ML021610713
ML021610713 | |
Person / Time | |
---|---|
Site: | Cook |
Issue date: | 06/10/2002 |
From: | Dyer J NRC/RGN-III |
To: | Bakken A American Electric Power Co |
References | |
EA-01-286 IR-01-017 | |
Download: ML021610713 (54) | |
See also: IR 05000315/2001017
Text
June 10, 2002
Mr. A. C. Bakken III
Senior Vice President
Nuclear Generation Group
American Electric Power Company
500 Circle Drive
Buchanan MI 49107
SUBJECT: D. C. COOK NUCLEAR POWER PLANT, UNITS 1 AND 2
NRC SPECIAL INSPECTION REPORT 50-315/01-17(DRP);
50-316/01-17(DRP); PRELIMINARY YELLOW FINDING
Dear Mr. Bakken:
On May 17, 2002, the NRC completed a Special Inspection at your D.C. Cook Nuclear Power
Plant regarding the essential service water (ESW) debris intrusion event of August 29, 2001.
The Special Inspection was conducted in accordance with the guidance of NRC Management
Directive 8.3, NRC Incident Investigation Program, Inspection Procedure 71153, Event
Followup, and Inspection Procedure 93812, Special Inspection. The enclosed report
documents the inspection findings which were discussed on May 17, 2002, with you and
members of your staff.
On August 29, 2001, Unit 1 was in cold shutdown and Unit 2 was operating at power when your
staff shut down the Unit 1 circulating water system for maintenance. Subsequent to the Unit 1
circulating water system shutdown, cross-flow currents within the common intake structure
caused significant amounts of debris to be entrained in the ESW system. Due to an unknown
pre-existing fault in the Unit 1 East ESW pump strainer basket, which allowed bypass flow, and
your practice of operating the ESW system fully cross-connected between both trains on both
units, the debris was transported throughout the ESW systems of both units, fouling most of the
heat exchangers dependent upon ESW. Because most components supplied by ESW were in
standby, this fouling continued undetected for approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />. Operators then
identified the problem during a scheduled, routine, quarterly surveillance of the ESW system in
Unit 2. A review of available data indicates that the emergency diesel generator (D/G) heat
exchangers appeared to be most limiting components for debris fouling. The flow to one D/G
decreased below the level of reliable indication, flow to two D/Gs decreased to 40% of nominal
flow with a declining trend, and the flow to the remaining D/G flow leveled out at approximately
40% of nominal flow. After discovery, the operators cycled ESW supply valves to the D/G heat
exchangers (the D/Gs were not operating) which improved flows to the heat exchangers.
However, due to continued concerns about the cause of the fouling, you elected to shut down
Unit 2 and correct the problem. Your staff replaced the damaged strainer basket, cleaned the
heat exchangers and revised your operating procedures to prevent cross-connecting ESW
system trains before restarting the units.
A. Bakken -2-
The Special Inspection began immediately after the event on August 30, 2001, and examined
activities conducted under your license as they relate to safety and compliance with NRC
regulations and the conditions of your license. The inspectors reviewed selected procedures
and records, observed activities, interviewed personnel, and conducted extensive onsite
reviews of the ESW and diesel generators systems in the weeks immediately following the
event. One finding was identified that appears to be significant. As described in Section
4OA3.4 of this report, documented instructions for installation of the ESW strainer baskets, an
activity affecting quality, were not of a type appropriate to the circumstances. Specifically, the
installation instructions for the Unit 1 East ESW pump discharge strainer basket, referenced by
Job Order 723483, did not contain adequate detail associated with the verification of critical
parameters affecting strainer basket alignment to prevent the basket from being deformed
during installation in 1989. Subsequent to the initial onsite inspection, the inspectors and
several NRC staff specialists continued to review information related to this finding including the
detailed engineering and probabilistic evaluations that you provided in January and April 2002.
These evaluations provided some useful inputs to our risk determination of this finding;
however, some of the assumptions you provided could not be supported or confirmed and were
not used.
This finding was assessed using the NRC Phase 3 Significance Determination Process and
preliminarily determined to be Yellow, a finding with substantial importance to safety that will
result in additional NRC inspection and potentially other NRC action. As described in more
detail in the inspection report, our determination considered the August 29, 2001, event
information, the engineering and probabilistic analyses you developed, generic risk information,
and engineering analyses performed by the inspectors. The accident sequence of most
concern was the loss of offsite power (LOOP) because of the vulnerability to the D/Gs created
by the damaged strainer and the cross-connected ESW systems. A single unit LOOP event
would result in a complete loss of the affected units circulating water system, and an
emergency start of both the associated D/Gs and ESW pumps. The NRC concluded that this
sequence would create a greater debris entrainment than the August 29 event; however, the
continued sweeping of the debris by the operating unit circulating water system and availability
of the operating units auxiliary feedwater system to feed the affected units steam generators
would provide substantial mitigation of the event. A dual unit LOOP would have a lower
initiating event frequency than the single unit LOOP, but the mitigative effects available during a
single unit LOOP would not be available. Our engineering assessment of simultaneously
stopping the circulating water pumps for both units concluded that the continued inrush of water
from Lake Michigan to the intake structure, after the dual unit LOOP, would sufficiently entrain
debris to provide significant fouling of the ESW system. This debris would bypass the Unit 1
East ESW pump strainer and disburse throughout heat exchangers in both units. Based on the
observed distribution of debris during the August 29 event, it appears that each of the D/G heat
exchangers could become fouled such that they could not be capable of supporting their
expected loads. The calculated change in core damage frequency and the large early release
frequency as a result of the damaged strainer were both determined to be Yellow.
A. Bakken -3-
This finding is also an apparent violation of NRC requirements and is being considered for
escalated enforcement action in accordance with the "General Statement of Policy and
Procedure for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600. The current
Enforcement Policy is included on the NRCs website at http://www.nrc.gov.
We believe that sufficient information was considered to make a preliminary significance
determination. However, before we make a final decision on this matter, we are providing you
an opportunity to present to the NRC your perspectives on the facts and assumptions used by
the NRC to arrive at the finding and its significance at a Regulatory Conference or by a written
submittal. If you choose to request a Regulatory Conference, it should be held within 30 days
of the receipt of this letter and we encourage you to submit supporting documentation at least
one week prior to the conference in an effort to make the conference more efficient and
effective. If a Regulatory Conference is held, it will be open for public observation. If you
decide to submit only a written response, such submittal should be sent to the NRC within 30
days of the receipt of this letter.
Please contact David G. Passehl at 630-829-9872 within 10 business days of your receipt of
this letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we
will continue with our significance determination and enforcement decision and you will be
advised by separate correspondence of the results of our deliberations on this matter.
Since the NRC has not made a final determination in this matter, no Notice of Violation is being
issued for this inspection finding at this time. In addition, please be advised that the number
and characterization of apparent violations described in the enclosed inspection report may
change as a result of further NRC review.
An additional human performance finding involving several examples of control room operator
weaknesses during the degraded ESW flow event was identified. This issue was determined to
be of very low safety significance (Green) and was determined to involve a violation of NRC
requirements. However, because of its very low safety significance and because it has been
entered into your corrective action program, the NRC is treating this issue as a Non-Cited
Violation, in accordance with Section VI.A.1 of the NRC Enforcement Policy. If you contest the
Non-Cited Violation, you should provide a response with the basis for your denial, within
30 days of the date of this inspection report, to the Nuclear Regulatory Commission,
ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional
Administrator, Region III; the Director, Office of Enforcement, United States Nuclear Regulatory
Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the D.C. Cook
facility.
A. Bakken -4-
In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter
and its enclosures will be available electronically for public inspection in the NRC Public
Document Room or from the Publicly Available Records (PARS) component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html.
Sincerely,
/RA by James Caldwell Acting for/
J. E. Dyer
Regional Administrator
Docket Nos. 50-315; 50-316
Enclosure: Inspection Report 50-315/01-17(DRP);
50-316/01-17(DRP)
cc w/encl: J. Pollock, Site Vice President
M. Finissi, Plant Manager
R. Whale, Michigan Public Service Commission
Michigan Department of Environmental Quality
Emergency Management Division
MI Department of State Police
D. Lochbaum, Union of Concerned Scientists
DOCUMENT NAME: G:\COOK\ML021610713.wpd
To receive a copy of this document, indicate in the box "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy
OFFICE RIII RIII RIII RIII RIII
NAME KOBrien/trn DPassehl SBurgess AVegel BClayton
DATE 06/ /02 06/ /02 06/ /02 06/ /02 06/ /02
OFFICE NRR RIII RIII RIII RIII
NAME Carpenter/via Clayton Congel Grant Dyer
telecon
DATE 05/31/02 06/ /02 06/ /02 06/ /02 06/ /02
OFFICIAL RECORD COPY
A. Bakken -5-
ADAMS Distribution:
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C. Ariano (hard copy)
DRPIII
DRSIII
PLB1
JRK1
BLB1
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MDS1
RJS2
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WMD
U.S. NUCLEAR REGULATORY COMMISSION
REGION III
Docket No: 50-315; 50-316
Report No: 50-315/01-17(DRP); 50-316/01-17(DRP)
Licensee: American Electric Power Company
Facility: D.C. Cook Nuclear Power Plant, Units 1 and 2
Location: 1 Cook Place
Bridgman, MI 49106
Dates: August 30, 2001 through May 17, 2002
Inspectors: B. Bartlett, Senior Resident Inspector
S. Burgess, Senior Risk Analyst
M. Cheok, Senior Reliability and Risk Analyst, NRR
K. Coyne, Resident Inspector
S. Jones, Senior Reactor Systems Engineer, NRR
K. OBrien, Senior Reactor Inspector
P. Prescott, Senior Resident Inspector, Duane Arnold
Approved by: Geoffrey E. Grant, Director
Division of Reactor Projects
SUMMARY OF FINDINGS
IR 05000315-01-17(DRP), IR 05000316-01-17(DRP); on 08/30/2001 - 5/17/2002, Indiana
Michigan Power Company, D.C. Cook Nuclear Power Plant, Units 1 and 2. Special Inspection.
