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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML20112G3871996-06-0404 June 1996 Potential Part 21 Rept Re Capscrews W/Trace Code of K7 Mfg by Cardinal Industries (Now Known as Accutech) & Distributed by Energy & Process Corp for Plant CP S/N 0194012.Pump/motor Would Remain Operational Throughout Worse Case Scenario ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20086G2931991-11-21021 November 1991 Part 21 Rept Re Failure of Model 763 & 763A Static Pressure Transmitters.Caused by Short Circuit in Connector Pin to Adjacent Mounting Screw.Engineering Drawings & Mfg Work Instructions Changed & Stock Purged of Subj Transmitters ML20059N5191990-10-16016 October 1990 Part 21 Rept Re Rod & Bearing Assembly Failures Noted by Wolf Creek Nuclear Operating Corp During Testing.Rept Will Be Issued Outlining Root Cause & Corrective Actions to Prevent Recurrence ML17223A7451990-01-26026 January 1990 Part 21 Rept Re Backup Rings Furnished in Spare Parts Seal Kits & in 25 Gpm 4 Way Valves as Part of Actuators Made of Incorrect Matl.Rings Should Be Viton & Have Been Identified as Buna N ML20246J0631989-08-29029 August 1989 Part 21 Rept Re Namco Refusal to Certify Design & Matls for Replacement Namco Limit Switches Supplied by Masoneilan. Initially Reported on 890825.Switches Put on QC Hold Until Final Disposition of Switches Determined ML20244D2901989-06-0101 June 1989 Part 21 Rept Re Buchanan 724 Terminal Blocks Supplied by Limitorque Corp,Rather than Correct Buchanan 524 Terminal Blocks.Caused by Error in Order Processing.Training Held to Ensure That Procedures Followed Correctly ML20235Y4811989-03-0303 March 1989 Part 21 Rept Re Cracked Welds Discovered on Striker Plates of GE Circuit Breakers.Initially Reported on 890130.GE Advised Util That Striker Plates Subj to Impact Loading Only When Breaker in Racked Out & Operated in Test Position ML20195F6191988-11-18018 November 1988 Part 21 Rept Re GE Magne-Blast Circuit Breakers.Initially Reported on 881116.Welds on All safety-related Breakers Will Be Repaired Prior to Entry Into Hot Shutdown ML20151W7841988-08-16016 August 1988 Part 21 Rept Re Cracking of Slides Used in Four Way Valves Furnished on Actuators for MSIVs Due to Brazing/Heat Treating of Slide Matl.All Sites Using Actuators Will Be Formally Notified by 880826.List Encl ML20151B4291988-04-0101 April 1988 Part 21 Rept Re Inconsistencies in Gould,Inc Certificate of Compliance Received W/Class 1E Fuses Procured from Planned Maint Sys Due to Fuses Not Being Qualified for Certain Specs.Initially Reported on 880329.Fuses Remain on Hold ML20234C7351987-06-23023 June 1987 Supplemental Part 21 Rept Re Silicone Foam Seal Anomolies at Wolf Creek Generating Station ML20211P7211987-02-23023 February 1987 Part 21 Rept Re Rockbestos Coaxial Cable Used in Sorrento Electronics Digital & Analog high-range Radiation Monitor. Insulation Resistance at High Temp Not High Enough for Ion Chamber & Associated Electronics to Operate Properly ML20153D8861986-02-17017 February 1986 Part 21 Rept Re Failure of Penetration & Conduit Seal Configurations During Fire Tests.Initially Reported on 860214.Evaluation of Number & Location of Defective Seals in Progress.Nrc Assistance Requested ML20137W2611985-09-30030 September 1985 Update to Part 21 Rept Re Insp for Cracked Welds Discovered in Generator Brackets.Insp for Callaway Unit 1 Postponed Until Next Refueling Outage (Probably Apr 1986).No Cracks Discovered During Insp at Wolf Creek ML20135E1161985-09-0505 September 1985 Part 21 Rept Re Use of Connectron non-IEEE Qualified Matl in Spare Part Terminal Blocks Supplied to Facilities. Appropriate Customers Notified.Terminal Blocks Should Be Reviewed to Identify Defective Matl ML20210G9921985-08-13013 August 1985 Part 21 Rept Re Failure of Isolated Worm Shaft Gear When Certain Critical Speeds Combined W/Repetitive Transfer of Actuator Clutch Mechanism from Manual (Handwheel) to Motor Drive Mode.Two Possible Solutions Noted