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| {{#Wiki_filter:C F O n'.1 'hG U. S. fJUCLL AH htGUL A IOHY CDY .it S';10*J 77lLICENSEE EVENT HEPORT comnot cLoco [_j_[_j_[_D @ | | {{#Wiki_filter:U. S. fJUCLL AH htGUL A IOHY CDY .it S';10*J C F O n'.1 'hG 77l LICENSEE EVENT HEPORT comnot cLoco [_j_[_j_[_D @ i (, |
| trLt Ast Pnifd OH TYPC ALL HEOUlHLO WI OnMArtOM i (,'ITl [G A_I f. [l I H [2_lC[0 J O_! 0 l 0 0 } Oj 0 l 0 l(L{0 0 j@[dI l1 (l [1_1GL f(T)s ;uct . a i.z. E i4 n uma r. . e | | trLt Ast Pnifd OH TYPC ALL HEOUlHLO WI OnMArtOM |
| .2 o uw.a is n.a s i vu . , - | | 'ITls ;[G A_I f. [l I H [2_lC[0 nJ O_! 0 l 0 uma |
| ..nr ,!@' IM'C$ l l }@l 015101010] 316 I C ]@l 016 L2jjlj 7 J1J@l017_]n_j r,17 lt s._.____a o u ou u.o .m-a umtm a n m .-m~tvc3a or scnierico aa rnocacu c,w. tot,E :ct @,J11 LAt 1220 CDT, MSIV Fast Closure Starton test for Unit 2 wa_s initiated.
| | . |
| Reactor[[scraved as a result of !'.SIV cl os u re. | | 0 } Oj 0 l 0 l(L{0 0 j@[dI l1 (l [1_1GL .a s i vu . , - |
| During the resulting transient, RCIC and E'CI J , 3l both isolated on steam line high dif ferential pressure. | | f(T) uct . a i.z. E i4 r. . e .2 o uw.a is n . |
| Technical specs 3/4. 7. 3. t; | | nr |
| _l, 4 1 and 3/4.5.1 Action A were met for both RCIC and HPCI respectively. | | ' IM 'C$ l l }@l 015101010] 316 I C ]@l |
| The ADS systc-lsl was operable and capable of performina its intended function. | | . 016umtm L2jjlj 7 J1J@l017_]n_j |
| Both the RCIC and EPCI j 2 c 7 ) I syste:"s were successfully started manually. | | __ _ |
| At time of occurrence Unit 1 was in cold l | | r,17 lt ,!@ |
| >I shutdown condition for maintenance, hanger modifications, and refueling.(continued) l o 83 ss$YS T E *.T CALSE C Mf S E COYP VALVE CCCE CCO ,, dCODt CCYSCNE NT CODE SUCCCCE SURCDDE ui[ s i r l@ l E l@ l E l@ l 11'Nl Si il RI U l@ [ S j@ l Z l @
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| pnia I C s /P C C ' r ^ '. r , , ACT,37 ptn'_./ C Ti U F L A *. T EinDa HOOns . . - | | tvc3a or scnierico aa rnocacu c,w. tot,E :ct @ |
| ;_'ili-)*wa s p i :.*un.: r-: TAKE*..l E lgl X j@ | | ,J11 LAt 1220 CDT, MSIV Fast Closure Starton test for Unit 2 wa_s initiated. Reactor [ |
| [ Aj@[C J@l Ol 1l C 2l[Y lQl N] g[NJ(glB l0 l1 l0 lg 33 s4_a.o 31 4g 41 42 42 4 47 cAust 0:n me ries e.o countcTrn. ;cncu @ | | , 3 |
| iit [RCIC and HPCI systems isolated on stem line hich differential pressure. | | [scraved as a result of !'.SIV cl os u re. |
| As systems j TIT] l isolated, they u,re man"111v started and later secured unon connletion of "SIV fx t.
| | During the resulting transient, RCIC and E'CI J |
| ]g l Closure startua test.
