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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20064F7011978-11-24024 November 1978 /03L-0 on 781025:during Pwr Oper,Intake Cooling Water Pumps Were Running When 3B Pump Motor Failed.The 3B Pump Motor Failed Because of Short Circuit in the Motor Windings ML20090E6071976-06-25025 June 1976 /01T:on 760611,boron Concentration of Injection Tank Below 20,000 Ppm Limit.Caused by Recirculation W/Low Concentration of Boric Acid Storage Tank B.Shutdown Initiated 1978-11-24
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
[Table view] |
Text
-
r LILENtibb EVENT HEPORT l
(
. . CONTROL 8 LOCK: SE P;;lNT ALL REOUIRED INFIRMATl!N)
uCE~SE NuMeER ,.
h(l F lL l TlP l Sl 7 89 14' 15 3l 0l l0 l-l0 l 0l 0 l0 l 0 [ l'Ol0 l l 4 l 1l1 l 1l1 l l 0 l1 l 25
30 31 32 CATEccRY SC A COCMET NUMBER* ' . EVENT OATE REPORT CATE <
01 CONT l' l 7 8 57 58 l lL l l0 l 5l0 l-l 0 l 2l 5 l 0l l0 l 6l1 l 1l7 l6 l l0 l 6 l 2 l 5 l 716 l !
59 60 61 60 69 74 75 - 60 l EVENT DESCRIPTION !
, 35 l During steady state operation, routine sampling showed that the boron l 7 89 80 (
, h l concentration of the boron injection tank (BIT) was below the Technical 7 89 60 l{
5 E hr,cification limit of 20.000 com. Corrective action was to initiate l 7 89 eo 05 7 89 l a shutdo m in accordance with Administrative Procedure 103. 8 and to com- l I
g @ lmence adding a concentrated boric acid solution to the BIT. The boron 60[
7 89 pnug 60 CE COCE COMPONENT CCCE MAM# R VOLA 110N L
7 0
l Sl H I d 89 10 lV I Al Il Vl E lX l 12 W lD l 0 l2 l 5 l y [
11 17 43 44 47 48 .
CAUSE DESCRIPTION ~
y e l Dilution of the Unit 3 LIT was caused by recirculation with the "B" BAST l
(
l 7 89 eo j 0 l which also had a low boron concentration. The reason for the low BAST l l 7 89 1O l boron concentration is discussed by Reportable Occurrence 251-76-4. 80 )
,7 89 FAcuTv METuco o,
. 80 l)
STATUS % POWER OTNER STATUS OtSCOVERY CSCOVERY DESCAPTCN 3
7 8 9 W 10 l 1l 0 l0 l l 12 13 N/A l 44
@ l N/A l 45 46 80 ACTMTV CCATENT
- RELEASED AMOUNT OF ACTMTV ~
12 (_Z_j OF yRELEASE l N/A l l LOCATON OF RELEASE N/A l 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES -
NUMBER TYPE CESCRPTON M l Ol 0 l 0 l [_Z.] l N/A l
7 89 11 12 13 60 PERSONNEL INJURIES NUMBER CESCAPTON 1
l 0l n l 0 l l N/A l i 7 89 11 12 80 PROBABL'E CONSEQUENCES -
5 Ql 7 89 N/A ,
l 60 LOSS OR OAMAGE TO_ FACIUTY TYPE DESCRFTCN Qdl 7 89 10 N/A l 80 PUBLICITY
, Ql 7 89 N/A l 60 ADOITIONAL FACTORS in l See page 2 for cont'inuation of Event Description l 7 89 80 8304040110 760625 gl gDRADOCK 05000250 .
7 89 l 60 NAME: b!. A. Schoppman PHONE: 305/552/3779 sFo ses.ooo
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REPORTABT.E OCCURRENCE 250-76-4 .!-
LICENSEE EVENT REPORT -
,_ PAGE TWO -
l . ,-
> . 1 Event Description-(Continued) ,
I concentration was returned to within specification and normal operation was resumed. A similar problem experienced by !
Unit 4 is reported in Reportable Occurrence 251-76-4. (250-76-4). J l
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June 25, 1976
. PRN-L'I-7 C-16 3
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7 l Mr. Norman C. Moseley, Director, Region II' '
. [f ,
! Office of Inspection and Enforcement . ' N'jS',,
- U. S. Nuclear Regulatory Commission -
230 Peachtree Str'eet, N.W., Suite 818 ;.l ,- ; *. - "-i.
a- :3h Atlanta, Georgia 30303 T _7. % , 5
Dear Mr. Moseley:
UY . ,y
._ .cy REPORTABLE OCCURRENCE 250-76-4 w
TURKEY POINT UNIT 3 \$ / /r 3 . -
DATE OF OCCURRENCE: JUNE 11, 1976 'Y l i
- LOW BORON CONCENTRATION.
l W
i j ..
! The attached Licensee Event Report is being submitted in
- accordance with Technical Specification 6.9.2 to provide i ' prompt notification of the subject occurrence.
1.
Very truly.yours,
! A. D. SCHMIDT ' '
l Vice President i
MAS /ao ,
4 Attachment ,
cc: Jack R. Newman, Esquire i: 'Directior, Office of Inspection and Enforcement -(40)
- Director, Office of Management Information and Program Control (3) l-J
. 6728 -
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