ML20236K739

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Insp Repts 50-277/87-17 & 50-278/87-17 on 870601-0717.No Violations Noted.Major Areas Inspected:Operational Safety, Shutdown Order Commitments,Radiation Protection,Physical Security,Control Room Activities & Licensee Events
ML20236K739
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 07/24/1987
From: Gallo R, Linville J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20236K676 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-2.K.3.18, TASK-TM 50-277-87-17, 50-278-87-17, IEB-85-003, IEB-85-3, NUDOCS 8708070237
Download: ML20236K739 (39)


See also: IR 05000277/1987017

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U. S. NUCLEAR REGULATORY COMMISSION

REGION I

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Report No. 50-277/87-17 & 50-278/87-17

Docket No. 50-277 & 50-278

License No. OPR-44 & DPR-56

Licensee: Philadelphia Electric Company

c.T 2301 Market-Street

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_ Philadelphia, Pennsylvania 19101

Facility Name: Peach Bottom Atomic Power Station Units.2 and 3

, Inspection At: Delta, Pennsylvania

Inspection'Conducte'd: June 1, 1987 to July 17, 1987

Inspectors: T. P. Johnson, Senior Resident Inspector

R. J. Urban, Resident Inspector

L. L. Scholl, Reactor Engineer

L. E. Myers, Resident' Inspector

S. D. Kucharski, Resident Inspector, Limerick

Revlewed By: OM1

.. / LT7iviile, Chief /

7/2347

'/ ' gat 6

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e 6 tor Projects Se on 2A,

vision of Reacto Projects

Approved By: Qfd5 [w '1 >4 1

R. W./ Gall , Chief, y date

Reactor Pr ts Branch 2,

Division of Reactor Projects

Inspection Summary: Routine, on site regular and backshift resident

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inspection'(210 hours0.00243 days <br />0.0583 hours <br />3.472222e-4 weeks <br />7.9905e-5 months <br /> Unit 2; 174 hours0.00201 days <br />0.0483 hours <br />2.876984e-4 weeks <br />6.6207e-5 months <br /> Unit 3) of accessible portions of

Unit 2 and 3, operational safety, shutdown Order commitments, radiation i

protection, physical security, control room activities, licensee events, j

surveillance testing, refueling and outage activities, Unit 2 core reload

and outage activities, maintenance, and outstanding items. In addition, a )

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review'of the apparently inoperable Control Room Ventilation Radiation

Monitoring System was conducted.

Results: One violation (section 4.4.5) for failing to perform a Technical

Specification surveillance test on the Unit 2 A loop of drywell spray. The ,

Control Room Ventilation Radiation Monitoring System has been incorrectly j

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configured and apparently out of service since initial plant startup (see

section 6.2.3). Annunciator auto / manual reset switches are neither

controlled nor documented. Several ESF actuations occurred on Unit 2 (see

section 4.2). An error by a licensed reactor operator resulted in a

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shutdown scram on Unit 2 (see.section 4.2.2). A partial loss of off site

power occurred on July 10, 1987 (see section 4.2.6). L'censee actions were

observed from the Control Room and were effective. The conduct of the Unit 2

core reload activities was also effective.

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I_ DETAILS

1.0 Persons Conta$ced

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,e?~ B. L. Clark, Administration Engineer

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.G. F. Dawson, Maintenance Engineer

A.'A, Fulvio, Technical Engineer

J..A. Jordan, Performance Engineer

J. C. Oddo, Nuclear Security Specialist

D. L. Oltmans, Senior Chemist

F. W. Polaski, Operations Engineer

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D. P. Potocik, Senior Health Physicist

G. R. Rainey, Superintendent Plant Services

M. B.,Ryan, Outage Engineer

D. C. Smith, Superintendent Operations

  • D. M. Smith, Manager, Peach Bottom Atomic Power Station

J. E. Winzenried, Staf f Engineer

Other licensee employees were also contacted.

l- *Present at exit interview on site and for summation of preliminary

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findings.

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2.0 plant Status

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2.1 Unit 2-

The unit began the inspection period with activities to return the

exchanged control rod drives to service to support core reload.

Other outage modi,fication, testing, and maintenance work was being

performed during to period. A reactor scram occurred on June 19,

1987, with the unit in a cold. shutdown condition (see section

4.2.2). Core reload began on June 22, 1987, and reload was

complete on July 1, 1987. The core was verified on July 2, 1937.

At the end of the report period, preparations for vessel

reassembly were in progress. Unit 2 remained in a cold shutdown

condition as required by NRC Order dated Manh 31, 1987.

M.2 Unit'3

The unit was maintained in a cold shutdown, with the reactor mode

switch in " shutdown" position, during the inspection period. This

was as required by NRC Order dated March 31, 1987.

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3.0 Previous Inspection Item Update

3.1 (0 pen) IE Bulletin 85-03. See section 4.4.3 of this report.

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4.0 Plant Operations Review

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4.1 Station Tours

The inspector observed plant operations during daily facility

tours. Most accessible plant areas were inspected.

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4.1.1 Control Room and facility shift staffing are frequently

checked for compliance with 10 CFR 50.54 and Technical

Specifications. The presence of a senior licensed operator { !

and the fluclear Operations Monitoring Team (f40MT) member

in the control room was verified frequently.

4.1.2 The inspector frequently observed that selected control

room instrumentation confirmed that instruments were '

operable and indicated values were within Technical

Specification requirements and normal operating limits.  !

ECCS switch positioning and valve lineups were verified

baseo on control room indicators and plant observations.

Observations included flow setpoints, breaker

positioning, PCIS status, and radiation monitoring

instruments.

4.1.3 Selected control room off-normal alarms (annunciators)

were discussed with control room operators and shift

supervision to assure they were knowledgeable of alarm

status, plant conditions, and that corrective action, if

required, was being taken. In addition, the applicable

alarm cards were checked for accuracy. The operators

were knowledgeable of alarm status and plant conditions.

On June 23, 1987, the inspector observed the once per

shift FPanalarm" annunciator alarm test conducted by the  ;

Unit 2 and 3 reactor operators. The inspector noted '

that for similar alarms on similar panels, some alarms

reset automatically (i.e., immediately when the alarm

was acknowledged) and some alarms had to be manually

reset (i.e., by depressing the reset push button). The

inspector checked Unit 2 alarm panel 20C205R versus Unit

3 alarm panel 30C205R. These alarm panels provide

annunciation for the reactor protection, neutron

monitoring, rod control and standby liquid control

systems. The 2(3)C205R panels have 45 alarm windows of

which 12 alarms were set up differently between Unit' 2 and

Unit 3 (i.e., manual vs. auto reset). The determination

as to whether an alarm will automatically or manually reset

depends on the position of an internal annunciator cam slide

switch. The inspector discussed the manual / auto reset

switch for alarms with operators and licensee management.

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The, inspector expressed a concern that the operators have

control and could reposition the auto / manual reset switch;

and, that 1,he required position of the switch was ne'ither

L ' I, documentecJon electrical prints nor on the alarm cards.

L The licensee- acknowledged this concern and on June 26, 1987,

-y issued a memo that directed the repositioning of auto / manual l

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, reset switches to the auto position to ensure consistency.

>} In addition, the licensee committed to performing an

s  ? evaluation to determine the permanent status of these auto /

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manual reset switches. The inspector will follow the status

of these annunciator auto / manual reset switches in a future

insprtion.

4.1.4 The inspector checked for fluid leaks by observing sump (

status, alarms, and pump-out rates; and discussed

reactor coolant system leakage with licensee personnel.

4.1.5 Shift relief and turnover activities were monitored

daily, including periodic backshift observations, to

ensure compliance with administrative procedures and

1 regulatory guidance. No inadequacies were identified.

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m 4.1.6 The inspector observed the m31n stack and both reactor

building ventilation stack radiation monitors and

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recorders, and periodically reviewed-traces from

backshift periods to verify that radioactive gas release

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rates were within limits and that unplanned releases had

not occurred. No inadequacies were identified.

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3 4.1.7 The inspector observed control room indications of fire

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'% detectiof instrumentation and fire suppression systems,

., monitored use of fire watches and ignition source

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," i controls, checked a sampling of fire barriers for

integrity, and observed fire-fighting equipment

,' ' stations. No inadequacies were identified.

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4.1.8 The inspecto" observed overall facility housekeeping

conditions, including control of combustibles, loose

trash and debris. Cleanup was spot-checked during and

after maintenance. Plant housekeeping was generally

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acceptable.

4.1.S The inspector observed the shutdown nuclear instrumentation

subsystems (source rege and intermediate range monitors)

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and the reactor protection system to verify that the required

channels were operable.

)h l On June 5,1987, during a routine control room tour, the

si inspector noted that there were differences in the Unit

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s 2 and Unit 3 RPS one line operater aid diagrams. The

, ( 'Jnit 2 diagrams (operator aid Nos. 84-21 and 38) and the j

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Unit 3 diagrams (operator aid Nos. 84-47 and 48) did not

accurately reflect the correct location of the RPS trip

breakers that were installed by modifications during

last refueling outage for each unit. In addition, a Unit

2 modification (MOD #1916) added a static inverter

supply to the alternate feed. The inspector discussed

these minor deficiencies with the on shift licensed

operators and STA. Pen and ink changes were made on the

affected RPS diagrams to reflect the correct alignment.

