ML20138G279
| ML20138G279 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 09/07/1996 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20138G258 | List: |
| References | |
| 50-277-96-06, 50-277-96-6, 50-278-96-06, 50-278-96-6, NUDOCS 9610210100 | |
| Download: ML20138G279 (32) | |
See also: IR 05000277/1996006
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U. S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket / Report No.
50-277/96-06
License Nos. DPR-44
50-278/96-06
Licensee:
PECO Energy Company
P. O. Box 195
Wayne, PA 19087-0195
Facility Name:
Peach Bottom Atomic Power Station Units 2 and 3
Dates:
July 7 - September 7,1996
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Inspectors:
W. L. Schmidt, Senior Resident inspector
F. P. Bonnett, Resident inspector
R. K. Lorson, Resident inspector
R. L. Nimitz, Senior Radiation Specialist, OCS
Approved By:
W. J. Pasciak, Chief
Reactor Projects Branch 4
Division of Reactor Projects
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9610210100 961010
ADOCK 05000277
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EXECUTIVE SUMMARY
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Peach Bottom Atomic Power Station
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Inspection Report 96-06
This integrated inspection report includes aspects of resident and region based inspection
of routine and reactive activities in: operations; surveillance and maintenance; engineering
and technical support; and plant support areas.
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Overall Assurance of Quality:
PECO operated both units safely over the period.
PECO responded well to identify and correct several equipment deficiencies in a timely
manner including mechanical prcblems with the Unit 3 high pressure coolant injection
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(HPCI) system, a Unit 3 safety relief valve (SRV) bellows failure, an electrical problem with
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the Unit 2 drywell sump flow integrator display, and several problems related to an
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electrical storm on August 17.
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Plant Operations:
Routine observations showed that operators conducted normal activities including shift
turnovers and pre-shift briefings well. Operators co7tinued to demonstrate good
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communication skills. Operators responded well to stabilize plant conditions following .
several transient events including: an electrical storm, a dual reactor feedwater pump.
lockup at Unit 2, a Unit 2 battery ground, a Unit 3 off-gas recombiner isolation, and HPCI
system gland seal condenser water leak at Unit 3 Operators took proper actions to enter
technical specification (TS) action statements as required.
Equipment operability, material condition, and housekeeping were acceptable in all cases.
Several minor discrepancies were brought to FECO's attention and were corrected. The
inspecto'rs identified no substantive concerns as a result of these walkdowns.
The inspector did note a performance weakn ass in that the operators did not identify that
the turbocharger air inlet damper was not properly positioned in accordance with system
operating (SO) procedures during the E2 emt rgency diesel generator (EDG) 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run.
PECO took actions to address this weakness
Maintenance and Surveillance:
PECO performed the NRC observed surveillance etivities well. The emergency service
water (ESW) and HPCI system testing verified system operability. Auxiliary operator
attention during the HPCI system identified and allowea correction of steam admission
valve stroke timing problems. The EDG 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> testing met 5 TS surveillanca
requirements (SR). Several issues regarding the E-2 EDG test concem'ac the turbocharger
air inlet damper operation and fuel oil filter operation remain to be reviewed in o future
inspection.
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(EXECUTIVE SUMMARY - CONTINUED)
PECO nuclear maintenance division (NMD) personnel and engineering responded well to the
HPCI steam admission valve stroking issue. Based on observation of the valve stroking
during testing, the inspectors believe that the system would have performed its safety
function, as designed prior to the repair. However, the need to remove the system from
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service to perform the repair could have been precluded had PECO implemented the vendor
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guidance on measuring and trending the pilot chamber pressure.
The inspector reviewed and closed licensee event report (LER) 3-96-002, finding that PECO
implemented thorough corrective actions to address mis-wiring of a residual heat removal
(RHR) room cooler fan, which caused it to rotate in the wrong direction. The safety
significance of this event was low since the wiring problem affected only one of the four
RHR pumps. The RHR pump would have started, but could have been adversely affected
by long term high room temperatures following an design basis accident (DBA). The
inspector considered this PECO identified and corrected violation a Non-Cited Violation,
consistent with Section Vll.B.I of the NRC Enforcement Manual.
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Enaineerina:
PECO performed wellin identifying issues surrounding the operation of the EDG and their
control circuits. However, weak analysis of an issue dealing with the time delay start of an
RHR pump in response to a loss of coolant accident (LOCA) with the associated EDG in
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test caused PECO to miss TS and updated final safety analysis report (UFSAR) compliance
issues. The inspectors found that modification review and subsequent post-installation
testing did not identify the RHR pump time delay issue. Further, previous PECO actions
taken to review the modification, as the result of prior problems with post-modification
testing verification of design function, did not identify this issue. Collectively, the
inspector considered that these issues represented an apparent violation of TS 3.8.1.17,
10 CFR 50.59,10 CFR 50 Appendix B; criterion Ill, " Design Control" and 10 CFR 50
Appendix B, Criterion XVI " Corrective Action." (Apparent Violation 96-06-01)
During the period, the inspectors observed good engineering support to identify and correct
equipment problems including: excellent system manager support to the HPCI steam
admission valve timing problem (See Section M4.2) and excellent support to restore power
to the Unit 2 feed pumps following a loss of power lock-up (See Section 02.2).
Engineering also provided excellent analysis of the effects of the electrical storm (see
Section 02.2).
Members of the NRC staff inspected PECO implementation of the 10 CFR 50.63, alternate
AC (AAC) system including the Conowingo Hydro-Electric Power Station and the station
blackout (SBO) equipment and procedures. Severalissues were identified dealing with the
NRC staff assumptions of how the Conowingo station supplied power to the SBO line and
the hydro-generation system reliability. The staff also questioned the use of wooden utility
pole in the Conowingo switchyard and the lack of instrumentation in the Peach Bottom
control room for monitoring the availability of the SBO line. This item was considered
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unresolved pending review of PECO's answers to the questions posed in the report
(Unresolved item 96-06-02).
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(EXECUTIVE SUMMARY - CONTINUED)
The inspectors completed their review of a previously identified issue where the standby
gas treatment system was operated in a mode not discussed in the UFFAR (Unresolved
item 95-27-02). Operation in this mode led to the inability of the syste.J to be single
failure proof and the inability under these conditions to meet the TS required 0.25 inches
of water negative differential pressure. This constituted an unidentified unreviewed safety
question in accordance with 10 CFR 50.59. The inspector considered this a violation of
10 CFR 50.59 (Violation 96-06-03). However, because of PECO's response to the
unresolved item and the corrective actions taken there is no response required to this
violation and Unresolved item 95-27-02 and Violation 96-06-03 were closed.
Plant Suooort:
PECO Energy, effectively implemented the revised Department of Transportation (DOT) and
NRC radioactive material shipping regulations (effective April 1,1996). The radiological
controls planning and preparation for the Unit 2 outage were considered very good.
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Improvement in management oversight of outdoor radioactive material storage areas and
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vendor dosimetry processing appeared warranted.
PECO's corrective actions for this event were adequate. However, the inspector
considered PECO's pre-job planning for this modification to be weak and noted that one
week elapsed from the initiation of the event until PECO implemented positive measures to
secure the unmonitored release path. This item will be further reviewed during an
upcoming NRC specialist inspection.
The inspector reviewed standby liquid control (SLC) system borated water sampling and
analysis. The inspector considered it a weakness that key shift operations personnel were
unaware of the SLC tank sampling evolution; particularly since the sampling procedure
required air mixing of the tank contents. The inspector noted that if not properly secured,
the air mixing could potentially affect the SLC system operation. The PECO system
manager indicated that the procedure would be reviewed to determine if any addh;onal
guidance was required.
During their continuing review process PECO identified several examples where the UFSAR
did not agree with current radiological material / waste and radiological control practices.
