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Category:PRELIMINARY NOTIFICATION OF EVENT OR OCCURRENCE (PNO
MONTHYEARPNO-I-97-068, on 971103,unplanned Shutdown Greater than 72 H Occurred.Oil Leaks Detected & Repaired.Third RCP Inspected & Engineers Found Low Seal Flow at Second Stage Pump Seal. Resident Inspectors Following Onsite Activities1997-11-0505 November 1997 PNO-I-97-068:on 971103,unplanned Shutdown Greater than 72 H Occurred.Oil Leaks Detected & Repaired.Third RCP Inspected & Engineers Found Low Seal Flow at Second Stage Pump Seal. Resident Inspectors Following Onsite Activities PNO-IV-97-050, on 970911,completed Repair of Reactor Caisson Leak by Reducing in-leakage to Less than Ten Gallons/Day. Informed State of CA1997-09-12012 September 1997 PNO-IV-97-050:on 970911,completed Repair of Reactor Caisson Leak by Reducing in-leakage to Less than Ten Gallons/Day. Informed State of CA PNO-I-97-018, on 970328,protest Related to TMI-2 Accident Occurred.Protesters Walked in Circle,Outside of Util Property,Blocking Plant Entrance Lane.Plant Notified NRC Headquarter to Inform of Event1997-03-28028 March 1997 PNO-I-97-018:on 970328,protest Related to TMI-2 Accident Occurred.Protesters Walked in Circle,Outside of Util Property,Blocking Plant Entrance Lane.Plant Notified NRC Headquarter to Inform of Event ML20203G2581993-02-19019 February 1993 PNO-IIT-93-001B:final Onsite Status Rept from NRC Iit. Team Has Completed Initial fact-finding Phase at TMI, Middletown,Pa Site.Meeting W/Licensee TMI Site Emergency Review Group Was Held on 930215 ML20203G2941993-02-16016 February 1993 PNO-IIT-93-001A:IIT Remains Onsite Gathering Data,Conducting Interviews,Inspecting Equipment,Meeting W/Licensee, Concurring in Licensee Action Plans & Analyzing Facts.Onsite Interviews Should Be Completed by 930218 ML20203G3231993-02-10010 February 1993 PNO-IIT-93-001:IIT Arrived Onsite & Initiated Investigation, Toured Facility & Examined Equipment Associated W/Event. Team in Early Stage of Conducting Interviews,Reviewing Procedures & Drawings & Analyzing Facts PNO-I-93-011, on 930207,during Shift Change,Unauthorized Vehicle Driven Into Plant Protected Area.Site Area Emergency Declared.Caused by Former Mental Patient.Precautionary Measures to Secure Plant Vital Areas Implemented1993-02-0707 February 1993 PNO-I-93-011:on 930207,during Shift Change,Unauthorized Vehicle Driven Into Plant Protected Area.Site Area Emergency Declared.Caused by Former Mental Patient.Precautionary Measures to Secure Plant Vital Areas Implemented PNO-V-92-017, on 920605,earthquake W/Richter Magnitude of 5.0 Occurred.Plant Walkdowns Performed & No Problems Noted1992-06-0505 June 1992 PNO-V-92-017:on 920605,earthquake W/Richter Magnitude of 5.0 Occurred.Plant Walkdowns Performed & No Problems Noted PNO-I-90-071, on 900829,resident Inspectors Informed That Concentration Value of 29,000 Pci/Liter of Tritium Found in Aug Sample of Groundwater Monitoring Station MS-2.No Tech Spec Release Limits Exceeded1990-08-30030 August 1990 PNO-I-90-071:on 900829,resident Inspectors Informed That Concentration Value of 29,000 Pci/Liter of Tritium Found in Aug Sample of Groundwater Monitoring Station MS-2.No Tech Spec Release Limits Exceeded PNO-I-89-081, on 890925,two Laborers Inadvertently Handled Core Debris That Could Have Resulted in Overexposure. Detailed Assessment Performed by Licensee to Establish Time Individuals Handled Source & Actual Doses Received1989-09-28028 September 1989 PNO-I-89-081:on 890925,two Laborers Inadvertently Handled Core Debris That Could Have Resulted in Overexposure. Detailed Assessment Performed by Licensee to Establish Time Individuals Handled Source & Actual Doses Received PNO-V-89-057, on 890921,earthquake of 5.1 Magnitude Occurred 45 Miles Southwest of Facility.Facility Shut Down Since Jul 1976 & Reactor Vessel Defueled.Licensee Conducted Insp of Facility & No Damage Identified1989-09-21021 September 1989 PNO-V-89-057:on 890921,earthquake of 5.1 Magnitude Occurred 45 Miles Southwest of Facility.Facility Shut Down Since Jul 1976 & Reactor Vessel Defueled.Licensee Conducted Insp of Facility & No Damage Identified PNO-I-89-056, on 890710,reactor Vessel Lower Head Cracks from Guide Tubes E-7 & G-6 Discovered.Tubes Substantially Damaged by Flow of Molten Fuel.Investigation & Cleanup Started1989-07-10010 July 1989 PNO-I-89-056:on 890710,reactor Vessel Lower Head Cracks from Guide Tubes E-7 & G-6 Discovered.Tubes Substantially Damaged by Flow of Molten Fuel.Investigation & Cleanup Started ML20244C6411989-04-0707 April 1989 PNS-I-89-003:on 890401,security Officer Allegedly Committed Homicide While on Vacation.Weapon Unconnected to Employment. Measures Taken to Preclude Individual from Returning to Work Pending Outcome of