and SPDS systems, and all radiation
 
monitoring system (RMS) displays were susceptible to a single point power failure mode.  The implementation of the design change introduced a single point failure mode which did not meet the design requirements specified in their Design Basis Document (DBD 60) sections 3.6.7.2 and 3.6.7.3.  Prior to the licensee's implementation of design
change ESR98-00436 in 1999, this single point vulnerability did not exist as the power
supply system had automatic switching capability on loss of one power source.  When the design change was implemented, the ERFIS, ERDS, and SPDS systems and RMS
 
displays were degraded as demonstrated by the resulting failures of those systems on multiple occasions including July 17, 2004 and June 12, 2012.  Additionally, all displays for those systems were lost in all of the emergency facilities including the radiation
monitoring system. 
 
 
20  On June 13, 2012, the licensee made an ev
ent notification to the NRC Operations
Center, 50.72(b)(3)(xiii) Loss of Emergency Assessment Capability, Offsite Response Capability, or Offsite Communications Capability for the emergency response facilities.
The report delineated that at 5:57 p.m. EDT on June 12, 2012, Brunswick Nuclear Plant
experienced a fault on the Emergency Response Facility Information System (ERFIS)
uninterruptible power supply (UPS) electrical bus 'A'. This resulted in a loss of site
Safety Parameter Display System (SPDS), Emergency Response Data System (ERDS)
and Plant Process Computer (PPC) for both Unit 1 and Unit 2.
During the loss of SPDS, the emergency response capability of that system was lost to
the site.  During the loss of ERDS, the automatic data transfer feature of that system
was lost for transmissions to the NRC, however manual data transfer was still available. During the loss of the PPC, automatic core thermal power averaging and automatic core
thermal limit monitoring was lost. Manual calculations were available for these functions. Unit 1 SPDS was restored to the Emergency Operations Facility (EOF) at 7:49 p.m. on
June 12, 2012. Unit 2 SPDS was restored to the EOF at 8:30 p.m. on June 12, 2012. 
The inverter was restored to service on June 17, 2012 at 12:00 noon.
  Inspectors determined that the licensee did not properly evaluate or consider the impact to all emergency response facilities and equipment prior to implementation of the
ESR98-00436 design change.  The inspectors concluded that the ERFIS, ERDS, and
SPDS systems required by the Brunswick Nuclear Plant Radiological Emergency Plan
were degraded from 1999 when the design change was installed to present.  Compensatory measures were put in place during the June 2012 event to manually obtain and log the required data from the instrumentation in the control room and
transmit to the emergency response facilities, and after the June 2012 event, the
licensee initiated a design change to restore the power configuration to those systems
back to the original design which would remove this failure mechanism.
Analysis:  The licensee's failure to properly evaluate or consider the impact to emergency response facilities of design change ESR98-00436 which was implemented in 1999 was a performance deficiency.  Specifically, the licensee introduced a single point failure mode which did not meet the design requirements specified in their Design
Basis Document (DBD 60) sections 3.6.7.2 and 3.6.7.3.  This resulted in the licensee's failure to ensure that adequate emergency response facilities and equipment were available as delineated in the Updated Final Safety Analysis Report (UFSAR) Section 7.7.1.9, and required by the Brunswick Nuclear Plant Radiological Emergency Plan,
Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).
The finding was more than minor because it adversely affected the Emergency Preparedness Cornerstone objective of ensuring that the licensee was capable of
implementing adequate measures to protect the health and safety of the public in the
event of a radiological emergency.  Specifically, the Facilities and Equipment attribute was affected during the time when the ERFIS, ERDS, SPDS, and all displays including
radiation monitors for the emergency response facilities were degraded, and as a result
did not meet 10 CFR 50.47(b)(8) Planning Standard program element, adequate emergency facilities and equipment to support the emergency response are provided
and maintained.  The finding was assessed for significance in accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance Determination Process. 
21  Attachment 2 of Appendix B, Failure to Comply Significance Logic is as follows:  Failure to comply; Loss of Risk Significant Planning Standard Function (RSPS), No; RSPS Degraded Function, No; Loss of Planning Standard Function, No; the result is a Green
finding.  The inspectors determined that this resulted in a low safety significance finding
(Green).  No cross-cutting aspect was assigned to this finding because the performance
deficiency occurred more than three years ago and is not reflective of current plant
 
performance.
Enforcement:  10 CFR 50.54(q)(2) requires, in part, a licensee to follow and maintain the
effectiveness of an emergency plan that meets the requirements in Appendix E to this part and, for nuclear power reactor licensee, the planning standards of 10 CFR 50.47(b).
The Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3, revision 80, states in part that special provisions have been made to assure that ample space and proper equipment are available to effectively respond to a full range of possible
 
emergencies.  Contrary to the above, from 1999, when design change ESR98-00436 was installed, until the compensatory measures were put in place in June 2012, the
licensee failed to maintain adequate emergency facilities and equipment to support emergency response when the ERFIS, ERDS, SPDS, and all displays including radiation monitors for the emergency response facilities were degraded due to the implementation
of the design change.  This resulted in failures of those systems on July 17, 2004 and
June 12, 2012.  The licensee has compensatory measures in place, entered this issue
their CAP as AR 542704, and initiated a design change to restore the power
configuration back to the original design.  Because the licensee entered the issue into its CAP and the finding is of very low safety significance (Green), this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC's Enforcement Policy:  NCV
05000325; 324/2012004-02, Failure to Maintain Reliability and Availability of Emergency
Response Equipment for Emergency Response Facilities.
 
.3 Assessments and Observations
  Selected Issue Follow-up Inspection:  EDG 2 wiring associated with Alternate Safe Shutdown (ASSD) Switch 2-DG-SS-A1
  a. Inspection Scope
  The inspectors performed a detailed review of AR 557897 associated with the wiring for
the EDG 2 Alternate Safe Shutdown (ASSD) Switch 2-DG-SS-A1. The issue was
discovered during a planned system outage for EDG2 during the week of August 26. 
The inspectors verified that the issue was captured completely and accurately in the CAP.  The inspectors evaluated the licensee's operability determinations and performed walk-downs with licensee staff of applicable fire areas as needed.  The inspectors
followed the licensee's actions to restore the wiring to its proper configuration and also
verified the extent of condition inspections for the remaining EDGs 1, 3 and 4 were
completed in a timely manner.  The inspectors reviewed the licensee's reportability
evaluation and subsequent 8-hour report made to the NRC in accordance with 10 CFR 50.72(b)(3)(ii)(B).  Additional documents reviewed are listed in the Attachment.
    b. Findings
 
22  Introduction:  The inspectors opened an unresolved item (URI) for this issue of concern to determine if a performance deficiency existed. 
Description:  A wiring discrepancy was identified during inspection of the EDG 2 ASSD switch 2-DG-SS-A1.  A contact in the circuit was determined to be bypassed that would
have the potential to prevent proper isolation of the EDG2 control circuits from the Main
Control Room (MCR) during an Appendix R fire event.  The inspectors plan to review the licensee's cause evaluation for this event and determine if a performance deficiency existed.  This issue is being tracked as URI 05000325; 324/2012004-03, EDG2 wiring on
ASSD switch.
4OA3  Follow-up of Events (71153 - 2 samples)
.1 Notice of Unusual Event for Fire in the Protected Area
 
   a. Inspection Scope
   a. Inspection Scope
  For the plant event listed below, the inspectors reviewed plant parameters, reviewed personnel performance, and evaluated performance of mitigating systems.  The
      Inspectors accompanied the licensee on a sampling basis, during their flooding and
inspectors communicated the plant events to appropriate regional NRC personnel, and compared the event details with criteria contained in IMC 0309, "Reactive Inspection
      seismic walk-downs, to verify that the licensees walk-down activities were conducted
Decision Basis for Reactors," for consideration of potential reactive inspection activities
      using the methodology endorsed by the NRC. These walk-downs are being performed at
As applicable, the inspectors verified that the licensee made appropriate emergency classification assessments and properly r
      all sites in response to a letter from the NRC to licensees, entitled Request for
eported the event in accordance with 10 CFR 50.72.  The inspectors reviewed the licensee's follow-up actions related to the events to assure that the licensee implemented appropriate corrective actions commensurate with
      Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Regarding
their safety significance.  
      Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights
* On August 2, 2012, a fire existed in the protected area on the Units 1 and 2 turbine building roof for approximately two hours, meeting the criteria for a Notice of Unusual Event declaration.
      from the Fukushima Dai-Ichi Accident, dated March 12, 2012 (ADAMS Accession No.
      ML12053A340).
  b. Findings
      Enclosure 3 of the March 12, 2012, letter requested licensees to perform seismic walk-
  One licensee identified violation is documented in Section 4OA7 of this report. 
      downs using an NRC-endorsed walk-down methodology. Electric Power Research
      Institute (EPRI) document 1025286 titled, Seismic Walk-down Guidance, (ADAMS
.2  (Closed) LER 05000325/2012-004-00, High Pressure Coolant Injection (HPCI)
      Accession No. ML12188A031) provided the NRC-endorsed methodology for performing
Inoperable Due to Erratic Governor Operation
      seismic walk-downs to verify that plant features, credited in the current licensing basis
    a. Inspection Scope
      (CLB) for seismic events, are available, functional, and properly maintained.
 
      Enclosure 4 of the letter requested licensees to perform external flooding walk-downs
On May 2, 2012, Unit 1 HPCI was declared inoperable due to erratic governor operation
      using an NRC-endorsed walk-down methodology (ADAMS Accession No.
during Surveillance Test 0PT-09.2, HPCI Syst
      ML12056A050). Nuclear Energy Industry (NEI) document 12-07 titled, Guidelines for
em Operability Test. The erratic governor operation was due to the failure of the Ramp Generator Signal Convertor (RGSC). The
      Performing Verification Walk-downs of Plant Protection Features, (ADAMS Accession
licensee determined that the root cause of the RGSC failure was due to a lack of a
      No. ML12173A215) provided the NRC-endorsed methodology for assessing external
replacement preventative maintenance (PM) for the RGSC, which had been installed for at least 22 years. The corrective actions included replacing the RGSC and creating a PM task to replace the RGSCs.  The licensee documented the root cause evaluation in 
      flood protection and mitigation capabilities to verify that plant features, credited in the
23  NCR 534364.  The inspectors reviewed the LER, the NCR, and corrective actions to determine whether the station adequately evaluated the condition.  
      CLB for protection and mitigation from external flood events, are available, functional,
 
      and properly maintained.
   b. Findings
   b. Findings
  One licensee identified violation is documented in Section 4OA7 of this report.  This LER is closed.
      Findings or violations associated with the flooding and seismic walk-downs, if any, will
4OA5 Other Activities
      be documented in future reports.
 
.1 (Discussed) NRC Temporary Instruction (TI) 2515/187, Inspection of Near-Term Task Force Recommendation 2.3 Flooding Walk-downs, and NRC TI 2515/188, Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walk-downs
 
  a. Inspection Scope
  Inspectors accompanied the licensee on a sampling basis, during their flooding and seismic walk-downs, to verify that the licensee's walk-down activities were conducted using the methodology endorsed by the NRC. T
hese walk-downs are being performed at all sites in response to a letter from t
he NRC to licensees, entitled "Request for Information Pursuant to Title 10 of the
Code of Federal Regulations 50.54(f) Regarding Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights from the Fukushima Dai-Ichi Accident," dated March 12, 2012 (ADAMS Accession No. ML12053A340).  


                                              24
Enclosure 3 of the March 12, 2012, letter requested licensees to perform seismic walk-
.2   (Discussed) Temporary Instruction (TI) 2515/182 - Review of the Implementation of the
downs using an NRC-endorsed walk-down methodology.  Electric Power Research Institute (EPRI) document 1025286 titled, "Seismic Walk-down Guidance," (ADAMS
      Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1
Accession No. ML12188A031) provided t
he NRC-endorsed methodology for performing seismic walk-downs to verify that plant features, credited in the current licensing basis
(CLB) for seismic events, are available, functional, and properly maintained. 
 
Enclosure 4 of the letter requested licensees to perform external flooding walk-downs using an NRC-endorsed walk-down methodology (ADAMS Accession No. ML12056A050).  Nuclear Energy Industry (NEI) document 12-07 titled, "Guidelines for
Performing Verification Walk-downs of Plant Protection Features," (ADAMS Accession
No. ML12173A215) provided the NRC-endors
ed methodology for assessing external flood protection and mitigation capabilities to verify that plant features, credited in the CLB for protection and mitigation from external flood events, are available, functional, and properly maintained.
  b. Findings
  Findings or violations associated with the flooding and seismic walk-downs, if any, will be documented in future reports.
   
24
 
.2 (Discussed) Temporary Instruction (TI) 2515/182 - Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1
 
   a. Inspection Scope
   a. Inspection Scope
  Leakage from buried and underground pipes has resulted in ground water contamination  
      Leakage from buried and underground pipes has resulted in ground water contamination
incidents with associated heightened NRC and public interest. The industry issued a guidance document, Nuclear Energy Institute (NEI) 09-14, "Guideline for the  
      incidents with associated heightened NRC and public interest. The industry issued a
Management of Buried Piping Integrity," (ADAMS Accession No. ML 1030901420), to describe the goals and required actions (commitments made by the licensee) resulting from this underground piping and tank initiative. On December 31, 2010, NEI issued  
      guidance document, Nuclear Energy Institute (NEI) 09-14, Guideline for the
Revision 1 to NEI 09-14, "Guidance for the Management of Underground Piping and  
      Management of Buried Piping Integrity, (ADAMS Accession No. ML 1030901420), to
Tank Integrity," (ADAMS Accession No. ML 110700122), with an expanded scope of  
      describe the goals and required actions (commitments made by the licensee) resulting
components which included underground piping that was not in direct contact with the soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182, "Review of the Industry Initiative to
      from this underground piping and tank initiative. On December 31, 2010, NEI issued
Control Degradation of Underground Piping and Tanks," to gather information related to the industry's implementation of this initiative.
      Revision 1 to NEI 09-14, Guidance for the Management of Underground Piping and
The instructors reviewed the licensee's programs for buried pipe and underground piping  
      Tank Integrity, (ADAMS Accession No. ML 110700122), with an expanded scope of
and tanks in accordance with TI-2515/182 to determine if the program attributes and  
      components which included underground piping that was not in direct contact with the
completion dates identified in Section 3.3 A and 3.3 B of NEI 09-14, Revision 1, were contained in the licensee's program and implementing procedures. For the buried pipe and underground piping program attributes, with completion dates that had passed, the  
      soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182,
inspectors reviewed records to determine if the attribute was in fact complete and to  
      Review of the Industry Initiative to Control Degradation of Underground Piping and
determine if the attribute was accomplished in a manner which reflected good or poor  
      Tanks, to gather information related to the industrys implementation of this initiative.
practices in management.  
      The instructors reviewed the licensees programs for buried pipe and underground piping
    b. Observations
      and tanks in accordance with TI-2515/182 to determine if the program attributes and
 
      completion dates identified in Section 3.3 A and 3.3 B of NEI 09-14, Revision 1, were
The licensee's buried piping and underground piping and tanks program was inspected in accordance with paragraphs 03.01.a through 03.01.c of TI-2515/182 and was found to  
      contained in the licensees program and implementing procedures. For the buried pipe
meet all applicable aspects of NEI 09-14 Revision 1, as set forth in Table 1 of the TI.  
      and underground piping program attributes, with completion dates that had passed, the
  Based upon the scope of the review described above, Phase I of TI-2515/182 was  
      inspectors reviewed records to determine if the attribute was in fact complete and to
completed.  
      determine if the attribute was accomplished in a manner which reflected good or poor
      practices in management.
  b. Observations
      The licensees buried piping and underground piping and tanks program was inspected
      in accordance with paragraphs 03.01.a through 03.01.c of TI-2515/182 and was found to
      meet all applicable aspects of NEI 09-14 Revision 1, as set forth in Table 1 of the TI.
      Based upon the scope of the review described above, Phase I of TI-2515/182 was
      completed.
   c. Findings
   c. Findings
  No findings were identified.  
      No findings were identified.
4OA6 Management Meetings
4OA6 Management Meetings
 