| | , 4 l both isolated on steam line high dif ferential pressure. Technical specs 3/4. 7. 3. t; _l s 1 and 3/4.5.1 Action A were met for both RCIC and HPCI respectively. The ADS systc- l 2 c l was operable and capable of performina its intended function. Both the RCIC and EPCI j |
| Test shop ocrsonnel were instructed to check calibration of 1 TF1 [ switches 2E51 ','017 and M018 (PCIC) and 2E4J-ND0 '. and N005 (HPCI). | | > |
| Calibrations for liTO 1 RCIC switches Pf 51 "Ol7 and N018 wore within acceatable rance.(continued) l8J 8 9 P.* E T " 'O C F | | 7 ) I syste:"s were successfully started manually. At time of occurrence Unit 1 was in cold l o I shutdown condition for maintenance, hanger modifications, and refueling. (continued) l 83 ss COYP |
| $ Artt,;v y, S1AIv,'' P; 7. E A 01 H f P '; T/.T L'S L;t ' ^ % r
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| * i Y DISCO'. f H Y C L " :4. P TIL | | ' |
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| | R E V t'; '7 "E QUE N11 AL OCCun R E P.CE PErCaT , |
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| | E V E *. T 4 E /. R FIE PQH i *.O CCOE TYPE NO l0l E |
| ,~a ...- , m Se 912- % / - 7 M 1 L'T.._V Grmno. Eupt Plt..Foo.-.rv.pa n, m -, , n tw iw n | | @ l(j:lP l=C') L7191 1-1 10 15 l9 l l/l 10 l 1 l lT l l-l |
| | _. : n u u 24 .o v 2 n 23 3, a< |
| | ACT,37 Er ;CT SHL' Dr / . ATT/ % 'T ' ' r O .; pnia I C s /P C C ' r ^ '. r , , |
| | TAKE*. ptn'_. |
| | / C Ti U F L A *. T EinDa HOOns . . - ; _'ili-) *wa s p i :. *un |
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| | l33E lgls4X j@ [ Aj@ [C J@ l Ol 1l C 31 2l [Y lQ 41 l N] g [NJ(g lB l0 l1 l0 lg 47 |
| | _a .o 4g 42 42 4 cAust 0:n me ries e.o countcTrn. ;cncu @ |
| | As systems j iit [RCIC and HPCI systems isolated on stem line hich differential pressure. |
| | TIT] l isolated, they u,re man"111v started and later secured unon connletion of "SIV fx t. ] |
| | g l Closure startua test. Test shop ocrsonnel were instructed to check calibration of 1 TF1 [ switches 2E51 ','017 and M018 (PCIC) and 2E4J-ND0 '. and N005 (HPCI). Calibrations for l iTO 1 RCIC switches Pf 51 "Ol7 and N018 wore within acceatable rance. (continued) l 8 9 8J |
| | $ Artt,;v y, P.* E T " 'O C F S1AIv, ''. P; 7. E A 01 H f P '; T/.T L'S L;t ' ^ % r |
| | * i Y DISCO'. f H Y C L " :4. P TIL s. |
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| | E LcjG) l010 Io J21 0 li N/A 41 l i Bl@L_ operator observatio" 43 g; I |
| | d il 13 ACTIVi1 Y C ON ! E f;T F~lE U!.D C5 * .fr' AYU'P.T Ot /.C T i V l1 Y D LGC AT!CN OT pr t t / r . |
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| | Grmno. Eupt Plt..Foo. -.rv. Se pa n, 912- % / - 7 M 1 L' |
| | |
| | Georgia . J.!"r Company Plant E. 1. Hatch Baxley, Georgia 3i,13 |
| | #. |
| | Evc- Dc,criptic, and Probable Co. sequences (continued) |
| | There have not been any simultaneous system isolations previously on the sub-ject RCIC a.:d HPCI systems on either Unit 1 or U-it 2. There were no per-sonnel injuries, overexposures, or any release of radioactive materials to the environment as a result of this occurrence. |
| | . |
| | Cause Description and Corrective Actions (continued) |
| | Cause of f<CIC isolation is not kncun at this . time and is under investigation by both utility and ::SSS supplier. Switch 2E41-:;035 setpoint was within acceptable range; however, switch '400'. was out of calibration. HPCI switch 2E41-l004 '.ms re-calibrated and returned to service. Opinion is diat switch calibration may not be sole cause of HPCI iso,latien and is also under in-vestigation. All switches involved are ITT Barton Model 253. Results of investigations and any followup testing will t;e reported in an updated LER. |
| | , |
| | w |
| | |
| | . |
| . | | . |
| Georgia . J.!"r Company Plant E. 1. Hatch Baxley, Georgia 3i,13#.Evc-Dc,criptic, and Probable Co. sequences (continued)
| | Narrative Report for LER 50-366/1979-59, Rev. 0 |
| There have not been any simultaneous system isolations previously on the sub-ject RCIC a.:d HPCI systems on either Unit 1 or U-it 2.
| | / |
| There were no per-sonnel injuries, overexposures, or any release of radioactive materials to the environment as a result of this occurrence.
| | # |
| .Cause Description and Corrective Actions (continued)
| | 9 On June 27,1979, at 1220 CDT, the MSIV Fast Closure startup test was init-iated for Hatch Unit 2. Initial reactor power das 975 (2365iMt). Reac-tor scram resulted due to MSIV clcsures. RCIC and IPCI systems isolated u.. steam line hirh differential pressure af Ler the reactor scram. Both systems were manually started by plant operatcrs. RCIC sys tem, af ter ran-ual start, ran throughout the duration of the M31V closure test. HPCI tras started at 1238 CDT to raise water level and was shut down at 1239 CDT by plant operator. |
| Cause of f<CIC isolation is not kncun at this . time and is under investigation by both utility and ::SSS supplier.
