ML20155D457

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Insp Repts 50-277/98-08 & 50-278/98-08 on 980811-0921. Violations Noted.Major Areas Inspected:Operations, Surveillances & Maintenance,Engineering & Technical Support & Plant Support Areas
ML20155D457
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 10/28/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20155D387 List:
References
50-277-98-08, 50-277-98-8, 50-278-98-08, 50-278-98-8, NUDOCS 9811030223
Download: ML20155D457 (40)


See also: IR 05000277/1998008

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  • ' U.'S, NUCLEAR REGULATORY COMMISSION

REGION I

License Nos. DPR-44

DPR-56

Report Nos. 98-08

98-08

Docket Nos. 50-277

50-278

. Licensee: PECO Energy Company

Correspondence Control Desk .

P.O. Box 195

Wayne, PA 19087-0195

Facility: Peach Bottom Atomic Power Station Units 2 and 3

Inspection Period: August 11,1998 through September 21,1998

Inspectors: A. McMurtray, Senior Resident inspector

M. Buckley, Resident inspector

B. Welling, Resident Inspector

B. Maier, Senior Reactor Engineer

S. Dennis, Operations Engineer

R. Nimitz, Senior Radiation Specialist

J. Carrasco, Reactor Engineer

L. Peluso, Radiation Specialist

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Approved by: Clifford J. Anderson, Chief

Projects Branch 4

Division of Reactor Projects

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9811030223 981028

PDR i

O ADOCK 05000277 '

PDR

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EXECUTIVE SUMMARY

Peach Bottom Atomic Power Station

NRC Inspection Report 50-277/98-08,50-278/98-08

This inspection report included aspects of licensee operations; surveillances and

rnaintenance; engineering and technical support; and plant support areas.

Operations:

> * The operators in the control room demonstrated very good communication

practices in their extensive use of three part communications. The operators

also demonstrated very good questioning attitudes in their pursuit of the scope of

a breaker problem and their review of procedures.

Peer checking and self checking were usually employed effectively. One error '

was noted in which the improper unit's procedure was initially used to substitute

computer variables for heat balance calculations but later corrected. Logs I

generally were kept accurately, but an erroneous plant status entry went

undetected through a shift turnover, indicating a cursory review of that entry.

(Section 01.1)

inspection due to poor system configuration control. These events resulted in an

entry into emergency operating procedures due to a steam leak on the non-

regenerative heat exchanger and an automatic engineered safety feature (ESF)

isolation. The causes were less than adequate turnovers between senior reactor

operators and non-licensed operators, incomplete post-maintenance testing

instructions, and an inadequate RWCU startup procedure.

Station personnel failed to properly maintain the RWCU startup procedure, l

resulting in a violation of Technical Specification 5.4.1, " Procedures." Although

station personnel had previously developed some initiatives to reduce plant

configuration control problems, they had not made sufficient progress

implementing them to preclude these events. (Section 02.1)

  • Operators did not verify that a torus-to-drywell vacuum breaker was closed

within 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> of the discovery of an unreliable indication, as required by

technical specifications. This event was caused by the failure to adhere to

equipment operator rounds and log review practices by operations personnel.

This non-repetitive, licensee-identified, and corrected violation is being treated as

a Non-Cited Violation, consistent with Section Vll.B.1 of the NRC Enforcement

Policy. (Section 02.2)

  • On August 22,1998, during performance of the Unit 3 turbine building rounds

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an equipment operator inadvertently shutdown the 3C drywell chiller. Since the

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Executive Summary (cont'd)

chiller was quickly restarted, the temperature and pressure increases in the

drywell were small and posed a small safety risk to the plant. l

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An engineering evaluation for a similar event that occurred on March 25,1997,

was not effective to preclude the August 22,1998 event. (Section O2.3) I

a On August 21,1998, unit 3 operators commenced a down power maneuver due

, to loss of cooling to the main transformer. The reduced load prevented a loss of

the main transformer and plant transient when the deluge system activated.

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The initial response by the operators for the loss of cooling to the mam

transformer and subsequent deluge activation was good. Due to the power I

reduction, the flow in the recirculation system loops became mismatched in l

excess of the Technical Specification limit. This cc,ndition was identified and

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corrected within the time allowable by Technical Specifications. Failure of ,

operations personnel to fully understand the effect of xenon on recirculation flow l

and closely monitor recirculation flow contributed to this involuntary entry into a  !

Technical Specification Action and Limiting Condition for Operation. (Section 1

04.1)

  • The Senior Reactor Operator Limited to Fuel Handling (LSRO) program was good

overall. The LSRO program guidelines and examinations were comprehensive

and well maintained by the program coordinator and LSRO license maintenance

was well documented. The areas of exam security, remediation, operator

feedback, and medical records were acceptable. (Section 05.1)  ;

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Maintenance: i

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e Control room deficiencies were controlled and adequately prioritized so that  !

critical Main Control room deficiencies were corrected in a timely manner.

However, some weaknesses, of minor safety significance, were noted with the {

clarity and implementation of the requirements in OM P-10.3, Revision 3, j

" Equipment Status List / Tagging of Deficiencies." (Section M2.1) j

e Weaknesses in maintenance planning and work practices led to a significant

water leak on the station fire main on August 23,1998. Water from the leak

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entered the safety related emergency service water /high pressure service water l

pump house via underground electrical conduits and degraded penetration seals.

The engineering evaluation, that the penetration sealleakage was within design

assumptions for a design basis flooding event, and pump operability was not

affected, was adequate. (Section M4.1)

Enaineerina:

e Construction activities on the east retaining wall of the independent spent fuel

storage installation were acceptable. Engineering personnel resolved

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Executive Summary (cont'd)

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construction deficiencies regarding as-built keyways and soil compaction in an

- effective manner, thus the ana / zed as-found condition of the east wall was

acceptable. The concrete mix delivery, testing, and pouring activities for the

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east retalning wall were acceptable. (Section E1.1)

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o Engineering personnel took prompt and effective corrective actions following

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their identification of the potential to bypass the pressure suppression function ,

of the torus during simultaneous purging of the torus and drywell as a result _

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of postulated failures, in accordance with the NRC Enforcement Policy,

Section Vll.B.3, Violations involving Old Design issues, the NRC is exercising

enforcement discretion and not citing this violation. (Section E2.1) ,

Plant Sucoort: 1

o PECO implemented, an effective radioactive waste processing, handling, storage,

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and radioactive material transportation program. Wastes were properly classified '

and packaged. (Section R1.1)

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, e Overall, radioactive waste and material processing and storage areas were

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! properly posted and controlled, and exhibited very good material condition. I

(Section R2)

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e Individuals responsible for radioactive waste processing activities exhibited a j

good knowledge level of reculatory requirements'and program procedures.

(Section R4)

.e- PECO provided generally good training of personnelinvolved in radioactive waste

activities. However, one individual had not received the a-priori specified training

for mechanics involved with radioactive weste activities and there was no

defined training program for new radwaste personnel brought into the radwaste

group and involved in radwaste shipping activities. PECO took action on these

matters. (Section R5)

e PECO implemented an appropriately staffed and defined organization for

radioactive waste processing, handling storage, and shipping. -(Section R6)

e PECO performed audits of appropriate depth and scope of radwaste processing,

handling, storage, and transportation activities, including training and

qualification of personnel. Corrective actions were initiated for identified

concerns. (Section R7) i

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e PECO provided generally good radiological controls oversight of incoming fuel

shipments. However, a violation of radiation protection procedures associated  !

. with source checking of an alpha contamination counting instrument was

identified by the NRC and was promptly corrected by PECO. (Section R8.3) l

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TABLE OF CONTENTS

EX EC UTIV E S U M M A RY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

TA BL E O F CO N T ENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v

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Summary of Plant Status ............................................1

1. Operations .....................................................1

01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.1 Sustained Control Room Observation . . . . . . . . . . . . . . . . . . . . . 1

02 Operational Status of Facilities and Equipment ................... 3

O2.1 Reactor Water Cleanup System Configuration Control Events

(Unit 3) and (Closed) LER 50-278/3-98-004 . . . . . . . . ....... 3

02.2 Torus /Drywell Vacuum Breaker Loss of Seated Indication (Unit 2) . 6 '

02.3 Inadvertent Shutdown of the 3C Drywell Chiller ............. 7

03- Operations Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . 9

03.1 Review of Normal Plant Startup Procedure . . . . . . . . . . . . . . . . . 9  !

03.2 Unexpected Start of the Motor Driven Fire Pump During Testing . . 9

04 Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . 10

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04.1 Operator Perforrnance During Loss of Cooling to the 3C Main

Transformer .....................................10

05 Operator Training and Qualification ..........................12

05.1 Limited Senior Reactor Operator (LSRO) Requalification Program . 12

11. M a in t e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

M1 Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . , 14

M1.1 General Observations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

M2 Maintenance and Material Condition of Facilities and Equipment . . . . . . 14

M2.1 Main Control Room Deficiencies .......................14

M3 Maintenance Procedures and Documentation ...................15

M3.1 Fix It Now Team Planning and Documentation . . . . . . . . . . . . . . 15

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M4 - Maintenance Staff Knowledge and Performance . . . . . . . . . . . . . . . . . 16

M4.1 Fire M ain Le a k . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16 '

111. E ng i n e e ri ng . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

,- El Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

E1.1 Installation of the ISFSI East Retaining Wall ............... 17

E2 Engineering Support of Facilities and Equipment .......... ...... 19

E2.1 (Closed) URI 50-277(278)/97-06-03and (Closed) LER 2-97-007

Potential for Bypass of Pressure Suppression Pool . . . . . . . . . . . 19

E2.2 Access and Alarm Failures to Protected Area and Vital Areas

Doors Due to Security Multiplexer Failure . . . . . . . . . . . . . . . . . 20

y E2.3 Core Spray, Residual Heat Removal and High Pressure Service Water

Motor Operated Valve Thermal Overload Wire Discrepancies . . . 21

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Table of Contents (cont'd)

