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Category:Deficiency Report (per 10CFR50.55e and Part 21)
MONTHYEARML23207A0762023-07-14014 July 2023 EN 56557 - Update to Part 21 Report Re Potential Defect with Trane External Auto/Stop Emergency Stop Relay Card Pn: XI2650728-06 ML23066A2212023-03-0707 March 2023 Velan, Inc. - Revised Part 21 Notification Re Butterfly Valves Found to Have a Number of Fasteners Loose ML22259A1732022-08-26026 August 2022 EN 55960 - Curtiss Wright Part 21 Report Re Potential Defect in Configuration of the Quick Disconnect Connector Cable Assemblies Supplied to McGuire and Catawba Nuclear Power Stations ML22201A1012022-07-18018 July 2022 Framatome, Inc. - 10 CFR Part 21 Notification of Existence of a Defect and Failure to Comply RA-22-0127, Interim Part 21 Report of a Deviation or Failure to Comply for Cutler-Hammer Relay2022-04-0808 April 2022 Interim Part 21 Report of a Deviation or Failure to Comply for Cutler-Hammer Relay ML20073G4572020-03-0909 March 2020 Carrier Corporation - Final Report Notification of Defect Pursuant to 10 CFR Part 21 for 17FA999-1200-107 Oil Pump ML20024D8232020-01-10010 January 2020 Carrier Corp., Interim Report/Notification of Defect Pursuant to 10 CFR Part 21 ML20016A2202020-01-10010 January 2020 Carrier - Interim Report/Notification of Defect Pursuant to 10 CFR Part 21 ML19347A4262019-12-10010 December 2019 General Atomics - Reportable Occurrence Under 10CFR21: Reported Failure in Analog High Range Radiation Monitor (RP-2C) MNS-16-078, Written Notification Joslyn Clark Overload Heater Element Part No. 24552016-10-19019 October 2016 Written Notification Joslyn Clark Overload Heater Element Part No. 2455 ML16281A2712016-09-30030 September 2016 Part 21 - Safety Related Component Welding by an Unqualified Welder ML16281A2702016-09-22022 September 2016 Part 21 - Initial Notification of Masterpact Breaker Fail to Close ML16278A4712016-09-22022 September 2016 Notification of 10 CFR Part 21 Condition, Masterpact Breaker Fail to Close ML16281A2722016-09-19019 September 2016 Part 21 Notification - Joslyn Clark Overload Heater Element Part Number 2455 ML16243A4752016-08-26026 August 2016 Part 21 Safety Related Component Welding by an Unqualified Welder ML16209A0502016-07-13013 July 2016 Part 21 - Furmanite Nuclear Grade Leak Seal Material FSC-N-1B ML16139A8322016-05-13013 May 2016 Part 21 - Initial Notification of Masterpact Breaker Fail to Close ML16139A8332016-05-13013 May 2016 Part 21 - Initial Notification of Masterpact Breaker Fail to Close ML16127A5952016-05-0404 May 2016 Rotork Controls Inc. Part 21 Notification Concerning V12 (Pt No. N69-921) and K5 (N69-838 & N69-926) Safety Related Micro Switches ML15103A2442015-04-0606 April 2015 Part 21 Report - Deviation of Hk Circuit Breaker Close Latch Spring ML15049A4582015-02-0606 February 2015 Thermo Gamma-Metrics, LLC - Part 21 Report Regarding Shutdown Margin Monitor Environmental Qualification Noncompliance ML14085A0122014-03-21021 March 2014 Notification of Part 21 - Sbm Selector Switches Contact Assembly Unplanned Manufacturing Change ML13165A3422013-06-12012 June 2013 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML13102A3032013-04-10010 April 2013 Part 21 Involving a Potential Weld Defect ML13079A3202013-03-18018 March 2013 Notification of Potential Part 21 Interim Report Re Possible Deviation or Defect in Nuclear Qualified High Efficiency Particulate Air Filters ML12348A1362012-12-13013 December 2012 Part 21 60-Day Interim Report Notification: Adequacy of Design Change in Am Magne-Blast Circuit Breakers ML12352A1232012-12-13013 December 2012 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML12318A0412012-11-0808 November 2012 Part 21 Report - Commercial Grade Dedication Not Properly Applied to Butterfly Valves ML12219A2312012-08-0303 August 2012 Us NRC 10CFR Part 21 Notification from Flowserve on Seal Cap for Kerotest 3/4, 1, 1-1/2, and 2 Y-Type Globe Valves ML11287A1392011-10-13013 October 2011 Stations - Amended 10CFR21 Notification - Identification of Defect Mackson, Inc. - Defective Tube Steel - NRC Event Number 46375 ML11186A8912011-07-0101 July 2011 Notification of