Also, the inspectors identified that the outdoor storage of radioactive materials was not
specifically described within the UFSAR. The specific issues presented no apparent
immediate safety concerns, however, the UFSAR should be updated to reflect current
practices, as appropriate. The review of the above matter relative to 10 CFR 50.59 and
the updating of the UFSAR in accordance with the 10 CFR 50.71(e)is considered an
unresolved item pending NRC evaluation. (Unresolved item 96-06-04).
The inspector closed Violation 95-23-01 - Failure to follow radiological controls in the " Hot
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Shop" and Unresolved item 95-27-01 - Review of 49 CFR Subpart H training requirements.
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TABLE OF CONTENTS
EX EC UTIVE SU M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii
TA B L E O F C O NT E N T S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v
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SUMM ARY OF PLANT ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
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OPERATIONS
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01
Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
01.1 General Comments
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02
Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 1
02.1 Routine Pla nt Tours . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
O2.2 Equipment Challenges
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04
Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . . 2
04.1 New Fuel Receipt Activities (60705) . . . . . . . . . . . . . . . . . . . . . 2
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MAINTENANCE AND SURVEILLANCE . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
M1
Conduct of Maintenance and Surveillance . . . . . . . . . . . . . . . . . . . . . . 3
Emergency Service Water Flowrate Verification . . . . . . . . . . . . . . . . . . 3
High Pressure Coolant injection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
Emergency Dit sel Generator Endurance Testing . . . . . . . . . . . . . . . . . . 3
M4
Maintenance Staff Knowledge and Performance . . . . . . . . . . . . . . . . . . 5
M4.1 Electrical Cable Installation (62707)
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M4.2 High Pressure Coolant injection System Steam Admission Stop
Valve Balance Chamber Pressure Adjustment - Unit 3 . . . . . . . . . 5
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M8
Miscellaneous Maintenance issues
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M8.1 (Closed) Licensee Event Report (LER) 3-96-002, Low Pressure
Coolant injection System Declared Inoperable Due to
inadequate Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . 6
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ENGINEERING
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Conduct of Engineering
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E1.1
EDG Modification Design issues - Apparent Violation 96-06-01
and Update to Unresolved item 96-04-04
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E2
Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . 10
E2.1
Station Blackout Line Review - Unresolved item 96-06-02 . . . . . 10
E2.2 Improper Control of the Standby Gas Treatment System -
Violation 96-06-03; (Closed) Unresolved item 9 5-27-02 . . . . . . 13
IV
PLANT SUPPORT . . . . . . . . . . . .
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R1
Radiological Protection and Chemistry Controls
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R 1.1 Radioactive Material Shipping - Temporary Instruction
2515/131 - Implementation of the Revised Regulations . . . . . . . 14
R1.2 Unit 2 Refueling Outage Radiological Controls
(Planning and Preparation)
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R1.3 External Exposure Controls - Use of National Voluntary
Laboratory Accreditation Program Accredited Dosimetry . . . . . . 16
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(TABLE OF CONTENTS - CONTINUED)
R2
Radiological Effluent Controls Program Review . . . . . . . . . . . . . . . . , . 18
R2.1 Holes Cut into Turbine Building Exterior Wall - Unit 3 . . . . . . . . 18
R3
Procedures and Documentation in Radiation Protection and Chemistry
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R3.1 Radioactive Material Shipping -Implementation of the Revised
R e g ula tio n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19
R4
Staff Knowledge and Performance in Radiation Protection and
C h e m i s t ry . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
R4.1 Standby Liquid Control Tank Sampling
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R5
Staff Training and Qualification in Radiation Protection and Chernistry . 21
R 5.1 Radioactive Material Shipping - Training of Personnel on the
Revised Regulations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21
R7
Quality Assurance in Radiological Protection and Chemistry
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R7.1 Radioactive Waste Processing, Handling, Storage, and
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Shipping (Program Audits)
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Misceila neou s is sue s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22
R8.1 Verification of Updated Final Safety Analysis Commitments
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R8.2 Previous Findings
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(Closed) Violation 95-23-01
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(Closed) Unresolved item 9 5 - 2 7 -01 . . . . . . . . . . . . . . . . . . . . . . . . . . 24
S1
Conduct of Security and Safeguards Activities . . . . . . . . . . . . . . . . . . 24
S1.1 Control of Safeguards Information . . . . . . . . . . . . . . . . . . . . . . 24
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M AN AG EM ENT M EETI N G S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
X1
Exit M eeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
LIST OF ACRONYMS USED
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SUMMARY OF PLANT ACTIVITIES
Unit 2 began the inspection period operating at 70% power and continued end-of-cycle
coastdown operations throughout the period, ending the period operating at 51% power.
Unit 3 began the inspection period operating at 100% power and remained at this power
for essentially the entire period. Throughout the period PECO reduced reactor power for
the following:
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July 16
Power reduced to 72% to perform main condenser waterbox cleaning.
PECO returned the unit to 100% power operation on July 17.
August 2
Power reduced to 70% to transfer the steam jet air ejectors and repair
a steam leak from the packing of the steam isolation valve. PECO
returned the unit to 100% power operation on August 3.
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August 6
Entered OT-106, " Condenser Low Vacuum" and reduced power to
85% in response to an off-gas recombiner isolation. The isolation
occurred while adjusting the 3B steam jet air ejector discharge
pressure. PECO returned the unit to 100% power on August 7.
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August 10
Ref Jced power to 55% to transfer the steam jet air ejectors. PECO
returned the unit to 100% on August 11.
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OPERATIONS
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Conduct of Operations'
01.1 General Comments (71707)
Routine observations showed that operators conducted normal activities including shift
turnovers and pre-shift briefings well. Operators continued to demonstrate good
communication skills. Operators responded well to stabilize plant conditions following
several transient events including: an electrical storm, a dual reactor feedwater pump
lockup at Unit 2, a Unit 2 battery ground, a Unit 3 off-gas recombiner isolation, and a HPCI
system gland seal condenser water leak at Unit 3.
02
Operational Status of Facilities and Equipment
O2.1 Routine Plant Tours
a.
Scope
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The inspectors used Inspection Procedure 71707 to perform routine tours of the facility
' Topical headings such as 01, M8, etc., are used in accordance with the NRC standardize
reactor inspection report outline. Individual reports are not expected to address all outline
topics.
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and also to walkdown accessible portions of the following engineered safety feature (ESF)
systems:
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HPCI - Units 2 and 3
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safety-related 125/250 VDC batteries - Unit 2
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RHR - Unit 2
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high pressure service water (HPSW)- Units 2 and 3
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ESW- Units 2 and 3
EDGs - Units 2 and 3
Equipment operability, material condition, and housekeeping were acceptable in all cases.
Several minor discrepancies were brought to PECO's attention and were corrected. The
inspectors identified no substantive concerns as a result of these walkdowns.
02.2 Equipment Challenges
a.
Scoce
The inspectors reviewed the actions taken by PECO to identify, assess, track, and correct
several emergent equipment problems involving the Unit 3 HPCI system, a Unit 3 SRV
bellows failure, the Unit 2 drywell sump flow integrator, and several problems related to an
electrical storm on August 17.
b.
Observations and Findinas
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Operability determinations and interim corrective actions initiated for the above deficiencies
were prompt and appropriate. PECO responded well to troubleshoot and correct the HPCI
and drywell integrator equipment deficiencies. Operators promptly restored equipment
affected by the electrical storm including: reactor core isolation cooling (RCIC), main stack
radiation monitoring, the SBO line, and a Unit 2 safety-related battery.
PECO operators responded well to an alarm indicating that the 3-71C SRV bellows had
failed. Troubleshooting determined that the bellows had failed and that the pressure
setpoint sensing section of the valve was inoperable, however, t.his did not affect the
ability to open the valve from the control room nor the automatic depressurization (ADS)
function of the valve. Operators correctly entered the SRV limiting condition for operation
action statement. A drywell entry will be required to repair the bellows.
c.