IV. Plant Support ................................................23

R1 Radiation Protection and Chemistry Controls (RP&C) . . . . . . . . . . . . . . 23

R1.1 Radioactive Waste Processing, Handling, Storage, and Shipping . 23

R2 Status of RP&C Facilities and Equipment ......................24

R3 RP&C Procedures and Documentation ........................25

R4 Staff Knowledge and Performance in RP&C ....................25

R5 Staff Training and Qualification in RP&C . . . . . . . . . . . . . . . . . . . . . . 26

R6 RP&C Organization and Administration . . . . . . . . . . . . . . . . . . . . . . . . 27

R7 Quality Assurance in RP&C Activities . . . . . . . . . . . . . . . . . . . . . . . . . 27

R8 Miscellaneous RP&C /sctivities .............................28

R8.1 (Closed) Violation (VIO) 50-277(278)/97-03-02 Failure to Assure

that the Turbine Building Atmosphere was Processed Through the

Turbine Building Gaseous Waste Treatment System . . . . . . . . . . 28 ,

R8.2 (Closed) VIO 50-277(278)/97-04-03 Violation of Locked High

Radiation Area Key Control . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

R8.3 Inspection of incoming Fuel Shipments . . . . . . . . . . . . . . . . . . . 28

R8.4 Security Oversight of Radwaste Activities ................ 30

V. Management Meetings ..........................................30

X1 Exit Meeting Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

X2 Review of Updated Final Safety Analysis Report (UFSAR) Commitments . 31

ATTACHMENTS

Attachment 1 - List of Acronyms Used

< - Inspection Procedures Used

-Items Opened, Closed, and Discussed

Attachment 2 - Maintenance Observations

- Surveillance Observations

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Report Details

Summary of Plant Status

PECO operated both units safely over the period of this report.

Unit 2 began this inspection period at 73% power, in end-of-cycle coastdown. Unit 2

power was at 60% at the end of the inspection period.

Unit 3 began this inspection period at 100% power. On August 14, unit load was reduced

to 84% due to a loss of service water to a main generator hydrogen cooler. Unit load was

reduced to 67% on August 21 due to degraded cooling of the 3C main transformer. Unit

power remained at 100% for the rest of the period.

1. Operations

01 Conduct of Operations

01.1 Sustained Control Room Observation

a. Insoection Scope (71715)

The inspectors conducted augmented observations of control room and other in-

plant activities from September 7 through September 11,1998. Some of the

activities the inspectors observed included:

  • Investigation documentation of a problem associated with racking out a

4 kilovolt diesel output breaker

e Biocide injection in service water systems

  • Pre-evolution brief of 3B recirculation pump scoop tube lockup and clamping

for motor refurbishment

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  • Several position turnovers and beginning of shift briefings _
  • Generation of troubleshooting, repair and test procedures for control room  !

indication circuit j

  • Performance of special test procedure for hydrogen injection l

' Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized reactor inspection report

outline. Individual reports are not expected to address all outline topics.

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b. Observations and Findinas

The operators conducted their activities in acccedance with the operations manual

procedures. They used three part communications routinely in their exchange of

information. Annunciator response was prompt, and alarm response procedures

were consulted for any annunciator alarms not anticipated. Anticipated alarms were

announced to the crew by the cognizant operator.  !

Peer checking was used where called for by the operations manual. Peer checking

was used for the diesel generator surveillance run and the recirculation pump scoop

tube lockup. Operators applying blocking tags on components performed self

checking to ensure that the correct components were tagged. The control room ,

supervisors showed appropriate oversight of infrequent tasks and test procedures, i

One exception to the otherwise excellent quality verification of control room j

activities was in the use of the wrong unit's routine test procedure for inserting a i

substitute value for recirculation loop flow rate in the plant computer heat balance I

equation. The inspector noted that a Unit 2 procedure initially was used on Unit 3 I

because it was printed on white paper, the color used for common unit procedures.

The operators quickly located the correct procedure prior to the actual performance

of the task referenced in the procedure, and the shift manager counseled the control

room team on the need to verify procedural accuracy when performing tasks. l

Control room logs were kept current. Technical specification action logs were

accurate. Entries were made in this log for potential as well as actual technical

specification action entries dealing with equipment unava'. lability. Two minor

exceptions were the insertion of erroneous unit status data into the unified

computer log at two shift turnovers. The inspectors noted these discrepancies, and

also noted that the first log error had not been noted by the control room team in

the log review conducted at the most recent shift turnover.

The operations teams, as led by the shift managers and their supervisory staffs, all

showed an excellent questioning attitude to abnormalindications and occurrences.

When a loose cable cover damaged a terminal strip during a breaker change out, the

operations team investigated several similar breakers for the same condition. One

control room supervisor noted a step in a surveillance procedure that was not

signed off even though there was no requirement that he conduct such a complete

review. He initiated action to correct the omission.

c. Conclusions

The operators in the contrni room demonstrated very good communication practices

in their extensive use of three part communications. The operators also

demonstrated very good questioning attitudes in their pursuit of the scope of a

breaker problem and their review of procedures.

Peer checking and self checking were usually employed effectively. One error was

noted in which the improper unit's procedure was initially used to substitute

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computer variables for heat balance calculations but later corrected. Logs generally

were kept accurately, but an erroneous plant status entry went undetected through

a shift turnover, indicating a cursory review of that entry.

02 Operational Status of Facilities and Equipment

O2.1 ' Reactor Water Cleanuo System Confiouration Control Events (Unit 3) and (Closedl

LER 50-278/3-98-004

a. Insoection Scooe (71707)

The inspectors reviewed two reactor water cleanup (RWCU) system configuration l

control events that resulted in an unplanned entry into emergency operating

procedures and an automatic engineered safety feature (ESP) isolation.

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b. Observations and Findinas

Non-Recenerative Heat Exchanaer Vent Valves left Op_en

On August 19,1998, while restoring the RWCU system to service following

maintenance, operators received a reactor building area temperature alarm in the 'B'

RWCU non-regenerative heat exchanger room. As required by procedure, operators  ;

promptly entered emergency operating procedures for secondary containment '

control. An equipment operator responding to the alarm heard a steam leak from I

the 'B' non-regenerative heat exchanger room. The sound diminished when the

RWCU inboard and outboard isolction valves were shut.

Operators entered the 'B' non-regenerative heat exchanger room and found the heat

exchanger vent valves partially open, inctead of closed, as required. Upon further  !

investigation, operations personnel identified that these valves were left out of

position due to poor configuration control of the system while preparing for

maintenance activities. 4

Operations personnel investigated this issue and determined that there were two

primary causes for these valves left out of position while preparing for maintenance

activities:

  • Shift turnover information regarding the RWCU system was less than

adequate. The turnovers between senior reactor operators and between non-

licensed equipment operators did not address the detailed status of the

system.

  • Shift supervision made incorrect assumptions with regard to the affected

trains when continuing with a RWCU system procedure. -.

The poor turnovers occurred during the performance of a cooldown and

depressurization procedure, which prepared the system for mahtenance. When

preparing the system for maintenance on August 16,1998, the operations shift

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partially opened the vent valves for both the 'A' and 'B' non-regenerative heat

exchangers based on the work control supervisor's interpretation of the intent l

of the depressurization and cooldown procedure. The relieving operations shift

crew continued with the procedure to prepare the system for maintenance. The

relieving crew believed, based on a precaution step in the depressurization and

cooldown procedure, that only the 'A' non-regenerative heat exchanger vent valves

had been opened in earlier steps. As a result, when the cooldown and

depressurization procedure directed the vent valves to be closed, the operators or:/ .

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closed the 'A' non-regenerative heat exchanger vent valves and did not close the l

, 'B' non-regenerative heat exchanger vent valves. The 'B' non-regenerative heat

exchanger vent valves remained partially cpen, when they should have been closed,

until the valves were found leaking steam, while returning the system to service, on  :

August 19,1998. The system restoration procedure, SO 12.1.A 3, Revision 19, 1

"RWCU System Startup for Normal Operation or Reactor Vessel Level Control," did

not contain instructions to verify that the non-regenerative heat exchanger vent

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valves were closed during system restoration. '

The review by the inspectors of this event revealed the following.

The work control supervisors stated that their turnover was cursory with  !

respect to the RWCU system configuration. They indicated that they relied ,

on the equipnient operators using the depressurization and cooldown l

procedure to conduct a detailed turnover.

  • The equipment operators' turnover effectively communicated the steps of the

depressurization and cooldown procedure that were completed. However, ,

the tumover did not address the train (s) of the system that were affected by I

these steps. l

  • The depressurization and cooldown procedure was infrequently performed.

One work control supervisor stated that this was the first time that he had

used the procedure.

  • The system restoration procedure did not identify the mispositioned valves

before the event occurred.

The inspectors determined that this event was an important operations performance

issue. . This system configuration control event occurred despite ongoing operations

focus and initiatives on configuration control and system restoration. This event

was similar to others discussed in NRC Inspection Reports 50-277(278)/98-01,

98 02, and 98-06,in which shift supervision made improper assumptions regarding

system configuration or operation.

.Joadeouate RWCU Restoration Followina Post-Maintenance Testina

On August 20,1998, an automatic isolation of the RWCU system occurred due to a

high flow condition. Operators were in the process of returning the system to

service and wers opening the inlet valve to the 'B' RWCU demineralizer when an

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inrush of water into the 'B' demineralizer was heard. Following the isolation,

operators took appropriate actions to verify the isolation was complete and to check

the integrity of the system. Since this was an automatic engineered safety feature

(ESF) actuation, operations supervision made a four hour notification to the NRC per

10 CFR 50.72.

The cause of the event was an incorrect system lineup following post-maintenance

testing, causing the 'B' demineralizer not to be properly filled and pressurized. After

investigation, operations personnel found that the 'B' demineralizer inlet valve had

been shut for post-maintenance testing and was not returned to the open position.

