ML20133A546

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Insp Rept 50-443/96-10 on 961001-1129.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering,Plant Support & Assurance of Quality
ML20133A546
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 12/24/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20133A513 List:
References
50-443-96-10, NUDOCS 9612310160
Download: ML20133A546 (21)


See also: IR 05000443/1996010

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION I

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Docket No.:

50-443

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. License No.:

NPF-86

Report No.:

50-443/96-10

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Licensee:

North Atlantic Energy Service Corporation

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Facility:

Seabrook Generating Station, Unit 1

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Location:

Post Office Box 300

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Seabrook, New Hampshire 03874

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Dates:

October 1,1996 November 29,1996

Inspectors:

John B. Macdonald, Senior Resident inspector

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David J. Mannai, Resident inspector

Accompanied by:

Javier Br'and, Resident inspector intern

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Approved by:

John Rogge, Chief, Projects Branch 8

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Division of Reactor Projects

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9612310160 961224

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EXECUTIVE SUMMARY

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Seabrook Generating Station, Unit 1

NRC Inspection Report 50-443/96-10

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a 7-week period of resident inspection.

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Operations:

The licensee response to the NRC identification of the presence of temporary

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shipping caps in the spare conduit ports of several pressure transmitters has been

excellent. The caps have been in place since original transmitter installation and are

inconsistent with vendor manuals. However, due to the specific transmitter

applications and environmental qualification classifications, instrument operability

was not effected. The licensee decision to establish a task force to verify or

establish proper configuration for a significant sample population of currently

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installed transmitters reflected sound issue scope and initial cerractive action

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perspectives.

In sharp contrast to the corrective actions perspectives evidenced above, the

licensee failed to talo :.,rompt or comprehensive initial corrective actions to

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concerns initially raised by the Nuclear Safety Audit and Review Committee

(NSARC) in March 1994 regarding the lack of performance of a 10 CFR 50.59

safety evaluation for a procedure revision that established new operational and

configuration parameters for the emergency feedwater (EFW) system. Ultimately,

the licensee properly evaluated the et,ncern, determined the EFW system

configuration established by the procedure revision to be outside the design- and

licensing-bases of the station, and reported the occurrence to the NRC in

accordance with 10 CFR 50.72 and 50.73 reporting criteria. However, because

initial corrective actions were neither prompt nor adequate, the failure to perform an

adequate evaluation when the subject procedure was revised is cited as a violation

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of the requirements of 10 CFR 50.59.

Control room operators alertly identified initial indications of potential primary

reactor coolant system to secondary system leakage. Chemistry samples verified

the presence of a minor leak of approximately 1.0 gallons per day (gpd) in the "C"

steam generator (SG), which is a small fraction of the technical specification limits

of 500 gpd through any one SG and 1.0 gallons per minute (gpm) through all four

SGs. Throughout the report period, the leakage rate varied from less than

detectable levels to approximately 1.0 gpd. Station management developed a well-

coordinated response to the initial leakage, and established conservative

administrative response actions in the event of increased leakage.

Maintenance:

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System engineers effectively evaluated the potential adverse effects of oilintrusion

into the emergency diesel generator (EDG) barring device micro-switches.

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Executive Summary (Cont.)

Continuing evaluation identified a component upgrade to make the switches less

vulnerable to foreign materialintrusion.

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The work plan for the attempted leak sealant repair of a steam line instrument root

valve was effectively supported by engineering evaluation that considered

appropriate American Society of Mechanical Engineers (ASME) Code requirements

and valve design and application information. Good independent quality oversight

of the work effort was evidenced when a quality control (OC) inspector identified

that a drill stop had been improperly set. Field supervision properly terminated the

repair attempt when it was determined that physical interferences would prevent

successful completion of the intended repair. A subsequent repair plan was

developed and successfully implemented.

A Licensee Event Report (LER) and its supplement (LER 96-03 and 96-03-01)

regarding EFW pump mechanical seal failure properly addressed the reporting

criteria of 10 CFR 50.73.

Enaineerina:

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Diagnostic motor operated valve (MOV) testing of containment building spray (CBS)

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valve, CBS-V 43, was well controlled. The replacement of'the actuator gear set to

restore assumed operational performance and design-bases margin was well

controlled and effectively implemented.

Plant Sunoort:

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Radiological protection program controls were observed to have been properly

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implemented. Workers were noted to be complying with established procedures

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and controls. Chemistry personnel effectively supported the initial verification and

subsequent monitoring of the minor primary to secondary system leakage.

A previously issued safeguards violation (50-443/96-02 03) regarding the lack of a

continual behavior observation program for contractors with unescorted access who

are absent from the station for extended periods (greater than 30 days) was closed

following a review that determined appropriate corrective actions had been

implemented to the access authorization and control processes.

Assurance of Quality

Overall, station management demonstrated good oversight of issues important to

safety as well as to corrective action processes. Response to the initial indications

of primary to secondary leakage were prompt and well coordinated, increased

monitoring intervals and administrative limits were established that were

significantly more conservative than existing station procedural or regulatory

requirements.