Conclusions
PECO responded well to identify and correct several equipment deficiencies in a timely
manner,
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Operator Knowledge and Performance
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04.1 New Fuel Receipt Activities (60705)
PECO began receipt of the new fuel assemblies in preparation for the Unit 2 refueling
outage on July 30. NMD personnel exercised caution during the handling and inspection of
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the new fuel assemblies. The appropriate procedures were present on the refueling floor.
Health physics (HP) personnel maintained proper radiological controls during the evolution.
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MAINTENANCE AND SllRVEILLANCE
M1
Conduct of Maintenance and Surveillance
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a.
Scone
The inspectors reviewed safety-related system surveillance testing of the ESW, HPCI, and
the EDGs.
b.
Observations and Findinas
Emeraency Service Water Flowrate Verification
The inspector observed portions of ESW flow verification surveillance testing, done to
verify adequate system flow to components including the emergency core cooling systems
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(ECCS) pump room coolers and the EDGs Auxiliary operators conducted the testing well
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and test results demonstrated system operability.
Hiah Pressure Coolant Iniection
The inspector observed the normal quarterly pump valve and flow testing at Unit 3. During
the initial start, the operator in the pump room identif%d leakage from the gland seal
condenser and requested that the control room stop the test. Communications between
the local operator and the control room were very good. During this start attempt, the
operator also noticed that the steam admission valve did not appear to open smoothly.
Following repairs to the gland exhaust condenser the surveillance test was rerun. The
inspector observed this test from the HPCI pump room. Prior to the test, engineering
personnel had stroked the steam admission valve using the oil system and it performed
properly. Engineering personnel were present during the system start to observe the
operation of the steam admission valve. The inspector observed that the valve started to
open normally and then opened quickly to the full open position, then partially re-closed,
and opened normally. The engineering personnel directed that the control room secure the
turbine until repairs to the steam admission valve could be completed.
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See Section M4.2 below for a discussion of the resolution of the steam admission valve
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Emeraenev Diesel Generator Endurance Testina
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The inspector made the following observations:
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Material condition before, during and after each test was good. However, the
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exhaust header to turbocharger gasket leaks continue to cause oilleakage and oil
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soaked lagging - which if not properly addressed could lead to a fire hazard.
During walkdown of the running E2 machine using the PECO SO procedure 52A.8.C
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- Diesel Generator Running Inspection, all conditions appeared normal, except that
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at approximately 2600 kW the inlet damper to the turbocharger combustion air inlet
plenum did not indicate open as required by the SO. Step 4.11 of the procedure
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states that when the machine is running with a load of at least 1900 to 2100 kW
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the operator should verify that combustion air has changed over to the outside air
filter by verification that the air inlet damper plunger is down. At loads less than
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1900 kW, the turbocharger inlet air is supplied by the engine driven supercharger.
The damper operates by the differential pressure generated as the turbocharger inlet
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plenum pressure decreases due to increased air flow through the turbocharger as
load increases.
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The inspector observed that the plunger was up at 2600 kW. The inspector also
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observed that the plunger was in the same position as the plungers for all the other
EDGs that were not running at the time. The inspector discussed this with the
operator, who stated that the plunger was in the correct position for the given
condition.
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The inspector subsequently reviewed the EDG technical manual and discussed the-
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condition with the system manager. It appeared that the plunger should have been
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down, but because the EDG was able to achieve its rated load capacity as
demonstrated by the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> load test, PECO did not have a specific safety concern
at the time.
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PECO committed to provide additional guidance to operators on the required
position of the air inlet plunger and to review the operation of the plunger during the
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next time the EDG was operated.
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The inspector found that the fuel oil pump discharge duplex filter (i.e., a filter with
two elements in parallel that may be switched from one element to the other using
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an internal switching valve) element in service had been switched during the 24
hour run. In general terms the only reason to switch filters is due to a high
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differential pressure conditions. Operators are required by SO 52.A.8D to verify
that the filter differential pressure is less than 10 psid. At 13 psid an installed
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annunciator alarms indicating that the operator should switch from the in-service to
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the standby filter element.
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The inspector noted that the SO did not provide guidance on what to do if the 10
psid was exceeded. Review of the annunciator alarm response procedure showed
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that the operator is not required to initiate a work order to replace the filter element
with the high differential pressure. It concerned the inspector that the procedures
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did not provide specific guidance to ensure that a dirty filter element would be
replaced and that no documentation indicated why the filter elements had been
switched during the E2 run. This was a concern since during a subsequent diesel
run for testing or in response to an accident, the operator could be left with two
dirty high differential pressure filter elements, which eventually could cause the EDG
to become unable to carry required loads.
c.
Conclusions
The surveillance activities observed were performed well. The ESW testing proved system
operability. Operator attention during the HPCI system identified and allowed correction of
a steam admission valve operating problems. The EDG 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> testing met the TS SRs.
The inspector did note a performance weakness in that the operators did not identify that
the turbocharger air inlet damper was not properly positioned in accordance with the SO
during the E2 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run. PECO took actions to address this weakness. Several other
outstanding issues with regard to the E-2 EDG test remain to be reviewed during a
subsequent report. Specifically, verification that the EDG air turbocharger air inlet damper
is functioning properly and that fuel oil filters are required to be changed out following
swapping from one to the other.
M4
Maintenance Staff Knowledge and Performance
M4.1 Electrical Cable Installation (62707)
The inspector compared the bend radius of several safety-related cables to the PECO
design criteria contained in drawing E-1317. The inspector reviewed the specified cable-
dimensions and then measured the bend radius for the selected cable installations and
determined that the cables met the E-1317 minimum bend radius requirements.
M4.2 High Pressure Coolant injection System Steam Admission Stop Valve Balance
Chamber Pressure Adjustment - Unit 3
a.
Insnection Scooe
The inspector reviewed PECO's response to a HPCI turbine steam admission stop valve
operating anomaly (See Section M1) and to an unexpectod HPCI turbine roll which
occurred while attempting to adjust the HPCI stop valve steam balance chamber pressure,
b.
Observations and Findinas
PECO attributed the HPCI steam admission stop valve operating anomaly to an improper
steam balance chamber pressure. PECO initially attempted to adjust the balance chamber
pressure in accordance with PECO maintenance procedure M-C-756-014 which generally
conformed to the guidance contained in General Electric Service information Letter (GE SIL)
352. During the initial adjustment, the HPCI turbine unexpectedly rolled and reached a
speed of 5000 revolutions per minute. The reactor operator alertly recognized this
abnormal condition and promptly isolated the turbine steam supply to stop the turbine.
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PECO attributed the HPCI turbine roll to a gage block that had been sized to the full length
of the pilot valve stroke and installed per M-C-756-014 to properly position the stop valve
pilot valve assembly during the balance chamber pressure adjustment. The gage block
unseated the steam admission stop valve and caused the turbine roll. PECO determined
that the short duration HPCI turbine roll did not cause any system damage. The inspectors
performed a external inspection of the HPCI system and concurred with PECO's
assessment.
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PECO successfully adjusted the stop valve steam balance chamber pressure utilizing a
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revised process which included an initial adjustment performed with a gage block
constructed to be less than the full pilot valve stroke. PECO then successfully retested and
declared the HPCI system operable on August 16. The inspectors noted that PECO's
engineering support throughout this event was good.
The inspectors noted a preventive maintenance (PM) program weakness in that PECO had
not been periodically monitoring the turbine stop valve balance chamber pressure as
,
recommended by GE SIL 352 and the vendor manual. The inspector reviewed PECO's
performance enhancement program (PEP) investigation for this event and noted that one of
the assigned corrective actions was to develop a PM program to periodically monitor the
balance chamber pressure.
c.
Conclusions
PECO nuclear maintenance division personnel and engineering responded well to this issue.
Based on observation of the valve stroking during testing, the inspectors believe that the
system would have performed its safety function, as designed prior to the repair.
However, the need to remove the system from service to perform the emergent repair
could have been precluded had PECO implemented the vendor guidance on measuring and
trending the pilot chamber pressure. PECO plans to review implementation of the vendor
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guidance as part of the PEP, in the near future.