      Exit Meeting Summary
Exit Meeting Summary
      On July 19, 2012, the inspectors presented inspection results of the triennial heat sink
  On July 19, 2012, the inspectors presented inspection results of the triennial heat sink  
      inspection to Mr. Michael Annacone and other members of the licensee staff. The
inspection to Mr. Michael Annacone and other members of the licensee staff. The 
25  inspectors confirmed that none of the potential report input discussed was considered
proprietary.
On September 18, 2012, the inspector presented inspection results of the TI-182, Phase
1 of the Underground Piping and Tanks Inspection by conference call to Mr. James
Burke, Site Director of Engineering, and other members of the licensee staff. The
inspector verified that all proprietary information was returned to the licensee.
On October 11, 2012, the inspectors presented inspection results from the quarterly
inspection to Mr. Annacone and other members of the licensee staff.  The inspectors
confirmed that any proprietary information received during the inspection period were
properly controlled or returned to licensee staff.
4OA7 Licensee-Identified Violations
  The following violations of very low significance (Green) were identified by the licensee
and are violations of NRC requirements which meet the criteria of the NRC Enforcement Policy, for being dispositioned as NCVs.
* 10 CFR 50.54(q) requires, in part, a licensee authorized to possess and operate a nuclear power reactor shall follow and maintain in effect emergency plans which meet the standards of 10 CFR 50.47(b).  Title 10 CFR 50.47(b)(4)
requires, in part, a standard emergency classification and action level scheme be used by the licensee.  Procedure 0PEP-02.1.1, Emergency Control - Notification
of Unusual Event, Alert, Site Area Emergency, and General Emergency, Step 5.7.2 states, that the emergency declaration will be made within 15 minutes after the availability of indications to plant operators that an emergency action level
has been exceeded.  Procedure 0PEP-02.1, Initial Emergency Actions, HU2.1,
requires the declaration of an Unusual Event when a fire is not extinguished
within 15 minutes of control room notification or verification of a control room fire alarm in any Table H-1 or Table H-3 areas.  Table H-1 includes the turbine building.  Contrary to the above, on August 2, 2012, a Notice of Unusual Event
(NOUE) was not classified within 15 minutes of a fire within the protected area
not being extinguished within 15 minutes of detection.  Specifically, when a fire
was reported on the Turbine Building roof to the Control Room and was not
extinguished within 15 minutes, conditions were met for classification of EAL HU2.1 in accordance with
Procedure 0PEP-02.1;
however, the EAL was not classified until approximately eight hours after the fire started.  This issue was
entered into the licensee's CAP as NCR 552984 and the licensee is performing a
root cause evaluation.
  Corrective actions included making a one hour report to the NRC for discovery of a condition that met the EAL classification for an NOUE after the fact.  The inspectors determined the finding was associated with an actual event implementation problem, and assessed the significance using IMC
0609, Appendix B, "Emergency Preparedness Significance Determination
Process." Using the Emergency Preparedness SDP, Sheet 1, "Failure to
Implement (Actual Event) Significance Logic" the inspectors determined the finding was of very low safety significance (Green) because the licensee failed to implement a risk significant planning standard (10 CFR 50.47(b)(4)) during an


actual Notice of Unusual Event.  
                                                25
26 
    inspectors confirmed that none of the potential report input discussed was considered
* 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," requires that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or
    proprietary.
drawings. Licensee procedure ADM-NGGC-0107, Equipment Reliability Process
    On September 18, 2012, the inspector presented inspection results of the TI-182, Phase
Guideline, steps 9.4.9 and 9.4.10 req
    1 of the Underground Piping and Tanks Inspection by conference call to Mr. James
uired component experts and preventive maintenance (PM) optimization to determine if there was a cost effective PM to prevent failure and then to develop the PM model. Contrary to the above, the Unit 1 high pressure coolant injection (HPCI) ramp generator signal converter (RGSC) did not have the appropriate preventive maintenance to prevent failure. As a result, the Unit 1 high pressure coolant injection (HPCI) system failed the HPCI System Operability Test performed on April 30, 2012 and was declared
    Burke, Site Director of Engineering, and other members of the licensee staff. The
inoperable. The licensee entered this issue into the CAP as NCR 534364. Corrective actions included replacing the RGSC and creating a PM task to replace the RGSCs on a specified frequency.  Using IMC 0609, Appendix A,
    inspector verified that all proprietary information was returned to the licensee.
"Phase 1 Initial Screening and Characterization of Findings," the inspectors
    On October 11, 2012, the inspectors presented inspection results from the quarterly
determined this finding required a Phase 2 analysis.  The Phase 1 screened this
    inspection to Mr. Annacone and other members of the licensee staff. The inspectors
Mitigating Systems Cornerstone finding to Phase 2 because the finding represented a loss of HPCI system and/or function. The inspectors, with the assistance of the regional Senior Risk Analyst, performed a Phase 2 analysis
    confirmed that any proprietary information received during the inspection period were
using the Saphire 8 Model.  109 hours of unavailability time was used for the
    properly controlled or returned to licensee staff.
analysis since HPCI was not required during the refueling outage from February
4OA7 Licensee-Identified Violations
23, 2012 through April 29, 2012. Based on the results of the Phase 2 analysis,  
    The following violations of very low significance (Green) were identified by the licensee
the inspectors determined the finding was of very low safety significance (Green).  
    and are violations of NRC requirements which meet the criteria of the NRC Enforcement
 
    Policy, for being dispositioned as NCVs.
ATTACHMENT:  SUPPLEMENTAL INFORMATION
    *      10 CFR 50.54(q) requires, in part, a licensee authorized to possess and operate
            a nuclear power reactor shall follow and maintain in effect emergency plans
            which meet the standards of 10 CFR 50.47(b). Title 10 CFR 50.47(b)(4)
            requires, in part, a standard emergency classification and action level scheme be
            used by the licensee. Procedure 0PEP-02.1.1, Emergency Control - Notification
            of Unusual Event, Alert, Site Area Emergency, and General Emergency, Step
            5.7.2 states, that the emergency declaration will be made within 15 minutes after
            the availability of indications to plant operators that an emergency action level
            has been exceeded. Procedure 0PEP-02.1, Initial Emergency Actions, HU2.1,
            requires the declaration of an Unusual Event when a fire is not extinguished
            within 15 minutes of control room notification or verification of a control room fire
            alarm in any Table H-1 or Table H-3 areas. Table H-1 includes the turbine
            building. Contrary to the above, on August 2, 2012, a Notice of Unusual Event
            (NOUE) was not classified within 15 minutes of a fire within the protected area
            not being extinguished within 15 minutes of detection. Specifically, when a fire
            was reported on the Turbine Building roof to the Control Room and was not
            extinguished within 15 minutes, conditions were met for classification of EAL
            HU2.1 in accordance with Procedure 0PEP-02.1; however, the EAL was not
            classified until approximately eight hours after the fire started. This issue was
            entered into the licensees CAP as NCR 552984 and the licensee is performing a
            root cause evaluation. Corrective actions included making a one hour report to
            the NRC for discovery of a condition that met the EAL classification for an NOUE
            after the fact. The inspectors determined the finding was associated with an
            actual event implementation problem, and assessed the significance using IMC
            0609, Appendix B, "Emergency Preparedness Significance Determination
            Process." Using the Emergency Preparedness SDP, Sheet 1, "Failure to
            Implement (Actual Event) Significance Logic" the inspectors determined the
            finding was of very low safety significance (Green) because the licensee failed to
            implement a risk significant planning standard (10 CFR 50.47(b)(4)) during an
            actual Notice of Unusual Event.


 
                                            26
Attachment SUPPLEMENTAL INFORMATION
    *    10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings,"
  KEY POINTS OF CONTACT
          requires that activities affecting quality shall be prescribed by documented
  Licensee Personnel
          instructions, procedures, or drawings, of a type appropriate to the circumstances
  M. Annacone, Site Vice President
          and shall be accomplished in accordance with these instructions, procedures, or
A. Brittain, Manager - Security
          drawings. Licensee procedure ADM-NGGC-0107, Equipment Reliability Process
J. Burke, Director - Site Engineering
          Guideline, steps 9.4.9 and 9.4.10 required component experts and preventive
K. Croker, Supervisor - Emergency Preparedness 
          maintenance (PM) optimization to determine if there was a cost effective PM to
          prevent failure and then to develop the PM model. Contrary to the above, the
          Unit 1 high pressure coolant injection (HPCI) ramp generator signal converter
          (RGSC) did not have the appropriate preventive maintenance to prevent failure.
          As a result, the Unit 1 high pressure coolant injection (HPCI) system failed the
          HPCI System Operability Test performed on April 30, 2012 and was declared
          inoperable. The licensee entered this issue into the CAP as NCR 534364.
          Corrective actions included replacing the RGSC and creating a PM task to
          replace the RGSCs on a specified frequency. Using IMC 0609, Appendix A,
          "Phase 1 Initial Screening and Characterization of Findings," the inspectors
          determined this finding required a Phase 2 analysis. The Phase 1 screened this
          Mitigating Systems Cornerstone finding to Phase 2 because the finding
          represented a loss of HPCI system and/or function. The inspectors, with the
          assistance of the regional Senior Risk Analyst, performed a Phase 2 analysis
          using the Saphire 8 Model. 109 hours of unavailability time was used for the
          analysis since HPCI was not required during the refueling outage from February
          23, 2012 through April 29, 2012. Based on the results of the Phase 2 analysis,
          the inspectors determined the finding was of very low safety significance (Green).
ATTACHMENT: SUPPLEMENTAL INFORMATION


C. Dunsmore, Manager - Shift Operations P. Dubrouillet, Manager - Training G. Galloway, Acting Manager, Nuclear Oversight  
                                SUPPLEMENTAL INFORMATION
C. George, Manager - BOP Systems  
                                  KEY POINTS OF CONTACT
S. Gordy, Manager - Maintenance
Licensee Personnel
L. Grzeck, Manager - Regulatory Affairs  
M. Annacone, Site Vice President
M. Hamm, Superintendent - Mechanical Maintenance F. Jefferson, Manager - Reactor Systems Engineering  
A. Brittain, Manager - Security
J. Kalamaja, Manager - Operations  
J. Burke, Director - Site Engineering
J. Krakuszeski, Plant General Manager  
K. Croker, Supervisor - Emergency Preparedness
 
C. Dunsmore, Manager - Shift Operations
R. Mosier, Communication Specialist  
P. Dubrouillet, Manager - Training
A. Padleckas, Superintendent - Nuclear Operations Performance D. Petrusic, Superintendent - Environmental and Chemistry A. Pope, Manager - Nuclear Support Services  
G. Galloway, Acting Manager, Nuclear Oversight
 
C. George, Manager - BOP Systems
J. Price, Manager- Design Engineering  
S. Gordy, Manager - Maintenance
 
L. Grzeck, Manager - Regulatory Affairs
W. Richardson, Engineering  
M. Hamm, Superintendent - Mechanical Maintenance
 
F. Jefferson, Manager - Reactor Systems Engineering
T. Roeder, Supervisor - Chemistry T. Sherrill, Licensing Senior Technical Specialist P. Smith, Superintendent - Electrical, Instrumentation, and Controls Maintenance  
J. Kalamaja, Manager - Operations
M. Talon, Buried Piping Program Manager  
J. Krakuszeski, Plant General Manager
J. Terrell, Corporate Buried Piping Program Manager  
R. Mosier, Communication Specialist
 
A. Padleckas, Superintendent - Nuclear Operations Performance
M. Turkal, Lead Engineer - Technical Support  
D. Petrusic, Superintendent - Environmental and Chemistry
J. Vincelli, Manager - Environmental and Radiological Controls B. Wilder, Engineering E. Wills, Director - Site Operations  
A. Pope, Manager - Nuclear Support Services
 
J. Price, Manager- Design Engineering
W. Richardson, Engineering
T. Roeder, Supervisor - Chemistry
T. Sherrill, Licensing Senior Technical Specialist
P. Smith, Superintendent - Electrical, Instrumentation, and Controls Maintenance
M. Talon, Buried Piping Program Manager
J. Terrell, Corporate Buried Piping Program Manager
M. Turkal, Lead Engineer - Technical Support
J. Vincelli, Manager - Environmental and Radiological Controls
B. Wilder, Engineering
E. Wills, Director - Site Operations
NRC Personnel
NRC Personnel
  R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects Region II  
R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects Region II
 
                                                                                    Attachment
Attachment LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
 
05000325/2012004-01
 
05000325;324/2012004-02 NCV  NCV Failure to Maintain Secondary Containment Operable During an OPDRV Activity. (Section 1R20) 
Failure to Maintain Reliability and Availability of
Emergency Response Equipment for Emergency
Response Facilities. (Section 4OA2.2)
Opened 
05000325;324/2012004-03


                  LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
    URI 
Opened and Closed
      
05000325/2012004-01          NCV  Failure to Maintain Secondary Containment Operable
EDG2 Wiring on ASSD Switch (Section 4OA2.3)  
                                  During an OPDRV Activity. (Section 1R20)
05000325;324/2012004-02     NCV  Failure to Maintain Reliability and Availability of
                                  Emergency Response Equipment for Emergency
                                  Response Facilities. (Section 4OA2.2)
Opened
05000325;324/2012004-03      URI  EDG2 Wiring on ASSD Switch (Section 4OA2.3)
Closed
05000325/2012-004-00          LER  High Pressure Coolant Injection (HPCI) Inoperable
                                  Due to Erratic Governor Operation (Section 4OA3.2)
Discussed
Temporary Instruction          TI  Inspection of Near-Term Task Force Recommendation
2515/187                          2.3 Flooding Walk-downs (Section 4OA5.1)
Temporary Instruction          TI  Inspection of Near-Term Task Force Recommendation
2515/188                          2.3 Seismic Walk-downs (Section 4OA5.1)
Temporary Instruction          TI  Review of the Implementation of the Industry Initiative
2515/182                          to Control Degradation of Underground Piping and
                                  Tanks, Phase 1 (Section 4OA5.2)
                                                                                    Attachment


     
                              LIST OF DOCUMENTS REVIEWED
       
Section 1R01: Adverse Weather Protection
Closed 
Procedures
05000325/2012-004-00
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake
  LER 
0PEP-02.6, Severe Weather
High Pressure Coolant Injection (HPCI) Inoperable
  2APP-UA-01, Annunciator Procedure for Panel UA-01
Due to Erratic Governor Operation (Section 4OA3.2)
2APP-UA-28, Annunciator Procedure for Panel UA-28
   
2OP-43, Service Water System Operating Procedure
 
OPS-NGGC-1305, Operability Determinations
Discussed      Temporary Instruction
2515/187 TI Inspection of Near-Term Task Force Recommendation 2.3 Flooding Walk-downs (Section 4OA5.1)
Temporary Instruction
 
2515/188 TI Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walk-downs (Section 4OA5.1)
 
Temporary Instruction
2515/182 TI Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1 (Section 4OA5.2) 
Attachment LIST OF DOCUMENTS REVIEWED  
Section 1R01: Adverse Weather Protection
  Procedures
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake  
0PEP-02.6, Severe Weather  
  2APP-UA-01, Annunciator Procedure for Panel UA-01 2APP-UA-28, Annunciator Procedure for Panel UA-28 2OP-43, Service Water System Operating Procedure  
 
OPS-NGGC-1305, Operability Determinations  
 
Nuclear Condition Reports
Nuclear Condition Reports
556860 556861 556862 556863 556864 556865  
556860         556861         556862       556863         556864       556865
556866 556867 556868 556869 556870 557375  
556866         556867         556868       556869         556870       557375
 
555023         545354         553946
555023 545354 553946  
 
Work Orders
Work Orders
550098 550100 550102 550015 545859 545861  
550098         550100         550102       550015         545859       545861
1828825 1828826 1643223 1775054
1828825       1828826       1643223       1775054
 
Drawings
D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2
Drawings D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2  
D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2
D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2 D-11597, Backdraft Damper with Extra Deep Frame F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping  
D-11597, Backdraft Damper with Extra Deep Frame
LL-FB-02103, Reactor Building, Elevation -17'0", Fire Barrier Penetrations, RHR-HPCI Room  
F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping
North Wall  
LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room
Miscellaneous  
        North Wall
0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator DBD-106, Hazards Analysis  
Miscellaneous
Engineering Change 80408R0, Flooding Design Basis Update  
0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator
Individual Plant Examination for Exte
DBD-106, Hazards Analysis
rnal Events Submittal, June 1995 Link Seal Vendor Manual Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality SD-43, Service Water System  
Engineering Change 80408R0, Flooding Design Basis Update
URS List of Flood Features Inspected
Individual Plant Examination for External Events Submittal, June 1995
URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007  
Link Seal Vendor Manual
 
Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality
SD-43, Service Water System
URS List of Flood Features Inspected
URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007
Section 1R04: Equipment Alignment
Section 1R04: Equipment Alignment
  Procedures
Procedures
Procedure 2OP-18, Core Spray System Operating Procedure  
Procedure 2OP-18, Core Spray System Operating Procedure
1OP-17, RHR System Operating Procedure  
1OP-17, RHR System Operating Procedure
2OP-10, Standby Gas Treatment System Operating Procedure
2OP-10, Standby Gas Treatment System Operating Procedure
Attachment  
                                                                                  Attachment
Drawings D-25024, Reactor Building Core Spray System Piping Diagram 9527-D-2025, sheets 1A and 1B, RHR System, Unit 1
F-04073, Reactor Building Standby Gas Treatment Piping Diagram


                                              4
Miscellaneous  
Drawings
DBD-10, Design Basis Document Standby Gas Treatment System  
D-25024, Reactor Building Core Spray System Piping Diagram
SD-10, System Description St
9527-D-2025, sheets 1A and 1B, RHR System, Unit 1
andby Gas Treatment System  
F-04073, Reactor Building Standby Gas Treatment Piping Diagram
Section 1R05: Fire Protection
Miscellaneous
  Procedures
DBD-10, Design Basis Document Standby Gas Treatment System
0FPP-014, Control of Combustible, Transient Fire Loads, and Ignition Sources 0PFP-CB, Control Building Pre-Fire Plans  
SD-10, System Description Standby Gas Treatment System
OPLP-01, Fire Protection Program Document  
Section 1R05: Fire Protection
OPLP-01.2, Fire Protection System Operability, Action, and Surveillance Requirements  
Procedures
0PFP-013, General Fire Plan 1PFP-RB, Reactor Building Pre-Fire Plans Unit 1 2PFP-RB, Reactor Building Prefire Plans Unit 2  
0FPP-014, Control of Combustible, Transient Fire Loads, and Ignition Sources
OPT-34.11.2.0, Portable Fire Extinguisher Inspection  
0PFP-CB, Control Building Pre-Fire Plans
1PFP-TB, Turbine Building Prefire plans  
OPLP-01, Fire Protection Program Document
OPLP-01.2, Fire Protection System Operability, Action, and Surveillance Requirements
0PFP-013, General Fire Plan
1PFP-RB, Reactor Building Pre-Fire Plans Unit 1
2PFP-RB, Reactor Building Prefire Plans Unit 2
OPT-34.11.2.0, Portable Fire Extinguisher Inspection
1PFP-TB, Turbine Building Prefire plans
Section 1R06: Flood Protection
Nuclear Condition Reports
490292
Drawings
F-03347, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Manholes
F-03343, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Plan
Section 1R07: Heat Sink Performance
Procedures
0ENP-2704, Administrative Control of NRC Generic Letter 89-13 Requirements
0ENP-2705, Service Water Heat Exchanger Thermal Performance Testing
0PM-ACU500, Inspection and Cleaning of the RHR/Core Spray Room Aerofin Cooler Air Filters
      and Coolers
0PM-STU500, Service Water Intake Structure Inspection and Cleaning
0CM-ENG521, Perfex Cooler Inspection and Repair
0E&RC-3212, Service/Circulating Water Chlorine Sampling
1PM-MEC502, Nuclear Service Water Header Inspection
1PM-MEC506, Conventional Service Water Header Inspection
2PM-MEC501, Nuclear Service Water Header Inspection
2PM-MEC505, Conventional Service Water Header Inspection
0PT-08.1.4a, RHR Service Water System Operability Test - Loop A
0AOP-18.0, Nuclear Service Water system Failure
0AOP-19-0, Conventional Service Water System Failure
                                                                                  Attachment


