PNO-III-88-090, on 881031,5,000 Gallons of Liquid Radwaste Leaked Through Failed Seal on Radwaste Evaporator HX in Radwaste Bldg.Util Drained Water Out of Radwaste Room & Decontaminated Affected Areas.No Liquid Entered Drain Sewer
ML20205P410 | |
Person / Time | |
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Site: | LaSalle |
Issue date: | 11/02/1988 |
From: | Greger R, Paul R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
References | |
PNO-III-88-090, PNO-III-88-90, NUDOCS 8811080116 | |
Download: ML20205P410 (1) | |
Similar Documents at LaSalle | |
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Category:PRELIMINARY NOTIFICATION OF EVENT OR OCCURRENCE (PNO
MONTHYEARPNO-III-99-020, on 990409,Unit 2 Had Been Shut Down Since Sept 1996 for Refueling Outage That Was Extended in Order to Address Extensive Equipment Condition.Util Completed Comprehensive Corrective Action Program1999-04-13013 April 1999
[Table view]PNO-III-99-020:on 990409,Unit 2 Had Been Shut Down Since Sept 1996 for Refueling Outage That Was Extended in Order to Address Extensive Equipment Condition.Util Completed Comprehensive Corrective Action Program PNO-III-98-047, on 981005,diver Lost Consciousness While in Unit 2 Suppression Pool.Diver Received Minor Contamination on Hair During Removal of Mask & Diving Suit.Diver Was Successfully Decontaminated1998-10-0606 October 1998 PNO-III-98-047:on 981005,diver Lost Consciousness While in Unit 2 Suppression Pool.Diver Received Minor Contamination on Hair During Removal of Mask & Diving Suit.Diver Was Successfully Decontaminated PNO-III-98-037, on 980724,Region III Issued Ltr to Util Indicating Sufficient Improvements Made to Support Unit 1 Restart.Unit 2 Will Remain Shut Down for Continuing Mods & Performance Improvement Activities1998-07-24024 July 1998 PNO-III-98-037:on 980724,Region III Issued Ltr to Util Indicating Sufficient Improvements Made to Support Unit 1 Restart.Unit 2 Will Remain Shut Down for Continuing Mods & Performance Improvement Activities PNO-III-97-096, on 971211,unloaded Handgun & Ammunition Found in Brief Case of Il Resident Inspector.Inspector Placed on Administrative Leave & Il State Police Performing Investigation1997-12-11011 December 1997 PNO-III-97-096:on 971211,unloaded Handgun & Ammunition Found in Brief Case of Il Resident Inspector.Inspector Placed on Administrative Leave & Il State Police Performing Investigation PNO-III-97-038, on 970423,Com Ed Announced Delay in Planned Startup of Lasalle Nuclear Power Station Until Spring 1998. Schedule Change Will Result in Initial Laying Off of Contract Workers Out of Contract Work Force at Site1997-04-24024 April 1997 PNO-III-97-038:on 970423,Com Ed Announced Delay in Planned Startup of Lasalle Nuclear Power Station Until Spring 1998. Schedule Change Will Result in Initial Laying Off of Contract Workers Out of Contract Work Force at Site PNO-III-97-030, on 970327,five of Six Simulator Crews Rated Unsatisfactory by Licensee & of 31 Operators Six passed,18 Failed as Individuals & Seven Failed Because of Crew. Operators That Failed Were Suspended1997-04-0303 April 1997 PNO-III-97-030:on 970327,five of Six Simulator Crews Rated Unsatisfactory by Licensee & of 31 Operators Six passed,18 Failed as Individuals & Seven Failed Because of Crew. Operators That Failed Were Suspended PNO-III-97-025, on 970311,licensee Declared Unusual Event After Determining,Water Level in LaSalle Lake Exceeded Plant Design Limits.Nrc Resident Inspectors Will Continue to Monitor Licensee Activities1997-03-14014 March 1997 PNO-III-97-025:on 970311,licensee Declared Unusual Event After Determining,Water Level in LaSalle Lake Exceeded Plant Design Limits.Nrc Resident Inspectors Will Continue to Monitor Licensee Activities PNO-III-96-074, on 961213,licensee Planned to Extend Outages for LaSalle Units to Address Operational & Engineering Issues Identified.Team Also Raised Some Concerns in Area of Plant1996-12-18018 December 1996 PNO-III-96-074:on 961213,licensee Planned to Extend Outages for LaSalle Units to Address Operational & Engineering Issues Identified.Team Also Raised Some Concerns in Area of Plant PNO-III-96-063A, on 961003,extension of Forced Outage & Special Insp Team Dispatched Update Made.Unit Shut Down on 960922 to Repair Turbine Control Valve1996-10-0404 October 1996 PNO-III-96-063A:on 961003,extension of Forced Outage & Special Insp Team Dispatched Update Made.Unit