ML19325D661
ML19325D661 | |
Person / Time | |
---|---|
Site: | Seabrook |
Issue date: | 07/28/1989 |
From: | Dudley N, Eselgroth P, Guenther F, Lois L, James Trapp, Wiggins J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML19325C164 | List: |
References | |
50-443-89-82, NUDOCS 8910250253 | |
Download: ML19325D661 (42) | |
See also: IR 05000443/1989082
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U.S. NUCLEAR REGULATORY COMMISSION
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REGION I
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Report No.: 50-443/89-82'
Docket No. 50-443
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License..No. NPF-67'
Priority
Category C
Licensee: ~Public Service of New Hampshire
New Hampshire Yankee Division
Post Office Box 300
Seabrook, New Hampshire 03874
Facility Name: Seabrook Station Unit No. 1
' Inspection At: Seabrook, New Hampshire
Inspection Conducted: June 28-30, 1989
Inspectors:
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P. W. Eseigp6th, Team Leader, R1
date
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(See attached sheet)
.N. F. Oudley, Sr. Resident Inspector, R1
date
(See attached sheet)
L. Lois, Team Member, NRR
date
(See attached sheet)
J. M. Trapp, Team Member, R1
date
(See attached sheet)
F. Guenther, Team Member, NRR
date
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Approved:
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.WiggigTeamManager,RI
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Inspection Summary:
See Executive Summary
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U.S. NUCLEAR REGULATORY COMMISSION
REGION I
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Report No.
50-443/89-82
Docket No..
50-443
License No.
Priority
Category C
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Licensee:
Public Service of New Hampshire
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New Hampshire Yankee Division
,
Post Office Box 300
Seabrook, New Hampshire 03874
Facility Name:
Seabrook Station Unit No. 1
Inspection At: Seabrook, New Hampshire
Inspection Conducted: June 28-30, 1989
Inspectors:
P. W. Eselgroth, Team Leader, R1
date
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N. F. Dudley, Senior' Resident, RI
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L. Lois, Team Member, NRR
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J,p.Trapp,idamMember,RI
date
F. Guenther, Team Member, NRR
date
' Inspection Summary:
See Executive Summary
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U.S. NUCLEAR REGULATORY COMMISSION
REGION I
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Report No.
50-443/89-82
Docket No.
50-443
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License No. .NPF-67
Priority
Category C
'
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Licensee: Public Service of New Hampshire
.
New Hampshire Yankee Division
Post Office Box 300
Seabrook, New Hampshire 03874
Facility Name:
Seabrook Station Unit No. I
4
Inspection At:
Seabrook, New Hampshire
'
Inspection Conducted: June 28-30,1989
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Inspectors:
P. W. Eselgroth, Team Leader, RI
date
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N. F. Dudley, Senior Resident, RI
date
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L. Lois, Team Member, NRR
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J. M. Trapp, Team Member, RI
date
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F. Guenther, Team Member, NRR
date
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Inspection Summary:
See Executive Summary
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TABLE OF CONTENTS
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'1. 0 Introduction
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1.1 Scope of Inspection
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1.2 Team Composition
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~ 2.0. Executive Summary . . . . . . . . . . . . . . . . . . . ...
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2.1 Event Summary
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- 2.2- Assessment Summary
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3.0 Event Detcription . . . . . . . . . . . . . . . . . . . . .
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'4.0
Plant and Equipment Performance . . . . . . . . . . . . . . .
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4.1
Introduction. . . . . . . . . . . . . . . . . . . . . .
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4.2 Plant Response . . . . . . . . . . . . . . . . . . . .
10'
4.2.1
RCP Trip to Steam Dump Valve (15-PV-3011 Failure Open
4.2.2 Steam Dump Valve MS-PV-3011 Failure Open to Closure of
All Steam Dump Valves
4.2.3 Steam Dump Valve Closure to Reactor Trip
4.2.4 Summary of Plant Equipment Response
4.3 Steam Dump Valves _. . . . . . . . . . . . .
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4.3.1
Introduction
4.3.2 MS-PV-3011 Failure to Modulate
4.3.3
Steam Dump Valve History
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4.3.4
Valve Failure Cause
4.3.5 Licensee Short-Term Response
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4.3.6 Licensee Long-Term Response
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5.0 Personnel Activities and Performance
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5.1 Operating Crew .
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TABLE OF CONTENTS
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5.1.1
Organization.and Responsibilities
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5.1.2. Training
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5.1.3 Pre-Test Briefing
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5.1.4 Crew Response
5.1.5. Performance Assessment
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5.2 Sta rtup Te st Group . . . . . . . . . . . . . . . . . .
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5.2.1 Organization and Responsibilities
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5.2.2 Test Procedures
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5.2.3 Training
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5.2.4 ' Pre-Test Briefing
5.2.5 Test Group Response
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5.2.6 Performance Assessment
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5.3 Management and Support Staff . . . . . . . . . . . . .
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Management and Other Support Personnel
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5.3.1
5.3.2. Management Responsibilities
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5.3.3 Management Response
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5.3.4
Performance Assessment
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6.0 Safety Assessment .
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6.1 Reactor Safety Significance of Event
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6.2 Safety Significance of Personnel Performance
7.0 Exit Interview ............................................
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TABLE OF CONTENTS
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, APPENDICES
Appendix A:
Chronology of. Events
Appendix B:
Chronology of Communications
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Appendix C:
Individuals Interviewed
Appendix D:
Entrance Interview ~ Attendees
Appendix E:
Exit Interview Attendees
Appendix F:
NRC Observations Regarding Seabrook
Natural Circulation Test
' Appendix G:
Augmented Inspection Team (AIT) Charter
Appendix H:
Plant and Equipment Performance Figures
Appendix I:
Acronyms and Initialisms
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1.0 Introduction
1.1 Scope of Inspectio_n
In response to the performance of a natural circulation test at the
Saabrook Station Unit No.1 in a manner. contrary to the test
procedure reactor tripping criteria on June 22, 1989, the NRC formed
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an Augmented Inspection Team (AIT) to determineithe event sequence,
causes and safety significance. This was accomplished by
establishing a chronology of the event (Appendix A) and accompanying
communications (Appendix B), and reviewing equipment perfonnan:e,
plant staff actions relative to this occurrence and applicable
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station procedures.
The NRC Team held an entrance interview with plant management and
support personnel on June 28, 1989 and performed the' inspection
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during the period of June 28-30, 1989. An exit interview was
conducted with plant management on June 30, 1989.
Individuals
interviewed during the course of the inspection are listed in
Appendix C.
Attendees at the entrance and exit interviews are listed
in Appendixr.5 D and E.
Appendix F contains the statement of NRC
observers present during the June 22nd test. Appendix G is the
memorandum of assignment of the AIT to this Seabrook Unit 1 event.
.
Appendix H contains plant and equipment performance figures,
1.2 Team Co:nposition
The team was composed of a team leader and four headquarters and
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regional specialists with expertise in plant operations, reactor core
and plant systems, operator training, test programs and management
control s .
2.0 Executive Summary
2.1 Event Summary
On June 22, 1989, the plant conducted the natural circulation test of
the primary system which is part of the reactor testing program.
This test gathers prirnary system data under controlled conditions to
derconstrate the ability of the reactor coolant system to remove decay
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heat using natural circulation.
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At the initiation of the test, the reactor was operating at about 2%
power and heat was being removed from the plant by the steam dump
valves.
Shortly after the point in the test where the reactor
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coolant pumps were turned off to establish natural circulation of
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the primary system coolant, one of the three controlling group steam
dump valves (MS-PV-3011) malfunctioned and went to the fully open
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position, resulting in a rate of heat removal from the primary system
beyond what was planned for the test.
At this time none of the
credefined criteria in the natural circulation test procedure
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(1-ST-22) for termination of the test were exceeded nor was the
MS-PV-3011 position problem recognized. The presence of this
equipment problem and the accompanying rate of heat removal resulted
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in a primary coolant average temperature transient that resulted in
the coolant level in the pressurizer decreasing towards one of the
. test's reactor trip criteria at the pressurizer 17% level.
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Prior to pressurizer level reaching the 17% point, the Unit Shift
Supervisor (USS), a Senior Reactor Operator, informed the Test
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Director (TD)- that one of "your limits" is being approached. When
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pressurizer level reached 17% (at which letdown is automatically
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isolated and pressurizer heaters are deenergized) the Senior Control
Room Operator (SCRO), whu is the primary side reactor operator,
informed the USS of this, but did not mention the associated reactor
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trip requirement. At this point the USS conferred with the TD; steam-
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dump valve MS-PV-3011 had been shut; the pressurizer level decrease
had been halted; and, pressurizer level had begun to increase.
It
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was on the basis of the pressurizer level recovery taking place that
the US$ decided to allow the reactor to continue to operate in support
of the test.
However, the USS did not correlate the isolation of
letdown indication with.the loss of pressure control and the need
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to trip the reactor in accordance with the pressurizer 17% level
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criterion,
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An increasiag reactor coolant pressure transient was now developing
due to the closure of the malfunctioning steam dump valve
(MS-PV-3011) with the subsequent recovery of pressurizer level, and
the USS directed that the reactor be tripped due to primary plant
pressure approaching the test procedure trip criterion.
The shift
crew then carried out the emergency operating procedures for a
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reactor trip and the natural circulation test (1-ST-22) was
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terminated.
2.2 Assessment Summary
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The conclusion of the AIT staff regarding the licensee's response
to the plant transient resulting from the malfunction of one of the
steam dump valves is that reactor plant safety was never in question.
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and with the exception of the significant error of not tripping the
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reactor at the point first called for by the test procedure and loss
of pressure control due to letdown isolation and pressurizer heater
deenergization, the operating staff performed well.
The following summary of assessments is provided with references to
the sections of the report where further details are documented:
The actual plant dynamic resconse was reviewed and compared to
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the post trip review predicted response. The plant responded as
predicted in the June 22nd natural circulation testing including
the very mild overcooling event which resulted from stoam dump
valve MS-PV-3011's failure to properly modulate.
(Section 4.1)
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Plant equipment was not ready to support the June 22nd test.
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Prior to commencing the test, a test prerequisite to confirm the
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availability of the steam dump system was signed off.
However, there was an open work order for post maintenance
stroke testing of steam dump valve KS-PV-3011. (Section 4.3.3)
The interviews of the Unit Shift Supervisor (USS), Senior
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Control Room Operator (SCRO) and Control Room Operators (CRO)
found them to be highly competent individuals, clearly aware of
their assignments for safe operation of the plant.
In
particular, the USS communicated that he had no doubts about
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being the one responsible for conduct of the test in a safe and
controlled manner.
(Section 5.1.1)
Training relative to the conduct of the natural circulation test
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which covered details of the expected plant response had been
accomplished about a year prior to the test. The AIT found no
evidence that such training had been repeated or refresher
training given since that time. (Section 5.1.2)
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A review of the pre-test briefing that was conducted for the
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operators by the Test Director determined that it was inadequate
with respect to covering the details of the testing to be
performed and thoroughly reviewing the reactor trip criteria.
(Section 5.1.3)
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The operating crew was observed to be conducting plant
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operations in a controlled, unfrenzied manner prior to, during
the test and following the reactor trip when the applicable
emergency operating procedures were entered and carried out
appropriately.