| | Immediate corrective actions initiated by plant operations personnel were to rianually start both RCIC and HPCI systems. Systems were successfully started manually. Redundant systems were available and capable of per-forming their intended functions. Test shop personnel were noti fied of the systers isolatien and were instructed to check calibration of steam line high differential pressure sJitches 2E51-N017 and N010 (RCIC)and 2E41-N004 and N005 (HPCI). |
| Switch 2E41-:;035 setpoint was within acceptable range; however, switch '400'. was out of calibration.
| | Test shop personnel found the calibration of the RCIC switchos to bc with- |
| HPCI switch 2E41-l004 '.ms re-calibrated and returned to service.
| | -in an acceptable range per procedure requirements. Cause-pf the RCIC sys-tc., isclatien on high dP is unkncun at this time and is under invcstigaticn by both utility and the NSSS supplier. |
| Opinion is diat switch calibration may not be sole cause of HPCI iso,latien and is also under in-vestigation.
| | Per the recocmendation of the NSSS supplier, instrurent piping for RCIC switches 2E51-N017 and N018 is being c.odified to correct piping gecaetry which could be a factor in the isolation of the systen The NRC resid;nt inspector was informed on 7-4-79, at 1010 CDT of the instrument piping mcd-ification. |
| All switches involved are ITT Barton Model 253.
| | HPCI high steam line differential pressure switches N004 and ND05 were checked for calibration. Switch 2Eal-N005 was found to be acceptable, hew-ever, switch N004 was out of calibration. Switch 2E41-N004 was recalibrat-ed and returned to service. Incorrect HPCI switch setpoint may not have been the sole cause of system isolation and will also be investigated. |
| Results of investigations and any followup testing will t;e reported in an updated LER.
| |
| , w
| |
| ..Narrative Report for LER 50-366/1979-59, Rev. 0
| |
| /#9 On June 27,1979, at 1220 CDT, the MSIV Fast Closure startup test was init-iated for Hatch Unit 2. | |
| Initial reactor power das 975 (2365iMt). | |
| Reac-tor scram resulted due to MSIV clcsures. | |
| RCIC and IPCI systems isolated steam line hirh differential pressure af Ler the reactor scram. | |
| Both u..systems were manually started by plant operatcrs. | |
| RCIC sys tem, af ter ran-ual start, ran throughout the duration of the M31V closure test. | |
| HPCI tras started at 1238 CDT to raise water level and was shut down at 1239 CDT by plant operator. | |
| Immediate corrective actions initiated by plant operations personnel were to rianually start both RCIC and HPCI systems. | |
| Systems were successfully started manually. | |
| Redundant systems were available and capable of per-forming their intended functions. | |
| Test shop personnel were noti fied of the systers isolatien and were instructed to check calibration of steam line high differential pressure sJitches 2E51-N017 and N010 (RCIC)and 2E41-N004 and N005 (HPCI). | |
| Test shop personnel found the calibration of the RCIC switchos to bc with--in an acceptable range per procedure requirements. | |
| Cause-pf the RCIC sys-tc., isclatien on high dP is unkncun at this time and is under invcstigaticn by both utility and the NSSS supplier. | |
| Per the recocmendation of the NSSS supplier, instrurent piping for RCIC switches 2E51-N017 and N018 is being c.odified to correct piping gecaetry which could be a factor in the isolation of the systen The NRC resid;nt inspector was informed on 7-4-79, at 1010 CDT of the instrument piping mcd-ification. | |
| HPCI high steam line differential pressure switches N004 and ND05 were checked for calibration. Switch 2Eal-N005 was found to be acceptable, hew-ever, switch N004 was out of calibration. | |
| Switch 2E41-N004 was recalibrat-ed and returned to service. | |
| Incorrect HPCI switch setpoint may not have been the sole cause of system isolation and will also be investigated. | |
| Upon completion of investigation of HPCI and FCIC isolation problem by utility and NSSS supplier, sunplemntal corrective actions will be taken and reported in an update to this LER. | | Upon completion of investigation of HPCI and FCIC isolation problem by utility and NSSS supplier, sunplemntal corrective actions will be taken and reported in an update to this LER. |
| At the time of the occurrence, Unit 1 was in a cold shutdu.:n condii n for maintenance, hanger modi ficaf ions , and refueling. | | At the time of the occurrence, Unit 1 was in a cold shutdu.:n condii n for maintenance, hanger modi ficaf ions , and refueling. Results of the Unit 2 investigation and corrective actions will be considered for application to Unit 1 systems. Previous failures of HPCI and RCIC systems on Unit 1 ind 2 uill be re-evaluated. |
