ML19270G367: Difference between revisions
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{{#Wiki_filter:}} | {{#Wiki_filter:LICENSEE EVENT REPORT coNTnot BLOCK: I l l l l l lh (PLEASE PnlNT on TYPE ALL HEOUIRED INFOHMATioN) 1 6 Tl]8IG 9 I ALICENSEE I E liCODE lH l1 l@[0 14 15 101010 10 1010 10 10 lo 10 LICENSE hvP.*uEH 23 l@l aLICEP.:et 2h l 11 l14l PE il JJll@lbi L Al I *sel@ | ||
oN'T d] S | |||
.[",%lLl@l015l010l013l2Il l@l015 l ll 817191@L015121417 19 l@ #4 7b SJ 60 61 DOCK ET NUYJ g R eM bJ EVENT DATE REPOH T DATE EVENT DESCntPTioN AND PHOBACLE CONSEQUENCES h | |||
@ l While sht>1hn for refunling_.on c;-19 79 ; rinrinn the_pnrfnmnce_ of Local Leak Rate ! | |||
@ l Testino per procedure HNP-1-3957. it was discovered that RHR r_e_ turn valves Ell-F015B I | |||
@ l and E11-F0178. and RHR pump suction valves were leakino in excess of scecif *ed crit- I , | |||
v. | |||
l | |||
@ l eria. Since these valves are the inboard and outuvard containment isolation valve I | |||
@ l pairs for primary containment penetration X138 and X2048 resoectivelv. a of tential I | |||
@ I' leakage path from primary containment to secondary containment exists. Refer to: 1 | |||
' | |||
E I LERs 76-28, 77-34, 78-17, 79-27, 79-28. - | |||
1 8 9 , | |||
DE COCE SLBCO E COMPONENT CODE SUSC^ E N | |||
SU E l C lF l@ l X l@ [z_J @ l V l A l L l V l E l X l@ [X_j@ [_XJ @ | |||
: 8 9 10 11 12 IJ 18 19 20 SEQUENTI AL OCCUR R E NCE REPORT REVISION E E R /810 CVENT YE AR REPORT NO. CODE TYPE N O. | |||
'. | |||
, | |||
@ gP,OR E l7l9l | |||
_ 21 22 l-l 23 l0l'l31 24 26 | |||
[d] | |||
27 1011 l 25 29 lT 30 | |||
[-l 31 | |||
[0_j 32 AK f4 A t CI4 PL AT 'E H HOURS SO IT D FLPS nL&. SL P LI E 9.1 A FA UR R i LB_1@l 33 34 z l@ l35z l@ lzl@ 101010 01 37 Ly_J@ | |||
41 lYl@ N l@ 'lX l 9191947l@ | |||
' | |||
; | |||
' | |||
3G 40 42 43 44 CAUSE oESCnlPTION AN0 CORRECTIVE ACTIONS h | |||
@l The cause of tha unacenotabla inab gn ratas for +hnen v=1vne is undar invas+igatinn. I l | |||
@l i | |||
Valve maintenance is not comolete at this time. In order te ccmoly with Tech. Snec. I pl 4.7. A.2 9, corrective maintenance will be performed as reauired to allow a satisfac- 1 El tory leakage rate for each containment isolation valve. The *as found" leakafe for I | |||
. g i each valve that requires maintenance will be (continued) I g 9 80 STA 5 % POWER OTHER STATUS iO RY DeSovtRV OESCRIPTION M LtLj @ l 01 Olu l @ l N/A l l''B l@l Local Leak Rate Test I | |||
; ' '' " " ** * | |||
' JuviTY CO0 TENT REtEaSE AVOUNT OF ACTIVITY LOCnacN or RELEASE | |||
.E*[z_1 * @D ' Or RELE ASELZ_1@l N/A | |||
" | |||
l l | |||
'' | |||
N/X | |||
* l PERSONNE L ExPOSOES NOVBER TYPE DESCRIPTION * | |||
;T] 10 l'o 10 l@l z l@l N/A l | |||
* ' '' | |||
PEnSONNE L iNsu' dies | |||
'' ** | |||
: m SCR,,,,0N @ | |||
g NU .ER o 010l@l N/A 2274 272 l | |||
. | |||
8 9 11 12 80 l 'T55E | |||
' | |||
" &^CTf,L'? | |||
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@ 'l 9060 60}D | |||
@eW J 9 | |||
@l to N/A 80 l | |||
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, | |||
E [$ $$Ut8lDE CHIPT60N N/A l l1lll1IIIIIll2 i e9 to 68 69 .. 80 E T. V. keene, Supt. M t. Eng. Se W. ONWW l | |||
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. _ _ _ . . . . . . . _ . _ . . | |||
. . . | |||
. | |||
- | |||
Georgia Power Company Plant E. I. Hatch Baxicy, Georgia | |||
* | |||
~ | |||
. | |||
. | |||
. | |||
. | |||