(Section 5.1.4)
During the Low Power Testing program prior to the June 22nd
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event, as well as during this event, there was no evidence
of pressure applied by management or anyone else to complete
testing at the expense of controlled, safe operation of the
plant.
In fact, the NRC has been aware of personnel assigned to
shift operating and test responsibilities having received
direction from management to proceed with testing in a
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controlled manner and specifically to not permit themselves to
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feel rushed into completing evolutions.
(Section 5.1.4)
ihe USS did not trip the reactor at the 17% pressurizer level, as
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called for in the test procedure (1-ST-22). He stated his reason
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was that the decrecsing pressurizer level was under control and
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turning around. The AIT concluded that a cause of this event was
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the lack of importance and/or sense of ownership placed on test
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procedure requirements by the USS as compared to his other operating
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requirements such as those contained in Technical Specifications
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and plant operating procedures.- Two other operators interviewed
also indicated the perception of a hierarchy'of importance for
procedural requirements'between test procedures and plant
operating procedures.
These misunderstandings on the part of
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the operators demonstrated an absence of recognition of test
procedure criteria as controlling requirements for
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operation under testing conditions.
(Section 5.1.4)
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The Shift Superintendent (SS) did not provide effective
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supervisory involvement in the conduct of this test. (Section
5.1.5)
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From the interviews of operating crew personnel it has been-
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concluded that these personnel now. recognize and understand that
the proper action was to have tripped the reactor before the
1-ST-22 trip criterion on pressurizer level was exceeded.
(Section 5.1.5)
The startup test group had responsibility to interrupt or
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terminate the test in the event that required plant conditions
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were not maintained.
However, no such recommend 4 tion was made
to the shift operating crew by the test group even though the
Startup Manager was made aware of the NRC's concern about the
plant being below a manual trip criterion. The overall
direction given by the test organization during the performance
of this test was inadequate.
(Section5.2.5)
From the interviews of startup group personnel it has been
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concluded that these personnel now recognize and . understand that
the proper action was to have terminated the test and recommend
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to the operating crew that the reactor be tripped before the
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1-ST-22 trip criterion on pressurizer level was 2xceeded.
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(Section 5.2.5)
During the conduct of 1-ST-22 and at the time when plant
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c.onditions had reached the reactor trip criterion associated
with pressurizer level, there were several plant management
representatives in the control room with the responsibility and
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authority to terminate test and plant operations when approved
procedures are not being followed. When members of management
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having specific responsibility and authority relative to safe
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operation of the plant are present in the control room, their
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presence in no way dilutes the responsibilities of the operating
crew and test group personnel assigned to shift. However, by
virtue of the particular responsibilities and authorities that
they do possess relative to safe plant operations, there is a
responsibility
particularly during unique testing situations -
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to keep themselves informed of key limits for operation and
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plant status relative to those limits and to take appropriate
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action relative to plant operation whenever others they have
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assigned to do this have not done so. This was not done by the
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management members present.
(Section5.3.3)
The initial management thrust following this event appeared to
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be to resolve any equipment problems necessary to resume
.testinD. An in-depth review of the cause or causes leading to
the improper conduct of the 1-ST-22 natural circulation test
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apparently did not take place prior to an initial management
decision to resume testing. A thorough review of this event
was not completed by the licensee until after the NRC raised
this issue with licensee management. (Section 5.3.3)
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3.0 Event Description
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The following description of the event was determined through
observations, interviews with the operators and review of the plant
computer traces and printouts. A chronology of the event is presented in
Attachment A.
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On June 22, 1989, the plant was at about 2% rated power in preparation for
the performance of tne natural circulation test, which was intended to
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demonstrate the ability of the reactor coolant system to remove decay heat
using natural circulation. At approximately 12:19 p.m., the reactor
coolant pumps were tripped. The loop average temperatures began to
increase, as' expacted, and the pressurizer level and pressure began to
increase. At 12:25 p.m.,
the steam dump valves began to modulate open and
one valve failed full open resulting in a rapid cooldown of the primary
system. During the cooldown, pressurizer level dropped below 17% at 12:29
p.m.
This caused an automatic isolation of letdown and deenergization of
- the pressurizer heaters.
The steam dump valve was manually shut at 12:31
p.m. and the cooldown was terminated.
Level in the pressurizer did not go
below 14%.
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Pressurizer level increased above 17% at 12:34 p.m. and a corresponding
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pressure overshoot occurred. At 12:35 p.m. the reactor was manually
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tripped due to primary plant pressure approaching the test procedure trip
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criteria.
The pressure rise was terminated prior to reaching the auto-
matic trip set point due to the manual reactor trip. A reactor coolant
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pump was started and primary plant temperatures were stabilized at 12:50
p.m.
At no time during the transient was a reactor protection or
engineered safeguards features actuation setpoint reached.
The natural circulation test contains a manual trip criterion which states
that the reactor must be tripped if pressurizer level decreases below 17%.
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NRC inspectors recognized that a manual trip was not initiated when
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pressurizer level dropped below 17% and informed the Startup Manager, the
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Test Director, and the Assistant Operations Manager of the requirement to
trip the reactor.
However, no apparent steps were taken to direct the
tripping of the reactor prior to the manual reactor trip for increasing
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primary pressure.
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4.0 Plant and Equipment performan g
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4.1
Introduction
This section covers plant dynamic response including the' steam dump
valves.. In accordance with the AIT charter the objective is to
" determine the expected plant response during a transition to natural
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circulation cooling and compare it to the actual plant dyncmic
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response observed during the event." In addition " assess the scope
and quality of ... licensee identified concerns and corrective
actions."
Information was collected through interviews with PSNH employees and
from GETARS (General Electric Transient Analog Recorder System).
This segment of the report is divided into two major parts:
1.
Plant response to an overcooling transient, and
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2.
Mechanical and electrical instrumentation aspects of the first
steam-dump valve-bank, before, during and after the test.
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4.2 Plant Response
For this test the reactor was heavily borated at 1150 ppm boron with
all control rods fully withdrawn except for bank D rods which were
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positioned at 130 steps out of the core (full out equals 228 steps).
There were no safety systems or safety functions bypassed for this
test however, the plant was being operated under special test
conditions which allowed the reactor to be critical at power without
reactor coolant pumps operating. All low reactor coolant flow trips
are automatically blocked below the P-7 permissive setpoint
(approximately 10% power).
There is adequate data collection by the plant's GETARS system
computer to reconstruct the vital plant parameter behavior with the
exception of the valve MS-PV-3011 response. The reason for the lack
of valve MS-PV-3011 data is that a connecting link of the (Bailey)
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positioner of the valve feedback mechanism had become disconnected
which affected both valve operation as well as the computer indica-
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tions.
For the primary coolant system transient there are three distinct
time segments, that is:
1.
From the RCP trip to the steam dump valve opening, 12:18:50 to
12:25:56 (5465 to 5891 sec in GETARS indication)
2.
From the opening of the steam dump bank to their closing
12:25:56 to 12:31:06 (5891 to 6202 see in GETARS indication)
3.
From the steam dump valve closing to reactor trip 12:31:06 to
12:35:54 (6202 to 6489 sec in GETARS indication)
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Total transient time 12:35:54 - 12:18:50 = 17 min-4 sec.
The following'three report subsections discuss each of the distinct
time segments in detail.
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4.2.1
RCp Trip to Steam Dump Valve MS-pV-3011 Failure Open-
After the RCPs were tripped, the total heat input into the primary
coolant system decreased by about 12 MWt, the total heat input from
the primary pumps. The reactor was already at about 2.2% power and
the steam dump valves were in manual because they were used to dis-
.
pose of the reactor total heat input of about 86 MWt, (i.e., 74 MWt
of nuclear heat and 12 MWt of primary pump input). With reactor
power at about 2.2% of rated power, Th and Tc loop temperatures
showed the initiation of natural circulation with Th rising to about
570*F and Tc dropping to 545'F and Tavg rising by a few degrees in
all loops.
(See Figures 1.1 to 1.4, Appendix H).
Pressurizer level
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and pressurizer pressure increased as the average reactor coolant
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temperature increased due to loss of forced circulation, see Figure
2 (Appendix H). Steam generator level stayed constant as well as
1.he charging and letdown flows, see Figure 3.
pressure began decreasing due to cooldown, see Figure 5.
Decreased
primary circulation rate caused coolant and fuel temperature in-
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creases in the core which in turn decreased core power due to
doppler feedback, see Figure 4.
The core configuration for the test
(control rod position and boron concentration) were such that the
moderator temperature coefficient was about zero thus, doppler was
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the only feedback. About 5 minutes into the test, core flow was
removing the generated heat, thus Th stopped rising. However, Tc
continued falling due to steam dumping. Therefore, Tavg began to
decrease.
Steam generator pressure was also decreasing due to the
mismatch between steam dumping level and power and heat production
before the RCP trip (at 86 MWt) and after the PCP trip (at 74 MWt).
With decreasing reactor power and Tavg, pressurizer pressure and
level began to decrease and at 12:24:56 (6 min 6 see into the test)
the (condenser) steam dump valve control was lost due to the Lo-Lo
Tavg interlock at 550*F (P-12). This occurred because this inter-
lock operates on the narrow range Tavg signal which is located on
a bypass loop and without forced circulation cools faster than the
P-12 was bypassed through control room switches
and the operator regained steam dump manual control through the
first valve bank on the steam pressure mode. As soon as P-12 was
bypassed the valves attempted to return to their existing demand
position at about 5%.
However, MS-PV-3015 was blocked due to a
pre-existing excessive air leak, valve MS-PV-3011 went open (i.e.,
probably f ailed to modulate) and only valve MS-PV-3019 operated
properly. Within 40 seconds valve MS-PV-3019 closed, but MS-PV-3011
most likely stayed open.
In this brief time interval steam demand
increased, charging flow continued to increase and pressurizer level
.
- - .
. - - . . .
- - -
.
. . - , -
.
- - . .
.
..
. .
- .
- . . . - - . -
-
lt . 3
[
o
.
.;
. ' .
t
-12-
'
"
0
3
continued to decrease. The operator. responding to decreasing pres-
surizer level, further decreased the letdown flow, see Figures 2,
3, and 5.
As soon as valve MS-PV-3011 closeo, steam generator level
showed a small rapid increass for a few seconds, see Figure 2.
i
In this first time segment the reactor responded as expected. All
major parameters varied in the expe:ted direction and within ex-
,
pected ranges.
Post-event inspection showed that MS-PV-3011
probably failed to modulate.
(
4.2.2
Steam Dump' Valve MS-PV-3011 Failure Open to Closure of All Steam
Dump Valves
Six seconds after MS-PV-3011 went closed the operator manually be-
'
gan to open the first steam-dump valve-bank to initiate energy dis-
posal. The valve-bank valves are supposed to modulate in unison
4
,
with instruments in manual pressure control. The control board sig-
nals for valves MS-PV-3015 and MS-PV-3019 were correct and as ex-
pected. However, valve MS-PV-3011 went fully open and stayed in
,
that position as was verified a few minutes later by actual obser.-
,
vition.
l
As steam dumping continued, pressurizer pressure and level decreased.
and the operator responded by increasing charging flow, decreasing
(to almost zero) the letdown flow and closing the main steam drains.
