ML20056A289

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Insp Rept 50-482/90-26 on 900601-30.Violations Noted.Major Areas Inspected:Plant Status,Operational Safety Verification,Monthly Surveillance Observation,Monthly Maint Observation & Plant Startup from Refueling
ML20056A289
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 07/30/1990
From: Joel Wiebe
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20056A286 List:
References
50-482-90-26, NUDOCS 9008060301
Download: ML20056A289 (14)


See also: IR 05000482/1990026

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APPENDIX B

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION IV

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NRC Inspection Report:

50-482/90-26

Operating License: NPF-42

Docket: 50-482

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Licensee: Wolf Creek Nuclear Operating Corporation (WCN00)

P.O. Box 411

Burlington, Kansas 66839

Facility Name: Wolf Creek Generating Station (WCGS)

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Inspection At: WCGS, Coffey County, Burlington, Kansas

Inspection Conducted: June 1-30, 1990

Inspectors:

M. E. Skow. Senior Resident Inspector

Project Section D, Division of Reactor Projects

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L. L. Gundrum, Resident Inspector,

Project Section D Division of Reactor Projects

D. V, Pickett, Project Manager

Project Directorate IV Division of Reactor Projects III, IV, and V

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and Special Projects, NRR

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W. B. Jones, Senior Project Engineer

Project Section D Division of Reactor Projects

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Approved:

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T S. Wiebe, Chief, Project Section D

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ivision of Reactor Projects

Inspection Summary

Inspection Conducted June 1-30, 1990 (Report 50-482/90-26}

Areas Inspected:

Routine, unannounced inspection including plant status -

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operational safety verification, monthly surveillance observation, monthly

maintenance observation, plant startup from refueling, onsite followup of

events at operating power reactors, and review of licensee event reports.

Results: The licensee's corrective action program failed to assure that

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previous corrective actions precluded recurrence of similar events.

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was illustrated in the corrective action response to licensee event

reports (LERs)90-004 and 90-010. These LERs failed to address adequate

corrective action _for scheduling of surveillance tests (paragraph 8.a) and the

control' of troubleshooting activities (paragraph 8.b).

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0008060301 900731

PDR

ADOCK 05000482

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Plant personnel were cognizant of surveillance and corrective maintenance

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requirements. Good radiation protection support was observed during

observation of surveillance maintenance activities.

The licensee's control of

troubleshooting activities continued to be a weak area, requiring additional

licensee management oversight.

Operations personnel performed their duties in accordance with the facility

license-requirements. The inspector reviewed the licensee's reactor posttrip

evaluations from the previous inspection period.

It was identified that the-

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evaluations were not performed in accordance with the posttrip review

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procedure.

The licensee's documentation of these posttrip reviews did not

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clearly identify the root cause, nor prescribe and verify that the necessary

corrective actions have been completed (paragraph 9).

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DETAILS

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Persons Contacted

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Principal Licensee Personnel

B. D. Withers, President and CEO

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  • J. A. Bailey, Vice President, Nuclear Operations

F. T. Rhodes, Vice President, Engineering and Technical Services

  • G. D. Boyer, Plant Manager
  • R. S. Benedict, Manager, Quality Control (QC)
  • H. K. Chernoff, Supervisor, Licensing
  • M. E. Dingler, Manager, Nuclear Plant Engineering (NPE) Systems

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  • T. J. Garrett, Manager, Nuclear Safety Analysis
  • W. Goshorn, Wolf Creek Coordinator, Kansas Electric Power Company

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  • R. L. Gourley, Supervisor, Mechanical Maintenance

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  • C, W. Fowler. Manager, Instrumentation and Control (l&C)

R. W. Holloway Manager, Maintenance and Modifications

  • R. L. Logsden, Manager, Chemistry
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J. MacTaygart, NPE, Wichita

  • A. S. Mah, duelear Safety Engineering
  • T. S. Morrill, Manager, Radiation Protection
  • D. G. Mosety, Supervisor, Operations
  • W. B. Norton, Manager, Technical Support
  • C. E. Parry, Director, Quality
  • J. M. Pippin, Manager, NPE
  • C, M. Sprout, Section Manager, NPE, WCGS

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  • J. D. Weeks, Manager, Operations

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  • S. G. Wideman, Senior Licensing Specialist
  • M. G. Williams, Manager, Plant Support
  • R. T. Wright, Supervisor, QA Audit

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The inspectors also contacted other members cf the licensee's staff during

the inspection period to discuss identified issues.