Cause Description and Corrective Actions (continued) recorded and will be reported in the Leak Rate Report. required by Appen- ., | |||
dix J of 10CFR50. . | |||
. | |||
9 2274 273 | |||
. | |||
* | |||
. | |||
; | |||
- | |||
s | |||
. | |||
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. | |||
. | |||
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4 i | |||
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I | |||
- | |||
NARRATIVE | |||
==SUMMARY== | |||
.q - | |||
. | |||
, | |||
s ( | |||
, | |||
, Durins the 1979 Refueling Outage, Type B and C Local Leak Rate Tests (LLRT) will Le performed to ccmply with Tech. Specs. Sections 4.7.A.2.e and 4.7.A.2.F | |||
. | |||
, | |||
and Appendix J to 10CFR50. This will involve subjecting potential leak paths, j i.e. containment penetrations (Type B Test) and containment isolation valves (Type C Tests) to the same test conditions that would occur post-LOCA. | |||
Conducting local leak rate test (LLRTs) allow discovery and elimination of leak paths thru the containment without performing the Integrated Leak , | |||
Rate Test (Type A Test) each. refueling outage. , | |||
Since the primary concern in the containment leakage test program is tot-al containment leakage, no specific acceptance ' criteria is defined for an ' individual Type B or Type C LLRT (excluding MSIVs). However, the logis-tics used in determining an unsatisfactory LLRT encompasses several factors. | |||
The valve design, size, service, etc. are considered in order to maintain . | |||
the total containment penetration leakage within the acceptance criter- , | |||
ia without imposing an unrealistic -leakage rate limit on an individual valve. | |||
- | |||
2274 274 | |||
. | |||
. | |||
e | |||
. | |||
t l | |||
'l 1 | |||
, | |||
. | |||
g -.. ee.- | |||
' | |||
.}} |
Revision as of 19:12, 27 October 2019
ML19270G367 | |
Person / Time | |
---|---|
Site: | Hatch ![]() |
Issue date: | 05/24/1979 |
From: | Thomas Greene GEORGIA POWER CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
Shared Package | |
ML19270G366 | List: |
References | |
LER-79-033-01T, LER-79-33-1T, NUDOCS 7906060222 | |
Download: ML19270G367 (3) | |
Text
LICENSEE EVENT REPORT coNTnot BLOCK: I l l l l l lh (PLEASE PnlNT on TYPE ALL HEOUIRED INFOHMATioN) 1 6 Tl]8IG 9 I ALICENSEE I E liCODE lH l1 l@[0 14 15 101010 10 1010 10 10 lo 10 LICENSE hvP.*uEH 23 l@l aLICEP.:et 2h l 11 l14l PE il JJll@lbi L Al I *sel@
oN'T d] S
.[",%lLl@l015l010l013l2Il l@l015 l ll 817191@L015121417 19 l@ #4 7b SJ 60 61 DOCK ET NUYJ g R eM bJ EVENT DATE REPOH T DATE EVENT DESCntPTioN AND PHOBACLE CONSEQUENCES h
@ l While sht>1hn for refunling_.on c;-19 79 ; rinrinn the_pnrfnmnce_ of Local Leak Rate !
@ l Testino per procedure HNP-1-3957. it was discovered that RHR r_e_ turn valves Ell-F015B I
@ l and E11-F0178. and RHR pump suction valves were leakino in excess of scecif *ed crit- I ,
v.
l
@ l eria. Since these valves are the inboard and outuvard containment isolation valve I
@ l pairs for primary containment penetration X138 and X2048 resoectivelv. a of tential I
@ I' leakage path from primary containment to secondary containment exists. Refer to: 1
'
E I LERs 76-28, 77-34, 78-17, 79-27, 79-28. -
1 8 9 ,
DE COCE SLBCO E COMPONENT CODE SUSC^ E N
SU E l C lF l@ l X l@ [z_J @ l V l A l L l V l E l X l@ [X_j@ [_XJ @
- 8 9 10 11 12 IJ 18 19 20 SEQUENTI AL OCCUR R E NCE REPORT REVISION E E R /810 CVENT YE AR REPORT NO. CODE TYPE N O.