In addition Th began to dacrease and Tc showed a sharp downturn,
resulting in decreasing Tavg. At this time nuclear power generation
shows a slight upturn from a minimum of about 1.4% due to excess
heat removal and fuel cooldown. Steam generator pressure decreased
due to excessive cooldown see Figures 2, 3 and 5.
l
This plant behavior, that is, excess cooling of the RCS, was caused
by valve MS-PV-3011's failure to modulate and being fully open.
The valve failure was established by visual inspection during the
transient. As this trend continued, at 12:28:54 the pressurizer
level fell below 17% (which is a procedural reactor trip level),
and, as a result, letdown isolated and pressurizer heaters de-
energized, causing the loss of normal pressurizer pressure con-
a
trol. At this point in time the pressurizer pressure was 2192
psia and reached a minimum value of 2179 psia. Pressurizer level
,
continued to fall and reached a minimum of 14.5% at which point
the operator closed the dump valves. Valves MS-PV-3011 and MS-
l
PV-3019 went fully closed.
In this time period the plant responded as expected in view of the
l
excess cooling of the RCS.
Each valve when fully open discharges
i
about 3.3% of total steam load, thus, with reactor power at about
!.
1.5%, valve MS-PV-3011 fully open and valve MS-PV-3019 partially
l
open the heat loss was at times over 4.0% and the primary system
j
heat loss exceeded the heat input from the reactor.
However, valve
MS-PV-3011 failed to modulate and the operator failed to trip the
!
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.
--
.
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.
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-13-
'
l
reactor as required.
(Note:
the valve failure to modulate is
discussed in paragraph 4.3.)
4.2.3
Steam Dump Valve Closure to Reactor Trip
Within a few seconds of steam dump valve closing, pressurizer pres-
sure and level began rising,
Charging rate was at 122 gpm (about
1% level / minute) and letdown was isolated.
Likewise, steam gene-
)
'
rator pressure and level began to rise after a small dip in the
i
level and an upturn in the pressure, see Figures 2, 3 and 5.
j
Reactor power leveled off at about 2.5%. As pressurizer level and
,
pressure increased rapidly the operator realized that pressure was
i
getting close to 2340 psia (another procedural trip requirement),
i
At 12:35:54 the reactor was tripped at a reactor pressure of about
2310 psia and the operators entered emergency operating procedure
l
E-0 in response to a reactor trip. The rise of pressurizer level
i
to 17% was recorded at 12:33:55.
Nerefore, the reactor stayed
!
below 17% for about 5 min.
l
!
In this time segment, the reactor coolant system responded as would
,
be predicted due to reduced cooling at high charr.ing rate and zero
!
letdown.
4.2.4
Summary of Plant Ecutoment Response
f
,
The plant response during operations t-iated to the natural circu-
!
lation test was as would be predicted, and all plant parameters be-
!
haved normally. A steam dump valve MS-PV-3011 failure to modulate
c
caused an unanticipated cooling of the reactor coolant system. All
phenomena were explainable and no unexplained parameter values were
i
observed.
i
4.3 Steam Dump Valves
4.3.1
Introduction
t
The origin of the primary cooling transient was the malfunction of
steam dump valve MS-PV-3011, which stuck open and failed to modu-
late.
This section reviews valve performance, operating record,
failure root cause and licensee short term and long term response.
Most of the information regarding the valves was obtained from
post-event examination.
i
t
4.3.2
MS-PV-3011 Valve Failure to Modulate
!
Post-event examination revealed that a connecting link nut to a
>
positioner arm fell off. This mechanism was providing the feedback
,
and the disconnected link explains the failure to modulate.
Never-
e
theless, valve MS-PV-3011 was able to respond to the final fully-
closed signal from the control room.
,
,
,
f
-- ,
,
, ,,- , . , , . , , - - , -, - - , , . . , , . . , , - - . ,
.
-.
- - - - , . , . -
.n-
-
. - . . . , - - , - - -
'
-14-
4.3.3
Steam Dump Valve Hittery
Interviews with the system support personnel, revealed the
l
following with respect to the steam dump valves:
1
MS-PV-3011 was stroked after the natural circulation test
.
and failed to operate properly due to mechanical binding.
Examination after removal of the valve mechanism revealed
that the binding was caused by stem misalignment and
,
interference with a guide bushing.
At the beginning of the preparation for the natural
<
circulation test, valve MS-PV-3011 was not ready to support
'
the test since work order WR87 WOO 5592 was still open for a
stroke test at NOP/NOT.
In spite of this, a test pre-
requisite to confirm the availability of the steam dump
system was signed off.
i
)
There is no indication as to when the linkage in valve
i
MS-PV-3011 failed,
it had been tested earlier from the
i
control room for close#open positioning, however, this
test would not reveal the linkage problem.
After the June 22nd event, binding was also found in valve
MS-PV-3019 but not enough to prevent open/close motion or
modulation.
Post-event testing of cil steam dump valves revealed that
seven of the twelve valves showed binding, scored stems
!
loose linkage or tight linkage.
In general, the history of
steam dump valvo system work orders indicates that there is
a valve maintenance or design ~ problem.
.
!
4.3.4
Valve Failure Cause
i
It is concluded that the MS-PV-3011 steam dump valve failure
l
cause is apparently inadequate valve maintenance or design.
!
Licensee personnel failed to follow through on a pending work
order and failed to recognize and resolve a maintenance problem
,
with the steam dump valves.
In addition the licensee failed to
l
adhere to test procedures by failing to assure that the required
j
test prerequisites and initial conditions were met before
p
commencing the test.
!
v
,
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l
l
.
.
.
-
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. _ .
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.
. .
- .
.
-
-
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a
t
,
-
,
-15-
4.3.5
Licensee Short-Term Response
The following actions were taken or initiated by the licensee
while the AIT was on the site:
i
dismantled the valve HS-PV-3011 mechanism for shop testing
i
'
'
called a vendor representative to the site
.
initiated extensive diagnostit. testing for all steam dump
'
valves,
replaced the valve MS-PV-3011 actuator with a new unit from
j
'
storage, and
i
performed a comprehensive logic circuit test.
These actions envelope an appropriate review of the behavior of
'
the steam dump valves and constitute a technically sound, prompt
!
and adequate response to the specific valve problem.
l
4.3.6
Licensee Lono-Term Response
,
Licensee personnel expressed their intent for a complete
detailed and in-depth investigation of the valve problem so as
'
to be able to take the appropriate corrective action.
,
It is the team's understanding that the licensee will
investigate:
generic failure rate data base for this type of valve
t
'
'
seek to verify whether valve usage (including surveillance
testing) is related to failure frequency, and
review (and if necessary revise) the current valve
i
maintenance and Surveillance program.
[
These actions appear to be appropriate.
t
r
5.0 personnel Activities and performance
,
5.1 Operatino Crew
-
5.1.1 Organization and Responsibilities
'
Seabrook Station's normal control room shift crew composition
and the crew composition that existed during the day shift on
June 22, 1989 were reviewed. Normally, while in mode 2
-
(startup) operations, the Unit I control room optrations staff
'
,
would consist of a Shift Superintendent (SS), a Unit Shift
Supervisor (USS), a Supervisory Control Room Operator (SCRO) and
a Control Room Operator (CRO). Both the SS and the USS possess
l
a senior reactor operator license and the SCR0 and CR0 must be
licensed as reactor operators or senior reactor operators.
This is consistent with the minimum requirements for licensed
operators per shift for on-site staffing of nuclear power units
-
-.
.
.. . _ .
. .
. - . .
.
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.
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!
.
-16-
l
specified in 10 CFR S0.54 and in the facility's Technical
!
'
Specifications.
In anticipation of performing the natural
l
circulation test on the morning of June 22, 1989, the normal
!
shift complement was augmented with additional CR0s to assist in
performing various control room functions: one operator was
[
held over from midnight shift to assist in acknowledging
secondary alarms; one was assigned to control steam generator
!
,
level and reactor coolant system temperature; a third operator
was assigned responsibility for turbine shell and chest warming
(he was never used, however); and a fourth additional operator
i
monitored the radiation monitor panels. This crew augmentation
,
allowed the operators normally assigned to the shift to
i
concentrate on the reactor and the primary plant.
The inspectors reviewed a number of facility licensee documents
!
in an effort to determine the operating shift crew's responsi-
,
bilities during normal operations and upset conditions and
during the startup test program.
j
Section 2.3 of the Seabrook Operations Management Manual (OPMM)
discusses the control room command function and states that the
$$ is the senior on-shift manager and is responsible for the
,
control room command function.
It goes on to state that the SS
may, and normally will, delegate this responsibility for each
unit to its respective USS. The SS, under Section 3.3.2 of the
!
OPMM, retains the authority to assume command of the control
room, or to order the shutdown of the reactor when, in his
judgement, such action is required to protect the safety of the
unit or the health and safety of the public.
Furthermore .the
i
,
SS is responsible for the safety and operation of the unit
!
equipment, in accordance with approved Station procedures.
-
Section 1.1 of the OPMM provides an overview of shift operations
and states that the SS maintains a broad perspective of
i
conditions affecting the status and safety of the unit, while
i
the USS maintains a comprehensive perspective of operational
conditions affecting the safety of the unit and is in charge of
'
.
the control room during emergencies.
Section 4.2.4 of the Startup Test Program Description (STPD)
states that the station staff will perform its normal job func-
tions as required to support plant operations and the startup
test program. Although the Test Director has the primary
responsibility for the execution of the test, the station
operating crew has the responsibility for the proper operation
of equipment, systems, and the plant and reserves the right to
,
take appropriate corrective actions whenever unsafe or unsatis-
factory conditions exist. A determination by the SS or USS that
i
a test would place the plant in an unacceptable condition is
identified in Section 4.3.5 of the STPD as an event which
constitutes grounds for a test interruption.
_.
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-37-
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,
Section 1.5 of the Seabrook Station Management Manual (SSMM)
{
addresses the issue of procedural adherence and states that
where a procedure exists, it shall be considered guidance
l
regarding the method of performing a function.
Procedures shall
l
be followed, but not without question.
If a procedure directs
,
an action contrary to what is considered proper, the operator
should question the procedure and seek resolution with appro-
[
.
priate supervisory personnel.
It states, however, that 6
,
procedure being questioned should not be deviated from on the
i
basis that it is being questioned.
5.1.2 Training
The inspection team reviewed the operators' startup test program
l
training completed in preparation for low power testing and
other aspects of the licensed operator training program which
'
may have had a bearing on this event.
l
During the period from April 14 to May 23, 1986, the facility's
plant reference simulator was used to train all the operators on
}
the tests that would be run during the startup program. The $$,
'
USS and the two CR0s having primary plant responsibility during
,
the natural circulation test were verified as having completed
!
.
that training. Additional classroom training on the low power
test program was conducted as part of the licensed operator
i
requalification training program during the period from
September 12 to October 21, 1988. This course was observed by
i
an NRC inspector and was addressed in Inspection Report 88-13.
l
The four-hour course, which was conducted by the Assistant
,
Startup Program Manager, provided a detailed description of the
.
startup testing program. The course topics included program
l
administration, organization, test equipment, and applicable
procedures, including 1-ST-22, the Natural Circulation Test.
'
The training also provided the operators with an awareness of
the startup test program structure.
The licensed operator initial and requalification training
programs were reviewed to determine whether deficiencies in
diagnostic and team training or in command and control and
procedural compliance training may have contributed to the event
,
on June 22.