The inspector will continue to review this area on a

continuing basis.

4.1.10 The inspector frequently verified that the required

off site electrical power startup sources and emergency

on site diesel generators were operable. A loss of the

  1. 3 startup source during a lightning storm occurred on

July 10,'1987 (see section 4.2.6).

4.1.11 The inspector monitored the frequency of in plant and

control room tours by plant and corporate managenient.

The. tours were generally adequate.

4.1.12 The inspector verified operability of selected safety

related equipment and systems by in plant checks of

valve positioning, control of locked valves, power

supply availability, operating procedures, plant

drawings, instrumentation and breaker positioning.

Selected major components were visually inspected for

leakage, proper lubrication, cooling water supply,

operating air supply, and general conditions. No

significant piping vibration was detected. The

inspector reviewed selected blocking permits (tagouts)

for conformance to licensee procedures. Systems checked

included the Unit 3 shutdown cooling (RHR) system, and

the Unit 2 and 3 High Pressure Service Water (HPSW)

systems.

On June 12, 1987, the inspector noted that the 3B HPSW

pump was supplying the 3C RHR heat exchanger via the A

to B loop cross connect line, i.e. , key lock MOV 3344

was open. The 3A HPSW was out of service for

maintenance and the 3C HPSW pump was noted as running  ;

hot. Thus, the 3B and 3D HPSW pumps were the only two l

available for Unit 3. The inspector noted that the Unit '

2 and Unit 3 HPSW systems can be cross connected by

opening norn, ally locked closed valves HV-516A and B.

However, no currently approved operating procedure

exists for this operation. The licensee stated that

special procedures (SP) had been written in the past for

cross connecting the Unit 2 and 3 HPSW systems. SP-162,

164, 184 and 186 were written for specific uses during ,

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years 1977 and 1983. The licensee stated that the  !

procedure for cross connecting HPSW would be addressed 1

in a system (5) procedure (S.3.2). The inspector will

review this new "S" procedure in a future inspection.

4.1.13 The inspector performed backshift and week-end tours of

the facility on the following days:

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June 21, 1987; 8:00 a.m. - 12:00 noon.

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June 28, 1987; 6:00 p.m. - 10:00 p.m.

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July 13, 1987; 5:20 a.m. - 7:00 a.m.

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July 16, 1987; 12:00 midnight - 1:45 a.m.

4.2 Followup On Events Occurring During the Inspection

4.2.1 Unit 2 ESF Actuation on June 2,1987

A half group III outside containment ventilation j

isolation and half scram occurred on Unit 2 at 4:40 p.m. '

on June 2, 1987. Unit 2 was in a refueling outage with

the entire core offloaded. The cause of the isolation

was loss of power to the 2B Reactor Protection System

(RPS) bus. The 2B RPS bus was being powered from the

alternate feed when circuit breaker #23 from the 20Y50

panel tripped. In addition, the 20Y50 panel feeder breaker

(#52-3691) at motor control center E124-R-C was noted as

being. tripped. Modifications to the 2B RPS MG set required

the bus to be supplied from the alternate feed. The

licensee reset the isolation and half scram after re-

energizing the 2B RPS. An ENS call was made at 5:45 p.m.

and the senior resident was notified. The cause of the

breaker trip was determined to be an inadequately designed

SOLA voltage regulating tr ansformer (20X40) causing higher

than normal primary current. The licensee intends to

replace the transformer prior to startup.

The inspector reviewed the licensee's Suspected Licensee

Event Report (SLER), upset report, LER (see section 6.2.3),

and discussed the event with licensed operators and engineers.

L No violations were noted.

4.2.2 Unit 2 Scram with Core Offloaded on June 19, 1987

At 3:49 a.m. on June 19, 1937, a reactor scram occurred

on Unit 2. At the time of the scram, surveillance

testing was in progress on the IRMs. The core was

offloaded and no rod motion occurred as all rods were

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fully inserted. IRM surveillance test (ST) 3.2.3 was

being performed in preparation for core reload. The

cause of the scram was an apparent personnel error by

the reactor operator performing the surveillance and was "

compounded by equipment malfunction. The operator

failed to reset a channel "B" half scram signal before

testing the "A" channel scram circuitry. The licensee

reset the scram signal and made an ENS call at 5:05 a.m.

The inspector reviewed the SLER, the upset report, ST

3.2.3, and control room logs. The inspector also

discussed'the event with the operator performing the ST

and with licensee management. The inspector concluded

that the event was caused by a licensed operator error,

compounded by several equipment malfunctions during the

ST.

4.2.3 Unit 2 ESF Actuation on June 30, 1987

An outboard Group II containment isolation occurred on

Unit 2 at 8:41 a.m. on June 30, 1987. Unit 2 was in a

refueling outage with most of the fuel bundles reloaded

into the core. A Reactor Water Cleanup (RWCU) outside

containment isolation relay, 16A-K27, was being replaud

because it had reached the end of its Environmentally

Qualified (EQ) lifespan. The work was being accomplished

under maintenance request form (MRF) #2-61F-8407725, and

the relay was blocked using maintenance work permit

  1. 3-61 F-84-07723.

When the electrician lifted lead AY-10 from coil terminal

  1. 10, several relays were heard actuating. The following

outside containment isolation valves auto closed: drywell

instrument N2; drywell equipment alarm sump; and drywell

floor drain sump. Associated alarms were also received in

the control room. The vertical lead (AY-10) that was lifted

from relay 16A-K27 was connected with several other relays.

Upon lifting lead AY-10, power was lost to relay 16A-K98

which caused the outboard Group II isolation. All-contain-

n.ent isolation valves closed as designed.

The resident inspector was in the control room when the

isolation occurred. An ENS call was made at 9:55 a.m.

The isolation was reset at 10:50 a.m., when the electricians

completed the replacement of 16A-K27. The inspector reviewed

the licensee's SLER and upset report, and discussed the

event with the STAS and licensed operators. The cause of

the isolation was use of an inadequate blocking permit, in

that panel internal wiring diagrams should have been con-

sulted when writing the permit. These diagrams depict how

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relays are in'erconnected. The licensee intends to submit

an LER, which will be reviewed in a future report. .No

additional deficiencies were identified and the inspector

had no further questions at this time.

4.2.4 011 Spills

At 2:15 a.m. on June 22, 1987, an oil spill from the

temporary diesel driven air compressor occurred on site.

The oil (approximately 25 gallons) flowed into the storm

sewer and was contained by inner and outer oil booms in

the discharge pond. The licensee had the oil cleaned up

and repaired the air compressor.

Subsequently, at 10:57 a.m. on July 1, 1987, the

licensee discovered that approximately 30 to 50 gallons

of oil had spilled into the Susquehanna River from a

different storm sewer. An additional 30 to 50 gallons

of oil were contained by an oil boom. Low river level '

in combination with the boom lodging on a rock allowed the

oil to flow into the rivet. the licensee determined that

the spill was #6 fuel oil. The spill was terminated'and a

contractor consultant, Underwater Technology (UT), came on

site and removed the oil from the river. The resident

inspector was notified by the licensee at 12:30 p.m. and an

ENS call was made at 4:15 p.m.

The inspector reviewed licensee actions as required by

procedure SE-6, Pollution Incident Prevention Plan, Rev.

5. SE-6 refers to notifications as required by

Environmental Technical Specifications (ETS). The ETS

were replaced by the Radiological ETS in 1984. Also,

SE-6 states that VIP International is the cleanup

consultant; however, UT is the current consultant for

oil cleanup. The inspector discussed these minor

deficiencies with licensee personnel who also had

identified the minor SE-6 errors. The licensee stated

that procedure SE-6 would be revised. The inspector

will review ~*a revised procedure in a future

inspectinn.

No violations were noted. l

4.2.5 Unit 2 ESF Actuatior. on July 10, 1987

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At 9:05 a.m. on July 10, 1987, the Unit 2 shutdown

cooling system isolated when a fuse blew. A loss of

power to the system II logic resulted in the closure of

MO-17 and 18 valves and tripping of the 2A RHR pump.

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The cause of the blown fuse is under investigation. The l

licensee replaced the fuse, reset the isolations, f

restored shutdown cooling and made a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> ENS call at

10:50 a.m. Unit 2 was in the refueling mode with

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coolant temperature at about 105 F.

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The inspector reviewed the SLER and control room logs,

and discussed the event with licensed operators. The

licensee intends to submit a LER for the event. The

inspector will review the LER in a future inspection.

No violations were noted.