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  • Denotes those personnel in attendance at the exit meeting held on June 29,

1990.

T. P. Gwynn, Deputy Director Division of Reactor Projects,. also

attended the exit.

2.

Plant Status

The plant operated at or near full power throughout the month. On June 2

9, and 23, 1990, power was reduced to 95 percent reactor thermal power

while maintenance work was performed on low pressure feedwater heater

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trains.

3.

~0yerational Safety Verification (71707)

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'.The purpose of this inspection was to ensure that the facility was being

operated safely and in conformance with license and regulatory

requirements.

It also was to ensure that the licensee's management

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control system was effectively discharging its responsibilities for

continued safe operation.

The methods used to perform this inspection

included direct observation of activities and equipment, tours of the

facility, interviews and discussions with licensee personnel, independent

verification of safety system status and limiting conditions for

operation (LCO), corrective actions, and review of facility records.

Areas reviewed during this inspection included, but were not limited to,

control room activities, routine surveillances, engineered safety feature-

operability, radiation protection controls, fire protection, security,

plant cleanliness, instrumentation and alarms, deficiency reports, and

corrective actions.

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Plant operations were generally performed in an acceptable manner.

The

inspectors noted that, in the plant cleanliness and health physics (HP)

areas, the licensee was continuing to clean up and perform decontamination

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of areas and equipment used during the refueling outage that ended in May

1990.

Equipment was being prepared for storage onsite until iequired for

the next outage. A discussion was held with the licensee concerning the

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general state of plant preservation.

The licensee stated that there'is an

ongoing long-term program in place to paint equipment and piping

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throughout the plant. This effort has been observed by the_ inspectors.

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In addition, the licensee has begun to paint some walls in the aux 1111ary

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building which would make decontamination easier in the event of a small

spill.

4.

Monthly Surveillance Observation (61726)

The purpose of this inspection was to ascertain whether surveillance of

safetj-significant systems and components was being conducted in

accordance with Technical Specification (TS). Methods used to perform this

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inspection included direct observation of licensee activities and review

of records.

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Items inspected in this area included, but were not limited to,

verification that:

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Testing was accomplished by qualified personnel in accordance with an

approved procedure;

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The surveillance procedure was in conformance with TS requirements;

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The operating system and test instrumentation was within its current

calibration cycle;

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Required administrative approvals and clearances were obtained prior

to initiating the test;

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LCOs were met and the system was properly returned to service; and

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The test data were accurate and complete and the test results met TS

requirements.

Surve111ances witnessed and/or reviewed by the inspectors are listed

below:

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STS10-913, Revision 7 " Containment Hydrogen Analyzer G5065B

Calibration Test"; and

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CHM 01-060, Revision 5, " Sampling of the Reactor Coolant System."

Selected inspector observations are discussed below:

a.

On June 7,1990, the inspector observed the performance of STS10-913

for the Containment Hydrogen Analyzer "B" train. This surveillance

is performed to verify operability of this accident monitoring

instrument as required by TS 3.3.3.6.

The I&C technicians were noted to be cognizant of the precautions and

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limitations specified in the surveillance test procedure. The

equipment was energized and maintained in standby for at least 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

prior to beginning the test.

The redundant channel was operable as

required with the reactor in Mode 1.

Prior to beginning the

surveillance test, an onshift licensed operator was n..ified of

the intent of the procedure and permission was granted by the operator

before the test was initiated.

The inspector noted that the technicians utilized test equipment

which was within its calibration test frequency.

Each required lead

was lifted in accordance with the test procedure.