Potential Part 21 Seal Failure and Leakage Associated with Model B5497-301 Valves ML11116A0962011-04-18018 April 2011 Submittal of 10 CFR 21 Notification - Identification of Defect Problem Investigation Process No.: M-11-01725 ML1108907632011-03-29029 March 2011 Notification of Potential Part 21 Re Paint Chips Discovered in Woodward Governors ML1106701702011-03-0404 March 2011 Notification of Potential Part 21 - Error in Value Body Drawing ML1105506152011-02-22022 February 2011 Duke Energy - Notification of Potential Part 21 Re Identification of Defect ML1102800152011-01-24024 January 2011 Notification of Potential Part 21 - Bus Disconnect Stab Assembly - 600V Essential Motor Control Centers ML1030601022010-10-29029 October 2010 Notification of Potential Part 21 Transfer of Information Concerning Control Components Inc. (CCI) Drag Valves ML1025304462010-09-0808 September 2010 Rotork Inc. Part 21 Notification Sintered Gear ML1009200932010-03-25025 March 2010 10 CFR21 Notification of a Potential Weld Defect ML0925902502009-09-0909 September 2009 Notification of Potential Part 21 Re Reporting of Defects and Non-Compliance - Engine Systems, Inc. Report No. 10CFR21-0097, Rev. 0. Woodward 2301A & DRU with Unapproved Supplier IC, P/N: 9903-303, 9903-337, 9903-444 and 9903-470 ML0925800812009-09-0909 September 2009 Notification of Potential Part 21 Involving Woodward Governors Using Unapproved Supplier Integrated Circuits ML0907611882009-03-11011 March 2009 Part 21 Notification - Defective Hk and K-Line Circuit Breaker Tension Springs ML0904104852009-02-0606 February 2009 Notification of Potential Part 21 Report (Draft) Re Defective ASME SA-193, Grade 6 Cap Screw Material ML0903502172009-01-27027 January 2009 Notification of Potential Part 21 Report from Fisher Controls International - Water Quality Deficiency ML0903502112009-01-16016 January 2009 Part 21 Report Re Identification of Defect Found in Basic Component. Initially Reported to NRC on 12/18/2008 ML0835404692008-12-18018 December 2008 Duke Energy Carolinas, Llc., Deficiency Report on Defective Digital Optical Isolators ML0831900172008-11-12012 November 2008 Notification of Potential Part 21 on All Dimensionally Verified Commercial Grade Items Processed Per Fisher Manufacture Procedure Fmp 2K28 ML0823901062008-08-25025 August 2008 Notification of Potential Part 21 on Failure of F and G Switches ML0727504702007-09-21021 September 2007 MPR Associates, Inc. - Report of Defect in Accordance with 10 CFR 21 ML0713703092007-03-0707 March 2007 Velan, Inc., Piston Check Cv Information 2023-07-14
[Table view] Category:Letter type:MNS
MONTHYEARMNS-18-044, Independent Spent Fuel Storage Installation (Isfsi), Submittal of 10 CFR 72.48 Summary Report from September 15, 2016 to July 26, 2018, No Changes, Tests, or Experiments2018-07-26026 July 2018 Independent Spent Fuel Storage Installation (Isfsi), Submittal of 10 CFR 72.48 Summary Report from September 15, 2016 to July 26, 2018, No Changes, Tests, or Experiments MNS-18-036, Redacted Response to the Request for Additional Information Regarding the License Amendment Request to Revise the Licensing Bases for Protection from Tornado Generated Missiles2018-07-0303 July 2018 Redacted Response to the Request for Additional Information Regarding the License Amendment Request to Revise the Licensing Bases for Protection from Tornado Generated Missiles MNS-18-042, Independent Spent Fuel Storage Installation (ISFSI)2018-06-28028 June 2018 Independent Spent Fuel Storage Installation (ISFSI) MNS-18-040, Submittal of Information Related to Pressurizer Surge and Spray Nozzle Thermal Sleeves Attachment Welds for License Renewal2018-06-26026 June 2018 Submittal of Information Related to Pressurizer Surge and Spray Nozzle Thermal Sleeves Attachment Welds for License Renewal MNS-18-039, Independent Spent Fuel Storage Installation (ISFSI)2018-06-19019 June 2018 Independent Spent Fuel Storage Installation (ISFSI) MNS-18-001, Application to Revise Technical Specifications to Adopt TSTF-234-A Revision 1, Add Action for More than One Dpri Inoperable2018-05-31031 May 2018 Application to Revise Technical Specifications to Adopt TSTF-234-A