ML20132E421
| ML20132E421 | |
| Person / Time | |
|---|---|
| Site: | Wolf Creek |
| Issue date: | 09/13/1985 |
| From: | Bruce Bartlett, Bundy H, Cummins J, Martin L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML20132E374 | List: |
| References | |
| 50-482-85-26, NUDOCS 8510010082 | |
| Download: ML20132E421 (15) | |
See also: IR 05000482/1985026
Text
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APPENDIX B
US NUCLEAR REGULATORY COMMISSION
REGION IV
NRC. Inspection Report: 50-482/85-26
LP: NPF-42
Docket: 50-482
Licensee: Kansas Gas and Electric Company (KG&E)
Post Office Box 208
Wichita, Kansas 67201
Facility Name: Wolf Creek Generating Station (WCGS)
Inspection At: Wolf Creek Site, Coffey County, Burlington, Kansas
Inspection Conducted: June 1 to July 31, 1985
Inspectors:
7 L If
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J. E. Cummins, Senior Reactor Inspector,
Date
Operations
(pars. 3, 4, 5, 6, 7, 8, 9, 10, 11,
12, and 13)
O M/AL.
,/aler
B. L. Bartlett, Resident Reactor Inspector,
Date
Operations .
(pars. 4, 5, 6, 7, 8, 9, 12, and 13)
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H. F. Bundy' Resident Reactor Inspector,
Date
Operations (pars. 4 and 13)
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Approved:
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Inspection Summary
Inspection Conducted June 1 to July 31, 1985 (Report 50-482/85-26)
Areas Inspected:
Routine, unannounced inspection including plant status;
followup on previously identified items; operational safety verification,
engineered safety features system walkdown; startup test witnessing, startup
test data review; onsite followup of events; site emergency drill;
enforcement conference (security); allegation followup; security; and plant
tours. The inspection involved 450 inspector-hours onsite by three NRC
inspectors including 67 inspector-hours onsite during offshifts.
Results: Within the 13 areas inspected, two violations were identified,
(failure ty.ontrol measuring and test equipment in accordance with
procedure, paragraph 4, and. temporary changes not incorporated in procedure as
required, paragraph 6). One unresolved item is identified in paragraph 12.
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DETAILS
1.
, Persons Contacted
Principal Licensee Personnel
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- G. L. Koester, Vice President-Nuclear
+o#C. C. Mason, Director-Nuclear Operations
+o#F. T. Rhodes, Plant Superintendent
J. A. Zell, Operations Superintendent
+oH. K. Chernoff, Licensing
oM. G. Williams, Supt. of Regulatory, Quality, and Administrative
Services
+oK. Peterson, Licensing
~
+#0. L. Maynard, Licensing Supervisor
W. B. Norton, Reactor Engineering Supervisor
oR. M. Grant, Director-Quality
- o#J. W. Johnson, Chief of Security
+C. J. Hoch, QA Technologist
0+W. M. Lindsay, Quality Systems Supervisor
+od. Hoyt, Emergency Plan Supervisor
J. Houghton, Operations Coordinator
A. Freitag, Nuclear Plant Engineering Site
o+R. Flannigan, Site Representative, Kansas City Power & Light
+F. D. McLaurin, Startup Manager
G. D. Boyer, Superintendent of Technical Support
M. Nichols, Health Physics Supervisor
- D. R. Smith, Superintendent of Plant Support
- i j.
The NRC inspectors also contacted other members of the licensee's staff
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during the inspection period to discuss identified issues.
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+ Denotes those personnel in attendance at the exit ineeting held on
July 1, 1985.
oDenotes those personnel in attendance at the exit meeting held on
August 5, 1985.
- Denotes those personnel attending the Enforcement' Conference held in
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Region IV on June 27, 1985.
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2.
' Plant Status.
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On June 6, 1985, the reactor plant-initially entered Mode 1 (power
' operation greater than 5%) and on June 12, 1985, the turbine generator
was synchronized to the grid for the first time. During this inspection
period, power ascension testing at the 20, 30, 50, and 75 percent power
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I,lateaus was completed.
