ML20140E851

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Insp Rept 50-482/97-09 on 970406-0517.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support,Re Violation Which Cites Licensee Failure to Comply W/Security Escort Requirements
ML20140E851
Person / Time
Site: Wolf Creek 
Issue date: 06/06/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20140E822 List:
References
50-482-97-09, 50-482-97-9, NUDOCS 9706120221
Download: ML20140E851 (19)


See also: IR 05000482/1997009

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

50-482

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License No.:

NPF-42

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Report No.:

50-482/97-09

Licensee:

Wolf Creek Nuc' ear Operating Corporation

Facility:

Wolf Creek Generating Station

Location:

1550 Oxen Lane, NE

Burlington, Kansas

Dates:

April 6 through May 17,1997

Inspectors:

J. F. Ringwald, Senior Resident inspector

J. L. Dixon-Herrity, Resident inspector

F. L. Brush, Resident inspector, Callaway

Approved By:

W. D. Johnson, Chief, Reactor Projects Branch B

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ATTACHMENT: Supplemental Information

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9706120221 970606

PDR

ADOCK 05000482

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PDR

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EXECUTIVE SUMMARY

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Wolf Creek Generating Station

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NRC Inspection Report 50-482/97-09

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Operations

The inspector identified a violation of Technical Specifications after noting a

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significant amount of debris in containment that the licensee failed to identify or

remove following Thermolag replacement in September 1996. The inspector

identified another violation of Technical Specifications after noting that the shift

supervisor failed to comply with the procedure for evaluating Technical Specification

operability (Section 04.1).

Licensee corrective actions in response to a failure of a containment isolation valve

were inadequate, resulting in a cited, licensee-identified violation (Section 08.3).

The inspector noted that the licensee's reliance on individual operator actions to

prevent operator distractions resulted in instances where operators did not

continuously monitor the control boards (Section 01.1).

Maintenance

The inspector identified deficient work planning and scheduling associated with a

preventive maintenance air filter replacement (Section M1.3).

The licensee identified and reported a noncited violation in Licensee Event

Report (LER) 50-482/96-003, resulting from the failure to maintain containment

closure during fuel movement (Section M8.3).

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The inspector identified a violation when operations personnel misunderstood

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engineering guidance and issued a general operating procedure with incorrect

guidance for cold overpressure mitigation for the normal charging pump

(Section E8.5).

Plant Support

A violation occurred when more than five visitors were escorted into vital areas by

only one security escort on multiple occasions without the permission of senior

licensee management. The generic f ailure of the escorts, security officers, and

control room personnel to be knowledgeable of and to enforce the escort ratio

requirements was a weakness.

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While a high integrity container rigging evolution was properly controlled and

posted, the inspector identified a weakness in the pre-evolution brief because the

brief failed to include contingencies for communication failures. This is significant

since radio communication to the crane control operator was, subsequently, lost

(Section S4.1).

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Report Details

Summarv of Plant Status

The plant operated at essentially 100 percent power throughout the inspection period.

1. Operations

01

Conduct of Operations

01.1 Operator Distractions

a.

Inspection Scope (7170Z1

The aspector reviewed operator practices regarding distractions in the control

room.

b.

Observations and Findinos

As part of a review of industry events involving operator distractions, the inspector

questioned several operators regarding their individual and crew practices for

dealing with distractions, particularly while engaging in critical tasks where an

operator distraction could have significant consequences, e.g., adding positive

reactivity, filling a contaminated tank, partially draining an operating system, etc.

The inspector questioned operators on four of the six operating crews. Operator

responses to these questions were quite varied. None of the answers suggested

that there was a standard practice offered, as part of management expectations or

from training, regarding how operators were to deal with distractions. While some

operators suggested that they had thought of some techniques to ensure that

distractions would not affect their operations, the majority of responses simply

indicated that operators would attempt to limit the impact of distractions on their

individual activities.

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From a crew perspective, the answers were just as varied. Crews did not describe

expectations or practices that would enable the crew to protect an individual

operator from distractions during critical tasks. Some operators and crews

discussed the possible use of followup buttons and some operators suggested that

they might attempt to help other operators respond to telephone calls, etc. while

they were involved in critical tasks. However, the crews did not demonstrate a

consistently effective method of dealing with distractions that would ensure that

they would not impact operations.