Section 1R06:  Flood Protection
                                              5
  Nuclear Condition Reports
0AOP-37.1, Intake System Blockages
490292
0O1-03.4, Unit 0 Outside Auxiliary Operator Daily Check Sheets
IPT-24.1-1, Service Water Pump and Discharge Valve Operability Test
Drawings F-03347, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Manholes F-03343, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Plan
0AI-81, Water Chemistry Guidelines
 
0A1-86, Service/Circulating Water Treatment Strategic Plan
Section 1R07: Heat Sink Performance
0SMP-SW1500, Sodium Hypochlorite Injection to the SW System
  Procedures
Nuclear Condition Reports
0ENP-2704, Administrative Control of NRC Generic Letter 89-13 Requirements 0ENP-2705, Service Water Heat Exchanger Thermal Performance Testing
392541       507589         339272         539775       497132         542399
0PM-ACU500, Inspection and Cleaning of the RHR/Core Spray Room Aerofin Cooler Air Filters
and Coolers 0PM-STU500, Service Water Intake Structure Inspection and Cleaning 0CM-ENG521, Perfex Cooler Inspection and Repair 0E&RC-3212, Service/Circulating Water Chlorine Sampling
1PM-MEC502, Nuclear Service Water Header Inspection
1PM-MEC506, Conventional Service Water Header Inspection
2PM-MEC501, Nuclear Service Water Header Inspection
2PM-MEC505, Conventional Service Water Header Inspection 0PT-08.1.4a, RHR Service Water System Operability Test - Loop A 0AOP-18.0, Nuclear Service Water system Failure
0AOP-19-0, Conventional Service Water System Failure 
5  Attachment 0AOP-37.1, Intake System Blockages 0O1-03.4, Unit 0 Outside Auxiliary Operator Daily Check Sheets IPT-24.1-1, Service Water Pump and Discharge Valve Operability Test  
 
0AI-81, Water Chemistry Guidelines  
0A1-86, Service/Circulating Water Treatment Strategic Plan  
0SMP-SW1500, Sodium Hypochlorite Injection to the SW System  
 
Nuclear Condition Reports
392541 507589 339272 539775 497132 542399  
 
Work Orders
Work Orders
01582632 01324149  
01582632     01324149
Drawings BN 43.0.01, Service Water System  
Drawings
 
BN 43.0.01, Service Water System
Calculations
Calculations
OSW-0096, Calculation for Tube Plugging and Fouling of Service Water Safety Related Heat
OSW-0096, Calculation for Tube Plugging and Fouling of Service Water Safety Related Heat
Exchangers OSW-0097, RHR and Core Spray Room Cooler Performance  
      Exchangers
G0050C-04, Design Basis Heat Loads from Vital Heat Exchangers  
OSW-0097, RHR and Core Spray Room Cooler Performance
G0050C-04, Design Basis Heat Loads from Vital Heat Exchangers
Miscellaneous
LTAM-BNP-12-0009, Formal Water Hammer Analysis for Service Water
DBD-43, Service Water System
DBD-17, Residual Heat Removal System
System Health Report, Q1-2012, RBCCW Unit 1
System Health Report, Q1-2012, Service Water
System Health Report, Q1-2012, Emergency Diesel Generators
Program Health Report, Q1-2012, GL 89-13 Program
EC-84365, Temporary Removal of Degraded Coating on Internal Surfaces of Service Water
      Pump Discharge Pipe Spools and Elbows
EC-85258, Replace Nuclear and Conventional Service Water Pump Discharge Elbow
2-E11-B002A, Final Eddy Current Inspection Report for RHR Heat Exchanger 2A,
      March 15, 2011
EDG-3-JWC-2010, Final Eddy Current Inspection Report for EDG-3 Jacket Water Cooler
      May 18, 2010
SD-63, Sodium Hypochlorite Injection System
Procedure Revision Requests
00549906      00549915      00549919      00549920      00549923      00549924
00550041      00550333
Section 1R11: Licensed Operator Requalification
Procedures
0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or
General Emergency
                                                                                  Attachment


                                              6
Miscellaneous
0PEP-02.1, Initial Emergency Actions
LTAM-BNP-12-0009, Formal Water Hammer Analysis for Service Water DBD-43, Service Water System  
AOP-17, Turbine Building Closed Cooling Water System
DBD-17, Residual Heat Removal System
AOP-19, Conventional Service Water System Failure
System Health Report, Q1-2012, RBCCW Unit 1
EM-78, Nuclear Power Facility Emergency Notification Form
System Health Report, Q1-2012, Service Water System Health Report, Q1-2012, Emergency Diesel Generators Program Health Report, Q1-2012, GL 89-13 Program
ENP-24.5, Reactivity Control Planning
EC-84365, Temporary Removal of Degraded Coating on Internal Surfaces of Service Water Pump Discharge Pipe Spools and Elbows EC-85258, Replace Nuclear and Conventional Service Water Pump Discharge Elbow
2EOP-01-LPC, Level/Power Control
2-E11-B002A, Final Eddy Current Inspection Report for RHR Heat Exchanger 2A, March 15, 2011 EDG-3-JWC-2010, Final Eddy Current Inspection Report for EDG-3 Jacket Water Cooler May 18, 2010 SD-63, Sodium Hypochlorite Injection System  
2EOP-01-RSP, Reactor Scram Procedure
 
OPS-NGGC-1000, Fleet Conduct of Operations
Procedure Revision Requests
TRN-NGGC-0420, Conduct of Simulator Training and Evaluation
00549906 00549915 00549919 00549920 00549923 00549924 
Miscellaneous
 
LORX-IPO-003 Scenario
00550041 00550333
Technical Specifications 3.7.1, Residual Heat Removal Service Water System
 
Technical Specifications 3.7.2.E, Service Water System and Ultimate Heat Sink
Section 1R11: Licensed Operator Requalification
Section 1R12: Maintenance Effectiveness
 
Procedures
Procedures
0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or
1OP-43, Service Water System Operating Procedure
 
MNT-NGGC-0001, Maintenance Rework Program
General Emergency 
0PT-06.1, SLC System Operability Test
6  Attachment 0PEP-02.1, Initial Emergency Actions AOP-17, Turbine Building Closed Cooling Water System  AOP-19, Conventional Service Water System Failure
0AOP-36.2, Station Blackout
EM-78, Nuclear Power Facility Emergency Notification Form
0PT-12.22, Load Test for SAMA Diesels
ENP-24.5, Reactivity Control Planning
ADM-NGGC-0101, Maintenance Rule Program
2EOP-01-LPC, Level/Power Control
 
2EOP-01-RSP, Reactor Scram Procedure OPS-NGGC-1000, Fleet Conduct of Operations TRN-NGGC-0420, Conduct of Simulator Training and Evaluation
 
Miscellaneous
LORX-IPO-003 Scenario Technical Specifications 3.7.1, Residual Heat Removal Service Water System Technical Specifications 3.7.2.E, Service Water System and Ultimate Heat Sink
Section 1R12: Maintenance Effectiveness
  Procedures
1OP-43, Service Water System Operating Procedure  
 
MNT-NGGC-0001, Maintenance Rework Program  
0PT-06.1, SLC System Operability Test  
0AOP-36.2, Station Blackout  
0PT-12.22, Load Test for SAMA Diesels ADM-NGGC-0101, Maintenance Rule Program  
Nuclear Condition Reports
Nuclear Condition Reports
546346 554488 549265 519703 477622 436705  
546346       554488         549265       519703       477622         436705
 
436703       409663         408997       401149       477561         477622
436703 409663 408997 401149 477561 477622  
401149
401149
Work Orders
Work Orders
1802757 2104000 1868030 1746181  
1802757       2104000         1868030       1746181
Drawings
Miscellaneous
FP-20234, R.P Adams CO, Inc, Strainers, Poro-Edge Automatic
Technical Specification 3.7.2, Service Water System and Ultimate Heat Sink
SD-05, Standby Liquid Control System
Maintenance Rule Unavailability Reports, January 2012 through August 2012
SAMA Diesels System Health Report, Q2-2012
Section 1R13: Maintenance Risk Assessment and Emergent Work Control
Procedures
0AI-144, Risk Management
0AP-022, BNP Outage Risk Management
0AP-025, BNP Integrated Scheduling
                                                                              Attachment


                                              7
Drawings  Miscellaneous
ADM-NGGC-0006, Online EOOS Model
FP-20234, R.P Adams CO, Inc, Strainers, Poro-Edge Automatic
ADM-NGGC-0104, Work Management Process
Technical Specification 3.7.2, Service Water System and Ultimate Heat Sink
WCP-NGGC-0500, Work Activity Integrated Risk Management Program
SD-05, Standby Liquid Control System  Maintenance Rule Unavailability Reports, January 2012 through August 2012
OPS-NGGC-1311, Protected Equipment
SAMA Diesels System Health Report, Q2-2012
Section 1R13: Maintenance Risk Assessment and Emergent Work Control
  Procedures
0AI-144, Risk Management 0AP-022, BNP Outage Risk Management
0AP-025, BNP Integrated Scheduling 
7  Attachment ADM-NGGC-0006, Online EOOS Model ADM-NGGC-0104, Work Management Process  
WCP-NGGC-0500, Work Activity Integrated Risk Management Program  
 
OPS-NGGC-1311, Protected Equipment  
 
Nuclear Condition Reports
Nuclear Condition Reports
559242   Miscellaneous  
559242
BNP EOOS Risk Assessment  
Miscellaneous
BNP EOOS Risk Assessment Report for Work Week 36  
BNP EOOS Risk Assessment
 
BNP EOOS Risk Assessment Report for Work Week 36
Section 1R15: Operability Evaluations
Section 1R15: Operability Evaluations
  Procedures
Procedures
0PT-12.2C, No. 3 Diesel Generator Monthly Load Test  
0PT-12.2C, No. 3 Diesel Generator Monthly Load Test
 
FP-20322, Diesel Generator Instruction Manual
FP-20322, Diesel Generator Instruction Manual  
OPS-NGGC-1305, Operability Determinations
OPS-NGGC-1305, Operability Determinations OPS-NGGC-1307, Operational Decision making  
OPS-NGGC-1307, Operational Decision making
 
Nuclear Condition Reports
250203        310500        318607        548370        549420    558810
Work Orders
542970
Drawings
D-25028, Reactor Building Closed Cooling Water System
F-09348, Diesel Generator No. 4 Circuits Control Wiring Diagram
Miscellaneous
EDG 1-4 Generator Bearing Oil Analysis
SD-39, Emergency Diesel Generators
Section 1R18: Plant Modifications
Procedures
EGR-NGGC-0028 Engineering Evaluation
0AI-68 Brunswick Nuclear Plant Response to Severe Weather Warnings
Engineering Changes
EC 88431, Service Water Building Drain Hub Baffle Plate Installation
EC 86304, Design Leak Tight Barriers at Reactor Bldg Rattle Spaces
Nuclear Condition Reports
Nuclear Condition Reports
250203 310500 318607 548370 549420  558810
559173        490292
                                                                            Attachment


Work Orders
                                              8
542970
Drawings
D-02041, Service Water System Piping Diagram
Drawings D-25028, Reactor Building Closed Cooling Water System F-09348, Diesel Generator No. 4 Circuits Control Wiring Diagram
F-04024, Service Water Intake Structure Ventilation System & Draining Piping
F-01027, Seismic Isolation Space
Miscellaneous  
Miscellaneous
EDG 1-4 Generator Bearing Oil Analysis  
UFSAR Updated Final Safety Analysis Report
SD-39, Emergency Diesel Generators
Section 1R19: Post Maintenance Testing
Section 1R18: Plant Modifications
Procedures
  Procedures
0PT-08.2.2C, LPCI/RHR System Operability Test
EGR-NGGC-0028 Engineering Evaluation
0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test
0AI-68 Brunswick Nuclear Plant Response to Severe Weather Warnings
Engineering Changes
EC 88431, Service Water Building Drain Hub Baffle Plate Installation
EC 86304, Design Leak Tight Barriers at Reactor Bldg Rattle Spaces
 
Nuclear Condition Reports
Nuclear Condition Reports
559173 490292
551048
Work Orders
 
1951825      2028895        2034614      2112268
8  Attachment
Drawings
Drawings D-02041, Service Water System Piping Diagram F-04024, Service Water Intake Structure Ventilation System & Draining Piping
D-25026, Sheet 2A, Residual Heat Removal System, Unit 1
F-01027, Seismic Isolation Space
Miscellaneous
 
Technical Specifications 3.5.1, Emergency Core Cooling System - Operating
Section 1R20: Outage Activities
Miscellaneous  
Procedures
UFSAR Updated Final Safety Analysis Report
0GP-01, Prestartup Checklist
Section 1R19: Post Maintenance Testing
0GP-02, Approach to Criticality and Pressurization of the Reactor
  Procedures
0GP-03, Unit Startup and Synchronization
0PT-08.2.2C, LPCI/RHR System Operability Test 0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test
0GP-05, Unit Shutdown
0GP-10, Rod Sequence Checkoff Sheets
0AI-127, Primary Containment Inspection and Closeout
0AP-22, BNP Outage Risk Management
0OI-01-01, BNP Conduct of Operations Supplement
0SP-12-001, EGM 11-003 OPDRV Activities
Nuclear Condition Reports
Nuclear Condition Reports
551048
561831        561899          561173        562188
Work Orders
Drawings
1951825 2028895 2034614 2112268
D-20022 Sheet 1, Piping Diagram Extraction Steam System, Unit 1
 
Miscellaneous
Main Control Room (MCR) Logs
Drawings D-25026, Sheet 2A, Residual Heat Removal System, Unit 1  
Outage Control Center (OCC) Logs
                                                                            Attachment


Miscellaneous
                                              9
Technical Specifications 3.5.1, Emergency Core Cooling System - Operating 
Unit 1 Key Safety Function Component Status Sheets
 
Operations Standing Instruction 12-052
Section 1R20: Outage Activities
Section 1R22: Surveillance Testing
 
Procedures
Procedures
0GP-01, Prestartup Checklist
0PT-07.2.4a, Core Spray System Operability Test - Loop A
0GP-02, Approach to Criticality and Pressurization of the Reactor
0MST-RHR21Q, CSS and HPCI Hi Drywell Pressure Trip Unit Chan Cal
0GP-03, Unit Startup and Synchronization
0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional
0GP-05, Unit Shutdown
0PT-12.12D, No. 4 Diesel Generator Monthly Load Test
0GP-10, Rod Sequence Checkoff Sheets 0AI-127, Primary Containment Inspection and Closeout 0AP-22, BNP Outage Risk Management
0PT-08.2.2B, LPCI/RHR System Operability Test - Loop B
0OI-01-01, BNP Conduct of Operations Supplement
0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test
0SP-12-001, EGM 11-003 OPDRV Activities
Nuclear Condition Reports
 
547945
Nuclear Condition Reports
561831 561899 561173 562188
 
Drawings D-20022 Sheet 1, Piping Diagram Extraction Steam System, Unit 1
 
Miscellaneous
Main Control Room (MCR) Logs
Outage Control Center (OCC) Logs 
9  Attachment Unit 1 Key Safety Function Component Status Sheets Operations Standing Instruction 12-052
Section 1R22: Surveillance Testing
  Procedures
0PT-07.2.4a, Core Spray System Operability Test - Loop A 0MST-RHR21Q, CSS and HPCI Hi Drywell Pressure Trip Unit Chan Cal 0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional  
0PT-12.12D, No. 4 Diesel Generator Monthly Load Test  
0PT-08.2.2B, LPCI/RHR System Operability Test - Loop B  
0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test  
Nuclear Condition Reports
547945  
Work Orders
Work Orders
2107649
2107649
Drawings D-25024, Reactor Building Core Spray System Piping Diagram
Drawings
D-25024, Reactor Building Core Spray System Piping Diagram
Miscellaneous
Technical Specification 3.5.1, Emergency Core Cooling System - Operating
UFSAR Section 6.3.3.7, Lag Times
Section 1EP6: Drill Evaluation
Procedures
0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or
General Emergency
0PEP-02.1, Initial Emergency Actions
0PEP-02.6.20, Dose Projection Coordinator
0PEP-03.4.8, Offsite Dose Projections for Monitored Releases
2EOP-01-RSP, Reactor Scram Procedure
EM-78, Nuclear Power Facility Emergency Notification Form
EMG-NGGC-0002, Offsite-Dose Assessment
OPS-NGGC-1000, Fleet Conduct of Operations
Nuclear Condition Reports
551255        551620          551698      552439
Section 4OA1: Performance Indicator Verification
Procedures
0E&RC-1006, Operation of the Reactor Building Sample Stations
0E&RC-2212, Calibration/Operation of Genie Gamma Spectroscopy System
REG-NGGC-0009, NRC Performance Indicators and Monthly Operating Report Data
                                                                                  Attachment


                                            10
Miscellaneous  
Miscellaneous
Technical Specification 3.5.1, Emergency Core Cooling System - Operating UFSAR Section 6.3.3.7, Lag Times
BNP-PSA-069, NRC Mitigating System Performance Index (MSPI) Basis Document
 