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3.
Followup on Previously Identified Items
(Closed) Infraction (50-482/78-13): Failure to Meet Concrete Acceptance
Criteria for Containment Base Mat
^
This item was transferred to NRR for evaluation. The NRR evaluation and
conclusion is contained in the Final Safety Analysis Report (FSAR) for
the Wolf Creek Station (NUREG-0881) in paragraph 3.8.4.
This item was
incorrectly identified in NRC Inspection Report 50-482/84-22 as
50-482/78-04-B.
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(Closed) Open Item (50-482/8427-03): Calibration Status of Installed
Instruments
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This open item tracked licensee actions to resolve inspector concerns
over the controls associated with normally installed plant
instrumentation used to support Technical Specification required
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surveillance testing.
In response to these concerns, the ifcensee has
pr epared a list of all such instruments and cross referenced the
instruments to the surveillances they support. The list has been
incorporated into Procedure ADM 02-300 along with requirements for the
instrument and control department.to notify operations any time one of
the instruments is found out of service or out of calibration.
Operations is tasked with the responsibility for assessing the impact of
- the instrument problem on the validity of the surveillance tests that
instrument supports. This item was closed in NRC Inspection Report
50-482/84-57 and 50-482/85-11 but was incorrectly identified as open
-item 50-482/8427-02.
(Closed) Open Item (50-482/8459-07): Corrections to 50% Pseudo Rod Drop
Test Procedure, SU7-SF09.2-
The 50% power pseudo rod cluster control assembly (RCCA) rod drop test
was deleted from the Wolf Creek power ascension test program. By letter
dated July 3,1985, the Office of Nuclear Reactor Regulation notified
' the licensee of its acceptance of the deletion of this test. Deletion
of the test was based on successful performance of the test on other
Westinghouse plants.
-(Closed) Open Item (50-482/8509-02):
Inclusion of Loop Resistance
Temperature Detector Response Times in Preoperational Test Procedure
SU3-SA01
Test Discrepancy Report No. 30 documented the inclusion of the required
response times into Preoperational Test Procedure, SU3-SA01.
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(Closed) Licensee Condition Attachment 2, Item 2.C(7) Qualification of
Persennel :
This license condition required KG&E to certify the individuals who will
be standing watch as shift advisors. . A list of the certified shift
advisors was.provided to the NRC via KG&E letter KMLNRC 85-128, dated
May 29, 1985, satisfying this license condition.
(Closed) SER Item (50-482/84-00-158): Alternative Shutdown Capability
for the Control Room
This item tracked the installation of five new isolation switches and
the modification of four existing isolation switches. These switch
changes were required to provide isolation of equipment from a control
room fire. To verify that this item was completed satisfactorily, the
NRC inspector reviewed licensee documentation of the required switch
changes, observed installed switches in the field, and reviewed
Procedure 0FN-00-017, Revision 3, Control Room Evacuation.
(Closed) SER Item (50-482/84-00-150): Seismic Qualification of
Thermccouple/ Core Cooling Monitor System
This item, tracked the onsite completion of Westinghouse Field Change
Notice (FCN) SAPM-10627. To ensure the field modifications were
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completed, the NRC. inspector reviewed a signed off copy of FCN
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SAPM-10627, discussed the modifications with licensee personnel, and
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inspected portions of the completed modifications in the field.
(Closed) SER Item (50-482/84-00-52): Post Implementation Review of
Emergency Support Facilities
This item was closed in NRC Inspection Report 50-482/85-11, but was
j.
incorrectly identified as SER-Item 50-482/84-00-50.
(Closed) SER Item (50-482/84-00-151): Setpoint Adjustment of Barton
Differential Pressure Switches
This item tracked the change in setpoint for Barton differential
pressure indicating switches model numbers 288A and 581A. From
discussions with licensee personnel and review of the WCGS Total Plant
Setpoint Document, the NRC inspector determined that the required switch
setpoints had been changed.