M8
Miscellaneous Maintenance issues
M8.1 (Closed) Licensee Event Report (LER) 3-96-002, Low Pressure Coolant injection
System Declared inoperable Due to inadequate Post-Maintenance Testing
This LER identified that, during a preventive maintenance activity in January 1996, the 3C
RHR room cooler fan motor had been mis-wired so that the fan would rotate in the reverse
direction. Additionally, PECO identified that the post-maintenance testing had not been
adequate since it did not detect the improper fan rotation. PECO determined that the
improper fan configuration could have rendered the 3C RHR pump inoperable for longer
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than the seven day time period permitted by TS 3.5.1. The inspector noted that PECO
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implemented thorough corrective actions; and that the safety significance of this event
was low since the RHR pump would have started and only have been affected by a long
term temperature increase in the room and because the wiring problem only affected one
of the four RHR pump room coolers. This PECO identified and corrected violation is being
treated as a Non-Cited Violation, consistent with Section Vll.B.I of the NRC Enforcement
Manual.
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ENGINEERING
E1
Conduct of Engineering
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E1.1
EDG Modification Design issues - Apparent Violation 96-06-01 and Update to
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Unresolved item 96-04-04
a.
Scooe
inspection Report 96-05 discussed severalissues dealing with the control circuits of the
EDGs and associated loads. In order to allow determination of the regulatory significance
of these issues, PECO was asked to provide an analysis of the licensing basis for the
EDGs. During review and determination of the licensing basis PECO identified two
additional issues.
The identified issues included:
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an EDG running during a routine test, with its output breaker open, would not have
automatically loaded onto its associated emergency bus following a LOOP event
(i.e. the EDG output breaker would close, trip and remain open without operator
action);
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the EDG output breaker would not automatically re-shut onto the emergency bus for
other LOCA/ loss of offsite power (LOOP) sequences. PECO believes that these
sequences are outside the design and licensing bases;
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the associated RHR pump breaker would not remain shut following a LOOP /LOCA
event if the EDG was initially running in parallel with an off-site source; and
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the RHR pump start sequence would be altered if either the E3 or E-4 EDGs were
operating in parallel with off-site power, and a LOCA (no LOOP) occurred; the C or
D RHR pump would immediately start (these pumps are normally started 8 seconds
after a LOCA), followed by an A or B RHR pump start 2 seconds after the LOCA.
The inspectors continued to review the EDG output breaker issues to determine their safety
and regulatory significance.
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b.
Findinas
The inspectors conducted a detailed review of the RHR pump time delay issue discussed
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above. The following list represents a chronology:
PECO completed a calculation (unreviewed by NRC) which they believed showed
that the offsite power system and the supplied components would not be adversely
effected by the timing sequence problem. PECO also discussed making a change to
the test procedures and providing information to the operation department - stating
that the calculation resolved the issue.
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PECO made preparations to run the 24-hour endurance testing on the E4 and E2
EDG to meet the 24-month frequency.
On August 7, the inspector identified that the RHR pump time delays for starting on
offsite power were included in TS and that the problem affected all the EDGs and
associated RHR pumps, not just E3 and E4. The inspector informed NRC and PECO
management that a TS change would be required if the RHR pump would knowingly
not start as defined in TS.
1
On August 9, during a control room tour the inspector found that PECO engineering
had issued a shift update notice (SUN) stating that the offsite source could support
the early starting of an RHR pump and that the time delays for the pumps would be
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declared inoperable during testing. The inspector believed that the PECO issued
direction to the operators represented a change to the TS time delays for the RHR
pumps. PECO stated that they had not changed the TS since they were entering
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the LCO for the instruments.
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The inspector stated to PECO, after discussions with the NRR PM, that this still
appeared to be an unauthorized change since the pump, if required to start, would
still knowingly start at a time that was different from the TS allowable limits, if its
associated EDG was running in the test mode. Further, the bases of TS did not
assume both relays would function outside their allowable limit, which would be
analogous to this condition. Rc6 , the TS assumed a failure of a relay to function.
This was why the design was sWie failure proof (i.e. two relays in parallel).
The inspector also stated to PECO that it appeared that the design and installation
of modification P-231 caused the problem and that if the situation had been known
4
at the time, they would have had to answered "YES" to a TS change being
required, while preparing the modification 50.59 evaluation.
PECO put all EDG testing on hold until the TS issue could be resolved.
On August 20, during a review of the TS SRs and the 50.59 safety evaluation for
the modification the inspector found:
The safety evaluation for modification P231 clearly stated that the EDG in
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test was to return to standby and loads were to automatically energize from
offsite power.
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SR 3.8.1.17 required that an EDG in test return to a standby condition and
that loads automatically sequence onto offsite power (as they would for a
LOCA without a LOOP) following a LOCA.
The inspector discussed the issue with the NRR PM and NRC Region I management
- the decision was that PECO, with the current design, could not meet this SR - 3.8.1.17. The inspector discussed this issue with PECO management. PECO
management determined that this specific SR was only applicable during EDG
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testing. This position was discussed with NRR and found acceptable.
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PECO determined that the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> endurance testing could be conducted by
declaring the EDG inoperable and by making the associated RHR pump unable to
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start and declaring it inoperable.
The inspector identified the following during the review:
When the EDGs were run for testing between the implementation of the improved
standard TS (January 1996) and July 1996, TS requirements for RHR pump start
time could not be met. As such, either plant would have been placed in an
unanalyzed condition if a LOCA had occurred during EDG testing. Specifically, the
station voltage study included the time delays for RHR pump starts as stated in TS.
The technical issue did not appear to be of large safety significance due to the
relatively short period of time that EDGs were run. Further, only one EDG was
tested at a time - the other three station EDGs and their associated RHR pumps
were operable.
PECO engineering review identified the technical issue. However, PECO did not
identify the TS compliance issues. Further, PECO used a calculation to justify
knowingly not meeting the TS time delays and documented this in a shift update
notice (SUN) to the operations department. This approach changed the timing
sequence outlined in the UFSAR, which was the sequence on which the TS time
delays were based.
Modification P-231 did no.
- complish its design intent as stated in the safety
evaluation for return of an EDG in test to standby and automatically sequence loads
onto offsite power, following a LOCA. Further:
The design review for the modification did not identify the conflict between
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the EDG breaker opening and the RHR pump starting following a LOCA.
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Post-modification testing was inadequate because it did not verify the
sequencing of RHR pumps following a LOCA with an EDG in test.
The RHR pump starting tin,e delay issue was not identified as part of PECO's
corrective actions following a previous escalated enforcement action dealing with
this modification. PECO stated in response to the previous escalated notice of
violation (PECO letter dated September 18,1995, in response to NRC Notice of
Violation, dated August 17,1995, based on inspection Report 95-11 findings), that
the modification acceptance testing for Modification P-231 had been completely
reviewed, with no additional problems identified.
c.
Conclusion
PECO performed wellin identifying issues surrounding the operation of the EDG and their
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control circuits. However, the analysis of the TS and the UFSAR was weak with respect
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to the RHR pump time delay issue with an EDG in test. The inspectors found that 1) the
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TS time delays could not have been met during EDG testing,2) PECO did not know that TS
limits existed for the time delays or that TS surveillance testing required that loads
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sequence onto the bus in accordance with the time delays,3) the use of a calculation and
a SUN amounted to an unauthorized change to the TS,4) modification review and
subsequent post-installation testing did not identify the RHR pump time delay issue, and
51 previous actions taken to review the modification, as the result of a previous problems
with post-modification testing verification of design function did not cause this issue to be
identified. Collectively, the inspector considered that these issues represented an apparent
violation of TS 3.8.1.17,10 CFR 50.59,10 CFR 50 Appendix B; criterion Ill, " Design
Control" and 10 CFR 50 Appendix B, Criterion XVI, Corrective Action." (Apparent
Violation 96-06-01)
E2
Engineering Support of Facilities and Equipment
During the period the inspectors observed good engineering support to identify and correct
equipment problems including: excellent system manager support to the HPCI steam
admission valve timing problem (See Section M4.2) and excellent support to restore power
to the Unit 2 feed pumps following a loss of power lock-up (See Section O2.2).