In each case, the

"as found" data was within its specified tolerance range. The data

was properly recorded within the procedure,

b.

On June 8, 1990, the inspector observed the drawing of a reactor

coolant sample and subsequent sample analysis. The control room was

notified of the intent to obtain the sample. The required valve

lineup was established by the operator to allow the chemistry

technician to draw the sample. The proper radiological controls were

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in place prior to obtaining the sample.

The inspector verified that

the chemistry technician had signed the appropriate procedure.

The system was purged for greater than 30 minutes prior to drawing

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the sample. The sample hood was noted to be properly positioned and

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the ventilation system taking a suction from inside the hood.

The sample was subsequently drawn and analyzed in accordance with

the surveillance procedure. The technicians were noted to be

cognizant of the test requirements and the tests were performed in

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accordance with the procedure.

Each test result was within the

established acceptance criteria.

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The inspector noted tnt both surveillances were conducted in accordance

with the surveillance p edure by qualified personnel.

In each case, the

surveillance procedure accomplished its intended verification. A

potential violation has been identified in paragraph 8.a of this report

for tne failure to resolve surveillance test scheduling errors.

5.

Monthly Maintenance Observation (62703)

The purpose of inspections in this area was.to ascertain that maintenance

activities on safety-related systems and components were conducted in

accordance with approved procedures and TS.

Methods used in this

inspection included direct observation, personnel interviews, and records

review.

Items verified in this inspection included:

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Activities did not violate limiting conuttions for operations and

that redundant components were operable;

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Required administrative approvals and clearances were obtained before

initiating work;

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Radiological controls were properly implemented;

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Fire prevention controls were implemented;

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Required alignments and surveillances to verify postmaintenance

operability were performed;

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Replacement parts and materials used were properly certified;

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Craftsmen were qualified to accomplish the designated task and

additional technical expertise was made available when needed;

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QC hold points and/or checklists were used and QC personnel observed

designated work activities; and

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Procedures used were adequate, approved, and up to date.

Portions of selected maintenance activities regarding the work

requests (WRs) were observed. The following WRs and related documents

were reviewed by the inspectors:

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No.

Activity

WR 50882-90

Oil sample from the "B" emergency diesel generator

WR 50273-90

Perform preventive maintenance on essential service

water Valve EF HV0052

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WR 50275-90

Perform preventive maintenance on essential service

water Valve EF HV0060

WR 02895-90

Perform corrective maintenance on centrifugal charging

pump flow control Valve BG FCV121.

WR 03534-90

DRPI Data "A" failure on Rod K-10

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Selected inspector observations are discussed below:

a.

On June 1,1990, the digital rod position indication (DRPI) system

simultaneously generated a number of alarms including the rod nonurgent

alarm, rod urgent alarm, rod bottom alarm, and rod position

indication (RPI) rod deviation alarm. Upon control room

acknowledgement of the alarms, only the rod nonurgent alarm for the

K-10 shutdown rod locked in. Panel lights indicated that only the

"B" train was providing input to the DRPI system with the "A" train

input faulted.

Review of the core parameters and the demand position

indication system by the control room operators verified that rod

movement had not occurred and that the K-10 shutdown rod remained

fully withdrawn from the core. A condition referred to as " half

accuracy" existed for the DRPI system monitoring the K-10 shutdown

rod. The licensee stated that a " half accuracy" condition does not

degrade DRPI system operability and that entry into TS 3.1.3,2 is not

appropriate.

Troubleshooting by I&C personnel on June 1, 1990, resulted in

replacing the K-10 circuit card in the DRPI cabinet in containment.

Upon replacement of the circuit card, the DRPI alarm cleared on the

control room panel.

However, it was noted by the inspector that

subsequent testing of the circuit card by I&C personnel did not

identify any apparent pr +' ems.

The DRPI alarms of June I surrounding the K-10 shutdown rod were

again repeated when troubleshooting was being performed on the DRPI

cabinet in containment on June 18, 1990.