They noted that a maintenance operator had shut both the demineralizer inlet and

outlet valves in order to satisfy an interlock and perform post-maintenance testing

(PMT) on solenoid valve SV-3-36B-030B,'B' demineralizer plenum vent valve. The

inlet valve should have been opened following PMT to provide the appropriate

configuration for restoration of the system.

The inspectors noNd that the PMT instructions in the work order did not address

positioning of the demineralizer inlet and outlet valves. Also, the documentation of

the completed PMT did not discuss any operation of the inlet and outlet valves.

The inspectors reviewed the procedure used for restoration of the RWCU system,

SO 12.1.A-3. The procedure stated that use of the RWCU system check-off list

was optional, "as directed by shift management." In this instance, shift

management determined that completion or partial completion of a check-off list

was not necessary. The inspectors also noted that none of the steps in this

procedure verified that the 'B' demineralizer inlet valve was in the proper position j

for system restoration. The inspectors concluded that SO 12.1.A 3 did not provide  ;

adequate instructions for verification of the 'B' domineralizer inlet valve position.  !

Operations adequately addressed short-term corrective actions for this issue.

The inspectors noted that SO 12.1.A-3 was revised following this event, on

September 12,1998, to include verification of the demineralizer inlet valve

positions. The inspectors performed an in-plant review of Licensee Event Report

(LER) 50-278/3-98-004,and identified no additional concerns,

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NRC Inspection Reports 50-277(278)/98-01,98-02 and 98-06 discussed a number ,

of instances of plant status / configuration control problems, some of which were the '

result of improper system restoration after maintenance or PMT. Violations for

plant status / configuration control problems were cited in NRC Inspection Reports

50-277(278)/98-01 and 98-06. As corrective actions for these issues, operations i

personnel developed the following initiatives:

  • improve configuration control within a clearance boundary
  • add system and equipment restoration details in work packages
  • implement plant impact plans i

Peach Bottom Atomic Power Station Technical Specification (TS) 5.4.1 requires that )

written procedures be established, implemented, and maintained covering the l

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activities in Regulatory Guide 1.33, Appendix A, which includes procedures for

reactor cleanup system startup. The inspectors determined, based on both of these

events, '. hat PECO failed to fully maintain SO 12.1.A-3 with regard to verification of

j' system configuration prior to startup. (VIO 50-278/98-08-01)

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l- The inspectors determined that this violation was repetitive since the corrective

actions for the previous violation cited in NRC Inspection Report 50-277(278)/98-01

j included making enhancements to station procedures. These enhancements were

j to preclude improper system restoration after maintenance and PMT. Also, the

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expectation was communicated to all station personnel of the importance of

notifying the control room of any system configuration changes made during the

, performance of maintenance and/or testing. Station personnel had not made

sufficient progress implementing these initiatives in order to preclude these events.

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c. Conclusions

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I Two Unit 3 reactor water cleanup (RWCU) system events occurred during this

i inspection due to poor system configuration control. These events resulted in an

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entry into emergency operating procedures due to a steam leak on the non-

i regenerative heat exchanger and an automatic engineered safety feature (ESF)

l isolation. The causes were less than adequate turnovers between senior reactor

operators and non-licensed operators, incomplete post-maintenance testing

i instructions, and an inadequate RWCU startup procedure.

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i Station personnel failed to properly maintain the RWCU startup procedure, resulting

! in a violation of Technical Specification 5.4.1, " Procedures." Although station

i personnel had previously developed some initiatives to reduce plant configuration

i control problems, they had not made sufficient progress implementing them to

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preclude these events.

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02.2 Torus /Drvwell Vacuum Breaker Loss of Seated Indication (Unit 2)

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a. Inspection Scope (71707)

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The inspectors reviewed operator rounds and logkeeping performance issues that

!- led to a technical specification violation associated with a torus /drywell vacuum  ;

breaker,

i

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b. Observations and Findinas

On August 24,1998, operators recorded on electronic rounds data that

torus /drywell vacuum breaker, AO-2-078-2504C,had lost its " seated" indication.

, On August 30,1998, operations personnel determined that the actions to verify

'

that the vacuum breakers were closed had not been performed, as required by

.

technical specifications.

1

Peach Bottom Atomic Power Station Technical Specification 3.6.1.6 bases specify ,
that if a torus /drywell vacuum breaker position indication is not reliable, then an l

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alternate method of ver'ifying that the vacuum breakers are closed shall be

performed within 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />. -This is necessary to ensure that a vacuum breaker is

not open, which would create the potential for overpressurization of the torus

during a loss of coolant accident. Operators failed to complete the required actions,

resulting in a violation of Technical Specification 3.6.1.6. This non-repetitive,

, licensee-identified and corrected violation is being treated as a Non-Cited Violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policy. (NCV 50-277/98-

08-02)

This event resulted, in part, from deficiencies in operations personnel

implementation of the rounds and log review processes:

  • Operators did not always enter comments on their logs for out-of-

coecification readings, contrary to operations rounds guidance.

i

Operators did not always notify supervision of unsatisfactory readings or

conditions.

  • Some electronic rounds data was not reviewed by shift management in a

timely manner as specified by operations guidance.

Operators also failed to recognize the potential safety impact of the loss of seated

indication for the vacuum breaker.

The inspectors reviewed completed corrective actions, which consisted of promptly

verifying the vacuum breaker position, revising the daily rounds data procedures,

>

and conducting briefings by operations management. Planned corrective actions

included an evaluation of equipment operator training on round sheet parameters,

inspection of the torus /drywell vacuum breaker, and revisions to electronic rounds

format. The inspectors determined that these completed and planned corrective

actions were adequate.

,

c. Conclusions

Operators did not verify that a torus-to-drywell vacuum breaker was closed within

10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> of the discovery of an unreliable indication, as required by technical

specifications. This event was caused by the failure to adhere to equipment

operator rounds and log review practices by operations personnel. This non-

repetitive, licensee-identified, and corrected violation is being treated as a Non-Cited

Violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy.

02.3 Inadvertent Shutdown of the 3C Drvwell Chiller

a. Insoection Scooe (71707 & 37551)

Inspectors reviewed the impact of an inadvertent shutdown of a Unit 3 drywell

chiller during reactor plant operation.

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b. Observations and Findinas I

!

.On August 22,1998, during performance of the Unit 3 turbine building rounds an l

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equipment operator inadvertently shutdown the 3C drywell chiller. The control

room operators received the "Drywell Chiller Trouble Alarm" annunciator and took

actions in accordance with the alarm response card. The equipment operator l

ir. formed the control room operators as to the cause of the shutdown. Since the )

cause was known, no troubleshooting had to be completed before chiller restart.

Fourteen minutes after shutdown, the 3C drywell chiller was restarted by the

equipment operator. During the drywell chiller shutdown the drywell bulk average

temperature increased about 2 F and drywell pressure increase .05 psi.

The inadvertent shutdown of the 3C chiller on August 22 was documented in PEP

10008858. Part of the corrective action for this PEP included an engineering change  ;

request (ECR) to evaluate the inadvertent shutdowns. This ECR resulted in an j

action request to fabricate and install a plastic guard to cover the ' Auto' and 'Stop' '

buttons on both Unit 2 and 3 chillers.

A similar event on the Unit 2 drywell chiller occurred on March 25,1997, resulting

in a temperature and pressure rise of the Unit 2 drywell. Operations personnel

initiated Performance Enhancement Program document (PEP) 10006793 to

l

investigate the apparent cause of this event. According to this PEP, the human j

factoring of the microprocessor control panel could set-up any individual to i

inadvertently shutdown a drywell chiller. Although the original corrective action for I

this issue recommended providing a barrier on the control panel, engineering

personnel decided that a physical barrier was not needed. Engineering personnel

based this decision on this being an isolated event, and concluded that additional

training of equipment operators would prevent this event from recurring.

'

The inspectors concluded that the engineering evaluation of the March 25,1997

inadvertent shutdown of a drywell chiller, was not effective since a similar event

occurred on August 22,1998.

c. Conclusions

On August 22,1998,during performance of the Unit 3 turbine building rounds an

equipment operator inadvertently shutdown the 3C drywell chiller. Since the chiller

, was quickly restarted, the temperature and pressure increases in the drywell were

small and posed a small safety risk to the plant.

An engineering evaluation for a similar event that occurred on March 25,1997, was

not effective to preclude the August 22,1998 event.

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03 Operations Procedurea and Documentation

1

03.1 Review of Normal Plant Startuo Procedure i

a. Insoection Scoce (71707) l

1

The inspectors reviewed procedure GP-2, " Normal Plant Startup," Revision 88, ,

following a reactor scram event at another nuclear power station during a startup l

evolution, when operators continuously withdrew a control rod after reaching

criticality and before reaching the point of adding heat.

b. Observations and Findinas

Peach Bottom procedure GP-2, " Normal Plant Startup," contained written guidance

4

for control rod withdrawal modes following criticality. The inspectors noted that

one of the procedural steps specifically allowed single notch or notch override

(continuous withdrawal) following criticality and prior to the point of adding heat.

However, a caution statement contradicted this step by stating that only notch

mode was allowed until " nuclear heat begins to increase reactor water

temperature."

'

The inspectors discussed this discrepancy with operators and learned that, in

practice, operators used only single notch mode, consistent with the caution l

statement. Operations personnel considered the procedural step to be inconsistent

with operating practices and promptly revised GP-2.

c. Conclusions

The GP-2, " Normal Plant Startup," procedure and operating practices provided

>

adequate assurance that continuous rod withdrawal following criticality and prior to

the point of adding heat would not occur at Peach Bottom. However, inspectors

identified inconsistencies in the procedure, and operations personnel determined i

that a revision was necessary to ensure the procedure reflected operating practices.