This Special Inspection was conducted by NRC resident, region-based and headquarters-based
inspectors and staff. The inspectors identified one preliminarily Yellow finding and one Green
finding. These findings were assessed using the applicable significance determination process
as a potentially safety significant finding that was preliminarily determined to be Yellow. The
significance of most findings is indicated by their color (Green, White, Yellow, Red) using
IMC 0609, Significance Determination Process (SDP). The NRCs program for overseeing the
safe operation of commercial nuclear power reactors is described at its Reactor Oversight
Process website at http://www.nrc.gov/NRR/OVERSIGHT/index.html. Findings for which the
SDP does not apply are indicated by No Color or by the severity level of the applicable
violation.
A. Inspector Identified Findings
Cornerstone: Mitigating Systems
- TBD. Documented instructions for essential service water (ESW) pump
discharge strainer maintenance did not contain adequate detail regarding critical
parameters for basket installation. Consequently, faulty strainer basket
installation practices contributed to the failure of an ESW pump discharge
strainer basket and created the potential for debris to bypass the strainer and
enter the ESW system. On August 29, 2001, the failed 1 East ESW pump
discharge strainer, in conjunction with the ESW system alignment with all normal
and alternate diesel generator (D/G) ESW supply valves open, caused
significant debris fouling of D/G heat exchangers. While operator actions
prevented the debris fouling from causing a complete loss of the D/Gs ability to
perform their emergency AC power safety function, the potential for a complete
loss of all emergency AC power during a loss of offsite power was determined to
exist. This issue is identified as Apparent Violation (AV) 50-315/01-17-01;
50-316/01-17-01. This finding was assessed using the applicable SDP as a
potentially safety significant finding that was preliminarily determined to be of
substantial safety significance. (Section 4OA3.3 and 4OA3.4)
- Green. The inspectors identified a Non-Cited Violation of Technical
Specification 6.8.1 associated with operator procedural adherence deficiencies
during the degraded ESW event of August 29, 2001. Specifically, the operators
failed to (1) effectively monitor the control boards for changing indications,
adverse trends, and abnormal indications, (2) effectively communicate receipt of
an abnormal temperature alarm for the CCW heat exchanger, and (3) enter the
CCW abnormal operating procedure as directed by the abnormal temperature
alarm response procedure.
2
The inspectors determined that the failure to adequately implement procedures
associated with control board monitoring, logkeeping, and annunciator response
had a credible impact on safety and therefore were more than a minor concern.
Specifically, these issues could reasonably result in the failure to identify and
promptly correct degradation of safety related equipment and therefore impact
the reliability and availability of a safety system. Because these performance
deficiencies contributed to delays in identifying degradation of the ESW and
CCW mitigating systems, the inspectors determined that these human
performance weaknesses were associated with the mitigating systems
cornerstone. Although this issue adversely impacted the licensees response to
the August 29, 2001 event, none of the performance deficiencies directly
resulted in the actual loss of safety system function or the loss of a single safety
system train for greater than its TS allowed outage time. Consequently, the
inspectors concluded that this issue was of very low safety significance (Green).
(Section 4OA4)
3
Report Details
Summary of Plant Event
On the evening of August 29, 2001, the plant experienced problems with Essential Service
Water (ESW) system performance on both Units, which subsequently resulted in an unplanned
shutdown of Unit 2. Unit 1 was already shutdown and in Mode 5 (Cold Shutdown) to support
circulating water system repairs. At 10:55 p.m. on August 29, 2001, plant staff noted
abnormally low ESW flow to both Unit 2 Emergency Diesel Generators (D/Gs) during a
Technical Specification (TS) surveillance test. The licensee entered TS 3.0.3 after the plant
staff determined that both D/Gs were inoperable due to debris buildup.
At 11:47 p.m. on August 29, 2001, the licensee exited TS 3.0.3 after ESW flow for the D/Gs
increased after the control room operators cycled the ESW supply valves to the D/Gs.
At 2:15 a.m. on August 30, 2001, control room operators observed abnormally low ESW flow to
the Unit 2 West Component Cooling Water (CCW) Heat exchanger and declared the Unit 2
West CCW train inoperable. The operators cycled the Unit 2 West CCW heat exchanger ESW
inlet and outlet valves to improve ESW flow; however, ESW flow remained below normal
values. Because the degraded ESW flow condition was not fully understood, the licensee
subsequently shut down Unit 2.
Subsequent NRC engineering evaluations of the conditions present on August 29, 2001,
indicated that the presence of similar conditions during a single or dual unit loss of offsite power
event could potentially result in a loss of all onsite emergency alternating current power.
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R04 Equipment Alignment (71111.04)
a. Inspection Scope
The inspectors performed complete safety system walkdowns of the following
risk-significant system:
Mitigating Systems Cornerstone
- Unit 1 ESW System
- Unit 2 ESW System
The inspectors selected this system based on its degraded performance and its risk
significance relative to the mitigating systems cornerstone. The inspectors reviewed
operating procedures, TS requirements, Administrative Technical Requirements (ATRs),
and system diagrams. In addition, the inspectors assessed the impact of ongoing work
activities on redundant trains of equipment in order to identify conditions that could have
rendered these systems incapable of performing their intended functions.
4
b. Findings
The inspectors assessed the condition of the ESW system, the adequacy of the
licensees root cause evaluation, and the effectiveness of corrective actions during this
complete safety system walkdown. Findings relative to the performance of this
inspection module are discussed in Section 4OA3, "Event Followup."
1R07 Heat Sink Performance (71111.07)
a. Inspection Scope
The inspectors observed or reviewed portions of the following heat exchanger
inspections:
- Unit 1 CCW heat exchangers, containment spray (CTS) system heat
exchangers, D/G heat exchangers, north control room air conditioning (CRAC)
heat exchangers and the auxiliary feedwater (AFW) pump room coolers.
These inspections were conducted following the ESW flow degradation event on
August 29, 2001. The inspectors assessed the heat exchanger condition relative to the
observed flow reduction to certain ESW cooled components and the potential for
common cause failure of ESW cooled components. Because ESW provided the
ultimate heat sink (UHS) for the emergency core cooling system, the inspectors
determined that this inspection was associated with the mitigating systems cornerstone.
b. Findings
The inspectors assessed the impact of the debris intrusion event on heat exchanger
capability in order to determine the safety impact of degraded ESW system performance
and the effectiveness of licensee corrective actions. Findings relative to the
performance of this inspection module are discussed in Section 4OA3, "Event
Followup," Subsections 4OA3.1, 4OA3.4, and 4OA3.5.
1R13 Maintenance and Emergent Work (71111.13)
a. Inspection Scope
The inspectors reviewed the risk assessment and risk management for the following risk
significant maintenance activities:
Mitigating Systems Cornerstone
- Unit 1 dual ESW train outage to support forebay cleaning
The inspectors selected this maintenance activity based on ESW system degraded
performance and its risk significance relative to the mitigating systems cornerstone.
The inspectors reviewed the scope of maintenance work to ensure that applicable safety
functions were maintained during the maintenance activity. The inspectors also
reviewed TS and ATR requirements and walked down portions of redundant safety
5
systems, to verify that risk analysis assumptions were valid and applicable requirements
were met.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
a. Inspection Scope
The inspectors evaluated the potential operability impact associated with the following
issues:
Mitigating Systems Cornerstone
- Operability of the ESW system following pump discharge strainer failure
- Operability of the D/Gs with degraded ESW flow
The inspectors selected these issues based upon their risk significance and their
importance to the special inspection. The inspectors reviewed the licensee's evaluation
and supporting documentation to assess the basis and quality for the operability
determination. The inspectors concluded that this inspection was associated with the
Mitigating Systems cornerstone.
b. Findings
The inspectors reviewed the operability impact of the degraded ESW flow condition to
determine the safety significance of the event and assess the effectiveness of the
licensee's corrective actions. Findings relative to the performance of this inspection
module are discussed in Section 4OA3, "Event Followup," subsections 4OA3.4 and
4OA3.5.
1R19 Post Maintenance Testing (71111.19)
a. Inspection Scope
The inspectors reviewed the post maintenance testing requirements associated with the
following scheduled maintenance activity:
6
Mitigating Systems Cornerstone
- Unit 1 CD D/G heat exchanger inspection
The inspectors reviewed post maintenance testing acceptance criteria specified in the
applicable corrective maintenance work orders. The inspectors verified that the
activities and acceptance criteria were appropriate for the scope of work performed.
Documented data was reviewed to verify that the testing was complete and that the
equipment was able to perform the intended safety functions.
b. Findings
No findings of significance were identified.
4. OTHER ACTIVITIES (OA)
4OA3 Event Followup (93812)
.1 Sequence of Events for Degraded ESW System Flow
a. Inspection Scope
The inspectors reviewed documentation and conducted interviews to determine the
sequence of events that resulted in degraded ESW flows to safety related equipment.
Additionally, the inspectors reviewed licensee actions during and immediately following
the degraded ESW event.
b. Findings
Based on a review of control room logs, operator statements, and plant process
computer data and instrumentation, the inspectors developed a sequence of events for
the degraded ESW flow event. The sequence of events covers the time period from
July 2001 through September 2001.