Case.Commonwealth of PA Informed PNO-I-88-096, on 880917,licensee Shut Down Unit to Troubleshoot &/Or Repair Cause of High Flow in Seal leak-off Line 1 for Reactor Coolant Pump D1988-09-19019 September 1988 PNO-I-88-096:on 880917,licensee Shut Down Unit to Troubleshoot &/Or Repair Cause of High Flow in Seal leak-off Line 1 for Reactor Coolant Pump D PNO-I-88-084A, on 880829,resident Inspectors Informed of Results of Drug Testing on Licensee Reactor Operator Involved in Altercation Described in PNO-I-88-084.Licensee Terminated Employee on Basis of Positive Test Results1988-08-30030 August 1988 PNO-I-88-084A:on 880829,resident Inspectors Informed of Results of Drug Testing on Licensee Reactor Operator Involved in Altercation Described in PNO-I-88-084.Licensee Terminated Employee on Basis of Positive Test Results PNO-I-88-075, on 880720,results of Independent Investigation Re Operator Sleeping on Duty Announced.Disciplinary Actions Including Dismissal,Reassignments to Lower Positions & Formal Reprimands Made Effective on 8807191988-07-20020 July 1988 PNO-I-88-075:on 880720,results of Independent Investigation Re Operator Sleeping on Duty Announced.Disciplinary Actions Including Dismissal,Reassignments to Lower Positions & Formal Reprimands Made Effective on 880719 PNO-I-88-055, on 880523,worker Slipped & Fell Into Reactor Vessel from Defueling Platform.Caused by Worker Unhooking Himself from Sling to Install Equipment in Reactor Vessel. Worker Decontaminated & Licensee Conducted Event Critique1988-05-23023 May 1988 PNO-I-88-055:on 880523,worker Slipped & Fell Into Reactor Vessel from Defueling Platform.Caused by Worker Unhooking Himself from Sling to Install Equipment in Reactor Vessel. Worker Decontaminated & Licensee Conducted Event Critique PNO-I-88-021, on 880216,licensee Commenced Power Decrease to Hot Shutdown Condition Due to Main Turbine Generator Stator Cooling Flow Problem.In Conjunction W/Ge,Licensee Plans Chemical Cleaning & Backflush Process of Sys1988-02-17017 February 1988 PNO-I-88-021:on 880216,licensee Commenced Power Decrease to Hot Shutdown Condition Due to Main Turbine Generator Stator Cooling Flow Problem.In Conjunction W/Ge,Licensee Plans Chemical Cleaning & Backflush Process of Sys ML20236V9011987-11-30030 November 1987 PNO-TMI-87-005:on 871124,licensee Informed NRC That Investigation Re 870709 Allegation of Shift Supervisor Sleeping on Shift Has Been Finalized & Rept Will Be Provided to Nrc.Util Dismissed Shift Supervisor Under Investigation ML20236P9971987-11-12012 November 1987 PNO-TMI-87-004:on 871026,improperly Solidified Shipment of Class B Waste Identified.Waste Transported to Barnwell Disposal Site from Facility.Corrective Actions to Be Submitted to State No Later than 871125 PNO-I-87-063A, on 870710,special Insp Team Dispatched to Facility to Review Licensee Efforts Re Allegations of Sleeping on Duty.Random Offshift Insp Identified No Evidence of Operators Inattention to Duties1987-07-13013 July 1987 PNO-I-87-063A:on 870710,special Insp Team Dispatched to Facility to Review Licensee Efforts Re Allegations of Sleeping on Duty.Random Offshift Insp Identified No Evidence of Operators Inattention to Duties PNO-I-87-063, on 870709,NRC & Util Received Anonymous Allegation Re Shift Supervisor Sleeping on Duty.Makeshift Beds Identified & Dismantled & Three Contract Employees Terminated for Sleeping Onsite1987-07-10010 July 1987 PNO-I-87-063:on 870709,NRC & Util Received Anonymous Allegation Re Shift Supervisor Sleeping on Duty.Makeshift Beds Identified & Dismantled & Three Contract Employees Terminated for Sleeping Onsite PNO-I-87-055, on 870612,reactor Shut Down Due to Increased Leakage from Letdown Cooler A.Letdown Cooler Will Be Replaced During 1-month Outage1987-06-15015 June 1987 PNO-I-87-055:on 870612,reactor Shut Down Due to Increased Leakage from Letdown Cooler A.Letdown Cooler Will Be Replaced During 1-month Outage PNO-I-87-049B, on 870612,NRC Informed That Confirmed Positive Drug Test Results Received on 10 Employees.One Employee Fired,One Reassigned & Eight Suspended.Positive Results for Licensed Operators or Mgt Personnel Not Received1987-06-15015 June 1987 PNO-I-87-049B:on 870612,NRC Informed That Confirmed Positive Drug Test Results Received on 10 Employees.One Employee Fired,One Reassigned & Eight Suspended.Positive Results for Licensed Operators or Mgt Personnel Not Received PNO-I-87-049A, updates Licensee Drug Investigation at Facility.Licensee Not Releasing Details to Media or Public Due to Ongoing Investigation.Notification Issued on 870601 Contained Typo.Actual Date of Notification Should Be 8705191987-06-0303 June 1987 PNO-I-87-049A:updates Licensee Drug Investigation at Facility.Licensee Not Releasing Details to Media or Public Due to