Shut Down on 960922 to Repair Turbine Control Valve PNO-III-93-052, on 930914,reactor Scram & Concurrent Loss of Offsite Power Occurred Caused by Failure of Station Auxiliary Transformer.Power Was Supplied & Two of Three Emergency Diesels Restored to Standby Condition1993-09-14014 September 1993 PNO-III-93-052:on 930914,reactor Scram & Concurrent Loss of Offsite Power Occurred Caused by Failure of Station Auxiliary Transformer.Power Was Supplied & Two of Three Emergency Diesels Restored to Standby Condition PNO-III-92-043, on 920827,while Unit 2 Reducing Power to 800 Mw,Turbine Tripped Due to Thrust Bearing Wear Detector Signal.Several Equipment Problems Occurred Following Scram. Operators Successfully Established Steam Flow to Condenser1992-08-27027 August 1992 PNO-III-92-043:on 920827,while Unit 2 Reducing Power to 800 Mw,Turbine Tripped Due to Thrust Bearing Wear Detector Signal.Several Equipment Problems Occurred Following Scram. Operators Successfully Established Steam Flow to Condenser PNO-III-89-057, on 890826,reactor Scrammed from 10 Percent Power,Apparently as Result of Pressure Spike in First Stage of Turbine1989-08-28028 August 1989 PNO-III-89-057:on 890826,reactor Scrammed from 10 Percent Power,Apparently as Result of Pressure Spike in First Stage of Turbine PNO-III-89-050, on 890801,turbine-driven Reactor Feedwater Pump B Acted Erratically When Operator Changed Level Control & Placed Pump Into Automatic.Recirculation Pump a Tripped to Permit Opening of Flow Control Valve.Cause Under Review1989-08-0202 August 1989 PNO-III-89-050:on 890801,turbine-driven Reactor Feedwater Pump B Acted Erratically When Operator Changed Level Control & Placed Pump Into Automatic.Recirculation Pump a Tripped to Permit Opening of Flow Control Valve.Cause Under Review PNO-III-89-050A, on 890801,turbine Driven Reactor Feedwater Pump B Started to Act Erratically While Operating at 98% Power.Licensee Currently Investigating Cause of Problem.Flow Control Valve Opened & Recirculation Pump a Restarted1989-08-0202 August 1989 PNO-III-89-050A:on 890801,turbine Driven Reactor Feedwater Pump B Started to Act Erratically While Operating at 98% Power.Licensee Currently Investigating Cause of Problem.Flow Control Valve Opened & Recirculation Pump a Restarted PNO-III-89-016A, on 890306,Unit 1 Returned to Operation Following Reactor Scram on 890302.Unit 2 Remained in Operation & Unit 2 Station Auxiliary Transformer,Which Failed on 890302,repaired & Returned to Svc1989-03-0606 March 1989 PNO-III-89-016A:on 890306,Unit 1 Returned to Operation Following Reactor Scram on 890302.Unit 2 Remained in Operation & Unit 2 Station Auxiliary Transformer,Which Failed on 890302,repaired & Returned to Svc PNO-III-89-016, on 890303,Unit 1 Reactor Scrammed from 86% Power as Result of Turbine Trip,Which Appeared to Be Related to Fault in Unit 2 Sys Auxiliary Transformer. Unit 1 Expected to Remain Shut Down for Three Days1989-03-0303 March 1989 PNO-III-89-016:on 890303,Unit 1 Reactor Scrammed from 86% Power as Result of Turbine Trip,Which Appeared to Be Related to Fault in Unit 2 Sys Auxiliary Transformer. Unit 1 Expected to Remain Shut Down for Three Days PNO-III-88-090, on 881031,5,000 Gallons of Liquid Radwaste Leaked Through Failed Seal on Radwaste Evaporator HX in Radwaste Bldg.Util Drained Water Out of Radwaste Room & Decontaminated Affected Areas.No Liquid Entered Drain Sewer1988-11-0202 November 1988 PNO-III-88-090:on 881031,5,000 Gallons of Liquid Radwaste Leaked Through Failed Seal on Radwaste Evaporator HX in Radwaste Bldg.Util Drained Water Out of Radwaste Room & Decontaminated Affected Areas.No Liquid Entered Drain Sewer PNO-III-88-018A, on 880309,technician Error Resulted in Both Recirculation Pumps Tripping Followed by Isolation of Steam Supply to Feedwater Heaters.Reactor Tripped When Power Spike Reached 118% Setpoint on High Aprm.No Fuel Damage Occurred1988-03-17017 March 1988 PNO-III-88-018A:on 880309,technician Error Resulted in Both Recirculation Pumps Tripping Followed by Isolation of Steam Supply to Feedwater Heaters.Reactor Tripped When Power Spike Reached 118% Setpoint on High Aprm.No Fuel Damage Occurred PNO-III-88-018, on 880309,reactor Scrammed.Caused by Technician Error.Licensee Elected to Place Unit in Cold Shutdown for Various Maint Activities.State of Il & NRC Notified1988-03-10010 March 1988 PNO-III-88-018:on 880309,reactor Scrammed.Caused by Technician Error.Licensee