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Executive Summary (Cont.)

The management decision to form a task force to verify or establish appropriate

instrument transmitter configurations reflected sound corrective action practices.

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Additionally, controls established to ensure proper conduct of an in-plant temporary

leak sealant repair effectively identified and ensured correction of improper tool

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settings prior to the initiation of the field work.

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However, station management did not aggressively ensure the timely technical

resolution of the NSARC concern initially raised in March 1994, regarding the

implementation of a revision to the startup feedwater pump (SUFP) operations

procedure without performance of a 10 CFR 50.59 safety evaluation it took

approximately two years of persistent effort on the part of the NSARC to heighten

the concern sufficiently before a detailed safety evaluation determined the

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procedure revision had authorized the establishment of an EFW configuration that

was outside the original design basis of the system.

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TABLE OF CONTENTS

EX ECUTIVE SUM M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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T AB LE O F CO NTENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

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1. Operations

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Cond uct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ,

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01.1 General Comments (71707)

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Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . . . . 1

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O 2.1 Transmitter Configuration Control (IFl 50-44 3/9 6-10-01 ) . . . . . . . . . . . . 1

O2.2 Turbine-Driven Emergency Feedwater Pump Exhaust Line Painting . . . . . 2

02.3 Indication of Primary to Secondary System Leakage . . . . . . . . . . . .

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Quality Assurance in Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

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07.1

(Closed) LER 96-04, " Emergency Feedwater System Valve Closure"

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(VIO 50-443/96-10-02)

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11. Maintenance

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Conduct of Maintenance

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M 1.1 EDG Barring Device Micro-switch

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M1.2 Leak Sealant repair

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Miscellaneous Maintenance issues

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M8.1 (Closed) LER 96-03 and LER 96-03-01, " Emergency Feed Water Pump

Mechanical Seal Replacement" . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

lll . En g in e e ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

E2

Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . . 11

E2.1

MOV Diagnostic Testing . . . . .

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IV. Plant Support

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R1

Radiological Protection and Chemistry Controls

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R 1.1

General Comments

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Conduct of Security and Safeguards Activities . . . . .

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S1.1 General Comment (71707, 71750) . . . . . . . . . . . . . . . . . . . . . .

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Quality Assurance in ' Security and Safeguards Activities .

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Closure of Previously identified Violation . . . . . . . . . . . . . . . . . .

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V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . .

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Table of Contents (Cont.)

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Exit M eeting Sum m a ry . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

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Other NRC Activities

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PARTI AL LIST OF PERSONS CONTACTED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

INSPECTION PROCEDURES USED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

LIST OF ACRONYMS USED

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REPORT DETAILS

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Summarv of Plant Status

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The facility operated at approximately 100% of rated thermal power throughout the

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inspection period with routine minor power reductions performed to support instrument

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calibrations and turbine valve testing. On November 25,1996, initialindications of

primary to secondary leakage were identified.

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l. Operations

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Conduct of Operations

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01.1 General Comments (71707)

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Using inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, routine operations were performed in

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accordance with station procedures and plant evolutions were completed in a

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deliberate manner with clear communications and effective oversight by shift

supervision. Control room logs accurately reflected plant activities and observed

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shift turnovers were comprehensive and thoroughly addressed questions posed by

the oncoming crew. Control room operators displayed good questioning

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perspectives prior to releasing work activities for field implementation. The

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inspectors found that operators were knowledgeable of plant and system status.

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Operational Status of Facilities and Equipment

a.

Insoection Scone (71707,62707)

The inspectors routinely conducted independent plant tours and walkdowns of

selected portions of safety-related systems during the inspection report period.

These activities consisted of the verification that system configurations, power

supplies, process parameters, support system availability, and current system

operational status were consistent TS requirements and UFSAR descriptions.

Additionally, system, component, and general area material conditions and

housekeeping status were noted.

02.1 Transmitter Configuration Control (IFl 50-443/96-10-01)

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Observations and Findinas

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On October 8,1996, during an independent tour of the service water (SW) pump

house, the inspectors noted that plastic foreign material exclusion (FME) shipping

caps were installed in the spare conduit ports on SW system pressure transmitters,

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1-SW-PT-8272 through 8274 and 1-SW-PT-8282 through 8284. This observation

was brought the attention of plant management who directed appropriate

engineering personnel to review this condition. Engineers subsequently verified that

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temporary shipping caps were installed in the subject transmitters and ACR 96-

1002 was generated.

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The SW pump house area where the subject transmitters are located, environmental

zone SW-1, is classified as a mild environment with respect to the station

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environmental qualification program required by 10 CFR 50.49. This classification

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does not specifically require that moisture accumulation at the terminal side of the

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transmitter housing be prevented by means such as a qualified environmental seal.

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Nonetheless, the vendor manual for the subject transmitter model, Rosemount 1153

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series-manual FP73280, directs that unused conduit ports be closed off with a

stainless steel pipe plug, with threads sealed by pipe thread sealant. Therefore,

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work request, WR 96 WOO 2012 was initiated to replace the plastic FME shipping

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plugs with stainless steel pipe plugs per the transmitter manufacturer specifications.