7
Date Time Event Description
July 1-2 Unit 1 and Unit 2 were operating in Mode 1 (Power
Operation) while the licensee performed biocide
treatment of the circulating water system for zebra
mussel control. Unit 1 Circulating Water (CW)
pump 13 reverse rotated following stoppage to
support biocide treatment. The licensee
determined that the CW pump 13 discharge valve
(1-WMO-13) was partially open and could not be
fully shut, resulting in backflow through the pump.
In order to stop the reverse rotation of CW pump 13
and allow restart of the pump, the licensee took the
Unit 1 main turbine offline and removed the CW
system from service . Following restart of CW
pump 13, Unit 1 was returned to full power.
August 27 Unit 1 was shut down to support repairs to CW
system valve 1-WMO-13.
Unit 2 continued to operate at full power.
August 29 ~6:30 a.m. Prior to the degraded ESW flow event, all ESW unit
cross tie valves were open and the normal and
alternate ESW supply valves to each D/G were
open. Initial ESW flows to the diesel generators
were approximately:
1 AB D/G= 920 gpm
1 CD D/G= 933 gpm
2 AB D/G= 860 gpm
2 CD D/G= 884 gpm
8
Date Time Event Description
August 29 11:06 a.m. The Unit 1 West ESW pump was started to support
Unit 1 cooldown to Mode 5 (Cold Shutdown). The
ESW system was aligned in the following
configuration:
- Unit 1 West and Unit 2 East ESW pumps
supplied their common ESW header with
associated unit cross-tie valves open
- Unit 1 East ESW pump supplied the Unit 1
East and Unit 2 West ESW common header
with associated unit cross-tie valves open.
The Unit 2 West pump was aligned for
standby operation.
- The normal and alternate ESW supply
valves to all D/Gs were open
August 29 11:26 a.m. Unit 1 commenced cooldown using Residual Heat
Removal (RHR) system to Mode 5. This cooldown
approximately doubled ESW flow rates in Unit 1.
August 29 1:14 p.m. - Unit 1 CW pumps 11, 12 and 13 were stopped in
1:36 p.m. succession. Circulating water pump 13 was
stopped last to minimize the potential for backflow
through the pump due to the degraded condition of
valve 1-WMO-13.
August 29 ~3:00 p.m. Unit 1 cooldown completed and ESW flow rates in
Unit 1 decreased. Although the operators did not
identify any abnormal ESW system conditions
during the cooldown, ESW flows to each of the D/G
indicate degradation:
1 AB D/G= 674 gpm
1 CD D/G= 791 gpm
2 AB D/G= 760 gpm
2 CD D/G= 744 gpm
August 29 7:00 p.m. Unit 2 commenced surveillance testing of the Unit 2
East ESW system in accordance with
Procedure 02 OHP 4030.STP.022E. The cross-tie
valve between the Unit 1 West and the Unit 2 East
ESW headers was shut in accordance with the
procedure.
9
Date Time Event Description
August 29 ~7:15 p.m. The ESW flows to the Unit 1 AB and the Unit 2 CD
D/G decreased below the UFSAR Table 9.8-5
minimum required flowrate of 540 gpm. Flows to
each D/G were:
1 AB D/G= 400 gpm
1 CD D/G= 575 gpm
2 AB D/G= 618 gpm
2 CD D/G= 532 gpm
August 29 ~8:00 p.m. Both Unit 2 D/G ESW flowrates decreased below
UFSAR Table 9.8-5 minimum required flowrate.
Flows to each D/G were:
1 AB D/G= 265 gpm
1 CD D/G= 447 gpm
2 AB D/G= 538 gpm
2 CD D/G= 475 gpm
August 29 ~10:30 p.m. The Unit 1 East CCW heat exchanger outlet
temperature exceeded the alarm setpoint of 95°F.
The reactor operator experienced difficulty in
increasing ESW flow to the affected heat
exchanger; consequently, the outlet temperature
remained above the 95°F alarm setpoint until
approximately 2:30 a.m. on August 30, 2001.
The reactor operator failed to log receipt of the high
temperature alarm in the control room log, did not
enter the abnormal CCW operating procedure as
directed by the associated annunciator response
procedure, and failed to adequately communicate
the difficulty in controlling CCW outlet temperature
to the operations shift crew.
Flows to each D/G were less than 40 percent of
flow rates prior to the event:
1 AB D/G = 96 gpm*
1 CD D/G = 360 gpm**
2 AB D/G = 363 gpm
2 CD D/G = 256 gpm
- The Plant Process Computer recorded the 1AB
D/G flow rate as "BAD DATA". A flow rate of
96 gpm was recorded prior to the "BAD DATA"
points.
10
Date Time Event Description
- The ESW flow rate for the 1 CD D/G remained
essentially constant for the remainder of the
event until the operators cycled system valves
to clear the debris blockage at approximately
12:40 a.m..
August 29 10:55 p.m. While performing the Unit 2 East ESW system
surveillance test procedure, the control room
operators noted that ESW flow to the 2 AB and
2 CD D/Gs were less than the surveillance test
acceptance criteria of 590 gpm. Unit 2 entered
TS 3.0.3 due to two inoperable D/Gs. It was later
determined that the limiting condition for operation
of TS 3.8.1.1.e should have been entered rather
than TS 3.0.3.
Unit 1 was informed of the low ESW flow condition
in Unit 2. Unit 1 also identified low ESW flow to the
1 AB and 1 CD D/G. Unit 1 entered TS 3.8.1.2 for
two inoperable diesel generators while in Mode 5.
August 29 11:47 p.m. The Unit 2 AB D/G was declared operable following
cycling of the remotely operated ESW supply
valves. Unit 2 AB D/G ESW flow improved to
approximately 800 gpm. Unit 2 exited TS 3.0.3 but
entered TS 3.8.1.1 for one inoperable D/G.
August 29 11:50 p.m. The Unit 2 CD D/G declared operable following
cycling of the remotely operated ESW supply
valves. Unit 2 CD D/G ESW flow improved to
approximately 800 gpm. Unit 2 exited TS 3.8.1.1.
August 30 12:40 a.m. The Unit 1 CD D/G declared available but remained
inoperable due to degraded ESW flow following
cycling of the remotely operated ESW supply
valves. ESW flow improved to 760 gpm.
August 30 1:25 a.m. The Unit 1 AB D/G declared available but remained
inoperable due to degraded ESW flow following
cycling of the remotely operated ESW supply
valves. ESW flow improved to 700 gpm.
11
Date Time Event Description
August 30 1:55 a.m. Unit 2 control room operators continued
performance of Unit 2 East ESW system
surveillance and aligned the normally isolated
Unit 2 East containment spray system (CTS) heat
exchanger for flushing in accordance with
02-OHP 4030.STP.022E.
At this time the source and extent of the debris
intrusion had not been positively identified and the
inspectors determined that this action could have
transported debris into the otherwise isolated CTS
heat exchanger. Because the source of debris
intrusion was later determined to be the Unit 1 East
ESW pump strainer (which was independent from
the Unit 2 East ESW header), this action did not
adversely impact the Unit 2 East CTS heat
exchanger.
August 30 2:09 a.m. The Unit 2 West ESW pump was started.
August 30 2:13 a.m. The Unit 2 ESW unit cross-tie valve, 2-WMO-706,
was shut to split the ESW systems. All four ESW
pumps were running with all unit cross-tie valves
closed.
August 30 2:15 a.m. Unit 1 East ESW and CCW trains were declared
inoperable (but available) due to degraded ESW
flow system. Actions associated with TS 3.7.3.1
and TS 3.7.4.1 were not applicable with Unit 1 in
Mode 5.
Unit 2 West CCW heat exchanger flow indicated
approximately 2000 gpm with outlet temperature
rising slowly at 92o F. Cycling of the ESW inlet and
outlet valves improved heat exchange flow to
5500 gpm. This flow rate was less than the
expected value of approximately 8500 gpm. Unit 2
entered TS 3.7.3.1 for the inoperable Unit 2 West
CCW loop.
August 30 2:30 a.m. Unit 2 East CTS heat exchanger declared operable
following completion of ESW surveillance testing
flush.
12
Date Time Event Description
August 30 2:45 a.m. Unit 2 control room operators started the south
control room air conditioning (CRAC) unit and
stopped the north CRAC for flushing during
02-OHP4030.STP.022E.
At this time the source and extent of the debris
intrusion had not been positively identified and the
inspectors determined that placing the south CRAC
unit into service could have allowed transport of
debris into the associated heat exchanger.
Because the source of debris intrusion was later
determined to be the Unit 1 East ESW pump
strainer (which was isolated from Unit 2 by closure
of 2-WMO-706), this action did not adversely
impact the CRAC unit.
August 30 3:45 a.m. Unit 1 AB D/G declared operable after closing and
de-energizing the alternate ESW supply remotely
operated valve from the Unit 1 East ESW header.
Unit 1 exited TS 3.8.1.2.
August 30 6:23 a.m. Licensee completed 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> report to the NRC
regarding degraded ESW flow to the D/Gs (Event
Number 38249).
August 30 7:55 a.m. Unit 2 commenced 15 percent per hour power
reduction for reactor shutdown.
August 30 1:36 p.m. Unit 2 entered Mode 2 (Reactor Startup).
August 30 1:47 p.m. Unit 2 entered Mode 3 (Hot Standby).
August 31 4:15 a.m. Unit 1 East motor driven auxiliary feedwater pump
(MDAFWP) inoperable due to low ESW flow to its
room cooler.
August 31 6:10 a.m. Unit 1 East MDAFWP declared operable after ESW
flow to room cooler restored.
September 3 12:28 p.m. Unit 2 entered Mode 5 and exited TS 3.7.3.1.