Elected to Place Unit in Cold Shutdown for Various Maint Activities.State of Il & NRC Notified PNO-III-87-153, on 871216,during Testing of Closing Function of Eight Msivs,Outboard MSIV on Steam Line C Opened, Indicating Fast Closure Solenoid Malfunctioned.Solenoids Replaced on Affected Misv.Investigation Continuing1987-12-21021 December 1987 PNO-III-87-153:on 871216,during Testing of Closing Function of Eight Msivs,Outboard MSIV on Steam Line C Opened, Indicating Fast Closure Solenoid Malfunctioned.Solenoids Replaced on Affected Misv.Investigation Continuing PNO-III-87-151, on 871209,licensee Identified Leak on Reactor Feed Pump B Min Flow Line to Condenser.Cause Unknown. Feedwater Pumps Visually Inspected.Power to Unit 2 Reduced to Take Pump out-of-svc for Closer Insp1987-12-11011 December 1987 PNO-III-87-151:on 871209,licensee Identified Leak on Reactor Feed Pump B Min Flow Line to Condenser.Cause Unknown. Feedwater Pumps Visually Inspected.Power to Unit 2 Reduced to Take Pump out-of-svc for Closer Insp PNO-III-87-081, on 870610,earthquake Measuring 5.0 on Richter Scale Occurred Near Lawrenceville,Il.Unusual Events Declared by Six Power Stations But No Damage Observed.Ground Motion Felt at Five Other Plants1987-06-11011 June 1987 PNO-III-87-081:on 870610,earthquake Measuring 5.0 on Richter Scale Occurred Near Lawrenceville,Il.Unusual Events Declared by Six Power Stations But No Damage Observed.Ground Motion Felt at Five Other Plants PNO-III-87-046, on 870228,radwaste Shipment Driver Arrested for Driving While Intoxicated After Truck Slid Off Roadway While Being Parked.Replacement Driver Sent.Truck Surveyed & Escorted Back to Plant Site1987-03-31031 March 1987 PNO-III-87-046:on 870228,radwaste Shipment Driver Arrested for Driving While Intoxicated After Truck Slid Off Roadway While Being Parked.Replacement Driver Sent.Truck Surveyed & Escorted Back to Plant Site PNO-III-87-041, on 870319,turbine Tripped & Caused Reactor Scram.Caused by Fault in 6.9-kV & 4,160-volt Lines from Auxiliary Transformer to in-house Busses.Fault Also Caused Arcing & Burning of Busses.Fire Extinquished1987-03-20020 March 1987 PNO-III-87-041:on 870319,turbine Tripped & Caused Reactor Scram.Caused by Fault in 6.9-kV & 4,160-volt Lines from Auxiliary Transformer to in-house Busses.Fault Also Caused Arcing & Burning of Busses.Fire Extinquished PNO-III-87-021, on 870206,unit Shut Down to Repair Crack in Weld in Hydraulic Control Sys for Reactor Recirculation Sys Flow Control Valve 1B.Leak Identified on 870204.Repair Completed & Reactor Returned to Operation on 8702091987-02-0909 February 1987 PNO-III-87-021:on 870206,unit Shut Down to Repair Crack in Weld in Hydraulic Control Sys for Reactor Recirculation Sys Flow Control Valve 1B.Leak Identified on 870204.Repair Completed & Reactor Returned to Operation on 870209 PNO-III-86-149, on 861217,seal on motor-driven Feedwater Pump Failed While Pump Was Being Started,Causing Leak of About 200 Gallons Per Minute.Water Was Drained to Radwaste Water Treatment Sys1986-12-17017 December 1986 PNO-III-86-149:on 861217,seal on motor-driven Feedwater Pump Failed While Pump Was Being Started,Causing Leak of About 200 Gallons Per Minute.Water Was Drained to Radwaste Water Treatment Sys PNO-III-86-079, on 860807,Region III Authorized Restart, Lifting 860602 Hold on Operation Imposed Due to Reactor Water Level Switch Problem.On 860806,IE Decision Issued in Response to Seneca,Il 2.206 Petition Re Emergency Plan1986-08-0808 August 1986 PNO-III-86-079:on 860807,Region III Authorized Restart, Lifting 860602 Hold on Operation Imposed Due to Reactor Water Level Switch Problem.On 860806,IE Decision Issued in Response to Seneca,Il 2.206 Petition Re Emergency Plan PNO-III-86-075, on 860731,village of Seneca,Il Filed Suit Against NRC to Prevent Resumption of Facility Operation.Suit Cites Alleged Shortcomings in Emergency Planning Activities & Troubled Performance Record1986-08-0101 August 1986 PNO-III-86-075:on 860731,village of Seneca,Il Filed Suit Against NRC to Prevent Resumption of Facility Operation.Suit Cites Alleged Shortcomings in Emergency Planning Activities & Troubled Performance Record PNO-III-86-058, on 860620,town of Seneca,Il Withdrew from Emergency Planning for Facility.Mayor Requests That Plant Not Be Permitted to Resume Operations Until Valid Emergency Plan Developed1986-06-20020 June 1986 PNO-III-86-058:on 860620,town of Seneca,Il