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The ACR evaluation was expanded by the licensee to inspect and verify or establish

as necessary the proper configuration of a population of 523 currently installed

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process transmitters. The licensee concluded this action was appropriate due to the

diversity of transmitter models and designs that could be installed in various service

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applications. A dedicated task force was established, with projected milestones of

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December 15,1996 for the completion of in-plant inspections and January 13,

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1997 for project completion and task force report issuance.

The inspectors have met w.i.1 the task force leader several times to verify project

scope, assurance of quality, incorporation of potential lessons learned into proper

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program processes, and to maintain status of observations. At the conclusion of

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the inspection report period, the task force had not identified any transmitter

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discrepancy that effected instrument operability or environmental qualification.

However, several minor deficiencies such as loose junction box door clamps,

missing qualification tags, and missing end caps for instrument drain line tubes had

been identified,

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Conclusions

The shipping caps that the inspector identified installed in the spare conduit ports of

the SW pressure transmitters have been in place since original installation.

Although these caps do not conform with vendor specifications, their installation in

this specific application does not effect instrument operability or qualification.

The licensee demonstrated excellent causal and corrective action analysis by

establishing a dedicated task force to provide positive verification of the design-

bases configuration requirements for a significant sample population of transmitters

currently installed in the station. Review of the final task force report and any

subsequent corrective actions will be tracked by an inspector follow-up item (IFl 50-

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443/96-10-01).

02.2 Turbine-Driven Emergency Feedwater Pump Exhaust Line Painting

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Observations and Findinas

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On October 11,1996, during a system walkdown with the system engineer, the

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inspector identified that the turbine-driven EFW (TDEFW) pump steam exhaust

piping had been painted blue. The color code procedure, SM 7.2, " Station Labeling

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Program," indicates that this piping should be painted white. More significantly, the

inspector questioned if the paint was qualified to the temperatures expected to be

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experienced in the exhaust line during design-bases operation of the TDEFW pump.

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ACR 96-1040 was initiated.

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The licensee provided a turbine specification sheet that indicated fullload exhaust

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temperature would be 235* Fahrenheit (F). Vendor specifications for the paint

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indicated the primer coat was temperature resistance rated to 350* F and the finish

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coat of colored paints are rated to 250

F.

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Conclusions

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The incorrect paint color coating for the TDEFW pump turbine exhaust line was of

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negligible significance. Additionally, the inspector verified that the labeling program

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had properly considered process piping temperatures in determining the chemical

qualities for the paint products. The inspector had no further questions regarding

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this issue.

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02.3 Indication of Primary to Secondary System Leakage

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a.

Insoection Scoce (71707)

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On November 25,1996, control room operators noted indications of potential

primary or reactor coolant system to secondary system leakage. At approximately

3:00 a.m., operators were preparing to regenerate a blowdown system cation filter

bed when the "C" SG blowdown radiation monitor alarm briefly went into the alert

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range. The alarm quickly cleared, however at approximately 8:00 a.m., the alarm

again went into alert and remained at slightly above normal readings. The operators

promptly notified chemistry and entered the off-normal procedure OS 1227.02,

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" Steam Generator Tube Leak." Chemistry initiated secondary system sampling with

increased frequency in accordance with procedure, CS 0905.08A. The inspector

reviewed Technical Specification (TS) 3.4.6.2, associated with reactor coolant

system leakage, procedure OS 1227.02, NUREG/CR-6365 " Steam Generator Tube

Failures," and held discussions with Chemistry Department personnel and senior

station management.

b.

Observations and Findinas

Chemistry confirmed the presence of a primary to secondary leak in the "C" SG by

use of gaseous isotopic analysis and determined the leak rate was very small

(approximately 1.0 gpd). TS 3.4.6.2 limits reactor coolant system leakage to 1.0

gpm total reactor-to-secorJary leakage through all Sgs and 500 gpd through any

one SG. The licensee prcmptly and aggressively began a thorough evaluation of the

indications of SG tube leakage. Senior station management provided strong

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oversight of and involvemei.t :T. :"aluation of the tube leak and development of

corresponding response strategies and contingencies. The station sought the most

current industry experience on SG tube leaks and contacted SG experts at

Westinghouse. The licensee established sampling and operational controls that

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were significantly more conservative than both general industry standards that had

been established by the Electric Power Research Institute (EPRI) guidance (150 gpd

totalleakage, rate of change of greater than 60 gpd in one hour shutdown criteria)

and TS requirements (500 gpd). An administrative limit of 60 gpd for initiating a

plant shutdown was imposed. Additionally, contingency repair plans were under

development to repair the source of the leakage during the next refueling outage or

sooner if conditions should sooner necessitate a forced shutdown. Frequent

briefings were conducted to inform station management of the status. At the

conclusion of the inspection report period, the SG tube leak had stabilized at

approximately 0.2 gpd.