Revision 1, Add Action for More than One Dpri Inoperable MNS-18-030, 2017 Annual Radiological Environmental Operating Report2018-05-15015 May 2018 2017 Annual Radiological Environmental Operating Report MNS-18-029, Resolution of Commitments Related to Review Request for the Aging Management Program and Inspection Plan for the McGuire Nuclear Station Units 1 and 2 Reactor Vessel Internals to Implement MRP-227-A2018-05-0909 May 2018 Resolution of Commitments Related to Review Request for the Aging Management Program and Inspection Plan for the McGuire Nuclear Station Units 1 and 2 Reactor Vessel Internals to Implement MRP-227-A MNS-18-029, McGuire Nuclear Station, Units 1 and 2 - Resolution of Commitments Related to Review Request for the Aging Management Program and Inspection Plan for the McGuire Nuclear Station Units 1 and 2 Reactor Vessel Internals to Implement MRP-227-2018-05-0909 May 2018 McGuire Nuclear Station, Units 1 and 2 - Resolution of Commitments Related to Review Request for the Aging Management Program and Inspection Plan for the McGuire Nuclear Station Units 1 and 2 Reactor Vessel Internals to Implement MRP-227-A MNS-18-028, Annual Radioactive Effluent Release Report2018-04-25025 April 2018 Annual Radioactive Effluent Release Report MNS-18-017, Non-Voluntary License Amendment Request (LAR) to Correct Non-Conservative Technical Specification 3.4.11 - PORVs2018-02-26026 February 2018 Non-Voluntary License Amendment Request (LAR) to Correct Non-Conservative Technical Specification 3.4.11 - PORVs MNS-18-018, McGuire, Units 1 & 2, Submittal of Emergency Plan Implementing Procedure Changes2018-02-22022 February 2018 McGuire, Units 1 & 2, Submittal of Emergency Plan Implementing Procedure Changes MNS-18-009, McGuire Nuclear Station, Units 1 and 2, Submittal of Emergency Plan, Revision 18-12018-01-31031 January 2018 McGuire Nuclear Station, Units 1 and 2, Submittal of Emergency Plan, Revision 18-1 MNS-18-003, End of Cycle 25 In-service and Steam Generator In-service Inspection Summary Reports2018-01-11011 January 2018 End of Cycle 25 In-service and Steam Generator In-service Inspection Summary Reports MNS-17-050, Review Request for the Aging Management Program and Inspection Plan for the Reactor Vessel Internals to Implement MRP-227-A2017-12-13013 December 2017 Review Request for the Aging Management Program and Inspection Plan for the Reactor Vessel Internals to Implement MRP-227-A MNS-17-048, Response to Request for Additional Information License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies2017-12-12012 December 2017 Response to Request for Additional Information License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies MNS-17-026, Submittal of License Amendment Request Proposing to Revise the Bases for Protection from Tornado-Generated Missiles2017-12-0808 December 2017 Submittal of License Amendment Request Proposing to Revise the Bases for Protection from Tornado-Generated Missiles MNS-17-042, McGuire Nuclear Station, Unit 1, Submittal of Cycle 26, Revision 0, Core Operating Limits Report2017-10-0909 October 2017 McGuire Nuclear Station, Unit 1, Submittal of Cycle 26, Revision 0, Core Operating Limits Report MNS-17-040, (Mns), Units 1 and 2 - Supplement to the High Frequency Supplement to Seismic Hazard Screening Report, Response NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force ..2017-09-27027 September 2017 (Mns), Units 1 and 2 - Supplement to the High Frequency Supplement to Seismic Hazard Screening Report, Response NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force .. MNS-17-038, Startup Ascension Summary Report Measurement Uncertainty Recapture Power Uprate2017-09-25025 September 2017 Startup Ascension Summary Report Measurement Uncertainty Recapture Power Uprate MNS-17-039, McGuire Nuclear Station, Units 1 and 2, Submittal of Emergency Plan, Revision 17-12017-09-19019 September 2017 McGuire Nuclear Station, Units 1 and 2, Submittal of Emergency Plan, Revision 17-1 MNS-17-031, License Amendment Request for Temporary Changes to Technical Specifications to Address an 'A' Train Nuclear Service Water System (Nsws) Non-Conforming Condition2017-09-14014 