On May 8,1997, the inspector observed control room activities continually from

8:09 a.m. until 9:39 a.m. During this period, the inspector noted that operators

generally maintained effective control board awareness. On one occasion, an

operator escorting a tour group called and asked the supervising operator if a

proposed control room tour would distract operators. However, on two occasions,

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external demands for operator attention caused the supervising operator and both

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reactor operators to be distracted at the same time. On one occasion, this period

extended for 4 minutes. During this 4-minute period, one of the external

distractions involved an off-shift senior reactor operator engaging the secondary

operator in a lengthy conversation.

c.

Conclusions

The inspector concluded that operators relied solely on their individual ability to

prevent distractions from affecting them during critical tasks. While management

generally expected operators to maintain control board awareness, operators had no

specific operating practices that would assist them in ensuring that distractions

would not affect critical tasks. On one occasion, the inspector observed all

operators in the control room become involved in distracting activities for a period

of 4 minutes.

04

Operator Knowledge and Performance

04.1 Containment Cleanliness

a.

Insoection Scoce (71707)

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The inspector accompanied licensee personnel during an at-power containment

entry. The inspector reviewed the material and housekeeping condition of the

containment.

b.

Observations and Findinas

On April 30,1997, the inspector noted a significant amount of trash and debris on

the 2026 foot elevation of the containment. The trash and debris consisted of small

wire, pieces of Thermolag and Darmat insulation material, duct tape, a small tube of

silicone lubricant, and similar items. The items had the potential, during a design

basis accident, to be transported to the containment sump and affect the

emergency core cooling system pump suctions. The licensee completed a detailed

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inspection of containment and removed debris that had the potential to cover

approximately 180 sq. in. of the inner screen of the containment sump. The

engineer evaluating the event determined that the debris could increase inner screen

blockage up to 1.9 percent. Design basis allows for up to 50 percent blockage of

both screens without effect on the net positive suction head of the pumps. The

licensee determined that this increase would not have caused any restriction of the

pump suctions during loss of coolant accident conditions.

The licensee concluded that most of the trash and debris was generated during the

Thermolag replacement effort during September 1996. The licensee had completed

a containment closecut inspection after the work was complete as required by

Procedure STS EJ-001, " Containment inspection," Revision 9. Step 8.1.1 of this

procedure required that the licensee verify by visual inspection that no loose debris

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was present in containment. The licensee subsequently performed a number of

routine containment entries and completed the required containment closecut

inspection. During these containment closecut inspections, the licensee failed to

identify and remove the debris. The failure of the licensee to remove the debris

from the containment is a violation of Technical Specification 6.8.1.a

(50-482/9709-01).

The inspector noted that the licensee had installed covers on the fire hose stations

in containment. The licensee stated that the covers were installed during Refueling

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Outage Vil during the Autumn of 1994. Licensee personnel immediately performed

a detailed walkdown of containment and removed covers from 13 fire hose stations.

Each cover had approximately 12 square feet of material.

During a loss-of-coolant condition, the covers potentially could be transported to the

containment recirculation sumps. The licensee initiated Performance improvement

Request (PIR) 97-1278 and Reportability Evaluation Request 97-032 to evaluate the

past operability issues. The inspector will review this evaluation when it is

complete and Unresolved item 50-482/9709-02 will track this issue.

After identifying the debris, the inspector informed operators of the concern

regarding the debris in containmern. The shift supervisor logged the concern at

12:20 p.m. on April 30,1997. However, the shift supervisor did not document any

consideration of the impact of the debris on the operability of the sumps until

2:30 p.m. Neither of these log entries provided a basis for an operability decision,

and the shift supervisor did not complete Form APF 26C-004-001, " Technical

Specification Operability Screening Checklist," required by Step 6.1.2 of

Procedure AP 26C-004, " Technical Specification Operability," Revision O. The

failure of the shift supervisor to log the justification of the operability determination

ani complete Form APF 26C-004-001 is a violation of Technical

Srecification 6.8.1.a (50-482/9709-03).