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Conclusions

The inspectors determined the licensee response to the tube leak was prompt,

thorough, and conservative which demonstrated sound safety perspectives. The

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licensee used recent industry information when developing response strategies,

which was considered very prudent given the industry experience with SG tube

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leaks and the sometimes rapid leak rate increase from a few gpd to several hundred

in a short period of time. The operators alertly responded to the radiation data

management system (RDMS) alarms. The inspectors observed good coordination

between the chemistry, health physics, and operations departments. Senior station

management involvement was strong and ensured appropriate station response.

The inspectors had no further questions.

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Quality Assurance in Operations

07.1 (Closed) LER 96-04, " Emergency Feedwater System Valve Closure"

(VIO 50-443/96-10-02)

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Inspection Scope (71707.40500)

On July 24,1996, the licensee submitted LER 96-04 which documented that

evaluations, completed on June 27,1996, had concluded that the alignment of the

startup feedwater pump (SUFP) to the steam generators (Sgs) via the emergency

feedwater (EFW) flow control valves for non-emergency operation was an

unanalyzed condition that significantly compromised safety. On June 27,1996,a

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one-hour non-emergency notification was made to the NRC operations Center in

accordance with the requirements of 10 CFR 50.72.

The inspector reviewed numerous documents that recorded the development of this

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issue from the initial identification of a concern in 1991 through issuance of LER 96-

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04. Documents of significant import included:

Station Information Report (SIR)91-036, dated December 6,1991

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Root Cause Analysis for SIR 91-036, No.91-013, dated January 31,1992

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UFSAR Section 6.8, " Emergency Feedwater System"

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TS Section 3.7.1.2, " Auxiliary Feedwater System"

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ON 1034.03, " Condensate System Operation" Rev 3, change 13

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OS1035.02, "Startup Feed Pump Operation," Rev 7, change 01-04

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TS Clarification, TS-148, " Emergency Feedwater System Operation"

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ACR 95-511, dated December 13,1995

Yankee Atomic Memo, " Review of ACR 95-511," dated May 24,1996.

Additionally, several Nuclear Safety Audit and Review Committee (NSARC) meeting

minute reports and correspondence to and from the NSARC and plant staff were

reviewed.

b.

Observations and Findinas

On April 2,1991, feedwater check valve, FW-V-330, did not stroke freely with the

plant maneuvering in Mode 3 (HOT STANDBY). The normal condensate and

feedwater flow path was required to be isolated in order to f acilitate repairs to the

valve. Rather than placing the reactor in a shutdown condition, the licensee

established a configuration in which the SUFP was isolated and the steam

generators were fed by the condensate pumps via the EFW system, with level being

maintained by the EFW flow control and isolation valves. The configuration was

established by a revision (Change 13 to Revision 3) to station procedure ON

1034.03, " Condensate System Operation." The plant remained in this configuration

for approximately three days until repairs to the feedwater check valve were

completed and the normal feedwater flow path was restored. During this period of

time, the plant was in the action statement of TS 3.7.1.2, applicable in Modes

1,2,and 3, which limits continued operation in this configuration to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

On December 6,1991, SIR 91-036 was ganerated due to questions regarding the

potential for the off-normal feedwater aligament to be in conflict with high energy

line break evaluations. A root cause analysn evaluation for SIR 91 036 (91-013,

dated January 31,1992) concluded that the orocedure revision that authorized the

off-normal feedwater alignment lacked an adequate 10 CFR 50.59 evaluation and

that inconsistencies existed between various station manuals and procedures that

govern the performance of 10 CFR 50.59 evaluations and procedure revisions. In

part due to SIR 91-036, Technical Clarification (TC), TS-148, was issued May 28,

1992 and revised August 21,1992, that further supported operation of the EFW

system non-emergency SG level control in the off normal feedwater alignment.

On January 27,1994, station procedure, OS 1035.02, "Startup Feed Pump

Operation," was revised (Change 01 to Revision 07) to authorize operation of the

SUFP and EFW flow control and isolation valves to maintain SG water level during

normal plant operations. TS-148 was referenced as technical support for the

procedure revision. Shortly after, on March 30,1994, the NSARC Operations

Subcommittee (NSARC OC) questioned the adequacy of the procedure revision

evaluation at NSARC OC meeting No. 94-01, as documented in NSARC OC meeting

minutes memorandum dated April 8,1994. Specifically, the NSARC OC expressed

concern that the procedure revision was implemented without the performance of a

10 CFR 50.59 evaluation. Further, the NSARC OC expressed concern that the

revision used a TC to support the revision. Licensing management subsequently

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issued memorandum, LIC 94-0396, dated June 16,1994, that clearly defined the

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controls, instruction, and limitations of a given TC.

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As a result of continued apparent differing opinions between the NSARC OC and

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plant staff regarding the need for a 10 CFR 50.59 evaluation for the newly

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developed EFW system operation, the NSARC elevated the issue to the attention of

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the Station Manager for SORC resolution in the August 23,1994 NSARC meeting

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(94-11), as documented in the meeting minutes report dated August 23,1994.