September 2017 License Amendment Request for Temporary Changes to Technical Specifications to Address an 'A' Train Nuclear Service Water System (Nsws) Non-Conforming Condition MNS-17-037, Submittal of Summary Report of Evaluations Performed Pursuant to 10 CFR 50.59 Changes, Tests, and Experiments During the Period from January 1, 2016 to March 31, 20172017-08-10010 August 2017 Submittal of Summary Report of Evaluations Performed Pursuant to 10 CFR 50.59 Changes, Tests, and Experiments During the Period from January 1, 2016 to March 31, 2017 MNS-17-033, Snubber Program Plan for the Fourth Ten-Year Lnservice Testing (IST) Interval2017-08-0202 August 2017 Snubber Program Plan for the Fourth Ten-Year Lnservice Testing (IST) Interval MNS-17-034, 16C4435-RPT-002, Rev. 1, 50.54(f) NTTF 2.1 Seismic High Frequency Confirmation for McGuire Nuclear Station.2017-07-24024 July 2017 16C4435-RPT-002, Rev. 1, 50.54(f) NTTF 2.1 Seismic High Frequency Confirmation for McGuire Nuclear Station. MNS-17-030, Response to March 12, 2012, Request for Information Enclosure 2, Recommendation 2.1, Flooding, Required Response 3, Flooding Focused Evaluation Summary Submittal2017-06-28028 June 2017 Response to March 12, 2012, Request for Information Enclosure 2, Recommendation 2.1, Flooding, Required Response 3, Flooding Focused Evaluation Summary Submittal MNS-17-023, Response to Request for Additional Information to License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies2017-05-25025 May 2017 Response to Request for Additional Information to License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies MNS-17-016, Nuclear Regulatory Commission (NRC) Annual Commitment Change Report2017-05-18018 May 2017 Nuclear Regulatory Commission (NRC) Annual Commitment Change Report MNS-17-020, Transmittal of McGuire, Units 1 and 2, 2016 Annual Radiological Environmental Operating Report2017-05-0505 May 2017 Transmittal of McGuire, Units 1 and 2, 2016 Annual Radiological Environmental Operating Report MNS-17-019, McGuire Nuclear Station, Units 1 and 2 - Submittal of Annual Radioactive Effluent Release Report2017-04-28028 April 2017 McGuire Nuclear Station, Units 1 and 2 - Submittal of Annual Radioactive Effluent Release Report MNS-17-008, Letter of Intent to Submit Plant-Specific Reactor Vessel Internals Inspection Plans2017-02-23023 February 2017 Letter of Intent to Submit Plant-Specific Reactor Vessel Internals Inspection Plans MNS-16-092, License Amendment Request to Revise Technical Specifications Section 5.5.2, Containment Leakage Rate Testing Program for Permanent Extension of Type a and Type C Leak Rate Test Frequencies2016-12-19019 December 2016 License Amendment Request to Revise Technical Specifications Section 5.5.2, Containment Leakage Rate Testing Program for Permanent Extension of Type a and Type C Leak Rate Test Frequencies MNS-16-091, License Amendment Request for Technical Specification 3.6.14, Divider Barrier Integrity.2016-12-0808 December 2016 License Amendment Request for Technical Specification 3.6.14, Divider Barrier Integrity. MNS-16-086, Emergency Plan, Revision 16-42016-12-0707 December 2016 Emergency Plan, Revision 16-4 MNS-16-078, Written Notification Joslyn Clark Overload Heater Element Part No. 24552016-10-19019 October 2016 Written Notification Joslyn Clark Overload Heater Element Part No. 2455 MNS-16-077, Responding to Request for Additional Information Related to License Amendment Request to Implement a Risk-informed Performance-Based Fire Protection Program2016-09-29029 September 2016 Responding to Request for Additional Information Related to License Amendment Request to Implement a Risk-informed Performance-Based Fire Protection Program MNS-16-070, Response to Request for Additional Information to Relief Request 16-MN-0032016-08-18018 August 2016 Response to Request for Additional Information to Relief Request 16-MN-003 MNS-16-060, Spent Fuel Pool Evaluation Supplemental Report, Response to NRC Request for Information Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident2016-08-18018 August 2016 Spent Fuel Pool Evaluation Supplemental Report, Response to NRC Request for