Unit 1 RHR MSPI Margin Reports, July 2011 to June 2012
Section 1EP6: Drill Evaluation
Unit 2 RHR MSPI Margin Reports, July 2011 to June 2012
 
Unit 1 RHR MSPI Derivation Reports, July 2011 to June 2012
Unit 2 RHR MSPI Derivation Reports, July 2011 to June 2012
REG-NGGC-0009, Attachment 4 - MSPI Unavailability Data Sheets, July 2011 to June 2012
REG-NGGC-0009, Attachment 6 - MSPI Unreliability Data Sheets, July 2011 to June 2012
Section 4OA2: Identification and Resolution of Problems
Procedures
CAP-NGGC-0200, Condition Identification and Screening Process
CAP-NGGC-0205, Condition Evaluation and Corrective Action Process
CAP-NGGC-0206, Performance Assessment and Trending
OERP, Radiological Emergency Response Plan
OPLP-37, Equipment Important to Emergency Preparedness and ERO Response
OPEP-02.6.21, Emergency Communicator
OPEP-04.2, Emergency Facilities and Equipment
ADM-NGGC-0119, Nuclear Safety Culture Program, Revision 01
Nuclear Condition Reports
AR 00201153, Adverse Trend - Failed ERFIS Multiplexer Modules
ACE CR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business Network
Miscellaneous
Down Time by Computer System Log
NIT Key performance indicators
ESR 98-00436, RAINS 99-0045, 50.59 Evaluation
ESR 98-00436, RAINS 99-0045, 50.54q Evaluation
Section 4OA3: Event Followup
Procedures
Procedures
0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or
0PT-09.2, HPCI System Operability Test
 
0PT-09.3, HPCI System - 165 PSIG Flow Test
General Emergency
ADM-NGGC-0107, Equipment Reliability Process Guideline
0PEP-02.1, Initial Emergency Actions  
0PEP-02.1, Initial Emergency Actions
0PEP-02.6.20, Dose Projection Coordinator
0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,
0PEP-03.4.8, Offsite Dose Projections for Monitored Releases
        and General Emergency
2EOP-01-RSP, Reactor Scram Procedure EM-78, Nuclear Power Facility Emergency Notification Form
0PEP-02.2.1, Emergency Action Level Bases
EMG-NGGC-0002, Offsite-Dose Assessment
OPS-NGGC-1000, Fleet Conduct of Operations
 
Nuclear Condition Reports
551255 551620 551698 552439
 
Section 4OA1: Performance Indicator Verification
  Procedures
0E&RC-1006, Operation of the Reactor Building Sample Stations 0E&RC-2212, Calibration/Operation of Genie Gamma Spectroscopy System
REG-NGGC-0009, NRC Performance Indicators and Monthly Operating Report Data 
10  Attachment
Miscellaneous
BNP-PSA-069, NRC Mitigating System Performance Index (MSPI) Basis Document
Unit 1 RHR MSPI Margin Reports, July 2011 to June 2012
Unit 2 RHR MSPI Margin Reports, July 2011 to June 2012
Unit 1 RHR MSPI Derivation Reports, July 2011 to June 2012
Unit 2 RHR MSPI Derivation Reports, July 2011 to June 2012 REG-NGGC-0009, Attachment 4 - MSPI Unavailability Data Sheets, July 2011 to June 2012 REG-NGGC-0009, Attachment 6 - MSPI Unreliability Data Sheets, July 2011 to June 2012
 
Section 4OA2: Identification and Resolution of Problems
  Procedures
CAP-NGGC-0200, Condition Identification and Screening Process
CAP-NGGC-0205, Condition Evaluation and Corrective Action Process
CAP-NGGC-0206, Performance Assessment and Trending
OERP, Radiological Emergency Response Plan OPLP-37, Equipment Important to Emergency Preparedness and ERO Response OPEP-02.6.21, Emergency Communicator
OPEP-04.2, Emergency Facilities and Equipment
ADM-NGGC-0119, Nuclear Safety Culture Program, Revision 01
 
Nuclear Condition Reports
Nuclear Condition Reports
AR 00201153, Adverse Trend - Failed ERFIS Multiplexer Modules ACE CR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business Network
534364        552815        552984
Work Orders
2107224      2107264      2107271        2107313
                                                                                  Attachment


                                                11
Miscellaneous  
Drawings
Down Time by Computer System Log
1-FP-02039, General Electric Gas Control Piping Diagram
NIT Key performance indicators ESR 98-00436, RAINS 99-0045, 50.59 Evaluation
D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2
ESR 98-00436, RAINS 99-0045, 50.54q Evaluation
Miscellaneous
 
10 CFR 50.72 Event Report 47893, High Pressure Coolant Injection Inoperable due to Erratic
Section 4OA3: Event Followup
      Governor Operation, May 2, 2012
 
LER 1-2012-004-00, High Pressure Coolant Injection Inoperable due to Erratic Governor
      Operation, June 29, 2012
System Description 19, High Pressure Coolant Injection System
Technical Specification 3.5.1, Emergency Core Cooling Systems and Reactor Core Isolation
      Cooling
Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event
      (After-the-Fact), August 2, 2012
NUREG-1022, Event Reporting Guidelines
Operator Logs, August 2, 2012
SD-59, Hydrogen Water Chemistry System
Section 4OA5: Other Activities
Procedures
Procedures
0PT-09.2, HPCI System Operability Test
EGR-NGGC-0209, Buried Piping Program, Rev. 3
0PT-09.3, HPCI System - 165 PSIG Flow Test
EGR-NGGC-0513, License Renewal Buried Piping and Tanks Inspection Program, Rev. 3
ADM-NGGC-0107, Equipment Reliability Process Guideline
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake
0PEP-02.1, Initial Emergency Actions 0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, and General Emergency 0PEP-02.2.1, Emergency Action Level Bases
0PEP-02.6, Severe Weather
 
2APP-UA-01, Annunciator Procedure for Panel UA-01
2APP-UA-28, Annunciator Procedure for Panel UA-28
2OP-43, Service Water System Operating Procedure
OPS-NGGC-1305, Operability Determinations
MNT-NGGC-004, Scaffolding Control
0PT-34.2.2.1, Fire Door, Pressure Boundary Door, ASSD Access/Egress Door, and Severe
      Weather/Flood Control Door Inspections
0AI-68, Brunswick Nuclear Plant Response to Severe Weather Warnings
0PEP-02.1.1, Emergency Control-Notification of Unusual Event, Alert, Site Area Emergency,
      and General Emergency
0PEP-02.6, Severe Weather
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake
Nuclear Condition Reports
Nuclear Condition Reports
534364 552815 552984
551646        551838        551964          550469        559173        556860
Work Orders
556861        556862        556863          556864        556865        556866
2107224 2107264 2107271 2107313 
556867        556868        556869          556870        557375        555023
11  Attachment
545354        553946
Drawings 1-FP-02039, General Electric Gas Control Piping Diagram
Work Orders
D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2
550098        550100        550102          550015        545859        545861
1828825                11828826      1643223        1775054        2113607
Miscellaneous
                                                                                      Attachment
10 CFR 50.72 Event Report 47893, High Pressure Coolant Injection Inoperable due to Erratic Governor Operation, May 2, 2012 LER 1-2012-004-00, High Pressure Coolant Injection Inoperable due to Erratic Governor Operation, June 29, 2012 System Description 19, High Pressure Coolant Injection System
Technical Specification 3.5.1, Emergency Core Cooling Systems and Reactor Core Isolation
Cooling Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event (After-the-Fact), August 2, 2012 NUREG-1022, Event Reporting Guidelines
Operator Logs, August 2, 2012
SD-59, Hydrogen Water Chemistry System
Section 4OA5: Other Activities
  Procedures
EGR-NGGC-0209, Buried Piping Program, Rev. 3 EGR-NGGC-0513, License Renewal Buried Piping and Tanks Inspection Program, Rev. 3 0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake
0PEP-02.6, Severe Weather
2APP-UA-01, Annunciator Procedure for Panel UA-01
2APP-UA-28, Annunciator Procedure for Panel UA-28 2OP-43, Service Water System Operating Procedure
OPS-NGGC-1305, Operability Determinations


MNT-NGGC-004, Scaffolding Control
                                              12
0PT-34.2.2.1, Fire Door, Pressure Boundary Door, ASSD Access/Egress Door, and Severe Weather/Flood Control Door Inspections 0AI-68, Brunswick Nuclear Plant Response to Severe Weather Warnings 0PEP-02.1.1, Emergency Control-Notification of Unusual Event, Alert, Site Area Emergency, and General Emergency 0PEP-02.6, Severe Weather
Work Requests
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake
546632         546540         546541       546543         544971       546174
 
546823         546824         546203       546274         546278
Nuclear Condition Reports
Drawings
551646 551838 551964 550469 559173 556860
D-11099, Reactor Building Miscellaneous Steel Pool Liners
 
D-2274, Diesel Cooling Water
556861 556862 556863 556864 556865 556866
D-25049, Reactor Building Piping Diagram Fuel Pool Cooling & Filtering System, Unit 1
 
D-26007, Reactor Building Fuel Pool Cooling & Filter System Plan EL 80-0 & Sections
556867 556868 556869 556870 557375 555023
D-26009, Reactor Building Fuel Pool Cooling & Filter System Miscellaneous Plans & Sections
 
D-27010, Supplemental Spent Fuel Pool Cooling System
545354 553946
F-25008, Reactor Building Arrangement & Details, Fuel Pool
 
D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2
Work Orders
D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2
550098 550100 550102 550015 545859 545861
D-11597, Backdraft Damper with Extra Deep Frame
 
F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping
1828825  1 1828826 1643223 1775054 2113607 
LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room
12 Attachment
        North Wall
Work Requests
1-FP-09319, Reactor Building Railroad Doors
546632 546540 546541 546543 544971 546174  
 
546823 546824 546203 546274 546278  
 
Drawings D-11099, Reactor Building Miscellaneous Steel Pool Liners D-2274, Diesel Cooling Water D-25049, Reactor Building Piping Diagram Fuel Pool Cooling & Filtering System, Unit 1  
D-26007, Reactor Building Fuel Pool Cooling & Filter System Plan EL 80'-0" & Sections  
D-26009, Reactor Building Fuel Pool Cooling & Filter System Miscellaneous Plans & Sections  
 
D-27010, Supplemental Spent Fuel Pool Cooling System F-25008, Reactor Building Arrangement & Details, Fuel Pool D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2  
D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2  
D-11597, Backdraft Damper with Extra Deep Frame  
F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping LL-FB-02103, Reactor Building, Elevation -17'0", Fire Barrier Penetrations, RHR-HPCI Room  
North Wall 1-FP-09319, Reactor Building Railroad Doors  
 
Corrective Action Document
Corrective Action Document
PRR 562261, Revise EGR-NGGC-0209 to strengthen the tie to the License Renewal Program  
PRR 562261, Revise EGR-NGGC-0209 to strengthen the tie to the License Renewal Program
Miscellaneous  
Miscellaneous
Calculation 2RB2-0012, Analysis for Spent Fuel Pool - Elevation of Top of Active Fuel  
Calculation 2RB2-0012, Analysis for Spent Fuel Pool - Elevation of Top of Active Fuel
Engineering Change 80408R0, Flooding Design Basis Update  
Engineering Change 80408R0, Flooding Design Basis Update
EPRI Report 1025286, Seismic Walk-down Guidance for Resolution of Fukushima Near-Term Task Force Recommendation 2.3: Seismic FP-75090, International Instruments INC, Instruments, Switchboard, Edgewise  
EPRI Report 1025286, Seismic Walk-down Guidance for Resolution of Fukushima Near-Term
System Description SD-43, Service Water System  
        Task Force Recommendation 2.3: Seismic
UFSAR Section 9.1.3.3, Fuel Pool Cooling and Cleanup System, Safety Evaluation  
FP-75090, International Instruments INC, Instruments, Switchboard, Edgewise
Units 1 and 2, Flood Protection Feature 6BL, Service Water Building, 4' Elevation, Pipe  
System Description SD-43, Service Water System
Penetration Seal\20-8" Pipe Sleeves Unit 1, SWEL 1 List Unit 1, SWEL 2 List  
UFSAR Section 9.1.3.3, Fuel Pool Cooling and Cleanup System, Safety Evaluation
Unit 2, SWEL 1 List  
Units 1 and 2, Flood Protection Feature 6BL, Service Water Building, 4 Elevation, Pipe
Unit 2, SWEL 2 List  
        Penetration Seal\20-8 Pipe Sleeves
URS Post Fukushima Project, NTTF Recommendation 2.3 Seismic Walk-down Training Record URS Project Number 30703-007, Near Term Task Force Recommendation 2.3 Seismic Walk-
Unit 1, SWEL 1 List
down Procedure  
Unit 1, SWEL 2 List
0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator DBD-106, Hazards Analysis  
Unit 2, SWEL 1 List
Engineering Change 80408R0, Flooding Design Basis Update  
Unit 2, SWEL 2 List
Individual Plant Examination for Exte
URS Post Fukushima Project, NTTF Recommendation 2.3 Seismic Walk-down Training Record
rnal Events Submittal, June 1995 Link Seal Vendor Manual Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality
URS Project Number 30703-007, Near Term Task Force Recommendation 2.3 Seismic Walk-
SD-43, Service Water System
down Procedure
13  Attachment URS List of Flood Features Inspected  URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007 Report Number 110311.401, Summary of Progress Energy Fleet Underground Piping and Tanks with the Scope of NEI 09-14 (Rev. 1), prepared by Structural Integrity Associates,
0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator
Inc., dated 12/07/2011 Assessment Number 531636, Quick Hit Self Assessment for HNP and BNP Buried Piping Program and the NRC TI-2515/182 Inspection, 08/15/2012 Specification 024-001 for Special Doors
DBD-106, Hazards Analysis
Section 4OA7: Licensee-Identified Violations
Engineering Change 80408R0, Flooding Design Basis Update
  Procedures
Individual Plant Examination for External Events Submittal, June 1995
0PEP-02.1, Initial Emergency Actions 0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, and General Emergency 0PEP-02.2.1, Emergency Action Level Bases
Link Seal Vendor Manual
Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality
SD-43, Service Water System
                                                                                    Attachment


Nuclear Condition Reports
                                                13
552815 552984  
URS List of Flood Features Inspected
 
URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007
Report Number 110311.401, Summary of Progress Energy Fleet Underground Piping and
Drawings 1-FP-02039, General Electric Gas Control Piping Diagram  
        Tanks with the Scope of NEI 09-14 (Rev. 1), prepared by Structural Integrity Associates,
D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2  
        Inc., dated 12/07/2011
Miscellaneous  
Assessment Number 531636, Quick Hit Self Assessment for HNP and BNP Buried Piping
Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event (After-the-Fact), August 2, 2012 NUREG-1022, Event Reporting Guidelines Operator Logs, August 2, 2012  
        Program and the NRC TI-2515/182 Inspection, 08/15/2012
Specification 024-001 for Special Doors
Section 4OA7: Licensee-Identified Violations
Procedures
0PEP-02.1, Initial Emergency Actions
0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,
        and General Emergency
0PEP-02.2.1, Emergency Action Level Bases
Nuclear Condition Reports
552815         552984
Drawings
1-FP-02039, General Electric Gas Control Piping Diagram
D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2
Miscellaneous
Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event
        (After-the-Fact), August 2, 2012
NUREG-1022, Event Reporting Guidelines
Operator Logs, August 2, 2012
SD-59, Hydrogen Water Chemistry System
SD-59, Hydrogen Water Chemistry System
                                                                                      Attachment
}}
}}

Latest revision as of 21:24, 11 November 2019

IR 05000325-12-004, 05000324-12-004; 07/01/12 - 09/30/12; Brunswick Steam Electric Plant, Units 1 & 2; Refueling and Other Outage Activities, Identification and Resolution of Problems
ML12312A082
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 11/07/2012
From: Randy Musser
NRC/RGN-II/DRP/RPB4
To: Annacone M
Carolina Power & Light Co
Shared Package
ML12325A266 List:
References
IR-12-004
Download: ML12312A082 (45)


See also: IR 05000324/2012004

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

November 7, 2012

Mr. Michael J. Annacone

Vice President

Brunswick Steam Electric Plant

P.O. Box 10429

Southport, NC 28461-0429

SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION

REPORT NOS.: 05000325/2012004 AND 05000324/2012004

Dear Mr. Annacone:

On September 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Brunswick Unit 1 and 2 facilities. The enclosed integrated inspection report

documents the inspection findings, which were discussed on October 11, 2012, with you and

other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

One NRC-identified and one self-revealing finding of very low safety significance (Green) were

identified during this inspection. These findings were determined to involve a violation of NRC

requirements. Further, two licensee-identified violations were determined to be of very low

safety significance and are listed in this report. The NRC is treating these findings as non-cited

violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance of these NCVs, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear

Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with

copies to the Regional Administrator Region II; the Director, Office of Enforcement, United

States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at the Brunswick Steam Electric Plant.

If you disagree with the cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the

Brunswick Steam Electric Plant.

M. Annacone 2

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Randall A. Musser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket Nos.: 50-325, 50-324

License Nos.: DPR-71, DPR-62

Enclosure: Inspection Report 05000325, 324/2012004

w/Attachment: Supplemental Information

cc w/encl: (See page 3)

ML12312A082_________________ x SUNSI REVIEW COMPLETE x FORM 665 ATTACHED

OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP

SIGNATURE JSD: /RA/ RAM RA for Via e-mail Via e-mail Via e-mail Via e-mail JGW: /RA/

MPS

NAME JDodson MCatts MSchwieg PNiebaum LLake MEndress JWorosilo

DATE 10/24/2012 11/07/2012 10/24/2012 10/29/2012 10/26/2012 10/25/2012 10/15/2012

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

OFFICE RII:DRP RII:DRS

SIGNATURE RAM: /RA/ Via e-mail

NAME RMusser MSpeck

DATE 11/7/2012 11/06/2012

E-MAIL COPY? YES NO YES NO

M. Annacone 3

cc w/encl: Lee Grzeck

Plant General Manager Regulatory Affairs Manager

Brunswick Steam Electric Plant Brunswick Steam Electric Plant

Progress Energy Progress Energy Carolinas, Inc.