The licensee's response to Violation 50-482/9621-05 stated, "The operations

manager expects that log entries will be detailed and able to support any

conclusions reached. To correct this problem, Administrative

Procedure AP 26C-004, ' Technical Specification Operability,' was revised to clearly

reflect that a detailed log entry will be made by the shift supervisor whenever the

shift supervisor records a decision concerning operability. This detailed log entry

willinclude the basis for the operability decision." The failure of the shift supervisor

to implement these corrective actions resulting from Violation 50-482/9621-05

suggests that the corrective actions for this problem were not fully effective.

c.

Conclusion

The inspector identified a violation associated with the failure of the licensee to

identify and remove debris from the containment. The inspector identified a second

violation associated with the shift supervisor not complying with the procedure for

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evaluating the Technical Specification operability associated with the debris and

other matenal found in containment. Immediate licensee corrective actions to

rerlove the debris and other material from containment were appropriate. An

uniesolved item will track the review of the impact of all material removed from

cor tainment on the past operability of the containment sumps.

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Miscellaneous Operations issues (92901,92700)

08.1 (Closed) Violation 50-482/9618-03: Violation of Technical Specification 3.9.4

(containment penetration open during core alterations). The corrective actions

taken in response to this event as described in LER 96-005 were not adequate

because the licensee failed to identify two additional procedures that would allow a

similar event to occur. The licensee verified that no additional procedures could

allow the event to occur and revised the two procedures identified. The errors

associated with the initial root cause evaluation were discussed with the operations

support staff. In addition to these corrective actions, the licensee recognized a

trend in the failure to completely address the root cause and identify effective

actions in response to LERs96-004 and 96-005. PIR 96-2592 was issued to

address this trend. The corrective actions in response to this included forming a

formal corrective action review board chaired by the Chief Operating Officer. This

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board will review the root cause determination and corrective action plan for all

significant PIRs. Organization changes were implemented to provide operations

personnel to support the corrective action process. Additional training was provided

for managers and personnel implementing the corrective action program. The

inspectors concluded that the licensee's subsequent corrective actions were

appropriate.

08.2 (Closed) Violation 50-482/9618-04 and LER 50-482/96007-01 Surveillance

required to be performed while shutdown performed 3t power. The inspector

verified the corrective actions described in the licensee's response letter, dated

February 14,1996, to be reasonable and complete with the excedon that the

response stated that this event was self-discovered. While the inadequate

postmodification testing was self-discovered, the fact that the surveillance testing

was performed at power and was required to be performed while shutdown was

identified by the inspector. Supplement 1 to LER 50-482/96007-01 addressed the

aspect of performing the additional testing at power when Technical Specifications

required them to be performed while shutdown. The root cause and corrective

actions reported were consistent with the response to this violation, and no

additional issues were identified. The licensee subsequently identified additional

examples as reported in LER 50-482/97-001. The inspector concluded that the

additional examples would not have reasonably been expected to have been

prevented by lessons learned from this violation. The root cause and corrective

actions for these additional examples will be reviewed during the review of the

LER 50-482/97-001.

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08.3 (Closed) LER 50-482/96-010: Failure of motor-operated Valve EF HV0034, "ESW 8

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to Containment Air Coolers." This report documents the failure of the valve to

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close during routine valve testing. The licensee determined that the root cause was

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inadequate pretensioning of the torque switch contact finger. The valve actuator

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had been replaced in response to a different concern during March 1996. The

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licensee determined that the Valve Operation Test and Evaluation System (VOTES)

test results after the replacement reflected the inadequate pretensioning and that

they had a previous opportunity to identify the problem after a similar failure that

occurred on July 28,1996. The licensee attributed the failure to three individual

failures: (1) lack of proper torque switch contact finger tension; (2) the failure to

identify or correct the problem during tne July 28,1996, event; and (3) the failure

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to identify the problem during VOTES testing on March 10,1996. Past similar

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f ailures causing confusion, a lack of a questioning attitude, inadequate maintenance

procedures, and a backlog of work for the motor-operated valve engineer were cited

as contributing factors.

The corrective actions taken by the licensee included: correctly pretensioning the

torque switch contact finger on the valve actuator, verifying that the VOTES test

data for all similar valves did not contain similar indications, revising the three

affected procedures, and developing a plan to eliminate the backlog of motor-

operated valve related work.