Information Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident MNS-16-062, Relief Request 16-MN-003 Alternative to Defect Removal Prior to Performing Temporary Repair Activities on Three-Inch-Diameter Nuclear Service Water System Piping2016-08-10010 August 2016 Relief Request 16-MN-003 Alternative to Defect Removal Prior to Performing Temporary Repair Activities on Three-Inch-Diameter Nuclear Service Water System Piping MNS-16-046, License Amendment Request for Technical Specification 3.6.14, Divider Barrier Integrity2016-06-30030 June 2016 License Amendment Request for Technical Specification 3.6.14, Divider Barrier Integrity MNS-16-056, License Amendment Request, One-Time Extension of Appendix J Type a Integrated Leakage Rate Test Interval, Response to Request for Additional Information2016-06-30030 June 2016 License Amendment Request, One-Time Extension of Appendix J Type a Integrated Leakage Rate Test Interval, Response to Request for Additional Information MNS-16-053, Relief Request 16-MN-002, Alternative to Defect Removal Prior to Performing Repair Activities on Nuclear Service Water System Piping2016-06-23023 June 2016 Relief Request 16-MN-002, Alternative to Defect Removal Prior to Performing Repair Activities on Nuclear Service Water System Piping MNS-16-052, Supplement to License Amendment Request for the Removal of Superseded Technical Specification Requirements, Dated May 5, 2016, TAC Nos. MF7682 and MF76832016-06-16016 June 2016 Supplement to License Amendment Request for the Removal of Superseded Technical Specification Requirements, Dated May 5, 2016, TAC Nos. MF7682 and MF7683 MNS-16-042, Withdrawal of Relief Request Serial No. 15-MN-0022016-05-17017 May 2016 Withdrawal of Relief Request Serial No. 15-MN-002 MNS-16-020, License Amendment Request Removal of Superseded Technical Specification Requirements2016-05-0505 May 2016 License Amendment Request Removal of Superseded Technical Specification Requirements MNS-16-041, Supplement to Final Notification of Full Compliance with Order EA-12-049, Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond Design Basis External Events and with Order EA-12-051..2016-05-0505 May 2016 Supplement to Final Notification of Full Compliance with Order EA-12-049, Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond Design Basis External Events and with Order EA-12-051.. MNS-16-036, Relief Request 16-MN-001, Limited Weld Examinations2016-04-28028 April 2016 Relief Request 16-MN-001, Limited Weld Examinations MNS-16-039, Submittal Revising Attachment s of License Amendment Request to Implement a Risk-Informed Performance-Based Fire Protection Program2016-04-26026 April 2016 Submittal Revising Attachment s of License Amendment Request to Implement a Risk-Informed Performance-Based Fire Protection Program MNS-16-026, Transmittal of Updated Final Safety Analysis Report, Revision 192016-04-0505 April 2016 Transmittal of Updated Final Safety Analysis Report, Revision 19 MNS-15-068, License Amendment Request to Technical Specification (TS) 3.6.13, Ice Condenser Doors.2016-03-24024 March 2016 License Amendment Request to Technical Specification (TS) 3.6.13, Ice Condenser Doors. 2018-07-03
[Table view] |
Text
(~DUKE Steven D. Capps
~ ENERGY
~ Vice President McGuire Nuclear Station Duke Energy MGOlVP I 12700 Hagers Ferry Road Huntersville, NC 28078 O: 980.875.4805 f: 980.875.4809 Steven.Capps@duke-energy.com Serial No. MNS-16-078 October 19, 2016 10 CFR 21.21 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001
SUBJECT:
McGuire Nuclear Station, Units 1 and 2 Docket Numbers 50-369 and 50-370, Renewed Facility Operating License NPF-9 and NPF-17 10 CFR Part 21 Written Notification Joslyn Clark Overload Heater Element, Part No. 2455 In accordance with 10 CFR 21.21 (d)(3)(ii), Duke Energy Carolinas, LLC (Duke Energy) is providing the required written notification within 30 days of the identification of a defect in Joslyn Clark Overload Heater Elements Part No. 2455. This notification was initially reported to the NRC Operations Center on September 19, 2016 (Event Number 52248). The enclosure to this letter provides the information required by 10 CFR 21.21(d)(4).