ML20117B8141985-05-0101 May 1985 Part 21 Rept Re Ruskin Fire Dampers Installed at Facility. Initially Reported on 850426.Fire Dampers Found in Discrepant Condition Will Be Reworked in Order to Assure Integrity & Proper Functioning ML20116E8481985-04-23023 April 1985 Part 21 Rept Forwarding Rev 1 to Insp Procedure for Investigating Emergency Diesel Generators for Fractured Welds on Air Deflectors.Rev Will Be Forwarded to Each Facility ML20116D3201985-04-22022 April 1985 Part 21 Rept Re Ruskin Mfg Co Welds Used to Join Damper to Damper & Damper Section to Mullion Plates.Welds Not in Accordance W/Approved Design Drawings.Drawing 5415 Revised to Indicate Weld Spacing.Drawing of Weld Spacing Encl ML20115J1361985-04-15015 April 1985 Forwards Insp Procedure for Investigating Emergency Diesel Generators for Fractured or Cracked Welds to Determine If Part 21 Problem Exists,Per Jg Borman ML20100E0651985-03-29029 March 1985 Part 21 Rept Re Series of Cracked Welds Discovered in Generators.Welds Occurred in Conical Baffle Section of Coil Guards.All Units Will Be Inspected.Affected Plants Listed NRC-85-3024, Part 21 Rept Re Possible Undetectable Failures in ESF Actuation Sys.Initially Reported on 791107.Possibility of Undetectable Failures Remain Under Certain Circumstances Despite Change in Hardware1985-03-22022 March 1985 Part 21 Rept Re Possible Undetectable Failures in ESF Actuation Sys.Initially Reported on 791107.Possibility of Undetectable Failures Remain Under Certain Circumstances Despite Change in Hardware ML20102B9531985-02-13013 February 1985 Supplemental Final Deficiency Rept (53564-K159) Re Concrete Coatings Inside Containment.Initially Reported on 841213. Coated Concrete Surfaces Inside Containment Will Perform Satisfactorily Under DBA Conditions ML20107B6931985-02-0707 February 1985 Final Deficiency Rept (53564-K161) Re Uncertainties in Resistance Temp Detectors Calibr.Westinghouse Evaluation Demonstrated That Revised Resistance Temp Detectors Uncertainty Acceptable ML20101T1211985-01-25025 January 1985 Final Deficiency Rept (53564-K159) Re Concrete Coatings Inside Containment.Initially Reported on 841213.Destructive Adhesion Tests Performed on Locations Selected by Sampling Plan to Verify Acceptability of Coatings ML20104B1471985-01-18018 January 1985 Final Deficiency Rept Re Insp of Structural Steel Welds. Initially Reported on 840918.Structural Concerns Identified & Corrective Action Repts Issued to Have Shims Less than 1/4 Inch Thick Placed Flush W/Mounting Frame ML20104A8671985-01-13013 January 1985 Final Deficiency Rept Re Standby Diesel Generator B Left Bank Turbocharger.Initially Reported on 840504.Caused by Loose Lock Nut on Left Bank Turbocharger Lubricating Oil Pump Centrifuge.Damaged Turbocharger Repaired & Inspected ML20104A8171985-01-13013 January 1985 Final Deficiency Rept Re Subcooling Core Monitor Alarm & Caution Relays.Initially Reported on 840821.Interposing Relays & Diodes Added to Sys to Minimize Potential for & Suppress Effects of Any Arcs Generated ML20114C9141985-01-13013 January 1985 Final Deficiency Rept (53546-K158) Re ASME Hangers & Component Supports.Initially Reported on 841212.Insulation Contractors Revised Procedures & Retrained Personnel to Preclude Further Tampering of Supports ML20104B9241985-01-13013 January 1985 Final Deficiency Rept Re Water Damaged Limitorque Motor Operators.Initially Reported on 840203.Caused by Leakage During Sys Flushing & Hydrostatic Testing Activities.Seals Added Inside Conduit & T-drains Installed in Operator ML20114D1081985-01-13013 January 1985 Final Deficiency Rept (53564-K118) Re safety-related Field Procurement by Constructor.Initially Reported on 840103. Complete Review of Constructor safety-related Purchase Orders Completed.All Nonconformance Repts Resolved ML20114C8441985-01-13013 January 1985 Final Deficiency Rept Re Microbiologically Induced Corrosion in Hxs.Initially Reported on 840601.All HXs Utilizing Lake Water for Cooling Medium Eddy Current Inspected for Microbiologically Induced