Electronic Mail Distribution Electronic Mail Distribution

Edward L. Wills, Jr. Randy C. Ivey

Director Site Operations Manager, Nuclear Oversight

Brunswick Steam Electric Plant Brunswick Steam Electric Plant

Electronic Mail Distribution Progress Energy Carolinas, Inc.

Electronic Mail Distribution

J. W. (Bill) Pitesa

Senior Vice President Paul E. Dubrouillet

Nuclear Operations Manager, Training

Duke Energy Corporation Brunswick Steam Electric Plant

Electronic Mail Distribution Electronic Mail Distribution

John A. Krakuszeski Joseph W. Donahue

Plant Manager Vice President

Brunswick Steam Electric Plant Nuclear Oversight

Electronic Mail Distribution Progress Energy

Electronic Mail Distribution

Lara S. Nichols

Deputy General Counsel Senior Resident Inspector

Duke Energy Corporation U.S. Nuclear Regulatory Commission

Electronic Mail Distribution Brunswick Steam Electric Plant

U.S. NRC

M. Christopher Nolan 8470 River Road, SE

Director - Regulatory Affairs Southport, NC 28461

General Office

Duke Energy Corporation John H. O'Neill, Jr.

Electronic Mail Distribution Shaw, Pittman, Potts & Trowbridge

2300 N. Street, NW

Michael J. Annacone Washington, DC 20037-1128

Vice President

Brunswick Steam Electric Plant Peggy Force

Electronic Mail Distribution Assistant Attorney General

State of North Carolina

Annette H. Pope P.O. Box 629

Manager-Organizational Effectiveness Raleigh, NC 27602

Brunswick Steam Electric Plant

Electronic Mail Distribution (cc w/encl - continued)

M. Annacone 4

cc w/encl contd:

Chairman

North Carolina Utilities Commission

Electronic Mail Distribution

Robert P. Gruber

Executive Director

Public Staff - NCUC

4326 Mail Service Center

Raleigh, NC 27699-4326

Anthony Marzano

Director

Brunswick County Emergency Services

Electronic Mail Distribution

Public Service Commission

State of South Carolina

P.O. Box 11649

Columbia, SC 29211

W. Lee Cox, III

Section Chief

Radiation Protection Section

N.C. Department of Environmental Commerce & Natural Resources

Electronic Mail Distribution

Warren Lee

Emergency Management Director

New Hanover County

Department of Emergency Management

230 Government Center Drive

Suite 115

Wilmington, NC 28403

M. Annacone 5

Letter to Michael J. Annacone from Randall A. Musser dated November 7, 2012

SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION

REPORT NOS.: 05000325/2012004 AND 05000324/2012004

Distribution w/encl:

J. Baptist, RII EICS

L. Douglas, RII EICS

OE Mail (email address if applicable)

RIDSNRRDIRS

PUBLIC

R. Pascarelli, NRR ((Regulatory Conferences Only))

RidsNrrPMBrunswick Resource

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-325, 50-324

License Nos.: DPR-71, DPR-62

Report Nos.: 05000325/2012004, 05000324/2012004

Licensee: Carolina Power and Light (CP&L)

Facility: Brunswick Steam Electric Plant, Units 1 & 2

Location: 8470 River Road, SE

Southport, NC 28461

Dates: July 1, 2012 through September 30, 2012

Inspectors: M. Catts, Senior Resident Inspector

M. Schwieg, Resident Inspector

P. Niebaum, Acting Senior Resident Inspector

J. Dodson, Senior Project Engineer (1R04, 1R05, 4OA2)

L. Lake, Senior Reactor Inspector (4OA5)

M. Endress, Reactor Inspector (1R07)

Approved by: Randall A. Musser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000325/2012004, 05000324/2012004; 07/01/12 - 09/30/12; Brunswick Steam Electric

Plant, Units 1 & 2; Refueling and Other Outage Activities, Identification and Resolution of

Problems

This report covers a three-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings were identified by the

inspectors. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

(SDP). The cross-cutting aspects were determined using IMC 0310, Components Within the

Cross-Cutting Areas. Findings for which the SDP does not apply may be Green or be assigned

a severity level after NRC management review.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Barrier Integrity

Green: The inspectors identified a Green non-cited violation (NCV) of TS 3.6.4.1,

Secondary Containment because the licensee did not maintain secondary containment

operable as required during a maintenance activity considered an operation with a

potential for draining the reactor vessel (OPDRV). Once questioned by the inspectors,

the licensee restored secondary containment, developed an Operation standing

instruction (12-052) to treat the activity as an OPDRV and placed this issue into its

corrective action program (CAP) as AR 562188.

The failure to maintain secondary containment operable while Unit 1 was in Mode 4 with

an OPDRV in progress was a performance deficiency. The finding was more than minor

because it was associated with the configuration control attribute of the Barrier Integrity

Cornerstone, and adversely affected the cornerstone objective to provide reasonable

assurance that physical design barriers (fuel cladding, reactor coolant system, and

containment) protect the public from radionuclide releases caused by accidents or

events because the Unit 1 secondary containment boundary was not preserved or

maintained. The inspectors evaluated the finding using Inspection Manual Chapter

(IMC) 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,

which required an analysis using IMC 0609 Appendix G since the reactor was in Mode 4

(cold shutdown). The finding was determined to be of very low safety significance

(Green) according to IMC 0609 Appendix G, Attachment 1, Checklist 6, since a

quantitative assessment (Phase 2 or Phase 3 evaluation) was not required. Specifically,

the inspectors determined that the licensee maintained adequate mitigation capability for

reactor vessel water level inventory and an event did not occur that could be

characterized as a loss of control. The cause of this finding was directly related to the

cross-cutting aspect of Accurate Procedures in the Resources component of the Human

Performance area, because the licensee did not consider the recirculation pump seal

replacement activity to be OPDRV based on procedural guidance that contains

exclusions to what are considered OPDRV activities. H.2(c) (Section 1R20)

3

Cornerstone: Emergency Preparedness

Green: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the

licensees failure to properly evaluate or consider the impact to emergency response

facilities of design change ESR98-00436 which was implemented in 1999. This resulted

in the loss of Emergency Response Facility Information System (ERFIS), Emergency

Response Data System (ERDS), Safety Parameter Display System (SPDS), and all

displays including radiation monitors for the emergency response facilities. Specifically,

the licensee failed to ensure that adequate emergency response facilities and equipment

were available as required by the Brunswick Nuclear Plant Radiological Emergency

Plan, Section 1.3.1.3 revision 80 and 10 CFR 50.47(b)(8). This issue was captured in the

licensees CAP as AR 542704.

The licensees failure to properly evaluate or consider the impact to emergency

response facilities of design change ESR98-00436 which was implemented in 1999 was

a performance deficiency. Specifically, the licensee introduced a single point failure

mode which did not meet the design requirements specified in their Design Basis

Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees failure

to ensure that adequate emergency response facilities and equipment were available as

delineated in the Updated Final Safety Analysis Report (UFSAR) Section 7.7.1.9, and

required by the Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3,

revision 80, and 10 CFR 50.47(b)(8). The finding was more than minor because it

adversely affected the Emergency Preparedness Cornerstone objective of ensuring that

the licensee was capable of implementing adequate measures to protect the health and

safety of the public in the event of a radiological emergency. Specifically, the Facilities

and Equipment attribute was affected during the time when the ERFIS, ERDS, SPDS,

and all displays including radiation monitors for the emergency response facilities were

degraded, and as a result did not meet 10 CFR 50.47(b)(8) Planning Standard program

element, adequate emergency facilities and equipment to support the emergency

response are provided and maintained. The finding was assessed for significance in

accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance

Determination Process. Attachment 2 of Appendix B, Failure to Comply Significance

Logic is as follows: Failure to comply; Loss of Risk Significant Planning Standard

Function (RSPS), No; RSPS Degraded Function, No; Loss of Planning Standard

Function, No; the result is a Green finding. The inspectors determined that this resulted

in a very low safety significance finding (Green). No cross-cutting aspect was assigned

to this finding because the performance deficiency occurred more than three years ago

and is not reflective of current plant performance. (Section 4OA2.2)

B. Licensee-Identified Violations

Violations of very low safety significance that were identified by the licensee have been

reviewed by inspectors. Corrective actions taken or planned by the licensee have been

entered into the licensees CAP. These violations and corrective action tracking

numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at rated thermal power (RTP), and operated at or near full

power until July 22, 2012 when reactor power was lowered to 52 percent to clear a fouled

circulating water debris filter and power was returned to RTP on July 23, 2012. On August 3,

2012, power was reduced to 70 percent for a rod sequence exchange and power was returned

to RTP on August 5, 2012. On August 5, 2012, power was reduced to 90 percent for control rod

improvement and power was returned to RTP on the same day. On August 8, 2012, power was

reduced to 65 percent for offsite transmission line work and power was returned to RTP on the

same day. On September 16, 2012, the reactor was shut down for forced outage to replace the

1A and 1B recirculation pump seal assemblies. Reactor startup commenced on September 27,

2012 and the main generator was synchronized to the grid on September 28, 2012. Reactor

power was raised to RTP on September 29, 2012. On September 30, 2012 reactor power was

reduced to 75 percent for a scheduled control rod improvement. Power ascension continued to

RTP for the remainder of the inspection period.

Unit 2 began the inspection period at RTP, and operated at or near full power until August 18,

2012, when power was reduced to 70 percent for a rod sequence exchange and power was

returned to RTP on August 19, 2012. On August 20, 2012, power was reduced to 86 percent

for control rod improvement and power was returned to RTP on August 21, 2012. On August

21, 2012, power was reduced to 94 percent for control rod improvement and power was

returned to RTP on August 21, 2012. On September 29, 2012, reactor power was reduced to

94 percent to support a scheduled rod improvement and returned to RTP later that day and

maintained RTP for the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 1 sample)

External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with

the design basis probable maximum flood. The inspectors reviewed the Updated Final

Safety Analysis Report (UFSAR), which depicted the design flood levels and protection

areas containing safety-related equipment, to identify areas that may be affected by

external flooding. The inspectors conducted a site walk-down of the service water

building, to ensure that erected flood protection measures were in accordance with

design specifications. The inspectors reviewed the sealing of equipment below the flood

line, adequacy of watertight doors, drain systems and sumps including check valves,

and maintenance and calibration of flood protection equipment. The inspectors also

reviewed operating procedures for mitigating external flooding during severe weather to

5

determine if the licensee planned or established adequate measures to protect against

external flooding events.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Quarterly Partial System Walk-downs (71111.04Q - 3 samples)

a. Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant

systems:

  • Unit 2 A train Core Spray (CS) system while B residual heat removal/service

(RHR/SW) was inoperable for a system outage on July 11, 2012;

  • Unit 1 Reactor Building Closed Cooling Water (RBCCW) on July 27, 2012; and

maintenance outage on September 19, 2012.

The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders, condition reports, and the impact of ongoing work activities on redundant trains

of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify that system components and support

equipment were aligned correctly and were operable. The inspectors examined the

material condition of the components and observed operating parameters of equipment

to verify that there were no obvious deficiencies. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the CAP with the appropriate significance characterization.

b. Findings

No findings were identified.

.2 Semi-Annual Complete System Walk-down (71111.04S - 1 sample)

a. Inspection Scope

On September 5, 2012 the inspectors performed a complete system alignment

inspection of the Unit 1 RHR system to verify the functional capability of the system.

This system was selected because it was considered both safety-significant and risk-

6

significant in the licensees probabilistic risk assessment. The inspectors walked down

the system to review mechanical and electrical equipment line-ups, electrical power

availability, system pressure and temperature indications, as appropriate, component

labeling, component lubrication, component and equipment cooling, hangers and

supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. A review of a sample of past and

outstanding work orders (WOs) was performed to determine whether any deficiencies

significantly affected the system function. In addition, the inspectors reviewed the CAP

to ensure that system equipment alignment problems were being identified and

appropriately resolved.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05Q - 5 samples)

Quarterly Resident Inspector Tours

a. Inspection Scope

The inspectors conducted fire protection walk-downs which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • Unit 1 and 2 Control Buildings 23' Elevation 1PFP-CB-7;
  • Unit 1 Turbine Building South Area 38 Elevation 1PFP-TB1-1k;
  • Unit 2 Reactor Building North 2A Core Spray Room 2-PFP-RB2-1b.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and had implemented

adequate compensatory measures for out-of-service, degraded or inoperable fire

protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed, that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP.

7

b. Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06 - 1 sample)

Annual Review of Cables Located in Underground Bunkers/Manholes

a. Inspection Scope

The inspectors conducted an inspection of underground bunkers/manholes subject to

flooding that contain cables whose failure could disable risk-significant equipment. The

inspectors performed walk-downs of risk-significant areas, including manhole 2-MH-

7SW, to verify that the cables were not submerged in water, that cables and/or splices

appear intact and to observe the condition of cable support structures. When applicable,

the inspectors verified proper dewatering device (sump pump) operation and verified

level alarm circuits are set appropriately to ensure that the cables will not be submerged.

Where dewatering devices were not installed; the inspectors ensured that drainage was

provided and was functioning properly.

b. Findings

No findings were identified.

1R07 Heat Sink Performance (71111.07T - 3 samples)

Triennial Review of Heat Sink Performance

a. Inspection Scope

The inspectors selected the Residual Heat Removal (RHR) Heat Exchanger 2A, Diesel

Generator (DG) 3 Jacket Water Cooler and the Core Spray (CS) Room Cooler 1A,

based on their risk-significance in the licensees probabilistic safety analysis and their

importance to safety-related mitigating system support functions in the NRCs model for

Brunswick Nuclear Power Plant, Units 1 and 2.

For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler

1A, the inspectors reviewed the licensees inspection, maintenance, and monitoring of

biotic fouling and macro-fouling programs, to determine if they were adequate to ensure

proper heat transfer. This was accomplished by determining whether the methods used

were consistent with accepted industry practices. The inspectors also reviewed the

licensees inspection and cleaning activities had established acceptance criteria

consistent with industry standards, and the as-found results were recorded, evaluated,

and appropriately dispositioned to maintain structural integrity.

For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler

1A, the inspectors reviewed the methods and results of heat exchanger performance

inspections. In addition, the inspectors reviewed the condition and operation of the RHR

Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler 1A to

8

determine if they were consistent with design assumptions in heat transfer calculations

and as described in the USFAR. This included determining whether the number of

plugged tubes was within pre-established limits based on capacity and heat transfer

assumptions. The inspectors also determined whether the licensee evaluated the

potential for water hammer and established adequate controls and operational limits to

prevent heat exchanger degradation due to excessive flow-induced vibration during

operation.

The inspectors determined whether the performance of the ultimate heat sink (UHS)-

Cape Fear River and its subcomponents such as piping, intake screens, pumps, valves,

etc. was appropriately evaluated by tests or other equivalent methods to ensure

availability and accessibility to the in-plant cooling water systems. The inspectors also

reviewed design changes to the service water system and the UHS.

The inspectors reviewed the licensees operation of the service water system and UHS.

This included a review of licensees procedures for a loss of the service water system or

UHS and the verification that instrumentation, which is relied upon for decision-making,

was available and functional. The inspectors also performed a system walk-down on the

service water system to determine whether the licensees assessment on structural

integrity was adequate and interviewed the respective system engineer. For buried or

inaccessible piping, the inspectors reviewed the licensees pipe testing, inspection, and

monitoring program to determine whether structural integrity was ensured and that any

leakage or degradation was appropriately identified and dispositioned by the licensee.

The inspectors performed a system walk-down of the service water intake structure to

determine whether the licensees assessment on structural integrity and component

functionality was adequate. The inspectors also determined whether service water

pump bay silt accumulation was monitored, trended, and maintained at an acceptable

level by the licensee, and that water level instruments were functional and routinely

monitored. The inspectors also determined whether the licensees ability to ensure

functionality during adverse weather conditions was adequate.

The inspectors reviewed condition reports related to the heat exchangers and heat sink

performance issues to determine whether the licensee had an appropriate threshold for

identifying issues and to evaluate the effectiveness of the corrective actions. Records

were also reviewed to verify that the licensee actions were consistent with Generic Letter

(GL) 89-13 licensee commitments, Electric Power Research Institute (EPRI) and other

industry guidelines. These inspection activities constituted three heat sink inspection

samples as defined in IP 71111.07-05.

b. Findings

No findings were identified.

9

1R11 Licensed Operator Requalification Program (71111.11Q - 2 samples)

.1 Quarterly Review of Licensed Operator Requalification Testing and Training

a. Inspection Scope

On August 13, 2012, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems, and to ensure that training was being conducted in accordance

with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan actions

and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

a. Inspection Scope

Inspectors observed and assessed licensed operator performance in the plant and main

control room, particularly during periods of heightened activity or risk and where the

activities could affect plant safety. Specifically, on September 16th, the inspectors

observed the Unit 1 shutdown and cooldown evolutions leading up to the forced outage

to repair the recirculation pump seals. The inspectors reviewed various licensee policies

and procedures listed in the Attachment.