'.
,
@ gP,OR E l7l9l
_ 21 22 l-l 23 l0l'l31 24 26
[d]
27 1011 l 25 29 lT 30
[-l 31
[0_j 32 AK f4 A t CI4 PL AT 'E H HOURS SO IT D FLPS nL&. SL P LI E 9.1 A FA UR R i LB_1@l 33 34 z l@ l35z l@ lzl@ 101010 01 37 Ly_J@
41 lYl@ N l@ 'lX l 9191947l@
'
'
3G 40 42 43 44 CAUSE oESCnlPTION AN0 CORRECTIVE ACTIONS h
@l The cause of tha unacenotabla inab gn ratas for +hnen v=1vne is undar invas+igatinn. I l
@l i
Valve maintenance is not comolete at this time. In order te ccmoly with Tech. Snec. I pl 4.7. A.2 9, corrective maintenance will be performed as reauired to allow a satisfac- 1 El tory leakage rate for each containment isolation valve. The *as found" leakafe for I
. g i each valve that requires maintenance will be (continued) I g 9 80 STA 5 % POWER OTHER STATUS iO RY DeSovtRV OESCRIPTION M LtLj @ l 01 Olu l @ l N/A l lB l@l Local Leak Rate Test I
- ' " " ** *
' JuviTY CO0 TENT REtEaSE AVOUNT OF ACTIVITY LOCnacN or RELEASE
.E*[z_1 * @D ' Or RELE ASELZ_1@l N/A
"
l l
N/X
- l PERSONNE L ExPOSOES NOVBER TYPE DESCRIPTION *
- T] 10 l'o 10 l@l z l@l N/A l
- '
PEnSONNE L iNsu' dies
**
- m SCR,,,,0N @
g NU .ER o 010l@l N/A 2274 272 l
.
8 9 11 12 80 l 'T55E
'
" &^CTf,L'?
'^c"
@ 'l 9060 60}D
@eW J 9
@l to N/A 80 l
t *
,
E [$ $$Ut8lDE CHIPT60N N/A l l1lll1IIIIIll2 i e9 to 68 69 .. 80 E T. V. keene, Supt. M t. Eng. Se W. ONWW l
.
, NAur or PnEPAnEn ,n out.
{
5 e * *
, , E
. _ _ _ . . . . . . . _ . _ . .
. . .
.
-
Georgia Power Company Plant E. I. Hatch Baxicy, Georgia
~
.
.
.
.
Cause Description and Corrective Actions (continued) recorded and will be reported in the Leak Rate Report. required by Appen- .,
dix J of 10CFR50. .
.
9 2274 273
.
.
-
s
.
b
.
.
.. - !I
4 i
- -
I
-
NARRATIVE
SUMMARY
.q -
.
,
s (
,
, Durins the 1979 Refueling Outage, Type B and C Local Leak Rate Tests (LLRT) will Le performed to ccmply with Tech. Specs. Sections 4.7.A.2.e and 4.7.A.2.F
.
,
and Appendix J to 10CFR50. This will involve subjecting potential leak paths, j i.e. containment penetrations (Type B Test) and containment isolation valves (Type C Tests) to the same test conditions that would occur post-LOCA.
Conducting local leak rate test (LLRTs) allow discovery and elimination of leak paths thru the containment without performing the Integrated Leak ,
Rate Test (Type A Test) each. refueling outage. ,
Since the primary concern in the containment leakage test program is tot-al containment leakage, no specific acceptance ' criteria is defined for an ' individual Type B or Type C LLRT (excluding MSIVs). However, the logis-tics used in determining an unsatisfactory LLRT encompasses several factors.
The valve design, size, service, etc. are considered in order to maintain .
the total containment penetration leakage within the acceptance criter- ,
ia without imposing an unrealistic -leakage rate limit on an individual valve.
-
2274 274
.
.
e
.
t l
'l 1
,
.
g -.. ee.-
'
.