(Closed) Open Item (50-482/8427-04): Availability of Information in
Auxiliary Shutdown Room
The NRC inspector verified that plant operating procedures, that provide
instructions for required operations from the auxiliary shutdown room,
have been placed in the room. The NRC inspector discussed the shutdown
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accomplished from the auxiliary shutdown room during Power Ascension
Test Procedure SU7-0014, " External to Control Room Shutdown," with the
cognizant shift supervisor (SS), and the SS stated that adequate
procedures and material were available in the auxiliary shutdown room.
4.
Operational Safety Verification
The NRC inspectors verified that the facility is being operated safely
and in conformance with regulatory requirements by direct observation of
licensee facilities, tours of the facility, interviews and discussions
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with licensee personnel, independent verification of safety system
status and limiting conditions for operations, and reviewing facility
records.
The NRC inspectors, by observation and direct interview,
verified the physical security plan was being implemented in accordance
with the security plan.
During a tour of_ the plant on June 26, 1985, the NRC inspector observed
Pressure Gauge WC 9967 connected to BN-FI-968.
This pressure gauge was
out of calibration, not installed in accordance with a temporary
modification order or approved procedure, and did not have a
10 CFR 50.59 applicability review.
Failure to control this modification
to plant equipment in accordance with procedures is an apparent
violar.on.
(50-482/8526-01)
5.
Engineered Safety Features (ESF) System Walkdown
The NRC inspectors verified the operability of ESF systems by walking
down selected accessible portions of the systems.
The NRC inspectors
verified valves and electrical circuit breakers were in the required
position, power was available, and valves were locked where required.
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The NRC inspectors also inspected system components for damage or other
conditions that might degrade system performance. The ESF systems
listed below were walked down during this inspection report period:
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Auxiliary feedwater system
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Reactor coolant charging system
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Safety injection system
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Residual heat removal system
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Containment spray, system
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Safety Class 1E 4.16KV AC system
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No violations or deviations were identified.
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6.
Startup Test Witnessing
Selected portions of the startup tests listed below were witnessed to
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ascertain conformance of the licensee to license and procedural
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requirements, to observe the performance of the staff, and to ascertain
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the adequacy of test program records, including preliminary evaluations
of test results.
507-8804 - RCS Flow Coastdown Measurement Test
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SU7-BB05 - Pressurizer Continuous Spray Flow Setting
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SU7-0009.1 - Load Swing at 30%
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SU7-0014 - External to Control Room Shutdown
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SU7-0020.2 - Turbine Generator Test at 20%
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5U7-0907.2 - Plant Performance
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SU7-SC03.2 - Thermal Power and Setpoint Data at 30%
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SU7-SE02.1 - Operational Alignment of Nuclear Instrumentation
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SU7-SE02.4 - Operational Alignment of Nuclear Instrumentation
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SU7-SE03.1 - Preliminary Axial Flux Difference Instrumentation at-
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50% Power
SU7-SE03.2 - Axial Flux Difference Instrumentation Calibration at
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75% Power
SU7-SF03.3 - Hot Full Flow Rod Drops
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SU7-SF03.4 - Hot No Flow Rod Drops
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SU7-SF09.1 - RCCA or Bank Worth, 30% Pseudo Rod Ejection
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SU7-SR01 - Incore Movable Detector
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SU7-SR04 - Incore Instrumentation Operability
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SU7-SR02 - Incore Movable Detector and Thermocouple Mapping at
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Power
SU7-AB01.1 - Automatic Steam Generator Level Control Test
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SU7-AB01.4 - Automatic Steam Generator Level Control Test
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SU7-0008.2 - Power Coefficient Determination
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SU7-0012 - Rod Drop and Plant Trip
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SU7-SF06.4 - Operational Alignment of Process Temperature
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Instrumentation at 75% Power
SU7-0010.1 - Large Load Reduction - 75% Power
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NRC inspector findings are discussed below:
While observing the adjustment of power range nuclear instruments per
Wolf Creek Work Request (WR) 91611-85, the NRC inspector determined that
the calorimetric had been run with a copy of Surveillance Procedure
STS SE-001, Revision 2, " Power Range Adjustment to Calorimetric," that
did not have applicable temporary changes incorporated in it. This
resulted in the nuclear instrument channels being adjusted to a power
level of 23.6.% when they should have been adjusted to 24.6% A followup
calorimetric was performed and the nuclear instruments were adjusted
accordingly.