  • Operator compliance and use of procedures.
  • Control board manipulations.
  • Communication between crew members.
  • Use and interpretation of plant instruments, indications and alarms.
  • Use of human error prevention techniques.
  • Documentation of activities, including initials and sign-offs in procedures.
  • Supervision of activities, including risk and reactivity management.
  • Pre-job briefs and crew briefs

10

This activity constituted one License Operator Requalification inspection sample and one

Control Room Observation inspection sample.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q - 3 samples)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk-

significant systems:

  • 1B Nuclear Service Water Pump smoking with vibration and strainer leakage on

pump start on June 26, 2012;

  • 2A Standby Liquid Cooling accumulator failure before operability run on September

10, 2012 (AR560026); and

  • Performance (unavailability and unreliability) history of the Severe Accident

Mitigation Alternatives (SAMA) diesels

The inspectors reviewed events where ineffective equipment maintenance may have

resulted in equipment failure or invalid automatic actuations of Engineered Safeguards

Systems and independently verified the licensee's actions to address system

performance or condition problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring; and

appropriate performance criteria for structures, systems and components

(SSCs)/functions classified as (a)(2) or appropriate and adequate goals and

corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization.

b. Findings

No findings were identified.

11

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant equipment listed

below to verify that the appropriate risk assessments were performed prior to removing

equipment for work:

  • Unit 2 yellow risk during emergent work on 2-E21-F015A, 2A Core Spray Full Flow

Test Bypass Valve, and scheduled maintenance on 2B RHR/residual heat removal

service water (RHRSW) on July 11, 2012;

  • Unit 1 yellow risk during 1B Recirculation Pump Variable Frequency Drive power

recovery, and planned maintenance on 1A RHR/RHRSW on July 26, 2012;

  • Unit 1 yellow risk during planned maintenance on 1B RHR/RHRSW September 4 to

September 6, 2012;

  • Unit 1 integrated risk during repair of 1B recirculation pump seal September 17 to

September 25, 2012;

These activities were selected based on their potential risk-significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

b. Findings

No findings were identified.

1R15 Operability Evaluations (71111.15 - 5 samples)

a. Inspection Scope

The inspectors reviewed the following five issues:

on July 6, 2012 (AR548370);

  • 2D RHRSW Booster pump coupling grease specification evaluation on July 12, 2012

(AR542025);

2012 (AR549420);

  • Reactor Building Close Cooling Water (RBCCW) piping corrosion in rattle space on

August 21, 2012 (AR557151); and

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  • EDG #4 alternate safe shutdown switch contact continuity indications on August 27,

2012 (AR558810)

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the UFSAR and TS to the licensees evaluations, to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations.

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18 - 2 samples)

a. Inspection Scope

The inspectors reviewed the two modifications listed below to determine whether the

modifications affected the safety functions of systems that are important to safety. The

inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results

and conducted field walk-downs of the modifications to verify that the modifications did

not degrade the design bases, licensing bases, and performance capability of the

affected systems.

  • Design leak tight barriers at reactor building rattle spaces (EC86304);

b. Findings

No findings were identified.

1R19 Post Maintenance Testing (71111.19 - 7 samples)

a. Inspection Scope

The inspectors reviewed the following seven post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • 0PT-12.2D, No. 4 Diesel Generator Monthly Load Test after replacement of the 60X

relay on July 23, 2012;

13

Test - Unit 2 RHRSW Loop B after the maintenance outage on July 12, 2012;

  • 0PT-08.2.2c, Low Pressure Coolant Injection/RHR System Operability Test - Unit 1

RHR Loop A after the maintenance outage on July 27, 2012;

  • 0PT-12.2C, EDG #3 Operability Test - Unit 2 after repair of jacket water pump on

August 16, 2012;

  • 0PT-15.6, Standby Gas Treatment Operability Test, Unit 1 B after relay replacement

on August 15, 2012;

replacement of Electronic Governor - Magnetic (EGM) on August 23, 2012; and

recirculation pump seal on September 26, 2012

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following, as applicable:

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing, and test documentation was properly

evaluated. The inspectors evaluated the activities against the UFSAR and TS to ensure

that the test results adequately ensured that the equipment met the licensing basis and

design requirements. In addition, the inspectors reviewed corrective action documents

associated with post-maintenance tests to determine whether the licensee was

identifying problems and entering them in the CAP and that the problems were being

corrected commensurate with their importance to safety.

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)

Other Outage Activities

a. Inspection Scope

The inspectors evaluated licensee outage activities for an unscheduled forced outage to

replace the 1B recirculation pump seal assembly. During the outage, the licensee made

the decision to replace the 1A recirculation pump seal assembly to address the potential

extent of cause/condition. The outage began on September 16, 2012 and concluded on

September 28, 2012. The inspectors reviewed activities to ensure that the licensee

considered risk in developing, planning, and implementing the outage schedule.

Additionally, the inspectors observed or reviewed the reactor shutdown and cool down,

outage equipment configuration and risk management, electrical lineups, control and

monitoring of decay heat removal, control of containment activities, performed a drywell

close out inspection, observed reactor startup and heat up activities, and identification

and resolution of problems associated with the outage. Documents reviewed are listed

in the Attachment.

14

b. Findings

Introduction: The inspectors identified a Green NCV of TS 3.6.4.1, Secondary

Containment because the licensee did not maintain secondary containment operable as

required during an activity considered an operation with a potential for draining the

reactor vessel (OPDRV).

Description: On September 19, 2012, the licensee was replacing the 1B recirculation

pump seal assembly while Unit 1 was in Mode 4 (cold shutdown). In an effort to properly

isolate the work area, the recirculation suction and discharge isolation valves were

tagged closed. Due to seat leakage across the isolation valves, the 1B recirculation

pump drain valve was uncapped and opened to maintain the pump body partially empty

to prevent water from impacting the work area while the pump seal was removed. The

pump drain leakage was sent to the drywell floor drain system. The 1B recirculation

pump seal replacement activity had the potential to drain the reactor vessel below the

top of the fuel because the recirculation loops penetrate the reactor vessel below the top

of active fuel. An OPDRV is described in the licensees technical specifications as an

operation with a potential for draining the reactor vessel. However, the licensee did not

recognize or consider this activity as an OPDRV due to inadequate procedural guidance

that was used to exclude this activity as an OPDRV. Specifically, the licensee adopted

the definition of an OPDRV in procedure 0OI-01.01 as provided in Enforcement

Guidance Memorandum (EGM)11-003 as any activity that could potentially result in

draining or siphoning the RPV water level below the top of the fuel, without taking credit

for mitigating measures. However, section 9.16.15.b.(2) of licensee procedure 0OI-

01.01, BNP Conduct of Operations Supplement, stated leakage through mechanical

joints (for example valve or flange packing leaks, seat leakage through an isolation

valve, flange leakage, etc) is not considered an OPDRV. On September 19, 2012, the

licensee relaxed Unit 1 secondary containment from 03:30 a.m. until 09:20 p.m. by

opening the reactor building air lock doors on the 20-foot elevation to increase ventilation

to the recirculation pump seal replacement work area in the Unit 1 drywell. This resulted

in Secondary Containment inoperability while Unit 1 was in Mode 4 during an OPRDV

activity. The inspectors questioned the licensees Operations staff on the decision to

make secondary containment inoperable during an OPDRV activity. Following this, the

licensee restored secondary containment, developed an Operation standing instruction

12-052 to treat this activity as an OPDRV and placed this issue into its CAP as AR

562188.

Analysis: The inspectors determined that the failure to maintain secondary containment

operable while Unit 1 was in Mode 4 with an OPDRV in progress was a performance

deficiency. The performance deficiency was more than minor because it was associated

with the configuration control attribute of the Barrier Integrity Cornerstone, and adversely

affected the cornerstone objective to provide reasonable assurance that physical design

barriers (fuel cladding, reactor coolant system, and containment) protect the public from

radionuclide releases caused by accidents or events because the Unit 1 secondary

containment boundary was not preserved or maintained. The inspectors evaluated the

finding using Inspection Manual Chapter (IMC) 0609, Attachment 4, Phase 1 - Initial

Screening and Characterization of Findings, which required an analysis using IMC 0609

Appendix G since the reactor was in Mode 4 (cold shutdown). The finding was

determined to be of very low safety significance (Green) according to IMC 0609

15

Appendix G, Attachment 1, Checklist 6, since a quantitative assessment (Phase 2 or

Phase 3 evaluation) was not required. Specifically, the inspectors determined that the

licensee maintained adequate mitigation capability for reactor vessel water level

inventory and an event did not occur that could be characterized as a loss of control.

The cause of this finding was directly related to the cross-cutting aspect of Accurate

Procedures in the Resources component of the Human Performance area, because the

licensee did not consider the recirculation pump seal replacement activity to be OPDRV

based on procedural guidance that contains exclusions to what are considered OPDRV

activities. H.2(c)

Enforcement: Unit 1 TS 3.6.4.1, Secondary Containment, required secondary

containment to be operable during modes one, two, three, during movement of recently

irradiated fuel assemblies in the secondary containment and during operations with a

potential for draining the reactor vessel (OPDRVs). Contrary to the above, on

September 19, 2012, Unit 1 secondary containment was not maintained operable during

an OPDRV activity. The licensee entered this issue in its CAP as AR 562188, and

restored secondary containment during the OPDRV activity. Because the licensee

entered the issue into its CAP and the finding is of very low safety significance (Green),

this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRCs

Enforcement Policy: NCV 05000325/2012004-01, Failure to Maintain Secondary

Containment Operable during an OPDRV activity.

1R22 Surveillance Testing

.1 Routine Surveillance Testing (71111.22 - 4 samples)

a. Inspection Scope

The inspectors either observed surveillance tests or reviewed the test results for the

following activities to verify the tests met TS surveillance requirements, UFSAR

commitments, in-service testing requirements, and licensee procedural requirements.

The inspectors assessed the effectiveness of the tests in demonstrating that the SSCs

were operationally capable of performing their intended safety functions.

Cal on July 10, 2012;

  • 0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional on July 24,

2012; and

  • 0PT-12.12D, No. 4 Diesel Generator Monthly Load Test on August 17, 2012;

b. Findings

No findings were identified.

16

.2 In-Service Testing (IST) Surveillance (71111.22 - 1 sample)

a. Inspection Scope

The inspectors reviewed the performance of Unit 1 LPCI/RHR System Operability Test -

Loop B on August 9, 2012 to evaluate the effectiveness of the licensees American

Society of Mechanical Engineers (ASME)Section XI testing program for determining

equipment availability and reliability. The inspectors evaluated selected portions of the

following areas: 1) testing procedures, 2) acceptance criteria, 3) testing methods, 4)

compliance with the licensees IST program, TS, selected licensee commitments, and

code requirements, 5) range and accuracy of test instruments, and 6) required corrective

actions.

b. Findings

No findings were identified.

.3 Reactor Coolant System Leak Detection Inspection Surveillance (71111.22 - 1 sample)

a. Inspection Scope

The inspectors observed and reviewed the test results for a reactor coolant system leak

detection surveillance, 0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure

Vessel Pressure Test, on September 28, 2012. The inspectors observed in-plant

activities and reviewed procedures and associated records to determine whether:

effects of the testing were adequately addressed by control room personnel or engineers

prior to the commencement of the testing; acceptance criteria were clearly stated,

demonstrated operational readiness, and were consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented; and the

calibration frequency was in accordance with TSs, the UFSAR, procedures, and

applicable commitments; applicable prerequisites described in the test procedures were

satisfied; test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other applicable

procedures; and test data and results were accurate, complete, within limits, and valid.

Inspectors verified that test results not meeting acceptance criteria were addressed with

an adequate operability evaluation or the system or component was declared

inoperable; equipment was returned to a position or status required to support the

performance of its safety functions; and all problems identified during the testing were

appropriately documented and dispositioned in the corrective action program.

b. Findings

No findings were identified.

17

1EP6 Emergency Planning Drill Evaluation (71114.06 - 2 samples)

a. Inspection Scope

The inspectors observed site emergency preparedness training drill/simulator scenarios

conducted on July 9, 2012 and July 25, 2012. The inspectors reviewed the drill scenario

narrative to identify the timing and location of classifications, notifications, and protective

action recommendations development activities. During the drill, the inspectors

assessed the adequacy of event classification and notification activities. The inspectors

observed portions of the licensees post-drill. The inspectors verified that the licensee

properly evaluated the drills performance with respect to performance indicators and

assessed drill performance with respect to drill objectives.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151 - 6 samples)

.1 Mitigating Systems Cornerstone

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) performance indicators listed above for the period from the third (3rd)

quarter 2011 through the second (2nd) quarter 2012. The inspectors reviewed the

licensees operator narrative logs, issue reports, MSPI derivation reports, event reports

and NRC Integrated Inspection reports for the period to validate the accuracy of the

submittals.

b. Findings

No findings were identified.

.2 Barrier Integrity Cornerstone

a. Inspection Scope

The inspectors reviewed licensee submittals for the Reactor Coolant System Specific

Activity performance indicator for the period from the third (3rd) quarter 2011 through the

second (2nd) quarter 2012. The inspectors reviewed the licensees RCS chemistry

18

samples, TS requirements, issue reports, and event reports for the period to validate the

accuracy of the submittals. In addition to record reviews, the inspectors observed a

chemistry technician obtain and analyze a reactor coolant system sample.

The inspectors sampled licensee submittals for the Reactor Coolant System Leakage

performance indicator for the period from the third (3rd) quarter 2011 through the second

(2nd) quarter 2012. The inspectors reviewed the licensees operator logs, RCS leakage

tracking data, issue reports, and event reports for the period to validate the accuracy of

the submittals.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152 - 2 samples)

.1 Routine Review of Items Entered Into the Corrective Action Program

a. Inspection Scope

To aid in the identification of repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed frequent screenings of items entered into

the licensees corrective action program. The review was accomplished by reviewing

daily action request reports.

b. Findings

No findings were identified.

.2 Assessments and Observations

Selected Issue Follow-up Inspection: UPS-A Failure and Loss of Emergency Response

Facility Information System (ERFIS), Plant Process Computer (PPC), Business Network

a. Inspection Scope

The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business

Network, for detailed review. This AR identified that a single failure caused the loss of

ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors

reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors

reviewed these reports to verify that the licensee identified the full extent of the issue,

performed an appropriate evaluation, and specified and prioritized appropriate corrective

actions. The inspectors evaluated the reports against the requirements of the licensees

CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action

Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.

19

b. Findings

No findings were identified

a. Inspection Scope

The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business

Network, for detailed review. This AR identified that a single failure caused the loss of

ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors

reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors

reviewed these reports to verify that the licensee identified the full extent of the issue,

performed an appropriate evaluation, and specified and prioritized appropriate corrective

actions. The inspectors evaluated the reports against the requirements of the licensees

CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action

Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.

b. Findings

Introduction: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the

licensees failure to properly evaluate or consider the impact to emergency response

facilities of design change ESR98-00436 which was implemented in 1999. As a result,

a number of temporary losses of ERFIS, Emergency Response Data System (ERDS),

SPDS, and all displays including radiation monitors for the emergency response facilities

occurred. Specifically, the licensee failed to ensure that adequate emergency response

facilities and equipment were available as required by the Brunswick Nuclear Plant

Radiological Emergency Plan, Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).

This issue was captured in the licensees CAP as AR 542704.

Description: In 1999, the licensee implemented design change ESR98-00436 for the

power supply to the ERFIS, ERDS, SPDS, and all displays including RMS for the

emergency response facilities. The licensee did not properly evaluate or consider the

impact to emergency response facilities and equipment prior to implementation of this

design change. As a result, the ERFIS, ERDS, and SPDS systems, and all radiation

monitoring system (RMS) displays were susceptible to a single point power failure mode.

The implementation of the design change introduced a single point failure mode which

did not meet the design requirements specified in their Design Basis Document (DBD

60) sections 3.6.7.2 and 3.6.7.3. Prior to the licensees implementation of design

change ESR98-00436 in 1999, this single point vulnerability did not exist as the power

supply system had automatic switching capability on loss of one power source. When

the design change was implemented, the ERFIS, ERDS, and SPDS systems and RMS

displays were degraded as demonstrated by the resulting failures of those systems on

multiple occasions including July 17, 2004 and June 12, 2012. Additionally, all displays

for those systems were lost in all of the emergency facilities including the radiation

monitoring system.

20

On June 13, 2012, the licensee made an event notification to the NRC Operations

Center, 50.72(b)(3)(xiii) Loss of Emergency Assessment Capability, Offsite Response

Capability, or Offsite Communications Capability for the emergency response facilities.

The report delineated that at 5:57 p.m. EDT on June 12, 2012, Brunswick Nuclear Plant

experienced a fault on the Emergency Response Facility Information System (ERFIS)

uninterruptible power supply (UPS) electrical bus A. This resulted in a loss of site

Safety Parameter Display System (SPDS), Emergency Response Data System (ERDS)

and Plant Process Computer (PPC) for both Unit 1 and Unit 2.

During the loss of SPDS, the emergency response capability of that system was lost to

the site. During the loss of ERDS, the automatic data transfer feature of that system

was lost for transmissions to the NRC, however manual data transfer was still available.

During the loss of the PPC, automatic core thermal power averaging and automatic core

thermal limit monitoring was lost. Manual calculations were available for these functions.

Unit 1 SPDS was restored to the Emergency Operations Facility (EOF) at 7:49 p.m. on

June 12, 2012. Unit 2 SPDS was restored to the EOF at 8:30 p.m. on June 12, 2012.

The inverter was restored to service on June 17, 2012 at 12:00 noon.

Inspectors determined that the licensee did not properly evaluate or consider the impact

to all emergency response facilities and equipment prior to implementation of the

ESR98-00436 design change. The inspectors concluded that the ERFIS, ERDS, and

SPDS systems required by the Brunswick Nuclear Plant Radiological Emergency Plan

were degraded from 1999 when the design change was installed to present.

Compensatory measures were put in place during the June 2012 event to manually

obtain and log the required data from the instrumentation in the control room and

transmit to the emergency response facilities, and after the June 2012 event, the

licensee initiated a design change to restore the power configuration to those systems

back to the original design which would remove this failure mechanism.