Ongoing Investigation.Notification Issued on 870601 Contained Typo.Actual Date of Notification Should Be 870519 ML20214R5151987-06-0202 June 1987 PNS-I-87-049:on 870319,licensee Notified Region I of Ongoing Drug Investigation.On 870601,local Tv Staion Told by Anonymous Source That Plant Workers Suspended as Result of Drug Testing.Licensee Ack Drug Investigation to Reporter ML20210C7191987-05-0404 May 1987 PNO-TMI-87-003:on 870503,4-inch Diameter Reinforced Rubber Pump Discharge Hose Ruptured on Defueling Water Cleanup Sys Spilling Approx 150 Gallons of Unfiltered Reactor Coolant. Three Persons Sprayed W/Water Decontaminated ML20205H2711987-03-26026 March 1987 PNO-TMI-87-002:on 870324,train Carrying Two Shipping Casks Containing TMI-2 Core Debris Struck Automobile in St Louis, Mo.Train Engine Received Minor Damage But Shipping Casks Not Damaged.No Release of Radioactive Matls Detected PNO-I-87-023, on 870323,reactor Critical Following 5-month Outage.Remote Shutdown Panel Test Conducted on 870322.Steam Generator Instruments Monitored Due to Lack of Agreement1987-03-24024 March 1987 PNO-I-87-023:on 870323,reactor Critical Following 5-month Outage.Remote Shutdown Panel Test Conducted on 870322.Steam Generator Instruments Monitored Due to Lack of Agreement ML20212D9241987-02-26026 February 1987 PNO-TMI-87-001:on 870225,radioactive Sample Container in Bed of Truck Discovered Offsite for 2 H.Caused by Container Apparently Placed in Truck When Matl Transported from One Onsite Location to Another.Container Sealed & Tagged PNO-I-87-006, in Dec 1986,licensee Informed Region I of Investigation of Employee Allegation Re Drug Use at Facility.Alleger Implicated 14 People.One Individual resigned,3 Tested Positive & 10 Cleared After Testing1987-01-28028 January 1987 PNO-I-87-006:in Dec 1986,licensee Informed Region I of Investigation of Employee Allegation Re Drug Use at Facility.Alleger Implicated 14 People.One Individual resigned,3 Tested Positive & 10 Cleared After Testing ML20211P9211986-12-16016 December 1986 PNO-TMI-86-005:on 861216,worker Injured in Reactor Bldg Containment When Temporary Lead Shield Fell.Worker Removed from Bldg After Receiving First Aid by Emergency Response Crew.Worker Decontaminated While En Route to Medical Ctr ML20203L3141986-08-20020 August 1986 PNO-TMI-86-004:on 860819,worker on Defueling Platform Injured When long-handled Tool in Reactor Vessel Dislodged from Temporary Storage Location,Pinning Hand Against Rack & Causing Laceration & Possible Fracture PNO-I-86-040, on 860602,reactor Scrammed Due to Trip of Main Turbine.Caused by Loss of Electrohydraulic Control Oil During Secondary Plant Electrical Power Supply Switching1986-06-0202 June 1986 PNO-I-86-040:on 860602,reactor Scrammed Due to Trip of Main Turbine.Caused by Loss of Electrohydraulic Control Oil During Secondary Plant Electrical Power Supply Switching ML20203J1821986-04-25025 April 1986 PNO-TMI-86-003:on 860425,contract Laborer Employed by Licensee Found Small Amount of Marijuana in Personnel Change Facility within Protected Area.Substance Turned Over to Security Personnel.Investigation Underway PNO-I-86-034, on 860424,plant Shut Down Due to Main Turbine Drain Line Steam Leak from Turbine Control Valve Header. Caused by Failed Weld at Socket Joint.Repairs Being Performed.Commonwealth of PA Notified1986-04-24024 April 1986 PNO-I-86-034:on 860424,plant Shut Down Due to Main Turbine Drain Line Steam Leak from Turbine Control Valve Header. Caused by Failed Weld at Socket Joint.Repairs Being Performed.Commonwealth of PA Notified PNO-I-86-033, on 860423,during Restart from Steam Generator Tube Insp Outage,Reactor Tripped from 8% Power on High RCS Pressure.Caused by Main Feedwater Transient in Which turbine-driven Pump Decreased Speed1986-04-23023 April 1986 PNO-I-86-033:on 860423,during Restart from Steam Generator Tube Insp Outage,Reactor Tripped from 8% Power on High RCS Pressure.Caused by Main Feedwater Transient in Which turbine-driven Pump Decreased Speed PNO-I-86-031, on 860421,loss of 4,160-volt Vital Bus & All Three Nonvital Buses Experienced.Caused by Vital Bus D Supply Breaker Fault & Trip.Power Restored to Nonvital Buses.Vital Bus D Supply Breaker Damaged1986-04-21021 April 1986 PNO-I-86-031:on 860421,loss of 4,160-volt Vital Bus & All Three Nonvital Buses Experienced.Caused by Vital Bus D Supply Breaker Fault & Trip.Power Restored to Nonvital Buses.Vital Bus D Supply Breaker Damaged PNO-I-86-024, on 860324,during Scheduled Outage Work in Reactor Bldg Five Workers Contaminated.Contamination Attributed to I-131 Evolving from RCS Water.Iodine Being Removed by Purging Reactor Bldg Air1986-03-26026 March 1986 PNO-I-86-024:on 860324,during Scheduled Outage Work in Reactor Bldg Five Workers Contaminated.Contamination