| Results of the Unit 2 investigation and corrective actions will be considered for application to Unit 1 systems. | | ,}} |
| Previous failures of HPCI and RCIC systems on Unit 1 ind 2 uill be re-evaluated. | |
| ,}} | |
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Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E2071994-05-0909 May 1994 LER 94-004-00:on 940416,discovered That Surveillance Frequency for Sp 34SV-SUV-008-1S Not Correct for Seven Primary Containment Vent & Purge Valves Due to Personnel Error.Surveillance Brought Up to date.W/940509 Ltr ML20029C8681994-04-25025 April 1994 LER 94-003-00:on 940329,automatic Reactor Shutdown Occurred Due to Trip of Main Turbine.Caused by Loss of Main Generator Field Excitation.Damaged Main Generator Exciter Rotor replaced.W/940425 Ltr ML20029C6981994-04-19019 April 1994 LER 94-002-00:on 940325,personnel Error Resulted in ESF Actuations.Personnel Counseled & Trained & EDG Control Circuit Wire repaired.W/940419 Ltr ML20046D5941993-08-18018 August 1993 LER 93-006-00:on 930721,determined That Valves Could Not Be Closed by Use of Normal Motive Power Due to Inadequate Procedural Controls Resulting in Valve Actuators Being Set Up Improperly.Isolated Affected penetration.W/930818 Ltr ML20045H7441993-07-0909 July 1993 LER 93-012-00:on 930615,automatic Reactor Scram & Isolation of Inboard Group 2 PCIS Valves Occurred.Caused by Loose Packing Nut on Instrument Isolation Valve.Valve Repaired & Similar Installations on Units checked.W/930709 Ltr ML20045B0371993-06-10010 June 1993 LER 93-009-00:on 930514,scram Occurred When Mode Switch Moved to Run Position Due to Blown Fuses in Rps.Procedures 52PM-B21-005-1S,52PM-B21-005-2S & 52GM-MEL-007-0S Revised. W/930610 Ltr ML20045B0401993-06-10010 June 1993 LER 93-010-00:on 930514,unplanned ESF Actuation Occurred Due to Less That Adequate Procedures.Procedures 34SV-B21-001-1S & 34SV-B21-001-2S, MSIV Closure Instrument Functional Test revised.W/930610 Ltr ML20045B0761993-06-10010 June 1993 LER 93-011-00:on 930521,partial Group 1 Primary Containment Isolation Sys Actuation Occurred Due to Component Failure. MSLRM Returned to Svc,Failed electro-pneumatic Control Valve in MSIVs replaced.W/930610 Ltr ML20045B7111993-06-10010 June 1993 LER 93-005-00:on 930521,unplanned Insertion of Manual Scram Initiated Due to Personnel Error.Personnel Involved Temporarily Removed from License Duties & Being Subjected to Formal discipline.W/930610 Ltr ML20045A2121993-06-0303 June 1993 LER 93-008-00:on 930505,determined That B Train of SBGT Sys Had Been Inoperable.Caused by Procedure Error.C/As Included Bringing Missed Surveillances Up to Date,Revising Procedures & Counselling personnel.W/930603 Ltr ML20044F6021993-05-21021 May 1993 LER 93-007-01:on 930504,unplanned ESF Actuations Occurred. Caused by Inappropriate Jumper Placement by Plant Engineer. Personnel Performing LSFTs Made Aware of Event & Instructed Not to Install Jumpers on Relay Contact arms.W/930521 Ltr ML20044F5851993-05-18018 May 1993 LER 93-004-00:on 930419,isolation Valve Unexpectedly Closed While Trip Unit Was Tested.Cause for Valve Closing Undetermined.Logic of Trip Unit Correctly Configured to Prevent Closing.No Corrective Actions taken.W/930518 Ltr ML20044D5931993-05-15015 May 1993 LER 93-005-00:on 930414,fuse 1D11-A-f14B Blew,Resulting in Initiation of Train B of Both Standby Treatment Sys Units & Isolation of Damper B of Both Secondary Containments.Blown Fuse & Several Relays in Logic Replaced ML20044D4881993-05-14014 May 1993 LER 93-004-00:on 930414,unplanned ESF Sys Actuation Occurred When LPCI Valve Automatically Reclosed.Caused by Inadvertent Grounding of Logic Circuit,Resulting in Blown Fuse.Fuse Replaced & Operating Order Issued ML20044D1111993-05-10010 May 1993 LER 93-003-00:on 930412,determined That Monthly Operability Test for DG 1B Not Performed During Required Performance Window on 930328.Caused by Personnel Error.Surveillance Coordinator Aware of causes.W/930510 Ltr ML20044C9891993-05-0303 May 1993 LER 93-003-00:on 930407,scram Time Testing on All Control Rods Not Completed Prior to Exceeding 40% Rated Thermal Power.Caused by Personnel Error.Personnel Counseled & Procedures Will Be revised.W/930503 Ltr ML20024G6961991-04-25025 April 1991 LER 91-007-00:on 910326,unknown Inadequacy in Jumper Connection Results in Scram During Surveillance in Cold Shutdown.Cause Unknown.Functional Test Completed & Surveillance Procedure revised.W/910422 Ltr ML20024G7401991-04-24024 April 1991 LER 91-008-00:on 910327,main Steam Isolation Valve Local Leak Rate Test Failed Due to Normal Equipment Wear Resulting in Degradation of Valve Seating Surfaces.Valves Repaired & retested.W/910424 