The control room operators

were not told by the-troubleshooting technicians that the alarms

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could come in, nor did the operators expect the indication and alarms

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to occur. Again the "A" train faulted and a " half accuracy" situation

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resulted in the indication for K-10 shutdown rod position, This

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failure to adequately control troubleshooting activities is a repeat

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of a similar problem identified in LER 90-010. " Technical

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Specification Violation - Simultaneous Inoperability of Two Auxiliary

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Feedwater Pumps Because of Support System Inoperability." The

corrective actions specified in the LER (described in detail in

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Section 8.b of this report) did not preclude repetition of the

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problems.

Even though the troubleshooting activity performed on

June 18, 1990, did not result in equipment inoperability, the event

illustrates that the licensee has not established the appropriate

management control of troubleshooting activities.

This event is used

as additional information which further demonstrates that the

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corrective action specified in LER 90-010 was not adequate. See

Section 8.b of this report for a description of the violation.

Following the second June 18, 1990, event, I&C personnel made a

containment entry on June 21, 1990. By disconnecting the power cable

from the K-10 circuit card at the DRPI cabinet and connecting it to a

specially designed rod position simulator, I&C personnel could

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identify whether the fault existed in cable connections between the

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control room and the DRPI cabinet or between the DRPI cabinet and the

actual K-10 rod.

The inspector obscrved the testing from the control

room. The inspector observed that operations and I&C personnel

discussed the need to maintain RPI in the control room throughout the

testing process.

In order to test the "A" train input, the control

room operators initially arijusted the DRPI mode selection switch from

monitoring both "A" and "B" train input to monitoring "B" train

only, multiple spurious ORPI alarms were generated (i.e., rod urgent

alarm, rod bottom alarm, and RPI rod deviation alarm).

However, when

the alarms were acknowledged, only the rod nonurgent alarm locked in.

General warning DRP1 alarm lights existed from all control and

shutdown rods during the testing due to the " half accuracy" condition

that existed due to isolation of the "A"

train input.

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Troubleshooting by I&C personnel using the rod position simulator

concluded that a fault existed in the power cable somewhere between

the DRPI cabinet in containment and the K-10 shutdown rod. The areas

of concern are physically located near to and behind the biological

shield wall and leads down to the reactor vessel upper internal area.

Due to as low as reasonably achievable (ALARA) considerations, the

licensee decided that further troubleshooting and entry behind the

biological shield wall would not be appropriate with the plant at

100 percent power.

Repairs to this system were deferred to the

forced outage list.

The DRPI system was returned to the " half

accuracy" condition for monitoring the K-10 shutdown rod position,

b.

WRs 50273-90 and 50275-90 were performed on June 6, 1990, to verify

proper positioning of the limit switches and to lubricate the valve

actuator including the geared limit switch.

The work was performed in accordance with approv9d WRs.

Prior to

beginning the work, the appropriate clearance w.s implemented, and

the operators entered into the required LCO for one train of

essential service water out of service.

No une;9ected conditions

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were noted by the craf tpersons or the inspector curing the

maintenance activity.

Following completion of the maintenance activity, a QC inspector

observed the setting of the limit switches. A postnaintenance test

was performed on the two valves prior to returning the system to

service.

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WR 02895-90 was performed on June 7, 1990, to repair a body-to-bonnet

1eak on centrifugal charging pump flow control Valve BG FCV121.

This valve had been worked during the previous refueling outage to

repair a similar type leak.

Prior to beginning the work, the required clearance boundaries were

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established and independently verified. A specific radiation work

permit (RWP) was initiated to identify the radiological hazards

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within the contaminated area around the valve and to specify the

necessary personnel controls. The operators followed the appropriate

LCO when the system was t en out of service.

The inspector observed that the maintenance personnel were adhering

to the RWP requirements.

HP assistance was requested.to control the

potentially contaminated water that would be released when the body-

to-bonnet was separated. The system configuration did not allow

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draining of the 1tne prior to performance of the maintenance

activity.

The potentially contaminated water was well controlled

within the designated ares.