Attributed to I-131 Evolving from RCS Water.Iodine Being Removed by Purging Reactor Bldg Air PNO-I-86-009A, on 860204,plant Restarted Following Outage to Replace Turbine Extraction Steam Bellows Inside Main Condenser1986-02-0505 February 1986 PNO-I-86-009A:on 860204,plant Restarted Following Outage to Replace Turbine Extraction Steam Bellows Inside Main Condenser ML20205J2231986-01-28028 January 1986 PNO-TMI-86-002:on 860128,electrician Passed Out on Defueling Platform While Changing Light Bulbs.Emergency Response Team Responded.Individual Examined,Frisked & Transported to Hosp. Cause Unknown PNO-I-86-009, on 860127,reactor Shut Down to Repair Leaking Expansion Bellows on Feedwater Heater Extraction Steam Line. Cause of Leakage Not Stated.Outage Should Last 1 Wk1986-01-27027 January 1986 PNO-I-86-009:on 860127,reactor Shut Down to Repair Leaking Expansion Bellows on Feedwater Heater Extraction Steam Line. Cause of Leakage Not Stated.Outage Should Last 1 Wk ML20137D9091986-01-13013 January 1986 PNO-TMI-86-001:on 860112,licensee Transferred First Three Loaded Fuel Canisters Out of Reactor Bldg Into Fuel Handling Bldg.Canisters Loaded W/Core Debris.Highest Radiation Level on Transfer Shield Surface Was 20 M/H PNO-I-85-095, on 851230,seal Failure on RCS Makeup Pump 1A Occurred,Spilling Approx 300 Gallons of Water on Floor.Nine Personnel Slightly Contaminated.Approx 46 Ci Released from Plant.Pump Drained.Personnel Cleaned Up Room1985-12-30030 December 1985 PNO-I-85-095:on 851230,seal Failure on RCS Makeup Pump 1A Occurred,Spilling Approx 300 Gallons of Water on Floor.Nine Personnel Slightly Contaminated.Approx 46 Ci Released from Plant.Pump Drained.Personnel Cleaned Up Room ML20138M2531985-12-16016 December 1985 PNO-TMI-85-011:on 851214,load Drop Event Occurred When Defueling Canister & Support Sleeve Fell Into Reactor Vessel.Both Retrieved & Restored to Original Configuration in Canister Positioning Sys Using Reactor Bldg Svc Crane ML20138L8001985-12-16016 December 1985 PNO-TMI-85-011:on 851214,load Drop Event Occurred When Defueling Canister & Support Sleeve Fell Into Reactor Vessel.Caused by Jib Crane Being Overweighted.Crane Taken Out of Svc Pending Evaluations Re Effects on Load Lift ML20138L0191985-10-28028 October 1985 PNO-TMI-85-010:on 851028,initial Phase of Defueling Damaged Reactor Core Will Begin.Defueling Will Involve Manipulation of Partial Fuel Assemblies in Preparation for Loading Into Canisters.Press Release Issued PNO-I-85-079, on 851016,steam Leak Identified on Drain Line from Associated Main Turbine Control Valve Header.Caused by through-wall Crack in Weld Associated W/Pipe Elbow.Power Reduced from 40% to Make Repairs1985-10-16016 October 1985 PNO-I-85-079:on 851016,steam Leak Identified on Drain Line from Associated Main Turbine Control Valve Header.Caused by through-wall Crack in Weld Associated W/Pipe Elbow.Power Reduced from 40% to Make Repairs PNO-I-85-067A, on 850924-25,failed Reactor Protection Sys Breaker Removed & Examined.Failure Caused by Mechanical Binding within Breaker Closure Assembly.Investigation Continuing1985-09-27027 September 1985 PNO-I-85-067A:on 850924-25,failed Reactor Protection Sys Breaker Removed & Examined.Failure Caused by Mechanical Binding within Breaker Closure Assembly.Investigation Continuing ML20132C4491985-09-25025 September 1985 PNO-TMI-85-009:error in Sr-90 Radiochemistry Quantitative Analysis Used Since 1981 for Solid Samples Resulted in Reporting of one-half Actual Value.Past Shipments of Radwaste to Hanford,Wa May Exceed 10CFR61.55 Requirements 1997-09-12
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000133/19990021999-09-29029 September 1999 Insp Rept 50-133/99-02 on 990915.No Violations Noted.Major Areas Inspected:Licensee Physical Security Program IR 05000289/19990071999-09-27027 September 1999 Insp Rept 50-289/99-07 on 990718-0828.No Violations Noted. Major Areas Inspected:Operations,Maint & Plant Support IR 05000289/19990041999-08-19019 August 1999 Insp Rept 50-289/99-04 on 990606-0717.Noncited Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000289/19990051999-07-0909 July 1999 Insp Rept 50-289/99-05 on 990510-28.No Violations Noted. Major Areas Inspected:Effectiveness of Engineering Functions in Providing for Safe Operation of Plant IR 05000289/19990061999-07-0808 July 1999 Insp Rept 50-289/99-06 on 990608-11.No Violations Noted. Major Areas Inspected:Licensee Emergency Preparedness Plan IR 05000289/19990031999-06-29029 June 1999 Insp Rept 50-289/99-03 on 990425-0605.No Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000289/19990021999-05-14014 May 1999 Insp Rept 50-289/99-02 on 990314-0424.Two Violations Noted & Being Treated as non-cited Violations.Major Areas Inspected: Aspects of Licensee Operations,Maint,Engineering & Plant Support.Security Program Met Safeguards Requirements IR 05000289/19990011999-04-16016 April 1999 Insp Rept 50-289/99-01 on 990131-0313.No Violations Noted. Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000133/19990011999-04-0808 April 1999 Insp Rept 50-133/99-01 on 990222-25 & 0308.No Violations Identified.Major Areas Inspected:Decommissioning Performance,Status,Organization,Maint & Cost controls,self- Assessments,Audits & Corrective Actions IR 05000289/19980091999-03-0505 March 1999 Insp Rept 50-289/98-09 on 981227-990130.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000289/19980081999-01-12012 January 1999 Insp Rept 50-289/98-08 on 981101-1226.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000289/19980071998-12-0303 December 1998 Insp Rept 50-289/98-07 on 980920-1031.No Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support,Including Results of Insps by Regional Inspector Re Emergency Preparedness & Radiological Controls IR 05000133/19980041998-11-20020 November 1998 Insp Rept 50-133/98-04 on 980901-03,1012-17 & 20-22.No Violations Noted.Major Areas Inspected:Review Work Activities Associated with Removal of 250 Ft Tall Ventilation Stack ML20154M0251998-10-15015 October 1998 Insp Rept 50-289/98-06 on 980810-27.Violations Noted.Major Areas Inspected:Engineering Activities Associated with Findings from NRC Architect Engineering Team Insp Completed in Jan 1997 & Documented in NRC Insp Rept 50-289/96-201 ML20154L9821998-10-15015 October 1998 Notice of Violation from Insp on 980810-27.Violation Noted: in Oct 1997,change to Facility as Described in Section 6.1, Eccs,Of TMI-1 Ufsar,Involving Unreviewed Safety Question,Was Made Without Prior Commission Approval IR 05000289/19980051998-10-0202 October 1998 Insp Rept 50-289/98-05 on 980726-0919.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support.Security Facilities & Equipment Were Well Maintain, Reliable & Met Licensee Commitments & NRC Requirements ML20153E9471998-09-24024 September 1998 Exam Rept 50-289/98-301 Conducted on 980824-27.Exam Results: Four SRO Applicants Passed All Portions of Initial License Exam IR 05000289/19980031998-09-0404 September 1998 Insp Rept 50-289/98-03 on 980524-0725.No Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000289/19980021998-06-22022 June 1998 Insp Rept 50-289/98-02 on 980322-0523.No Violations Noted. Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support IR 05000133/19980031998-05-22022 May 1998 Insp Rept 50-133/98-03 on 980427-30.No Violations Noted. Major Areas Inspected:Decommissioning Performance & Status, Organization,Mgt & Cost Controls & Radioactive Waste Treatment,Effluents & Environ Monitoring IR 05000133/19980021998-05-14014 May 1998 Insp Rept 50-133/98-02 on 980414-15.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program Including Review of Alarm Stations,Physical Barriers, Detection Aids,Assessment Aids & Mgt Effectiveness IR 05000289/19980011998-04-0909 April 1998 Insp Rept 50-289/98-01 on 980125-0321.No Violations Noted. Major Areas Inspected:Plant Operations,Maint,Engineering & Plant Support IR 05000133/19980011998-02-27027 February 1998 Insp Rept 50-133/98-01 on 980126-29.No Violations Noted. Major Areas Inspected:Organization,Mgt & Cost Controls, Safety Reviews,Design Changes & Mods,Sf Pool Safety,Cold Weather Preparations & Decommissioning Performance Review IR 05000289/19970101998-02-26026 February 1998 Insp Repts 50-289/97-10 & 50-320/97-03 on 971102-980124. Violations Noted.Major Areas Inspected:Maint,Engineering & Plant Support.License Operator Requalification Program, Corrective Actions Program & Security Also Inspected ML20197A8771998-02-26026 February 1998 SALP Rept 50-289/98-99 for Period 960805-980124 ML20203L7821998-02-26026 February 1998 Notice of Violation from Insp on 971102-980124.Violation Noted:Licensee Not Review & Approve Substantive Change to Existing Inservice Test Surveillance Procedure. Page 25 of Incoming Submittal Not Included ML20199H6141998-01-27027 January 1998 Notice of Violation from Insp on 970907-1101.Violation Noted:Pressurizer Power Operated Relief Valve Was Returned to Svc Without Performing an IST to Verify Proper Valve Operation After Valve Replaced ML20203D7591997-12-0202 December 1997 Insp Rept 50-289/97-09 on 970907-1101.Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support Over 8 Wk Period PNO-I-97-068, on 971103,unplanned Shutdown Greater than 72 H Occurred.Oil Leaks Detected & Repaired.Third RCP Inspected & Engineers Found Low Seal Flow at Second Stage Pump Seal. Resident Inspectors Following Onsite Activities1997-11-0505 November 1997 PNO-I-97-068:on 971103,unplanned Shutdown Greater than 72 H Occurred.Oil Leaks Detected & Repaired.Third RCP Inspected & Engineers Found Low Seal Flow at Second Stage Pump Seal. Resident Inspectors Following Onsite Activities IR 05000289/19970081997-10-0909 October 1997 Insp Rept 50-289/97-08 on 970728-0906.No Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support & Results of Announced Insp in Area of Emergency Preparedness ML20217H3281997-10-0808 October 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $210,000.Violation Noted:On 940601,design Bases Were Not Correctly Translated Into Operating Procedures Re Switchover of Dhrs Pumps from Bwst to Reactor Building Sump ML20198R2831997-10-0303 October 1997 EN-97-096:on 971008,notice of Proposed Imposition of Civil Penalty in Amount of $210,000 Issued to Licensee.Action Based on Violations Involving Design Engineering,Equipment Classification & Corrective Actions IR 05000133/19970021997-10-0101 October 1997 Insp Rept 50-133/97-02 on 970513-0911.Violations Noted.Major Areas Inspected:Organization,Mgt & Cost Controls,Employee Concern Program,Decommissioning projects,10CFR50.59 SE Program,Annual Environ Rept Reviews & Maint & Surveillance ML20217D6381997-10-0101 October 1997 NOV from Insp on 970513-0911.Violation Noted:Process Water Monitor Was Set to Alarm at 300,000 Counts Per Minute PNO-IV-97-050, on 970911,completed Repair of Reactor Caisson Leak by Reducing in-leakage to Less than Ten Gallons/Day. Informed State of CA1997-09-12012 September 1997 PNO-IV-97-050:on 970911,completed Repair of Reactor Caisson Leak by Reducing in-leakage to Less than Ten Gallons/Day. Informed State of CA IR 05000289/19970061997-08-19019 August 1997 Insp Repts 50-289/97-06 & 50-320/97-02 on 970616-0727. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support ML20210R9801997-08-19019 August 1997 Insp Repts 50-289/97-06 & 50-320/97-02 on 970616-0727. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support ML20210R9641997-08-19019 August 1997 Notice of Violation from Insp on 970616-0727.Violation Noted:Licensee Failed to Implement EP Implementing Procedure EPIP-TMI-.03,Exhibit 1, Emergency Notifications & Call Outs ML20149K0171997-07-23023 July 1997 Insp Rept 50-289/97-07 on 970428-0502 & 0512-16.Violations Noted.Major Areas Inspected:Engineering ML20149K0081997-07-23023 July 1997 Notice of Violation from Insp on 970428-0502 & 0512-16. Violations Noted:On 970430,LER 97-03,did Not Contain Clear, Specific,Narrative Description of What Occurred IR 05000289/19970051997-07-11011 July 1997 Insp Rept 50-289/97-05 on 970428-0615.No Violations Noted. Major Areas Inspected:Plant Operations,Maint,Engineering & Plant Support ML20148S2321997-06-27027 June 1997 Insp Rept 50-289/97-04 on 970512-15.Violations Noted. Major Areas Inspected:Insp Evaluated Licensee Performance During Remedial EP Exercise IR 05000289/19970031997-05-29029 May 1997 Insp Rept 50-289/97-03 on 970303-0427.Apparent Violations Being Considered for Escalated Enforcement Action IAW NUREG-1600.Major Areas Inspected:Plant Operations,Maint, Engineering & Plant Support IR 05000289/19970021997-04-24024 April 1997 Insp Rept 50-289/97-02 on 970305-07.No Violations Noted. Major Areas Inspected:Insp Evaluated Licensee Emergency Response Capabilities Demonstrated During Biennial Full Participation EP Exercise ML20137W9391997-04-15015 April 1997 Insp Rept 50-289/96-201 on 961202-20 & 970106-10.No Violations Noted.Major Areas Inspected:Conduct of Engineering,Insp Scope & Methodology,Makeup & Purification Sys,Decay Heat Removal Sys & Control of Calculations PNO-I-97-018, on 970328,protest Related to TMI-2 Accident Occurred.Protesters Walked in Circle,Outside of Util Property,Blocking Plant Entrance Lane.Plant Notified NRC Headquarter to Inform of Event1997-03-28028 March 1997 PNO-I-97-018:on 970328,protest Related to TMI-2 Accident Occurred.Protesters Walked in Circle,Outside of Util Property,Blocking Plant Entrance Lane.Plant Notified NRC Headquarter to Inform of Event ML20140B7051997-03-21021 March 1997 Insp Repts 50-289/97-01 & 50-320/97-01 on 970106-970302. Violations Noted.Major Areas Inspected:Plant Operations, Maintenance,Engineering & Plant Support IR 05000289/19960091997-01-22022 January 1997 Insp Rept 50-289/96-09 on 961119-970105.No Violations Noted. Major Areas Inspected:Operations,Engineering,Maint & Plant Support ML20135F1641996-12-0606 December 1996 Notice of Violation from Insp on 960929-1118.Violation Noted:Scaffold tied-off & Supported by Safety Related Pipe Support for Nuclear River Water Sys W/O Prior Engineering Evaluation & Approval IR 05000289/19960071996-11-18018 November 1996 Insp Rept 50-289/96-07 on 960929-1118.Violations Noted. Major Areas Inspected:Conduct of Operations, Quality Assurance in Operations & Conduct of Maint 1999-09-29
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V' .