4.2.6 Partial Loss of Off Site Power on July 10, 1987

At 3:28 p.m. on July 10,- 1987, a lightning strike during

a storm caused a partial lass of off site power. The

3435 breaker tripped resulting in a loss of power to the #3

startup source for both units. This resulted in a loss

of the #2 and #3 13 KV non vital auxiliary buses, and a

fast transfer of the Unit 2 E-2Z and E-42, and Unit 3

E-13 and E-33 4KV emergency buses to the #2 startup

emergency source. The fast transfers actuated as

designed and no diesel generator starts occurred. Group

II and III containment isolations occurred on both

units, including a loss of shutdown cooling. Unit 2 was

in the refuel mode with the reactor cavity flooded and

cross-connected to the spent fuel and equipment pools.

Coolant temperature was approximately 105 F. Unit 3 was

in the shutdown mode with coolant temperature at about

150 F. The licensee transferred loads to the #2 startup

source per proceaure S.8.3.D.3 and restored shutdown

cooling at 4:12 p.m. on Unit 2 and at 4:40 p.m. on Unit

3. The licensee made a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> ENS call at 5:15 p.m. for

the ESF actuation. The #3 startup source was restored

and the licensee normalized the electrical lineup at

6:55 p.m.

The senior resident inspector was in the control room

prior to and during the event observing licensee

actions. The inspector verified that actions were in

accordance with procedure S.8.3.D.3, " Unscheduled

Tripping of #3 Off Site Power Source, Rev. 7, 10/24/86.

Licensee management reported to the control room within

minutes of the event. The inspector noted that the

control room shif t supervisors (engineers) took command

and controlled the recovery actions.

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The inspector observed the restoration of shutdown

cooling on both units in accordance with S.3.2.C.I. No

unacceptable conditions were noted. Overall response by

the licensee was effective.

4.2.7 Unit 2 Reactor Mode Switch Positioning July 11, 1987

At 5:30 p.m. on July 11, 1987, the licensee made a 4

hour ENS call reporting an event that occurred at 1:05

p.m. The event was the repositioning of the reactor

mode switch from the shutdown to the refuel position

wi th all IRM detector cables disconnected. At 1:19 p.m.

the reactor mode switch was returned to the shutdown

position. The licensee initially determined that this

was reportable as a 30 day LER. However, after further

review the licensee determined that it was reportable under

the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> requirement of 50.72.B.2.111.

The inspector reviewed control room logs and Technical

Specification (TS) 3.1/4.1 and its associated basis. I

The i spector alse discussed the event with licensed

opera;. ors and licensee management. TS 3.1.A, Table

3.1.1 (note 7) requires the IRM high flux scram function

to be operable when the reactor mode switch is in the

refuel position. All control rods were already fully

inserted, and the CRD system was previously blocked by

shift permit #3-87-567. This block prevents any control

rod movement. Thus, the inspector determined that the

licensee had adhered to TS 3.1.A, Table 3.1.1 (note 1)

actions which requires all rods to be inserted within

four hours if a RPS trip function is unavailable. In

additicn, t'. ~: t;J a fcc t!,e refvel moot RPS trip

functions is that it ensures that shifting to the refuel

mode while at power does not diminish the protection

provided by the RPS.

The inspector concluded that repositioning the reactor

mode switch was acceptable for existing plant conditions.

4.3 Logs and Records

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The inspector reviewed logs and records for accuracy,

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completeness, abnormal conditions, significant operating changes

and trends, required entries, operating and night order propriety,

correct equipment and lock-out status, jumper log validity,

conformance with Limiting Conditions for Operations, and proper

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reporting. The following logs and records were reviewed: Nuclear

Operations Monitoring Team Log, Shift Supervision Log, Reactor ) '

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Engineering' Logs, Unit 2 Reactor Operator's Log, Unit 3 Reactor (

Operator's Log, Control Operator Log Book and STA Log Book, Night '

Orders, Radiation Work Permits, Locked Valve Log, Maintenance

Request Forms, Temporary Circuit Modification Log, and Ignition

Source Control Checklists. Control Room logs were compartJ l

with Administrative Procedure A-7, Shift Operations. Frequent

initialing of entries by licensed operators, shift supervision,

e and licensee on-site management constituted evidence of licensee

review. No unacceptable conditions were identified.

4.4 Refueling Outage Activities

4.4.1 Unit 2 Core Reload

The inspector reviewed Special Procedure (SP)-1021,

" Plant Conditions Necemary to Reload Fuel Unit 2," for

Technical Specification requirevnents associated with

loading fuel into the reactor vessel. SP-1021 was

reviewed in the control room while it was being

implemented and after it had been completed. All steps

had been completed and signed off satisfactorily. All

changes to SP-1021 were handled properly and in

accordance with procedures. The inspector questioned

the operators concerning SP-1021 and found them

knowledgeable of the procedure. The SP was also

discussed with licensee engineers, and the inspector

independently verified that specific steps were

adequately performed. The inspector also reviewed

selected "Shif t Training Bulletins" to verify the

informatier was accurate and complete.

Unit 2 core reload began on June 22, 1987. A review of

the following documentation was performed:

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FH-6C " Fuel Movement and Core Alteration Procedure  !

During a Fuel Handling Outage," Revision 19, March

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FH-6C, Appendix 1, " Core Component Transfer i

Authorization Sheet."

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S-14.1-2, " Operation of the Unit 2 Refueling

Platform Controls and Interlocks," Revision 0, May

8, 1984.

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5-14.2, " Moving Fuel from the Fuel Pool to the

Reactor," Revision 5, May 8, 1984. >

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S-14.3, " Moving Fuel from the Reactor to the Fuel

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S-14.4, " Moving Fuel Within the Reactor," Revision

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ST-12.1-3, " Refueling Interlock Functional Test,"

Revision 1, October 31, 1984.

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ST-3.1.2, "SRM Core Monitoring Test," Revision 9,

Janua ry 11, 1985.

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ST-3.1.3, "SRM Functional and Calibration Check,"

Revision 5, October 29, 1983.

The inspector monitored the following items associated

with core reload through direct observation of fuel

handling and Control Room activities:

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The operability of refueling interlocks

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The operability of source ronge monitoring (SRM)

instrumentation

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Availability of direct communication between the

control room and the refueling bridge

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The presence of a senior licensed operator

supervising fuel handling activities

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The operability of the standbv gas treatment system

and secondary containment

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The radiological precautions for fuel handling

including adherence to the RWP

--

The presence of an HP technician in the fuel floor

area

)

I

--

The precautionary measures for preventing the {

intrusion of foreign objects into the reactor I

cavity )

--

The operation of the refueling bridge and

associated fuel handling equipment

--

Reactor vessel and fuel pool water level and

clarity requirements

j

--

Fuel and component accountability in the spent fuel

pool and in the reactor core

- - _ _ _ _ _ _ _ _ _ _- __

.

-

,

13

--

Reactor mode switch locked in " refueling" position

--

The operability and required full insertion of all

control rods

--

Unit 2 reactor operator cognizance of refueling

activities and direct monitoring of SRM levels and

changes (count rates and period changes).

Fuel loading was completed at 11:53 p.m. on July 1,1987.

The core was verified complete at 10:35 a.m. on July 2,

1987. Overall, coordination and conduct of the refueling

activity was considered to be effective. Within the scope

of this review of fuel loading activities, no unacceptable

conditions were identified.

4.4.2 Unit 2 Stuck Fuel Bundle No. 49-40

The inspector attended the Nuclear Review Board (NRB)

meeting that was held to review the cause of Unit 2

stuck fuel bundle 49-40 which was encountered during the

fuel offload on Unit 2. The meeting was held at PECo

headquarters on June 2, 1987. The fuel bundle problem

was initially reviewed in NRC Inspections 277/86-10 and

277/86-09.

The NRB was briefed by members of the Peach Bottom

technical staff on the findings of their investigation

to determine the cause for fuel bundle 49-40 sticking in

its fuel support piece. The binding was caused by a

piece of foreign material in the coolant flow stream

which impacted on and deformed the fuel assembly lower

tie plate. The foreign material was a sphere approximately

7/8 inches in diameter, brown in color, non-magnetic and

with a dose rate of 15 R/hr at one foot. It was recovered

during the investigation. The fuel bundle remains stuck in .

its fuel support piece in the spent fuel pool. .

The licensee concluded that the spherical object most

probably entered the vessel during the 1984-85 pipe 1

replacement outage. The fuel bundle lower tie plate was I

apparently deformed by repeated impact by the object. The I

object is probably stainless steel with an activity of 7-8 I

curies. )

Future actions to be performed by the licensee include:

1

--

Possible inspection of additional fuel locations I

for foreign objects.

\ . . _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ - _ _ _ _ _ _ _ - _ _ , _ _ _ . _ _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

l : 4- -

i 14

.

--

Attempt to separate the fuel bundle from its fuel'

support piece for additional examination.

--

Incorporate tool handling equipment visual

I inspection for missing parts at completion of each

l job.

l

--

Send object to GE for analysis.

The NRB discussion was probing and thoroughly explored

the safety implications of the problem. The NRB l

concluded that actions taken were adequate to support i

reloading of the Unit 2 core.

The inspector verified that a quorum of NRB members and

alternates was present per Technical Specification 6.5.2

and NRB administrative procedures.

