ML20112E128
| ML20112E128 | |
| Person / Time | |
|---|---|
| Site: | Neely Research Reactor |
| Issue date: | 06/20/1972 |
| From: | Kirkland R Neely Research Reactor, ATLANTA, GA |
| To: | US ATOMIC ENERGY COMMISSION (AEC) |
| Shared Package | |
| ML20112E009 | List: |
| References | |
| NUDOCS 9606050158 | |
| Download: ML20112E128 (2) | |
Text
.o
-,)-
4 s..
-~-
,-,y-,y-
~
ATLANYA. GEORGIA $0332:me (404) 8734211 Nuclear and Biological Sciences Division June 20, 1972 U. S. Atomic Energy Commission Division of Reactor-Licensing Washington, D. C.
20545
Reference:
Docket 50-160
~
Subject:
Primary Coolant Leakage Gentlemen:
This letter is to inform you of an incident at the Georgia Tech Research Reactor involving a leak in the D 0 primary coolant system and its subsequent a
interim repair.
On February 23, 1972, a small pinhole leak was fou-d at a weld on the primary coolant system.
This weld is the seal between the reactor coolant outlet line and a 3/4-inch level sensing line that penetrates the reactor outlet line.- The aluminum weld was peened and the leak was stopped.
The estimated D 0 loss was 75 lbs.
2 On February 21, 1972, the reactor was not operated. During both the 7 to 3 and the 3-11 shift, the crew were engaged in preventive maintenance work in the reactor containment building. Personnel on the 7-3 shift entered the pipe tunnel and found, on the floor, part of a split packing follower flange from the gasketed seal between the primary coolant outlet line and the graphite space surrounding the vessel.
The crew replaced the split flange. Immediately below the flange, a 3/4-inch aluminum pipe penetrates the primary-coolant outlet line. The 3/4-inch line runs up inside the outlet line to a point inside and at the bottom of the reactor vessel; it provides the liquid ac"high" side signal'to a differential pressure transducer for sensing reactor vessel level.
We believe that, during the installation of the split flange, stress was applied to the adjacent 3/4-inch line which subsequently resulted in the opening of a smalla p'ia' hole leak in the weld.
The pipe tunnel was not entered again until two days later prior to a normal reactor startup. At this time the leak was detected.
Several repair alternatives were considered as well as the operating conditions of the system at the location of the leak.
System. pressure is approximately 7-9 psi and operating temperature is 85-95 F.
It was decided that an attempt would be made to carefully peen the soft aluminum and close up the pinhole.
This was subsequently done. This repair is not considered to be the final solution to the problem but only an interim measure. After stepping the leak, a special " collection cone" and leak sensing 9606050158 960524 PDR ADOCK 05000160 l
H PDR
~ ~ ~ ~ " ~ "
U.-S. Atomic Energy Commissica Peg 2 2
-......... -.... ~. ~
~... - -. -..... _. _ ~.
l Juns 20, 1972 1
)
i.
i device was attached to the primary coolant line to detect any leakage. This leak detection system has been tested and shown to work satisfactorily. Initially on l
a daily basis, the pipe tunnel and weld were visuolly checked before startup and following shutdown of the reactor. This frequency has now been reduced to a weekly check.
I i
When the conversion of the plant for 5MW operation is done, there is work scheduled to be performed in the pipe tunnel involving the primary coolant lines. Our current plans are to incorporate final repair to the D 0 leak until a
that time when the fuel is unloaded from the core and the vessel and line are drained. We currently anticipate an ammendment to our license permitting con-version of the reactor to be approved in September, 1972.
Should you require any additional information on the above, please advise me.
i l
Sincerely yours, l
/
i R. S. Kirkland Reactor Supervisor l
i I
RSK:bc cc: Nuclear Safeguards Consnittee Control Room File i
i l
8 s
N 1
ee ee mane
,