Corrosion ML20114C7981985-01-13013 January 1985 Final Deficiency Rept Re Removal & Replacement of ASME Components in Support of Cleaning & Flushing Activities. Initially Reported on 840711.Investigation Into Handling & Storage of ASME Components Removed from Sys Conducted ML20112D8061985-01-0404 January 1985 Final Deficiency Rept Re MSIV Lockwashers.Initially Reported on 841207.Lockwashers Installed Via Startup Field Rept I-SU-122 & Will Be Completed Prior to Fuel Load ML20112F5421985-01-0303 January 1985 Forwards Dec 1984 Status Rept Re 10CFR50.55(e)/Part 21 Open Items RBG-19-803, Final Deficiency Rept DR-234 Re Short Cap Screws,Shallow Bolt Holes,Damaged Dowel Pins & Damaged or Missing Lock Devices for Hanger Block Bolts in Check Valves Supplied by Velan Engineering,Ltd.Initially Reported on 8411281984-12-28028 December 1984 Final Deficiency Rept DR-234 Re Short Cap Screws,Shallow Bolt Holes,Damaged Dowel Pins & Damaged or Missing Lock Devices for Hanger Block Bolts in Check Valves Supplied by Velan Engineering,Ltd.Initially Reported on 841128 ML20101N0481984-12-0707 December 1984 Final Deficiency Rept Re RCS Resistance Temp Detector Calibr Data.Initially Reported on 840801.Manufacturer Calibr Procedures Revised to Allow Recalibr at Facility.All Resistance Temp Detectors Will Be Replaced or Refurbished ML20101K8531984-12-0707 December 1984 Final Deficiency Rept Re Certification of Lead Auditor for Technical Metals,Inc.Initially Reported on 840524.Samples from Production Lots Remaining in Site Warehouse Chemically Analyzed & Found Acceptable ML20101L5631984-12-0707 December 1984 Supplemental Final Deficiency Rept Re Installation of 3-h Rated Hollow Metal Fire Door Frames.Initially Reported on 840525.Existing Caulking Replaced W/Approved Flame Retardant Adhesive Sealant ML20101N1871984-12-0707 December 1984 Final Deficiency Rept Re Heat Numbers W/More than One Pipe Schedule.Initially Reported on 831213.Two Piping Spool Pieces Replaced W/Correct Schedule of Pipe.Exam of All Installations of Subj Heats Revised to Prevent Recurrences ML20101L3591984-12-0707 December 1984 Final Deficiency Rept Re Lubricating Oil Piping Sys for Safety Injection Pumps & Centrifugal Charging Pumps. Initially Reported on 840717.Replacement of safety-related Equipment W/O QA Program Will Be Repeated Per QA Program ML20101M1031984-12-0707 December 1984 Final Deficiency Rept Re ITE-Gould Containment Cooling for Mechanical Interlocks.Initially Reported on 840316. Instruction Manual Revised to Change Installation Instructions of Size 5 Mechanical Interlock Assembly ML20101D3011984-12-0505 December 1984 Forwards Status Rept for Oct & Nov 1984 Re 10CFR50.55(e) & Part 21 Items ML20100R5131984-12-0101 December 1984 Final Deficiency Rept Re Standby Diesel Generator Lube Oil keep-warm Pumps Supplied by Crane-Deming.Pumps Will Be Designed for Reliability.Interim Pumps Reliable for Use Until ASME Rated Pumps Available ML20100C1161984-11-19019 November 1984 Deficiency Rept Re Pressurizer PORVs Preoperational Test Discrepancies.Special Operations Procedure Will Be Performed to Resolve Existing Test Discrepancies ML20099K7801984-11-16016 November 1984 Final Part 21 & Deficiency Rept Re Turbine Driven Auxiliary Feedwater Pump Governor Valve Stem Guide Bushings.Initially Reported 841017.Investigation Revealed That Defictive Parts Described by Terry Corp Installed at Facility ML20099K8291984-11-13013 November 1984 Final Part 21/deficiency Rept Re Pressurizer PORV Failing to Close During Preoperational Test.Initially Reported 841011. Resolution Will Be Provided by 841119 ML20099H1601984-11-0909 November 1984 Final Deficiency Rept Re ex-core Neutron Detector Field Cabling.Initially Reported on 841009.All Damaged Triaxial Cables & Connectors Repaired &/Or Replaced.All Insulation Panels Verified to Be Properly Reinstalled 1996-06-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1521999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Wolf Creek Generating Station.With