No violations were identified.

,

4.4.3 Motor Operated Valves (MOVs) Testing

In response to IE Bulletin 85-03, the licensee is

performing MOVATS testing on Unit 2 High Pressure Coolant

Injection (HPCI) and Reactor Core Isolation Cooling (RCIC)

MOVs. Testing has determined that four valves do not meet

the engineering calculated motor thrust requirements. The

valves include the following: RCIC minimum flow (13-27),

RCIC Condensate Storage Tank (CST) test return (2.3-30),

RCIC torus suction (13-41), and HPCI inside containment

steam supply (23-15). Based on this information, the

licensee made an ENS call at 5:22 p.m., on June 8, 1987,

and informed the senior resident inspector. The apparent

cause of the low motor thrust is associated with the spring

packs and belleville washers. The licensee is repairing

the defective spring packs and performing retests. In

addition, differential pressure testing is scheduled during

restart.

The inspector reviewed the licensee's test results and

SLER; discussed the testing with licensee engineers,  ;

maintenance and vendor personnel; and monitored test i

implementation with licensee and vendor personnel. The  !

licensee intends to submit an LER for these MOV test

failures. In addition, Unit 3 testing will be performed

as well as possible additional testing for other Unit 2

and 3 MOVs IE Bulletin 85-03 remains open pending the

completion of licensee testing, submittal to the NRC of ,

test results, and NRC reviews.

r

._________-____a

_ _ _ _ _ _ . _ _ - _ - _

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i

1

4.4.4 Unit 2 Standby Liquid Control System (SLCS)

Modifications

The licensee performed modifications (MOD 867) on the

Unit 2 SLCS to meet the requirements of 10 CFR

50.62(c)(4) for anticipated transients without scram

(ATWS) risk reduction. The SLCS must have an equivalent

capacity of 86 gpm injection at 1394 weight natural

sodium pentaborate. In order to achieve this, the

licensee selected an enriched baron solution of

approximately 60?; Boron-10 isotope. Thus a lower SLCS

capacity (flow rate) and a lower concentration may be

acceptable. MOD 867 changed the boron enrichment, and

minimum tank level and temperature requirements for the

SLCS.

Since the MOD required a Technical Specification (TS)

change, prior NRC approval was required. NRR approved

the TS change (Amendment Nos. 122 and 126) on June 2,

1987. The inspector reviewed the following: the MOD

package (including the safety evaluation, PORC approval,

MRFs, and other documentation); the revised system

operating, surveillance test and annunciator procedures;

and TS Amendment Nos. 122 and 126. The inspector also

reviewed the "Shif t Training Bulletin" and interviewed

selected licensed operators with respect to their

knowledge of the SLCS and related modifications. The

operators interviewed demonstrated adequate knowledqe of

the SLCS modifications. The inspector verified tht. the

SLCS was operable prior to Unit 2 core reload by

performing an ESF walkdown (see detail 4.5) and that

SP-1021 procedural signoffs for SLCS operability were

appropriate (see detail 4.4.1).

During the review of ST 7.1.1-2, " Unit 2 Standby Liquid

Control T;nk Baron Solution Analysis," the inspector

noted that the licensee used an average SLCS pump flow

rate rather than the lowest flow rat 9. TS 3.4.3 requires

that multiplication of boron concentr:s'. ion (weight percent),

pump flow rate and boron enrichment m: .t be greater than

1.0. The inspector stated that using an average SLCS pump

flow rate is less conservative than using the lowest value.

The difference for ST 7.1.1-2 performed on June 2, 1987,

was as follows:

--

SLCS pump A - 52.25 gpm

e . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _

- _ _ - - _ - _ _ - - _ _ _ _

-

...

16

9

--

SLCS pump B - 55.55 gpm I

--

Average -

53.90 gpm

--

result using average SLCS flow = 1.32 )

--

result using lowest SLCS flow = 1.28 l

The TS 3.4.3 requirement was met in both cases. After

discussions with licensee personnel, a representative

stated that the procedure (ST 7.1.1-2) would be revised  !

to incorporate using the lowest SLCS pump flow rate.

The inspector will review the revised ST 7.1.1-2 in a

future inspection.

No violations were noted.

4.4.5 Containment Spray Systems  ;

l

On June 10, 1987, during implementation- t a planned

system modification, another boiling water reactor

(BWR/3) discovered the presence of corrosion products in

the primary containment spray headers and nozzles in the

drywell. A significant amount of rust flakes were found

in the header and nozzles such that blockage may have

occurred during system initiation.

1

The purpose of the containment spray system is to scrub

radionuclides and to reduce pressure in primary

containment for structural considerations by condensing

steam in the drywell or torus during accident conditions

by spraying these areas with torus water. In response

to this BWR containment spray deficiency, the inspectors

conducted a review of the containment spray systems at ,

Peach Bottom 2 and 3. As part of this review, the i

documents listed in Attachment 2 were reviewed. The ]

inspectors also had discussions with licensee system, d

technical, performance, and In Service Inspection (ISI)

engineers.

Primary containment spray in the drywell consists of two

independent twelve inch ring headers mounted on the

drywell wall at elevations 161' and 172'. The pipe is

manufactured from carbon steel in accordance with ASTM

specification A106 Grade B. Each ring header has 160

equally spaced brass 1 1/2" Fogjet nozzles (1 1/2-7G40).

The upper header (loop A) nozzles point downward at a 53

l angle from horizontal, and the lower header (loop B)

nozzles point downward at a 28 angle from horizontal.  !

l

l

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -

___-_-.

.

.  !

17

J

.

Primary containment spray in the torus consists of one

four inch ring header suspended from the center of the

torus ceiling at elevation 122'. The header completely

circles the torus and is concentric with the torus, )j

There are sixteen equally spaced (one per torus bay) '

brass 1 1/2" Fulljet nozzles. All of these nozzles point

,. vertically downward. Either RHR loop A or B can supply

l- the torus ring header.

l

The licensee wrote two maintenance request forms (MRFs ',

8704666, 8704668) to inspect the drywell and torus spray

headers in Unit 2. On June 18, 1987, test engineers and

ISI engineers performed a visual (direct and

fiberoptic) examination of the three headers and

several nozzles. The licensee findings were:

--

For the A drywell spray loop, three nozzles were

removed (#88, #122, #159). All three nozzles and

several inches of header pipe on each side of the ,

removed nozzles showed minimum surface rust. The '

same nozzles were removed from the B loop and

indications were similar. 1

--

For the torus spray loop, four nozzles were removed

(#3,#6,#10,#14). Nozzle #3 was clean, the

piping on each side of the nozzle had minimum

surface ast and a piece of glass (3/4") from a

light bulb was found in the pipe. Nozzle #6 had a

slight buildup of loose powder rust that would not

interfere with the nozzle flow path. The piping on

each side of the nozzle had minimum surface rust.

Both nozzle #30 and #14 were clean and minimum

surface rust was seen in the pipe on each side of

the nozzles.

The inspectors reviewed the licensee's inspection and

findings. The licensee stated that they would inspect

the Unit 3 primary containment spray headers by the end

of July. The inspectors will follow up on the Unit 3

inspection in a future report.

In addition to this review, the inspector also looked at

what type of surveillance tests or inspections are

conducted on the primary containment spray system. The

only activity performed on the primary containment spray

system is an air test on the drywell and torus headers

and nozzles once every five years as required by

Technical Specification (TS) 4.5.8.1d. This requirement

is satisfied by the performance of Surveillance Test

(ST) 12.2, " Containment and Torus Sparger Air Test."

. - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ -

_ _ _ _ _ __

.

. -

l

18 j

.

I

The inspector reviewed past performances of ST 12.2 to

determine if any blockages or abnormalities were

encountered. For Unit 3, ST 12.2 was performed in its

entirety on January 1, 1979, and again on August 17,

1983. A partial of ST 12.2'(torus spray sparger) was

performed on October 23, 1985, another partial of ST

12.2 ( A loop of the drywell sparger) was performed on

'

October 27, 1985, and ST 12.2 was entirely complete on

November 20, 1985 when the B loop of the drywell sparger

was air tested. The inspector found no discrepancies with i

the performance of these tests and had no further questions

on the Unit 3 STs. .'

The inspector also ieviewed completed ST 12.2 for Unit

2. The following partial ST 12.2 were performed: July '

19, 1980, partial of torus; July 24, 1980, partial of A

and B loop drywell (ST complete); June 19, 1985, partial

of torus. Thus, ST 12.2 was last completed in its entirety

on July 24, 1980. Therefore, ST 12.2 was required to be

fully completed again by October 24, 1986 (including the

25'J grace period), to fulfill the five year requirement of

an. air test on the drywell and torus headers and nozzles

as' stated in TS 4.5.B.1d. As of July 17,.1967, the partial

A and B loop drywell header air tests had not yet been

performed to entirely complete ST 12.2 by October 24, 1986.

This is an apparent violation of TS 4.5.B.1d (277/87-17-01).