Reactor power was maintained constant dur;ng this
evolution.
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Step 3.1.1 of the licensee's Administrative Procedure ADM 02-021, "Use
of Procedures in Operations," requires that, prior to use, a procedure
will be verified to insure.that it has all changes incorporated in it.
Perfomance of this surveillance using a copy 'of STS SE-001 that did not
have the latest changes incorporated is an apparent violation.
(50-482/8526-02)
7.
Startup Test Data Review
a.
The following test data packages were reviewed by the NRC
inspectors for:
Verification that all test changes, including deletions, were
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approved, reviewed, and incorporated properly.
Verification that all test deficiencies were resolved in
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accordance with the appropriate procedures.
Verification that deficiencies which constitute a reportable
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occurrence as defined by Technical specifications (TS) have
been properly recorded.
Verification that the as run copy of the completed test data
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package was properly completed.
Verification that the test suninary and evaluation were
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completed in accordance with procedure.
Verification-that the test results were properly approved.
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SU7-SF03.1, " Cold, No Flow Control Rod System Testing,"
Revision 3, dated March 29, 1985.
SU7-SF03.2, " Cold, Full Flow Control Rod System Testing,"
Revision 2, dated April 6, 1985.
SU7-SF03.3, " Hot, No Flow Control Rod System Testing,"
Revision 2, dated April 26, 1985.
SU7-VF03.4, " Hot, Full Flow Control Rod System Testing,"
Revision 2, dated April 26, 1985.
SU7-SF09.1, "RCCA or Bank Worth Measurement at Power (30%
Power Pseudo Rod Ejection)," Revision 1, dated
June 23, 1985.
SU7-5011, " Initial Criticality and Low Power Test Sequence,"
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Revision 3, dated May 17,_1985.
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SU7-5012, " Initial Synchronization and 20% Power Test
Sequence," Revision 2, dated April 28, 1985.
SU7-S013, " Power Ascension and 50% Power Test Sequence,"
Revision 3, dated June 19, 1985.
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SU7-BB02, " Pressurizer Heater and Spray Capability Test,"
Revision 1, dated April 10, 1985.
SU/-BB04, "Rx Coolant System Flow Coastdown Test, Revision 1,
dated May 19, 1985.
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SU3-BB13, "Special Test Procedure for Pressurizer Relief
Valve," Revision 0,
b.
The following tests were reviewed by the NRC inspectors for:
Verification that the cognizant engineering function has
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evaluated the test results and has signified that the testing
demonstrated that the system met design requirements.
Verification that the licensee specifically compared test
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results with established acceptance criteria.
Verification that those personnel responsible for review and
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acceptance of test results have documented their review and
acceptance of the data package and the evaluation.
Verification of quality assurance / safety group t r other
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independent review of test results as prescribe.d in FSAR or
other commitments.
Verification that those personnel charged with responsibility
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for review and acceptance of test results have documented
their review and acceptance of the data package and the
evaluation.
SU7-BB03, " Reactor Coolant System Flow Measurement,"
Revision 1, dated March 24, 1985.
SU7-SR04, "Incore Instrumentation Operability Test,"
Revision 2, dated April 26, 1985.
SU7-S010, " Post Core Loading Precritical Test Sequence,"
Revision 3, dated May 19, 1985.
SU7-SE02.2, " Operational Alignment of Nuclear
Instrumentation," Revision 2, dated May 2, 1985.