Withdrew from Emergency Planning for Facility.Mayor Requests That Plant Not Be Permitted to Resume Operations Until Valid Emergency Plan Developed PNO-III-86-052B, on 860601,reactor Level Switches Failed to Actuate Properly.Testing of Operability of Switches Begun. Licensee Declared All ECCS Inoperable for Both Units1986-06-0909 June 1986 PNO-III-86-052B:on 860601,reactor Level Switches Failed to Actuate Properly.Testing of Operability of Switches Begun. Licensee Declared All ECCS Inoperable for Both Units PNO-III-86-052A, on 860601,reactor Feedwater Pump Failed to Trip.Augmented Investigation Team Determined Problem Caused by Setpoint Variation.Reactor Placed in Cold Shutdown1986-06-0505 June 1986 PNO-III-86-052A:on 860601,reactor Feedwater Pump Failed to Trip.Augmented Investigation Team Determined Problem Caused by Setpoint Variation.Reactor Placed in Cold Shutdown PNO-III-86-052, on 860601,both Feedwater Pumps Tripped During Surveillance Test,Causing Reactor Water Level to Decrease Below Scram Level.Investigation to Determine If ATWS Occurred or If Instrumentation Faulty Underway1986-06-0202 June 1986 PNO-III-86-052:on 860601,both Feedwater Pumps Tripped During Surveillance Test,Causing Reactor Water Level to Decrease Below Scram Level.Investigation to Determine If ATWS Occurred or If Instrumentation Faulty Underway PNO-III-86-044, on 860509 & 11,reactor Scrammed on Low Reactor Water Level & After Receiving Group 1 Isolation Signal on High Main Steam Line Flow,Respectively.Util Decided to Repair Suspect Reactor Recirculation Pump Seal1986-05-13013 May 1986 PNO-III-86-044:on 860509 & 11,reactor Scrammed on Low Reactor Water Level & After Receiving Group 1 Isolation Signal on High Main Steam Line Flow,Respectively.Util Decided to Repair Suspect Reactor Recirculation Pump Seal PNO-III-86-039, on 860425,licensee Received in-plant Telephone Call from Unidentified Male Re Bomb Threat.Area Evacuated & Facility Searched.No Bomb Found.Licensee Security Organization Continuing Investigation1986-04-28028 April 1986 PNO-III-86-039:on 860425,licensee Received in-plant Telephone Call from Unidentified Male Re Bomb Threat.Area Evacuated & Facility Searched.No Bomb Found.Licensee Security Organization Continuing Investigation PNO-III-86-021, several Mechanical Snubbers Found Inoperable During Augmented Inservice Program to Demonstrate Operability of Shock Absorbers.Failed Snubbers Found in safety-related Sys,Including RHR Sys,Msiv,Hpcs & LPCS1986-03-12012 March 1986 PNO-III-86-021:several Mechanical Snubbers Found Inoperable During Augmented Inservice Program to Demonstrate Operability of Shock Absorbers.Failed Snubbers Found in safety-related Sys,Including RHR Sys,Msiv,Hpcs & LPCS PNO-III-86-015, on 860219,contractor Employee Suffered Apparent Back Injuries & Possible External Contamination in Fall from Ladder in Unit 1 Drywell.Individual Accompanied to Hosp by Licensee rad-protection Personnel1986-02-19019 February 1986 PNO-III-86-015:on 860219,contractor Employee Suffered Apparent Back Injuries & Possible External Contamination in Fall from Ladder in Unit 1 Drywell.Individual Accompanied to Hosp by Licensee rad-protection Personnel PNO-III-86-005, on 860122,during Ultrasonic Testing on Recirculation Sys Welds,Two Cracks Discovered on 12-inch Diameter Piping.Consultant Investigating Cause of Cracks & Determining Corrective Action1986-01-23023 January 1986 PNO-III-86-005:on 860122,during Ultrasonic Testing on Recirculation Sys Welds,Two Cracks Discovered on 12-inch Diameter Piping.Consultant Investigating Cause of Cracks & Determining Corrective Action PNO-III-85-062, on 850719,confirmatory Action Ltr Issued Requiring Review of All Canceled or Rejected Change Requests to Verify Status of Drawing Changes Prior to Restarting Both Reactors1985-07-19019 July 1985 PNO-III-85-062:on 850719,confirmatory Action Ltr Issued Requiring Review of All Canceled or Rejected Change Requests to Verify Status of Drawing Changes Prior to Restarting Both Reactors PNO-III-85-060, on 850712,facility Shut Down for Maint on RHR Sys Train a Shutdown Cooling Injection Valve & Train B Suppression Pool Spray Valve.Valves Failed Local Leak Rate Testing.Outage Expected to Last Until 8507221985-07-16016 July 1985 PNO-III-85-060:on 850712,facility Shut Down for Maint on RHR Sys Train a Shutdown Cooling Injection Valve & Train B Suppression Pool Spray Valve.Valves Failed Local Leak Rate Testing.Outage