There are no regulatory commitments contained in this letter or its enclosure.
If you have any questions or need additional information regarding this matter, please contact Lee A. Hentz at (980) 875-4187.
Sincerely,
~~~
Steven D. Capps
Enclosure:
10 CFR 21.21 Written Notification www.duke-energy.com
U.S. Nuclear Regulatory Commission MNS-16-078 Page 2 cc: (with enclosure)
Catherine Haney Regional Administrator U.S. Nuclear Regulatory Commission - Region II Marquis One Tower 245 Peachtree Center Ave., NE Suite 1200
. Atlanta, GA 30303-1257 G.A. Hutto Ill Senior Resident Inspector U.S. Nuclear_Regulatory Commission McGuire Nuclear Station V. Sreenivas NRC Project Manager U.S. Nuclear Regulatory Commission One White Flint North, Mail Stop 8-G9A 111555 Rockville Pike Rockville, MD 20852-2738
Enclosure
't 10 CFR 21.21 Report Page 1 of 4 WRITTEN REPORT PER 10 CFR 21.21(d)(4)
(i) Name and address of th~ individual or individuals informing the Commission.
Steven D. Capps Vice President McGuire Nuclear Station 12700 Hagers Ferry Road Huntersville, NC 28078 (ii) Identification of the facility, the activity, or the basic component supplied for such facility or such activity within the United States which fails to comply or contains a defect.
Facility:
McGuire Nuclear Station (McGuire), Units 1 and 2 Docket Nos. 50-369 and 50-370 Renewed License Nos. NPF-9 and NPF-17 Basic Component:
Joslyn Clark Overload Heater Element Part Number 2455 (iii) Identification of the firm constructing the facility or supplying the basic co.mponent which fails to comply or contains a defect.
Specialty Product Technology, manufacturer of Joslyn Clark Overload Heater Elements This basic component was procured in accordance with the Duke Energy Commercial Grade Program and dedicated for use in safety related applications.
(iv) Nature of the defect or failure to comply and the safety hazard which is created or could be created by such defect or failure to comply.
Three of 18 overload heater elements, purchased as a lot, had insufficient top weld material. One failed in-service during a post maintenance test, the second and third failed during a visual and mechanical inspection (flex test). An extent of condition review inspected over 500 similar Joslyn Clark overload heater elements. No other inventory was found with a top weld issue. The dedicated overload heater elements, from this lot, were not transferred or sold to any third party customers.
These overload heater elements are used in motor starters for the Emergency Diesel Generator (EOG) ventilation fans. This condition was discovered during post maintenance testing of the 2A EOG on July 27, 2016. None of the defective overload heater elements were installed in Operable EOG ventilation fan motor starters. The Evaluation of the deviation determined that a Substantial Safety Hazard would have
Enclosure
': 10 CFR 21.21 Report Page 2 of 4 been created if the defective overload heater elements were installed and left uncorrected.
(v) The date on which the information of such defect or failure to comply was obtained.
McGuire evaluated this condition in accordance with Duke Energy procedure AD-LS~
ALL-0018 Rev. 0, "Evaluating and Reporting of Defects and Noncompliance in accordance with 10 CFR 21." The Discovery process, determination of a Deviation, was completed on August 18, 2016. The Evaluation process, determination of a Substantial Safety hazard, was completed on September 15, 2016. The Deviation was first reported to the NRC via facsimile on September 19, 2016 (EN 52248).