SU7-SE03.1, " Preliminary Axial Flux Difference Instrumentation
Calibration," Revision 1, dated June 28, 1985.
No violations or deviations were identified.
8.
Onsite Followup of Events
The NRC inspector performed onsite followup of the nonemergency events
listed below. The NRC inspector observed control room personnel
response,* observed instrumentation indicators of reactor plant
parameters,* reviewed logs and computer printouts, and discussed the
event with cognizant personnel . The NRC inspector verified the licensee
had responded to the event in accordance with procedures and had
notified the NRC and other agencies as required in a timely fashion.
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Engineered safety feature actuations that occurred during the report
period are listed in the table below. The NRC inspector will review the
license event report (LER) ~for each of these events and will report any
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findings in future NRC inspection reports.
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- When availability of the NRC inspector allowed observation of these
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activities.
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Summary of all ESF Actuations during June and July are listed below:
Date
Event **
Plant Status
Cause
6-2-85
CRVIS
Mode 3
Spike on radiation monitor
6-4-85
Mode 3
6-5-85
CRVIS
Mode 3
Spike on radiation monitor
6-6-85
Rx Trip
Mode 1
Lo-Lo S/G level
6-7-85
CRVIS
Mode 3
Spike on radiation monitor
6-9-85
Mode 2
Main feedwater pump trip
6-9-85
Mode 2
Hi-Hi S/G level
6-11-85
Mode 1
Hi-Hi S/G level
6-13-85
Rx Trip /AFAS
Mode 1
Lo-Lo S/G level
6-14-85
Mode 1
Hi S/G level
6-23-85
Rx Trip
Mode 1
RTB "A" accidentally opened
6-24-85
Rx Trip /AFAS
Mode 2
Lo-Lo S/G level
7-2-85
CRVIS
Mode 3
Spike on radiation monitor
7-5-85
Mode 1
Spike on radiation monitor
7-5-85
CRVIS
Mode 1
Hi-Hi S/G level
7-7-85
CRVIS
Mode 1
Spike on radiation monitor
7-8-85
CRVIS
Mode 1
Spike on radiation monitor
7-8-85
CRVIS
Mode 1
Spike on radiation monitor
7-9-85
CRVIS
Mode 1
Spike on radiation monitor
7-9-85
Rx Trip
Mode 1
Lo-Lo S/G level
7-10-85
Rx Trip
Mode 1
Lo-Lo S/G level
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7-10-85
MFIVA
Mode 2
Hi S/G level
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7-11-85
Mode 2
Hi S/G level
7-11-85
Rx Trip
Mode 1
Hi flux on IR
7-12-85
CRVIS
Mode 3
Broken detector tape
7-12-85
CRVIS
Mode 3
Spike on radiation monitor
7-12-85
CRVIS
Mode 3
Spike on radiation monitor
7-17-85
CRVIS
Mode 1
Faulty bypass switch
7-20-85
D/G Start
Mode 1
Relay accidentally bumped
7-22-85
CRVIS
Mode 1
Broken detector tape
7-23-85
Rx Trip /AFAS
Mode 1
Loss of control power
7-28-85
CRVIS
Mode 1
Spike on radiation monitor
7-31-85
Rx Trip /AFAS
Mode 1
PR HI negative rate
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CRVIS.- Control room ventialtion isolation
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AFAS - Auxiliary feedwater actuation signal
Rx Trip - Reactor trip
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MFIYA'- Main feedwater isolation valve actuation-
S/G - Steam generator-
RTB - Reactor trip breaker
IR - Intermediate range
PR - Power range
Specifics of the reactor trip and related events that occurred on
June 13, 1985, are discussed below:
At 03:45 CDT on June 13, 1985, with reactor plant power at approximately
15%, the main turbine generator was manually tripped due to excessive
vibration. Subsequent to the turbine trip at 03:53 CDT the operating
main feedwater pump 'A' tripped. The operator manually started the -
motor driven auxiliary feedwater pumps and reestablished feedwater flow
to the steam generators. When steam generator water levels continued to
decrease, the operator attemped to start the turbine driven auxiliary
feedwater pump, but it tripped on overspeed when the operator opened the
steam supply valves to the turbine out of sequence (i.e., the
trip /trottle valve was oper.ed prior to opening the main steam supply
val ve) . At 04:00 CDT a low-low level condition in steam' generator 'B'
caused a reactor trip, an auxiliary feedwater actuation, and a steam
generator blowdown and sample isolation. A feedwater isolation also
occurred due to low reactor coolant system average temperature in
conjuction with the reactor trip. At the time, the auxiliary feedwater
actuation occurred the motor driven auxiliary feedwater pumps were
already running having been manually started as described above. All
engineered safety features and reactor protection system equipment
operated per design requirements. When the operator closed the main
staam line isolation valves (MSLIV) manually in the slow-close mode to
help reduce reactor coolant syste:a cooldown, the ' A' steam generator
MSLIV failed to close. The valve closed when the operator manually went
-to the fast-close mode.