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Engineering also provided excellent analysis of the effects of the electrical storm (see
Section O2.2).
E2.1
Station Blackout Line Review - Unresolved item 96-06-02
a.
Scope
On July 9, members of the NRR staff reviewed the implementation of PECO's commitment
to 10 CFR 50.63 " Station Blackout." PECO made commitments relative to 10 CFR 50.63
in their August 6,1992 submittal and their July 13,1995 submittalin support of a TS
change allowing use of the SBO line to lengthen the allowable out-of-service time for a
single EDG. The AAC power source used by Peach Bottom consists of (1) a dedicated
direct power line, buried beneath the Conowingo pond between the Conowingo Hydro
Electric Station and Peach Bottom, and (2) installed hydroelectric wrbines at Conowingo
configured to be able to feed the tie line and associated switchgear and transformers at
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both Conowingo and Peach Bottom.
The inspectors walked down the Conowingo Hydroelectric Station, including the generating
equipment, the switchyard, and the control room. The inspectors also reviewed operating
procedures with Conowingo staff to determine the contingency steps necessary to
reconfigure Conowingo generating equipment to feed the SBO tie-line. At Peach Bottom,
the inspectors walked down the switchyard and the control room and discussed
procedures for energizing safety-related switchgear from the SBO line,
b.
Observations and Findinas
The inspectors developed the following facts based on the walkdowns:
Of the 11 hydro units at the Conowingo Station, six units (6,7,4,5,10, and 11)
may be used as an SBO power source for Peach Bottom. The other units could be
used as SBO power sources, but require additional switching operations and have
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not been tested to connect to the Peach Bottom safety-related buses within one
hour,
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in addition to the 11 units, there are two smaller auxiliary hydro-generators
(1500 kW,440 Vac) used to supply station auxiliaries (battery chargers, oil pumps,
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etc.), in tM event of a loss of offsite power at Conowingo. Normally, offsite power
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(220 kVi, inrough a step down transformer, supplies the auxiliary power.
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The Conowingo staff described how auxiliary power, including auxiliary hydro-
2
generators are always in operation and that with auxiliary power available, startup
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and operation of the generating units is straightforward,
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Procedures were available at the Conowingo Station to energize the SBO line during
complete loss of offsite (220 kV) power by utilizing one of the six hydro units,
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The Conowingo staff indicated that Conowingo is a peaking station, with limited
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times during the year when the main hydroturbines are neither generating power nor
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operating as electrical condensers (spinning reserve).
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The SBO line is normally energized, from the Conowingo switchyard. If a hydro-
generating unit is not supplying the SBO line it is energized from the PECO offsite
grid.
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The SBO line from the Conowingo transformer, in the Conowingo switchyard, to the
underground conduit was supported by a wood utility pole, in addition, physically
adjacent transformers, which serve commercial lines, also route their output power
to the grid via adjacent wood utility poles,
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In the Peach Bottom control room circuit breaker and transformer tap changer
controls are present, however, in the normal standby condition there is no direct
indication of the voltage or frequency of the SBO line.
The inspectors developed the following issues:
o
During the review of the SBO rule implementation at Peach Bottom, the NRC staff
mis-understood that the SBO line is always energized through a hydro unit. In their
submittal dated August 6,1992, PECO stated that five of the eleven generating
units at Conowingo are normally running as electrical condensers and are available
as spinning reserves. In such a condition, PECO estimated that the time required to
provide power to the 33kV SBO system would be about five minutes. In the
August 6,1992 submittal, PECO also stated that if no Conowingo units are in
service, the initial actions required by the Conowingo operators would be to start
several of the Conowingo units and that these actions would take an additional ten
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minutes. At the time, the NRC staff did not understand that this statement implied
that there were times when the main hydroturbines at Conowingo are neither
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generating power nor operating as electrical condensers,
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In the August 6,1992 submittal, PECO stated that because the SBO line would be
normally powered, it was considered an on-line system in accordance with
NUMARC 87-00, item B.13. As such, PECO provided target availability numbers for
the SBO line but stated that there is no target for reliability for normally on-line
systems. The inspectors noted that there are times that the SBO line is powered
from the grid and no Conowingo hydroturbines are generating or serving as spinning
reserves. As such, the NRC staff does not consider the SBO AAC source (the SBO
line and generating units) to be a normally on-line source.
In its submittal dated August 6,1992, PECO stated all components of the SBO line
would be " capable of withstanding the effects of likely weather-related events."
The inspectors observed all major componen" of the line and concluded that, with
the possible exception of the wooden utility
1s, all components appeared to be
adequately protected from weather-related events.
In a letter dated July 13,1995, submitted in support of a revision to the TS that
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allowed out of service t me for inoperable diesel generators, the licensee stated that
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voltage and frequency on the SBO line would be verified periodically during times
the EDG was inoperable. During the walkdown, the NRC staff did not observe
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direct indication of voltage and frequency associated with the Conowingo line.
c.
Conclusion
Based on the findings discussed above, the implementation of 10 CFR 50.63 was
considered an unresolved item (Unresolved item 96-06-02), PECO needs to address the
following concerns:
The frequency with which at least one of the SBO hydro-generators is operating,
the frequency with which at least one of the SBO hydro-generator is operating as an
electrical condenser, and the frequency with which none of the SBO hydro-
generators are not operating.
The reliability of the AAC source given that there are times when none of the SBO
generating units are on-line. The licensee did not provide any reliability data for the
hydro units. The staff accepted the availability of 95 percent based on the
understanding that at least one of the hydro units that supply power to the
Conowingo line will be operating all the time. Since the hydro unit will not be
operating all the time, the licensee needs to address how the NUMARC 87-00
criterion on reliability for AAC power source is being met.
Clarify how the use of wood utility poles was consistent with the stated design
criteria of being " capable of withstanding the effects of likely weather-related
events." The licensee needs to provide justification on the use of wooden poles
and exposed cable connecting the underground portion of the AAC line at the 33 kV
substation at Conowingo to meet the requirements of NUMARC 87-00, Appendix B,
item B.3.
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Clarify how these periodic voltage and frequency verifications are performed
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including a discussion of the location of associated instruments and location of
associated displays. On July 13,1995, in response to Condition 3 (documented in
!
the NRC letter dated April 7,1995), the licensee stated that the periodic
surveillance of the SBO line would include verification of voltage and frequency to
ensure connection capability to the PBAPS onsite distribution system. Also,
!
provide details on the verification of the connectability of the AAC line.
E2.2 Improper Control of the Standby Gas Treatment System - Violation 96-06-03;
-(Closed) Unresolved item 95-27-02
a.
Scope
As documented in inspection Report 95 27, the NRC found that PECO procedures allowed
the possibility that the standby gas treatment (SBGT) system could be run in an
unanalyzed mode. Specifically, the inspectors found that operation of this safety-related
system taking a suction on the reactor buiWing equipment cell exhaust during reactor water
cleanup (RWCU) system resin regeneration had not been analyzed in the updated final
safety analysis report. Subsequently, PECO identified that system procedures allowed
operating configurations where it would not have been able to provide the design negative
pressure differential on the secondary containment following a design basis accident with a
single failure. At the time PECO took corrective actions to address the concerns during
subsequent SBGT operations.
However, the issue remained unresolved pending safety significance review of PECO
answers to several questions concerning the previously unidentified single failure
vulnerability.
1.
What would be the overall effect on reactor building negative pressure if the
postulated single failure occurred?
2.
How would operators respond to the postulated single failure condition and in what
time frame?
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3.
Based on the answers to questions 1 and 2, what would be the overall effect on
offsite/onsite doses and operability of the SBGT filters?