Expected to Last Until 850722 PNO-III-85-044, on 850531,unit Manually Scrammed Due to Decreasing Vacuum in Condenser.Caused by Rupture of Flexible Expansion Joint on Discharge Side of Circulation Pump 1B Flooding Crib House & Causing Loss of All Svc Water1985-06-0303 June 1985 PNO-III-85-044:on 850531,unit Manually Scrammed Due to Decreasing Vacuum in Condenser.Caused by Rupture of Flexible Expansion Joint on Discharge Side of Circulation Pump 1B Flooding Crib House & Causing Loss of All Svc Water PNO-III-85-042, on 850527,security Personnel Discovered Water Bubbling Out of Ground Near Condensate Storage Tank.Caused by Broken Pipe 20 Ft Below Ground.Leak Halted When Personnel Closed Valve,Isolating Tank1985-05-28028 May 1985 PNO-III-85-042:on 850527,security Personnel Discovered Water Bubbling Out of Ground Near Condensate Storage Tank.Caused by Broken Pipe 20 Ft Below Ground.Leak Halted When Personnel Closed Valve,Isolating Tank PNO-III-82-071, on 820729,received Part 21 Rept Via Telcon W/Zack Co Re Documentation Discrepancies for Welds Made to HVAC Components at La Salle & Possibly at Clinton & Midland.Welder of Record May Not Be Actual Welder1982-07-30030 July 1982 PNO-III-82-071:on 820729,received Part 21 Rept Via Telcon W/Zack Co Re Documentation Discrepancies for Welds Made to HVAC Components at La Salle & Possibly at Clinton & Midland.Welder of Record May Not Be Actual Welder PNO-III-82-070, on 820728,Region III Received Copy of 2.206 Petition to Revoke Ol,Containing Info from Affidavits by Il Atty General,Govt Accountability Project & Zack Co Re QA Problems.News Media Interest Expected1982-07-29029 July 1982 PNO-III-82-070:on 820728,Region III Received Copy of 2.206 Petition to Revoke Ol,Containing Info from Affidavits by Il Atty General,Govt Accountability Project & Zack Co Re QA Problems.News Media Interest Expected PNO-III-82-068, on 820503,allegations from Former Employee of HVAC Contractor Received Re False or Incomplete QA Documentation for HVAC Work at Sites.Special Insp of Zack Co & Facilities Initiated1982-07-22022 July 1982 PNO-III-82-068:on 820503,allegations from Former Employee of HVAC Contractor Received Re False or Incomplete QA Documentation for HVAC Work at Sites.Special Insp of Zack Co & Facilities Initiated PNO-III-82-067, on 820719,rept Issued Re Allegations Concerning Adequacy of Const.No Technical Issues Preclude Licensee from Operating Unit 1 Above 0% Power.Addl Allegations Re HVAC Will Be Investigated1982-07-16016 July 1982 PNO-III-82-067:on 820719,rept Issued Re Allegations Concerning Adequacy of Const.No Technical Issues Preclude Licensee from Operating Unit 1 Above 0% Power.Addl Allegations Re HVAC Will Be Investigated PNO-III-82-057, on 820621,criticality Achieved W/O Incident & within Predicted Margins Via Control Rod Withdrawal.Licensee Restricted to Zero Testing Pending NRC Resolution of Allegations Re Const Deficiencies1982-06-21021 June 1982 PNO-III-82-057:on 820621,criticality Achieved W/O Incident & within Predicted Margins Via Control Rod Withdrawal.Licensee Restricted to Zero Testing Pending NRC Resolution of Allegations Re Const Deficiencies PNO-III-82-031, State of Il Atty General Requested NRR to Institute Show Cause Proceeding Against Util for Suspension of NRC Consideration of Fuel Loading & Low Power Testing License1982-03-25025 March 1982 PNO-III-82-031:State of Il Atty General Requested NRR to Institute Show Cause Proceeding Against Util for Suspension of NRC Consideration of Fuel Loading & Low Power Testing License ML20249A0581978-01-23023 January 1978 PNO-78-010:on 780120,const Craft Employee Was Fatally Injured.Accident Occurred While Operating Electric Hoist. Operator Leaned Outside of Protective Cage & Head Struck Pipe ML20151U9411977-05-0505 May 1977 PNO-77-073,on 770505,laborers Strike Occurred.Cause of Strike Unknown.No Press Release Has Been Made by NRC of Comm Ed Co.Region III Received Notification of Occurrence by Telcon ML20151U3991977-02-23023 February 1977 PNO-77-030:on 770222,licensee Reported That Pickets from Cement Masons,Local 297,placed at Construction Site Stopped All Construction Activity.Illegal Jurisdictional Stike Anticipated to Last Remainder of Week 1999-04-13 Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS MONTHYEARIR 05000373/19990151999-10-0606 October 1999