03.2 Unexoected Start of the Motor Driven Fire Pumo Durina Testina

a. Insoection Scoce (71707)

'

The inspectors reviewed documentation for the maintenance on the H-1 fire hydrant

and discussed with operations personnel the circumstances that resulted in the

unc- acted starr of the motor driven fire pump,

b. Observations and Findinas

On August 23,1998, the motor driven fire pump unexpectedly started during post-

maintenance testing of the H-1 fire hydrant. During this testing, the fire system

pressure dropped low enough to cause an automatic start of the pump when the

hydrant isolation valve was opened. The inspectors determined that the fire system

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had not been fully filled and vented and that the system pressure dropped as the  !

system filled when the hydrant isolation valve was opened. The inspectors noted l

that there was no Action Request or PEP written for this issue.

The inspectors reviewed the work order activity report and the routine test, (RT)-O-

37B-382-2," Fire Hydrant inspection and Flush (Miscellaneous)" and discussed this

issue with operations personnel. The inspectors noted that neither the work order

or the RT had instructions to fill and vent the system before starting the post-

maintenance testing or any precautions that the motor driven fire pump could start

during the opening of the hydrant isolation valve. In NRC Inspection Report 50-

277(278)/97-08,the inspectors noted a similar event when an unexpected

automatic start of the motor driven fire pump occurred during clearance restoration

of the fire system.

c. Conclusions

On August 23,1998, the motor driven fire pump unexpectedly started during post-

maintenance testing of the H-1 fire hydrant. Neither the work order or the routine

test procedure contained any documentation to inform operators that the motor

driven fire pump could start during the hydrant post maintenance testing nor did

these documents contain instructions to fill and vent the fire system after work was

performed.

Several unexpected equipment status changes, some involving safety related

components, have been documented in NRC inspection reports during the past year.

Even though this issue involved an unexpected change in the status of the motor

driven fire pump, it was not documented in any of the licensee's corrective action

systems so that it could be tracked and trended.

04 Operator Knowledge and Performance

04.1 Operator Performance Durina loss of Coolino to the 3C Main Transformer

a. Insoection Scooe: (71707)

The inspectors observed and reviewed equipment and control rocm operators

actions for the 3C Main Transformer loss of cooling occurrence.

b. Observations and Findinas

On August 21,1998, with Unit 3 operating at 100%, the control room received the

"3 TRANS TROUBLE" Alarm. The #6 oil pump had failed due to a burnt wire and

when the operator, following the alarm response card, switched the local control to

manual, all of the cooling fans and oil pumps tripped off.

The unit 3 operators commenced a down power maneuver due to loss of cooling to

the main transformer to reduce the heat load on and potentialloss of the main

transformer.

. _ _ __ . __ . _ _ _ _ _ _ . .

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Electricians repaired the burnt wire for the #6 oil pump and checked the other main

transformers for similar problems. While bringing the cooling system back into

service, the operators started each cooling fan and oil pump at periodic intervals.

Although operations personnel were aware that a high temperature rise could

actuate the transformer fire protection deluge system, the operators did not fully

ac. count for the temperature rise wh7n the #5 fan and oil pump were started. This

resulted in the deluge system immediately detecting a high temperature rise and

actuating as designed. The operators quickly isolated the system.

Operations personnel told the inspectors that a plant transient could have occurred,

if the deluge system had sprayed on the transformer with the unit at full power, due

to transformer oil temperature and pressure changes. With generator output

significantly reduced, the deluge activation did not cause a transformer transient

and the unit remained on line. The inspectors determined that actuation of the

deluge system was not expected. Although the deluge system could have been

bypassed to prevent activation, there was no guidance in the procedure for

restoring the cooling system for the main transformer, to deactivate or bypass the

deluge system while bringing the cooling system back to operation.

During the down power maneuver, the operators created a speed mismatch of 50

RPM between the recirculation pumps which resulted in a loop flow mismatch that

was recorded in the reactor operator's log as within the Technical Specification (TS) '

requirements. During a subsequent panel walkdown by the shift supervisors, the i

loop flow mismatch had increased to greater than TS limits. A one hour Technical

Specification Action (TSA) was entered, the 'B' recirculation pump speed was i

lowered so that loop flow mismatch was reduced, and the TSA was exited within '

27 minutes,

iI

The inspectors independently determined that the operators allowed a loop flow

mismatch during the down power maneuver based on reviews of operator logs and

recirculation flow data. The inspectors noted that the effect of xenon following the  ;

downpower caused recirculation loop flows to change which resulted in the

'

increase in loop flow mismatch. The inspectors determined, based on discussions

with shift management that, although the operators thoroughly understood the

effects of xenon on power they did exhibit a lack of full understanding of the

effects of xenon on recirculation loop flow. Therefore the operators did not control

recirculation flow before the effect of xenon increased loop flow mismatch outside

the LCO range. By more closely monitoring the recirculation loop flow, the

operators could have prevented an involuntary entry into a Technical Specification

Action and Limiting Condition for Operation.

c. Conclusion

On August 21,1998, unit 3 operators commenced a down power maneuver due to

loss of cooling to the main transformer. The reduced load prevented a loss of the

main transformer and plant transient when the deluge system activated.

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The initial response by the operators for the loss of cooling to the main transformer

and subsequent deluge activation was good. Due to the power reduction, the flow  ;

in the recirculation system loops became mismatched in excess of the Technical

'

Specification limit. This condition was identified and corrected within the time

allowable by Technical Specifications. Failure of operations personnel to fully

understand the effect of xenon on recirculation flow and closely monitor

recirculation flow contributed to this involuntary entry into a Technical Specification

' Action and Limiting Condition for Operation.

05 Operator Training and Qualification

05.1 Limited Senior Reactor Operator (LSRO) Reaualification Proaram

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a. 1Dsoection Scope (71001)

.

The inspectors evaluated the dual site, Limerick / Peach Bottom, PECON LSRO

requalification training program to verify its compliance with 10 CFR 55. NRC

Inspection Procedure 71001, Licensed Operator Requalification Program Evaluation,  !

and NUREG-1021 Interim Rev.8 - ES-702 were used for the evaluation.

The inspectors evaluated the following program areas:

  • Program guIdel;nes -
  • Operating and written examinations  ?
  • Exam security

i

  • Management oversight -license activation and maintenance of records,

remediation, training, attendance, feedback system, and medical records

i

. PECON procedures and documents associated with the LSRO training program and

. its implementation were also reviewed. ,

The observation of the annual operating exam was not performed during this

inspection and will be performed during the LSRO training cycle in 1999. i

b. Observations and Findinas

' Proaram Guidelines '

The inspectors reviewed PECON procedures LSRO-9500,"LSRO Course Plan," and i

LSRO-OOOO, " Multi -Site Fuel Handling Director," and determined they acceptably i

- described a program which met 10 CFR 55 requirements and previous written  !

l

commitments by PECON to the NRC. Additionally, the inspector reviewed the LSRO

. program subject index and selected LSRO classroom and practical job performance  ;

lesson plans and found that their content was comprehensive and well maintained i

by the program coordinator.

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Qpjeratina and Written Examinations

The inspectors reviewed three written biennial examinations and two annual

operating exams and determined thes/ 9cceptably sampled the items specified in 10

CFR 55. The inspectors also found f. hat the exams adequately assessed knowledge

level in the area of abnormal and emergency procedures. Additionally, it was noted

that a large percontage of the questions in the exams were of the more challenging,

higher order, analytical type.

The inspectors reviewed job performance measures (JPMs) and found that they met

the qualitative guidelines of the inspection procedure and the PECON program. The

JPMs reviewed included those for normal, emergency, and abnormal conditions,

Exam Security

The inspectors reviewed the security measures taken by the facility for exam

development and administration, and determined that programmatic controls were

satisfactory, with no indications of exam compromise.

Activation and Maintenance of Operator Licenses 1

The inspectors reviewed the programmatic controls that PECON used for

maintaining an active license and for reactivating a license while meeting the

requirements of 10 CFR 55.53 and found them to be Greptable. The inspectors ,

reviewed various training attendance records, includng niissed training make-up

sessions or exams, and determined that controls for rnain:enance and reactivation

of operator licenses were good.

Remedial Trainina Proaram

The inspectors reviewed remediation records for two individuals who had failed the

biennial written exams. The inspectors found that the remediation packages l

developed by the training coordinator were appropriate for the weaknesses

{

demonstrated and were properly documented in accordance with PECON i

procedures.

Operator Feedback  :

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The inspectors reviewed the feedback records for the past three years and found  ;

that management review and disposition was timely.

Medical Records i

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The inspectors also reviewed all LSRO medical files to ensure that medical exams  !

were being conducted biennially in accordance with 10 CFR 55.21 and determined  !

that requirements were met.

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c. Conclusion

The inspectora concluded that the Senior Reactor Operator 1.imited to Fuel Handling

(LSRO) program was good overall. The LSRO program guidelines and examinations

were comprehensive and well maintained by the prograra coordinator and LSRO

license maintenance was well documented. The inspectors also determined that the

areas of exam security, remediation, operator feedback, and medical records were

acceptable.

11. Maintenance

M1 Conduct of Maintenance

M 1.1 General Observations

NRC Inspection Procedures 62707 and 61726 were used in the inspection of plant

maintenance and surveillance activities. The inspectors observed and reviewed i

selected portions of the maintenance and surveillance test activities listed in '

Attachment 2.

The work and testing performed during these activities was professional and

,

thorough. Technicians were experienced and knowledgeable of their assigned

tasks. The work and testing procedures were present at the job site and actively

used by the technicians and operators for activities observed. Good pre-job briefs

were observed prior to the performance of the surveillances observed. Applicable

procedures were present in the control room and at the job sites during surveillance

testing and were appropriately used.

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 -Main Control Room Deficiencies

a. Insoection Scoce (61726 & 62707)

The inspectors reviewed the Equipment Status list, action requests designated as

Main Control Room (MCR) deficiencies, and the non-outage maintenance backlog to

assess the effectiveness of the licensee's corrective maintenance of MCR

deficiencies that impact the operators ability to maintain reliable and safe plant

operation.

b. Observations and Findinas

Main control room deficiencies (MCRDs) were identified and tracked by Action

Requests (ARs). The ARs dealing with MCRDs were noted as either control room

deficiencies or critical control room deficiencies. The inspectors noted that

currently there were 56 control room deficiencies listed on outstanding ARs.