ML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20212A0251999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Wolf Creek Generating Station.With ML20217P6451999-08-30030 August 1999 Requests Commission Approval to Publish Encl Pr,Rg & SRP & to Issue Encl Ltr to Parties of Wolf Creek Transfer Proceeding Re Disposition of Existing Antitrust License Conditions in Event OL Transfer Approved ML20210R5741999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Wolf Creek Generating Station ML20210J1561999-07-29029 July 1999 Rev 0 to Wolf Creek Generating Station,Unit 1 Pressure & Temp Limts Rept ML20210R5921999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20209H0821999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20210R5871999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1021999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1071999-04-30030 April 1999 Revised MOR for Apr 1999 for Wolf Creek Generating Station ML20206P8261999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Wcgs.With ML20196L3401999-04-30030 April 1999 Rev 1 to WCGS Cycle 11 Colr ML20210R5841999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Wolf Creek Generating Station ML20205Q0761999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Wolf Creek Generating Station.With ML20207K5991999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Wolf Creek Generating Station.With ML20207K9761998-12-31031 December 1998 Annual SER 14,for Period 980101-1231, for WCGS ML20199E6531998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Wolf Creek Generating Station.With ML20195C0011998-12-31031 December 1998 Ks City Power & Light Co 1998 Annual Rept & Financial Statements as of 981231 & 1997 for Ks Electric Power Cooperative,Inc ML20195B9901998-12-31031 December 1998 Western Resources Annual Rept for 1998 ML20198D7321998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Wolf Creek Generating Station.With ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20195E7591998-11-10010 November 1998 WCNOC Proposed PASS Function Reduction ML20195D1791998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Wolf Creek Generating Station.With ML20154L4591998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Wolf Creek Generating Station.With ML20153G2771998-09-30030 September 1998 Rev 1 to WCAP-15079, Wolf Creek Heatup & Cooldown Limit Curves for Normal Operation ML20153G2851998-09-30030 September 1998 Rev 1 to WCAP-15080, Evaluation of Pressurized Thermal Shock for Wolf Creek ML20153G2691998-09-30030 September 1998 Rev 1 to WCAP-15078, Analysis of Capsule V from Wolf Creek Nuclear Operating Corp Wolf Creek Reactor Vessel Radiation Surveillance Program ML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20151W1491998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Wcgs.With ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20237B0841998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Wolf Creek Generating Station ML20236P3441998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Wolf Creek Generating Station ML20236P3481998-05-31031 May 1998 Corrected Page of MOR for May 1998 for Wolf Creek Generating Station ML20249A0171998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Wolf Creek Generating Station ML20249B2451998-05-18018 May 1998 Nonproprietary Version of Revised Chapters 4 & 5 to Rev 4 of HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants for Ue & Wcnoc. Chapters 4 & 5 Reflect Editorial Revs ML20248C3681998-05-18018 May 1998 Non-proprietary Version of Rev 4 to HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants ML20247H0901998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Wolf Creek Generating Station ML20216J7791998-04-15015 April 1998 SER Approving Requests for Relief I1R-46 Through I1R-49 & I2R-21 Submitted by Licensee on 970523.Relief for Exam Category B-A,Item B1.12,RPV Shell Welds Deferred Until Licensee Satisfies Regulations for Augmented Rv Exam ML20216C2641998-04-0606 April 1998 SER Accepting Addl Info Re GL 92-08, Thermo- Lag 