The inspector noted that the initial submittal of the LER identified that the hcensee

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was not in compliance with Technical Specification 3.7.4. The inspector identified

the licensee's failure to enter Technical Specification 3.6.3 in NRC Inspection

Report 50-482/96-18. This concern was discussed with the licensee at the exit

meeting on October 18,1996. The inspector discussed the failure to address the

f ailure to meet Technical Specification 3.6.3 in the LER with the licensee. As a

result, the licensee revised the LER to identify Technical Specification 3.6.3. The

licensee documented this failure in the response to Violation 50-482/9704-01,

dated April 23,1997. The root cause identified for this failure was an incomplete

investigation of PIR 97-2528 due to inadequate interface among organizations. The

operations department was not given an opportunity to provide input to the

evaluation. The corrective action review board discussed in Section 08.2 was not

in existence when the PIR was evaluated. Procedure AP 28A-001, " Performance

improvement Request," Revision 7, was to be revised to provide guidance for when

a multidiscipline team approach should be used to perform evaluations of significant

PIRs.

The inspector reviewed the LER and found that it did not adequately address the

f ailure of personnel to initiate a PIR, as documented in NRC Inspection

Report 50-482/96-18. The LER identified a lack of a questioning attitude, but did

not address the failure to initiate a PIR. PIR 96-2528, which was initiated to

perform a root cause analysis, indicated that a PlR was not initiated because

PIR 95-2502, which documented a similar issue, had not been closed.

Procedure AP 28A-001, " Performance improvement Request," requires that a PIR

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be written for problems or potential problems (equipment operation that does not

occur as required). The inspector discussed the event with an engineer in the plant

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trending and evaluation group. The engineer explained that, because PIR 95-2502

had already been evaluated and the corrective action taken, a similar event could

not be added and that a new PIR had to be written. The inspector discussed the

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failure to write a PIR with the manager of support engineering. The manager agreed

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that PIR 96-2528 did not address the failure to write a PIR and verified that no

corrective action had been taken to address this concern.

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The inspector concluded that the licensee failed to completely understand the event

and that the root cause and corrective actions taken failed to address the failure of

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licensee personnel to follow procedures for problem identification. The failure to

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maintain motor-operated containment isolation Valve EF HV0034 operable is a

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violation of Technical Specification 3.6.3 (50-482/9709-04).

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11. Maintenance

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Conduct of Maintenance

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M1.1' General Comments on Maintenance Activities

a.

Insoection Scoce (62707)

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The inspectors observed all or portions of the following work activities.

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Task 33

install motor alignment jack bolt lugs

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on Safety injection Pump A

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115516

Task 2

Repair Centrifugal Charging Pump A

oil reservoir top gasket leak

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119029

Task 1

Replace air filter on

Damper GK HZO184E

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119886

Task 1

Megger test of Centrifugal Charging

Pump A

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119894

Task 1

Lubricate breaker for Residual Heat

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Removal Pump A

119894

Task 2.

Instrumentation and control

postmaintenance testing for Residual

Heat Removal Pump A breaker

119895

Task 1

Lubricate breaker for Centrifugal

Charging Pump A

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b.

Observations and Findinns

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Except as noted in Section M1.3, the inspectors found no concerns with the

maintenance observed.

c.

Conclusions

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Except as noted in Section M1.3, the inspectors concluded that the maintenance

activities were being performed as required,

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M1.2 General Comments on Surveillance Activities

The inspectors observed all or portions of the following surveillance activities.

a.

Inspection Scope (61726)

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STS EF-001, Revision 7

Essential service water valve check

STS EJ-100A, Revision 19

Residual heat removal system inservice

Pump A test

STS EN-100A, Revision 11

Containment Spray Pump A inservice pump

test

STS IC-209B, Revision 6

4 kV degraded voltage trip actually device

operational Test NB02 bus separation

Group 4

STS SE-001, Revision 21

Power range adjustment to calorimetric

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b.

Observations and Findinas

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The inspectors found no concerns with the surveillances observed.

c. Conclusions

The inspectors concluded that the surveillance activities were being performed as

required.

