ML19312E503

From kanterella
Jump to navigation Jump to search
LER 80-024/03L:on 800430,while Making Containment Insp, Discovered Cracked Weld on 11B Reactor Coolant Pump Control Bleedoff Line.Caused by Metal Fatigue Induced by Vibration. Pipe Replaced & Weld Repair Performed
ML19312E503
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 05/30/1980
From: Davis S, Huseby D
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19312E497 List:
References
LER-80-024-03L-01, LER-80-24-3L-1, NUDOCS 8006050035
Download: ML19312E503 (1)


Text

- ._ - _-

LICENSEE EVENT REPORT 4

i

] CONTnOL sLOC:e I i l l 1  ! Ih (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1140l@l 5 7 G A T 68l@

l lo ! t8 l9l M iLICENSEE 7

D l CCCOE l C I N ! 115 l@l 010 l- uCENst to l010101010 Nuv8ER l- 101025 l@l4 26 l1uCEN5E 11 IlTYPE CON'T 10111 5$$lLj@l0ISl010l0l31117}@l014[3101810l@l0151310lBiOl@

OOCKET NUM8 gn 68 69 EVENT DATE 14 75 AEFORT DATE 80 7 8 60 63 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1012l l AT 0515 UHILE MAKING A CONTAINMFNT TN90rCTTOM TuF OpF?ATnP nicenVrQrn fi l I

10 31 I CRACKED WELD ON 11B REACTOR COOLANT PUMP (RCP) CONTROL BLEED 0FF LINE 1o44Il(T.S. 6.9.1.9.d). SINCE THE LEAK COULD fl0T BE ISOLATED FROM THE RCP SEAL I lo J s1 LTHE REACTOR WAS PLACED IN COLD SHUTDOWN TO FACILITATE REPAIRS. THE IWELD I

l o le 1 l REPAIRED AND THE UNIT RETURNED TO SERVICE AT 1910 Ori E/5/80. THIS IS NOT I

I o I 7 I I A REPETITIVE OCCURRENCE.

l 10181I

' CooE C $E sueci!E COM*CNENT CODE sL8C Of S E lol9l 7 8 9 l Cl Bl@ lE l@ lC l@ l Pl Il Pl El Xl Xl@ l Al@ l Zl@

to 11 12 13 18 1y 20 EVENT VE AR REP RT C CCE Y LE A RO

@ gegT l 8l Ol l-l 10 12 l 4 l l/l 1013! lLl l-l l bl 21 22 23 24 26 27 28 29 30 31 32 K N ACT ON O #LANT VET NOUAs sB i 80A .. sP 1 MAN FACTURER lBl@lZl@

JJ 34 lCl@

36 l Zl@

Jo_

l 0l 01 0l 01 3 40 U@

el l42 Yl@ l43Ni@ lBl518l0l@

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTICNS l

lt I o 11 THIS CRACK WAS LOCATED IN THE HEAT AFFECTED ZONE OF THE WELD JOINING THIS 4" f

li t i l I LONG.1" DI AfdETER. SCHED. 80 SP0OL TO THE SEAL. APPARENT CAUSE WAS METAL FATIGUE l

, I i I 2 I I TNnurCD BY VIBRATION HFAT-UP/COOLDOWN CYCLES . AND/OR BRITTLENESS FROM WELDING I

ii t3l l ON INITIAL INSTALLATION. THE FAILED PIPE WAS REPLACED AND A WELD REPAIR FERFORMED.

t

! I ENGINEERING REVIEW AND EVALUATION HAS BEEN INITIATED. J Ii i4 i C'

'sTAh'E v ooEa eTwf a status @ eisEtifv' oiscovEav oEsCai Tion @

li15llDl@ l0l0l0l@ln

' '2 NA u

l lBl@lOPERATOROBSERVATION

.. .0 I

Ainviry Co'R1E Nr LOCATION OF RELEASE l1 AELEAsED OF RELE AsE l6' l* l7 l@lZl@l AMOUNT OF ACTIVITv NA l l NA _j

,EaseNNEL ExecsSEs

~uveia Tv,E CEsCai,TiaN @

li 17110 lo 10 l@lLj@l NA i

, Eases ~E'L ,wULs Nuv.E. oEsCai, Tion @

l li la *l l0 lo 10 l@l NA l kss,an cagyAc,E ,o rACiufv g l

l'isi 8IT 7 9 l@l 10 NA 80

'SsV E 1 : 101 I N [@ l DESCRIPTIONNA l i lli!!!l111!li 68 39 80 ;

7 8 9 to S. M. DAVIS /D. E. HUSEBY PHONE: (3011?60 4742/4R16 2 NAME OF PREPAAER 800605OQ3y

.. - . .. - - - - _. .. __