[Table view]Insp Repts 50-373/99-15 & 50-374/99-15 on 990729-0916.One Violation Noted & Being Treated as Ncv.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000373/19990141999-09-0808 September 1999 Insp Repts 50-373/99-14 & 50-374/99-14 on 990809-13.No Violations Noted.Major Areas Inspected:Quality of Emergency Preparedness Program,Related Audits & Emergency Response Facilities & Equipment IR 05000373/19990131999-08-25025 August 1999 Insp Repts 50-373/99-13 & 50-374/99-13 on 990804-06 & 09-11. No Violations Noted.Major Areas Inspected:Effectiveness of Licensee Fire Protection Program IR 05000373/19990121999-08-17017 August 1999 Insp Repts 50-373/99-12 & 50-374/99-12 on 990623-0728.No Violations Noted.Major Areas Inspected:Plant Operations, Maint,Engineering & Plant Support IR 05000373/19990111999-07-14014 July 1999 Insp Repts 50-373/99-11 & 50-374/99-11 on 990614-18.No Violations Noted.Major Areas Inspected:Routine,Announced Insp Assessed Effectiveness of Licensee Solid Radioactive Waste (Radwaste) Mgt & Transportation Program IR 05000373/19990041999-07-13013 July 1999 Insp Repts 50-373/99-04 & 50-374/99-04 on 990513-0622.No Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plant Support IR 05000373/19990031999-05-19019 May 1999 Insp Repts 50-373/99-03 & 50-374/99-03 on 990401-0512.Two Violations Noted & Being Treated as non-cited Violation. Major Areas Inspected:Aspects of Licensee Operation,Maint, Engineering & Plant Support IR 05000373/19990101999-05-14014 May 1999 Insp Repts 50-373/99-10 & 50-374/99-10 on 990419-23. Violations Noted.Major Areas Inspected:Security Procedures & Documentation,Staff Knowledge & Performance,Security Force Training & Qualification & Quality Assurance in Security IR 05000373/19990091999-05-0303 May 1999 Insp Repts 50-373/99-09 & 50-374/99-09 on 990406-09.No Violations Noted.Major Areas Inspected:Operational & Outage Radiation Protection Program IR 05000373/19990071999-05-0303 May 1999 Insp Repts 50-373/99-07 & 50-374/99-07 on 990329-0402. Non-cited Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000373/19990081999-04-20020 April 1999 Insp Repts 50-373/99-08 & 50-374/99-08 on 990311-26.No Violations Noted.Major Areas Inspected:Review of Engineering Changes & Plant Matl Condition in Preparation for re-start of Unit 2 IR 05000373/19990021999-04-16016 April 1999 Insp Repts 50-373/99-02 & 50- 374/99-02 on 990217-0331.Non- Cited Violation Identified.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support PNO-III-99-020, on 990409,Unit 2 Had Been Shut Down Since Sept 1996 for Refueling Outage That Was Extended in Order to Address Extensive Equipment Condition.Util Completed Comprehensive Corrective Action Program1999-04-13013 April 1999 PNO-III-99-020:on 990409,Unit 2 Had Been Shut Down Since Sept 1996 for Refueling Outage That Was Extended in Order to Address Extensive Equipment Condition.Util Completed Comprehensive Corrective Action Program ML20205D7051999-04-0202 April 1999 Notice of Violation from Insp & Investigation Concluded on 981119.Violation Noted:On 980511,supervisor Employed by Raytheon Corp Contractor at Lasalle,Confirmed Odor of Alcohol on Employee & Failed to Perform for-cause FFD Test ML20205D5891999-03-29029 March 1999 Notice of Violation from Insp & Investigation Concluded on 981119.Violation Noted:On 980511,supervisor Employed by Raytheon Corp Contractor at Lasalle,Confirmed Odor of Alcohol on Employee & Failed to Have Require for-cause Test IR 05000373/19990011999-03-10010 March 1999 Insp Repts 50-373/99-01 & 50-374/99-01 on 990106-0216.No Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000373/19980231999-02-0202 February 1999 Insp Repts 50-373/98-23 & 50-374/98-23 on 981121-990105.No Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plant Support IR 05000373/19980261998-12-18018 December 1998 Insp Repts 50-373/98-26 & 50-374/98-26 on 981026-1106.No Violations Noted.Major Areas Inspected:Engineering & Assessment of Actions Planned or Completed to Address Number of Events Discussed in LERs IR 05000373/19980221998-12-17017 December 1998 Insp Repts 50-373/98-22 & 50-374/98-22 on 981010-1120.No Violations Noted.Major Areas Inspected:Plant Operations, Maint,Engineering & Plant Support IR 05000373/19980251998-12-16016 December 1998 Insp Repts 50-373/98-25 & 50-374/98-25 on 981102-06.No Violations Noted.Major Areas Inspected:Findings & Conclusions from Special Insp of Licensee Operator Workaround Program IR 05000373/19980211998-11-0707 November 1998 Insp Repts 50-373/98-21 & 50-374/98-21 