Results of Essential Service Water Inspections
Following shutdown of Unit 2, the licensee performed inspections on the ESW system to
determine the cause and extent of condition of degraded ESW system performance. The
results of significant ESW system inspections conducted after implementation of the
licensees immediate corrective actions following the event are summarized below:
13
Component Inspection Results
Unit 1 East ESW pump Deformation of the strainer basket and resultant bypass
discharge strainer flowpath around the basket was identified. Additionally,
the basket support bracket was deformed.
Unit 1 East CCW Heat Inspections identified the following:
Exchanger
- 213 tubes were obstructed with debris (approximately
10 percent tube blockage). All tubes were cleaned
using a hand brush.
- Approximately 1.5 cubic feet of debris found in the
interpass region and about one half cubic foot of
debris found in the inlet plenum.
- Debris measuring greater than 1/8 inch (the ESW
strainer mesh size) was identified in the heat
exchanger. In general, the debris consisted of zebra
mussel shells and sand.
Note: The CCW heat exchanger is a two pass shell and
tube heat exchanger with ESW flowing through
the tube side.
Unit 1 West CCW Heat Inspections identified the following:
Exchanger
- 33 tubes blocked with silt and debris (approximately
1.5 percent tube blockage)
- Minimal amounts of shells and debris
Note: 85 additional tubes in the Unit 1 West CCW heat
exchanger were mechanically blocked during
previous maintenance activities.
Unit 1 East CTS Heat Inspection identified the following:
Exchanger
- Very light silting, less than 1/4 inch thick in the lower
shell area. No shells were found.
Note: The CTS heat exchanger is a shell and U-tube
heat exchanger with ESW flowing on the shell
side.
Unit 1 AB D/G Heat Inspection identified minimal amounts of debris and no
Exchangers tube blockage.
14
Component Inspection Results
Unit 1 CD D/G Heat Inspection of the 1 CD D/G heat exchangers identified
Exchangers the following:
- Lube oil cooler had 14 blocked tubes with debris and
7 partially blocked tubes (approximately 10 percent of
the heat exchanger tubes had some blockage and
were degraded). All tubes were cleaned.
- The jacket water heat exchanger had 14 tubes
blocked with debris (approximately 6 percent total had
some blockage and were degraded). Two tubes
remained blocked after cleaning.
Unit 1 North CRAC Inspection of the CRAC unit identified minimal debris and
no blocked tubes.
Unit 1 East MDAFWP Inspection of room cooler identified 18 pre-cooler tubes
Room Cooler fully blocked with debris and 18 pre-cooler tubes partially
blocked with debris (approximately 27 percent of the
pre-cooler tubes had some blockage and were
degraded). The associated job order stated that the
pre-cooler section was "full of dirt, zebra mussels, and a
steel ball."
Unit 1 West MDAFWP Inspections identified 1 pre-cooler tube of 132 total tubes
Room Cooler blocked with a small amount of sand and mussel shell
debris.
Unit 1 East Turbine Approximately one pound of debris was removed from
Driven Auxiliary the room cooler during flushing activities. Inspections
Feedwater Pump identified that 7 of 48 pre-cooler tubes were blocked with
(TDAFWP) Room sand, silt and/or zebra mussel shells.
Cooler
Unit 1 West TDAFWP 10 of 48 pre-cooler tubes were blocked with zebra
Room Cooler mussel shells and sand.
Unit 2 West CCW Heat Inspections identified less than 24 tubes blocked with
Exchanger weed-like growth, tubercles, and zebra mussel shells
(approximately 1 percent tube blockage). Because this
inspection was performed approximately 4 weeks after
the event, normal system flow through the heat
exchanger could have facilitated cleanup of debris.
15
Component Inspection Results
Unit 2 West CTS Heat This heat exchanger was not inspected immediately
Exchanger following the event, but was inspected during the January
2002 Unit 2 refueling outage. Results of inspections
performed on February 4, 2002 identified minor amounts
of debris, including sand and shell fragments, on top of
tube sheet (4 - 6 cups total).
Unit 2 AB D/G Heat Inspection identified:
Exchangers
- 6 partially blocked tubes in the lube oil heat
exchanger (less than 3 percent tube blockage).
- 2 partially blocked tubes in the jacket water heat
exchanger (less than 1 percent tube blockage).
All tubes were cleaned.
Unit 2 CD D/G Heat Inspection identified:
Exchangers
- 2 blocked tubes in the lube oil heat exchanger (less
than 1 percent tube blockage).
- 3 blocked tubes in the jacket water heat exchanger
(less than 2 percent tube blockage).
Unit 2 North CRAC Inspection identified no blocked tubes.
Heat Exchanger
Unit 2 West MDAFWP Inspection of room cooler identified 5 pre-cooler tubes
Room Cooler fully blocked with debris and 11 pre-cooler tubes blocked
at the inlet with debris (approximately 12 percent of the
pre-cooler tubes had some blockage and were
degraded)
Unit 2 West TDAFWP Inspections identified 18 of 48 pre-cooler tubes to be
Room Cooler blocked with zebra mussel shells and sand. Condenser
coil for refrigeration unit also appeared to be partially
blocked.
.2 Adequacy of Licensee Response to ESW Low Flow Condition Including Emergency
Plan Implementation
a. Inspection Scope
The inspectors reviewed the licensees immediate corrective actions in response to the
ESW low flow condition and the corrective actions to restore the ESW trains to their
design and licensing basis.
16
b. Findings
Initial Identification
The inspectors determined that control board indication of the trend of the degrading
ESW flow could have been identified by the operators at least 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> prior to the initial
identification of the degraded flow. The delay in the identification of the low flow by the
operators was due, in part, to the failure of the operators to perform hourly control board
walkdowns recommended by procedure. The inspectors determined that operator
practice was to no longer perform the recommended walkdowns. However, the delay in
the identification did not result in a significant impact on event recovery actions.
Initial Response
The inspectors determined that the operators initial response to the event was
adequate to ensure that reactor safety was maintained. The operators ensured that the
reactor coolant system (RCS) temperature was being maintained within the required
parameters and the ability to cool the RCS was maintained. In addition, the Unit 2
operators promptly informed the Unit 1 control room operators upon the identification of
the degraded ESW flow.
The inspectors determined that the Unit 2 Unit Supervisor (US) inappropriately entered
TS 3.0.3 upon declaring both Unit 2 D/Gs inoperable. Inoperability of both D/Gs
required an entry into Limiting Condition of Operation (LCO) TS 3.8.1.1.e, which
required that two offsite power source circuits be demonstrated operable within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.
Although the wrong TS LCO was entered, the licensee performed the off-site power
operability verifications and complied with the time limits specified in TS 3.8.1.1.e.
The licensee identified that the Unit 1 US failed to enter TS 3.1.2.3, for inoperable
boration flow paths, when the D/Gs were inoperable. The action statement required that
no core alterations be performed. Since no core alterations were in progress, the
TS LCO was met.
The operating crews correctly diagnosed the low ESW flow and were able to improve
ESW flow to the D/Gs by repeatedly cycling ESW supply and return flow valves.
Approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> after initially identifying the degraded ESW condition, the
operators closed the ESW unit cross-tie valves so that each unit was receiving ESW
flow only from its associated ESW pumps. The licensee did not identify that ESW flows
to the Unit 1 East and Unit 2 West CCW heat exchangers were degraded until after the
ESW cross tie valves were shut. The inspectors determined that communication
inadequacies contributed to the 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> delay in the identification of the low ESW flows to
the CCW heat exchangers. For example, the Unit 1 high CCW temperature condition
was not adequately communicated to the Senior Reactor Operators, and the Unit 2
operators were not promptly informed of the high Unit 1 CCW temperature.
Emergency Classifications
The licensee did not declare an emergency classification for this event. The operations
Shift Manager and Operations Director considered declaring an emergency
17
classification at approximately 4:30 a.m. following the initial indications of degraded
ESW flow. The licensees emergency plan and implementing procedures have no
specific Emergency Condition Categories (ECC), Initiating Condition (IC), or Emergency
Action Level (EAL) that would address significantly reduced ESW flow. Emergency
Condition Category S-5, Loss of Systems Needed to Achieve/Maintain Hot Shutdown,
was most appropriate; however, the entry conditions required a complete loss of the
function with entry into EOP FR-H1, Response to Loss of Secondary Heat Sink, or
FR-C1, Response to Inadequate Core Cooling. The ECC for Site Emergency
Coordinator (SEC) Judgement did give a threshold value of In the judgement of the
SEC: Conditions indicate that plant safety systems may be degraded, and increased
monitoring of plant functions is needed. Under the licensees procedures this would
result in the declaration of an Unusual Event. The inspectors concluded that a
declaration of an Unusual Event should have been made due to the degradation of
multiple trains of safety-related equipment on each unit. However, the failure to declare
an Unusual Event was determined to not constitute a violation of regulatory
requirements.
Subsequent Response
The licensee was conducting an ESW system surveillance test during the event. While
the performance of the surveillance aided the operators in the identification of the
degraded ESW flow, continuation of the surveillance test procedure could have
exacerbated the heat exchanger fouling. For example, the CTS heat exchanger and
South CRAC heat exchanger isolation valves were opened per the surveillance
procedure, which could have introduced debris into these otherwise clean heat
exchangers. However, subsequent analysis of the heat exchangers by the licensee
determined that heat exchanger performance was not affected.