The inspector further investigated the method in which

partially performed surveillance tests ere tracked. See

section 7.3.

i

4.5 Engineered Safeguards Features (ESF) System Walkdown

The inspector performed a detailed walkdown of portions of the

Standby Liquid Control System (SLCS) in order to independently

verify the operability of the Unit 2 and 3 systems. The SLCS

walkdown included verification of the following items:

--

Inspection of system equipment conditions.

--

Confirmation that the system check-off-list (COL) and

operating procedures are consistent with plant drawings.

--

Verification that system valves, breakers, and switches are  !

properly aligned.  !

'

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_ . _ _ _ _ _ _ _ _ _ _ _ _ __

_ - _

__ - - _-

I

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la

19

.

1

l

i

--

Verification that instrumentation is properly valved in and i

operable.

--

Verification that valves required to be locked have {

appropriate locking devices.

--

Verification that control room switches, indications and

controls are satisfactory.

--

Verification that surveillance test procedures properly

implement the Technical Specifications surveillance

requirements.

No violations were identified.

5.0 TMI Action Plan (TAP) Items Review

5.1 TAP Item II.K.3.18.C, Modification of ADS Logic (Closed - Unit 2)

The Unit 2 Automatic Depressurization System (ADS) has been

modified in accordance with TAP Item II.K.3.18 to automatically

initiate in the absence of a high drywell . pressure initiation

signal. The ADS functions as a backup to the High Pressure

Coolant Injection System (HPCI) by depressurizing the reactor

vessel so that low pressure systems may inject water for core

cooling. The ADS was previously actuated upon coincident signals

of reactor vessel low water level, hiah drywell pressure, a low

pressure Emergency Core Cooling System (ECCS) pump running, and a

105 second time delay which allows ADS to be bypassed if the

operator believes the actuation signal is erroneous or if vessel

water level can be restored. However, for transient and accident

events ei ? f: ~ r ~ "u: 'i ? d g.: F:::u e, e 4 r-e fure :r

j

degraded by a loss of HPCI, manual actuation of the ADS would be 4

required to ensure adequate core cooling.

To reduce the dependence for manual actuation to ensure adequate

core cooling, the licensee installed bypass timers which wil'1

automatically by pass the drywell high pressure condition required

for ADS actuation if recctvP vessel water level remains below the

ADS initiatich setpoint (level 1) for a sustained period. After a

set time delay of nine minutes (plus or minus one minute) and the

103 second time delay, ADS will automatically actuate in the

absence of a drywell high pressure signal if a reactor vessel low

water level condition still exists and a low pressure ECCS pump is

running.

Four, nine minute time delays have been added, one for each ADS

drywell high pressure initiation channel. There are two ADS

actuation channels (Division 1 and Division 2), either of which

can perform the required ADS function. There are two bypass .

timers associated with each ADS division. The low reactor water I

. _ _ _ _ _ _ _ _ _

.. .

<

.

..

. 20

level signal is sealed in so that the bypass time (nine minutes)

will not automatically reset upon recovery of low reactor water

level. The 105 second actuation timer will reset if reactor water

level recovers above the trip setpoint (-106") before it times

out.

Another modification made to the Unit 2 ADS consists of the

addition of two ADS manual inhibit switches (one per ADS division)

that permit the operator to override the ADS automatic blowdown

logic if necessary. These manual inhibit switches are located on ~

control room panel C03 near the controls for the safety relief

valves. A key-locked switch is used for the manual inhibit -

function to provide a means of limiting the potential for

inadvertent actuation cf the manual inhibit. Alarms alert the

operator of time-out of the bypass timer and activation of the ==

manual inhibit switches.

'{

The above ADS logic modification was approved by NRR in Technical

Specification (TS) Amendments Nos. 106 and 110, datad March 5, 1985.

The modification was completed on Unit 3 during the 1985-1986

refueling outage and on Unit 2 during the 1987 refueling outage. ,

The inspector reviewed completed modification package No. 633 and

associated documentation including: safety evaluation,

construction job memo, electrical schemat cs (MI-S52), PORC

approval sheets, modification acceptance test results, maintenance

request forms and related checklists. The inspector reviewed TS

Amendment Nos. 106 and 110, BWR Owners Group Evaluation of the ADS ,

Logic Modification; and related NRC/PECo correspondence on the '

subject. The inspector also reviewed the revised plant procedures

which implemented this ADS logic change including surveillance

test procedures, system operating procedures, alarm cards, and

emergency operating (TRIP) procedures. The inspector discussed

the modification with licensee engineers and plant licensed

operators.

I Within the scope of the review of actions taken by the licensee in

response to TAP Item II.K.3.18.C for Unit 2, no unacceptable

conditions were noted. TAP Item II.K.3.18.C is closed for Unit 2.

TAP Item II.K.3.18.C was reviewed and closed for Unit 3 in NRC

Inspection 278/86-07.

6.0 Review of Licensee Event Reports (LERs)

6.1 LER Review

The inspector reviewed LERs submitted to the NRC to verify that

the details were clearly reported, including the accuracy of the ',

description and corrective action adequ;cy. The inspector

.

_ - _ _ _ _ _ . _ . _ _ . . _ - _ _ . - -

- _ _ _ _ _ _ _ _ _ -

c. .

,

21

determined whether further information was required, whether

generic-implications were indicated, and whether the event

.

,

warranted on-site followup. The following LERs were reviewed: j

LER No.

LER Date

Event Date Subject

2-87-06 Primary Containment Isolation System (PCIS) Group II

May 22, 1987 due to RPS "B" Motor Generator (MG) set trip

April 23, 1987

  • 2-87-08 Control Room Ventilation Radiation Monitor

July 1, 1987 Inoperability i

May 29, 1987

  • 2-87-09 PCIS Group III due to loss of power to "B" RPS bus

July 9, 1987

June 2, 1987

  • 3-87-06 PCIS Group III during bus transfer

June 12, 1987

May 14, 1987

6.2 LER On-Site Followu2 i

For LERs selected for en-site followup and review (denoted by

asterisks above), the inspector verified that appropriate

corrective action was taken or responsibility was assigned and

that continued operation of the facility was conducted in

accordance with Technical Specifications and did not constitute an

unreviewed safety question as defined in 10 CFR 50.59. Report

accuracy, compliance with current reporting requirements and

applicability to other site systems and components were also

reviewed.

6.2.1 LER 3-87-06 concerns a PCIS Group III isolation and half

scram that occurred on Unit 3 on May 14, 1987. The

cause of the isolation was a trip of the "B" RPS bus on

overvoltage during diesel generator paralleling

evolutions. The event was reviewed in NRC Inspection

277/87-15 and 278/87-15. The licensee concluded that i

the root cause of event was operator error compounded by

procedural inadequacies. The inspector concurred with

this determination. However, the inspector also

concluded that another contributing factor to the event

was inadequate training as discussed in NRC Inspection

277/87-15 and 278/87-15.

- _ - _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ____ ._ _ _ - _ __ _ _ _ - -

.

,.

22

L i

6.2.2 LER 2-87-09 concerns a PCIS half Group III containment

l ventilation isolation that occurred on Unit 2 on June 2,

1987. The event is discussed in section 4,2.1 of this

r: port. No inadequacies were noted relative to this

LER.

I

6.2.3 Control Room Ventilation Radiation Monitor  !

'

i

l

Background-

The licensee informed the NRC on July 2, 1987, and

reported in.LER #2-87-08 that incorrect piping

configurations existed in the control room ventilation

radiation monitoring (CRVRM) system. The inlet ports of

three of the four solenoid valves had the piping  !

reversed. As a result, the CRVRM system would.not have j

been able to detect abnormal radiation conditions as '

designed. The licensee discovered the incorrect 1

configuration on May 29, 1987, during troubleshooting of  !

low sample system flow. The CRVRM system provides for

control room emergency filter actuation on high

radiation and for control room isolation on high-high

radiation. The solenoid valves provide for switching of

sample points from the normal air supply to the

emergency air supply on a high radiation signal. As a

result of these piping configuration errors, the CRVRM

systen may rot have been able to perform its safety

function during accident conditions and control room

exposures may have exceeded design values.

.

The peach Bottom control room is common to Units 2 and

3. The CRVRM system functions to sample the air

entering the control room under normal operating

conditions to analyze the air for noble gases, iodine,

and particulate. Normal control room ventilation is

swapped over to emergency filtration during high noble

gas radiation conditions, and isolated (both normal and

emergency modes) during high-high noble gas radiation

conditions or equipment failure. The system also l

monitors the air entering the control room via the j

emergency ventilation duct after a high radiation

swapover. The sampling is accomplished via solenoid ] ,

valves SV-0760A thru D. Each solenoid valve has two l

inlet ports (one piped to the normal ventilation duct j

and the other to the emergency duct) and one exhaust '

port. Only one of the two inlet ports is open at any

given time. During normal operation the four solenoids

are de-energized, and, if piped correctly, the normal

ventilation duct is being sampled. Should high radiation

conditions occur in the normal ventilation duct, the four

- _ - ______ ___- _ _ - - . __ - _ _- _ _ _ _ _ _ _ _ _ _ _ _

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, .