M1.3 Ventilation Damoer Preventive Maintenance

a.

inspection Scoce (62707. 37551)

The inspector observed the initial approvals and performance of the preventive

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maintenance task to replace the air filter supplying control building isolation damper

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Actuator GK HZ-184E.

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b.

Observations and Findinas

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On April 22,1997, the inspector observed instrument and controls technicians sign

onto Work Package 119029, Task 1, to replace the air filter supplying

Actuator GK HZ-184E. The technicians asked the superintendent, central work

authority, if a risk assessment had been completed for this work. The

superintendent responded by saying that, since the work was on the schedule, it

had been evaluated during the risk assessment for all scheduled work. The

technicians then questioned why the fan was still running and asked how the fan

was to remain inoperable during their work to prevent equipment damage. The

superintendent recognized that a clearance order was needed to protect the damper

and told the technicians that a clearance order would be prepared to support this

work. The inspector reviewed the work package and noted that the planner had not

identified that a clearance order would be needed in order for the technicians to

perform this work.

While personnel prepared the clearance order, the technicians walked down the

work area and noted that the scaffolding had a "Do Not Use" tag on it. They

questioned maintenance support personnel who replied that the use of this scaffold

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was awaiting an inspection by engineering personnel, and this had not been

acamplit.hed yet due to scheduling problems.

After resolving the clearance order and scaffolding issues, the technicians

completed the work without further planning or scheduling problems.

c.

Conclusions

The inspector concluded that the planning for this task was deficient in that the

planner and package rev; ewers failed to recognize the need for a clearance order.

The scheduling of this work was also deficient in that the work was scheduled to be

performed prior to the completion of the scaffold preparation.

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Miscellaneous Maintenance issues (92902,92700)

M 8.1 (Closed) Insoection Followup Item 50-482/9612-01: Protection set test jacks. This

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item involved problems with secure connections between test leads and protection

set test jacks during the performance of surveillance testing. As a result of the

inspector's observations, the licensee inspected the test leads, replaced any suspect

test leads, and initiated Work Request 113992 to inspect the test jacks on every

card in the protection sets. During the performance of Work Request 113992,

technicians identified every worn test jack. With this data, the licensee initiated

Work Requests 117657,117662,117664, and 117666 to replace every identified

worn test jack during Refueling Outage IX. In addition, this issue was discussed

with allinstrumentation and controls technicians during shop discussions and

reinforced the management expectation that technicians be particularly sensitive to

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test jack continuity during surveillances performed prior to Refueling Outage IX.

The inspector concluded that the licensee's response to this issue was appropriate.

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M8.2 (Closed) Violation 50-482/9614-03: Safety-related ::witchgear breaker cubicle door.

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The inspector verified the corrective actions described in the licensee's response

letter, dated November 5,1996, to be reasonable and complete. No similar

problems were identified.

M8.3 (Closed) LER 50-482/96-003: Failure to maintain containment closure. This item

involved the licensee's discovery that workers failed to secure a blind flange which

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replaced a main steam safety valve during refueling and, therefore, failed to

maintain containment closure required by Technical Specification 3.9.4. The

licensee identified the root cause as insufficient work package guidance and a

contributing cause as work planners not having standard procedural guidance for

what constituted effective containment closure. While the work package planner

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was aware that the flanges were for containment closure, the work package only

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stated that these flanges were for foreign material exclusion. Corrective actions

included establishing effective containment closure, revising the affected work

package and all related work packages to clearly identify that the flanges are to be

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for containment closure with specific guidance on how to install them, training of

the maintenance planners on containment closure requirements, and the

incorporation of clear guidance into licensee procedures to provide a clear standard

for what will constitute effective containment closure in the future. The failure of

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the licensee to maintain containment closure during refueling is a violation of

Technical Specification 3.9.4. This licensee-identified and corrected violation is

being treated as a noncited violation, consistent with Section Vil of the NRC

Enforcement Policy (50-482/9709-05).

M8.4 (Closed) Violation 50-482/9614-01: Simultaneous maintenance on motor-driven

auxiliary feedwater pump Trains A and B. The inspector verified the corrective

actions described in the licensee's response letter, dated November 5,1996, to be

reasonable and complete. No similar problems were identified.