,. . IMMEDIATE e' PRELIMINARY NOTIFICATION
, April 25,1979 PREI.IMINARY NOTIFICATION OF EVENT OR UTUSUAI, OCCURRENCE -PNO-79-67AF This preliminary notification constitutes sununary information of an eNnt of safety or public interest significance. The information presented is~
a summary of information as of 7:00 a.m. on April 25, 1979. .
Facility: Three Mile Island Unit 2 Middletown, Pennsylvania (DN 50-320)
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Stibj ecta NUCLEAR INCIDENT AT THREE MILE ISLAND Plant Status In the course of transferring feedwater flow to the auxiliary noz=les, a carryover of water into the steam line was experienced, resulting g in water impingement in the main turbine. An operator-initiated turbine trip at about 3:00 p.m. stopped the impingement. The feedwater was being diverted to the auxiliary feedvater sparger in preparation for I secondary system modification for adding a closed cooling r,yr: tem. !
Steam is currently being admitted to the main condenser through the :
turbine bypass valves. This change in cooling mode will not affect '
6 dish preparations for natural cirenlation operations. The average
' M primary coolant temperature has increased to 224 degrees F. The highests incore thermocouple reading.is 312 degrees F.
As a result of changing the charcoal filters in the A Trains of the -
Auxiliary and Fuel Handling Building Ventilation Systems, the iodin'.e discharges have been reduced by approximately 80 percent. The I charcoal filters of Auxiliary Building Ventilation System Train B l have been replaced. This system was placed in service at 5:30 a.m. l April 25. I Following a briefing of the Governor's Office, a press briefing was t held to outline the anticipated schedule for achieving long term ]
cooling status. A copy of the press release is attached.
Environmental Status Three Aerial Measuring System (ARMS) Surveys were made on April 24, 1979. No radioactivity above natural background was detected, y [ _ CONTINUED ~
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- g. .gIMMEDIATEPRELIMINARYNOTIFICATION , ,
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W k^h oso20 2 -30
. i j Continued April 25, 1979 (
j Page 2 PNO-79-67AF i
i t c Iodine concentration at Unit 2 ventilation stack (Analyzed by NRC Mobile Laboratory). ,, {
Date/ Time Activity (uCi/ce) .
~0 4/24 (0408) - 4/24 (0637) 3.0 x 10 4/24 (0642) - 4/24 (0813) 4.2 x 10",8 4/24 (0815) - 4/24 (1215) 3.1 x 10 -
4/24 (1217) - 4/24 (1600) 1.6 x 10,83
, , , . _, 4/24 (1602) - 4/24 (1955) 2.4 x 10 -8 4/24 (1958) - 4/25 (0001) 2.6 x 10 Offsite Measurements j
Radiation Levelt Offsite radiation levels identified by NRC survey teams continue to be consistent with natural background levels (0.02 mR/hr maximum).
These results were obtained from routine daily surveys performed downwind on the east. side of the Susquehanna River at distances up i i gg to five miles north and south of the site. gy Dose rates (47 locations) as measured by NRC thermoluminescent '
dosimeters (TLDs) for the past 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period continue to be consis- ,
tent with natural background levels.
NRC Environmental Samples (Samples tak,en offsite within 3 miles of site analyzed in mobile laboratory)
Nunber of I Sample Type Date of Sample Samples Results air 4/24-25 6 Less than MDA*
milk 4/23 3 Less than MDA daily air 4/23-24 1 Less than MDA
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EPA Environmental Samples (Analyzed at Remote Laboratory) ,
Number of >
Sample Type Date of Sample Samples Results air 4/23 28 Less than MDA ,33 air 4/23 '
3 Range from 2.3 to 7.1 x 10 1 microcuires per cubic centi-
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meter (0.23 to 0.71 picoeuries )
1
.. per cubic meter) air #,,
4/20 2 One sample was less 'than MDA. One sample indicated 168 picoeuries per cubic meter of Xe-133.**
Both samples indicated approximate background levels of Kr-85.