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After removing the bonnet, the licensee identified that the gasket

was off center, resulting in the body-to-bonnet leakage. A new

gasket was installed, and the valve reassembled.

New packing was

also installed. The torquing of the bonnet to the valve body was

observed by a QC inspector. During the maintenance activity, HP

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t :hnicians surveyed the area outside the controlled contamination

area to ensure that the contaminated area was not increasing.

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valve was subsequently tested in accordance with the established

postmaintenance test.

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The licensee's performance in the area of troubleshooting continued to be

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a weakness.

The corrective maintenance activities were correctly performed

in accordance with the maintenance procedures by qualified maintenance

personnel.

6.

. Plant Startup from Refueling (71711)

In addition, the following additional procedures were. incorporated into

this inspection in accordance with Inspection Procedure 71711:

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Surveillance of Core Power Distribution Limits (61702)

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Calibration of Nuclear Instrumentation Systems (61705)

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Core Thermal Power Evaluation (61706)

The following tests for heatup, approach to critica1'ty, and core phys 4s

were witnessed and/or reviewed and found to have be9n conducted in

accordance with approved procedures:

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STS SF-003, Revision 2, " Digital Rod Position Indication Test";

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STS RE-007, Revision 4, " Rod Drop Time Measurement";

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RXE 01-002, Revision 2, " Reload Low Power Physics Testing";

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STS RE-Oll, Revision 4 and Temporary Procedure Change MI 90-491, "RCS

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  • ts1 Flow Rate Measurement";

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F a nE-013, Revision 3, "Incore-Excore Detector Calibration"; and

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STS10-201, Revision 8 and Temporary Procedure Change MI 90-516,

" Analog Channel Operational Test 7300 Process Instrumentation

Protection Set

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Primary personnel responsible for the major steps in obtaining the results

of the computer analysis code calculations from the initial incore flux

map data were interviewed. A flux map printout at greater than 50 percent

power was reviewed with the reactor engineering supervisor.

It was

verified that control rod insertions, core power level, and burnup at the

time of the flux map were part of the input to the code. The review

confirmed that all detectors independently traversed a reference

calibration instrument tube. The printout included the relative set of

measured fission rates as seen by the detector for each thimble location

following normalization.

The axial flux differences and quadrant power tilt limits were maintained

during startup.

The source, intermediate, and power range calibrations

and the incore-excore detector calibrations were performed as required.

The site reactor engineering staff were knowledgeable regarding the

computer codes being used and ADM 01-077, Revision 4, " Computer Software

Administrative Controls." The reactor engineering staff organization is

authorized by the licensee to have four people.

The staff has two

experienced engineers and one engineer being trained for the position.

One position is vacant.

The Cycle 5 reload safety evaluation was reviewed.

The current Updated

Safety Analysis Report (USAR), Revision 3, dated March 12, 1990, was

reviewed to ascertain the parameters for the previous Cycle 4,

Chapter 4,

" Reactor," still reflected the description-for Cycle 3.

Cycle 4 started

in-January 1989. This failure to update the USAR is an apparent violation

of the requirements of 10 CFR 50.71(e)(4), which requires revisions to

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the USAR to be filed annually and to reflect all changes up to a maximum

of 6 months prior to the date of filing (482/9026-03).

The licensee

revised their procedure for updating the USAR prior to the end of the

. inspection period. Because the criteria specified in Section V.A of the

Enforcement Policy was satisfied, a cited violation will not be issued.

The licensee controlled the heatup, approach to criticality, and core

physics test in e.::cordance with the approved procedures. Good

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communication between the operators and site reactor engineering staff

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was evident. The licensee's implementation of the requirements specified

in 10 CFR 50,71(e)(4) needs to be improved.

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Onsite Followup of Events at Operating Pnwer Reactors (93702)

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The purpose of this inspection activity was to provide onsite inspection

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of events at operating power reactors.