It was determined that these subjects are addressed
i
in classroom and simulator training during the initial and
i
requalification training programs. Operations Training Standard
i
Number 3, dated January 1989, states that procedural adherence
is required with deviation allowed only after procedure changes
have been made or in the case of the emergency response
l
procedures by invoking 10 CFR 50.54(x).
This training standard
is endorsed by both the Operations and Training Managers.
Interviews with a Training Department representative indicated
that the operators are trained to comply with all approved
station procedures, regardless of whether they are operations
.
_
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-- - - -
_
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- -
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!
!
,
t
,
-18-
!
t
procedures, administrative procedures or test procedures. The
'
CR0s are instructed to advise the USS when and if reactor trip
criteria are approached and/or exceeded and to trip the reactor
l
unless directed otherwise by the U$S.
!
>
5.1.3 Pre-Test Briefing
The licensee's requirements for operating crew briefings were
'
reviewed to determine whether those conducted in preparation for
the natural circulation test were adequate.
Section 1.8 of the
,
OPMM addresses shift evolution briefings and states that they
!
shall be conducted for individuals involved in the performance
!
of the evolution.
The detail of the briefing depends on the
!
complexity, logistics or number of people involved in the
!
evolution.
Evolutions involving many individuals, especially
from two or more departments or disciplines, may require large
formal briefings or planning sessions.
It goes on to state that
complex evolutions requiring close coordination of individuals
should include the following five elements:
review of the
appropriate section of the procedure by key individuals;
!
examination of each inc'.ividual's specific involvement and
responsibility; discussion of expected results or performance;
i
'
review of precautions, limitations, emergency actions to be
taken if contingencies arise; and assurance that everyone
understands the required interface and communications required.
l
!
The inspection team interviewed the operators involved with the
conduct of the Natural Circulation Test,1-ST-22, on June 22,
1989, and it was determined that the operators were not briefed
!
as a crew prior to commencing the test procedure. The operating
7
crew members were individually briefed by the Test Director (TD)
during the early hours of their shift.
Copies of the procedure
,
j
had been distributed to the operators the preceding day but not
l
all the operators had taken the time to review it in detail; the
,
USS reviewed the procedure on the morning of June 22nd. The
l
primary plant CR0s were given copies of the manual reactor trip
!
criteria, Attachment 9.3 of the test, just prior to commencing
i
the test. One of the CR0s and the SS never received an
individual briefing. The $$ did, however, read the procedure
three days before the test was attempted, but he did not have
a copy available to him at the time it was being performed,
r
Immediately prior to commencing the test, the TD provided a
general overview briefing of the test objectives and procedure
geared for the management observers and operators from other
crews present in the back of the control room. This briefing
i
provided a brief overview of the test and was not directed to
the operator: performing the test.
I
!
-
-
.
..
-
- -
-
-
-.
..
--- -
71
-
-
-
..
\\
-19-
i
'
Discussions with NRC inspectors who were present during earlier
phases of the low power testing program indicated that the
.
pre-test briefings for the natural circulation test were less
1
thorough than others had been; previous tests h
also generally
included some sort of pre-shift group briefing i tiher than
relying solely on individual briefings. The SS did not find out
j
until after the test was aborted that the operators in his crew
i
'
had net been prcperly briefed, and the USS indicated during his
I
interview that while other pre-test briefings have been short,
)
they have generally been more thorough than what was done for
the natural circulation test.
,
i
5.1.4 Crew Response
l
'
A detailed description of the event is provided in Section
4.0 of this inspection report and a chronology of significant
.
events is provided in Appendix A.
A chronology of communica-
tions during the event is provided in Appendix B.
,
It became evident during the operator interviews that the
primary CR0s and the USS were aware that pressurizer level was
decreasing and approaching the 17% manual reactor trip criterion
!
specified in Attachment 9.3 to 1-ST-22. The $$, not being as
familiar with the test trip criteria as the rest of the
,
operating crew and not having a copy of the procedure to which
'
he could refer, suspected that level had decreased to less than
or equal to 17% when he heard letdown isolate, but he did not
associate the letdown isolation with a manual trip requirement.
The primary CR0s and the USS were aware that letdown had
i
isolated at 17% pressurizer level and that the manual reactor
t
trip criterion had been satisfied,
i
The question of why the operators did not promptly trip the
reactor when they realized that pressurizer level had decreased
below the 17% trip criterion was pursued by the inspection team
-
in the interviews.
The primary CR0s knew that the US$ was aware
of the level control problems and that he was also aware, as
they were, of the requirement to manually trip the reactor.
However, the CR0s never actually recommended to the USS that
the reactor be tripped.
Interviews with the CR0s indicated
that they were generally aware of discussions taking place
.
1
between the USS and the Test Director (TD) regarding the loss
of pressurizer level. The US$ informed the TD that pressurizer
level had decreased below "your limit."
In the interim, the
i
US$ directed the primary CR0s to monitor. level and to report
when it reached 15%. At about this time the control room
received a report from an operator in the plant that one of
the condenser steam dump valves had failed full open. The valve
was promptly closed, terminating the cooldown transient and
reversing the pressurizer level decrease at approximately 14.5%.
Both level and pressure began to recover quickly after closing
'
,
-
. - -
- _ - - - . .
-.
..-
.
. .
-
.-.
-
. - -
. - . - .
-
!
,
-
~20-
i
l
!
the failed open steam dump valve, and the operators quickly
!
tried to restore pressurizer pressure control capability.
l
Without pressurizer spray or letdown capability, pressure rapidly
increased past 2300 psig and was approaching the high pressure
reactor trip setpoint of 2385 psig. Realizing that pressure
>
was continuing to rise, the USS directed that the reactor be
.
manually tripped. The total elapsed time from the point when
!
pressurizer level decreased below 17% until the operators
!
manually tripped the reactor was approximately five minutes.
l
lt was apparent from the operator interviews that there was no
,
doubt in their minds that the command and control function in
l
the control room rested with the USS and not with the TD. The
l
USS informed the TD that level was at 17% and decreasing but
i
t
he failed to recognize that the test procedure 17% pressurizer
level trip criterion required him to direct chutdown of the
i
reactor at this point without further discussion or deliberation.
During his interview, the USS indicated that he did not trip the
'
reactor because other operating procedures do not require a trip
,
until a lower pressurizer level. Since pressurizer level
,
appeared to be stabilizing as it passed through 17%, he made the
decision not to insert a manual reactor trip at that time.
It
,
was only after the steam dump valve was closed and pressurizer
!
pressure began to rapidly increase toward the automatic trip
i
setpoint that the US$ decided that recovery from the transient
l
l
was not feasible and a manual trip was necessary.
}
!
l
The NRC inspectors who were present du"ing the natural circula-
i
!
tion test witnessed the crew's response to the reactor trip and
their performance of the emergency operating procedures. No
performance deficiencies were noted during this post trip
response.
l
Through observations and interviews the inspectors determined
i'
the Emergency Operating Procedures (EOPs) were adequately
implemented following the manual reactor trip.
The Emergency
,
Operating Procedures are normally implemented with two operators
!
l
at the control panel, however during the natural circulation
I
test there were four operators at the control panel.
No prior
discussion had been held by the USS as to how the operators were
l
to implement the E0Ps. At the inception of EOP implementation
.
I
the operator's recognized the need to adjust to the situation
!
and reached an unspoken agreement that only two of the four
l
operators would conduct the E0P procedure. As a result one
of the additional operators who was designated as the Shift
'
Technical Advisor (STA) performed the EOP control board
manipulations.
If the E0P recovery had been extended, the
inspectors were uncertain whether this operator would have been
free to perform his STA responsibilities.
Forty-five minutes
'
af ter the manual trip the NRC was notified in accordance with
-
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.
- - - -
- - - - .
. -
. -
- . - .
.-. -
[
i
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!
'
-21-
!
i
,
10 CFR 50.72 by the Shift Superintendent. This was well within
,
the four hour reporting requirement,
j
,
5.1.5 performance Assessment
'
The operating crew did not comply with an explicit procedural
!
requirement to manually trip the reactor even though they were
.
fully aware that the established trip criterion had been
!
exceeded.
The CR0s should have recommended to the USS that the
!
reactor be tripped before level exceeded the 17% pressurizer
l
level criterion. The operator interviews revealed an apparent
I
tendency by some of them to place higher priority on satisfying
some procedural requirements than others. Some of the operators
'
had attached a greater safety significance and importance to
!
complying with a Technical Specification or emergency operating
procedure requirement than, for instance, a test procedure
!
requirement.
Subsequent to arriving at this conclusion from the
!
!
operator interviews, the team viewtd a video tape of the
June 22nd natural circulation test in which the US$, when
discussing the pressurizer level problem with the TD, referred
,
to the 17f4 pressurizer level reactur trip criterion as "your
?
limit".
The USS apparently felt comfortable that the situation
was under control since he had not yet approached a lower level
i
trip criterion established in the emergency operating pro-
'
cedures.
This hierarchical approach to procedural compliance
is not endorsed by the facility's administrative policies nor
!
by the operators' licensing and continuing training programs.
'
i
The pretest briefing conducted for 1-ST-22 appears to have been
>
-
inadequate in that the operators were never formally briefed as
'
a group to address the five elements identified in Seabrook
[
Station's OPMM.
All complex evolutions, particularly those
!
involving new or infrequently performed tasks, should be
thoroughly briefed. The fact that the natural circulation test
simulator training had been performed over three years earlier
i
and the classroom training was almost a year old should have
t
provided added incentive to ensure that the operators receive
some refresher training and were thoroughly briefed prior to
l
commencing the test.
The fact that the operators on shift that
morning had not routinely worked together as a crew should have
,
emphasized the need to examine, during the pretest briefing,
each operator's specific involvement and responsibility and
understanding of the required interfaces and communications.
These observations and the assignment of the STA function to a
'
panel operator, discussed in the previous section, indicate the
,
need for more thorough planning and preparation to have been
'
done prior to this test.
Although the SS normally serves an oversight function in the
control room, his level of awereness, knowledge and involvement
of shift evolutions was not commensurate with the significance
-
-
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- . - .
. . .
-
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. .
l
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v
'
.gg.
L
and complexity of this test.
The fact that the natural circu-
'
,
lation test is one of the first evolutions performed with a
critical reactor and the fact that the test involves abnormal
operating conditions should have been sufficient to raise the
$$'s level of awareness and involvement.
i
i
NDTE:
The video taping referenced above was done by the licensee for
)
use by the training department in future training sessions. The
-
inspection team found the video tape to be supportive of the
information obtained from the interviews and the resultant
conclusions.
,
5.2 Startup Test Group
5.2.1 Organization and Responsibilities
The organization and responsibilities of the startup staff are
!
delineated in the Startup Test Program Description (STPD), Rev.
2.
The Startuo organization is led by the Startup Manager. The
Startup Manager has tFe overall responsibility for the initial
startup program and reports to the Station Manager.
The
l
Startup Supervisor reports to the Startup Manager.
The Startup
i
Supervisor is responsible for detailed coordination of the
startup test program.
Reporting to the Startup Supervisor
are the Shift Test Directors. The Shift Test Director's
responsibilities include in part to insure required test
conditions are established in a safe and prudent manner, and
i
meintained as necessary for test performance. The startup
staff normally present in the control room during startup test
performance are the Shift Test Director and the Test Director.