M8.5 (Closed) Violation 50-482/9614-02: Clearance order hung on a molded case

breaker without a secured lock hasp. The inspector verified the corrective actions

described in the licensee's response letter, dated November 5,1996, to be

reasonable and complete. No similar problems were identified.

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E8

Miscellaneous Engineering issues (92903)

E8,1

(Closed) Inspection Followuo item 50-482/9603-13: Auxiliary boiler reliability. This

item was left open because a fuel oil transfer pump removed from service for

corrective maintenance on October 31,1996, was still out of service on

January 11,1997. The pump bearings and mecMnical seal were replaced and the

pump was returned to service on February 25,1997. The remaining activities to

improve the reliability of the auxiliary boiler are still planned as described in NRC

Inspection Report 50-482/96-24.

E8.2 (Closed) Inspection Followun item 50-482/9612-03: Turbine-driven auxiliary

feedwater pump dropping resistor f ailure. This item was opened to review the root

cause analysis and corrective actions taken in response to repeat resistor failures.

The inspector reviewed the root cause analysis and the corrective actions taken.

The resistor failed because the heat sink body for the resistor was not properly

drilled during the manufacturing process. This prevented adequate heat transfer in

the resistor. The licensee noted that this problem could not have been identified

during receipt inspection. The corrective actions included upgrading the resistor to

a 250 watt resistor in lieu of 72 watts to provide excess heat dissipation and

increasing the receipt acceptance criteria to include load testing at twice the

expected normal load.

E8.3 (Closed) Insoection Followuo item 50-482/9618-06: Fuel building concrete

degradation. The licensee identified that a small piece of concrete had broken off of

one of the corbels that support the fuel building crane. The licensee identified that

it occurred due to spalling. The licensee determined that, during plant construction.,

the form used for the concrete pour had separated. Following the pour, the excess

concrete was removed by grinding. The licensee stated that the grinding likely

initiated a weakness in the corner. Also, fuel building crane operation imparted

some vibrations into the concrete. The comoination of the two weakened the piece

and caused the spalling. The licensee stated that the spalling did not affect the

structural integrity of the corbel. Additionally, since the corbel was not in the

vicinity of the spent fuel pool, there was no concern with concrete falling into the

pool. During walkdowns, neither the inspector nor licensee personnel identified this

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condition in locations where the concrete could fallinto the spent fuel pool.

E8.4 { Closed) Violation 50-482/9618-07: Inadequate postmodification test. The

inspector verified the corrective actions described in the licensee's response letter,

dated February 14,1996, to be reasonable and complete. No similar problems

were identified.

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E8.5 (Closed) Unresolved item 50-482/9704-05: Cold overpressure mitigation related to

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the normal charging pump installation. This item involved the failure of operations

support personnel to implement procedural guidance for cold overpressure

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mitigation for the normal charging pump in a manner that was consistent with the

assumptions and guidance provided by engineering. Specifically,

Procedure GEN 00-006, " Hot Standby to Cold Shutdown," Revision 36, permitted

operators to operate the normal charging pump with reactor coolant system

temperature as low as 325 F. Design Change Package 4590 indicated that the

normal charging pump was to be placed in pull-to-lock whenever operators operated

the plant in the low-temperature overpressure protection mode. Engineering and

operations personnel both knew that low-temperature overpressure protection mode

meant 368 F. Engineering used this terminology so that the guidance would be

accurate even when future coupon sample analyses result in future changes in the

temperature where cold overpressure mitigation is required. Without clarifying the

point with design engineering personnel, operations support personnel assumed the

allowance that permitted the positive displacement charging pump to be operated as

low as 325 F also applied to the normal charging pump. PIR 97-0439 addressed

this issue and documented that this concern was determined to have occurred due

to poor communications between operations and design engineering. However, the

only corrective actions identified in PIR 97-0439 were the revision of all affected

procedures and the inclusion of this closed PIR in required reading for operations

support personnel. When the inspector questioned why the PIR corrective actions

failed to address the identified concern, engineering personnel responded that this

was not required for nonsignificant PIRs. The inspector acknowledged that the

program did not require a detailed root cause determination and corrective actions

to address the root cause for nonsignificant PIRs, yet noted that corrective actions

that failed to address identified concerns were ineffective in resolving the issue.