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Two more NSARC meetings passed without resolution of the concern. It was not

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until April 13,1995, that the licensee confirmed the intention to perform a 10 CFR

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50.59 evaluation. The evaluation was performed in June 1995, however the

NSARC assessed the evaluation as weak, lacking in technical as well as design- and

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licensing-bases information. Due to the apparent lack of a success path on this

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issue, NSARC issued ACR 95-511 on December 13,1995.

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Ultimately on May 1,1996, at the direction of the Senior Site Officer acting as the

NSARC Chairman, Yankee Atomic conducted a comprehensive evaluation of ACR

95-511 as well as the historical documents on the procedure change. The

evaluation, " Review of ACR 95-511," dated May 24,1996, concluded that the

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procedure revision placed the EFW system in a configuration that was outside the

design- and current licensing basis for the plant. The evaluation determined that;

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operation of the EFW system in non-emergency modes contradicted past licensee

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statements and supporting licensing documents; operation with the EFW flow

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control and isolation valves throttled for non-emergency SG level control was not

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evaluated with respect to the UFSAR; and, TS 4.7.1.2.1.a.1 requires that the EFW

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flow control and isolation valves be open at all times during non-emergency plant

operations. The specific vulnerability involved a scenario in which the EFW flow

control and isolation valves would be shut to support the starting sequence of the

SUFP coincident with the receipt of a station blackout.

Licensee evaluation concurred with the Yankee Atomic review of ACR 95-511, and

on June 27,1996, the licensee notified the NRC in accordance with 10 CFR 50.72

of the unanalyzed EFW alignment. Immediate corrective actions included deleting

use of the EFW system for non-emergency SG level control. Other corrective

actions were directed at clarifying 10 CFR 50.59 requirements, issuing standing

orders that would reinforce that EFW flow control and isolation valves should not be

throttled, and revision to TS-148.

c.

Conclusions

UFSAR Section 6.8.1 states that the design basis for the EFW system is to provide

the capability to remove heat from the reactor coolant system during emeraency

conditions when the main feedwater system is not available, including small LOCA

cases. Additionally, for station blackout, the turbine-driven EFW pump will operate

during the four-hour coping period to cool down and maintain the secondary side

pressure at about 250 psig. This section further states that for all other modes of

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plant operation, including startup, hot standby, and normal operation up to full

power load, the EFW system is depressurized and has zero flow.

.

Additionally, the UFSAR Section 6.8.2 description of the EFW system states that

{

the open position of the flow control valves for system limiting conditions will be

I

set to insure the minimum flow of 470 gpm to three Sgs and a minimum total flow

j

of 650 gpm to four Sgs with one EFW pump operable. Further, the UFSAR Section

i

6.8.3 safety evaluation states that the flow regulating valves in each EFW line are

l

normally open, and are sized to pass the required flow under accident conditions.

The only action necessary to establish EFW flow is to start the pumps.

,

I

TS 3.7.1.2 states that in Modes 1,2, and 3 at least three independent steam

!

generator auxiliary feedwater pumps and associated flow oaths shall be operable.

I

i

The licenser

"isions to station procedures, ON 1034.03, " Condensate System

i

Operation," e Mril 1991 and OS 1035.02, "Startup Feed Pump Operation," in

January 19M. established procedural guidance authorizing non-emergency

feedwater flow paths to the Sgs through the EFW system, with SG level being

controlled by throttling the EFW flow control and isolation valves. The procedures

l

were revised without performance of safety evaluations consistent with the

!

requirements of 10 CFR 50.59 to determine if the changes involved an unreviewed

i

safety question as defined in 10 CFR 50.59. It is recognized that the plant has

l

actually been operated in the off-normal configuration authorized by ON 1034.03

'

one time from April 2-5,1991 and that the off-normal alignment authorized by OS

'1035.02 has never been established. Notwithstanding, the failure to perform safety

[

evaluations to determine if revision of procedures ON 1034.03 and OS 1035.02

i

involved an unresolved safety question as defined by 10 CFR 50.59 is a violation.

j

(VIO 50-443/96-10-02)

l

!

Several related aspects of this issue are of concern to the inspectors. Initially, the

!

NSARC and NSARC OS expressed obvious concern for the lack of a 10 CFR 50.59

l

evaluation with respect to the OS 1035.02 revision at meetings for approximately

[

two years beginning in March 1994, without satisfactory resolution. Ultimately, the

!

Senior Site Officer and NSARC chairman, on May 1,1996, directed that an

l

immediate resolution to the concern be achieved. Secondly, the licensee originally

justified the revision on the basis of a technical clarification, TS-148. When a

!

subsequent 10 CFR 50.59 safety evaluation was performed it was qualitative in

nature, lacking technical rigor supported by design and licensing basis information.

!

Finally, the corrective action processes, including resolution to NSARC issues

through initiation and resolution of associated ACRs, similarly lacked technical rigor

j

and were not prompt or timely. These issues were discussed in detail with licensee

management and will be addressed in the licensee response to the attached Notice

l'

of Violation.

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11. Maintenance

M1

Conduct of Maintenance

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M1,1 EDG Barring Device Micro-switch

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a.