on 980901-1009.No Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support PNO-III-98-047, on 981005,diver Lost Consciousness While in Unit 2 Suppression Pool.Diver Received Minor Contamination on Hair During Removal of Mask & Diving Suit.Diver Was Successfully Decontaminated1998-10-0606 October 1998 PNO-III-98-047:on 981005,diver Lost Consciousness While in Unit 2 Suppression Pool.Diver Received Minor Contamination on Hair During Removal of Mask & Diving Suit.Diver Was Successfully Decontaminated IR 05000373/19980191998-09-24024 September 1998 Insp Repts 50-373/98-19 & 50-374/98-19 on 980716-0831.No Violations Noted.Major Areas Inspected:Plant Operations, Maint,Engineering & Plant Support IR 05000373/19980201998-09-0808 September 1998 Insp Repts 50-373/98-20 & 50-374/98-20 on 980812-13. Non-cited Violation Noted.Major Areas Inspected: Circumstances Surrounding 980723 Incident Re Transfer of Radioactive Samples from Storage Areas on Refuel Floor IR 05000373/19980171998-09-0202 September 1998 Insp Repts 50-373/98-17 & 50-374/98-17 on 980713-17.No Violations Noted.Major Areas Inspected:Security Program Aspect of Plant Support ML20237A5901998-08-0707 August 1998 Notice of Violation from Insp on 980713-16.Violation Noted: on 980526,two Construction Laborers Permitted to Enter Unit 2 a Reactor Water Cleanup Heat Exchanger Room,W/O Satisfying Provisions of TS 6.1.1.1 IR 05000373/19980181998-08-0707 August 1998 Insp Repts 50-373/98-18 & 50-374/98-18 on 980713-16. Violations Noted.Major Areas Inspected:Effectiveness of Aspects of Radiation Protection Program IR 05000373/19980151998-07-24024 July 1998 Insp Repts 50-373/98-15 & 50-374/98-15 on 980706-21. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering Performance Areas ML20236U3841998-07-24024 July 1998 Notice of Violation from Insp on 980706-21.Violation Noted: as of 980717,testable Valves 1FP-160A,160B,161,236 & 234 in Fire Protection Sys Lines That Supply Fire Suppression Water to Control Room Not Cycled in Preceding 12 Months PNO-III-98-037, on 980724,Region III Issued Ltr to Util Indicating Sufficient Improvements Made to Support Unit 1 Restart.Unit 2 Will Remain Shut Down for Continuing Mods & Performance Improvement Activities1998-07-24024 July 1998 PNO-III-98-037:on 980724,Region III Issued Ltr to Util Indicating Sufficient Improvements Made to Support Unit 1 Restart.Unit 2 Will Remain Shut Down for Continuing Mods & Performance Improvement Activities IR 05000373/19980121998-07-23023 July 1998 Insp Repts 50-373/98-12 & 50-374/98-12 on 980511-0605.No Violations Noted.Major Areas Inspected:Operations & Effectiveness of Corrective Action Program IR 05000373/19980111998-07-23023 July 1998 Insp Repts 50-373/98-11 & 50-374/98-11 on 980605-0716.No Violations Noted.Major Areas Inspected:Plant Operations, Maint & Engineering IR 05000373/19980161998-07-23023 July 1998 Insp Repts 50-373/98-16 & 50-374/98-16 on 980626-0706.No Violations Noted.Major Areas Inspected:Observations of Crew Performance During Dynamic Simulator Requalification Exam IR 05000373/19980011998-07-0202 July 1998 Insp Repts 50-373/98-01 & 50-374/98-01 on 980423-0605. Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plan Support ML20236L4541998-07-0202 July 1998 Notice of Violation from Insp on 980423-0605.Violation Noted:Two Operators,Performing OOS Tag Removal & Positioning of Control Room Ventilation Sys Dampers,Did Not Perform an apart-in-time Independent Verification ML20248M1271998-06-0505 June 1998 Notice of Violation from Insp on 980319-0421.Violations Noted:As of 980421,licensee Failed to Adequately Perform Combustible Loading Calculations Required by LaSalle Administrative Procedure 240-6,rev 36,dtd 970821 IR 05000373/19980051998-06-0505 June 1998 Insp Repts 50-373/98-05 & 50-374/98-05 on 980319-0421. Violations Noted.Major Areas Inspected:Engineering IR 05000373/19980091998-05-22022 May 1998 Insp Repts 50-373/98-09 & 50-374/98-09 on 980311-0422. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000373/19980041998-04-10010 April 1998 Insp Repts 50-373/98-04 & 50-374/98-04 on 980124-0310.