The Test Director reports to the Shift Test Director and is
t
responsible to perform individual startup tests.
At the time of the Natural Circulation Test Performance,
the Startup Supervisor was the Acting Shift Test Director.
During the performance of the Natural Circulation Startup
l
Test, 1-ST-22, the Startup Manager, Shif t Test Director,
.
and Test Director were all present in the Control Room.
The responsibilities of the Startup Staff and the Station
Operating crew for specific activities are provided in Table 1-1
.
of the Startup Test Program Description.
Test coordination and
i
direction activity is designated as being the responsibility of
the Startup Test Department.
The responsibility for systems and
equipment operations is delegated to the Station Operating crew.
4
Section 4.3.5 of the Startup Test Program Description states
l
that the Startup Supervisor or the Shift Test Director will
t
I
determine if a startup test should be interrupted. An example
l
of events which may warrant a test interruption provided in the
"
Test Program Description is the inability to maintain plant
1
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.~.
n
,
.
)
.
.
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-23-
,
!
conditions as specified in the startup test.
Section 4.3.6 of
l
the Startup Test Program Description states that the Startup
i
Manager, Startup Supervisor, or Shift Test Director will
i
i
i
determine if a test will be terminated. An example of a test
1
.
termination event is if the performance of a test procedure
i
'
reveals design or equipment deficiencies which prevent the
i
objectives and/or acceptance criteria from being met. During
'
.
the natural circulation test, a plant condition (pressurizer
)
level greater than 17%) was not maintained due to the steam dump
!
valve problem which prevented test objectives from being met.
'
However, no interruption or termination action was taken by the
i
Test Organization,
i
l
5.2.2 Test Procedures
i
>
Methods to change Startup Test Procedures are described in the
Startup Test Program Description. Test procedure changes may be
made utilizing two methods.
For major changes, a procedure
revision is required.
Procedure revisions undergo extensive
i
review and comment cycles including review by Westinghouse.
The
procedure is recon. mended for approval by the Startup Manager and
reviewed by the Station Operations Review Com:nittee (SORC) prior
!
to being approved by the Station. Manager.
Field procedure
'
.
changes fall into two categories: intent changes and non-intent
changes.
Procedure changes which involve a change of intent
,
!
must be reviewed and approved by the Startup Supervisor, SORC,
and the Station Manager prior to being implemented.
Non-intent
procedure changes (e.g. editorial changes) must be reviewed and
l
approved by the Startup Supervisor and the Unit Shift Supervisor
,
(or another SRO) prior to implementation.
In the event that the
l
,
Startup Supervisor is unavailable the Shift Test Director may
'
provide this review and approval.
Non-intent changes are
reviewed by 50RC within 14 days of implementation.
l
A review of the Seabrook startup test procedures is documented
i
j
in NRC inspection reports 50-443/86-31, 86-48 and 88-13.
Each
!
of the inspection reports describes a small number of minor
i
l
procedure changes which, if incorporated, would more clearly
!
or correctly state procedural steps and test objectives.
The applicable changes described in the inspections were
incorporated into the startup test procedures prior to
implementing the Zero Power Test Program. The inspections
concluded that the startup test procedures were well prepared
and technically sound. Also, the number of test procedure
p
changes made during the test program thus far appears to be
less than other comparable facility test programs.
l
l
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_
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,
5.2,3 Trainino
'
Training requirements for the Shif t Test Director and the Test
!
'
Director are provided in the Startup Test Program Description,
Rev. 2, Section 5.2, " Personnel Training." The Shift Test
Director, and Test Director were provided training in those
l
aspects of the programppplicable to procedure compliance, test
,
performance, and test documentation. This training was provided
to students as a formal classroom lecture.
In addition, the
j
Shif t Test Directors and Test Directors were also provided
!
training on selected transients which might be expected as
abnormal occurrences during various startup tests. This
training covered general transient conditions which could occur
5
and did not explicitly cover cooldown transients during natural
circulation.
The transient training was provided on a self
l
study basis, without formal training handouts or lesson plans,
,
with an examination given at the end of the self study period.
Both the Shift Test Director and the Test Director met the
i
training requirements' described in the Startup Test Program
i
Description.
In addition, both the Shift Test Director and Test
Director attended an additional course on transient analysis
-
which was conducted in the simulator. No members of the Startup
i
Organization are operator license holders at the Seabrook
Station, nor are they required to be.
,
5.2.4
Pre-Test Briefino
Procedure 1-ST-22, Rev 2., " Natural Circulation Test " Step
i
,
3.2 states that " Personnel involved with the performance of
'
this procedure have been briefed on the procedure content
and informed of their respective duties." The Test Director
provided information copies of test procedure 1-ST-22 Rev. 2,
.
,
to the primary desk, the Unit Shif t Supervisor's desk, and the
!
f.
Shif t Superintendent's desk a few days prior to initiating this
procedure.
The actual execution of the pre-test briefing and
i
sign-off of the procedural step occurred a few hours prior to
,
l.
initiating the test by the Test Director speaking with the
l
,
l
licensed operators individually on shift. The briefings were
very short according to the operators, but did cover the manual
i
,
l
trip criteria. The Test Director supplied copies of the manual trip criteria and expected plant response, Attachment 9.3 of
l
1-ST-22, to the primary operator, reactor controls operator, and
l
Unit Shif t Supervisor just prior to the test. The control board
'
operators and the Unit Shift Supervisor responsible for shift
operation, stated in interviews following this event that they
-
were made aware of the 17% pressurizer level trip criterion
during the pre-test briefing with the exception of one of the
-
two control board operators assigned to assist the shift crew
who stated he was not briefed and was not aware of the manual trip criteria.
l
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1
_._ _ __. _ _ . . .
,
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.
.
_ _ . , _ . . . _ . . .
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-
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(
)
,
,
~25-
'
)
i
!
5.2.5 Test Group Response
l
The startup test group crew response was derived from
1
observations made by the inspectors during the event and
interviews held with the startup group staff following the
event.
The Startup personnel present in the control room during
i
the event were the Startup Manager, Shift Test Director, Test
,
Director, and other supporting Startup Engineers. Of the
l
Startup Staff only the Test Director was positioned inside the
'
operating area, other members of the Startup Group witnessed the
test from inside the control room but outside the operating
area.
Prior to the event the Test Director was communicating
i
test instructions with the operating staff and monitoring test
,
data. Af ter the reactor coolant pumps were tripped, per the
'
test procedure, and the test initiated, the Test Director
primarily monitored computer and panel indications. The Test
Director stated that during the event he was aware that the
pressurizer level had decreased below the manual reactor trip
criteria of 17% when it was announced by the control board
operator that letdown had isolated. At this point the Test
i
Director did not recommend to the Unit Shift Supervisor to trip
the reactor.
He indicated to the Unit Shift Supervisor that he
,
would monitor computer trends for Tavg to assure that the 15
l
minute Technical Specification on Lo-Tavg was not violated.
Performing this task essentially removed the Test Director
!
from the overview t,f plant status.
During the period when
l
pressurizer level was below 17%, an NRC inspector monitoring
l
the test activities expressed a concern to the Test Director
,
l
that the pressurizer level was below the manual trip criteria.
Following this communication the Test Director stated that he
'
told the Unit Shift Supervisor that the NRC has a problem with
being below the manual trip criterion. The Test Director stated
that the USS said he was handling it. At no time during this
test did the Test Director recommend that the operators manually
,
trip the plant.
,
The Shift Test Director was monitoring test activities from
,
outside the operating area. The Shift Test Director stated that
he was aware of the manual trip criterion for pressurizer level
I
and that the value was exceeded during the test.
He stated that
he focused on attempting to analyze the on going transient and,
l
therefore, did not provide an advisory role to the operating
staff. At no time during this transient were recommendations
provided by the Shift Test Director to the operating staff.
The Startup Mar,ager was monitoring test activities from outside
the operating area.
The Startup Manager stated that he first
became aware of the pressurizer level being below the 17% trip
l
criterion when informed of such by the NRC inspector monitoring
-
startup testing.
The Startup Manager did not communicate the
-
.
- - . -.
-
-
.
- . - .
.
.- -
. -
-.
.
4
~26-
,
inspector's concerns to the operating crew or other members of
the Startup Staff.
5.2.6 Performance Assessment
l
The inspection team concluded that the pre-test briefing
performed by the Test Director was conducted in a fragmented and
.
abbreviated manner. Due to the interactions which occur between
,
plant systems and operator actions, it is important to perform
the operator pre-test briefings as a group rather than in a
piece meal fashion.
Three levels of the Startup organization were aware that the
pressurizer level was below the manual trip criterion during the
Only after the NRC inspector voiced a concern did a
startup organization member (Test Director) indicate a concern
to the operating staff. At no time during the performance of
.
this test did any member of the startup group communicate to
the station operating staff a recommendation to interrupt or
terminate the test procedure. The technical guidance provided
by the startup organization to the operating staff during this
event was inadequate.
In general, the startup organization became more occupied with
individual tasks at the expense of maintaining at least one
individual with overall responsibility for overview and
technical input to the Unit Shift Supervisor for conduct of
the test procedure.
5.3 Management and Support Staff
5.3,1 Management and Other Support Personnel
During the performance of the test there were approximately
seven managers in the main control room.
The Vice President
of Nuclear Production was the most senior manager present.
The Operations Manager and the Assistant Operations Manager
were the only managers in the control board area.
Approximately twenty licensed operators, in addition to the
operating crew, were in the main control room to observe the
natural circulation test to fulfill the commitment in Final
Safety Analysis Report (FSAR) request for additional information
response.
These operators remained outside the control board
area, did not become involved with plant operations and
maintained a quiet presence throughout the test.
5.3.2 Management Responsibilities
The responsibilities of the Station Manager and the Assistant
Station Manager, both of whom were present in the control room
L
+
,
L
-27-
F
during the test, are delineated in the Nuclear Production
Management Manual (NPMM). The Station Manager is responsible
for ensuring the station is operated and maintained in
accordance with applicable requirements and he serves as
chairman of the Station Operation Review Committee ($0RC). The
Station Manager has the authority to direct reactor shutdown
when conditions may endanger equipment status or the health and
.
safety of the public. The Assistant Station Manager is
responsible for n.aintenance of the programs and procedures
needed to operate the station in accordance with applicable
requirements and he also has the authority to direct the reactor
to be shutdown.
The responsibilities for the Operations Manager and the
Assistant Operations Manager are delineated in the Operations
Management Manual (OPMM).
The Operations Manager is responsible
to direct operating activities in a safe and reliable manner,
supervise the Assistant Operation Manager and he is a member of
t
50RC.
He has the authority to order the shutdown of the reactor
.
when action is required to protect the safety of the station or
!
the health and safety of the public. The Assistant Operations
Manager has the responsibility for safe operation of the unit's
equipment and directs the activities of the members of the
operating crews.
He also has the authority to order shutdown of
the reactor.
5.3.3 Manacement Response
Of the managers interviewed, two were aware, during the test,
that pressurizer level had dropped below 17%. The Station
.
Manager was the only manager interviewed that knew of the
existence of a trip criterion on pressurizer level but was
unfamiliar with the exact criterion. Most of the staff
members interviewed are members of the 50RC which had reviewed
and approved the natural circulation test procedure.