Inspection Scoce (62707)

On October 7,1996, the inspector observed portions of the "A" EDG load test

being performed per station procedure EX 1804.001.

b.

Observations and Findinas

During a walkdown of the EDGs, the inspector noted that engine lube oil was

dripping directly onto the barring device lower micro-switches that are designed to

,

prevent a start of the EDG with the barring device engaged. There is an upper

l

(DGA/B-ZS BD1) and lower micro-switch (DGA/B-ZS BD2) for the barring device on

each engine; only the lower micro-switch would be vulnerable to the oil leakage

i

from the barring device. This observation was brought to the attention control room

)

personnel who directed appropriate system engineering personnel to evaluate this

observation.

)

1

5

System engineers verified the inspector observation and initiated ACR 96-1067,

'

- The licensee evaluation concluded that oil could enter the micro-switch casing and

potentially prevent the switch from functioning. The oilis non-conductive and does

not present an electrical short circuit potential. The primary micro-switch reliability

concern would be that the switch may remain in its current state position and not

respond to a change in barring device status. This concern presents minimal safety

concern because the upper micro-switch would be capable of actuating the

protective parallel circuit and prior to use of the barring device, the associated EDG

would be removed from service and other administrative and physical controls

would prevent automatic engine startup. Also should micro-switch remain in the

engaged position after the barring device is removed from the EDG, a common EDG

local annunciator and control room computer digital alarm point (Drawings 31087,

SH-E93/8a,b,f 1-NHY-503490, 506393, and 9763-M-510000) would provide

indication of the switch failure prior to returning the EDG to service.

System engineers contacted the micro-switch vendor, who indicated an optional

rubber boot was available to minimize the potential of foreign materials entering the

switch. An engineering work request was initiated for design engineering personnel

to evaluate installing the rubber boot seals. Additionally, WRs 96 WOO 2024 through

96 WOO 2027 were generated to correct the source of the oilleakage and to inspect

the micro-switches.

r

c.

Conclusions

!

!

It appeared that the minor oil leakage from the barring device had been present for

i

some time prior to being brought to the attention of the licensee by the inspector.

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The inspector reviewed micro-switch logic diagrams and concurred in the licensee

conclusion that failure of a micro-switch would be of minimal personnel or

equipment safety significance. Subsequent engineering evaluation of the condition

!

was thorough and identified a potential component enhancement involving the

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rubber boot seal for the micro-switches.

'

M1.2 Leak Sealant repair

a.

Inspection Scoce (62707.37551)

Previously during the second refueling outage (ORO2) main steam instrument root

valve, MS-V-56 was repacked with undersized packing. MS-V-56 is the root valve

for steam pressure transmitter FW-PT-544, which inputs to the safety injection and

steam line isolation two-out-of-three low steam line pressure logic. The transmitter

also provides post accident monitoring capability. The licensee controlled the root

valve on its backseat to limit packing leakage, however over the course of the

current operating cycle the packing performance had degraded. WR 96WOOO845

was generated to perform a temporary leak sealant injection repair of the packing

gland. The inspector reviewed the work request, applicable sections of Section XI

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of the ASME Code governing repair of ASME class components, station procedure,

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MS 0526.09, "On Stream Leak Repairs," discussed specific work-related controls

with cognizant engineers, and directly observed portions of the field work.

u.

Observations and Findinas

On October 29,1996, the licensee held a pre-evolution briefing, placed transmitter,

FW-PT-544, in bypass, and initiated the work activity. The actual physical work

was performed by contractor technicians with direct licensee supervision and

quality oversight. The injection preparation was a two step process involving an

initial drill of 0.312 inches to a depth of approximately 0.360 inches for the

installation of an injection valve followed by a center drill into the packing gland.

The depth of the initial drill was controlled by setting a drill stop. At a pre-

determined procedure hold point, license OC personnel alertly identified that the

contractor technician had improperly set the drill stop. The stop was properly set

and the initial drill was performed. However, due to physical interferences, the drill

was not perpendicular to the packing gland and the minimum specified injection

valve thread engagement of 3 turns could not be obtained.

The licensee supervisor suspended the work effort, engineering personnel evaluated

further repair options, and ACR 96-1114 was initiated. An initial operability

determination (OD) that was largely qualitative was rejected by operations

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management. A subsequent OD, ODF No.96-015, dated October 30,1996, that

was supported by design-basis assumptions and calculations was approved. The

OD concluded that with the drilled hole the valve maintains its original design

requirements and remains operable.

On November 13,1996, the licensee implemented WR 96 WOO 2299, that

performed an ASME Section XI code repair of the drilled hole. Following completion

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of the code repair, the WR directed closure of the root valve and sequential removal

of the packing gland follower nuts and cleaning of the follower stud threads and

attempting to make up all the free travel on the follower. This effort proved

successful and leakage from the packing gland was stopped.

c.

Conclusions

!

The initial packing gland leak repair plan was well developed, however it was of a

high degree of difficulty due to physical interferences. The repair plan was

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discussed in detail with NRC Region i ASME Code and temporary leak sealant repair

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specialists during a conference call on November 1,1996. Licensee QC personnel

provided excellent independent oversight as evidenced by the identification of the

improperly set drill stop.