Specific inspection activities

included:

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Observing plant status;

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Evaluating the significance of the events, performance of safety

systems, and actions taken by the licensee;

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Confirming that the licensee had made proper notification of the

events and of any new developments or significant changes in plant

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conditions; and

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Evaluating the need for further or continued NRC response to the

events.

The following items were considered during the followup:

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Details regarding the cause of the event;

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renology;

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n .ctioning of safety systems as required by plant conditions;

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Radiole

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.scensee actions to correct the cause of the event; and

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ctions taken or planned prior to resumption of facility

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Selected events rec Jiring licensee event reports (LERs) that occurred

during this report seriod are listed in the table below:

Date

Event *

Plant Status

Cause

6/13/90

ESFAS

Mode 1

Loss of No. 7 transformer

(100% power)

caused loss of power to

XNB01 Class 1E transformer

6/19/90

TS violation

Mode 1

Chemistry TS action

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(100% power)

statement time limits

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6/19/90

TS violation

Mode 1

GT RE21A went into

(100% power)

accident / isolate mode

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ESFAS - Engineered Safety Natures Actuation Signal

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TS V W ica - Technical Specification Violation

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T4 mspracts verified that the licensee's initial response to these

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avens ves oppropriate.

Plant response to the initiative event was also

appropriate when applicale

The inspectors will review the LERs for these events and will report any

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findings in a subsequent inspection report.

8.

Review of Licensee Event Reports (92700) and Evaluation of Licensee

Self-Assessment Capability (40500)

a.

LER 90-004, " Technical Specification Surveillance Requirement Not

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Satisfied Because of Personnel Error in Scheduled Surveillance Test."

The corrective action was to proceduralize the requirement to check

the past due surveillance procedures inquire report (PDSIR) on a

weekly basis as a minimum. A similar commitment was made by the

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licensee in 1987.

This similar committment was documented in

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LER 87-014 to require the frequency of checking the PDSIR weekly,

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More recently, LER 89-016, issued September 8, 1989, addressed a

failure to meet a TS surveillance requirement because of an error in

scheduling. A noncited violation (482/8923-01) was issued in

1989 for-the-licensee's failure to perform the surveillance test on

schedule and enter TS 3.0.3 after discovery.

The failure to perform

the surveillance test in 1989 was due to a schedulin0 error.

The inspectors reviewed the past due surveillance report dated

June 22,'1990,.and found that it had 87 entries. The entries did not-

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accurately reflect actual cases of missed surveillance tests. The

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inspectors concluded that the POSIR has not been effective in

identifying missed surveillance tests. This appears 'o be partially

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because of the number of invalid entries in the PDSIR.

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licensee's surveillance test scheduling computer preg' Jam, which

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developes the PDSIR, does not minimize the report output sufficiently

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to allow for a simple review of missed surveillance test. The

licensee's failure to identify corrective action which would reduce

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the probability of similar events occuring in the future in

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accordance with 10 CFR 50.73 is an apparent violation (482/9026-01),

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b.

LER 90-010, " Technical Specification Violation - Simultaneous

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Inoperability of Two Auxiliary Feedwater Pumps Because of Support

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System Inoperability." At 7:32 a.m. (CDT), Emergency Diesel

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Generator "A" was removed from service for planned maintenance. This

rendered the "A" auxiliary feedwater pump (AFP) inoperable according

to TS and the appropriate LC0 was logged.

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At 3:45 p.m., it was discovered that the inspection access door

for the AFP "B" room cooler was removed, thereby rendering the "B"

AFP inoperable.

Investigation revealed that the hatch had been

removed at approximately 8 a.m.

Therefore, two AFPs had been

inoperable for a period of approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

Per TS 3.7.1.2,

the plant should have been in at least hot standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

with two AFPs inoperable.

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There were two corrective actions stated in the LER. The first

action was to convey to operations and maintenance personnel that

inspection access doors must be installed in order to ensure

operability of room coolers.

The second action was to make

maintenance personnel aware of the necessity to thoroughly discuss

troubleshooting activities in detail with the shift supervisor prior

to commencement of the activity.