Ltr ML20029B0691991-03-0505 March 1991 LER 91-002-00:on 910203,partial Outboard Group 2 Primary Containment Isolation Sys Isolation Signal Resulted in Closure of Containment Isolation Valves.Caused by Failed Relay Coil.Coil replaced.W/910301 Ltr ML20029B0621991-02-26026 February 1991 LER 91-001-00:on 910129,determined That Setpoints for Condensate Storage Tank Level Switches Not Set to Initiate Required Transfer When 10,000 Gallons Water Available.Caused by Inadequate Documentation.Setpoints raised.W/910226 Ltr ML20028H8431991-01-27027 January 1991 LER 90-024-00:on 901228,pretreatment Monitoring Station Offgas Samples Not Collected & Analyzed within 4 H of Increased Fission Gas Release.Caused by Misinterpretation of Tech Specs.Personnel instructed.W/910125 Ltr ML20044A6411990-06-22022 June 1990 LER 90-011-00:on 900601,full Reactor Protection Sys Actuation Occurred When Mode Switch Moved to Run Position, Resulting in Scram Signal on MSIVs Less than 90% Open.Caused by Personnel Error.Individual counseled.W/900622 Ltr ML20043G7111990-06-15015 June 1990 LER 90-004-00:on 900521,personnel Error & FSAR Deviation Occurred & Resulted in Tech Spec Violation.Procedure 62CI-OCB-031-OS Incorrectly Directed Personnel to Periodically Open Airlock Doors.Memo issued.W/900615 Ltr ML20043G7141990-06-15015 June 1990 LER 90-009-00:on 900522,determined That Requirements of Tech Spec 3.14.2,Actions 105 & 107 Not Met.Caused by Inadequate Procedure.Normal Range Monitoring Sys Restored to Operable Status & Procedure 64CH-SAM-005-OS revised.W/900615 Ltr ML20043G7581990-06-0808 June 1990 LER 90-001-01:on 900112,component Failure & Inadequate Design Caused Group I Isolation & Scram W/Main Steamline Isolation Valves Less than 90% Open.Root Isolation Valves Replaced W/New Type of valve.W/900608 Ltr ML20043C7281990-05-31031 May 1990 LER 90-008-00:on 900505,determined That Reactor Vessel Head Vent Valves 1B21-F004 & 1B21-F005 Closed Contrary to Tech Spec 3.7.C.2.a(2) Requirements.Caused by Cognitive Personnel Error.Reactor Vessel Head Vent Valves reopened.W/900531 Ltr ML20043A5091990-05-14014 May 1990 LER 90-006-00:on 900418,discovered That Wiring Error Existed in Junction Box Leading to Strip Recorder That Resulted in Inadequate Tech Spec Surveillance.Caused by Personnel Error. Wiring Error Corrected & Personnel counseled.W/900514 Ltr ML20043A5131990-05-14014 May 1990 LER 90-007-00:on 900419,determined That Errors in Calculations for Measuring Feedwater Flow Resulted in Nonconservative Calibr of Flow Transmitters.Caused by Error in Design Calculation.Transmitters recalibr.W/900514 Ltr ML20042E6851990-04-27027 April 1990 LER 90-003-00:on 900328,reactor Scram & Group II Containment Isolation Occurred.Caused by Inadequate Procedure.Procedure Will Be Changed to Require Instruments to Be Pressurized to Process Pressure Before Valved Into svc.W/900423 Ltr ML20042E6841990-04-27027 April 1990 LER 90-005-00:on 900329,safety Relief Valves Experienced Setpoint Drift in Excess of Tolerance.Caused by corrosion- Induced Bonding of Surface Between Pilot Valve Disc & Seat. Valves refurbished.W/900424 Ltr ML20012D8861990-03-19019 March 1990 LER 99-004-00:on 900219,trip Setpoint for Isolation of Liquid Radwaste Effluent Line on Low Dilution Flow Not Set Correctly.Caused by Inadequate Procedure.Procedure Revised temporarily.W/900319 Ltr ML20012C2891990-03-12012 March 1990 LER 90-003-00:on 900212,determined That Surveillance Procedures for Monthly Functional Testing of Drywell High Pressure Instrumentation Logic Channels Less than Adequate. Caused by Personnel Error.Procedures revised.W/900312 Ltr ML20011F4291990-02-26026 February 1990 LER 90-002-00:on 900131,discovered That Functional Test of Turbine Stop Valve Position Limit Switches Not Performed. Caused by Personnel Error When Writing Recent Rev.Rev to Procedure 34SV-C71-001-1S/2S written.W/900226 Ltr ML20006E2891990-02-0707 February 1990 LER 90-001-00:on 900112,reactor Scrammed Because MSIVs Were Less than 90% Open.Caused by Component Failure & Configuration of Condenser Vacuum Sensing Lines & Instruments.Valves replaced.W/900207 Ltr ML20006E0111990-02-0606 February 1990 LER 90-002-00:on 900114,RWCU Experienced High Differential Flow,Indicating Possibility of Leak in Sys.Caused by Component Failure & Less than Adequate Mounting for Relay. Relay Replaced W/Time Delay relay.W/900206 Ltr ML20006A8881990-01-22022 January 1990 LER 90-001-00:on 900104,HPCI Pump Declared Inoperable Due to Rated Flow Not Maintained During Surveillance Testing. Caused by Component Failure.Defective Resistor Replaced & Procedure 34SV-E41-002-1S performed.W/900122 Ltr ML20005E6541990-01-0202 January 1990 LER 89-010-00:on 891204,determined That Plant Was Not Fully