Operations section management demonstrated good standards by rejecting the

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initial OD that lacked design- and operational-bases technical evaluation. The

subsequent OD was properly supported and approved.

The repair plan for the unsuccessful leak sealant attempt was well developed.

Notwithstanding, it appears that the work planning process initially overlooked the

,

less intrusive and technically challenging repair option of gland follower stud thread

cleaning which ultimately proved successful, in favor of the leak sealant repair

option. The inspector had no additional questions regarding this activity.

>

M8

Miscellaneous Maintenance issues

M8.1 (Closed) LER 96-03 and LER 96-03-01, " Emergency Feed Water Pump Mechanical

f

Seal Replacement"

On May 21,1996, with the plant operating at 100% of rated thermal power the

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TDEFW pump was rendered inoperable when sparks were observed emanating from

the outboard mechanical seal area during quarterly flow surveillance testing. The

seal was disassembled and determined to have been improperly installed during the

last refueling outage in November-December 1995. The licensee performed a

formal root cause analysis which concluded a mechanical seal design deficiency and

inadequate corrective actions for a previously identified event as the primary causes

for the event. A contributing cause was inadequate predictive maintenance

techniques. NRC Inspection Report 50-443/96-04 documented the event including

a Notice of Violation for the improper seal assembly.

The LER properly documented the event and contained the appropriate reporting

requirements of 10 CFR 50.72. Any further NRC inspection of this event will be

documented in follow-up of the violation and violation corrective actions response

documents. The inspector had no further questions regarding closecut of the LER.

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E2

Engineering Support of Facilities and Equipment

E2.1

MOV Diagnostic Testing

a.

Insoection Scoce (62707,37551)

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On October 22,1996, the licensee removed motor operated valve, CBS-V-43, from

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service to perform diagnostic testing. The MOV actuator is a Limitorque SMB-000

model. The design-bases functions of the valve are to automatically open on a "P"

i

signal to allow sodium hydroxide to gravity feed to the refueling water storage tank

(RWST) and to close to terminate transfer of the spray additive to the RWST. The

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inspector reviewed TS 3.6.2.2.b, RTS 96RM19204001, WR 96 WOO 2181, and

discussed various aspects of the work activity with involved personnel.

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b.

Observations and Findinas

1

Initially, the valve was removed from service and the appropriate actions per TS 3.6.2.2.b. thu limit continued operation with CBS-V-43 inoperable to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />,

were initiawd. Performing technicians identified minor discrepancies for limit switch

settings for valve position indicating lights. Additionally, technicians identified that

the Bellville washer stack for the spring pack was not properly configured. Each of

these discrepancies were corrected prior to completion of diagnostic testing,

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However, subsequent diagnostic testing identified that peak unseating force

exceeded predicted values, in order to restora design-bases margins to the

actuator, the motor pinion and worm shaft gear sets were replaced. Post-

maintenance diagnostic testing indicated that with the new gear sets installed that

approximately 114% of predicted design margins were restored to the actuator.

'

c.

Conclusions

The licensee appropriately and conservatively addressed each discrepancy and test

deficiency encountered. Replacement of the valve actuator gear set reflected sound

understanding and respect for reliability and design margin goals of the MOV

program established in response to NRC Generic Letter 89-10. The testing results

and corrective actions were discussed with the NRC Region 1 MOV specialist during

an October 24,1996 conference call.

Notwithstanding the above noteworthy technical performance, the inspectors

concluded that the licensee could have better planned for a contingency to replace

the actuator gear set based on other recent plant experience. Specifically,

diagnostic testing of the redundant flow path spray additive valve, CBS-V-38, had

recently been conducted with similar as-found reductions in design margins. In the

case of the CBS-V-38 valve adequate margins were restored by torque switch and

limit switch adjustments. Based on the similarity of valve design, operational

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application, and test experience, the licensee should have anticipated similar as-

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found test data for the CBS-V-43 valve. However, the on-line maintenance planning

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was largely focused on diagnostic test performance with an absence of meaningful

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initial engineering assessment for the potential for design margin reductions that

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would necessitate detailed reactive engineering support. The net effect of the lack

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of contingency planning.was a probable increase in the time that CBS-V-43

remained out of service. It should be noted that CBS-V-43 was returned to service

within the TS 3.6.2.2.b allowed outage time. The inspector had no additional

.

questions regarding this maintenance activity.

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IV. Plant Suonort

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R1

Radiological Protection and Chemistry Controls

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R1.1 General Comments

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a.

Inspection Scope

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During the inspection period the inspector toured the radiologically controlled area

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(RCA) on several occasions to observe radiological controls practices,

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b.

Observations and Findinas

The Seabrook Station radiological controls technicians at the RCA checkpoint were

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attentive and provided assistance to radiation workers to assure proper work

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practices were used when radiation workers signed in and out of the RCA. The

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inspector determined that radiation area postings were proper and well marked and

survey recults were current and posted properly. All personnel observed were

properly wearing dosimetry while in the RCA. A sampling of high radiation area

doors identified no discrepancies with locking or posting requirements.