23 l

.

solenoids energize, thereby closing the port from the normal l

ventilation duct and opening the port from the emergency duct. '

Licensee Review and Conclusion

With Unit 2 in the refuel mode and Unit 3 in cold

shutdown, on May 29, 1987, at approximately 10:00 a.m.,

the licensee discovered that incorrect piping

configurations ex.isted in the CRVRM system.

Specifically, the sample lines from the normal

ventilation duct and the emergency ventilation duct to

solenoid valve SV-0760B were reversed. Similar

discrepancies existed for SV-0760A and SV-07600. The

sample lines to SV-0760C were piped correctly. The

discovery occurred during investigation of suspected low

flow through the "B" channel of the CRVRM system.

Technical Specification 3.11.A.5 states that "at least l

one of two main control room intake air radiation l

mor.itors shall be operable with the inoperable chanr.el I

failed safe whenever the control room emergency /

ventilation air supply fans and filter trains are

required to be operable by 3.11.A.1 or filtration of the

control room ventilation intake air must be initiated."

As a result of the piping configuration errors, the

licensee determined that the CRVRM system would not have

been able to detect abnormal radiation conditions as

designed. The system has been in this condition for an

undetermined amount of time. Since the channels were

not failed safe during this time period, nor was

filtration+t-of the control room ventilation intake air in

of te '4~~-+ determined that a failure to comply

with the requirements of Technical Specification 3.11.A.5 occurred. The licensee determined that this

was reportable under the requirements of 10 CFR

50.73(a)(2)(1)(B) involving a condition prohibited by

technical specifications.

As reported in the LER,the licensee determined that as a

result of the piping configuration errors, the control

room emergency ventilation system, which is designed to

provide control room habitability during accident

conditions, would not have been able to perform its j

function as designed. '

The licensee performed a preliminary analysis using

methodology consistent with the " Design Review of Plant  !

Shielding" submitted in response to NUREG-0737, Item (

II.B.2.2. The results of this preliminary analysis show

that although the normal ventilation was not being

I

)

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24

.

sampled from the correct duct, automatic swapover of the

control room ventilation system from the normal mode to

the emergency mode would have occurred during accident

conditions consistent with those assumed in the

NUREG-0737 submittal, but the swapover would have been

delayed by 72 minutes. This delay translates to a less

than 1% increase in control room operator exposures (180

day total integrated dose) for the postulated accident

duration and these exposures would have been maintained

at a small fraction (less than 10%) of the GDC-19 dose

limits of 30 rem thyroid, 5 rem whole body, and 30 rem

skin. The swapover would have been delayed because,

prior to entering the control room, the ductwork

branches off to a portion of the emergency duct. It was

from this portion of the emergency duct that the

misaligned radiation monitoring system was obtaining its

samples rather than from the normal ventilation duct.

Therefore, the system ductwork configuration would have

allowed contaminated air to reach the ventilation

radiation monitors (although delayed) thereby effecting

an automatic swapover to emergency filtration.

In addition, the licensee determined that the

consequences of the piping configuration errors would be

minimized due to (1) a Continuous Air Monitoring (CAM)

device which is installed in the control room as a

backup to the ventilation radiation monitoring system,

and (2) the actions specified in the station emergency

procedure for control room air supply high radiation

which require immediate radiation and air surveys in the

control room and at the control room ventilation intake.

In the event of contaminated air in the control room the

CAM would have alerted the control rocm operators who

would then have responded to the abnormal radiation

condition in accordance with the emergency procedure,

including manual swapover or isolation of the control

room if necessary.

The licensee determined that the root cause of the event

was unknown. Plant engineering staff conducted an

investigation to determine the cause. Maintenance

Request Forms and Plant Modifications documentation were

reviewed in an effort to pinpoint the cause of the

discrepancy. It is believed that the condition has

existed since initial installation of the system (prior

to 1974 commercial operation). Upon discovery of the i

sampling point discrepancies, the licensee realigned the )

sample lines to SV-0760 A, B and D to the correct con- l

figuration.

l

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, . . .

l 25

1

). Additionally, the licensee checked all other ventilation

l radiation monitoring systems for proper piping

configurations. No discrepancies were found. Also, the

'

. licensee stated that a study would be initiated of other

safety systems that depend on sensing process parameters

,

to gain confidence that this deficiency an isolated

1

event. Many process parameters have be- properly

sensed in the past because they have ini..ated Reactor

Protection System actuations, Emergency Core Cooling

System actuations and Primary Containment Isolation

System actuations. The licensee plans to examine those

portions of safety systems that sense process parameters

that have never initiated an emergency safeguard feature  !

and determine if the surveillance tests on that portion

of the system would uncover any installation errors, or

even subsequent process line blockages. If any portiotis

of safety systen are identified as having the potential

to have installation deficiencies or subsequent line

blockages the licensee will develop plans to ensure these

portions can function properly. The results of this study

will be reported in a revision to the LER.

NRC Review and Conclusion

The inspector reviewed the LER #2-87-08, and related

documentation (Attachment 3) and discussed it with

licensee engineers and operators. The inspector

verified that the CRVRM system is safety related as

stated in the FSAR, 0-List, and Technical Specifications 3.11.A/4.11.A and their Bases.

A walkdown of the CRVRM system was conducted by the

inspector with the licensee system engineer on July 9,

1987. During the walkdown the inspector questioned the

engineer with regard to the system operation, trouble-

shooting and repair activities. The engineer stated that

the incorrect piping configuration was discovered during

troubleshooting of apparent low sample flow conditions in

the "B" channel of the CRVRM system. The condition had

apparently been determined by cleaner than nor. mal filter

changes and a small difference in two sataple pump (A and B)

vacuum gauges. The licensee disconnected the sample lines

and performed flow tests with nitrogen. Based on these

tests, the licensee concluded that three of four lines were

piped incorrectly. The inspector confirmed this by dis-

cussions with the licensee system engineer.

___-___ ___________________- _______ _ _ _ -

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26

.

l

The inspector reviewed construction and preoperational

test records for the control room ventilation system and

for the CRVRM system. These records indicate that the

L system was turned over in October 1973. The startup

test for the CRVRM system (#73-4) was performed in May

1973; however, valves SV-760A,B,C&D were not' proper Q

material. This test exception was approved. The valves

were replaced, field inspected, and accepted in September

1973 (reference MRF #2-73-1167). The inspector concluded

that the cause of the incorrect piping configuration was

inadequate construction installation and QC verification of

the CRVRM system.

The inspector reviewed CRVRM system TS 3.11.A. TS 3.11.A.5 requires at least one of the two radiation

monitors to be operable with the failed channel in a

tripped condition. This is required when the CRVRM

system is required to be operable per TS 3.11. A.1 (e.g. ,

either unit is required to have secondary containment).

If TS 3.11.A.5 cannot be met, the filtration of the

control room air intake is required to be initiated with

the emergency filter and fan. Thus, the licensee has

been in apparent violation of 15 3.11.A.5 for both units

since the date of the Operating License, e.g., October

25, 1973 (Unit 2) and July 2, 1974 (Unit 3). (277/87-17-02).

The control room emergency ventilation system is designed

such that the control room is habitable under accident

conditions. The CRVRM system provides system actuation on

high radiation and system isolation on high high radiation.

Thus, a safety related system may not have been able to

perform its functi;n as designed.

The inspector reviewed the licensee's control room

continuous air monitoring (CAM) system and procedure j

E-7, " Control Room Air Supply High Radiation, Rev. 5. 1

The CAM system provides for radiation monitoring (beta f

and alpha) of the control room air. The CAM system is j

not required by Technical Specifict.tions, however the J'

licensee maintains the CAM in service. The inspector

reviewed the CAM system operation, testing, and

maintenance. In addition, the inspector questioned

control room operators and technicians with regard to

CAM operation, testing and use during implementation of

E-7 (actual high radiation in the control room). The

inspector determined that operators and technicians were

knowledgeable of the CAM system in the control room.

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The licensee analyzed the ability of the control room

emergency ventilation to swapover even though the piping

configuration was in error. The inspector reviewed this

preliminary analysis as stated in the LER. The review

of the final analysis will be performed in a future

inspection.

The inspector reviewed surveillance testing (ST) for the

CRVRM system. TS 4.11.A.4 requires operability testing

of the CRVRM system every three months. ST 9.8 tests

the CRVRM system by performing a functional test on the

initiation and control logic. The inspector discussed

ST 9.8 with licensee engineering and test personnel.

The licensee stated that a new procedure (ST 4.7.3) is

being written to calibrate the CRVRM detectors

(RIS-0760A and B). The licensee had identified a

deficiency with respect to their ST program apparently

caused by the fact that TS 4.11.A doesn't directly

require a calibration test for the CRVRM system. The

inspector will review this ST procedure in a future

inspection.

The CRVRM system high and high-high trip setpoints could

not be verified by the preoperational and startup test

data nor instrument data sheets. The inspector

questioned the licensee with respect to these setpoints.