.3 Determination of Root Cause for ESW Low Flow Condition
a. Inspection Scope
The inspectors reviewed the as-found condition of components of the ESW system
including the Unit 1 East ESW pump discharge strainer. The inspectors' review
included the observation of heat exchanger end bell removal, pump discharge strainer
inspections, and flushing activities. The inspectors also interviewed individuals involved
in these activities and reviewed the licensees apparent root cause for the ESW low flow
condition.
b. Findings
The licensee evaluated the root cause of the degraded ESW flow event and concluded
that the root cause of the event was the following:
"The root cause for this event was that a strainer basket was installed incorrectly
during basket replacement activities that occurred in the 1989 time frame. The
failure to adjust the height of the basket to align the top edge of the basket with
the lip of the strainer body allowed the basket to be placed in compression when
the >> 700 lb. strainer lid was reinstalled. The compressive force exerted by the lid
18
caused the basket mesh to tear in the area of the weld on the baskets vertical
support bracket and was the initiating event for the resultant damage and
eventual failure of the basket."
The licensee inspected all eight ESW strainer baskets and identified that the Unit 1 East
ESW pump discharge strainer east basket had a weld failure on the height adjustment
bracket that allowed the bracket to bend and drop the basket by approximately 3 inches.
This deformation allowed a bypass of debris greater than the 1/8" strainer mesh size.
The passage of debris greater than the normal strainer mesh size resulted in fouling of
heat exchangers in the ESW system and the consequent flow degradation experienced
on August 29, 2001. The licensee reviewed past maintenance performed on the failed
strainer and concluded that the strainer was initially damaged during a basket
replacement that occurred in 1989.
The inspectors assessed the licensees root cause methodology and conclusions and
determined that the licensee adequately identified the root cause of the degraded ESW
flow event. The inspectors concluded that the licensees approach was reasonable, and
adequately addressed contributing causes to the event. The inspectors reviewed
records from the Unit 1 East ESW pump discharge strainer replacement conducted in
1989 and concluded that the strainer installation instructions used in 1989 were
inadequate. The instructions provided for replacement of the strainer baskets,
contained in Job Order 723483, lacked sufficient detail to ensure that critical parameters
associated with strainer installation were maintained. Specifically, the JO 723483
instructions did not contain sufficient detail regarding adjustment of strainer basket
height within the strainer housing or verification that the installation prevented basket
bypass paths greater than 1/8" in size. The inspectors determined that the failure to
provide adequate instructions for ESW strainer basket maintenance constituted a
violation of regulatory requirements.
10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," stated, in
part, that activities affecting quality shall be prescribed by documented instructions,
procedures, or drawings of a type appropriate to the circumstances. The inspectors
determined that the documented instructions for installation of the ESW strainer
baskets, an activity affecting quality, were not of a type appropriate to the
circumstances. Specifically, the Unit 1 East ESW pump discharge strainer east basket,
was installed on April 18, 1989 in accordance with Job Order 723483. The strainer
basket installation instructions referenced by Job Order 723483 did not contain
adequate detail associated with the verification of critical parameters affecting strainer
basket alignment during installation. The failure to adequately align the ESW strainer
basket within the strainer housing would allow debris greater than 1/8" in size to bypass
the strainer or allow damage to the basket vertical support bracket during strainer cover
re-installation. This issue is identified as Apparent Violation (AV) 50-315/01-17-01;
50-316/01-17-01. This finding was assessed using the applicable SDP as a potentially
safety significant finding that was preliminarily determined to be Yellow. The details of
the SDP evaluation are contained in Section 4OA3.4 below.
.4 Specific and Generic Impacts of ESW Debris Intrusion
19
a. Inspection Scope
Subsequent to the August 2001 debris intrusion event, the licensee conducted
engineering and probabilistic evaluations that assessed the specific and generic impacts
of the failed IE ESW system strainer on ESW supported systems. The licensee
described their engineering evaluation in Technical Report NTS-2002-002-REP, ESW
Debris Intrusion Event Evaluation, Revision 0, completed in January 2002. The
licensee described their probabilistic evaluation in Technical Report
NTS-2002-010-REP, Debris Intrusion Into the Essential Service Water System -
Probabilistic Evaluation, Revision 0, completed in April 2002. The inspectors reviewed
the evaluations, assessed their fidelity to the August 2001 data, and used the
evaluations and other design information to determine the capability of ESW supported
safety-related systems to perform their functions during the August 2001 event and
applicable design basis events.
b. Findings
b.1 Engineering Evaluation
The licensees engineering evaluation examined the August 2001 debris intrusion event
and the potential consequences of a similar debris intrusion following a single unit loss
of offsite power (LOOP) event. The evaluation considered debris entrainment within the
intake structure and ESW system, the hydraulic characteristics of the ESW-D/G system,
and the performance characteristics of the ESW-D/G heat exchangers. As a separate
part of the engineering evaluation, the licensee developed a revised single unit LOOP
initiating event frequency, a human performance reliability analysis of the operators
response to a similar debris intrusion event, and a plant-specific Large Early Release
Frequency (LERF) analysis.
Debris Entrainment
Overall, the licensees engineering evaluation concluded that debris intrusion events,
assuming a failed 1 East ESW strainer, could not be precluded. Debris intrusion into
the ESW system was expected to occur following a single unit LOOP event, a seismic
event that causes a LOOP, or during a severe storm that resulted in a LOOP event.
Though not explicitly stated, the engineering evaluation focused on a single unit LOOP
event. A detailed review of the potential for and consequences of a dual unit LOOP
event were not evaluated. During discussions with the inspectors, the plant staff
indicated their belief that a single unit LOOP event would result in entrainment of the
largest amount of debris.
The licensees engineering evaluation determined that low vertical flow velocities were
required to entrain debris in the intake structure, on the order of 0.15 feet/second for
sand and 0.30 feet/second for shells. Once entrained, the evaluation calculated that the
debris could take up to an hour to re-settle to the intake structure floor depending on the
hydrofoil effect associated with the shells. The plant staff assumed that intake structure
cross flows, created during the August 2001 event and expected to exist following a
single unit LOOP event, would entrain the greatest amount of debris. However, the
licensees engineering evaluation did not assess the potential for intake structure cross
20
flows or intake structure debris to be entrained by flow perturbations following a dual unit
LOOP.
Once debris was ingested into the ESW system, the engineering evaluation determined
that flow rates on the order of 140 gallons/minute were necessary to maintain the debris
suspended within the flow of a horizontal section of 6 inch diameter ESW supply piping
to the D/G heat exchangers. Based upon calculations , flow rates of 200 and
400 gallons/minute were determined to be needed to maintain sand and shells,
respectively, suspended in the flow of a vertical section of 6 inch diameter pipe. Though
the engineering evaluation recognized that lower flow rates could maintain shells within
the flow stream if shell hydrofoil effects were considered.
The inspectors reviewed the licensees records of circulating and service water intake
structure inspections and determined the intake structure often contained debris,
e.g. sand, silt, and mussel shells. The debris was typically located in the quiescent flow
regions of the intake structure, including directly in front of the ESW pump bays. Recent
and past operating experience indicated that debris, present in the intake structure
quiescent flow areas, could be entrained in the circulating and essential service water
flows as a result of intake structure flow disturbances. Changes in the circulating and
essential service water system flow rates, severe weather, and LOOP events were all
conditions capable of causing intake structure flow disturbances.
The inspectors reviewed the August 2001 circulating and essential service water system
operating information and determined that significant changes in the intake structure
flow patterns were the most likely cause for debris entrainment. The changed flow
patterns entrained debris, previously located in quiescent flow areas, and transported
the debris to the 1 East ESW system pump suction area. This effect was consistent
with the staggered shutdown of the Unit 1 circulating water pumps, which limited
perturbations of the intake structure water inventory; the continued operation of the
Unit 2 circulating water pumps, which caused a significant change in the intake structure
water flow patterns; and the observed gradual degradation of ESW system flow to the
D/Gs.
The inspectors also determined that a larger short-term ingestion of debris would likely
occur as a consequence of either a single unit LOOP, dual unit LOOP, or severe
weather event. These events would be expected to cause both changes to the intake
structure flow patterns, as observed with the August 2001 event, and significant intake
structure water perturbations, due to an approximate 10 to 12 foot increase in the intake
structure water level following a dual unit LOOP. As a result, the inspectors concluded
that a dual unit LOOP event would likely result in a significantly larger ingestion of debris
over a shorter period of time than that created by the circulating water system cross-flow
associated with the August 2001 event or which would likely occur following a single unit
LOOP.
ESW-D/G Hydraulic Characteristics
The licensees engineering evaluation determined an approximate percentage of
blocked ESW-D/G heat exchanger tubes that would be necessary to cause the
August 2001 observed degraded flow conditions. Initial results indicated that plugging in
21
excess of 90% of the heat exchanger tubes would be necessary to cause the observed
flows. Because of the ease with which the operators were able to restore flow through
some of the heat exchangers, the licensee rejected the engineering evaluation initial
conclusion that a high percentage of tubes were blocked.
As an alternate hypothesis, the licensee conjectured that the August 2001 degraded
flow conditions were caused by a combination of blocked tubes and the buildup of a
porous debris pile on the heat exchanger tube sheets. The debris pile was assumed to
be composed of a combination of shells, sand, and silt. The majority of the buildup was
assumed to occur at the ESW-D/G lube oil heat exchanger tubesheet for the
August 2001 event. While the presence of a debris pile would significantly decrease
ESW-D/G flow rates, the licensee assumed that only a limited number of heat
exchanger tubes would not be available for heat transfer.
Based upon computer logs of ESW-D/G flow data from the August 2001 event, the
licensees engineering evaluation concluded that the buildup of a debris pile on a heat
exchanger tubesheet would: 1) be self-limiting with a minimum average ESW-D/G flow
rate of 200 gallons/minute; 2) occur initially at the D/G lube oil heat exchanger inlet
tubesheet; and, 3) be limited to a single ESW-D/G heat exchanger tubesheet location
during a LOOP event. The evaluation supported the minimum average ESW-D/G flow
rate by rejecting non-numerical computer data recorded for the 1 AB D/G and by
averaging the remaining lowest recorded flow values. The evaluation supported the
single location debris buildup position by assuming that the debris piles were inherently
unstable and could not be maintained, due to a constant loss of material, if the source of
new material was lost due to a change in the ESW-D/G flow path following a LOOP.