Evaluation and applicable corrective actions that were taken by the
licensee to correct the problems encountered during this event were as
follows:
The cause of the main feedwater pump ' A' trip that initiated the
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event was not identified. Prior to -restart following the trip, the
licensee tested the main feed pump and its related control circuits
for proper operation and calibration. The main feed pump was
operated for several hours while key parameters were monitored with
test instrumentation. During this operation of the main feed pucp,
no indication of a malfunction was detected. Additional test
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instrumentation for monitoring key parameters was left installed on
.the pump during subsequent operatians to trend pump performance and
help identify any malfunctions.
All' operators were instructed on the proper sequence of valve
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operations for starting the turbine driven auxiliary feedwater
pumps.
The failure of the main steam isolation valve in the slow-close
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mode was due to low hydraulic oil reservoir level caused by a
. leaking 'O' ring. The 'O' ring was replaced correcting the -
probl em.
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Th) violations or deviations were identified.
9.
Emergency Drill Observation
On June 20, 1985, the NRC resident inspectors observed an emergency
preparedness' field exercise that was conducted by the licensee. The
-purpose of the drill was to train appropriate personnel to respond to a
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radiological emergency at WCGS. The players in the drill performed the
actions they would.be required to perform in an actual event and used
emergency procedures .where appropriate to respond to the simulated
events 1that took ~ place. Appropriate Coffey County personnel also
participated in the drill and the Coffey County Response Center was
. activated. The WCGS training' simulator was used to simulate reactor
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plant conditions and responses during the accident scenario.
-The NRC inspectors observed drill activities in the technical support-
center, the emergency operations facility, and the simulator control
room.' The NRC inspector 'also attended the licensee's critique of the
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drill at its conclusion.
No violations'or deviations were identified.
10. Enforcement Conference
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On June 27,'1985, an enforcement conference with KG&E management was
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held in the NRC Region IV offices to discuss NRC concerns in the area of
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. security at WCGS. The events that generated the NRC concerns had been
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identified during an onsite visit by a Region IV security inspector and
Lby the resident: inspector. Details of. the NRC concerns were reported in
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NRC Inspection Report 50-482/85-27. Licensee representatives at the
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enforcement conference described corrective actions that were~being
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taken in the areas of concern.
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11. Allegation Followup
On June 3,1985, an anonymous alleger, via a letter, related the
following concern to.the NRC inspector:
" Rainwater flows from a manhole through conduit into the health physics
lab and if rain can flow into the lab there is.a possibility that-
radioactive substances could leak out."
The NRC inspector in following up on the above concern determined the
following from discussions with ifcensee personnel and a review of
related documents:
Rainwater did flow into the hot chemistry lab (a radiologically
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controlled area). .The flow was from a manhole through electrical
conduit.
On May 28, 1985, Plant Modification Request (PMR) No. 01023 was
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issued. This PMR recommended that the conduit-feeding into the hot
chemistry lab from the manhole be plugged (sealed).