A licensee representative stated that engineering is

determining the correct setpoints. The current high

trip setpoint is 400 CPM for each detector; however, the

high-high setpoint could not be determined. ST 9.8

records these setpoints which are 400 CPM for high le el

and a dial setting for hign-high level. The inspector

reviewed standard TS (STS) for the CRVRM system.

STS specify requirements for CRVRM system alarm / trip

setpoints and surveillance requirements for channel

calibration. These CRVRM trip setpoints and calibration

requirements are unresolved pending licensee

determination and subsequent NRC review. (UNR

277/87-17-03)

Summary

As a result of apparent inadequate construction, QC, and

preoperational test verifications; the CRVRM system has

been incorrectly configured since Unit 2 and 3 startup

(1973,1974). Thus, the plant has been in apparent

violation of TS 3.11.A.5 and a safety system may not have

been able to perform as designed. The licensee identified

this non-conforming condition during system troubleshooting.

Otherwise, this condition may have gone undetected for a

_ _ - _ - _ _ _ _ _ _ _ _ -

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1

L longer period of time. A review of similar systems has not

, determined any other deficiencies. Mitigating factors for

! the inoperability of the CRVRM system include a functional

control room CAM and emergency procedure E-7. In addition,

the licensee has preliminarily determined that the incorrect 1

i

CRVRM system configuration would have allowed a delayed

swapover to the emergency ventilation system.

7.0 Surveillance Testing

The inspector reviewed surveillance tests (STs) to verify that testing

had been properly scheduled, approved by shift supervision, control

room operators were knowledgeable regarding testing in progress,

approved procedures were being used, redundant systems or components

were available for service as required, test instrumentation was

calibrated, work was performed by qualified personnel, and test

acceptance criteria were met.

7.1 Surveillance Tests Reviewed  :

The inspector reviewed the following corrpleted STs:

--' ST 7.1.1-2, " Unit 2 Standby Liquid Control Tank Boron ,

Solutinn Analysis," Rev. O, 4/29/87, performed on Unit 2 on

'6/1/87.

--

ST 13 8-2, " Unit 2 Standby Liquid Control Injection Test,"

Rev. 0, 5/18/87, performed on Unit 2 on 6/2/87.

--

ST 6.1.2, " Standby Liquid Control Pump Functional Test for

ISI," Rev. 2, 12/19/86 performed on Unit 2 on 2/4/87.

--

ST 12.2, " Containment and Torus Sparger Air Test," various

revisions, performed on Unit 2 on 1/1/79, 8/17/83, 10/23/85,

10/27/85 and on Unit 3 on 6/19/80, 6/24/80, 6/19/85, and

11/20/85.

With the exception of ST 7.1.1-2 (see detail 4.4.4) and ST 12.2

(see detail 4.4.5 and 7.3), no unacceptable conditions were

identified.

7.2 Partial Surveillance Tests

Ir. Combined Inspection Report 50-277/85-29; 50-278/85-33, a violation

was issued concerning a failure to test three Unit 3 relief valves

after the other eight valves were tested under partial surveillance

tests. The violation was noted by the inspector in October 1985.

The licensee's response to the violation stated that the cause of

the remaining missed partial surveillance test was a failure to

l

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29

follow administrative procedure A-3, " Procedure for Temporary

Changes to Approved Procedures." After a review of corrective t

action, this violation was closed in Combined Inspection Report

50-277/86-19; 50-278/86-20.

Based on a similar apparent violation detailed in this inspection

report (detail 4.4.5), the inspector reviewed the method in which gg

the licensee tracks partial surveillar:e tests. For the review,

the inspector had discussions with the performance engineer,

system engineer and surveillance test coordinator, and reviewed

administrative procedures A-3, " Procedure for Temporary Changes to

Approved Procedures," Rev. 8 and A-43, " Surveillance Testing System,"

Rev. 18.

The inspector determined that the licensee's computer software

program for surveillance tests (STARS) cannot completely

differentiate between partially completed STs and completed STs.

A partially completed ST can be entered into STARS, but it will

not appear on the " Grace Period Surveillance Test Report" or

" Overdue Test Report." Once the partial ST is reviewed and is

removed from the " Tests Awaiting Official Verification Report,"

the ST will not reappear until its next surveillance period.

Therefore, required portions of the ST may not be completed unless

the cognizant supervising engineer manually tracks the partial ST

until it is totally complete.

The performance engineer stated that plans for obtainir.g an

updated STARS program that could track partial STs was being

discussed. The resident inspector will foliow this item as part

of the apparent violation in detail 4.4.5.

8.0 Maintenance

For the following maintenance activities the inspector spot-checked

administrative controls, reviewed documentation, and observed portions

of the actual maintenance: l

Maintenance

Procedure /

Document Eouipment Date Observed

S.4.2.J Control Rod Operation Functional June 2, 1987

Test

MRF MS7-4771 2C HPSW Pump June 22, 1987

_ _ _ _ _ _ _ .

_ - _

4 -

l .- 30 )

1

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,

Administrative controls checked included maintenance request forms

(MRFs), blocking permits, fire watches and ignition source controls,

item, handling reports, QC involvement, plant conditions, TS LCOs,

equipment turnover information, and post maintenance testing.

Documents reviewed included maintenance procedures, material

certifications, RWPs,.MRFs, and receipt inspections.

_

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l

No inadequacies were identified.

1

9.0 M diation Protection

l

CQring the report period, the inspector examined work in progress in

hoth units, including health physics (HP) procedures and controls, ,

dosimetry and badging, protective clothing use, adherence to radiation

work permit (RWP) requirements, radiation surveys, radiation protection

instruments use, and handling of potentially contaminated equipment and

materials.

The inspector observed individuals frisking in accordance with HP

procedures. A sampling of high radiation doors was verified to be

i locked as required. Compliance with RWP requirements was verified

during each tour. RWP line entries were reviewed to verify that

personnel had provided the required information and 'pecple working in

RWP areas were observed to be meeting the applicable requirements. No

unacceptable conditions were identified.

10.0 Phy_sical Security

10.1 Routine Observations

The inspector monitored security activities for compliance with

the accepted Security Plan and associated implementing procedures,

including: operations of the CAS cnd SAS, checks of vehicles

on-site to verify proper control, observation of protected area

access control and badging procedures on each shift, inspection of

physical barriers, checks on control of vital area access and

, escort procedures. No inadequacies were id.entified.

10.2 Watchman Asleep on June 21, 1987

The Plant Manager found a security watchman asleep at the Unit 2

drywell access at about 4:00 p.m., on June 21, 1987. The watchman

s

was escorted off site by the sergeant of the guards, and the

watchman subsequently quit. No work was in progress in the

drywell and an HP control point was not established. The licensee

informed the senior resident inspector of this occurrence at 7:00

a.m., on June 22, 1987. The licensee investigated the incident

and the NRC reviewed 1^. in Inspection 277/87-20; 278/87-20.

<

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10.3 Drug Allegation (RI-87-A-0070)

!

On June 18, 1987, the inspector received a call from an anonymous

source alleging that a contractor worker was a habitual drug user.

The inspector notified the licensee of this information. The

licensee's security organization and the contractor's management

performed an investigation. The licensee informed the inspector

that the individual admitted drug use in the past.

The contractor worker's employer requested that he submit to a drug

test; he refused and his employment was. going to be terminated.

,

However, the employee was advised by a lawyer to take the drug test.

l' A drug test was administered on June 29, 1987, and the results were

'

negative.

The individual does not currently have access to the peach Bottom

l protected area. Readmittance to the protected area will be

l determined pending f urther licensee investigation. Tne inspectors

L will follow this issue.

1

10.4 Controlled Substance Found During Search

At 1:09 p.m. on July 8,1987, a contractor employee was found to

be carrying a controlled substance in a cigarette pack while

trying to enter the orotected area. During the required routine

search, a security guard noticed a piece of tape covering the

opening of the cigarette pack. Upon examination, a small bag of

white powder was discovered.

The contractor employee is a janitor employed by International

Systems Services (ISS) and has been working at peach Bottom since

October 1985. He stated that the substance was methamphetamine

and he has never brought in .or used drugs in the protected area.

However, he did admit to storing drugs in his car on licensee

property. The individual had access only to administrative

..< buildings within the protected area and did not have vital area ]

,

. access.

The contractor worker's employment was terminated by ISS, his

security badge was pulled and he was escorted off site. The

substance was sent to the state lab for analysis. The Nuclear

Employee Data System (NEDS) and the Pennsylvania State Police in

York were notified.

The inspectors had no further questions.

11.0 In-Office Review of public and Special Reports

The inspector reviewed the following:

--

Monthly Operating Report for May 1987, dated June 15, 1987.

  • _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -

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Special Report for,the Motor Driven Fire Pump Out-of-Service,

dated June'5, 1987.

h

i

No unacceptable conditions were noted. \

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< 12.'0 Unresolved Items

]

, Unresolved items are items about which more information is required to

- ascertain whether they are acceptable violations or deviations. Two

unresolved items'are discussed in section 6.2.3.