Meeting Surveillance Requirements of Tech Spec Table 4.3.6.4-1,item 10.b.Caused by Inadequate Procedure.Recorder Calibr Steps to Be Removed from procedure.W/900102 Ltr ML20005E1851989-12-27027 December 1989 LER 89-009-00:on 891129,reactor Protection Sys Actuation Occurred from Scram Discharge Vol High Level Condition. Caused by Equipment Failure.Backup Temporary Air Compressor Placed Into Svc & Blown Fuse replaced.W/891227 Ltr ML20005E5131989-12-22022 December 1989 LER 89-017-00:on 891128,discovered That Efficiency Factors Used for Old Liquid Radwaste Discharge Radiation Monitors Incorrect.Caused by Personnel Not Incorporating Updated Efficiency Factor Into Sys software.W/891222 Ltr ML19332F8691989-12-14014 December 1989 LER 89-018-00:on 891114,sys High Differential Flow Condition Occurred Causing Actuation of Primary Containment Isolation Sys Valve Group 5 Logic Resulting in Closure of RWCU Valve. Caused by Personnel Error.Personnel counseled.W/891214 Ltr ML19332E6141989-11-30030 November 1989 LER 89-016-00:on 891103,discovered That Procedures 57SV-C51-001-1/2S Did Not Fully Test Rod Block Monitor Function.Caused by Procedural Deficiency.Limiting Condition for Operation Initiated & Procedure revised.W/891130 Ltr ML19332D8791989-11-29029 November 1989 LER 89-008-00:on 891102,RWCU Sys Experienced Partial Primary Containment Isolation Sys Group 5 Isolation Involving Valve 2G31-F004.Caused by Component Failure of Relay 2G31-R616D. Relay replaced.W/891129 Ltr ML19324C3271989-11-0808 November 1989 LER 89-014-00:on 891010,primary Containment Isolation Sys Group 5 Isolation Occurred Due to Opening of Valve 1G31-D002A.Caused by Personnel Error.Personnel Counseled & Memo Issued Re Confirming commands.W/891108 Ltr ML19325F1781989-11-0606 November 1989 LER 89-015-00:on 891009,diesel Generator 1R43-S001B Failed to Start Manually During Monthly Generator Test.Caused by Personnel Error & Incorrect Model Number Assigned to Pump. Pump Replaced & Oil Drained from cylinders.W/891106 Ltr ML19332B6191989-10-31031 October 1989 LER 89-013-00:on 891003,RWCU Sys Valve 1G31-F020 Closed, Rendering Inservice Reactor Coolant Monitor Inoperable. Caused by Cognitive Personnel error.In-line Conductivity Surveillance Initiated & Personnel counseled.W/891031 Ltr ML19325E6911989-10-31031 October 1989 LER 89-012-00:on 891003,plant Operators Received Indication That RWCU Sys Experiencing High Differential Flow Which Resulted in Isolation of Primary Containment Isolation Sys Valves.Caused by Component failure.W/891031 Ltr ML19327B3281989-10-23023 October 1989 LER 89-007-00:on 890926,four Safety Relief Valves Had Exhibited Drift in Mechanical Lift Setpoints in Excess of 3% Tolerance Specified by Inservice Testing Requirements.Root Cause Being Investigated.Valves refurbished.W/891023 Ltr ML19327B2991989-10-23023 October 1989 LER 89-006-00:on 890926,Procedure 34SV-SUV-019-2S, Surveillance Checks Did Not Fully Implement Requirements of Tech Spec Table 4.3.2-1.Caused by Personnel Error. Personnel Counseled & Procedure revised.W/891023 Ltr ML20024F4081983-09-0101 September 1983 LER 83-079/03L-0:on 830809,main Steam Line & Reactor Water Sample Valve Relay 1A71-K7A Determined Operating in Degraded Mode.Caused by Component Failure.Coil & Contacts Replaced. W/830901 Ltr ML20024F3341983-09-0101 September 1983 LER 83-064/03L-0:on 830811,during post-maint Review of DCR 83-76 Determined Torus Vent Valves Instrument Air Piping Returned to Svc W/O Performance of HNP-6907.Caused by Personnel oversight.W/830901 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D3061999-10-13013 October 1999 SER Accepting Licensee Proposed Changes to Edwin I Hatch Nuclear Plant Emergency Classification Scheme to Add Emergency Action Levels Related to Operation of Independent Spent Fuel Storage Installation HL-5845, Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Ei Hatch Nuclear Plant.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A6641999-09-13013 September 1999 Safety Evaluation Authorizing Relief Request RR-V-16 for Third 10 Yr Interval Inservice Testing Program HL-5836, Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Edwin I Hatch Nuclear Plant.With ML20210J9631999-08-0202 August 1999 SER Finding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20210J9271999-08-0202 August 1999 SER Finds That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves at Plant,Susceptible to Pressure Locking or Thermal Binding HL-5818, Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5805, Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207E7631999-06-0303 June 1999 Safety Evaluation Concluding That Licensee Proposed Alternative to Use Code Case N-509 Contained in RR-4 Provides Acceptable Level of Quality & Safety.Considers Rev 2 to RR-4 & RR-6 Acceptable HL-5795, Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ehnp Units 1 & 2. with ML20206G1691999-05-0404 May 1999 SER Approving Requirements of Istb 4.6.2(b) Pursuant to 10CFR50.55a(a)(3)(ii) HL-5784, Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5766, Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20207M1891999-03-11011 March 1999 SER Accepting Relief Request for Authorization of Alternative Reactor Pressure Vessel Exam for Circumferential Weld HL-5755, Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20206P6981999-01-0707 January 1999 Ehnp Intake Structure Licensing Rept HL-5726, Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20196J4931998-12-0707 December 1998 Safety Evaluation Accepting Proposed Alternatives in Relief Requests RR-V-12,RR-V-15,RR-P-15,RR-V-7,RR-V-12,RR-V-14 & RR-V-15 HL-5714, Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With HL-5706, Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Hatch Nuclear Plant Units 1 & 2.With ML20155B6121998-10-28028 October 1998 Safety Evaluation of TR SNCH-9501, BWR Steady State & Transient Analysis Methods Benchmarking Topical Rept. Rept Acceptable HL-5691, Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Ei Hatch Nuclear Plant,Units 1 & 2.With ML20153G2481998-09-24024 September 1998 SE Concluding That Licensee Implementation Program to Resolve USI A-46 at Plant Adequately Addressed Purpose of 10CFR50.54(f) Request ML20239A2531998-09-0303 September 1998 SER Accepting Licensee Request for Relief Numbers RR-17 & RR-18 for Edwin I Hatch Nuclear Plant,Units 1 & 2.Technical Ltr Rept on Third 10-year Interval ISI Request for Reliefs for Plant,Units 1 & 2 Encl HL-5675, Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20238F7131998-08-31031 August 1998 9,change 2 to QAP 1.0, Organization HL-5667, Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5657, Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures1998-07-30030 July 1998 Ro:On 980626,noted That Pami Channels Had Been Inoperable for More than Thirty Days.Cause Indeterminate.Licensee Will Replace Automatic Function W/Five Other Qualified Pamis of Like Kind in Drywell & Revised Procedures ML20236W3441998-07-30030 July 1998 Safety Evaluation Accepting Relief Requests for Second 10-yr ISI for Plant,Units 1 & 2 ML20236V5191998-07-28028 July 1998 Safety Evaluation Accepting Proposed License Amend Power Uprate Review ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L1821998-07-0707 July 1998 Safety Evaluation Accepting 980428 Proposed Alternative to ASME Boiler & Pressure Vessel Code,Section Xi,Repair & Replacement Requirements Under 10CFR50.55a(a)(3) HL-5653, Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5640, Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20248B8651998-05-15015 May 1998 Quadrennial Simulator Certification Rept HL-5628, Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant1998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Ei Hatch Nuclear Plant HL-5604, Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20216B2711998-02-28028 February 1998 Extended Power Uprate Safety Analysis Rept for Ei Hatch Plant,Units 1 & 2 HL-5585, Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5571, Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 11998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Edwin I Hatch Nuclear Plant,Unit 1 HL-5551, Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 ML20199B0561997-12-31031 December 1997 Rev 0 GE-NE-B13-01869-122, Jet Pump Riser Weld Flaw Evaluation Handbook for Hatch Unit 1 HL-5581, Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 21997-12-31031 December 1997 Annual Operating Rept for 1997, for Ei Hatch Nuclear Plant Units 1 & 2 HL-5533, Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 21997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Ei Hatch Nuclear Plant,Units 1 & 2 HL-5514, Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 21997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Edwin I Hatch Nuclear Plant,Units 1 & 2 ML20212A1981997-10-16016 October 1997 Safety Evaluation Denying Licensee Request for Relief from Implementation of 10CFR50.55a Requirements Re Use of 1992 Edition of ASME Code Section XI for ISI of Containments ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20211H5311997-10-0101 October 1997 Rev 2 to Unit 1,Cycle 17 Colr ML20211H5251997-10-0101 October 1997 Rev 3 to Unit 1,Cycle 17 Colr 1999-09-30
[Table view] |
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,J11 LAt 1220 CDT, MSIV Fast Closure Starton test for Unit 2 wa_s initiated. Reactor [
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[scraved as a result of !'.SIV cl os u re.