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000373/19980081998-04-0101 April 1998 Insp Repts 50-373/98-08 & 50-374/98-08 on 980317-19.No Violations Noted.Major Areas Inspected:Evaluation of Licensee Performance During Plant Biennial Exercise of Emergency Plan IR 05000373/19980071998-03-25025 March 1998 Partially Withheld Insp Repts 50-373/98-07 & 50-374/98-07 on 980223-27.No Violations Noted.Major Areas Inspected:Plant Support ML20217D0671998-03-23023 March 1998 Insp Repts 50-373/97-23 & 50-374/97-23 on 971222-980306. Violations Noted.Major Areas Inspected:Engineering ML20217D0611998-03-23023 March 1998 Notice of Violation from Insp on 971222-980306.Violation Noted:Licensee Failed to Ensure,Through Documentation & Other Activities That Applicable Design Basis & Regulatory Requirements Translated Into Procedures & Instructions IR 05000373/19980061998-03-18018 March 1998 Insp Repts 50-373/98-06 & 50-374/98-06 on 980223-27.No Violations Noted.Major Areas Inspected:Chemistry & Radiological Environ Monitoring Programs & Selected RP Program Activities IR 05000373/19970171998-02-27027 February 1998 Insp Repts 50-373/97-17OL & 50-374/97-17OL on 971020-24 & 980121-22.No Viiolations Noted.Major Areas Inspected:Review of Licensed RO & SRO Requalification Training Programs, Including Review of Written & Operating Exam Matls IR 05000373/19980031998-02-18018 February 1998 Insp Repts 50-373/98-03 & 50-374/98-03 on 980126-30.No Violations Noted.Major Areas Inspected:Review of Emergency Preparedness Program,An Aspect of Plant Support IR 05000373/19970221998-02-0505 February 1998 Insp Repts 50-373/97-22 & 50-374/97-22 on 971219-980123.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000373/19970181998-01-26026 January 1998 Insp Repts 50-373/97-18 & 50-374/97-18 on 971024-1218.No Violations Noted.Major Areas Inspected:Initial Operability Evaluation of Potential DG Cooling Water Piping Waterhammer ML20199F5291998-01-23023 January 1998 Insp Repts 50-373/97-20 & 50-374/97-20 on 971101-1218. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 07100101/20120181998-01-23023 January 1998 Notice of Violation from Insp on 971101-1218.Violation Noted:Activities Affecting Quality Were Not Accomplished IAW Applicable Procedures 1999-09-08 |
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PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE--PNO-III-88-90 Date November 2,1988
~
This preli[ninary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically'all that is known by the Region III staff on this date.
Facility: Comonwealth Edison Company Licensee Emergency Classification: 4 LaSalle Units 1 & 2 X Notification of an Unusual Event &et/
Marseilles, IL 61341 Alert Site Area Emergency Docket Nos. 50-373; 50-374 -
General Emergency Not Applicable
Subject:
5000 GALLON LEAK IN RADWASTE BUILDING About 6 a.m. (CST), October 31, 1988, the licensee discovered that approximately 5000 gallons of liquid radwaste had leaked through a failed seal on a radwaste evaporator heat exchanger in the Radwaste Building. A floor drain near the evaporator was plugged, allowing the liquid to accumulate in the room where the heat exchanger was located. About 10 gallons of the liquid from the room seeped through a crack in the wall, dripping onto a concrete pad on the outside of the Radwaste Building and then into a drain pit.-
Th2 licensee has drained the water out of the radwaste room and is decontaninating the affected areas, including the outside drain pit. The 10 gallons which leaked through the wall were isolated; no releases from the plant protected area occurred.
There were no injuries or personnel contamination. No radioactive material was released to the environment.
Region III (Chicago) dispatched a radiation specialist to the scene. He reviewed the licensee's radiation survey information, verified that no liquid entered the stonn sewer, and that proper radiological controls were in place. Region III will continue to monitor the licensee's course of action. >
Tha State of Illinois will be notified. The licensee has issued a news release. ;
The resident inspectors were notified of this event at about 11 a.m. (CST), October 31, 1988. This infonnation is current as of 11 a.m. (CST), November 2,1988.
CONTACT:
Paul v&}u fn R. Greger (FTS 388-5644) i DISTRIBUTION: I WFN 1 MNBB 1WFN E/W WFN 1 t Chainnan Zech ATOD NF OTA RM5r !
Com. Carr IWFN Mail To:
i Com. Rogers PA Resident Inspector Offices _ DCS (Original) 4 Com. Curtiss OGC Resident Inspector DOT (Trans.Only)
SECY j OGC-H FAX TO: Nicholson Lane Regions CA INPO/l0) RE5 Region I GPA NSAC /lo? Region !! -g i ACRS Licensee /30 Region IV L l PDR HQS. Operations Officer # [ Region Y }
Region III O j f 8811000116 881102 Rev. June 1988 PDR I&E PNO-III-88-090 PDC