The failure of operations personnel to establish Procedure GEN 00-006 in

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accordance with the guidance provided by engineering is a violation of Technical Specification 6.8.1.a (50-482/9709-06).

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IV Plant Support

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R1

Radiological Protection and Chemistry Controls

R 1.1

Hiah Intenrity Cpntainer Manioulation

a.

Insoection Scooe (71750)

The inspector observed the movement of a high integrity container filled with

approximately 90 cubic feet of low-speUfic activity spent resin.

b.

Observations and Findinas

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On April 22,1997, health physics technicians moved a high integrity container from

the solid radwaste disposal with segmented shield area to high level storage in the

radwaste building. The evolution was controlled and all workers involved with the

move knew which technician was leading the evolution. Radiation area postings

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were adequate to provide proper warning to other workers not involved in the

evolution, and appropriate public address announcements were made to caution

workers to avoid unnecessary entry into the area during the move. Two health

physics technicians were stationed in the radwaste building in areas where they

could monitor the changing dose level, and they monitored radiation levels in a

sufficient number of different locations to ensure that the adjacent areas remained

properly posted.

The crane operator and lead technician had a remote indication that displayed the

height of the grapple, but did not have the height of the high integrity container and

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sling immediately available. Therefore, the crane operator and lead technician could

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not use the remote indication to determine how much clearance there was between

the bottom of the high integrity container and other objects that it could contact

during the move. Since the cameras dit. not clearly display this clearance, the crane

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operator relied on communication with t;,e lead health physics technician controlling

the overall evolution in order to ensure that there was adequate clearance between

the bottom of the container and the wall, floor, or other objects.

The lead health physics technician directed the evolution from the field using a

wireless radio headset to communicate with the crane operator. The transceiver

and battery pack were clipped to the lead technician's safety harness. Because the

safety harness straps were larger than the belt clip, the lead technician had

difficulty keeping the transceiver clipped to the harness. At one point, another

technician informed the lead health physics technician that the transceiver was

,

unclipped. A few minutes later, the inspector observed the transceiver become

unclipped and fall to the concrete floor.

The inspector asked the radwaste supervisor how the prejob briefing dealt with

potential communication difficulties between the cranc operator and the lead health

physics technician. The supervisor replied that all the technicians knew to stop the

job if communications failed, but that the pre-evolution briefing did not specifically

address contingency plans associated with a communications failure.

The inspector reviewed the certificate-of-compliance and operating instructions from

the vendor of the high integrity container and determined that the rigging evolution

complied with the requirements and limitations of the vendor documents.

c.

Conclusions

The rigging evolution was properly controlled, met vendor requirements, was

adequately posted, and was performed with good radiation exposure control. The

inspector noted one weakness in that health physics technicians did not specifically

discuss preplanned contingencies for a possible communications failure during the

pre-evolution briefing. The inspector also observed that the crane operator did not

have information readily available that permitted remote monitoring of the clearance

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between the bottom of the high integrity container and the floor, wall, or other

object that it could contact during the fift.

Security and Safeguards Staff Knowledge and Performance

S4

S4.1 Excessive Vital Area Visitor-Escort Ratio

Lnj;pection Scopo (71750)

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a.

The inspector reviewed the circumstances surrounding the identification that

security escorts exceeded the visitor-to escort ratio required by the security plan.

b.

O_bservatens and Findinas

On May 8,1997, one tour group consisting of an escort and six visitors toured the

control room. Despite the fact that the group was relatively large, the control room

The

operators were not sensitive to the site's 5:1 escort ratio requirement.

inspectors later observed one tour group leaving another vital area and asked the

escort what the escort-to-visitor limits were. The escort said that the limit was ten

The inspectors observed another tour group and asked the

visitors per escort.

second escort the same question. The escort said that the ratio limit was six

visitors per escort in vital areas, but was five visitors per escort in the control room

and this was the reason why the second tour group did not visit the control room.

The inspectors then asked two security guards the same question and were told

that the 5:1 ratio requirement only applied in the radiologically controlled area, an

incorrect understanding of the escort requirements. The inspector subsequently

informed the security superintendent of these findings. The security operations

supervisor later informed the inspector that security personnel had initiated

significant PIR 97-1358, Safeguards Event Log Entry 53, and incident

Report 5-8-1219.