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The inspectors reviewed PECO's February 28,1996, response to this unresolved item and
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the supporting engineering calculation.
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b.
Findinas
PECO concluded the following:
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While not able to maintain the designed 0.25 inches of water vacuum differential on
!
the reactor building, the SBGT systems could have provided sufficient negative
pressure to ensure a monitored release for wind speeds up to 23 MPH.
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Plant procedures and routine actions would have enabled the operators to identify
and correct the low negative pressure conditions quickly following a LOCA.
As a bounding analysis, PECO also conducted an analysis to determine the effects
of no SBGT operation during the first 10 minutes following a LOCA which indicated
that neither the control room habitability dose per 10 CFR 50 Appendix A, General
Design Criteria 19 nor the offsite dose limits of 10 CFR 100 would be exceeded.
The inspectors found:
The SBGT system would have been able, with operator actions, to maintain
negative pressure and provide a monitored vent path, in all conditions. However,
operator action is not assumed by design for the first 10 minutes following a design
basis accident.
The calculations conducted were well documented and based on good engineering
judgement and used conservative assumptions,
c.
Conclusion
The operation of the SBGT system in a mode not described in the UFSAR, led to the
inability of the system to be single failure proof and the inability, under these conditions, to
meet the TS required 0.25 in of water negative differential pressure. This constituted an
unidentified unreviewed safety question in accordance with 10 CFR 50.59. The inspector
1
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considered this a violation of 10 CFR 50.59 (Violation E -06-03) However, because of
PECO's response to the unresolved item and the corrective actions taken there is no
response required to this violation. Unresolved item 95-27-02 and violation 96-06-03 are
considered closed.
IV
PLANT SUPPORT
R1
Radiological Protection and Chemistry Controls
R1.1 Radioactive Material Shipping - Temporary Instruction 2515/131 - Implementation of
the Revised Regulations
a.
Scoce (Tl 2515/133)
The inspector reviewed the implementation of the revised DOT and NRC radioactive
material shipping regulations (effective April 1,1996) outlined in Federal Register (FR)
Notices 60 FR 50292 and 60 FR 50248, dated September 28,1995. The inspector
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compared applicable effective regulations with the licensee's procedures and program, and
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discussed regulatory requirements with cognizant licensee representatives.
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b.
Observations and Findinas
The inspector ccncluded that the licensee implemented the effective (as of April 1,1996)
portions of the recent changes in DOT and NRC regulations. The licensee made revisions
to procedures to incorporate the changes including verification of updates to vendor
supplied computer programs. However, the inspector found that the licensee's program
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did not:
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provide guidance relative to determination of the degree of uniformity of low
specific activity (LSA) radioactive material.
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specifically address the unshielded dose rate criterion (1 rem / hour at 3 meters) for
packages of low specific activity and surface contaminated materials.
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specifically address the new design specifications for casks outlined in 10 CFR
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71.73,
e
provide guidance relative to ensuring all radioactivity present (e.g., fixed, removable,
neutron activation produced) was accounted for, for shipping purposes.
Though the licensee's staff was aware of these specifications, the described program did
not contain specific guidance relative to implementation of the above requirements. The
inspector did not identify any violations associated with the lack of specific program
guidance. The licensee indicated that the radioactive material shipping program would be
reviewed for enhancement, as necessary.
c.
Conclusion
No safety concerns were identified. Overall, the licensee effectively implemented the
revised radioactive material shipping regulations and revised procedures accordingly.
R1.2 Unit 2 Refueling Outage Radiological Controls (Planning and Preparation)
a.
Scope (83750)
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The inspector selectively reviewed the radiological controls planning and preparation for the
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Unit 2 refueling outage. The inspector reviewed records, discussed outage planning with
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licensee representatives, reviewed various radiological controls goals including radiation
exposure goals, and observed activities to verify necessary planning and preparations and
management support for radiological controls planning. Areas reviewed included increase
of health physics staff; supervisory control over contract technicians; special training,
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including use of mockup training; work package review by health physics personnel, dose
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reduction methods, radwaste reduction; and use of lessons learned from previous outages.
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b.
Observations and Findinas
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The inspector's review indicated that the licensee provided overall effective planning and
preparation for outage radiological controls work activities, including outage work scope
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coatrol. The Station ALARA Council approved outage dose goals and objectives including
. an aggregate occupational exposure goal of 250 person-rem.
The licensee planned to increase the health physics staff to support outage work and
planned to use PECO radiation protection personnel in lead capacities over contracted
technicians. Lessons learned from previous outages were incorporated into outage
,
planning. Mock up training was provided as appropriate. The licensee appeared to be
effectively controlling work scope. The inspector reviewed expected accumulated radiation
exposure for the planned outage and noted general agreement with the Unit 2 outage
accumulated exposure goal. Identified tasks had been assigned to various radiation work
permits. The inspector noted that essentially all significant planned work had received an
ALARA review (243 person rem reviewed as compared to an expected 250 person-rem).
The licensee planned to use area based planning to control unnecessary scaffolding
removal and re-installation. The inspector noted that the licensee established a source
term reduction team whose purpose was to review the station radiological conditions and
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recommended initiatives to reduce radiation dose rates.
The following observation was made:
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The inspector questioned licensee ALARA personnel as to the effectiveness of dose
reduction techniques used for various outage tasks (e.g.,' control rod drive removal
and replacement, snubber inspections, and in-service inspections). In particular, the
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inspector attempted to determine the relative accumulated radiation e.xposure
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sustained by workers for various tasks as compared to similar reactor facilities
where the same task had been performed. The licensee's ALARA personnel were
not readily able to discuss relative performance as compared to similar facilities and
similar tasks. The inspector indicated such inter-comparisons may provide
opportunities for occupational exposure reduction. The licensee's personnel
indicated this matter would be reviewed,
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c.
Conclusion
The licensee implemented generally very good ALARA planning for the Unit 2 refueling
outage.
R1.3 External Exposure Controls - Use of National Voluntary Laboratory Accreditation
Program Accredited Dosimetry
a.
Scope (83750)
The inspector selectively reviewed the status of testing of the licensee's vendor supplied
personnel whole body monitoring device and the scope of accreditation provided by the
National Voluntary Laboratory Accreditation Program (NVLAP) for the vendor supplied
dosimetry. 10 CFR 20.1501(c) requires that personnel dosimeters that are used in
4
accordance with 10 CFR 20.1502(a) be processed by a processor accredited by the
.
NVLAP for the appropriate types of radiation. Voluntary and redundant dosimeters, as well
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as direct and indirect reading pocket ionization chambers and those dosimeters used to
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measure the dose to extremities, are excepted from this requirement. The inspector
reviewed records and discussed the program with cognizant licensee personnel,
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b.
Observatic.1s and Findinas
The inspector noted that, for a period prior to October 1994, the licensee had provided
personnel whole body dosimetry via its own NVLAP accredited onsite radiation dosimetry
program. In October 1994, the licensee outsourced the dosimetry program to a vendor.
The inspector requested applicable audits, test data, and scope of accreditation for the
vendor supplied dosimetry.
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The inspector determined that NVLAP's scope of accreditation fu the vendor provided
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dosimetry covered applicable testing criteria when use of the vendor dosimetry was -
initiated in late 1994. The inspector determined that the licensee initiated blind (spike)
testing of the vendor dosimetry during the first calendar quarter of 1995. The initial blind
spike test results indicated apparent difficulty by the vendor in assessing shallow radiation
dose. The licensed attributed the problem to a low average beta radiation energy (88 Kev)
at the station and indicated that the dosimetry would over-respond (i.e., provide
conservative results) to the low energy beta radiation. Notwithstanding the licensee's
identification of this problem, the inspector made the following observations.