Several of these deficiencies were corrected but the ARs remained open to provide

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15

for equipment monitoring. When critical control room deficiencies were identified

during this inspection, they were corrected in an expedited manner.

An equipment deficiency log and control rod drive (CRD) deficiency log were kept

by control room personnel to identify control room deficiencies. These logs made

up the equipment status list. The equipment status list was updated biweekly. The

operators reviewed and maintained both logs to track the status of control room

significant deficiencies.

The inspectors reviewed the equipment deficiency log. During this review, the

inspectors noted that the oldest outstanding significant MCRD was over a year old

on unit 2 and over six months old for unit 3 and that five and 13 significant MCRDs

were open for units 2 and 3, respectively. However, the inspectors determined that

all items on the significant MCRD log had minor safety impact and were scheduled

for work.

The inspectors noted that some of the requirements in OM-P-10.3, Revision 3,

" Equipment Status List / Tagging of Deficiencies" were vague. During tours of the

main control room, the inspectors observed that each MCRD had an equipment

deficiency tag, but that some tags were inconsistent with OM-P-10.3 or other work

control procedures. The inspectors determined that these inconsistencies were of

minor safety significance,

c. Conclusions

Control room deficiencies were controlled and adequately prioritized so that critical

Main Control room deficiencies were corrected in a timely manner. However, some

weaknesses, of minor safety significance, were noted with the clarity and

implementation of the requirements in OM-P-10.3, Revision 3, " Equipment Status

List / Tagging of Deficiencies."

M3 Maintenance Procedures and Documentation

M3.1 Fix It Now Team Plannina and Documentation

a. insoaction Scope (62707)

The inspectors reviewed approximately 15 completed work orders performed by the

Fix l.t Now (FIN) team.

b. Observations and Findinos

The FIN team work order documentation was usually consistent with FIN

. . administrative procedures. The documentation appropriately reflected such items as

work scope, parts, procedures / prints, and post-maintenance testing requirements.

In one instance, incomplete corrective maintenance documentation led to repetitive

problems on temporary emergency cooling tower replenishment pumps. These

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problems reduced the number of pumps available, but did not affect the operability

of the replenishment capability.

c. Conclusions . 1

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Most Fix-It-Now (FIN) team work order documentation was consistent with FIN

administrative procedures, however; incomplete documentation led to repetitive ,

problems on temporary emergency cooling tower replenishment pumps. I

M4 Maintenance Staff Knowledge and Performance

M4.1 Fire Main Leak 1

a. Insoection Scope (37551. 62707 & 71707) l

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The inspectors reviewed an event in which a pipe coupling separated on the station

fire main during maintenance on a fire hydrant. Water from the leaking fire main

exceeded the capacity of the storm drains and then entered the Unit 2 safety-

related emergency service water /high pressure service water pump hause via

. underground electrical conduits.

I

b. Observations and Findinas 1

On August 23,1998, a leak on the station fire main occurred wher, a 6" pipe

separated from a coupling upstream of a block valve. Maintenanco workers were

working in the vicinity of the coupling. This event was caused by weaknesses in

both maintenance planning and work practices.

Planning issues: A lack of knowledge or understanding of the design of the

pipe coupling upstream of the' block valve contributed to this event. This

<

coupling was a slip-fit compression fitting that separated while maintenance

technicians were working on the downstream hydrant coupling. Normally,

the failed coupling was supported laterally by two tie rods clamped between

the hydrant and the piping upstream of the coupling, and by a thrust block at

the hydrant. Both the tie rods and the thrust block had been removed to <

permit replacement of the hydrant, thus allowing the coupling to separate.

Planners did not have detailed information on the design of the coupling or

the function of the tie rods. Planners did not direct maintenance personnel

to uncover the coupling, thus missing an opportunity to visually check the

coupling before the work was accomplished. Also, planners did not use two-

valve isolation for the work.

  • Maintenance Practice issue: Maintenance personnel left the pipe coupling

.

covered with dirt, thus they were not aware of its configuration and the

potential hazard associated with removing the tie rods.

Water accumulated in the outside yard area in the vicinity of the fire hydrant, due to

exceeding the capacity of the storm drains in the area. Water seeped into electrical

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conduits via manholes that connected to underground cable duct banks. The water

then leaked into the emergency service water /high pressure service water pump

house structure through these cable duct banks and degraded penetration seals.

Sump pumps in the pump house prevented any water accumulation. PECO

engineers promptly evaluated the impact of the degraded penetration seals on pump

operability and determined that no operability concems existed. Engineering

personnel also extrapolated the pump house in-leakage rate to the design basis

flood level and postulated that in-leakage at flood levels would have been within the

capacity of the sump pumps. (The design basis flood scenario is a flood of about

twelve feet above the ground level outside the pump housa. The water level

outside the pump house actually reached about three inches). The Peach Bottom

flood analysis allowed for cables to exist in a wet environment, and some conduit

seepage was acceptable. The inspectors reviewed the engineering analysis and

operability determinations from this event and had no concerns.

c. Conclusions '

7

WeakneIes in maintenance planning and work practices led to a significant water

lesk on the station fire main on August 23,1998. Water from the leak entered the

i

safety related emergency service water /high pressure service water pump house via i

underground electrical conduits and degraded penetration seals. The engineering l

evaluation, that the penetration sealleakage was within design assumptions for a

design basis flooding event, and pump operability was not affected, was adequate.

Ill. Enaineerina

E1 Conduct of Engineering

E1.1 Installation of the ISFSI East Retainina Wall j

a. Insoection Scope (60851 & 60853)

The inspectors reviewed independent spent fuel storage installation (ISFSI)  ;

engineering and construction activities affecting the concrete placement of the east i

retaining wall, including physicalinspection of the installation. The inspector also

reviewed field activities associated with the soil compaction testing and inspection j

of the subsurface of soil of the ISFSI east retaining wall. The inspector evaluated i

the site and reviewed construction records.  !

1

b. Observations and Findinas i

Assessment of Construction Activities ]

!

To protect the ISFSI storage pad from an adjacent hill and undermining due to a

slope drop, retaining walls were constructed to the east and the west of the storage

pad. The design and construction of these retaining walls was performed in

accordance with 10 CFR 72 Subpart G " Quality Assurance" requirements. These i

retaining walls are designated as important to safety (ITS). j

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The inspectors reviewed the construction of the east retaining wall, in particular, the

construction joints. Concrete for the east retaining wall was poured in sections,

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which interlocked through construction joints called keyways. The inspectors

reviewed an evaluation of construction discrepancies made on the dimensioning of

<

two 6'f the keyways. The design specified that each keyway be 8" wide by 3"

, deep. PECO personnel identified that the keyways on the south construction joint

'

of wall No. 02A and the north construction joint of wall No. 05 used incorrect

2

keyway dimensions (approximately 5.5" wide by 3" deep). Engineering personnel

documented this evaluation in Engineering Change Record (ECR) 98-02355. As a

! part of the corrective actions, PECO personnel stopped additional concrete pours

and analyzed the as-found condition.

The inspectors reviewed calculation NCR-98-02355,which assessed the as-found I

configuration (reduced size of keyway) of the construction joint at the east wall.

The inspectors found the calculation and conclusion acceptable. The assumptions  !

in the calculation were conservative, and the approach used to calculate the shear

forces acting on the reduced keyway were acceptable. The calculation showed that

the as-found configuration for the reduced size of the keyway was within shear i

allowables established in the main design calculation of the east wall.

Soil Comoaction Activities

The inspectors reviewed Field Change Request (FCR) No. 98-OO811-10,which was

prepared to document and disposition the two field density tests which failed to

achieve the required degree of compact'on (95 percent). The FCR disposition in

both cases accepted the condition "as-is" based on engineering judgement. The

inspectors reviewed the engineering judgement determination and determined that

this was acceptable because the deviation was not substantial. The inspectors

verified that this was an isolated case and PECO personnel have ensured 95% )

compaction was achieved in all tested locations since this deviation was discovered. '

Concrete Mix Deliverv. Testino. arid Pourina Activities

The inspectors observed the concrete mix delivery, testing, and pouring activities

for the east retaining wall. The inspectors noted that the concrete pounng was l

being conducted in an acceptable manner. i

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Concrete was being shipped from Havre de Grace, Maryland, which was l

approximately one hour from ISFSI site. The inspectors noted that the specified l

maximum time of 90 minutes, from batching the concrete till p.,uring, was being

enforced to maintain quality and achieve the desired compressive strength. This

was evident when PECO personnel rejected two truck loads of concrete because j

the loads were not poured within 90 minutes.

'

The inspectors noted that the testing of the newly arrived concrete was properly 1

completed. Tests included slump, air entrainment, concrete and ambient air i

temperatures, and weight. Batch tickets were reviewed by PECO personnel and

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contained appropriate information, including data on the concrete mixture, time of

batching, and truck number.

c. Conclusion I

The inspectors concluded that the construction activities on the east retaining wall

of the independent spent fuel storage installation were acceptable. Engineering .

personnel had resolved construction deficiencies regarding as-built keyways and soil l

compaction in an effective manner, thus the analyzed as-found condition of the east

wall was acceptable. The concrete mix delivery, testing, and pouring activities for

the east retaining wall were acceptable.  !

E2 Engineering Support of Facilities and Equipment

l

E2.1 (Closed) URI 50-277(278)/97-06-03and (Closed) LER 2-97-007 Potential for  !

Bvoass of Pressure Suporession Pool l

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a. Inspection Scope (92903)

4

The inspectors reviewed licensee actions taken in response to the identification of I

the potential to bypass the pressure suppression function of the torus.