330-1 Fire Barriers, for Plant ML20216F6101998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Wolf Creek Generating Station ML20217H3491998-03-31031 March 1998 SER Accepting Operational Quality Assurance Program Description Change for Wolf Creek Generating Station ML20217H7241998-03-30030 March 1998 SER Accepting Proposed Change to Operational Quality Assurance Program for Plant ML20216G1971998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Wolf Creek Nuclear Operating Corp ML20202H0721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Wolf Creek Generating Station ML20217G4311997-12-31031 December 1997 Western Resources 1997 Annual Rept & Financial Statements for Years Ended 971231 & 1996 for Ks Electric Power Cooperative,Inc ML20203H0151997-12-31031 December 1997 Annual Operating Rept 13 for Jan-Dec 1997 ML20217G3711997-12-31031 December 1997 Kansas City Power & Light Co 1997 Annual Rept ML20216D7771997-12-31031 December 1997 Annual SER 12 for Jan-Dec 1997, for Wolf Creek Generating Station 1999-09-30
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KANSAS GAS AND ELECTRIC COMPANY THE: ELECTFaC COMPANY GLENN L KOESTER vice oneseormt.muctram November 13, 1984 Mr. R.P. Denise, Wolf Creek Task Force b Reactor Projects Branch 2 )j U.S. Nuclear Regulatory Commission Region IV { g g 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas 76011 i y KMLNRC 84-196 Re: Docket No. STN 50-482 Subj: Final 10CFR50.55(e) Report - Pressurizer Power Operated Relief Valves (53564-K155)
Dear Mr. Denise:
The attachment to this letter provides the final report submitted pursuant to 10CFR50.55(e) concerning the pressurizer power operated relief valves (PORV) at Wolf Creek Generating Station (WCGS). This matter was initially reported Ly Mr. it.K. Chernoff of Kansas Gas and Electric Company (KG&E) to Mr. John Boardman of the Nuclear Regulatory Commission, Region IV, on October 11, 1984.
Kansas Gas and Electric's plans for resolution of the pressurizer PORV preoperational test discrepancies will be provided to the NRC under separate cover by November 19, 1984.
If you have any questions concerning this matter, please contact me or Mr. Otto Maynard of my staff.
Yours very truly, I
V Glenn L. Koester Vice President - Nuclear GLK:jlh xc:RCDeYoung l FO'Connor (2)
IIBundy At tach .
8411290504 841113 -
qDRADOCK 05000482 PDR l h,yt 201 N. Market -Wichtra, Kansas - Mad Address: PO. Box 208 I W1chita, Kansas 67201 - Telephone: Area Code (316) 2616451 1
I WOLF CREEK PRESSURIZER POWER OPERATED RELIEF VALVES (PORV)
Safety Evaluation Sunnary The Wolf Creek PORV's failed to close during a specific preoperational test. This safety evaluation summary report is intended to define the conditions under which the valve malfunctioned; describe the reason for the failure to close; explain the corrective action that was taken; and provide assurance of valve operability.
Introduction The Wolf Creek pressurizer power operated relief valves (PORVs),
manufactured by Garrett, are 3" x 6" and are solenoid operated. They are intended to control pressurizer pressure to a value below the fixed high-pressure reactor trip setpoint for a 110% load rejection assuning failure of the pressurizer spray system. They also provide a safety grade means for reactor coolant system depressurization to achiev e cold shutdo wn .
Additionally, they serve as part of the cold overpressure mitigation system
( COMS) .
The PORVs are not required to open in order to prevent overpressurization of the reactor coolant system for the loss of load event discussed in the Overpressure Protection Report. The pressurizer safety valves perform this function assuming pressurizer spray and PORVs fail to operate.
The PORVs are electrically actuated valves which respond to a signal from the pressure sensing system or to manual control. They are provided with Class 1E direct position indication in the main control room. For each valve there are indication li6 hts and alarms that are activated by stem-actuated limit switches.