As of the date of this inspection, the licensee had not resolved this issue and was
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continuing to review it. The problem append to be attributable to calibration
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difficulties associated with a very steep energy versus response curve for the
dosimeter when subjected to low energy beta radiation,
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The inspector's review of the fourth quarter 1995 NVALP test data indicated that
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the vendor provided personnel dosimeter failed dosimetry test Category Vil
(combined high energy gamma and beta radiation) of the applicable natior'al
standard (ANSI. N13.11). The licensee's Radiation Protection Manager was
unaware of this failure indicating apparent weaknesses in oversight of vendor
activities.
The individual directly tasked with oversight of radiation protection dosimetry issues
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appeared to have limited experience in personnel dosimetry programs. .The licensee
indicated direct supervisor oversight was provided for the individual's dosimetry
related activities. The licensee indicated a training / qualification program for the
individual would be established and implemented.
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The licensee was reviewing these matters at the close of the inspection.
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c.
Conclusions
The personnel whole body dosimeter used by the licensee had received NVLAP
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accreditation and appeared to provide reasonable radiation exposure measurement.
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However, the low energy response problem of the dosimeter should be resolved. Further,
there appeared to be a need for enhanced management oversight of the vendor provided
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dosimetry services.
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R2
Radiological Effluent Controls Program Review
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R2.1 Holes Cut into Turbine Building Exterior Wall- Unit 3
a.
Scope
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The inspector reviewed a PECO identified event involving a low level unmonitored release
from the Unit 3 turbine building (TB) which began on July 18 and ended on July 25. The
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inspector discussed the event with key HP personnel, attended briefings, and reviewed the
PEP investigation results.
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b.
Observations and Findinas
PECO was initially slow to identify, bm followed-up well, an unmonitored gaseous release
path from the TB. The event occurred during the installation of ventilation duct supports
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for the new plant egress and radiochemistry laboratory (PEARL) building.
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The following is the sequence of events:
7/16 Installation work began, HP technicians verified the TB roof area clean.
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7/18 A worker cuts the first opening through the side of the TB; thus creating the
unmonitored release path.
7/24 A PECO engineer expressed concern that the TB openings could represent an
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unmonitored vent path. PECO and contractor personnel assessed the work
site and concluded that there was minimal air flow through the TB oper.ings
and that no further action was necessary.
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7/25 HP technicians sampled the TB area inside the plant and detected noble
gasses. The TB openings were then covered and sealed.
o
7/26 PECO initiated a PEP to investigate the event.
PECO assessed the possibility of an unmonitored release and determined that:
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The openings were not properly covered after completion of the work activities,
o
The modification safety evaiuation did not address the potential for a release event.
2
e
The TB is not part of the secondary containment so that a barrier breach document
was not required.
e
PECO initially assumed that the TB was maintained at a negative pressure so that
no air could escape the TB except through the ventilation exhaust. PECO later
determined that some areas in the TB could experience a positive pressure based on
the ventilation line-up.
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The volume of air flowing to the outside with respect to the TB exhaust flow was
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insignificant. PECO calculated the potential release as about one-millionth of the
allowable limit based on a conservative airflow assumption that the combined
leakage through the openings was equivalent to ten percent of the total TB exhaust.
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As corrective actions PECO revised the work order activities to add the following additional
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work controls:
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HP was notified prior to cutting the final two openings and performed monitoring of
the openings once per shift.
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All openings were sealed or flashed with permanent siding at the end of each shift.
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Only one opening was made at a time.
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PECO's corrective actions for this event were adequate. However, the inspector
considered PECO's pre-job p.'anning for this modification to be weak and noted that one
week elapsed from the initiation of the event until PECO implemented positive measures to
secure the unmonitored release path. This item will be further reviewed during an
upcoming NRC specialist inspection.
R3
Procedures and Documentation in Radiation Protection and Chemistry
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R3.1 Radioactive Material Shipping -Implementation of the Revised Regulations
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a.
Scope (Tl 2515/133)
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The inspector selectively reviewed radioactive waste shipments made since implementation
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of the revised DOT and NF.J regulations (effective April 1,1996). The review was against
criteria contained in 10 CFR 20,61, and 71; and 49 CFR 100-199.
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b.
Observations and Findinas
The licensee did not make any Type B quantity shipments (e.g., resin shipments) since
implementation of the revised shipping regulations (April 1,1996). The licensee had made
several low activity / exempt quantity shipments. The inspector reviewed four such
shipments and determined that the radioactive waste shipping program was implemented
and the radioactive material contents o' packages were properly determined. Packages
were classified, described, packaged, marked, and labeled (as appropriate). Shipping
records were complete and well maintained. The individuals involved in shipping activities
were generally very knowledgeable of applicable requirements.
c.
Conclusion
No safety concerns or violations were identified. The licensee effectively implemented the
revised DOT a. d NRC radioactive material shipping regulations.
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R4
Staff Knowledge and Performance in Radiation Protection and Chemistry
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R4.1 Standby Liquid Control Tank Sampling
a.
Scope
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The inspector observed the sampling of the Unit 2 SLC tank following surveillance test
procedure ST-C-095-801-2, " Standby Liquid Control Tank Boron Solution Analysis" on July
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17. Additionally, the inspector observed a portion of the sample analysis performed
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according to chemistry procedure CH-C-105, " Boron Analysis By Automatic Titration."
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b.
Observations and Findinas
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The chemistry technicians followed ST-C-095-801-2 while drawing the sample from
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the SLC tank.
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The SLC tank sampling was not included in the work week plan and the on-shift
work control and shift supervisors were unaware that the SLC tank was to be
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sampled.
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The on-shift reactor operator (RO) was not aware that the SLC tank had been
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sampled. The chemistry technicians had informed the previous shift RO about the
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tank sampling, however, they did not sample the tank until about two hours into the
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next shift.
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The procedure did not provide any guidance for restoration of the SLC system
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during the sampling process if required by an event condition.
!
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One of the chemical reagents used in the enalysis had three different shelf life labels
attached to its storage bottle. The chemistry technician used the most limiting shelf
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life label to determine that the reagent had exceeded its shelf life, however, the
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inspector was concerned that the number of different tags could lead to confusion.
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c.
Conclusions
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The inspector considered it a weakness that ke/ shift operations personnel were unaware
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of the SLC tank sampling evolution; particularly since the sampling procedure required air
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mixing of the tank contents. The inspector noted that if not properly secured the air
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mixing could potentially affect the SLC system operation. The PECO system manager
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indicated that a the procedure would be reviewed to determine if any additional guidance
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R5
Staff Training and Qualification in Radiation Protection and Chemistry
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R5.1 Radioactive Material S' nipping - Training of Personnel on the Revised Regulations
a.
Scope (Tl 2515/133)
The inspector reviewed the training, on the revised radioactive material shipping
regulations, provided to personnel involved in radioactive waste generation, processing,
handling, storage, packaging, and shipping activities (as appropriate). The inspector
reviewed training records, lesson plans, and discussed training with cognizant licensee
personnel. The inspector reviewed organization charts and reviewed the training records of
selected personnel who were involved in the aforementioned activities.
b.
Observations and Findinas
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A vendor provided specific training on the revised regulations in late 1995. Applicable
personnel attended the training including radioactive material shipping personnel, quality
assurance personnel, and training personnel. Training personnel subsequently provided
training on the revised regulations for other personnel involved in radioactive waste
processing, handling, storage, packaging, and shipping activities (as appropriate).
The following observation was made.
The revised NRC/ DOT regulations, including corrections thereto, were formally
provided to the public via Federal Register Notices. The inspector noted that,
although the licensee receives Federal Register Notices, the licensee's radioactive
material shipping personnel were not made cognizant of these changes via the
licensee's internal distribution program. Rather, the personnel principally became
aware of the notices through industry meetings or other means. The inspector
questioned whether applicable personnel would be made aware of regulation
changes, within a timely fashion. The inspector did note that the licensee did
receive periodic updates of radioactive material shipping regulations via a vendor
service. However, it was not apparent which method of notification provided the
most timely update of the staff on important regulatory changes. The licensee
indicated the internal distribution of Federal Register Notices would be reviewed,
c.