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b. Observations and Findinas

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A potential bypass flow path existed by which the drywell air space could

.

communicate with the torus air space through a six-inch containment purge nitrogen

supply piping. On October 21,1997, station personnel reported this issue pursuant

to 10 CFR 50.72 as a condition outside the design basis of the plant. Licensee

Event Report (LER) 50-277(278)/2-97-07 reported this issue on November 19,

1997.

Following the identification of this condition, engineering personnel drafted non-

conformance reports and a shift update notice for operations to notify all shift

personnel. Engineers also changed several procedures to prevent simultaneous ,

purging of the drywell and torus. Further, operations personnelissued a

administrative clearance to disable the drywG inboard purge supply valves on both

1 units to prevent simultaneous purging of J+ 6rnell and torus.

1

-

PECO corporate engineers completed an evmuation of other potential bypass paths

in June 1998. They concluded that other potentialleakage paths were either not

credible, or were significantly smaller than the equivalent of a one-inch hole limited

by technical specifications. This evaluation also concluded that the interim

i disposition of disabling the drywellinboard purge supply valves was acceptable until l

a final disposition was approved.

Engineering personnel attributed the cause of the event to an original design

deficiency in that the design requirements for lines which connect the drywell

airspace to the torus airspace were not adequately specified. Single failure and

.

.

20

electricalindependence design criteria were not originally applied to the drywell and

torus inboard purge supply valves.

The inspectors reviewed engineering activities for this issue, discussed them with

selected engineers, and conducted an in-plant review of the LER. The inspectors

determined that this issue was an apparent violation of 10 CFR 50 Appendix B,

Criterion Ill, " Design Control." However, the inspectors noted that it was licensee-

identified as a result of review', of industry operating experience and General

Electric 10 CFR Part 21 notification No SC97-4 dated October 15,1997. In

addition, the inspectors concluded that station personnel took prompt and effective

interim corrective actions as described above, and this issue was not likely to be

identified through routine efforts, in accordance with the NRC Enforcement Policy,

Section Vll.B.3, Violations involving Old Design issues, the NRC is exercising

enforcement discretion and not citing this violation as noted in separate

correspondence issued on October 28,1998. (NCV 50-277(278)/98-08-03)

c. Conclusions

Engineering personnel took prompt and effective corrective actions following j

their identification of the potential to bypass the pressure suppression function

of the torus during simultaneous purging of the torus and drywell or as a result

of postulated failures. In accordance with the NRC Enforcement Policy,

Section Vll.B.3, Violations involving Old Design issues, the NRC is exercising l

enforcement discretion and not citing this violation. l

l

E2.2 Aacess and Alarm Failures to Protected Area and Vital Areas Doors Due to Security

Multiplexer Failure

a. Inspection Scone (37551 & 71750)

The inspectors observed the response of security personnel to several failures of the

protected area and vital area doors due to a security computer multiplexer failure.

The inspectors also discussed this issue with security management and the security

system manager.

b. Observations and Findinas

Twice on August 12,1998 and then again on August 19 and August 24, the #1

security computer multiplexer failed. This failure caused the protected area and

vital area doors to f ail closed and rendered the alarm functions on the doors

inoperable. Security personnel implemented compensatory actions for this failure

per site security plan operating procedures. The inspectors discussed the

compensatory actions with security management. The inspectors noted that the

response by the security force to this multiplexer failure was adequate and the

failure of the doors had no adverse impact on plant operations. Operations

personnel were provided keys to allow access through locked doors while the

security computer was down. Each of the computer multiplexer failure events were

noted in the security log.

.

.

21

The system manager for the security system reviewed these failures and believed

that they were due to a power surge in the system. No root cause was determined

for these failures by the end of the inspection period.

The inspectors discussed this issue with engineering personnel. The inspectors

noted that engineering was initially slow to investigate this issue because the

system manager was offsite in training. Full investigation or this issue did not occur

until after the fourth failure of the security system when the system manager

returned from training,

c. Conclusions

Security personnel responded adequately to four failures of the security computer

multiplexer ir August 1998. The failures caused vital and protected area doors to

fait closed without alarm functions.

Engineering personnel failed to fully investigate and support this issue until after the

fourth failure. This contributed to delays in determining the root cause of the

multiplexer failures.

4

E2.3 Core Sorav Residual Heat Removal and Hiah Pressure Service Water Motor

poerated Valve Thermal Overload Wire Discrepancies,

a. Inspection Scone (37551)

The inspectors reviewed the findings and actions by engineering personnel for

thermal overload wiring discrepancies on motor operated valves (MOVs). l

Differences were identified between the installed wiring and the drawings for the l

Core Spray (CS), Residual Heat Removal, and the High Pressure Service Water

valves on both units.

b. Observations and Find _ings

l

During the review of a multiple high impedance fault calculation, engineering

personnel noted that the thermal overloads for the unit 2 CS suction MOVs (MO-2-

14-007A,B,C,D) were in the control circuit. However, on the unit 3 CS suction

MOVs (MO-3-14-007A,B,C,D),the thermal overloads for the control circuits were

permanently bypassed. The unit 3 CS valves were operable since they have no

automatic safety function, were key locked open, and would only be closed to act

as primary containment isolation valves when the CS system was secured and/or

tested.

~ . - , - - - - - - . - . - - - - - - - . - - . . - . . - . -

.. - . - - .~._ - - . -

..

, 22

A walkdown of the system by maintenance planning, on August 6 through

'

August 19,1998, revealed that the actual wiring did not match the schematic

drawings. Although the schematics showed that the wiring for the MOVs on both

units were the same, the as-found did not match the schematic drawings for the

unit 3 CS suction MOVs. Station personnel found the thermal overloads in series

with the control power ground connection on the unit 3 MOVs. This could result in

the control power being open circuited on thermal ovccload operation resulting in a

loss of position indication. However, an alarm in the control room would still )

indicate thermal overload activation. Although this wiring configuration was not in

accordance with the schematic drawing, it still resulted in the de-onergizing of the

MOV on a thermal overload condition. l

Station personnel compared the wiring configurations of several other MOVs with  !

the schematics and found that similar discrepancies existed for the residual heat

removal (RHR) system suction and cross connect valves and the high pressure

ervice water (HPSW) outlet valves on the RHR heat exchangers. Initial evaluations  ;

'

indicated that these valves functioned the same as the unit 3 CS suction MOVs and

were operable based on the same criteria used to evaluate the CS MOVs.

The inspectors noted that engineering's evaluation found the thermal overload

protection changed when the alternate power supply from the remote shutdown I

panel was used due to the as-found wiring for one of the RHR suction and HPSW l

MOVs on each unit. Further evaluation of these RHR and HPSW valves was on- I

going and tracked though the licensee's corrective action request system.

Engineering personnel noted that the initial operability evaluations did not address

the thermal overload protection concern that occurred when the alternate power

supply was used.

The inspectors reviewed documentation from the discovery of the wiring

discrepancies, the wiring rchematics, and the operability evaluations for the core

,

spray suction valves. The inspectors noted during this review that these wiring

discrepancies had existed for a long time.

c. Conclusion

Although discrepancies existed between the as-found condition and the schematics

for thermal overload wiring on several core spray, residual heat removal, and high

pressure service water motor operated valves, none of these discrepancies resulted

in the valves being inoperable. Initially, the most significant problem due to this

issue was the loss of valve position indication during a thermal overload actuation. ,

However, further evaluations of thermal overload protection for these motor  !

operated valves, during the use of the alternate power supply, was under review by

the engineering personnel and was documented in the licensee's corrective action

system. I

!

l

!

.- . , - - - , -,

__

,

.

23

1

IV Plant Support

R1 Radiation Protection and Chemistry Controls (RP&C)

R 1.1 Radioactive Waste Processina. Handlina, Storaae, and Shionina

l

a. Insoection Scoce (86750)  !

The inspectors reviewed and discussed sources of radioactive waste at the station,

waste processing and volume reduction efforts, and storage of waste. The

i

inspectors evaluated the methodology for radioactive waste concentration averaging  !

and the development of scaling factors used to estimate hard to detect l

radionuclides (e.g., Pu-239, Am 241). The inspectors reviewed waste classification I

practices and selectively reviewed radioactive waste shipping records for shipments (

of radioactive waste and other radioactive materials made since the previous  !

inspection. The inspectors also performed a test of the emergency response

contact listed on the licensee's radioactive material shipping papers. In addition,

the inspectors observed various radwaste loading and shipping activities including

loading of a cask with a high integrity container of spent resins and loading and

shipment of packages of slightly contaminated soil, i

l

The review was against selected criteria contained in 10 CFR 20; 10 CFR 61;

10 CFR 71; 49 CFR 100-179; applicable certificates of compliance for various NRC

licensed shipping casks; the Updated Final Safety Analysis Report; and applicable

NRC Branch Technical Positions.

b. Observations and Findinas

PECO continued to aggressively review and evaluate methods to reduce generated

radioactive waste volumes. PECO implemented actions to minimize dry activated

waste and process waste and was closely tracking and monitorin0 numerous

performance indicators relative to radioactive waste program performance including

plant leaks to reduce waste volumes. Of particular note was PECO's initiatives to

request industry audits of its solid and liquid waste programs to identify areas for

enhancen Mt and waste volume reductions.

PECO implemented appropriate scaling factors for use in determining curie content

of hard to detect radionuclides and was implementing applicable NRC Branch

Technical Position (BTPs) guidance regarding waste concentration averaging.

Waste was properly classified relative to 10 CFR 61 requirements.

The radioactive waste / material shipping program was generally well implemented.

Radioactive material shipping documentation was well maintained and available for

review. Individuals responsible for shipping activities were knowledgeable of

applicable requirements.

PECO was a registered user of the NRC licensed casks used for shipping purposes

and maintained up-to-date cask certificates of compliances associated drawings and

. - . . - . - _ - . - - - ---_.---- .- --

7

-

'

l I

4

.-. .

. 24

. disposal facility licenses. Shipments of radioactive materialin NRC licensed casks

,

were performed in accordance with certificato of compliance requirements.