The Plant Safety Review Committee approved PMR No. 01023 on
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May 29, 1985.
Wolf Creek WR No. 08208-85 documents completion of the sealing of
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the conduits between the manhole and the chemistry hot lab.
WR No. 08208-85 was completed on July. 22,1985.
Subsequent to the completion of the conduit sealing, health physics
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personnel performed a leak test on the hot chemistry lab and no
leaks were detected.
Chemistry department personnel stated to the.NRC inspector that the
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water no longer leaks into the chemistry hot lab.
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The NRC inspector determined from the above that the allegation was
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substantiated and that the licensee had taken 'dequate action to correct
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the problem.
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No violations or deviations were identified.
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12. Security
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The.NRC inspectors verified the physical security plan was being
implemented by observing:
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The security organization is properly manned and the security
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personnel are capable of performing their assigned functions.
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Persons within the protected area (PA) display their identification
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badges, when in vital areas are properly authorized and when
required are properly escorted.
Vehicles are properly authorized, searched, and escorted or
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controlled within the PA.
Persons and packages are properly cleared and checked before entry
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into the PA is permitted.
The effectiveness of the security program is maintained when
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security equipment failure or impairment requires compensatory
measures to be employed.
Response to threats or alarms, or discovery of a condition that
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appears to require additional precautions is consistent with
procedures and the physical security.
Selected NRC inspector comments are noted below:
On July 23, 1985, the NRC inspector observed an incident in which
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it appeared that a KG&E security officer failed to maintain control
of a nonlicensee designated vehicle (LDV) within the PA as required
by licensee procedures. Upon- further followup, the NRC inspector
determined that the security officer had maintained control as
required. The vehicle had been left unoccupied and running, but
within the line of vision of the escorting security officer. As'a
result of this incident, a meeting was held with licensee
management in which the licensee voluntarily committed to:
a.
Issue a letter that all non-LDV drivers would be required to
sign that stated the rules and regulations which the driver
would be expected to follow.
b.
Better define and proceduralize the requirements to be
followed before the driver of a non-LDV could leave his
vehicle.
c.
To investigate the desirability of further restricting the
number of vehicles which can be escorted by a security
officer.
On July 31, 1985, at approximately 6:40 a.m., the NRC inspector
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observed a contract security officer outside the door to the valve
house to the condensate storage tank apparently sleeping. The NRC
inspector requested a licensee security officer who had just exited
the turbine building to awaken the contract officer. Upon
questioning by the NRC inspector the contract security officer
admitted to being drowsy but stated she had not been asleep. A
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search of the immediate area revealed no unauthorized persons and
the contract officer was relieved of her station. The NRC
inspector verified that the area was not a vital area and that the
physical security plan did not require a security officer to be
posted at that location. The officer in question has been
counseled by her supervisors on the seriousness of being
inattentive to duty.
Since the area was nonvital the security post
was not required by procedure and it is no longer manned.
As a result of an NRC inspector's question concerning the security
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background investigation of a KG&E employee, it was determined that
licensee's procedures do not define the limits under which a
security background investigation should be performed for certain
employees under certain conditions. The licensee committed to
contact the Region IV security specialists to determine these
limits and to proceduralize them. The NRC inspector will continue
to follow this item until the limits have been identified and
incorporated into procedures. This is an unresolved item.
(50-482/8526-03)
13. Plant Tours
At various times during the course of the inspection period the NRC
inspectors conducted general tours of the reactor building, auxiliary
building, radwaste building, fuel handling building, control building,
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turbine building, and the secured area surrounding the buildings.
During the tours, the NRC inspector observed housekeeping practices,
fire protection barriers and equipment, maintenance on equipment, and
discussed various subjects with licensee personnel.
No violations or deviations were identified.
14. Exit !!eetings
The NRC inspectors met with licensee personnel to discuss the scope and
findings of this inspection on July 1 and August 5,1985. The NRC
inspectors also attended exit meetings conducted by other region based
NRC inspectors.
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