CONTINUED
- IMMEDIATE PRELIMINARY NOTIFICATION l
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Continued Page 3 April 25, 1979 PNO-79-67AP All EPA samples were taken at distances greater than 2 miles from this site. '
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- MDA - minimum detectable activity.
- Maximum Permissible Concentration for Xe-133 is 300,000 picoeuries' per cubic meter.
The' Commonwealth of Pennsylvania has been informed of these results.
Attachment:
Press Release Dated 4/24/79 Contaett Distribution: Transmitted H St ~2' I v-Chairman FIEdrie Commissioner Bradford S. J. Chilk, SECY I Coassissioner Kennedy Commissioner Ahearne- C. C. Kassnerer, CA Conseissioner Gilinsky (For Distribution)
Transmitted: MNBD ~ P. Bldg L. V. Gossick, EDO H. R. Denton, NRR J. G. Davis, Region I IE )
H. L. Ornstein, EDO g.
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m R, C. DeYoung, NRR Reg, ion'II _
i J. J. Fouchard,.PA R. J. Mattson, NRR Region III l
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! N. M. Haller MPA V. Stello, NRR Region IV L IN R. C. Ryan, OSP R. S. boyd, NRR Region V H. K. Shapar, ELD J SS Bldg . (MAIL)
W. J. Dircks, NMSS J. J. Cummings, OIA i
S. Levine, RES R. Minogue, SD M ) IE (THI) Site (Provide copy to STATE)
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White House Situation Room j FDAA' (Provide copies to the Administrator and the Operations. Center)
EPA DOE /EOC PEMA BRP (State of PA)
DCPA BEW (Pickup)
Handcarry (FAA)
IMMEDIAIE '
I PRELIMINARY NOTI.F-ICATION j
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Attachment to PNO-79-67AF FOR IMMEDIATE RELEASE i
i ._+ April 24, 1979 .
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The NRC staff today announced a tbnetable for placing the Three .
Mile Island Unit 2 reactor on natural circulation cooling. As i stated on previous occasions, it is now possible to cool the reactor by natural convection circulation if difficulties arise l
with presently operating equipment. It is, of course, preferable L
to place the plant on natural circulation in a planned fashion
- while presently available plant instruments and equipment remain
[ functioning; However, if instrumentation in the plant does not ;
l retain its reliability and the various backup methods presently available do not function adequately, it may be necessary to place f the plant on natural circulation at that time, j The excessive non-condensable gases in the system have been !
removed and are now at an acceptable level.
The phased reduction in primary system temperature has nov reached
' approximately 175*F. ' This reduction in temperature is greater g
.";;.; _ than originally anticipated with steaming in the steam generator ha3 A. ~
l Assuming current instrumentation continues to perform satisfactorily,
! the following timetable for a planned transition to natural circula-l tion has been established. The sequences planned to reach this
l 1. The "B" steam generator will be placed in a water solid condition by April 29th. ,
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- 2. The "A" steam generator will be placed in a water solid condition by April 30th.
- 3. Action needed to upgrade the backup cooling capability of the existing decay heat removal system will be completed by May 1. l
- 4. With these steps completed, the primary system recirculation pump will be shut off on May 2nd and the system will then go into natural circulation. --
There areca~ number of 'o'ther ongoing actions at the plant. - - '
- 1. Radioactive ef fluent filter systems within the plant have been upgraded. An independent redundant charcoal filter system, which will serve as a second stage of removal, has been under construction for some time. The new system is
. expected to be operational by May 2nd.
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.2. Modifications are currently in progres's that will permit the
secondary side of the "B" steam generator to be operated in a closed system, i.e., without the need for the availability of the main condenser. This activity is scheduled for comple-tion for May 7th. Closed system cooling of stcan generator B is not essential to establish stable natural circulation cooling.
- 3. The "A" steam generator also will be modified to permit operation in a closed system. This modification also is not required t.o establish natural circulation. Its schedule for completion is currently estimated to be the middle of May.
- 4. The passive level and pressure control system that will augment existing plant systems is expected to be completed by mid-May. This system is not needed to achieve natural circula-tion, but it is prudent to add this redundancy to the existing plant equipment for long term monitoring of natural circula-tion cooling. ,
f@$$~ 5. Modifications on the onsite electrical system are currently %
being made. Additional diesel, generators have been delivered to the site to provide a backup power supply, and are currently being placed on their foundations. Electrical instrumentation and other necessary connections will be completed by April 27th.
- 6. There are a number of additional modifications being made within the facility that are related to the long term recovery from the accident. Such modifications include adding an additional decay beat removal system with equipment to process and remove the radioactive materials from the primary coolant system; the installation of additional tanks to provide for storage of contaminated water that may result
! from decontamination activities; installation of additional i
contaminated water processing equipment, and general decon-tamination activities needed in the auxiliary building.
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