The inspectors determined that the engineering evaluation likely overestimated the
percentage of blocked tubes necessary to cause the observed August 2001 degraded
flow conditions. The inspectors noted that the licensees evaluation did not consider
several factors which would affect the blocked tube estimate including entry and exit
pressure losses caused by changes in the ESW mass flow velocity and an increased
flow resistance caused by the presence of a two-phase mixture down stream of the
jacket water heat exchanger. The inspectors estimated the percentage of blocked
tubes, which alone could have caused the observed degraded flow conditions, to be well
in excess of 50% but less than the near 90% values initially calculated in the licensees
engineering evaluation.
The inspectors performed independent flow hydraulic calculations and concluded that a
relatively thin filter bed, on the order of 3 inches or less, of sand could have caused the
observed degraded flow conditions. The filter bed was assumed to be developed from
an initial layer of shell fragments and other debris on tubesheet with a subsequent
buildup of a variety of particle sizes of sand, silt, and clay particles forming a filter bed of
relatively low porosity. The calculation results were noted to be very sensitive to the bed
composition because of the ability of the smaller particles to fill the flow paths between
the larger sand particles. Based upon post August 2001 photographs of heat exchanger
tubesheets, which showed some tubes still blocked by wedged shell fragments and
other debris, the inspectors concluded that the observed ESW-D/G flow reduction was
most likely caused by a combination of heat exchanger tube blockage and a
non-uniform debris pile buildup on the heat exchanger tubesheet.
22
The inspectors evaluated the computer logs of ESW-D/G flow data for the August 2001
event and determined that the data did not specifically support the licensees
assumptions of a self-limiting debris buildup, with a minimum ESW-D/G flow rate of
200 gallons/minute, or a single heat exchanger tubesheet debris pile buildup location.
While the computer logs of ESW-D/G flows did indicate that the 1 CD ESW-D/G flow
leveled off at a degraded flow rate of 350 gallons/minute; data for the 1 AB ESW-D/G
indicated a steady decreasing trend which lowered flow below the level of reliable
indication. In addition, computer logs for the Unit 2 ESW-D/G flow rates indicated that
both Unit 2 ESW-D/G flow rates experienced a decreasing trend with low recorded flow
values of approximately 300 and 250 gallons/minute. Operator and computer logs of
ESW flow data also indicated that not all debris piles were inherently unstable, a pre-
condition for a self-limiting process. The logs indicated that the ESW-D/G flows
appeared to drop relatively rapidly, as the blockage built up, and the ESW-component
cooling water (CCW) and 1 AB D/G heat exchanger flows remained degraded, despite
several attempts by the operators to clear the blockage. Combined, these data
indicated that ESW system debris piles were not self-limiting or unstable in their buildup,
with a minimum ESW-D/G flow rate of 200 gallons/minute.
Based upon information provided in the licensees engineering evaluation, the
inspectors concurred with the licensees contention that a debris pile buildup was most
likely to occur at the first flow restriction in the ESW-D/G flow path. However, the
inspectors also noted that the first flow restriction location would change during the
course of the plants response to a LOOP event potentially resulting in multiple debris
piles restricting ESW-D/G flow. Initially, the first flow restriction would be at the D/G
lube oil heat exchanger tubesheet, as observed during the August 2001 event.
However, once the D/Gs began to operate, the first flow restriction location would
change, due to an automatic system re-alignment, to either the inlet to the D/G air
after-cooler temperature control valve or to the D/G air after-cooler heat exchanger
tubesheet. A debris buildup at either of these locations may be quicker to develop and
may be more difficult to clear than a debris build up at the lube oil heat exchanger due to
vertical piping upstream of the three-way valve and the smaller air after-cooler heat
exchanger intake head volume. Additionally, the presence of distributed pressure
drops, due to multiple debris piles, would also reduce the effectiveness of operator
actions to flush debris from the system.
ESW-D/G Cooler System Performance Characteristics
The licensees engineering evaluation considered the minimum ESW-D/G flow required
to maintain D/G lube oil and jacket water coolers within maximum allowed parameters
assuming variable degree and location of heat exchanger plugging, tube fouling, and
design event loading. Overall, the evaluation determined that approximately
140 gallons/minute ESW-D/G flow was required to assure minimum D/G performance
during a LOOP event. This calculation assumed the blockage of up to 60% of one pass
of the D/G heat exchanger tubes and design fouling. Approximately 200 gallons/minute
ESW-D/G flow was required to assure minimum D/G performance during a LOOP-loss
of coolant accident (LOCAL). This calculation assumed the blockage of up to 50% of
one pass of the heat exchanger tubes and design fouling. Calculations for both cases
indicated that the minimum ESW-D/G flow required to maintain the D/G lube oil and
23
jacket water cooler within maximum allowed parameters increased rapidly with
increased tube blockage beyond the levels stated above.
The inspectors determined that the licensees engineering evaluation did not consider
several factors which would affect the calculated minimum flows necessary to support
continued D/G functioning. Examples included: 1) entry and exit pressure losses
caused by changes in the ESW-D/G mass flow velocity through a smaller number of
heat exchanger tubes; 2) an increased ESW-D/G flow resistance caused by the
presence of a two-phase mixture down stream of the jacket water heat exchanger at
reduced ESW-D/G flow rates, and; 3) changes in the ESW-D/G heat transfer rates due
to the presence of a debris bed which would have degraded ESW-D/G flow through the
individual tubes. While the exact impact on the minimum ESW-D/G flow rate of each of
these factors was not determined, the inspectors concluded that the overall level of
ESW-D/G flow rate, necessary to support continued D/G functioning, was significantly
less than the Updated Final Safety Analysis Report (UFSAR) value of 540
gallons/minute and may be approximated by the licensees calculations.
Single Unit LOOP Initiating Event Frequency
In conjunction with the engineering analysis, the licensee proposed that both the
August 2001 event and the generic impacts of an ESW-D/G debris intrusion event
should be evaluated using a revised single unit LOOP initiating frequency. Based upon
recent changes to the plant switchyard, the licensee conducted a review of data from
several databases (including NUREG/CR-5496 and NUREG/CR-5750) to determine a
revised initiating event frequency for a single unit LOOP event at a dual unit site. In
conducting the analysis, the licensee assumed that a single unit LOOP was the risk
dominant event, and that a dual unit LOOP event would not result in sufficient debris
entrainment in the ESW-D/G flow. Therefore, the licensees analysis only considered
single unit LOOP events at dual unit sites. The analysis eliminated all dual unit LOOP
events, as well as events that the licensee determined to be not applicable to the plant.
Based upon the analysis, the licensee proposed that a single unit LOOP initiating event
frequency of 0.004 per year should be used to evaluate the August 2001 and a potential
generic ESW-D/G debris intrusion event.
The inspectors reviewed the licensees analysis and determined that the proposed
initiating event frequency may be an underestimation for the following reasons:
- Although the licensees analysis credited the plant-specific electrical distribution
system as being unique and better than assumed in the generic cases (by
eliminating events that the licensee believed could not occur at the plant), there
was no similar effort done for the plant-specific electrical distribution system to
determine if any plant-specific events could occur that could not occur at the
other plants. Thus, only a limited scope comparison was performed. (One
example would be that, although hurricane events were eliminated due to plants
location, vulnerability to events caused by ice storms were not explicitly
considered.)
- The licensee included data from sites like Indian Point, Nine Mile Point and
Fitzpatrick that share control of switchyard activities among differing licensees.
24
Data from these sites may not be appropriate for use in determining a plant-
centered loss of offsite power initiating event frequency for D.C. Cook because
D.C. Cook may be more vulnerable to a common cause failure or switchyard
error that may result in a loss of offsite power to both units.
- The licensees assumption that the dual unit LOOP initiator will not entrain debris
into the ESW-D/G was not considered a valid assumption. Therefore, the
licensees elimination of dual unit initiators from inclusion in the overall initiating
event frequency was not acceptable. The generic frequency of severe weather
events, which are the most probable cause for dual unit LOOP events, was
approximately 0.007 per year, about twice the licensees estimate for the single
unit initiator.
Based upon current generic estimates of a single unit LOOP initiating frequency and
plant specific information provided by the licensee, the inspectors concluded that the
single unit LOOP initiating frequency for the plant could be lower than the generic
frequency. However, the inspectors did not consider the differences to be supported to
the extent to justify a plant-specific initiating frequency one tenth the generic initiating
frequency (0.004 versus 0.046). Based upon licensee provided information and
engineering judgement, the inspectors used a single unit LOOP initiating frequency of
0.01 for subsequent NRC risk analyses.
Human Error Probability Analysis
The licensee performed an analysis to estimate the human error probability (HEP)
associated with operator actions to recover ESW-D/G flow to the heat exchangers for a
single unit and dual unit LOOP event. The HEP for a single unit event was estimated to
be 0.05 for the recovery prior to the initiating event and for recovery during a single unit
LOOP event. The licensee estimated the HEP for operator action to recover for a dual
unit LOOP event to be either 0.13 or 1.0 depending on the time available. The HEP
analyses took into account cognitive as well as execution errors. Although the licensee
did not have approved procedures or training for the recovery actions credited in the
analyses, the licensee concluded that credit could be taken for the actions since
operators had actually performed the actions during the August 2001 ESW-D/G
intrusion event.