! PECO implemented its emergency notification requirements for shipments by use of -

'

a vendor service listed on its shipping manifests as a point of contact for in-transit

shipping problems. When contacted, the vendor accurately described emergency

response actions for the shipment (dewatered resin) in transit.

J

i

c. Conclusions

l-

4

PECO's radioactive waste transportation program, including processing, handling,

, -storage, and transportation was effective. Wastes were properly classified and

, packaged.

R2 Status of RP&C Facilities and Equipment

,

a. Inspection Scoce (86750)

,

)<

l

The inspectors toured various radwaste and radioactive material storage areas '

j including the radwaste building, the south radwaste storage location, and the low l

r level waste storage area.

.

b. Observations and Findirigs -

Areas were generally well maintained, properly posted, and controlled. No

abandoned areas containing unprocessed, stored, or spilled waste was detected.

There was a limited amount of waste stored in the radwaste processing and storage ,

'

areas. Waste storage and processing areas exhibited generally very good material

condition. PECO was actively cleaning and painting the facility.

- *

  • The overhead pipes located in the 91'6" elevation of the floor drain pump room

exhibited some surface rusting. PECO had previously evaluated the pipes,

concluded the rust to be minor surface rust, and was monitoring the condition of

the pipes in the room.

The documented inventory of material contained in the south waste storage area

was not fully up-to-date. One package was marked as indicating it contained

material but the inventory list for the area indicated the container was empty.

PECO updated the list and took action to ensure the list was maintained current by

use of formal reporting of material transferred into the area,

c. Conclusions

Overall, radioactive waste and material processing and storage areas were properly

posted and controlled, and exhibited very good material condition.

.. . .- . - . - - - .-- --- - .-. - - - - . . - . . - - _

. . ,

.

4 '

25

R3 RP&C Procedures and Documentation

'

a. Inspection Scope (86750)

,

i

The inspectors discussed changes in radioactive waste processing, handling, and l

shipment procedures and programs since the previous inspection with personnel '

responsible for these areas.

i

b. Observations and Findinos I

There were no major changes identified in the radioactive waste processing,

handling, storage, and shipment procedures and programs since the previous

inspection.

There were very few staff or organization changbs in the radwaste management

4

group. New personnel coming into the group were provided training and prohibited

from performing tasks for which they were not yet qualified.

4

PECO was developing a 10 CFR 50.59 safety evaluation ta support injection of

9

noble metals into the reactor coolant in late 1998. PECO concluded that no adverse

radiological controls impact was associated with the injection including impact on l

radwaste processing, handling, or transportation programs.

PECO had established and implemented procedures for evaluation and survey of ,

,

materials not normally considered radioactive (e.g., sewage) to determine if the l

material should be considered contaminated and disposed of at licensed facilities.

c. Qnclusions

There were no major changes identified in the radioactive waste processing,

- -

- handling, storage, or shipment procedures and programs since the previous

inspection. PECO implemented its program for monitoring of normally non-

radioactive material (e.g., sewage).

R4 Staff Knowledge and Performance in RP&C

'

4

a. Insoection Scope (86750)

The inspectors evaluated general staff knowledge of radioactive waste processing,

handling, storago, and shipping requirements during the inspection,

b. Observations and Findinos

PECO personnel responsible for radioactive waste processing, handling, storage and

radioactive material transportation exhibited a good knowledge level of regulatory

requirements and program procedures. The personnel were aware of, and

knowledgeable of applicable regulatory requirements, including procedural

specifications, DOT rules and regulations, and radiological surv;y and assessment

methodologies.

- - - - - . - - _-- --.-.___.-.__

-

s

y

.

.

26

c. Conclusions

Individuals responsible for radioactive waste processing activities exhibited a good

knowledge level of regulatory requirements and program procedures.

R5 Staff Training and Qualification in RP&C

a. Inspection Scone (86750)

The inspectors reviewed the training provided to personnel involved in radioactive

waste generating, processing, and handling activities against criteria contained in

NRC Bulletin 79-19 and 49 CFR 172, Subpart H. The inspectors reviewed training

records and lesson plans and discussed training with cognizant PECO personnel.

b. Observations and Andinas

Based on a review of job tasks at the station, PECO had previously established a ,

training matrix to ensure that appropriate training was provided to applicable

personnel. PECO met the training requirements for station personnel via general

employee training and special training modules developed to address applicable

requirements.

One individual (mechanic) involved with transfer of radioactive waste and loading of

a cask shipment on August 20,1998, had not received the training previously

prescribed for his position in the a-priori developed employee training matrix

described above. The mechanic transferred waste from the station to the low level

waste storage facility and routinely loaded waste into shipping casks for transport.

The individual was noted to be knowledgeable of his specific task requirements and j

. was provided continuous direct oversight by radioactive material shipping l'

coordinators.

PECO initiated an evaluation of the adequacy of the individual's training for his .

assigned tasks and believed he may have possessed appropriate training relative to

49 CFR 172, and NRC Bulletin 79-19, acquired in advanced radworker training and

waste minimization training. PECO initiated action to place this matter into its

corrective action program. PECO also initiated action to determine why the

i individual had not received the a-priori specified training hnd if the training was

necessary. PECO took action to ensure other mechanics involved in waste handling

i. had received appropriate training.

There was no apparent defined training program for new radwaste personnel

, involved with radwaste shipping activities. PECO was taking action to review, and

. adopt, as appropnate, a proposed common program to be implemented at its

j . nuclear stations. One individual had recently been transferred into.the radwaste

, group and a PECO radwaste manager provided job specific procedure training and j

L on-the-job training. The individual possessed previous radwaste oversight

. experience. The training was considered adequate.

i

i

4

-- .- __. - , - - - . - - _ _ . .

- _ . _ - - . - - - . . . - . , .

. . ._ _ _ . _. . _ _ - - - . _ . _ _ _ . . _ _ . _ . ..__. __. _ ____-. _

,

.

, g n'

.

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27

c. Conclusions

- PECO provided generally good training of personnel involved in radioactive waste

activities However, one individual had not received the a-priori specified training

for mechanics involved with radioactive waste activities and there was no defined

training program for new radwaste personnel involved in radwaste shipping

[ activities. PECO took appropriate action on these matters.

i. .

R6 RP&C Organization and Administration

,

a. Insoection Scoce (86750)

>

!

The inspectors reviewed the current radioactive waste processing organization, I

j including staffing, responsibilities and authorities. The inspectors evaluated PECO's

j performance in this area by discussion with cognizant personnel and review of .

I applicable administrative and organizational records.

>

l b. Observations and Findinas

! ,

.

i The review of the current radioactive waste processing organization indicated that  !

there were no significant changes in the organization or its responsibilities and j

authorities since the previous inspection in this area. I

PECO radwaste management indicated that the current radwaste organization would

i be disbanded, in the near future, with its various subgroups incorporated into the

chemistry, radiation protection, and plant engineering groups, as appropriate, for

, purposes of enhancing efficiency and effectiveness. No immediate safety concerns

-

were identified relative to thic proposal. PECO was aware of the need to update

j organizational administrative documents, as appropriate, to reflect the new

-

organization, j

c. Conclusions

s

i. PECO continued to implement an appropriately staffed and defined organization for

i

radioactive waste processing, handling storage, and shipping.

1  :

l R7 Quality Assurance in RP&C Activities

t

,

a. Inspiq1 ion Scope (86750)

,

.The inspectors reviewed PECO's audits, assessments, and surveillances of its

i- radioactive waste handling, processing, and storage programs, as well as audits of

l the Process Control Program, against the criteria contained in its Quality Assurance

J. Program,10 CFR 20, and 10 CFR 71, Subpart H, Quality. Assurance.

,

p b. Observations and Findinas

i PECO performed various audits and surveillances of its radwaste processing,

j- -handling, storage,-and transportation programs including its process control

program. Training audits for applicable personnel were also conducted. The

<

4

-, - - - , , - --v , , - - - - - -

p.

. .._ _ . _ _ _ . _ . _ . . _ - _ ___ ___ _ . . _.. _ _ _... _ ._ _ _ _ _ . . . .

.

A

.

j 28  ;

, station's Nuclear Review Board recommended areas for additional review,

i > '

Oversight activities were performed using appropriate check lists and qualified

L personnel were used in lead audit capacities. Appropriate corrective action

{' - measures were init:ated for areas for enhancement. Audits were of appropriate  ;

j depth and scope.  !

!

c. Conclusions

4

2 '

, PECO performed audits of appropriate depth and scope of radwaste processing,

' handling', storage, and transportation activities, including training and qualification

i _- of personnel. Corrective actions were initiated for identified concerns.

R8 Miscellaneous RP&C Activities

fi

t R8.1 (Closed) Violation (VIO) 50-277(2781/97-03-02 Failure to Assure that the Turbine  !

j' Buildina Atmosphere was Processed Throuah the Turbine Buildina Gaseous Waste

y Treatmcnt System

.

)

i During a review of the design modificetion involving the north wall of the Unit 3 -

turbine building, it was determined that the processing and monitoring of the turbine

building atmosphere was not adequately performed. In response to NOV

50-278/97-03-02, dated May 16,1997, PECO attributed the violation to a lack of j

detail in the work order and inadequate verbal communication between the work

planner and the Health Physics planner. To mitigate future errors the licensee

revised four procedures to clarify communication expectations and regulatory

i, Mance. The corrective actions were reviewed and found to be reasonable. The

violttion is closed.

R8.2 (Closed) VIO 50-277(278)/97-04-03 Violation of Locked Hiah Radiation Area Kev

Control

The corrective actions taken by PECO for this violation were previously described in

NRC Inspection Report No. 50-277(278)/97-04, dated July 24,1997. PECO

implemented the corrective actions described therein. A review of high radiation

area access controls during this inspection found that access doors to high radiation

areas were properly locked and proper administrative controls were implemented for

keys to these areas.