Analysis: The licensees failure to properly evaluate or consider the impact to

emergency response facilities of design change ESR98-00436 which was implemented

in 1999 was a performance deficiency. Specifically, the licensee introduced a single

point failure mode which did not meet the design requirements specified in their Design

Basis Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees

failure to ensure that adequate emergency response facilities and equipment were

available as delineated in the Updated Final Safety Analysis Report (UFSAR) Section

7.7.1.9, and required by the Brunswick Nuclear Plant Radiological Emergency Plan,

Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).

The finding was more than minor because it adversely affected the Emergency

Preparedness Cornerstone objective of ensuring that the licensee was capable of

implementing adequate measures to protect the health and safety of the public in the

event of a radiological emergency. Specifically, the Facilities and Equipment attribute

was affected during the time when the ERFIS, ERDS, SPDS, and all displays including

radiation monitors for the emergency response facilities were degraded, and as a result

did not meet 10 CFR 50.47(b)(8) Planning Standard program element, adequate

emergency facilities and equipment to support the emergency response are provided

and maintained. The finding was assessed for significance in accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance Determination Process.

21

Attachment 2 of Appendix B, Failure to Comply Significance Logic is as follows: Failure

to comply; Loss of Risk Significant Planning Standard Function (RSPS), No; RSPS

Degraded Function, No; Loss of Planning Standard Function, No; the result is a Green

finding. The inspectors determined that this resulted in a low safety significance finding

(Green). No cross-cutting aspect was assigned to this finding because the performance

deficiency occurred more than three years ago and is not reflective of current plant

performance.

Enforcement: 10 CFR 50.54(q)(2) requires, in part, a licensee to follow and maintain the

effectiveness of an emergency plan that meets the requirements in Appendix E to this

part and, for nuclear power reactor licensee, the planning standards of 10 CFR 50.47(b).

The Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3, revision 80,

states in part that special provisions have been made to assure that ample space and

proper equipment are available to effectively respond to a full range of possible

emergencies. Contrary to the above, from 1999, when design change ESR98-00436

was installed, until the compensatory measures were put in place in June 2012, the

licensee failed to maintain adequate emergency facilities and equipment to support

emergency response when the ERFIS, ERDS, SPDS, and all displays including radiation

monitors for the emergency response facilities were degraded due to the implementation

of the design change. This resulted in failures of those systems on July 17, 2004 and

June 12, 2012. The licensee has compensatory measures in place, entered this issue

their CAP as AR 542704, and initiated a design change to restore the power

configuration back to the original design. Because the licensee entered the issue into its

CAP and the finding is of very low safety significance (Green), this violation is being

treated as an NCV, consistent with Section 2.3.2 of the NRCs Enforcement Policy: NCV

05000325; 324/2012004-02, Failure to Maintain Reliability and Availability of Emergency

Response Equipment for Emergency Response Facilities.

.3 Assessments and Observations

Selected Issue Follow-up Inspection: EDG 2 wiring associated with Alternate Safe

Shutdown (ASSD) Switch 2-DG-SS-A1

a. Inspection Scope

The inspectors performed a detailed review of AR 557897 associated with the wiring for

the EDG 2 Alternate Safe Shutdown (ASSD) Switch 2-DG-SS-A1. The issue was

discovered during a planned system outage for EDG2 during the week of August 26.

The inspectors verified that the issue was captured completely and accurately in the

CAP. The inspectors evaluated the licensees operability determinations and performed

walk-downs with licensee staff of applicable fire areas as needed. The inspectors

followed the licensees actions to restore the wiring to its proper configuration and also

verified the extent of condition inspections for the remaining EDGs 1, 3 and 4 were

completed in a timely manner. The inspectors reviewed the licensees reportability

evaluation and subsequent 8-hour report made to the NRC in accordance with 10 CFR

50.72(b)(3)(ii)(B). Additional documents reviewed are listed in the Attachment.

b. Findings

22

Introduction: The inspectors opened an unresolved item (URI) for this issue of concern

to determine if a performance deficiency existed.

Description: A wiring discrepancy was identified during inspection of the EDG 2 ASSD

switch 2-DG-SS-A1. A contact in the circuit was determined to be bypassed that would

have the potential to prevent proper isolation of the EDG2 control circuits from the Main

Control Room (MCR) during an Appendix R fire event. The inspectors plan to review the

licensees cause evaluation for this event and determine if a performance deficiency

existed. This issue is being tracked as URI 05000325; 324/2012004-03, EDG2 wiring on

ASSD switch.

4OA3 Follow-up of Events (71153 - 2 samples)

.1 Notice of Unusual Event for Fire in the Protected Area

a. Inspection Scope

For the plant event listed below, the inspectors reviewed plant parameters, reviewed

personnel performance, and evaluated performance of mitigating systems. The

inspectors communicated the plant events to appropriate regional NRC personnel, and

compared the event details with criteria contained in IMC 0309, Reactive Inspection

Decision Basis for Reactors, for consideration of potential reactive inspection activities.

As applicable, the inspectors verified that the licensee made appropriate emergency

classification assessments and properly reported the event in accordance with 10 CFR

50.72. The inspectors reviewed the licensees follow-up actions related to the events to

assure that the licensee implemented appropriate corrective actions commensurate with

their safety significance.

  • On August 2, 2012, a fire existed in the protected area on the Units 1 and 2 turbine

building roof for approximately two hours, meeting the criteria for a Notice of Unusual

Event declaration.

b. Findings

One licensee identified violation is documented in Section 4OA7 of this report.

.2 (Closed) LER 05000325/2012-004-00, High Pressure Coolant Injection (HPCI)

Inoperable Due to Erratic Governor Operation

a. Inspection Scope

On May 2, 2012, Unit 1 HPCI was declared inoperable due to erratic governor operation

during Surveillance Test 0PT-09.2, HPCI System Operability Test. The erratic governor

operation was due to the failure of the Ramp Generator Signal Convertor (RGSC). The

licensee determined that the root cause of the RGSC failure was due to a lack of a

replacement preventative maintenance (PM) for the RGSC, which had been installed for

at least 22 years. The corrective actions included replacing the RGSC and creating a

PM task to replace the RGSCs. The licensee documented the root cause evaluation in

23

NCR 534364. The inspectors reviewed the LER, the NCR, and corrective actions to

determine whether the station adequately evaluated the condition.

b. Findings

One licensee identified violation is documented in Section 4OA7 of this report. This LER

is closed.

4OA5 Other Activities

.1 (Discussed) NRC Temporary Instruction (TI) 2515/187, Inspection of Near-Term Task

Force Recommendation 2.3 Flooding Walk-downs, and NRC TI 2515/188, Inspection of

Near-Term Task Force Recommendation 2.3 Seismic Walk-downs

a. Inspection Scope

Inspectors accompanied the licensee on a sampling basis, during their flooding and

seismic walk-downs, to verify that the licensees walk-down activities were conducted

using the methodology endorsed by the NRC. These walk-downs are being performed at

all sites in response to a letter from the NRC to licensees, entitled Request for

Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Regarding

Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights

from the Fukushima Dai-Ichi Accident, dated March 12, 2012 (ADAMS Accession No.

ML12053A340).

Enclosure 3 of the March 12, 2012, letter requested licensees to perform seismic walk-

downs using an NRC-endorsed walk-down methodology. Electric Power Research

Institute (EPRI) document 1025286 titled, Seismic Walk-down Guidance, (ADAMS

Accession No. ML12188A031) provided the NRC-endorsed methodology for performing

seismic walk-downs to verify that plant features, credited in the current licensing basis

(CLB) for seismic events, are available, functional, and properly maintained.

Enclosure 4 of the letter requested licensees to perform external flooding walk-downs

using an NRC-endorsed walk-down methodology (ADAMS Accession No.

ML12056A050). Nuclear Energy Industry (NEI) document 12-07 titled, Guidelines for

Performing Verification Walk-downs of Plant Protection Features, (ADAMS Accession

No. ML12173A215) provided the NRC-endorsed methodology for assessing external

flood protection and mitigation capabilities to verify that plant features, credited in the

CLB for protection and mitigation from external flood events, are available, functional,

and properly maintained.

b. Findings

Findings or violations associated with the flooding and seismic walk-downs, if any, will

be documented in future reports.

24

.2 (Discussed) Temporary Instruction (TI) 2515/182 - Review of the Implementation of the

Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1

a. Inspection Scope

Leakage from buried and underground pipes has resulted in ground water contamination

incidents with associated heightened NRC and public interest. The industry issued a

guidance document, Nuclear Energy Institute (NEI) 09-14, Guideline for the

Management of Buried Piping Integrity, (ADAMS Accession No. ML 1030901420), to

describe the goals and required actions (commitments made by the licensee) resulting

from this underground piping and tank initiative. On December 31, 2010, NEI issued

Revision 1 to NEI 09-14, Guidance for the Management of Underground Piping and

Tank Integrity, (ADAMS Accession No. ML 110700122), with an expanded scope of

components which included underground piping that was not in direct contact with the

soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182,

Review of the Industry Initiative to Control Degradation of Underground Piping and

Tanks, to gather information related to the industrys implementation of this initiative.

The instructors reviewed the licensees programs for buried pipe and underground piping

and tanks in accordance with TI-2515/182 to determine if the program attributes and

completion dates identified in Section 3.3 A and 3.3 B of NEI 09-14, Revision 1, were

contained in the licensees program and implementing procedures. For the buried pipe

and underground piping program attributes, with completion dates that had passed, the

inspectors reviewed records to determine if the attribute was in fact complete and to

determine if the attribute was accomplished in a manner which reflected good or poor

practices in management.

b. Observations

The licensees buried piping and underground piping and tanks program was inspected

in accordance with paragraphs 03.01.a through 03.01.c of TI-2515/182 and was found to

meet all applicable aspects of NEI 09-14 Revision 1, as set forth in Table 1 of the TI.

Based upon the scope of the review described above, Phase I of TI-2515/182 was

completed.

c. Findings

No findings were identified.

4OA6 Management Meetings

Exit Meeting Summary

On July 19, 2012, the inspectors presented inspection results of the triennial heat sink

inspection to Mr. Michael Annacone and other members of the licensee staff. The

25

inspectors confirmed that none of the potential report input discussed was considered

proprietary.

On September 18, 2012, the inspector presented inspection results of the TI-182, Phase

1 of the Underground Piping and Tanks Inspection by conference call to Mr. James

Burke, Site Director of Engineering, and other members of the licensee staff. The

inspector verified that all proprietary information was returned to the licensee.

On October 11, 2012, the inspectors presented inspection results from the quarterly

inspection to Mr. Annacone and other members of the licensee staff. The inspectors

confirmed that any proprietary information received during the inspection period were

properly controlled or returned to licensee staff.

4OA7 Licensee-Identified Violations

The following violations of very low significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of the NRC Enforcement

Policy, for being dispositioned as NCVs.

  • 10 CFR 50.54(q) requires, in part, a licensee authorized to possess and operate

a nuclear power reactor shall follow and maintain in effect emergency plans

which meet the standards of 10 CFR 50.47(b). Title 10 CFR 50.47(b)(4)

requires, in part, a standard emergency classification and action level scheme be

used by the licensee. Procedure 0PEP-02.1.1, Emergency Control - Notification

of Unusual Event, Alert, Site Area Emergency, and General Emergency, Step

5.7.2 states, that the emergency declaration will be made within 15 minutes after

the availability of indications to plant operators that an emergency action level

has been exceeded. Procedure 0PEP-02.1, Initial Emergency Actions, HU2.1,

requires the declaration of an Unusual Event when a fire is not extinguished

within 15 minutes of control room notification or verification of a control room fire

alarm in any Table H-1 or Table H-3 areas. Table H-1 includes the turbine

building. Contrary to the above, on August 2, 2012, a Notice of Unusual Event

(NOUE) was not classified within 15 minutes of a fire within the protected area

not being extinguished within 15 minutes of detection. Specifically, when a fire

was reported on the Turbine Building roof to the Control Room and was not

extinguished within 15 minutes, conditions were met for classification of EAL

HU2.1 in accordance with Procedure 0PEP-02.1; however, the EAL was not

classified until approximately eight hours after the fire started. This issue was

entered into the licensees CAP as NCR 552984 and the licensee is performing a

root cause evaluation. Corrective actions included making a one hour report to

the NRC for discovery of a condition that met the EAL classification for an NOUE

after the fact. The inspectors determined the finding was associated with an

actual event implementation problem, and assessed the significance using IMC 0609, Appendix B, "Emergency Preparedness Significance Determination

Process." Using the Emergency Preparedness SDP, Sheet 1, "Failure to

Implement (Actual Event) Significance Logic" the inspectors determined the

finding was of very low safety significance (Green) because the licensee failed to

implement a risk significant planning standard (10 CFR 50.47(b)(4)) during an

actual Notice of Unusual Event.

26

requires that activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances

and shall be accomplished in accordance with these instructions, procedures, or

drawings. Licensee procedure ADM-NGGC-0107, Equipment Reliability Process

Guideline, steps 9.4.9 and 9.4.10 required component experts and preventive

maintenance (PM) optimization to determine if there was a cost effective PM to

prevent failure and then to develop the PM model. Contrary to the above, the

Unit 1 high pressure coolant injection (HPCI) ramp generator signal converter

(RGSC) did not have the appropriate preventive maintenance to prevent failure.

As a result, the Unit 1 high pressure coolant injection (HPCI) system failed the

HPCI System Operability Test performed on April 30, 2012 and was declared

inoperable. The licensee entered this issue into the CAP as NCR 534364.

Corrective actions included replacing the RGSC and creating a PM task to

replace the RGSCs on a specified frequency. Using IMC 0609, Appendix A,

"Phase 1 Initial Screening and Characterization of Findings," the inspectors

determined this finding required a Phase 2 analysis. The Phase 1 screened this

Mitigating Systems Cornerstone finding to Phase 2 because the finding

represented a loss of HPCI system and/or function. The inspectors, with the

assistance of the regional Senior Risk Analyst, performed a Phase 2 analysis

using the Saphire 8 Model. 109 hours0.00126 days <br />0.0303 hours <br />1.802249e-4 weeks <br />4.14745e-5 months <br /> of unavailability time was used for the

analysis since HPCI was not required during the refueling outage from February

23, 2012 through April 29, 2012. Based on the results of the Phase 2 analysis,

the inspectors determined the finding was of very low safety significance (Green).

ATTACHMENT: SUPPLEMENTAL INFORMATION

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

M. Annacone, Site Vice President

A. Brittain, Manager - Security

J. Burke, Director - Site Engineering

K. Croker, Supervisor - Emergency Preparedness

C. Dunsmore, Manager - Shift Operations

P. Dubrouillet, Manager - Training

G. Galloway, Acting Manager, Nuclear Oversight

C. George, Manager - BOP Systems

S. Gordy, Manager - Maintenance

L. Grzeck, Manager - Regulatory Affairs

M. Hamm, Superintendent - Mechanical Maintenance

F. Jefferson, Manager - Reactor Systems Engineering

J. Kalamaja, Manager - Operations

J. Krakuszeski, Plant General Manager

R. Mosier, Communication Specialist

A. Padleckas, Superintendent - Nuclear Operations Performance

D. Petrusic, Superintendent - Environmental and Chemistry

A. Pope, Manager - Nuclear Support Services

J. Price, Manager- Design Engineering

W. Richardson, Engineering

T. Roeder, Supervisor - Chemistry

T. Sherrill, Licensing Senior Technical Specialist

P. Smith, Superintendent - Electrical, Instrumentation, and Controls Maintenance

M. Talon, Buried Piping Program Manager

J. Terrell, Corporate Buried Piping Program Manager

M. Turkal, Lead Engineer - Technical Support

J. Vincelli, Manager - Environmental and Radiological Controls

B. Wilder, Engineering

E. Wills, Director - Site Operations

NRC Personnel

R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects Region II

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000325/2012004-01 NCV Failure to Maintain Secondary Containment Operable

During an OPDRV Activity. (Section 1R20)

05000325;324/2012004-02 NCV Failure to Maintain Reliability and Availability of

Emergency Response Equipment for Emergency

Response Facilities. (Section 4OA2.2)

Opened

05000325;324/2012004-03 URI EDG2 Wiring on ASSD Switch (Section 4OA2.3)

Closed

05000325/2012-004-00 LER High Pressure Coolant Injection (HPCI) Inoperable

Due to Erratic Governor Operation (Section 4OA3.2)

Discussed

Temporary Instruction TI Inspection of Near-Term Task Force Recommendation

2515/187 2.3 Flooding Walk-downs (Section 4OA5.1)

Temporary Instruction TI Inspection of Near-Term Task Force Recommendation

2515/188 2.3 Seismic Walk-downs (Section 4OA5.1)

Temporary Instruction TI Review of the Implementation of the Industry Initiative

2515/182 to Control Degradation of Underground Piping and

Tanks, Phase 1 (Section 4OA5.2)