Through interviews with the management staff and review of
management responsibilities in the NPMM and the OPMM it was
determined that four of the managers interviewed had the
authority to direct a reactor shutdown. However, none of these
managers communicated to the USS a need to trip the reactor when
i
pressurizer level decreased below 17%.
i
The Station Manager stated he was not sure why the USS did not
trip the reactor but believed it was due to the training the USS
had received in the simulator. The Operations Manager stated
that the US$ did not trip the reactor because the USS knew the
cooldown was causing the pressurizer level drop and that the US$
knew the cooldown was under control.
During an interview conducted on June 24, 1989, the Station
4
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.-m.
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,
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\\
Manager stated that he recognized soon after the reactor trip
l
on June 22, 1989, that the failure to follow procedures was a
j
significant problem but had been unable to conduct a full
,t
discussion of the problem with his management team prior to
i
meeting with the VP Nuclear Production at approximately 5:00
(
p.m.
'
i
During a conference call on June 22, 1989 with the Region I
'
Branch Chief at 6:00 p.m. the VP Nuclear Production indicated
,
that the procedural compliance issue would be looked at and put
i
in proper perspective and that if the event occurred again he
I
would expect the operators to trip the reactor. The VP of
!
Nuclear Production initially indicated a desire to restart the
.
reactor early the next morning but agreed to postpone reactor
}
startup until after a follow-up conference call.
5
During the follow up conference call at 7:30 a.m. on
June 23, 1989, the licensee outlined the planned modification to
f
their management manucis that would provide additional guidance
on the implementation of procedures and outlined the briefings
!
that were planned with all shift crews to present the new
6
guidance. As a result of a subsequent phone call between the
!
Deputy Regional Administrator and the President of New Hampshire
!
Yankee Division a Confirmatory Action Letter was issued
requiring that a complete review and analysis of the event be
formally prepared and presented to the NRC prior to reactor
!
restart.
Immediately after the phone conversation the license's
Event Evaluation Team, the Human Performance Evaluation System
i
team, and the Independent Review Team were assigned to perform
'
separate evaluations of the event.
l
5.3.4
Performance Assessment
'
The initial management thrust following this event appeared
to be to resolve any equipment probitms necessary to resume
testing. An in-depth review of the cause or causes leading to
f
the improper conduct of the 1-ST-22 natural circulation test
!
.
apparently did not take place prior to an initial management
decision to resume testing. An extensive review of this event
was not completed by the licensee until after the NRC raised
this issue with licensee management.
During the conduct of 1-ST-22 and at the time when plant
conditions had reached the reactor trip criterion associated
i
with pressurizer level, there were several plant management
!
representatives in the control room with the responsibility
and authority to terminate the test and plant operations when
approved procedures are not being followed.
This was not done.
When a member of management having specific responsibility and
authority relative to safe operation of the plant is present
in the control room, their presence in no way dilutes the
..
._
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.-.
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-
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[
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r
responsibilities of the operating crew and test group personnel
l
l
assigned to shift. However, by virtue of the particular
!
responsibilities and authorities that they do possess relative
l
to safe plant operations, there is a responsibility -
particularly during unique testing situations - to keep them-
i
selves informed of key limits for operation and plant status
i
relative to those limits and to take appropriate action relative
i
'
to plant operation whenever others they have assigned to do this
have not done so. Plant management present did not do this in
'
the case of the 17% pressurizer level trip criterion that was
exceeded. The reactor was subsequently shut down by the USS
!
when the transient response of another parameter, primary plant
.
pressure, caused the USS to take this action.
l
6.0 Safety Assessment
6.1 Reactor Safety Significance of the Event
,
!
The aspect:, of this event which cause the plant t.ansient to be
.
different from the intended natural circulation cest transient are
i
'
the failure of valve MS-PV-3011 to modulate and the fact that the
operators did not manually trip the reactor based on pressurizer
level. The excess cooling of the reactor coolant system is of
[
little or no reactor plant safety significance in that it is very
!
'
minor by comparison to other analyzed events (steam line break,
inadvertent initiation of a coolant loop, etc.) and these have
'
been analyzed and shown to be acceptable. The June 22nd event
,
is, therefore, totally bounded by these other analyzed events.
.
6.2 Safety Significance of Personnel performance
,
The failure of the operating crew to trip the reactor when required
by the test procedure during the June 22nd test; the failure of test
'
group personnel to recommend tripping of the reactor at that point
and the failure of management present in the control room to
,
exercise their responsibilities in this situation, despite the fact
-
the plant was being operated under a Technical Specification Special
Test Exception, is safety significant. Also, the apparent willingness
of management to proceed with testing following the June 22nd
occurrence without first completing a thorough review and causal
factor assessment is safety significant.
-
Test procedures often involve placing the plant in unusual
conditions for operation, conditions which are not routinely
'
experienced nor necessarily adequately covered by normal operating
procedures. Use of test procedures results in operation under an
'
approved margin of safety only when strictly followed. These test
procedures are carefully developed, utilizing industry experience
and expertise, are carefully reviewed and only approved after
confidence is established in their ability to assure plant s&fety.
The conduct of tests such as the natural circulation test in which
,
--
-
7-
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, , ,
,
, - , , - - . , , - - , -
- , - , . -
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--
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.
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-30-
,
the reactor is critical without reactor coolant pumps operating is
an example of testing under unusual conditions, conditions which call
for a heightened sensitivity to plant status and attention to strict
procedural adherence. Neither shift operators, the key test group
personnel nor the managers present in the control room during the
June 22nd test demonstrated an adequate understanding of this.
'
As stated in the previous section, the particular plant transient
which resulted from the combination of the steam dump valve
equipment problem and failure to follow the test procedure reactor
trir criterion did not significantly challenge the plant margin to
safety.
However, the operational practice exhibited by the
personnel in the control rcom was unacceptable.
The AIT concluded that all operations, test group and management
personnel interviewed now recognize that testing can proceed only if
done so in accordance with the test procedure requirements and that
if testing should for any reason proceed otherwise the test
procedure must first be formally revised. The AIT found no
indications of uncertainty or equivocation about this during the
site visit.
7.0 Exit Interview
On June 30, 1989 a preliminary exit interview was held with licensee
management to review the observationr,and assessments of the AIT. The
licensee was informed at the time that this interview might not be the
final exit for this inspection.
During this inspection, the NRC
inspectors received no comments from the licensee that any of their
inspection items or issues contained proprietary information. No written
material was provided to the licensee during this inspection.
On July 5,1989, the team briefed regional management on the results of
the inspection.
The licensee was informed by NRC Region I management that
f
the above exit interview would be considered the final exit.
,
r
i
5
t
!
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.
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APPENDIX A
CHRONOLOGY OF EVENTS
INSPECTOR
i
TIME:
EVENT:
OBSERVATIONS / ACTIONS:
'
,
12:18:00
Pre-RCP trip conditions
Pressurizer (PIR) pressure
i
2237.2 psig, PZR level 25.54%
,
Wide Range T cold $55.8 F.
t
All rods withdrawn except
bank 0 (step 133)
i
12:18:50
RCP breakers are opened
,
All 12 RCS low flow alarms
are received
12:25:15
Steam dumps control lost due
to permissive P-12 actuation
at $50'F Low Tavg
12:25:19
Steam dumps 3019 and 30))
began to open when P-12 was
manually bypassed.
.,
All steam dumps in bank should
i
modulate together
!
12:25:21
Steam dump valve 3011 closes
12:25:21
Steam dump valve 3011 opens
,
12:25:23
Steam dump valve 3011 closes
f
12:25:23
Steam dump valve 3011 opens
!
12:25:25
Steam dump valve 3011 closes
12:25:58
Steam dump valve 3019 closes
12:25:59
Steam dump valve 3015 closes
.
12:26:04
Steam dump valve 3011 fails open
!
,
12:28:59
PZR level at 17%
PZR heaters deenergized
Letdown isolated
'
12:30:55
Lowest PZR level 14.5%
Lowest PZr; pressure 2179.0 psig
.
. _ _ _
.
_.
. - .
.-
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,
f
CHRONOLOGY OF EVENTS
INSPECTOR
i
>
!
TIME:
EVENT:
OBSERVATIONS / ACTIONS:
.
12:31:06
Steam dump valve 3011 closes
12:32(about)
NRC inspector discussed
f
'
need for trip with Startup
'
,
Manager
>
12:32:55
Avg. wide range Tavg 539.97'F
!
12:33 (about)
NRC inspector discussed
need for trip with SRI and
Deputy Regional
Administrator
!
i
12:33:55
PZR level 17.95%
12:34 (about)
NRC inspector discussed
need for trip with Test
Director
12:35:54
Manual reactor trip train A
>
12:35:54
Reactor trip breakers A and
B open
,
,
12:35:55
Avg. wide range Tavs 541.90*F
,
i
12:35:55
Highest PZR pressure 2311 psig
P
12:37:10
PZR beaters restored
i
Key: PZR HI LVL Trip
92%
i
'
PZR LO LVL Trip
None
PZR Heaters and Letdown Isolation
17% PZR LVL
,
PZR HI Press Trip
2385 psig
,
PZR LO press Trip
1945 psig
1865 psig
PORV open
2385 psig
i
t
i
!
!
!
c
APPENDIX 8
CHRONOLOGY OF COMMLINICATIONS
l
f
DATE
TIME
EVENT
.
'
June 19
Operating crew members provided copies of
i
.
natural circulation (NC) test procedure.
[
,
t
June 22
09:00 a.m.
Lead Test Director provides trip criteria
sheets and individual briefings to Unit
i
'
Shif t Supervisor (USS), Senior Control Room
l
Operator (SCRO), and Control Room Operator
'
(CRO).
-
11:30 a.m.
Test Director (TO) provides briefing on
t
overview of NC test to main control room.
'
'
12:19 p.m.
Reactor Coolant Pumps are tripped.
12:27 p.m.
SCR0 informs US$ that pressurizer (P2R) level
is falling and going to go below 17%.
USS
~
directs CR0 secondary to secure all steam
demand. USS Informs TD that PZR Level is
'
going below 17%.
12:29 p.m.
PZR Level below 17%; letdown isolates and PZR
heaters deenergize; Shift Test Director
!
(STO) knows P2R level is below 17% and takes
no action.
"
USS Informs TD that PZR level is below "Yout-
'
,
Limit."
USS Directs SCR0 to keep eye on PZR and report
when P2R level reaches 15%.
'
.
Secondary CR0 believes decision has been
!
reached to continue with test but does not
know how decision was reached or
,
communicated to crew.
'
Shift Superintendent and Operations Manager
knew plant was below 17% PZR level but did
not know trip criterion and took no action,
i
12:31 p.m.
SCR0 and US$ discuss PZR level reaching 14.5%.
+
Phone call to Main Control Room from operator
g
in plant saying steam dump valve was full
open.
SCR0 reports pZR level increasing.
i
USS directs SCR0 to restore auxiliary spray
capabilities.
.-
_
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.
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I
,
!
l
CHRONOLOGY OF COMMUNICATIONS'
f
!'
DATE
TIME
EVENT
l
12:32 p.m.
NRC Inspector discusses with Startup Manager
($M) requirement to trip plant and receives
i
no verbal response. SM observed communications
.