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c.

Conclusions

The inspector determined that Seabrook Station was properly implementing the

station radiological controls program requirements in the areas inspected.

Radiological controls personnel were knowledgeable of station procedures and

provided good oversight of radiation workers. Department managers were observed

in the field observing and supervising department personnel.

$1

Conduct of Security and Safeguards Activities

S 1.1 General Comment (71707, 71750)-

The inspectors observed security force performance during inspection activities.

Protected area access controls were found to be properly implemented during

random observations. Proper escort control of visitors was observed. Security

3

officers were alert and attentivo to their duties. Of particular note, the inspectors

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consistently found that security force members performing compensatory post

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duties during security computer power supply upgrades to be fully aware of watch

requirements.

P7

Quality Assurance in Security and Safeguards Activities

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P7,1

Closure of Previously identified Violation

(Closed) VIO 50-443/96-02-03: The licensee failed to effectively implement a

developed procedure which addressed contractors with unescorted access into the

protected area that are away from Seabrook Station for more than 30 days and

have not been under a continual behavioral program.

With respect to the above violation, the inspectors determined that the corrective

actions described in the licensee's May 24,1996 letter, in response to the NRC's

Notice of Violation, were reasonable, complete, and appeared to be effective.

V. Manaaement Meetinas

X1

Exit Meeting Summary

,

The inspectors presented the inspection results to members of licensee

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management, following the conclusion of the inspection period, on December 23,

1996. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified.

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X3

Other NRC Activities

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Conference calls between NRC managers and technical staff specialists and licensee

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managers and technical staff leads we,re performed on the following dates.

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October 24,1996-To discuss technical aspects of the MOV diagnostic test

results and subsequent repairs to CBS-V-43. (Section E2.1)

November 1,1996-To discuss technical aspects of the temporary leak

sealant repair of main steam instrument root valve, MS-V-56. (Section

M1.2)

November 15,1996-To perform a final exit for an MOV inspection. The

results of the inspection will be documented in a combined NRC Inspection

Report.

.

November 27,1996 To discuss technical aspects of the indication of primary

to secondary leakage. (Section 04.1)

)

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

W. Diprofio, Unit Director

G. Kline, Technical Support Manager

R. White, Design Engineering Manager

J. Peterson, Maintenance Manager

J. Gnllo, Operations Manager

B. Seymour, Security Manager

W. Leland, Chemistry and Health Physics Manager

NRC

Albert W. DeAgazio, Project Manager

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INSPECTION PROCEDURES USED

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IP 37551:

Onsite Engineering

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IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing

Problems

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IP 61726:

Surveillance Observation

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IP 62707:

Maintenance Observation

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IP 64704:

Fire Protection Program

IP 71707:

Plant Operations

)

IP 71750:

Plant Support Activities

IP 73051:

Inservice Inspection - Review of Program

IP 73753:

Inservice Inspection

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IP 83729:

Occupational Exposure During Extended Outages

IP 83750:

Occupational Exposure

IP 92700:

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

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Facilities

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IP 92902:

Followup - Engineering

IP 92903:

Followup - Maintenance

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IP 93702:

Prompt Onsite Response to Events at Operating Power Reactors

ITEMS OPENED, CLOSED, AND DISCUSSED

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Ooened

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Inspector Follow-up Item 50-443/96-10-01, " Review of Transmitter Configuration Task

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Force Report"

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Violation 50-443/96-08-01, " Failure To Perform 10 CFR 50.59 Safety Evaluation"

)

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Closed

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LER 96-04, " Emergency Feedwater System Valve Closure," dated July 24,1996

LER 96-03, " Emergency Feedwater Pump Mechanical Seal Replacement," as supplemented

September 12,1996

,

Violation 50-443/96-02-03, " Failure to establish access controls for contractors with

unescorted access who would be absent from the site for more than 30 days

Discussed

None

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LIST OF ACRONYMS USED

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ACR

Adverse Condition Report

ASME

American Society of Mechanical Engineers

CAS

Central Alarm Station

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CBS'

Containment Building Spray

EDG

Emergency Diesel Generator

[

EFW

Emergency Feedwater

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FME

Foreign Material Exclusion

gpd

gallons per day

.

gpm

gallons per minute

!

LCO

Limiting Condition for Operation

!

MOV

motor operated valve

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MPCS

Main Plant Computer System

'NSARC

' Nuclear Safety and Audit Review Committee

!

NSARC OS

NSARC Operations Subcommittee

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psig

pounds per square inch gauge

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QC

Quality Control

RHR

Residual Heat Removal

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SG

Steam Generator

SIR

Station Information Report

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SORC

Station Operations Review Committee

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SUFP

Startup Feedwater Pump

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SW

Service Water

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TDEFW

Turbine Driven Emergency Feedwater Pump

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TS

Technical Specifications

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UFSAR

Updated Final Safety Analysis Report

WR

Work Request

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