The inspectors reviewed the analysis methodology used by the licensee and concluded
that the methodology was acceptable and was applied correctly. The inspectors also
determined that the licensees assumption of credit for the operators proper
implementation of the unproceduralized and untrained recovery actions was appropriate
given the fact that these actions were actually carried out during the August 2001 event.
Although a level of uncertainty existed as to how much time might be available for
operator action during a single unit LOOP event, the inspectors determined that the
licensees HEP estimate of 0.05 was reasonable if sufficient time was available
(i.e., time from the start of a LOOP event to the time when below reliable indication of
ESW-D/G flow through the heat exchanger exceeds 5 to 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />). The 0.05 was
considered optimistic for recovery times of 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> or less. For a dual unit LOOP event,
the inspectors determined that an HEP of 0.13 was appropriate when the operators
25
would have approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to response. This is the value used for subsequent
NRC risk analysis of a dual unit LOOP event. If the operators did not have sufficient
time to respond, less than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, the inspectors determined that ESW-D/G flow from
the opposite Unit could not be credited for valve cycling or heat exchanger flushing
actions. In these cases, an HEP of 1.0 was considered appropriate.
Prior to the August 2001 ESW-D/G debris intrusion event, the licensee developed a
plant-specific large early release frequency (LERF) estimate. Using methodology
described in NRC document NUREG/CR-6595 and figure 2-2 of the document, the
licensee estimated a plant-specific LERF to CDF ratio of 0.1. During discussions with
the NRC of the engineering evaluation of the August 2001 intrusion event, the licensee
proposed that risk analyses of the event should use the plant-specific LERF to CDF ratio
value of 0.1.
The inspectors reviewed documentation provided by the licensee to support their
proposed use of a LERF to CDF ratio of 0.1. The inspectors determined that the
licensee evaluation only modeled a single unit LOOP, therefore adequate time was
postulated for ESW-D/G recovery and for onsite and offsite emergency response. As a
result of the credit taken for these actions, a large fraction of the core damage
sequences were allocated to the non-large early release category. Only approximately
16 percent of the revised core damage sequences were considered in calculating the
LERF.
In the NRCs risk evaluations of the ESW-D/G debris intrusion event that lead to core
damage sequences, a station blackout event was modeled. In these cases,
containment hydrogen igniters were not considered available due to an absence of
required power. In such scenarios, recent NRC studies (e.g., studies for the
containment significance determination process and for the resolution of the generic
issue for the combustible gas issue) indicated that the conditional probability of large
early release given a core damage event for an ice condenser containment was
approximately 0.82.
Considering that both the licensees and the NRCs LERF values were developed using
NRC guidance, though with differing assumptions, and the potential uncertainty in
assessing the effectiveness of the licensees onsite and offsite emergency response
efforts, a LERF value of 0.4 was used in subsequent NRC risk analyses.
b.2 Probabilistic Evaluation
Subsequent to and in support of the licensees engineering evaluation discussed above,
the licensee performed a probabilistic evaluation of the impact of a failed ESW-D/G
strainer on the plants response following a LOOP event. The evaluation assumed a
single or dual unit LOOP as the initiating event [Block 1] and identified a logical
sequence of steps [Blocks 2 through 9] which could lead to D/G failure as a result of
debris intrusion into the ESW-D/G flow. The licensees probabilistic evaluation
considered the likelihood of the sub-events which collectively comprised an ESW-D/G
debris intrusion event. The probabilistic evaluation considered debris intrusion events
26
following both single and dual unit LOOPs. The licensee selected subjective
probabilities for each of the steps using an expert elicitation technique similar to one
described in NUREG/CR-5424. The individual probabilities were then combined to
determine the conditional failure probability of each sequence of steps. These results
were then incorporated into the plant probabilistic risk analysis model to determine
resultant increases in the core damage frequency (CDF) and large early release
frequency (LERF). Results of these efforts indicated only slight increases in the CDF
and LERF values, 2.8E-07 per year and 4.2E-08 per year, respectively.
The inspectors evaluated the engineering and probability information provided for each
of the licensee-defined blocks. The results of the individual block evaluations were then
combined into an D/G common cause failure factor. This factor was then used to
modify SPAR model risk analysis results. Based upon information provided in the
licensees probabilistic evaluation, the inspectors developed a common cause failure
factor of 0.14 for a single unit LOOP event and 0.024 for a dual unit LOOP event. Using
the NRCs SPAR model and the assumptions stated below, the inspectors and NRC
Headquarters staff determined that the delta CDF and LERF values for the issue were
1.8E-05 per year and 7.1E-06 per year, respectively.
A summary of the inspectors assessment of the licensees overall evaluation
methodology and the individual block results were as follows.
Overall Methodology
The inspectors reviewed the overall evaluation methodology and NUREG/CR 5424. The
inspectors determined that the overall methodology was reasonable and that the
identified steps in the sequence of events were consistent with the course of events that
would be necessary for a debris intrusion event to occur. However, the inspectors also
determined that the subjective probability scale developed by the licensee using the
referenced NUREG/CR 5424 was not consistent with the information provided in the
NUREG/CR 5424. Instead of the relatively continuous scale proposed and used in the
NUREG/CR 5424, the licensees scale tended to stratify event probabilities near 1.0 and
0. As a result, the licensees under-estimation of one or two steps in a sequence of
steps would tend to significantly decrease the overall probability for a sequence.
Several sequences appeared to have been affected by the licensees use of their
subjective probability scale, as described below.
Block 1: Loss of Offsite Power
The licensees analysis assumed the LOOP event, either single or dual unit, as a given.
Therefore, this probability was set equal to 1.0.
The inspectors used a similar approach to developing their common cause factor.
Therefore, the inspectors also considered the probability for this Block to be 1.0.
Block 2: Suspended Debris is Sufficient to Challenge the ESW-D/G System
The licensee evaluated this Block as the combined probability that flows coming into the
intake structure contained a sufficient amount of debris with the probability that changes
27
to the intake structure flow caused the entrainment of a sufficient amount of debris to
challenge the ESW-D/G system. Using a combination of plant data and industry
information, the licensee developed probabilities for each of several sub-blocks
identified necessary to construct the overall probability. The resultant Block single unit
and dual unit LOOP probabilities were 0.1033 and 0.0189, respectively.
The inspectors reviewed the sub-blocks used to construct the overall probability for
Block 2 and concurred with the licensees general characterization of the sub-blocks.
However, the inspectors did not agree with the licensees assumptions that: 1) debris
generation, as a result of wind and wave action, was independent of the severe weather
initiating event frequency; 2) debris, brought into the intake structure and of concern for
challenging the ESW-D/G system, would be very unlikely (P=0.05) to bypass the
traveling screens; 3) intake structure water vertical velocities, developed during an
inrush of water following a dual unit LOOP, would be unlikely (P=0.1) to entrain debris
resident between the traveling screens and the ESW pumps, and; 4) debris, present
between the traveling screens and the ESW pumps, would be unlikely (P=0.1) to be of
sufficient quantities to challenge the ESW-D/G system.
Since Items 1 and 2 above did not contribute significantly to the final probability for
Block 2, the inspectors did not further evaluate these items.
Of the remaining items, the inspectors determined that engineering judgement
accounted for differences in the probabilities assumed for Items 3 and 4. Specifically,
for Item 3, the inspectors assumed that the inrush of approximately 1.6 million
gallons/minute of water, expected to occur immediately after a dual unit LOOP event,
would provide sufficient energy and flow velocities to cause local eddies and vertical
water velocities sufficient to entrain debris located in the previous quiescent flow areas
of the intake structure (P=1.0). In their analysis, the licensee assumed that the intake
structure vertical water velocities would be limited to the bulk rate of rise of the intake
structure water level, a level which may not support entrainment of significant quantities
of debris. For Item 4, the inspectors assumed that debris was present in sufficient
quantities, between the traveling screens and the ESW pump intakes, to challenge the
ESW system approximately one half of the time each year (P=0.5). This value was
considered a conservative estimate based upon the licensees practice of cleaning 1/2 of
the intake structure during unit refueling outages, on an approximate once every
9 month time frame.
Block 3: Suspended Debris Reaches the ESW Pump Suction
The licensee assumed that, if sufficient debris was suspended in the intake structure
water, it was nearly certain that at least some of the debris would reach the Unit 1 East
ESW pump suction and be ingested. Therefore, the licensee assigned a probability of
0.99 to this block.
The inspectors used a similar approach to developing their common cause factor.
Therefore, the inspectors considered the probability for this Block to be 1.0.
Block 4: Failed Strainer Basket is in Service During a LOOP Event
28
The licensee evaluated this block as a combination of probabilities that the failed 1 East
ESW strainer was in service at the start of a LOOP event or was brought into service
during the LOOP event as a result of an automatic timer or due to sensed high
differential pressure across the undamaged duplex strainer. Results of the licensees
evaluation indicated a single unit LOOP probability of 1.0 and a dual unit LOOP
probability of 0.77.
The inspectors reviewed the sub-blocks used to construct the overall probability for
Block 4 and concurred with the licensees general characterization of the sub-blocks and
the resultant probabilities.
Blocks 5 and 6: ESW Flow is High and Ingested Debris Bypasses the 1 East ESW
Strainer
The licensees analysis proposed that all sequences, which could result in the D/Gs
being affected by ingested debris, include two steps which were dependent upon the
presence of high ESW flow rates. High ESW flow rates were characterized as a flow
rate greater than 5000 gallons/minute. The relative probability of having high ESW flow
rates was determined based upon ESW system heat loads throughout the year.
Assuming the presence of high ESW flow rates, the analysis concluded that debris
entering the ESW strainer housings would have a high likelihood of being able to reach
the 1 East ESW pump strainer defect and pass through into the ESW-D/G flow stream.