.
between US$ and TD and takes no action.
!
'
,
12:33 p.m.
NRC Inspector discusses need for trip with
L
Senior Resident Inspector ($RI) and Deputy
l
Regional Administrator.
12:34 p.m.
TO informs US$ that Tavg below required
Technical Specification limit,
j
SS orders 15 minute clock started for Tavg
i
"
below limit.
!
NRC Inspector discusses need for trip with TD.
TD approaches US$ and provides update on Tavg.
,
SRI discusses with Assistant Operations
'
Manager need for trip.
Assistant Operations Manager confirms with TD
need for trip.
l
SCR0 reports letdown almost restored.
-
US$ directs SCR0 to watch delta T on PZR spray
line.
.
Assistant Operations Manager approaches USS.
USS directs primary CR0 to manually trip
!
the reactor due to increasing pressure.
!
SCR0 requests additional time to establish
,
Auxiliary Spray.
I
12:36 p.m.
US$ directs trip.
Reactor is tripped.
Assistant Operations Manager informs
Operations Manager of requirement to trip.
>
-
.
22:45 p.m.
Deputy Regional Administrator informs VP
l
Nuclear Production that NRC has concern with
!
operator's failure to follow procedures.
1:00 p.m.
Licensee management meeting sets schedule for
i
restart as morning of June 23.
1:20 p.m.
SS notifies NRC Operations Center of manual
,
i
2:00 p.m.
The licensee's Incident Investigation Team,
Post Trip Review Team and Self-Assessment
Team Were Established.
2
.
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,
CHRONOLOGY OF COMMUNICATIONS
)
DATE
TIME
EEENT
l
.
3:30 p.m.
Post Trip Review Meeting was held and dealt
i
'
with equipment and procedural issues.
,
I
4:30 p.m.
Station Manager and Assistant Station Manager
began to discuss the procedural compliance
problem when they were called into meeting
L
with Vice President (VP) Nuclear Production.
l
6:00 p.m.
Conference Call Between VP Nuclear Production
l
and NRC Regional Branch Chief. Agreement
i
reached to delay startup at least until
i
7:30 a.m. June 23.
June 23
7:30 a.m.
Conference Call Between VP Nuclear Production
,
and NRC Regional Branch Chief. Agreement
!
reacted to delay startup until return call
!
f rorr NRC.
12:00 p.m.
Discussion between Deputy Regional Administrator
and President of New Hampshire Yankee resulted
'
in issuance of Confirmatory Action latter.
f
.
1:50 p.m.
Event Evaluation Team, Human Performance
Evaluation System and Independent Review
'
Team established.
.
I
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'
APPENDIX C
INDIVIDUALS INTERVIEWED
'
,
h
The following is a list of the individuals interviewed, by title, and a summary
l
of their responsibilities during the natural circulation test.
,
TITLE
ROLE OR RESPONSIBILITY
,
Control Room Operator (CRO)
Responsible for Rod Control Panel,
Rod Control Panel
Shif t Technical Adviser Primary Board
,
Operator. During E0Ps responsible for
'
tripping reactor when automatic trip
i
setpoint is exceeded.
,
Assistant Station Manager
Observer who has authority to direct
reactor shutdown.
Senior Control Room Operator (SCRO)
Responsible for PZR, Primary Panel and
CVCS.
Responsible for tripping reactor
,
when automatic trip setpoint is
i
'
exceeded.
Test Director (TD)
Responsible for performance of
i
individual Startup Test.
-
Operations Manager
Observer / Management oversite; has
authority to direct reactor shutdown.
,
CR0
Responsible for assisting CR0 on
Balance of Plant Panels
secondary panels. Responsible for
tripping reactor when automatic trip
setpoint is exceeded.
Startup Manager
Observer / Supervisory oversite; overall
responsibility for the Initial Startup
i
Program.
,
'
CR0
Responsible for Steam Generaor
Secondary Panel
Feedwater and Steam Dumps.
i
Licensed Operator
Responsible for acknowledging Alarms on
,
Radiation Monitor Status Panel.
Shift Superintendent
Provides requisite technical expertise
to the Unit Shift Supervisor in the
event of any abnormal operational
occurrence. Authority to order
shutdown of reactor.
_._-
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t
.
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.
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l
TITLE
ROLE OR RESPONSIBILITY
j
Production Services Manager
Observer for Self Assessment Team.
Station Manager
Observer has authority to direct
reactor shutdown.
-
,
,
!
Assistant Operations Manager
Observer; has authority to order
reactor shutdown.
{
CR0
Acknowledge alarms on Reactor Coolant
Turbine Generator Chest Warming
Pump trip.
,
Shift Test Director
Coordinate overall plant operations
'
'
Reactor Startup Supervisor
to insure required test conditions are
maintained in a safe and prudent
,
manner.
.
.
Vice President Nucicar Production
Observer.
i
Manager Operational Support
Observer.
Unit Shif t Supervisor (USS)
Responsible for conducting operation
,
with approved procedures.
Has
!
auti.ority to order reactor shutdown.
+
Senior Simulator Instructor
Video tape plant response for future
training.
,
OTHER INDIVIDUALS INTERVIEWED
[
$
Assistant Startup Manager
System Support Department Manager
Engineer (I&C)
j
Engineer
Operational Programs Manager
l
,
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475 ALLENDALE ROAD
KINO oF PRUS$1A. PENNSYLVANIA 19404
June 26, 1989
)
I
MEMORANDUM FOR:
William T. Russell, Regional Adminis,trator
TROM:
Thomas T. Martin, Deputy Regional Administrator
SUBJECT:
NRC OBSERVATIONS REGARDING SEABROOK NATURAL
l
CIRCUIATION TEST
+
,
As requested, please find enclosed a composite narrative of
l
NRC observations regarding the licensee's preparation for and
r
conduct of the Seabrook Natural circulation Test.
The narrative
,
was developed as a joint effort of Noel Dudley, Senior Resident
Inspector, Jim Trapp, Reactor Engineer and myself.
A
M&
-
Thomas T. Martin
.
Deputy Regional Administrator
.
Enclosure:
As Stated
cc:
J. Taylor, DEDO
T. Murley, NRR
,
J. Wiggins, RI
D. Haverkamp, RI
N. Dudley, RI
J. Trapp, RI
,
._.,_._,,,__,-----w----
- - - - * - - - - - - * * - - * - - * - * - - - * * - - - * " ' ' ' - ' - " ' * " - * ' " "
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._
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._
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-
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4
9
t
'
ENCLOSURE
,
NRC OBSERVATIONS REGARDING SEABROOK
-
NATURAL CIRCULATION TEST
,
i
Tim Martin, Deputy Regional Administrator, Noel Dudley, Senior
'
-Resident
Inspector
(SRI),
and Jim
Trapp,
Reactor
Engineer,
,
'
representing the NRC, were present in the Seabrook Control Room on
June 22, 1989, to observe the preparations for and conduct of the
-
licensee's natural circulation test.
All three NRC participants
i
had reviewed and discussed the test procedure. The shift operating
crew in the control Room consisted of a Shift Superintendent, Unit
Shift Superintendent,
Senior Control Room Operator and three
,
control Room Operators.
With the exception of the licensee's
operating
crew,
several
operations
department
managers
and
several test engineers, all personnel (approximately 40 total) were
outside the immediate area of the controls and approximately 25
feet from the control panels.
The observers maintained a minimum
noise level throughout tha test preparations and conduct.
In preparation for the test, the Lead Test Engineer (LTE) presented
e
a very general discussion of the test to be conducted.
The LTE
>
stated he would review separately with the operating crew the
conditions
requiring a reactor trip.
(The SRI believes he
subsequently observed this briefing taking place.)
In recognition
of the assembled observers' inability to read panel indications,
the SRI requested a description of plant parameters presor.ted on
large CRT's that were observable from outside the operating area.
,
'
The operating crew identified the parameters displayed on each CRT
to enable the observers to follow the transient.
Preparations for the test and conduct of the operating crew
appeared to be conservative, cautious, and thorough.
The initial
operating conditions, needed to initiate this test, required time
to establish.
Key operating parameter oscillations required
dampening while establishing the initial test conditions.
These
oscillations were normal and occurred because many controllers were
required by the test procedure, to be placed in manual control.
At this point, there was no basis for any concern in the minds of
the NRC observers.
When the plant was finally st.abilized at - 34 power, the Unit Shift
Supervisor (USS) announced the test was starting.
Two individuals
were utilized to trip the four reactor coolant pumps nearly
,
'
simultaneously.
The transient was predicted to last 10-50 minutes
and the operators appeared to conscientiously monitoring their
controls.
Neutron flux level was noted to decrease, initiating
quiet discussion between Mr. Martin and Mr. Dudley, given the
stated test prerequisite to reach a zero moderator temperature
coefficient.
-
.
. .
.
.
._. _ . _ _ _ ... _ . _ _ _ _ _ .. _ _ . _ __ ,. _ _ . _ _
_ _ .
_
. ~
_ _ . .
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._ . . _ _ _ -
_
.
. _ _ _ . __
,
,
.
2
.
'
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l
i
.
,
,
l
Jim Trapp, was the first NRC observer to detect a problem, noting
(
!
panel
. indications
of
an
automatic
de-energization
of
the
pressurizer heaters and isolation of letdown.
From previous
l
experiences as a licensed individual at another facility, he
i
. recalled this occurred at about 184 pressurizer level, just
!
'
slightly above the 174 level that the test procedure instructed
,
l
operators to manually trip the reactor.
Mr. Trapp asked a Senior
l
Reactor Operator (SRO), who was also an observer and not part of
'
the current shift operating crew, what their isolation setpoint
i
was. He learned it was 174, the condition under the current test
'
procedure requiring the operators to manually trip the reactor.
Althougn
the
plant
was
not
currently
in danger,
Mr.
Trapp
immediately went to the Startup Manager at the Test Engineer's
table.
Mr. Trapp advised the manager, who had authority to stop
the ' test,
that the heaters trip and letdown isolates at 174
,
l
pressurizer level and that they were now operating below the
criteria for manually tripping the reactor.
The manager continued
,
to watch the in-progress test, appeared to take no action, and gave .
l
no oral response; but did appear to hear Mr. Trapp's concern.
!
Mr. Trapp then went to Mr. Dudley and Mr. Martin, informing them
of his concern that the licensee had met conditions requiring a
manual trip, for about two minutes, and the lack of response to
that information by the Startup Manager.
This discussion took
L
about thirty seconds.
Pressurizer level, as shown on the CRT, was
i
now offscale low and the Senior Control Room Operator (SCRO)
appeared to be initiating additional makeup with a corresponding
increase in indicated pressure, showing that pressuriser level was
being restored.
Mr. Trapp then went over to talk to the Lead Test Director (LTD)
who had his back to the control console and was reviewing data from
a printer.
Mr. Trapp informed the LTD, an individual who could
recommend halting the test, that they were operating below the
level requiring a manual trip of the reactor. The LTD examined his
printout, said something to the effect that he would get back to
him, and turned, walked over to the Unit Shift Supervisor (USS) and
communicated to that individual.
The USS, an SRO with authority
to order a reactor trip, was directing the activities of the
operating crew.
The SRI, noting that Mr. Trapp was not getting a satisfactory
response, immediately went over to the Assistant Operations Manager
(AOM), an SRO with authority to stop the test, and advised that the
pressurizer level was below 174, requiring a manual reactor trip.