Conclusion
No violations or safety concerns were identified. The licensee provided appropriate
training of personnel, on the revised radioactive material shipping regulations.
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R7
Quality Assurance in Radiological Protection and Chemistry (83750)
R7.1 Radioactive Waste Processing, Handling, Storage, and Shipping (Program Audits)
a.
Scope (83750)
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The inspector reviewed selected audits, assessments, and surveillances of the radiological
1
controls program. The review was against criteria contained in Updated Final Safety
Analysis Report Chapter 13.8.
b.
Observations and Findinas
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The licensee implemeusd a generally broad based audit and surveillance program in the
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area of radiological controls. The quality assurance organization completed numerous
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performance based surveillances of ongoing activities. Audits were of good quality and
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appropriately qualified auditors were used to perform the audits, surveillances, and
assessments,
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The radiological controls organization initiated, in early 1996, a comprehensive radiological
controls program performance evaluation program. The program provided for a review and
evaluation of all program performance indicators on a quarterly basis that could be used to
identify areas for improvement in the radiological controls program. This was considered a
very good initiative.
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The licensee performed a comprehensive analysis of self-identified findings associated with
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nuclear maintenance group performance. The effort was initiated to identify root causes of
performance deficiencies and improve overall performance. The analysis was considered a
very good initiative.
c.
Conclusion
No safety concerns or violations were identified. Overall, surveillances and audits were of
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good quality as were licensee initiatives to improve performance.
R8
Miscellaneous issues
4
R8.1 Verification of Updated Final Safety Analysis Commitments
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a.
Scoce (83750)
!
A recent discovery of a licensee operating its facility in a manner contrary to the UFSAR
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description highlighted the need for a special focused review that compares plant practices,
procedures, and/or parameters to the UFSAR description. While performing the inspections
discussed in this report, the inspectors reviewed the applicable portions of the UFSAR that
related to the areas inspected.
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In particular, the inspector reviewed storage of radioactive materialincluding radioactive
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waste, relative to UFSAR descriptions and also reviewed the ,10 CFR 50.59 evaluation for
various outdoor radioactive material storage locations.
b.
Observations and Findinas
The licensee initiated a comprehensive review of the entire UFSAR in early 1996 to identify
incorrect or ambiguous statements and typographical errors. The review was performed in
two phases and involved a designated team of engineers. The licensee identified several
UFSAR issues with respect to the radiological controls area and radiological waste systems
and storage and brought them to the inspector's attention, as follows:
e
Relative to the solid radioactive waste portion of the review (UFSAR Chapter 9),
including ciry active waste, the licensee identified no incorrect statements, about 24
apparent ambiguous statements, and a number of typographical errors.
e
Relative to the liquid radioactis' traste portion of the review (AR Nos. A0999850,
A1025406), the lice nsee identified ses aral inaccuracies associated with UFSAR
(e.g., description of the location of the intake sample station depicted on UFSAR
Figure 9.2.5., lack of neutralization of the Chemical Waste Tank contents prior to
transfer, and accuracy of UFSAP. Figure 9.2.1B),34 apparent ambiguous
statements, and eight typographical errors.
e
Several inconsistencies associated with radiological controls program
elements / practices (AR No. A0998476) described in UFSAR Chapters 7,12, and 13
(e.g., use of electronic dosimetry versus pocket ion chambers, and use of two levels
of radiation protection technician training versus four levels).
In addition the inspector identified the following inconsistencies between the wording of
the UFSAR and observed plant practices, procedures and/or parameters, regard in outside
storage of radiological material / waste:
e
There was no apparent specific information, however, a licensee 10 CFR 50.59
evaluation identified several outdoor radioactive material storage / staging areas some
of which were not used. It appeared that the licensee should update the UFSAR to
reflect its outdoor radioactive material storage / staging practices.
e
The 10 CFR 50.59 evaluation, performed for outdoor storage of radioactive
material, did not addmss the storage of seven trailers behind the 135' elevation of
the radioactive wastr, building. The inspector noted that the trailer storage
appeared to be wel! within restrictions on radiation dose rates presented in the 10 CFR 50.59 evaluation, for other storage locations.
e
There were no surveillance criteria for evaluation of the material condition / integrity
of non-seven containers in outdoor storage locations. Several containers observed
at the South Yard exhibited significant rusting and faded and illegible radioactive
material information labels.
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The inspector's review did not identify any apparent significant safety concerns associated
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with the findings. The licensee had initiated actions (e.g., Action Requests) to review the
findings and update the UFSAR and applicable drawings, as appropriate.
.
c.
Conclusions
f
Several examples were identified by the licensee where the UFSAR did not agree with
current radiological material / waste and radiological control practices. Also, the inspectors
)
identified that the outdoor storage of radioactive materials was not specifically described
,
within the UFSAR. The specific issues presented no apparent immediate safety concerns,
d
however, the UFSAR should be updated to reflect current practices, as appropriate. The
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review of the above matter relative to 10 CFR 50.59 and the updating of the UFSAR in
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accordance with the 10 CFR 50.70 (e) is considered an unresolved item pending NRC
evaluation. (Unresolved item 96-06-04).
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R8.2 Previous Findings
d
(Closed) Violation 95-23-01
This violation involved failure to sdhere to radiation protection procedures during work in
4
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the " Hot Shop" and involved contractor personnel. The inspector's review indicated that
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the licensee implemented the corrective actions outlined in its November 2,1995, and
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January 3,1996, responses to the violation dated September 22,1995. Of particular note
was the licensee's actions to develop a contractor contract specification for use in
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establishing contracts with contractors. A guidance document for use by station staff
when utilizing contractors was also developed.
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(Closed) Unresolved item 95-27-01
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During a previous inspection, the inspector was not able to verify licensee conformance
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with 49 CFR 172 Subpart H training requirements. Specifically, the licensee was not able
to provide sufficient records to indicate provision of appropriate training, identity of target
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populations who should have received the training, or a training plan for those individuals.
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The inspector's review indicated that the licensee reviewed the work activities of station
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work groups in order to evaluate the need to provide specific training relative to 49 CFR
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172 Subpart H requirements, identified the target populations needing the training, verified
that appropriate personnel had received the required training, and verified that a training
plan had previously been in place. The licensee determined that appropriate training had
been provided. The inspector selectively reviewed the training provided, including the
target populations, and concluded that appropriate training had been provided, including
"
certification.
4
S1
Conduct of Security and Safeguards Activities
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a
S1.1 Control of Safeguards Information
On July 10, PECO reported, according to 10 CFR 73.71, that a number of documents
containing safeguards information had not been properly controlled. PECO implemented
s
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25
appropriate controls for the affected documents. PECO subsequently reviewed the event
and indicated that the uncontrolled documents did not impact any plant safeguard
capabilities. The NRC plans to review this event during a future specialist security
inspection.
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V
MANAGEMENT MEETINGS
X1
Exit Meeting Summary
At the conclusion of the report period, on September 19, the inspectors discussed the
findings and conclusions and the overall period conclusions with members of licensee
management. In all cases the licensee acknowledged the findings and conclusions
presented,
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LIST OF ACRONYMS USED
Alternate AC (AAC)
Automatic depressurization (ADS)
Department of Transportation (DOT)
Design basis accident (DBA)
Emergency core cooling systems (ECCS)
Emergency diesel generators (EDGs)
Emergency service water (ESW)
General Electric Service information Letter (GE SIL)
Health physics (HP)
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High pressure coolant injection (HPCI)
High pressure service water (HPSW)
Loss of coolant accident (LOCA)
Nuclear maintenance division (NMD)'
Performance enhancement program (PEP)
Preventive maintenance (PM)
Reactor core isolation cooling (RCIC)
Shift update notice (SUN)
Standby gas treatment (SBGT)
Surveillance requirements (SR)
System operating (SO)
Updated final safety analysis report (UFSAR)
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