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake

0PEP-02.6, Severe Weather

2APP-UA-01, Annunciator Procedure for Panel UA-01

2APP-UA-28, Annunciator Procedure for Panel UA-28

2OP-43, Service Water System Operating Procedure

OPS-NGGC-1305, Operability Determinations

Nuclear Condition Reports

556860 556861 556862 556863 556864 556865

556866 556867 556868 556869 556870 557375

555023 545354 553946

Work Orders

550098 550100 550102 550015 545859 545861

1828825 1828826 1643223 1775054

Drawings

D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2

D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2

D-11597, Backdraft Damper with Extra Deep Frame

F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping

LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room

North Wall

Miscellaneous

0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator

DBD-106, Hazards Analysis

Engineering Change 80408R0, Flooding Design Basis Update

Individual Plant Examination for External Events Submittal, June 1995

Link Seal Vendor Manual

Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality

SD-43, Service Water System

URS List of Flood Features Inspected

URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007

Section 1R04: Equipment Alignment

Procedures

Procedure 2OP-18, Core Spray System Operating Procedure

1OP-17, RHR System Operating Procedure

2OP-10, Standby Gas Treatment System Operating Procedure

Attachment

4

Drawings

D-25024, Reactor Building Core Spray System Piping Diagram

9527-D-2025, sheets 1A and 1B, RHR System, Unit 1

F-04073, Reactor Building Standby Gas Treatment Piping Diagram

Miscellaneous

DBD-10, Design Basis Document Standby Gas Treatment System

SD-10, System Description Standby Gas Treatment System

Section 1R05: Fire Protection

Procedures

0FPP-014, Control of Combustible, Transient Fire Loads, and Ignition Sources

0PFP-CB, Control Building Pre-Fire Plans

OPLP-01, Fire Protection Program Document

OPLP-01.2, Fire Protection System Operability, Action, and Surveillance Requirements

0PFP-013, General Fire Plan

1PFP-RB, Reactor Building Pre-Fire Plans Unit 1

2PFP-RB, Reactor Building Prefire Plans Unit 2

OPT-34.11.2.0, Portable Fire Extinguisher Inspection

1PFP-TB, Turbine Building Prefire plans

Section 1R06: Flood Protection

Nuclear Condition Reports

490292

Drawings

F-03347, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Manholes

F-03343, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Plan

Section 1R07: Heat Sink Performance

Procedures

0ENP-2704, Administrative Control of NRC Generic Letter 89-13 Requirements

0ENP-2705, Service Water Heat Exchanger Thermal Performance Testing

0PM-ACU500, Inspection and Cleaning of the RHR/Core Spray Room Aerofin Cooler Air Filters

and Coolers

0PM-STU500, Service Water Intake Structure Inspection and Cleaning

0CM-ENG521, Perfex Cooler Inspection and Repair

0E&RC-3212, Service/Circulating Water Chlorine Sampling

1PM-MEC502, Nuclear Service Water Header Inspection

1PM-MEC506, Conventional Service Water Header Inspection

2PM-MEC501, Nuclear Service Water Header Inspection

2PM-MEC505, Conventional Service Water Header Inspection

0PT-08.1.4a, RHR Service Water System Operability Test - Loop A

0AOP-18.0, Nuclear Service Water system Failure

0AOP-19-0, Conventional Service Water System Failure

Attachment

5

0AOP-37.1, Intake System Blockages

0O1-03.4, Unit 0 Outside Auxiliary Operator Daily Check Sheets

IPT-24.1-1, Service Water Pump and Discharge Valve Operability Test

0AI-81, Water Chemistry Guidelines

0A1-86, Service/Circulating Water Treatment Strategic Plan

0SMP-SW1500, Sodium Hypochlorite Injection to the SW System

Nuclear Condition Reports

392541 507589 339272 539775 497132 542399

Work Orders

01582632 01324149

Drawings

BN 43.0.01, Service Water System

Calculations

OSW-0096, Calculation for Tube Plugging and Fouling of Service Water Safety Related Heat

Exchangers

OSW-0097, RHR and Core Spray Room Cooler Performance

G0050C-04, Design Basis Heat Loads from Vital Heat Exchangers

Miscellaneous

LTAM-BNP-12-0009, Formal Water Hammer Analysis for Service Water

DBD-43, Service Water System

DBD-17, Residual Heat Removal System

System Health Report, Q1-2012, RBCCW Unit 1

System Health Report, Q1-2012, Service Water

System Health Report, Q1-2012, Emergency Diesel Generators

Program Health Report, Q1-2012, GL 89-13 Program

EC-84365, Temporary Removal of Degraded Coating on Internal Surfaces of Service Water

Pump Discharge Pipe Spools and Elbows

EC-85258, Replace Nuclear and Conventional Service Water Pump Discharge Elbow

2-E11-B002A, Final Eddy Current Inspection Report for RHR Heat Exchanger 2A,

March 15, 2011

EDG-3-JWC-2010, Final Eddy Current Inspection Report for EDG-3 Jacket Water Cooler

May 18, 2010

SD-63, Sodium Hypochlorite Injection System

Procedure Revision Requests

00549906 00549915 00549919 00549920 00549923 00549924

00550041 00550333

Section 1R11: Licensed Operator Requalification

Procedures

0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or

General Emergency

Attachment

6

0PEP-02.1, Initial Emergency Actions

AOP-17, Turbine Building Closed Cooling Water System

AOP-19, Conventional Service Water System Failure

EM-78, Nuclear Power Facility Emergency Notification Form

ENP-24.5, Reactivity Control Planning

2EOP-01-LPC, Level/Power Control

2EOP-01-RSP, Reactor Scram Procedure

OPS-NGGC-1000, Fleet Conduct of Operations

TRN-NGGC-0420, Conduct of Simulator Training and Evaluation

Miscellaneous

LORX-IPO-003 Scenario

Technical Specifications 3.7.1, Residual Heat Removal Service Water System

Technical Specifications 3.7.2.E, Service Water System and Ultimate Heat Sink

Section 1R12: Maintenance Effectiveness

Procedures

1OP-43, Service Water System Operating Procedure

MNT-NGGC-0001, Maintenance Rework Program

0PT-06.1, SLC System Operability Test

0AOP-36.2, Station Blackout

0PT-12.22, Load Test for SAMA Diesels

ADM-NGGC-0101, Maintenance Rule Program

Nuclear Condition Reports

546346 554488 549265 519703 477622 436705

436703 409663 408997 401149 477561 477622

401149

Work Orders

1802757 2104000 1868030 1746181

Drawings

Miscellaneous

FP-20234, R.P Adams CO, Inc, Strainers, Poro-Edge Automatic

Technical Specification 3.7.2, Service Water System and Ultimate Heat Sink

SD-05, Standby Liquid Control System

Maintenance Rule Unavailability Reports, January 2012 through August 2012

SAMA Diesels System Health Report, Q2-2012

Section 1R13: Maintenance Risk Assessment and Emergent Work Control

Procedures

0AI-144, Risk Management

0AP-022, BNP Outage Risk Management

0AP-025, BNP Integrated Scheduling

Attachment

7

ADM-NGGC-0006, Online EOOS Model

ADM-NGGC-0104, Work Management Process

WCP-NGGC-0500, Work Activity Integrated Risk Management Program

OPS-NGGC-1311, Protected Equipment

Nuclear Condition Reports

559242

Miscellaneous

BNP EOOS Risk Assessment

BNP EOOS Risk Assessment Report for Work Week 36

Section 1R15: Operability Evaluations

Procedures

0PT-12.2C, No. 3 Diesel Generator Monthly Load Test

FP-20322, Diesel Generator Instruction Manual

OPS-NGGC-1305, Operability Determinations

OPS-NGGC-1307, Operational Decision making

Nuclear Condition Reports

250203 310500 318607 548370 549420 558810

Work Orders

542970

Drawings

D-25028, Reactor Building Closed Cooling Water System

F-09348, Diesel Generator No. 4 Circuits Control Wiring Diagram

Miscellaneous

EDG 1-4 Generator Bearing Oil Analysis

SD-39, Emergency Diesel Generators

Section 1R18: Plant Modifications

Procedures

EGR-NGGC-0028 Engineering Evaluation

0AI-68 Brunswick Nuclear Plant Response to Severe Weather Warnings

Engineering Changes

EC 88431, Service Water Building Drain Hub Baffle Plate Installation

EC 86304, Design Leak Tight Barriers at Reactor Bldg Rattle Spaces

Nuclear Condition Reports

559173 490292

Attachment

8

Drawings

D-02041, Service Water System Piping Diagram

F-04024, Service Water Intake Structure Ventilation System & Draining Piping

F-01027, Seismic Isolation Space

Miscellaneous

UFSAR Updated Final Safety Analysis Report

Section 1R19: Post Maintenance Testing

Procedures

0PT-08.2.2C, LPCI/RHR System Operability Test

0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test

Nuclear Condition Reports

551048

Work Orders

1951825 2028895 2034614 2112268

Drawings

D-25026, Sheet 2A, Residual Heat Removal System, Unit 1

Miscellaneous

Technical Specifications 3.5.1, Emergency Core Cooling System - Operating

Section 1R20: Outage Activities

Procedures

0GP-01, Prestartup Checklist

0GP-02, Approach to Criticality and Pressurization of the Reactor

0GP-03, Unit Startup and Synchronization

0GP-05, Unit Shutdown

0GP-10, Rod Sequence Checkoff Sheets

0AI-127, Primary Containment Inspection and Closeout

0AP-22, BNP Outage Risk Management

0OI-01-01, BNP Conduct of Operations Supplement

0SP-12-001, EGM 11-003 OPDRV Activities

Nuclear Condition Reports

561831 561899 561173 562188

Drawings

D-20022 Sheet 1, Piping Diagram Extraction Steam System, Unit 1

Miscellaneous

Main Control Room (MCR) Logs

Outage Control Center (OCC) Logs

Attachment

9

Unit 1 Key Safety Function Component Status Sheets

Operations Standing Instruction 12-052

Section 1R22: Surveillance Testing

Procedures

0PT-07.2.4a, Core Spray System Operability Test - Loop A

0MST-RHR21Q, CSS and HPCI Hi Drywell Pressure Trip Unit Chan Cal

0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional

0PT-12.12D, No. 4 Diesel Generator Monthly Load Test

0PT-08.2.2B, LPCI/RHR System Operability Test - Loop B

0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test

Nuclear Condition Reports

547945

Work Orders

2107649

Drawings

D-25024, Reactor Building Core Spray System Piping Diagram

Miscellaneous

Technical Specification 3.5.1, Emergency Core Cooling System - Operating

UFSAR Section 6.3.3.7, Lag Times

Section 1EP6: Drill Evaluation

Procedures

0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or

General Emergency

0PEP-02.1, Initial Emergency Actions

0PEP-02.6.20, Dose Projection Coordinator

0PEP-03.4.8, Offsite Dose Projections for Monitored Releases

2EOP-01-RSP, Reactor Scram Procedure

EM-78, Nuclear Power Facility Emergency Notification Form

EMG-NGGC-0002, Offsite-Dose Assessment

OPS-NGGC-1000, Fleet Conduct of Operations

Nuclear Condition Reports

551255 551620 551698 552439

Section 4OA1: Performance Indicator Verification

Procedures

0E&RC-1006, Operation of the Reactor Building Sample Stations

0E&RC-2212, Calibration/Operation of Genie Gamma Spectroscopy System

REG-NGGC-0009, NRC Performance Indicators and Monthly Operating Report Data

Attachment

10

Miscellaneous

BNP-PSA-069, NRC Mitigating System Performance Index (MSPI) Basis Document

Unit 1 RHR MSPI Margin Reports, July 2011 to June 2012

Unit 2 RHR MSPI Margin Reports, July 2011 to June 2012

Unit 1 RHR MSPI Derivation Reports, July 2011 to June 2012

Unit 2 RHR MSPI Derivation Reports, July 2011 to June 2012

REG-NGGC-0009, Attachment 4 - MSPI Unavailability Data Sheets, July 2011 to June 2012

REG-NGGC-0009, Attachment 6 - MSPI Unreliability Data Sheets, July 2011 to June 2012

Section 4OA2: Identification and Resolution of Problems

Procedures

CAP-NGGC-0200, Condition Identification and Screening Process

CAP-NGGC-0205, Condition Evaluation and Corrective Action Process

CAP-NGGC-0206, Performance Assessment and Trending

OERP, Radiological Emergency Response Plan

OPLP-37, Equipment Important to Emergency Preparedness and ERO Response

OPEP-02.6.21, Emergency Communicator

OPEP-04.2, Emergency Facilities and Equipment

ADM-NGGC-0119, Nuclear Safety Culture Program, Revision 01

Nuclear Condition Reports

AR 00201153, Adverse Trend - Failed ERFIS Multiplexer Modules

ACE CR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business Network

Miscellaneous

Down Time by Computer System Log

NIT Key performance indicators

ESR 98-00436, RAINS 99-0045, 50.59 Evaluation

ESR 98-00436, RAINS 99-0045, 50.54q Evaluation

Section 4OA3: Event Followup

Procedures

0PT-09.2, HPCI System Operability Test

0PT-09.3, HPCI System - 165 PSIG Flow Test

ADM-NGGC-0107, Equipment Reliability Process Guideline

0PEP-02.1, Initial Emergency Actions

0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,

and General Emergency

0PEP-02.2.1, Emergency Action Level Bases

Nuclear Condition Reports

534364 552815 552984

Work Orders

2107224 2107264 2107271 2107313

Attachment

11

Drawings

1-FP-02039, General Electric Gas Control Piping Diagram

D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2

Miscellaneous

10 CFR 50.72 Event Report 47893, High Pressure Coolant Injection Inoperable due to Erratic

Governor Operation, May 2, 2012

LER 1-2012-004-00, High Pressure Coolant Injection Inoperable due to Erratic Governor

Operation, June 29, 2012

System Description 19, High Pressure Coolant Injection System

Technical Specification 3.5.1, Emergency Core Cooling Systems and Reactor Core Isolation

Cooling

Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event

(After-the-Fact), August 2, 2012

NUREG-1022, Event Reporting Guidelines

Operator Logs, August 2, 2012

SD-59, Hydrogen Water Chemistry System

Section 4OA5: Other Activities

Procedures

EGR-NGGC-0209, Buried Piping Program, Rev. 3

EGR-NGGC-0513, License Renewal Buried Piping and Tanks Inspection Program, Rev. 3

0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake

0PEP-02.6, Severe Weather

2APP-UA-01, Annunciator Procedure for Panel UA-01

2APP-UA-28, Annunciator Procedure for Panel UA-28

2OP-43, Service Water System Operating Procedure

OPS-NGGC-1305, Operability Determinations

MNT-NGGC-004, Scaffolding Control

0PT-34.2.2.1, Fire Door, Pressure Boundary Door, ASSD Access/Egress Door, and Severe

Weather/Flood Control Door Inspections

0AI-68, Brunswick Nuclear Plant Response to Severe Weather Warnings

0PEP-02.1.1, Emergency Control-Notification of Unusual Event, Alert, Site Area Emergency,

and General Emergency

0PEP-02.6, Severe Weather

0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake

Nuclear Condition Reports

551646 551838 551964 550469 559173 556860

556861 556862 556863 556864 556865 556866

556867 556868 556869 556870 557375 555023

545354 553946

Work Orders

550098 550100 550102 550015 545859 545861

1828825 11828826 1643223 1775054 2113607

Attachment

12

Work Requests

546632 546540 546541 546543 544971 546174

546823 546824 546203 546274 546278

Drawings

D-11099, Reactor Building Miscellaneous Steel Pool Liners

D-2274, Diesel Cooling Water

D-25049, Reactor Building Piping Diagram Fuel Pool Cooling & Filtering System, Unit 1

D-26007, Reactor Building Fuel Pool Cooling & Filter System Plan EL 80-0 & Sections

D-26009, Reactor Building Fuel Pool Cooling & Filter System Miscellaneous Plans & Sections

D-27010, Supplemental Spent Fuel Pool Cooling System

F-25008, Reactor Building Arrangement & Details, Fuel Pool

D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2

D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2

D-11597, Backdraft Damper with Extra Deep Frame

F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping

LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room

North Wall

1-FP-09319, Reactor Building Railroad Doors

Corrective Action Document

PRR 562261, Revise EGR-NGGC-0209 to strengthen the tie to the License Renewal Program

Miscellaneous

Calculation 2RB2-0012, Analysis for Spent Fuel Pool - Elevation of Top of Active Fuel

Engineering Change 80408R0, Flooding Design Basis Update

EPRI Report 1025286, Seismic Walk-down Guidance for Resolution of Fukushima Near-Term

Task Force Recommendation 2.3: Seismic

FP-75090, International Instruments INC, Instruments, Switchboard, Edgewise

System Description SD-43, Service Water System

UFSAR Section 9.1.3.3, Fuel Pool Cooling and Cleanup System, Safety Evaluation

Units 1 and 2, Flood Protection Feature 6BL, Service Water Building, 4 Elevation, Pipe

Penetration Seal\20-8 Pipe Sleeves

Unit 1, SWEL 1 List

Unit 1, SWEL 2 List

Unit 2, SWEL 1 List

Unit 2, SWEL 2 List

URS Post Fukushima Project, NTTF Recommendation 2.3 Seismic Walk-down Training Record

URS Project Number 30703-007, Near Term Task Force Recommendation 2.3 Seismic Walk-

down Procedure

0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator

DBD-106, Hazards Analysis

Engineering Change 80408R0, Flooding Design Basis Update

Individual Plant Examination for External Events Submittal, June 1995

Link Seal Vendor Manual

Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality

SD-43, Service Water System

Attachment

13

URS List of Flood Features Inspected

URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007

Report Number 110311.401, Summary of Progress Energy Fleet Underground Piping and

Tanks with the Scope of NEI 09-14 (Rev. 1), prepared by Structural Integrity Associates,

Inc., dated 12/07/2011

Assessment Number 531636, Quick Hit Self Assessment for HNP and BNP Buried Piping

Program and the NRC TI-2515/182 Inspection, 08/15/2012

Specification 024-001 for Special Doors

Section 4OA7: Licensee-Identified Violations

Procedures

0PEP-02.1, Initial Emergency Actions

0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,

and General Emergency

0PEP-02.2.1, Emergency Action Level Bases

Nuclear Condition Reports

552815 552984

Drawings

1-FP-02039, General Electric Gas Control Piping Diagram

D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2

Miscellaneous

Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event

(After-the-Fact), August 2, 2012

NUREG-1022, Event Reporting Guidelines

Operator Logs, August 2, 2012

SD-59, Hydrogen Water Chemistry System

Attachment