(vi) In the case of a basic component which contains a defect or fails to comply, the number and location of these components in use at, supplied for, being supplied for, or may be supplied for, manufactured, or being manufactured for one or more facilities or activities subject to the regulations in this part.
Twenty (20) Joslyn Clark Overload Heater Elements part Number 2455 were purchased in 2009 by Purchase Order 115586. Two did not pass receipt inspection (failed resistance test) and were returned to the supplier. Eighteen (18) were dedicated and checked into stock (suspect lot).
Three Overload Heater Elements from the suspect lot were installed in the 2A 1 EOG ventilation fan motor starter on July 26, 2016. The fan motor tripped during the functional verification, prior to declaring the EOG Operable. Upon inspection, one element was found open at the top weld. One more opened after a flex test. All three were replaced from a different lot.
Three Overload Heater Elements from the suspect lot were installed in the 2A2 EOG ventilation fan motor starter on July 26, 2016. The fan motor completed its functional verification. Upon re-inspection and flex testing by Engineering, the three Overload Heater Element top welds were firmly attached. These were determined to be acceptable and not replaced.
Two Overload Heater Elements from the suspect lot were allocated from stock for the 2A2 EOG ventilation fan motor starter inspection but not used. One was determined to be acceptable by Engineering. One was found defective (open at top weld).
Four more Overload Heater Elements from the suspect lot were allocated from stock and inspected by Engineering (visual and flex test) prior to installation. All top welds were firmly attached. Three are installed in the 282 EOG ventilation fan motor starter and one is installed in the 182 EOG ventilation fan motor starter. Both fan motors completed their functional verification.
Six Overload Heater Elements from the suspect lot were installed in the non-safety related turbine building supply fan motor starters on April 28, 2016. These fans motors have operated successfully since April 2016. These Overload Heater Elements were not re-inspected since they are installed in a non-safety related application.
Enclosure
'r' 10 CFR 21.21 Report Page 3 of 4 (vii) The corrective action which has been, is being, or will be taken; the name of the individual or organization responsible for the action; and the length of time that has been or will be taken to complete the action.
a) The following restriction (HOLD) wcis placed on Joslyn Clark-Elizabethtown NC by Duke Energy for all future purchase orders until actions c) and d) below are complete:
Joslyn Clark shall notify Duke Energy prior to manufacturing of all overload heaters supplied to Duke Energy, so source inspection can be performed to ensure proper weld quality (or to evaluate if internal over-checks are needed). For all other products provided by Joslyn Clark, they shall notify Duke Energy prior to final testing and release for shipment so Procurement Engineering can evaluate if additional source inspections or material over-checks are needed. This was completed on September 15, 2016.
b) An extent of condition review performed by Duke Energy Procurement Engineering inspected over 500 similar Joslyn Clark overload heater elements. No other inventory was found with a top weld issue. This was completed on October 2, 2016.
c) To address product quality issues, Specialty Product Technology, manufacturer of Joslyn Clark Overload Heater Elements, has performed a cause evaluation and is taking corrective actions to improve their welding processes. These actions are expected to be completed by October 31, 2016.
Individual Responsible for the action:
Marta 0. Rosa Ramos Senior Quality Engineer NQA-1 Lead Auditor Specialty Products Technologies 2100 W Broad Street Elizabethtown, NC 28337 Office: (910) 879-5812 d) Duke -Energy will revise/enhance the Commercial Grade Dedication package for the Joslyn Clark Overload Heater Elements. This action is expected to be complete by November 15, 2016.
Individual Responsible for the action:
John Yankoglu Electrical Procurement Engineer 13339 Hagers Ferry Road Huntersville, NC 28078 Phone: 980 875-4853 (viii) Any advice related to the defect or failure to comply about the facility, activity, or basic component that has been, is being, or will be given to purchasers or licensees.
None.
Enclosure 10 CFR 21.21 Report Page 4 of 4 (ix) In the case of an early site permit, the entities to whom an early site permit was transferred.
This event does not involve an early site permit.