Figure 1 shows the functional schematic of the PORV. The mode of operation of the valve is as follows:
The valve is a line-pressure actuated , solenoid-controlled , relief valve of the caged-plug type. The schematic diagram of Figure 1 shows the unit with the solenoid de-energized and the valve closed. Inlet pressure (either vapor or water) flows into the valve inlet connection and is ported through the solenoid seat to the actuator head chamber of the valve. Inlet pressure is also ported underneath the piston and through the cage holes to surround the plug. The forces tending to hold the valve closed incluie the pressure in the actuator head chamber acting on the entire piston area and the actuator spring load. Inlet pressure also acts on the annular area beneath the piston (and outside the seat d iameter) in a direction to open the valve. Since the annular area is less than the total piston area, the closing force predoninates and the plug is held down against the seat with a force equal to the value of inlet pressure multiplied by the seat area.
f P:go Two When the solenoid is energized , the magnetic force acts on the solenoid armature to move the ball from the vent seat (as shown) to the opposite seat, thus sealing off inlet pressure from the actuator head chamber. At the same time, the actuator heed pressure is vented to discharge through the vent seat of the solenoid. With the actuator head chamber now at discharge pr essur e , inlet pr essure acting on the annular area is sufficient to overcome the actuator spring load. The plug moves away from the seat in the direction to open the valve.
As the valve opens, pressure inside the case builds up underneath that portion of the plus exposed to discharge pressure. Because of the pressure drop through the cage flow holes, this pressure is less than inlet pressure but higher than the discharge pressure. The targe seating force that exits when the valve is closed is thus turned into an opening force, causing the plug to move to the full-lift position.
When the solenoid is de-energized, the ball moves back to the seat as shown, sealing off the path to discharge and repressurizing the actuator head chamber with inlet pressure. With the plug in the full-lift position, the opening force consists of inlet pressure acting on the annular area and cage pressure acting on the base of the plug. The closing forces (consisting of inlet pressure in the actuator head chamber and the actuator spring load) overcome the opening forces and cause the plug to move toward the seat.
Discharge pressure drops to a minimum as the valve reseats, and the valve is once more held in the closed position by a force that is equal to inlet pressure multiplied by the seat area.
Discussion of Valve Malfunction It was in the closing mode, described above, in which the valves m al func tion ed . Speci ficall y, the valves were being operated in the manual mode, discharging steam, and being held open for a period of approximately 32 seconds. Prior to opening the valve, the inlet piping (consisting of approximately fourteen feet of vertical downward run loop seal) was filled with cold water as were the valves thenselves. The valves are located in a c&npartment which is below the top of the pressurizer. This location away fran the bap of the pressurizer results in valves being substantially colder than if they were at the top of the pressurizer. Valve ambient temperature at Wolf Creek is approximately 90 degrees fahrenheit.
l The preoperational test itself required approximately 32 seconds or continuous operation to achieve pressure relief of 200 psi. The pur pose o f the test is to verify valve stroke time and leakage after the valve has been opened for more than two seconds. This test simulates certain conditions l
which may be encountered during plant operation such as loss of load. The valve equipnent specification contains requirements such as t valve cycle time; discharge fluid rates; nunber of design cycles; etc. These design
, requirements are adequate to assure that the valve will perform its intended I function.
Page Three In addition to assuring operability through equipment specification requirements, considerable testing has been performed on these valves. This testing includes preoperational tests at other foreign and domestic plants and the following successful tests at Wolf Creek. At Wol f Cr eek , tests performed in the automatic mode, during which the valve remained open for a period of approximately two seconds, were successful. Additionally all Wolf Creek testing per formed without a cold loop seal was completed successfully. Further, a number of isothermal tests have been performed on the Garrett Power Operated Relief Valves. These include the EPRI Safety and Relief Valve Test Program, and Garrett operability tests. In these tests, the valves closed as required.
When the valves failed to close when signaled after the discharge period of approximately 32 seconds, the motor-o perated block valves, which are installed upstream of the PORVs and whose function is to preclude the loss of reactor coolant if a leak should develop in a PORV, were closed. Closing of the PROVs was observed to occur simultaneously with block valve closure. This occurred because the head actuator chamber ( which was isolated) was at approximately 500 psis, the normal discharge pressure.
Closure of the block valve reduced inlet pressure. Since the active area above the piston is three times greater than that below the piston, the 500 psig was sufficient to overcome the falling inlet pressure.
Summary of Investigation The postulated causes for the valve malfunction considered were: solenoid failure, plug to cage binding, and failure to get required fluid pressure to actuator head chamber. Proper solenoid operation was verified. The fact that the valve operated as designed in the autonatic mode and inspection of the valve internals showed no evidence of binding (i.e., gouging etc.),
eliminated the binding supposition. There fore , there was strong indication that the third postulated cause, that of failure to get required fluid pressure to the actuator head chamber, was the source of the mal func tion .