During this period, the LTD returned to the printer, and the AOM
asked was it true they should have tripped the reactor.
When told
yes, the AOM went to the Operations Manager, another SRO with
.
.
. .
..
.
. .
..
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.
_ .
--
- _ _ . _ . - .
_ .
- - - . .
.-
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.,
,
,
3
,
authority to direct tripping the reactor, and the USS, and appeared
to communicate with both individuals,
j
.
Subsequently, -and without a clear impression of whether the
'
response was or was not prompted by the expressed NRC concern, with
pressurizer pressure and level now rapidly increasing and again on
the.CRT scale, the USS directed a control Roon Operator (CRO) to
-
'
trip the reactor.
The SCRO, an individual who could independently
trip the reactor, indicated he was about to re-establish control
J
and requested a delay.
The USS told him no and the CRO then
tripped the reactor.
The NRC observers then watched the apparent smooth performance of
,
the required
Emergency Operating
Procedures,
discussed their
perception of why the operators initially failed and subsequently
decided to trip the reactor, and discussed.the safety significance
of what had been observed.
The role of the Shif t Superintendent
during the event was not apparent to the NRC observers.
'
Mr. Martin informed the Vice President (VP) of Operations, while
still in the Control Room,
that the NRC staff was concerned that
i
the operators did not follow their procedures and manually trip
,
l-
the reactor .when pressurizer level
fall below 174.
The VP
acknowledged the concern, indicated they would review the event and
offered no explanation for the operators' actions.
The NRC observers remained in the Control Room until the reactor
coolant pumps were restarted and the plant war again stable.
At
.
no time during the event did NRC personnel grab a licensed
individual, raise their voices or manipulate the controls. The NRC
,
l
observers' concern during the entire event was that their was no
,
safety reason for not following the procedure; therefore, it should
-
have been followed.
NRC actions were predicated on their concern,
the fact that we were not authorized to order licensed activities
and that, in this instance, the reactor was never in danger.
Subsequently, Mr. Trapp and Mr. Dudley were directed by Mr. Martin
to observe the
post trip reviews to assess licensee performance,
but not to parttcipate in the licensee's deliberations.
l
1
,
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.
JUN 2 71989
{
-
1
MEMORANDUM FOR:
William F. Kane, Director
Division of Reactor Projects
FROM:
William T. Russell
Regional Administrator
.
SUBJECT:
AUGMENTED INSPECTION TEAM ( AIT) - MANUAL REACTOR TRIP
DURING NATURAL CIRCULATION TEST AT SEABROOK STATION UNIT 1
3
You are directed to perform an Augmented Inspection Team (AIT) review of
the causes, safety implications, and associated licensee actions which led to
and followed, both immediately and subsequently, the manual reactor trip that
,
occurred during the natural circulation test at Seabrook Station Unit 1 on
'
June 22, 1989.
The inspection shall be conducted in accordance with NRC
Manual Chapter 0513, Part III, and additional instructions in this memorandum.
DRP is assigned responsibility for the overall conduct of this inspection. Jim
Wiggins is designated as the Regional Team Manager and Peter Eselgroth as the
onsite Team Leader.
The Team will also include participants from the Division
of Reactor Safety and from NRR.
OBJECTIVE
The general objectives of this Ali are to:
a.
Conduct a timely, thorough, and systematic review of the circumstances
surrounding the June 22, 1989 event;
b.
Collect, analyze, and document all relevant data and factual information
~
to determine the causes, conditions, and circumstances pertaining to the
event, including the response to the event by the operations and
technical support staffs and by licensee management;
c.
Assess the safety significance of the event and communicate to Regional
management the facts and safety concerns related to the problems
identified; and to
d.
Evaluate the adequacy of the licensee's internal post-trip review of the
event.
.
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Memorandum for William F. Kane
2
4
SC0pE OF THE IN$pECTION
j
The AIT response should identify and document the relevant facts and determine
the probable causes of the event.
It should also critically examine the
licensee's response to the event. The Team Leader will develop and implement
a specific, detailed inspection plan addressing this event upon his arrival
onsite.
-
As a minimum, the AIT should:
a.
Develop a detailed chronology of the event;
b.
Determine the root cause(s) of the event;
'
c.
Determine the expected response of the plant during a transition to
natural circulation cooling and compare it to the actual plant dynamic
response observed during the event;
d.
Assess the adequacy of the training and briefings provided by the
licensee to its staff in preparation for the natural circulation test;
e.
Assess the adequacy of the responses of the operations and technical
support staffs to the event;
f.
Assess the scope and quality of the licensee's internal review of the
event, including its initial (preliminary) and final (detailed) post-trip
review; and,
'
g.
Assess the scope and quality of short-term actions and gather information
l
related to the long-term actions intended to prevent recurrenes of the
"
i-
event, including internal and external communication / dissemination of
licensee-identified concerns and corrective actions.
SCHEDULE
The AIT.shall be dispatched to Seabrook Station so as to arrive and commence
,
the inspection no later than 9:00 a.m. , June 28, 1989. A written report on this
inspection will be provided to me within 3 weeks of completion of on-site
I
inspection ef fort.
.
1
l
l
,
,
_. _ . . _ _
.
.
_ _ _ _ ,
,_
-
-
Memort.ndum for Willian. F. Kane
3
!'
'
,
'
F
b
' TEAM' COMPOSITION.
I
The assigned Team meabers are as follows:
James Wiggins', RI
Regional Team Manager
-
L
Onsite Team Leader
Peter Eselgroth, R1
-
'-
Onsite Team Members
Noel Dudley, Senior Resident' Inspector
-
James Trapp, RI
.
Lambros Lois, NRR/SRXB
Fred Guenther, NRR/LOLB
I
h
.,
William T. Russell
Regional Administrator
,
I
cc:
S. Varga, NRR
'R. Wessman, NRR
T. Martin, DRA
'S, Collins, DRP
B. Boger, DRS
,
,
Teat, Members
e
6
9
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'1
['.
' APPENDIX H
(.
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Pl. ANT AND EQUIPMENT PERFORMANCE
..
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APPENDIX I
,
ACRONYMS AND INITIALISMS
i
I
AIT.
Augmented Inspection Team
CAL.
Confirmatory Action Letter
-
i
CFR
Code of Federal Regulations
,
'
CR0
Control Room Operator
E0P
Emergency Operating Procedure
Final Safety Analysis Report
i
GETARS
General Electric Transient Analog
Recorder System
I-ST-22
Natural Circulation Special Test
Magawatts
MWt
Megawatts thermal
Normal Operating Pressure
- .
NOT
Normal Operating Temperature
NPMN-
Nuclear Production Management Manual
OPMM
Operations Management Manual
PSNH-
Public Service of New Hampshire
PZR
Pressurizer
SCRO.
Senior Control Room Operator
!
'
50RC
Station Operative Review Committea
Shift Supervisor-
SSMM
Seabrook Station Management Manual
STPD
Start Test Program Description (STPD)
.
Tc
Primary Coolant Cold Leg Temperature
TD
Test Director
i
T
Primary Coolant Hot Leg Temperature
'
H
Tavg
Average Primary Coolant Temperature
!
USS
Unit Shift Supervisor
l
Vice President
'
1
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i
ENCLOSURE 2
,
Enforcement Conference Issues and Related Regulatory Requirements
1.
The* following activities appear to be contrary to:
Criterion V, requiring adherence to appropriate procedures; to 10 CFR 50,
Appendix B, Criterion XI requiring adherence to test procedures; to Final
,
Safety Analysis Report (FSAR) Section 14.2 specifying that 1) the initial
startup program be administered in accordance with an approved startup
'
procedure, and 2) that Startup Test Direction personnel will perform
startup test coordination and direction functions; and to Natural Circu-
lation Startup Test Procedure 1-ST-22.
a.
During the performance of Startup Test Procedure 1-ST-22 on
June 22, 1989, pressurizer-level reached the 17% criterion requiring
a reactor trip in accordance with Attachment 9.3 to the procedure,
and the reactor was not tripped by the operating shift as required
(Report Details 5.1.4,5.1.5).
b.
Startup Test 1-ST-22 prerequisite 3.6.7 confirming the availability
of main steam dump valve MS-0V-3011 was signed of f despite the valve
not being properly ready to support the test because work order
WR87W005592, requiring a stroke test at normal operating temperature
'
and pressure, was still open (Report Detail 4.3.3).
The failure of
MS-PV-3011 during performance of 1-ST-22 initiated the June 22, 1989,
test transient,
c.
Startup Test 1-ST-22 pre-test briefings were not conducted as required,
in that the Test Step 3.2 provisions for personnel involved with pro-
cedure performance to be briefed on procedure condect and test per-
formance was not accomplished for one of the two control board oper-
ators assigned to assist the shift crew (Report Detail 5.2.4).
Fur-
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ther, the briefings which were conducted ware not appropriate because
they were conducted for individuals in a fragmented and abbreviated
manner and not for the operators as a group (Report Details 5.2.4,
5.2.6), because the shift supervisor's awareness and knowledge was
not commensurate with the significance and complexity of the test
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(Report Detail 5.1.5), and because the operators accepted violation
of a test procedure trip requirement (Report Detail 5.1.5).
These
conditions were evaluated as contributors to the June 22, 1989 fail-
ure to trip the plant as required by Startup Test 1-ST-22.
In addition, inasmuch as simulator training on the startup test program
was conducted in April and May of 1986 and classroom training on low
power testing was last conducted in September and October of 1988
(Report Details 5.1.2,5.1.5), a lack of recent training was a potential
additional contributor to the June 22, 1989 failure to trip the plant
as required.
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Enclosure 2
2
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4
d.
'During performance of Startup Test 1-ST-22 on June 22, 1989, the
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Startup Manager, Shift Test Director, and Test Director were present
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in the control room.
No interruption or termination action was in-
itiated by the Startup Organization when the 17% pressurizer level
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reactor trip criterion of Startup Test 1-ST-22 was. reached nor was
the operating staff counselled by the Startup Organization that a
reactor trip was required under the existing conditions (Report De-
tails 5.S.5, 5.2.6).
2.
The following appear to be contrary to: 10 CFR 50, Appendix B, Criterion
XVI which requires that measures be established te assure that conditions
adverse to quality be promptly identified and corrected, and to assure
that the cause for each significant condition adverse to quality and the
corrective action taken be reported to appropriate levels of management;
and to the FSAR Chapter 13.1.2.2 operating shift management. provisions;
and to the assignment of responsibilities for implementation of those pro-
visions in accordance with the Operations Management Manual,
a.
Subsequent to the June 22, 1989 failure to effect a plant trip during
conduct of Startup Test 1-ST-22, licensee management failed to
promptly resolve associated personnel performance failures (Report
Detail 5.3.3).
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b.
During performance of Startup Test 1-ST-22 on June 22, 1989, managers
present in the control room included the Operations Manager, who is
responsible for the operation of the unit's equipment in accordance
with approved station procedures, and the Assistant Operations Manager,
who directs the activities of the shift superintendents.
Both of
these managers have the authority to order a reactor shutdown and
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were observing Startup Test 1-ST-22 performance in the control board
area (Report Detail 5.3.2).
Neither of these managers effectively
implemented his oversight. responsibility during the test.
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