R8.3 Inspection of incomina Fuel Shioments

a. Insoection Scope (86750)

The inspectors reviewed radiological controls oversight of incoming fuel shipments.

b. Observations and Findinas

- PECO was receiving new fuel for the Unit 2 outage. Radiation protection (RP)

technicians performed radiological surveys of the incoming fuel shipping containers

-including using an alpha contamination smear counting system to check smears of

the incoming packages for alpha contamination.

p

-.. - - . . - - -

.

.

29

RP procedure HP-C-403, " Instrument Quality Checks," Revision 0, required in

Section 7.4.2, that if 3 or more consecutive values, were in the warning band,

notify the Instrument Physicist, who would evaluate the Control Chart and

determine the instruments physical condition and determine whether to place the

instrument out of service or continue use, if continued use was permitted, the

instrument Physicist was to denote this on the Control Chart and initial and date the

entry. The warning level was defined in the procedure as the range on the control

chart between + 2 sigma and + 3 sigma and between -2 sigma and - 3 sigma

values.

The inspectors reviewed the Control Chart source check data for the instrument on

August 18,1998. The inspectors determined that 3 consecutive instrument source

check values fell outside of two sigma during the period August 16-17,1998.

, The radiation protection technician who performed the source check did not act on

the matter and a second technician did not recognize the problem. The Control

Chart listed only one of several acceptance criteria. The instrument had been used

for counting of smears of incoming fuel shipments and the instrument's Control

Chart was not initialed to permit its continued use. This was identified by the

inspectors as a violation of Technical Specification 5.4.1 for failure to properly

, implement procedure HP-C-403. (VIO 50-277(278)/98-08-04)

PECO placed this matter in the PEP program, initiated an evaluation of the alpha

smear counting instrument, and determined that the instrument was functioning

properly and exhibited proper efficiency when source checked. PECO reviewed

beta-gamma smear survey results and did not identify any removable contamination

on incoming fuel shipments. PECO reviewed other in-field counting instruments and

did not identify any similar problems. PECO revised its instrument Control Charts to

include all procedure specified acceptance criteria for evaluation of source check

results. PECO concluded the individual who had performed the check was aware of

the procedure requirements but forgot to initiate a call to the Instrument Physicist. i

PECO coached the involved individual and discussed the event at all hands

meetings.  !

l

c. Conclusion

PECO provided generally good radiological controls oversight of incoming fuel

shipments. However, a violation of radiation protection procedures associated with i

'

source checking of an alpha contamination counting instrument was identified by

the NRC and was promptly corrected by PECO.

t

.. . _ ._ ._ __ __ _ _ _- _ __.

.

O'

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30

R8.4 Security Oversiaht of Radwaste Activities

a. Insoection Scoce (71750 & 86750)

' The inspectors reviewed PECO's loading and transfer of a high integrity container

into the process shield at the low level waste storage facility for transfer into the

protected area.

b. Observations and Findinas

PECO stored its vendor supplied high integrity containers, upon receipt, in a locked i

building outside of the protected area. The containers were subsequently loaded i

into a waste processing shield, under observation of security personnel, and

transferred into the protected area to the waste fill station by personnel authorized

Protected Area access. The large lids of the containers were sealed.

Although security personnel routinely provided oversight of the loading and transfer j

of the containers, there were no clearly described expectations regarding the degree

of security oversight to be provided for the activity (e.g., inspection of the bottom

of the transfer shield or opening and inspection of non-sealed small areas).

.

The acting Security Manager agreed that inspection of the containers could be I

enhanced and suspended transfer of the high integrity containers into the protected

area pending establishment of additional guidance for conducting an inspection of

the containers. The acting Security Manager stated that this additional guidance

would be added to the security training program to ensure that security personnel

met the revised expectations regarding review of the container loading and closure

operations.

c. Conclusions

PECO provided security oversight of high integrity containers transferred into the

Protected Area. However, clearly described expectations regarding the degree of

security oversight of this activity was not fully provided. PECO enhanced

inspection guidance and added the revised expectations to the security training

. program.

1

V. Manaaement Meetinas l

X1 Exit Meeting Summary

l

The inspectors presented the results of the inspection to members of the licensee

management on September 23,1998. The licensee acknowledged the findings I

presented. No proprietary information was identified by the licensee.

l

l

l

._

.

._ - _ . _ . _ _ . - _ _ _ . _ _

e

.

31

X2 Review of Updated Final Safety Analysis Report (UFSAR) Commitments

, A discovery of a licensee operating their facility in a manner contrary to the

Updated Final Safety Analysis Report (UFSAR) description highlighted the need for a

special focused review that compares plant practices, procedures and/or parameters I

to the UFSAR descriptions. While performing the inspections discussed in this

report, the inspectors reviewed the applicable portions of the UFSAR that related to

the areas inspected. The inspectors verified that the UFSAR wording was

consistent with the observed plant practices, procedures and /or parameters.

1

I

l

e

J

l

\

l

1

3

i

l

l

4 i

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l

,..: . . . . . . . . . . . - . - . - . - .. . - . . . . . . - . . . . - . . - - . - .. ..

, ,

.e:

.;

ATTACHMENT 1

LIST OF ACRONYMS USED -

~

'

'AO[ abnormal operating i

AR - action request

,

BTP Branch Technical Position

CM. Corrective Maintenance

CRD Control Rod Drive

'

CS Core Spray

DOT- Department of Transportation

ECR Engineering Change Request

ESF Engineered Safety Feature

FCR Field Change Request ,

FIN Fix-It-Now

GP general procedure ,

'

ISFSI independent spent fuel storage installation

ITS Improved Technical Specifications

JPM Job Performance Measure

LCO. limiting condition for operation

j LER licensee event report

j. LOCA. loss of coolant accident

-

LSRO Limited Senior Reactor Operator

~

MCRD Main Control Room Deficiency

MOV _ motor operated valve

-NCV. non-cited violation

NOTICE notice of violation

i

PECO Peco Energy

'

[ PkCON Peco Nuclear

PEP performance enhancement program

PDR public document room ]

PMT Poct-Maintenance Testing

RO Reactor Operator *

RP radiation protection

RPM radiation protection manager

RWCU reactor water cleanup

RHR residual heat removal

RT Routine Test

ST surveillance test

TS technical specification

TSA technical specification action

'UFSAR updated final safety analysis report - )

I

!

- , . . _ _ _ . . - -

__ __ _ .

,

S

.

Attachment 1. 2

INSPECTION PROCEDURES USED

IP 37551 Onsite Engineering Observations

IP 60851 Design Control of IFSFI Components

IP 60853 On-Site Fabrication of Components and Construction of an IFSFl

IP 61726 Surveillance Observations

IP 62707 Maintenance Observations

IP 71001 Licensed Operator Requalification Program Evaluation

IP 71707 Plant Operations

IP 71715 Sustained Control Room and Plant Observation

IP 71750 Plant Support Observations

IP 84750 Radioactive Waste Treatment, and Effluent and Environmental Monitoring

IP 86750 Solid Radioactive Waste Management and Transportation of Radioactive

Materials

IP 92903 Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-278/98-08-01 VIO RWCU System Startup Procedure

Ooened/ Closed

50-277/98-08-02 NCV Torus /Drywell Vacuum Breaker Loss of Seated

Indication (Unit 2)

50-277/98-08-03 NCV Potential for Bypass of Pressure Suppression Pool

50-278/98-08-03 NCV Potential for Bypass of Pressure Suppression Pool

50-277/98-08 04 VIO Failure to Adhere to Radiation Protection Procedures for

Source Checking Instruments

50-278/98-08-04 VIO Failure to Adhere to Radiation Protection Procedures for

Source Checking Instruments

Qlosed

50-277/97-03-02 VIO Failure to Assure that the Turbine Building Atmosphere

was Processed Through the Turbine Building Gaseous

Waste Treatment System

50-278/97-03-02 VIO Failure to Assure that the Turbina Luilding Atmosphere

was Processed Through the Turt 'e Building Gaseous

Waste Treatment System

50-277/97-04-03 VIO Violation of Locked High Radiation Area Key Control

50-278/97-04-03 VIO Violation of Locked High Radiation Area Key Control

50-277/2-97-007 LER Potential for Bypass of Pressure Suppression Pool

50-278/2-97-007 LER Potential for Bypass of Pressure Suppression Pool

50-278/3-98-004 LER Reactor Water Cleanup System Automatic Isolation

50-277/97-06-03 URI Potential for Bypass of Pressure Suppression Pool

50-278/97-06-03 URI Potential for Bypass of Pressure Suppression Pool

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ATTACHMENT 2

Maintenance Observation _g: Observed On:

M-018-003 New Fuel Receipt and Inspection August 23

M-053-011 Cleaning and Inspection of Powell August 31  :

Series P-51000 Metal-Clad Switchgear l

C0183052 Refueling Water Pump B - Inspect / Repack September 10

Seals

C0182395 Recirculation Motor Generator Oil Cooler September 12 ,

Setpoint Change 1

1

M-056-001 480 Volt Motor Control Center September 16

Circuit Breaker Assembly and

Cubicle Terminal Maintenance

2

Surveillance Observations: Observed On:

TRT #98-025 Reactor Water Cleanup System 16A Valve August 24

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Troubleshooting (Unit 2)

ST-O-052-704-2 E4 Diesel Generator 24 Hour August 26 i

Endurance Test

Sl2K-54-E32-XXFM Functional Test of E32 4KV Septembe'r 3

Undervoltage Relays

RT-O-40C-530-2(3) Drywell Temperature Monitoring September 16

ST-O-052-413-2 E3 Diesel Generator Fast Start September 16  !

and Full Load Test {

TRT #98-050 2B Loop of HPSW,2B Loop of RHR September 16

in S/D Cooling, Unit 2 ILRT Valve

RT-O-003 990-2 Control Rod Stroke Speed September 17

ST-O-10-306-3 B RHR Loop Pump Valve Flow September 17

and Unit Cooler Functional and  !

Inservice Test

i

Sl3N-60B-RBM-AICS Calibration / Functional check of September 20

Rod Block Monitor "A"

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