By reviewing the valve design in conjunction with detailed manufacturing drawings it was determined that differentici thernal expansion between the valve cage and the valve body bore in which the cage is housed, would cause the cage-to-body annulus to be reduced in size even to a point of total closur e . This annulus serves as a path for inlet fluid to travel to the solenoid port and eventually to the actuator head chamber as defined i prev iousl y. To verify this supposition, a subsequent manual test, similar to the tests in which malfunction occurred , was per formed with the v alve body heated to 228 degrees fahrenheit. The valve functioned as required providing strong support to the prenise that differential thermal expansion was the cause of the malfunction. It should be noted that by heating the valve body to 223 degrees fahrenheit the valve body bore was increased by six mila which results in an additional annular clearance under the flow conditions.
In review of the valve manufacturing drawings, it was determined that the maximum and minimum radial annular clearance at ambient temperature when the parts (valve body and cage) are machined to within specified tolerances are nine and six mils (0.009 - 0.006) respectively with diametral clearance being eighteen to twelve mils (0.018 - 0.012).
Page Four Based on the in formation from the testing described above and the small manufacturing tolerances, an analysis was performed to determine the effects of differential temperature on the valve body and cage. Figure 2 is a plot of the results and shows that for 100 degrees fahrenheit of temperature differential the annular gap is reduced by approximately three and one half mils ( .0035) . This is based on the expansion of the cage with no expansion of the valve bod y . By heating the valve in the successful test, approximately six mils (0.006) annular clearance was added due to the thermal expansion of the valve body at its initial condition of 228 degrees fahrenheit.
This phenonenon was then analyzed to determine the effects of gap closure on fluid flow with a homogeneous flow model. The results substantiate the heated test results and the differential expansion premise. Specifically, for all relief conditions, the minimum annular diametral gap between the body and the cage necessary for the PORV to function properly is 1.12 mils.
With the valve starting cold (90 degrees fahrenheit) and suddenly exposed to high pressure steam (650 degrees fahrenheit) it will take 5.75 seconds for the annular orifice gap to be reduced from 15 mils to 1.12 mils. In 7.47 seconds, the annular orifice is completely closed off. If the annular orifice gap started out at 13 mils, it would take approximately 9 seconds for the gap to be reduced to 1.12 mils. By 11 seconds, the 18 mil gap would be canpletely clo sed . In this analysis the cage expands as a function of time and temperature and the thermal expansion of the valve body during these time intervals is negligible.
Corrective Action Taken The valves under discussion were disassembled and dimensions of the body bore I.D. and cage 0.D. were taken. This showed that the diametral annular clearances at ambient temperature were nominally 15 mils and 18 mils for the two v alv es . A field change notice (FCN) was prepared to machine the cages to an 0.D. of 4.55 to 4.57 inches, thereby provid ing a final diametral annular clearance of 114 mils and 111 mils respectively. This action was taken with full cognizance and technical support / assurance by the valve designer / manufacturer (Garrett) and Westinglause.
In designing the valve to meet the specification requirements, the designer kept the annular clearance sna11 so that it would serve as a filter to prevent any debris that may be entrained in the fluid from fouling the three-way ball valve of the solenoid. Ibwev er , the v alv e manufacturer (Garrett) has deternined that the clearance provided by this design need not be this sna11. Garrett has also confirmed that the machining to resize the cage is a product improvement.
Summary and Conclusion The Walf Creek pressurizer PROVs failed to close after a discharge of water followed by steam which was conducted manually for an extended period of time. Ihe cause of this malfunction was determined to be differential
Page Five thennal expansion (valve bod y to cage) resulting in a restriction of an essential fluid flow path to the valve actuator head assembly.
Identification of the cause of the malfunction is supported by testing in other operating modes, successfully repeating the failed test with red uced differential tenperatures, and a detailed engineering analysis.
A valve modification, specified by Westinghouse and concurred with by Garrett (the valve designer / manufacturer) has been made which corrects the malfunction without having any deleterious effects on valve function.
Based on the infonnation contained herein and supporting documentation, it is concluded that the Garrett pressurizer power-operated relief valves will function under all design conditions.
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