Security Procedure SEC 01202, " Personnel Access to Protected Area,"

Revision 31, Step 6.5.2.6, required the visitor-to escort ratio to be no more than

10:1 in the protected area and 5:1 in vital areas, unless prior permission had been

The f ailure of more than one escort to

obtained from senior licensee management.

comply with the security procedure requirements is a violation of Technical Specification 6.8.1.c (50-482/9709-07).

c.

Conclusions

A violation occurred when more than five visitors were escorted into vital areas by

only one security escort on multiple occasions without the permission of senior

The generic f ailure of the escorts, security officers, and

licensee management.

control room personnel to be knowledgeable of and to enforce the escort ratio

requirements was a weakness,

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>

V. Manaaement Meetinas

X1

Exit Meeting Summary

,

The inspectors presented the inspection results to members of licensee management at the

,

conclusion of the inspection on May 20,1997. The licensee acknowledged the findings

presented.

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The inspectors asked the licensee whether any materials examined during the inspection

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should be considered proprietary. No proprietary information was identified.

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ATTACHMENT

SUPPLEMENTAL INFORMATION

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

C. W. Fowler, Manager, Integrated Planning and Scheduling

O. L. Maynard, President and Chief Executive Officer

B. T. McKinney, Plant Manager

R. Muench, Vice President Engineering

W. B. Norton, Manager, Performance Improvement and Assessment

R. L. Sims, Manager, System Engineering

C. C. Warren, Chief Operating Officer

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INSPECTION PROCEDURES USEC_

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IP 37551

Onsite Engineering

,

IP 61726

Surveillance Observations

IP 62707

Maintenance Operations

IP 71707

Plant Operations

IP 71750

Plant Support Activities

IP 92700

Onsite Follow-up of Written Reports of Nonroutine Events at Power

Reactor Facilities

IP 92901

Followup-Plant Operations

IP 92902

Followup - Maintenance

IP 92903

Followup - Engineering

ITEMS OPENED. CLOSED. AND DISCUSSED

Opened

50-482/9709-01

VIO

Failure to remove debris from containment

(Section 04.1)

50-482/9709-02

URI

Fire hose station covers (Section 04.1)

50-482/9703-03

VIO

Operability evaluation for debris in containment

(Section 04.1)

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50-482/9709-04

VIO

Failure to maintain motor-operated containrnent valve

operable (Section 08.3)

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50-/482/9709-06

VIO

Cold overpressure mitigation related to the normal

charging pump installation (Section E8.5)

50-482/9709-07

VIO

Excessive vital area visitor escort ratio (Section S4.1)

Closed

50-482/96 003

LER

Failure to maintain containment closure (Section M8.3)

50-482 f 96-007-01

LER

Surveillance required to be performed while shutdown

performed at power (Section 08.2)

50-482/96-010

LER

Failure of motor-operated Valve EF HV0034

(Section 08.3)

50-482/9603-13

IFl

Auxiliary boiler reliability (Section E8.1)

50-482/9612-01

IFl

Protection set test jacks (Section M8.1)

50-482/9612-03

IFl

Turbine-driven auxiliary feedwater pump dropping

resistor failure (Section E8.2)

50-482/9614-01

VIO

Simultaneous maintenance on motor-driven auxiliary

feedwater pump Trains A and B (Section M8.4)

50-482/9614-02

VIO

Clearance order hung on a molded case breaker without

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a secure lock hasp (Section M8,5)

50-482/9614-03

VIO

Safety-related switchgear breaker cubicle door

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(Section M8.2)

50-482/9618-03

VIO

Violation of Technical Specifications 3.9.4

(Section 08.1)

50-482/9618-04

VIO

Surveillance required to be performed while shutdown

performed at power (Section 08.2)

50-482/9618-06

IFl

Fuel building concrete degradation (Section E8.3)

50-482/96'i8-07

VIO

Inadequate postmodification test (Section E8.4)

50-482/9704-05

URI

Cold overpressure mitigation related to the normal

charging pump installation (Section E8.5)

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Ooen and Closed

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50-482/'s709 05

NCV

Failure to maintain containment closure (Section M8.3)

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