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TS 6.8 requires that written procedures shall be established,

implemented, and maintained covering the applicable procedures

rcrommended in Appendix A of Regulatory Guide (RG) 1.33, Revision 2,

February 1978.

Section 9, Item a, states, " Maintenance that can

affect the performance of safety-related equipment should be properly

preplanned and performed in accordance with written procedures,

documented instructions, or drawings appropriate to the circumstance."

The next statement in Section 9. Item a, states " Skills normally

possessed by qualified maintenance personnel may not require

step-by-step delineation in a procedure."

The corrective actions stated in the LER are considered inadequate

because the administrative centrols do not require that activities

that can affect safety-related equipment or the control room

operators' ability to assess plant status be controlled with a

written procedure. A further demonstration of the inadequacy of the

corrective action specified in LER 90-010 was the inadequate control

of maintenance troubleshooting which occurred on June 18, 1990, and

is further described in Section 5.a of this report for work on the

ORPI system,

,.

If adequate corrective action'had been-taken, the potential for

io

'

operator confusion during the troubleshooting of the DRPI monitor

might have been avoided.

This is a second example of a potential

violation (482/9026-01).

The licensee's corrective action for this

'

LER and the potential violation will be reviewed by the NRC staff

'

(482/9026-01).

LER 90-10 is closed.

.

9.

Followup on a Previously Identified NRC ltem (92701)

(Closed) Unresolved Item (482/9022-02):

Posttrip Reviews - The posttrip

reviews for May 14, 17, and 19, 1990, were reviewed. Attachment A of

3

ADM 02-400, Revision 7, "Posttrip Review," was used as the basis for

'

documentation.

Section 6.5.1 states that strip-chart recordings must

accurately reflect real time to have meaningful information.

The

s

j

_ _ _ _ _ _ .

.

{e

.

.

i

14

strip-charts included in all three V p reports did not indicate real time.

Another item noted was the failure to complete Section 6 of Attachment A

for the posttrip review for the May 14, 1990, trip.

Section 6.12.1

requires that the actual or suspected cause of the trip and any abnormal

or degraded indication identified during the transient shall be documented

in Part 6 of the posttrip review report.

However, that information was

contained in other portions of the report.

In addition, the posttrip

review for the May 19, 1990, trip did not address all the actions taken to

correct the known cause of the trip as well as the actions taken to check

other similar equipment for possible generic problems.

Efforts taken by

the licensee to look for additional contributing causes were not listed

in the posttrip review. The purpose for the posttrip review, as stated in

ADM 02-200, Sections 1.1 and 2.1, is to diagnose the cause of the trip,

ascertain the proper function of safety-related and other important

equipment prior to restart, and provide a documented review of the results

that will permit a determination to be made as to the readiness of the

plant to safely return to operation.

Part of ensurir.g the plant is ready

for restart is to look for less obvious contributing causes and to ensure

that all necessary corrective actions have been completed.

Failure to

have thorough and complete posttrip reviews is a violation for failure to

follow procedure (482/9026-02).

During the review of the procedure, the following concerns were noted:

o

Section 6.13.1 states, "The maximum and minimum values of parameters

on Attachment A shall be compared with their design specification."

Part 3 of the posttrip review report is to be used to document this

safety assessment.

Part 3 of Attachment A lists the parameters and

provides columns for the minimum and maximum values.

No value for

the design specification is listed nor is there a column to document

the design value,

o

Part 3 of Attachment A lists specified parameters. There are no

additional lines to allow the documentation of any additional

parameters that the reviewer may feel are significant, such as the

. rate of increase or decrease of Tavg.

Unresolved Item 482/9022-02 is closed.

10.

Exit Meeting (30703)

The inspector met with licensee personnel (denoted in paragraph 1) on

June 29, 1990. The inspector summarized the scope and findings of the

inspection. The licensee did not identify as proprietary any of the

information provided to, or reviewed by, the inspectors. M r. T . P . Gwyn n ,

Deputy Director, Division of Reactor Projects, Region IV, also attended

the exit meeting.