13.0 Management Meetings '

. 13.1 Preliminary Igyection Findings

A verbal summary of preliminary findings was provided to the

'

Manager, Peach Bottom Stacion at the conclusion of the inspection.

During the inspection, licensee management was periodically

notified verbally of the preliminary findings by the resident

.irrpectors. No written inspection material was provided to the )

' licensee during the inspection. No pr0 pietary information is

,

1.1cluded in this report.

)3.2AttendanceatManagementMeetingsConductedbyRegionBased

Inspectors

Inspection Reporting

S Date \ Subject Report No. Inspector

6/15-19/87 IE Bulletin 87-16/16 Varela

80-11 (Masonry

i

':1 .)

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,.

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6/15-17/87 EQ 87-18/18 Paolino

4  ;

6/1-5/p?x Containment 87-19'19 Chung

Integrity

,6/28-7/2/87 Security 87-20/20 Bailey

7/13-17/87 Radiological 87-21/21 Oragoun'

Controls

13.3NRCRecionI/100 Management Meeting on June 17, 1987

\

g;'i On June 17, 1987, a management meeting was held at Peach Bottom

Station. At this meeting, PECo discussed the status of actions in

response to the NRC Order c'ated March 31, 1987. The licensee

o.fiscussed the status of the MAC investigation and their security

investigation; updated the status of the NOMT; discussed future

l

.o.

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plans for training, shift organization, and procedures update;

ana, discussed the PECo " Commitment to Excellent Program". A list

of meeting attendees is included in Attachment 1. The inspector

will continue to follow this area. l

l

13.4 NRC/Harford County, Maryland Meetina on June 23, 1987 I

On June 23, 1987, NRC representatives attended the Harford County i

(MD) Council Meeting in Bel Air, MD. The meeting purpose was to l

brief the Council regarding the status of the Shutdown Order,

investigations, and followup. The inspector attended the meeting.

13.5 NRC/PECo Meeting at Bethesda, Maryland on July 15, 1987

On July 15, 1987, a ranagement meeting was held at NRC

headquarters in Bethesda, MD. At this meeting, PECo discussed the

status of their actions in response to the NRC Order, including

their recovery plan (" Commitment to Excellence"). The inspector  !

attended the meeting. A meeting summary will be provided by NRR.

The inspector will continue to follow this area.

1

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ATTACHMENT 1

PECo/NRC Meeting i

June 17, 1987

NRC Attendees

T. P. Johnson, SRI, PBAPS

R. M. Gallo, Branch Chief Project Branch 2, Region I

W. F. Kane, Director, Division of Reactor Projects, Region I

W. V. Johnston, Acting Director, Division of Reactor Safety, Region I

J. C. Linville, Section Chief, PB2, DRP, Region I

R. E. Martin, NRC Pr oject Manager, USNRC/NRR

R. J. Urban, Resident Inspector, PBAPS

B. Clayton, Regional Coordinator, NRC

S. F. Shankman, Region I Operator Licensing

M. T. Miller, State Liaison Officer Region I

J. H. Williams, Project Engineer, Region I

D. S. Morisseau, Training and Assessment Specialist, NRR

State of Maryland Attendees

W. Bonta, Engineer, State Department of Health

P. Perzynski, Staff, State Department of Health

T. Magette, Administrator, Nuclear Evaluations, MD Power Plant Research

Program

State of Pennsylvania Attendees

W. Dornsife, Chief, Division of Nuclear Safety, PA Department of

Environmental Resources

S. Maingi, Nuclear Engineer, PA Department of Environmental Resources

PECo Attendees

G. F. Daebeler, Assistant to Plant Manager for Commitment to Excellence

Program

E. P. Fogarty, Project Manager, Commitment to Excellence Program

Dr. W. F. Hushion, Medical Director ,

G. M. Leitch, Manager, Nuclear Generation Department

E. J. Bradley, Associate General Counsel

J. W.. Gallagher, Vice President, Nuclear Operations

D. M. Smith, Manager, Peach Bottom Atomic Pcwer Station

A. B. Donell, Nuclear Operations QA Division, Site Supervisor

C. J. McDermott, Manager, Public Information

R. H. Logue, Assistant to Manager, Nuclear Support Department

J. W. Jones, Assistant Manager, Public Information

P. E. Webster, Senior Public Information Representative

P. J. Duca,. Procedures Coordinator

t. - - . - . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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Others

H. R. Abendroth, Senior Engineer, Atlantic Electric l

M. A. Phillips, Senior Engineer, Public Service Electric & Gas

C. D. Schaefer, Electrical Operations, Delmarva Power .

, C. W. Thayer, Management Analysis Company $

! J. R. Coughlin, Lead Scheduler

W. L. Fauth, Consultant

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ATTACHMENT 2

Documents Reviewed for Containment Spray System

1. Peach Bottom Atomic Power Station, Units 2 & 3, Updated Final Safety

Analysis Report

2. Peach Bottom Atomic Power Station, Units 2 & 3, Technical

Specifications

3. Surveillance Test ST 12.2, " Containment and Torus Spray Sparger Air

Test", Rev. 3, 5/28/85

4. Administrative Procedure A-3, " Procedure for Temporary Changes To

Approved Procedures," Rev. 8, 10/20/86

5. Bechtel Design Drawings 6280-C2-362 " Field Assembly for Drywell Spray

Headers", and 6280-C2-321, " Suppression Chamber Internal Spray Header

Assembly"

6. Vendor Technical Manuals for Fulljet Spray Nozzles (6280-C2-85-1) and

Fogjet Nozzles (6280-C2-84-1)

7. Field Inspection Report #1087-2439, "RHR Drywell and Torus Containment

Spray Header", June 18, 1987

8. P&ID M-361, " Residual Heat Removal System"

_ _ _ _ _ _ _

,.

. .

ATTACHMENT 3

Control Room Ventilation Radiation Monitoring System Documentation Reviewed

--

UFSAR' sections 10.13 and 7.12.5

!

--

Peach Bottom Q-List section 17.0, Rev. 22

--

TS 3.11.A/4.11.A and Bases

--

E-7, Control Room Air Supply High Radiation, Rev. 5, 7/1/80

--

ST-9.8, Control Room Emergency Ventilation and Radiation Monitor

Functional Test, Revision 11, 10/28/85

--

RT 7.6.2, Periodic Operational Check and Inspection of CAMS, Rev. O,

11/8/82

--

RT 7.6.1, Periodic Calibration and Maintenance of CAMS, Rev. 2, 6/29/87

--

RT 7.6.3, Periodic Filter Change and Check of CAMS, Rev. 1, 4/15/87

--

Alarm Cards 00C214 #2 and #3 (Control Room Vent Supply Rad A, B)

--

P&ID M-393, Control Room Ventilation Flow Diagram, Revision 10, 2/26/85

--

E-255. Rev. 17, ESD Control Room Annunciators

--

P&ID M-384, Control Room Temperature Control Diagram, Revision 19,

6/16/80

--

LFE Instruction Book #6280-M236-37-1, Vent Rad Monitoring System

--

P&ID M-328, Cooling & Heating Piping Systems, Revision 14, 11/30/76

--

Spec M-236, Radiation Monitoring Systems

--

P&ID M-334, Ventilation Radiation Monitoring System, Revision 15,

10/31/83

--

QAD M-834, Ventilation Radiation Monitoring System, Revision 4

--

S.12.6.2.A, Normal Operation of the Control Room Ventilation, Revision

1, 03/19/87

--

S.12.6.2.A, COL, Control Room Radiation Monitor Sample Station Check

List, Revision 0, 08/30/82

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S.12.6.2.B, Setup of Contral Room Emergency Vent System for Automatic

Operation, Revision 2, 05/18/87

--

S.12.6.2.C, Control Room Purge Air System, Revision 0, 01/18/73

1

--

S.12.6.2.0, Routine Inspection of Control Room Ventilation System,

l Revision 2, 05/18/87

--

S.12.6.1.A, Aligning the Control Room Chilled Water System Valving in

Preparation for Control Room Chi'ler Startup, Revision 0, 11/16/72

--

S.12.6.1A, COL, Control Room Chilled Water Startup, Revision 3,

06/18/b0

--

S.12.6.1.B, Starting Up the Control Room Chilled Water System Normal

Cveration, Revision 0, 11/16/72

--

S.12.6.1.0, Loss of the Control Room Chiller Units and/or the Control

Room Chilled Water Pumps, Revision 1, 06/24/80

--

S.12.6.1.E, Chemical Addition to the Control Room Chilled Water System,

Revision 1, 06/17/80  !

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S.12.6.1.F, Routine Inspection - Control Room Chiller Operating,

Revision 0, 10/29/80 i'

--

E-1674, ESD Ventilation Radiation Monitoring System, Revision 5

--

Peach Bottom Startup Tests No. 73-4 and 74 and Construction Turnover

Information for Control Room Radiation and Ventilation Systems (1973)

--

MRFs 2-73-1167, 2-63-M-86-8740, 2-63M-87-4198

f

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