During the resulting transient, RCIC and E'CI J
, 4 l both isolated on steam line high dif ferential pressure. Technical specs 3/4. 7. 3. t; _l s 1 and 3/4.5.1 Action A were met for both RCIC and HPCI respectively. The ADS systc- l 2 c l was operable and capable of performina its intended function. Both the RCIC and EPCI j
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7 ) I syste:"s were successfully started manually. At time of occurrence Unit 1 was in cold l o I shutdown condition for maintenance, hanger modifications, and refueling. (continued) l 83 ss COYP
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As systems j iit [RCIC and HPCI systems isolated on stem line hich differential pressure.
TIT] l isolated, they u,re man"111v started and later secured unon connletion of "SIV fx t. ]
g l Closure startua test. Test shop ocrsonnel were instructed to check calibration of 1 TF1 [ switches 2E51 ','017 and M018 (PCIC) and 2E4J-ND0 '. and N005 (HPCI). Calibrations for l iTO 1 RCIC switches Pf 51 "Ol7 and N018 wore within acceatable rance. (continued) l 8 9 8J
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Evc- Dc,criptic, and Probable Co. sequences (continued)
There have not been any simultaneous system isolations previously on the sub-ject RCIC a.:d HPCI systems on either Unit 1 or U-it 2. There were no per-sonnel injuries, overexposures, or any release of radioactive materials to the environment as a result of this occurrence.
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Cause Description and Corrective Actions (continued)
Cause of f<CIC isolation is not kncun at this . time and is under investigation by both utility and ::SSS supplier. Switch 2E41-:;035 setpoint was within acceptable range; however, switch '400'. was out of calibration. HPCI switch 2E41-l004 '.ms re-calibrated and returned to service. Opinion is diat switch calibration may not be sole cause of HPCI iso,latien and is also under in-vestigation. All switches involved are ITT Barton Model 253. Results of investigations and any followup testing will t;e reported in an updated LER.
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Narrative Report for LER 50-366/1979-59, Rev. 0
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9 On June 27,1979, at 1220 CDT, the MSIV Fast Closure startup test was init-iated for Hatch Unit 2. Initial reactor power das 975 (2365iMt). Reac-tor scram resulted due to MSIV clcsures. RCIC and IPCI systems isolated u.. steam line hirh differential pressure af Ler the reactor scram. Both systems were manually started by plant operatcrs. RCIC sys tem, af ter ran-ual start, ran throughout the duration of the M31V closure test. HPCI tras started at 1238 CDT to raise water level and was shut down at 1239 CDT by plant operator.
Immediate corrective actions initiated by plant operations personnel were to rianually start both RCIC and HPCI systems. Systems were successfully started manually. Redundant systems were available and capable of per-forming their intended functions. Test shop personnel were noti fied of the systers isolatien and were instructed to check calibration of steam line high differential pressure sJitches 2E51-N017 and N010 (RCIC)and 2E41-N004 and N005 (HPCI).
Test shop personnel found the calibration of the RCIC switchos to bc with-
-in an acceptable range per procedure requirements. Cause-pf the RCIC sys-tc., isclatien on high dP is unkncun at this time and is under invcstigaticn by both utility and the NSSS supplier.
Per the recocmendation of the NSSS supplier, instrurent piping for RCIC switches 2E51-N017 and N018 is being c.odified to correct piping gecaetry which could be a factor in the isolation of the systen The NRC resid;nt inspector was informed on 7-4-79, at 1010 CDT of the instrument piping mcd-ification.
HPCI high steam line differential pressure switches N004 and ND05 were checked for calibration. Switch 2Eal-N005 was found to be acceptable, hew-ever, switch N004 was out of calibration. Switch 2E41-N004 was recalibrat-ed and returned to service. Incorrect HPCI switch setpoint may not have been the sole cause of system isolation and will also be investigated.
Upon completion of investigation of HPCI and FCIC isolation problem by utility and NSSS supplier, sunplemntal corrective actions will be taken and reported in an update to this LER.
At the time of the occurrence, Unit 1 was in a cold shutdu.:n condii n for maintenance, hanger modi ficaf ions , and refueling. Results of the Unit 2 investigation and corrective actions will be considered for application to Unit 1 systems. Previous failures of HPCI and RCIC systems on Unit 1 ind 2 uill be re-evaluated.
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