Without the presence of high ESW flow rates, ingested debris was assumed to be
retained in the strainer housing, probability of high flow and strainer bypass equal to
0.14.
Based upon the information provided in the evaluation, the inspectors could not
independently confirm the basis for the proposed high ESW flow rate steps.
Specifically, the inspectors could not validate the licensees technical basis for
concluding that ESW flow rates of greater than 5000 gallons/minute were necessary to
transport debris within the ESW strainer housing from the inlet point up to the strainer
defect location, a change in elevation of approximately 2 feet. In addition, the inspectors
noted that evaluation did not consider the presence of a second bypass path or the
consequences of a buildup of debris within the housing during post-LOOP periods with
low ESW flow rate. As a result, the inspectors concluded that debris which entered the
ESW pump suction was transported into the ESW-D/G flow stream, probability of
strainer bypass for all flow conditions equals 1.0.
Block 7: Ingested Debris Reaches the Unit 2 D/G Heat Exchangers
The licensees analysis proposed that debris which entered the ESW-D/G flow stream
had a certain probability of reaching the Unit 2 D/G heat exchangers based, in part, on
the system pre-LOOP ESW system alignment and ESW system demand. Because the
ESW-D/G system included both train and Unit cross ties, the 1 East ESW pump, with its
faulted strainer, had the potential to feed any and both ESW-D/G trains for both Units.
This was the situation during the August 2001 event. However, the licensees analysis
appropriately highlighted that during a LOOP condition, all four ESW pumps would be in
operation. This condition would change the post-LOOP ESW system flow dynamics and
result in a significantly decreased cross flow, and debris transport, through the Unit
29
cross tie. The licensees analysis also proposed that only one of the four normal ESW
system pre-LOOP alignments would result in sufficient Unit cross flow to carry debris
from Unit 1 to Unit 2.
The inspectors reviewed the licensees basis for the proposed probability and concurred
that the post-LOOP starting of all four ESW pumps would change the system flow
characteristics and the relative likelihood that debris, ingested through the 1 East ESW
pump, would reach the Unit 2 D/Gs. However, the inspectors did not concur with the
licensees conjecture that a minimum 2500 gallons/minute of Unit 1 to Unit 2 cross flow
was necessary to transport debris between the Units during a post-LOOP alignment.
Instead, the inspectors concluded that debris could be transported from Unit 1 to Unit 2,
at varying rates, even with very low cross flow rates, due to the relatively short, 15 foot,
cross tie connection distances. Lower post-LOOP debris transport rates between the
Units would provide the operators with another opportunity to recognize and correct or
halt ESW-D/G plugging of the Unit 2 D/Gs. As a result, the inspectors concluded that
the proposed step probability of 0.25 was appropriate.
30
Block 8: ESW Flow Degradation Impacts D/G Function
In this block, the licensee estimated the probability that debris, having reached the D/G
coolers, would impact the D/G function. Through a review of information gathered from
the August 2001 event, the licensee concluded that only 1 of the 4 D/Gs were actually
impacted by the debris intrusion. As a result, the licensee assumed a per D/G impact
probability of 0.25. In their development of the event trees for these sequences, the
licensee further treated this failure probability as an independent random variable. This
approach resulted in an overall failure probability for the 4 D/G system of approximately
0.004.
Based upon an independent review of operator and computer logs from the
August 2001 event, the inspectors determined that 3 D/Gs were impacted by the debris.
Specifically, the 1AB D/G experienced less than reliable flow indication conditions, and
the two Unit 2 D/Gs were trending to a less than reliable flow indication condition. The
1CD D/G experienced degraded flow which levelized at approximately
350 gallons/minute and was not considered substantially impacted by the debris
intrusion. Based, in part, on the observed August 2001 debris intrusion D/G impacts,
the inspectors concluded that the probability of a debris intrusion event impacting an
individual D/G was approximately 0.75. The inspectors assumed a probability that all
4 D/Gs would be impacted by a debris intrusion event to be approximately 0.25.
Block 9: Condition is Not Identified and Cleared by the Operators
In this block the licensee proposed to assign the HEP values previously developed and
evaluated by the inspectors as a part of the engineering evaluation. The
licensee-proposed HEP values were 0.054, for a single unit LOOP event, and 0.13, for a
dual unit LOOP event, respectively.
The inspectors reviewed and concurred with the methodology used to develop these
probabilities as discussed in Section 4OA3.4.b.1 of this report.
b.3 Essential Service Water Supported Safety Function Capability Assessment
The ESW system provided essential cooling for the D/G turbocharger air aftercoolers,
and the lubricating oil and jacket water coolers. Each D/G could be aligned to either the
East or West ESW supply header in the associated unit via normal and alternate ESW
supply valves. The associated safety train supplied normal ESW cooling while the
opposite safety train supplied alternate ESW cooling. The D/G ESW supply valve
control logic was designed to fully open both the normal and alternate ESW motor
operated supply valves in response to a diesel start signal.
Based upon independent review of operator and computer logs from the August 2001
event, post shutdown inspections of the ESW system heat exchangers, requirements
specified in the licensees UFSAR, and the licensees engineering and probabilistic
evaluation of the specific and generic impacts of the August 2001 event, the inspectors
determined that one of the two Unit 1 D/Gs experienced a less than reliable ESW-D/G
31
flow condition and may not have been able to perform its intended function, had it been
called upon. The second Unit 1 D/G also experienced degraded ESW-D/G flow,
however; the degraded ESW-D/G flow had stabilized and was sufficient to support D/G
operations during a post-LOOP environment. The two Unit 2 D/Gs also experienced
degraded ESW-D/G flow conditions as a result of the debris intrusion and were trending
to a less than reliable flow indication condition when the operators identified the
degrading condition. At the time the operators identified the degraded ESW-D/G to the
Unit 2 D/Gs, the ESW-D/G flow rates were still sufficient to support D/G operations
during a post-LOOP environment. However, the observed negative trend in the
ESW-D/G flow rates may have resulted in the D/Gs being unable to continue to function
in a very short time.
Considering the damaged condition of the 1 East ESW strainer basket, the less than
reliable ESW-D/G flow condition for one of the D/Gs, degraded flow for two of the
remaining D/Gs, and a review of engineering and probabilistic evaluations developed by
the licensee, the inspectors concluded that, absent operator intervention, a similar
debris intrusion event could cause ESW flow degradation to the heat exchangers for all
four D/Gs and result in the D/Gs being unable to perform their assumed safety function
in a post-LOOP environment. The loss of the emergency alternating current (AC) power
safety function had a credible impact on safety and therefore was of more than minor
concern. Because the D/Gs supported the operation of accident mitigation equipment,
the inspectors determined that this issue was associated with the Reactor Safety-
Mitigating Systems cornerstone. During a Phase 1 Significance Determination Process
(SDP) screening of issue, the inspectors concluded that the issue represented a
credible actual loss of safety function and therefore required a Phase 2 SDP Review.
During the Phase 2 SDP review, the licensee provided the engineering and probabilistic
evaluations of the specific and generic impacts of an ESW-D/G debris intrusion event.
In order to properly incorporate the additional licensee-provided information, a Phase 3
SDP assessment was performed.
Risk Assessment Considerations
The inspectors and NRC Headquarters staff evaluated the risk significance of the
inspection finding (failed ESW strainer which allowed a significant amount of debris to
enter and form flow blockages in the ESW-D/G system) in terms of internal events using
the NRC SPAR model. Consistent with the guidance for the SDP, the change in core
damage frequency (CDF), stemming from the identified failed ESW strainer was
assessed. The assessment focused on LOOP events which could: 1) cause debris,
present in the intake structure, to be entrained and ingested into the ESW system, and;
2) result in the Units to rely upon the D/Gs for onsite AC power. The assessment
assumed:
- An initiating event frequency of 0.01 for a single unit LOOP and 0.007 for a dual
unit LOOP.
- An exposure time of 1 year, the maximum timeframe used for these time
calculations, based upon evidence which indicated that the ESW strainer failure
had likely occurred during initial installation in 1989.
32
- Cross flows within the intake structure, following a single unit LOOP event, would
entrain sufficient debris in the ESW-D/G flow stream to cause less than reliable
ESW-D/G flow through the D/G heat exchangers within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
- Inrush flows into the intake structure, following a dual unit LOOP event, would
entrain sufficient debris in the ESW-D/G flow stream to cause less than reliable
ESW-D/G flow through the D/G heat exchangers within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.
- Debris entrained within the intake structure would resettle to the intake structure
floor within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> after the flow perturbation or change had subsided.
- Frequency-weighted non-recovery curves associated with plant-centered, grid,
severe weather, and extreme weather events for a single unit LOOP; and,
frequency-weighted non-recovery curves associated with severe and extreme
weather events for a dual unit LOOP.
- Operator recovery from less than reliable ESW-D/G heat exchanger flow
conditions were characterized by human error probabilities of 0.054 for a single
unit LOOP and 0.13 for a dual unit LOOP.
- The electrical distribution system does not include capability to electrically
cross-tie between the Unit 1 and Unit 2 safety related busses.
- The motor driven auxiliary feedwater systems could be cross tied between Units
for a single unit LOOP.
- A common cause failure factor was used to account for probabilities that:
1) insufficient debris would be available within the intake structure; 2) the failed
1 East ESW strainer may not be in service during the LOOP event; 3) pre-LOOP
system alignments may delay or reduce the debris transported from Unit 1 to
Unit 2, and; 4) all debris intrusion events may not result in all of the D/Gs
experiencing less than reliable ESW-D/G flow conditions. A value of 0.14 was
used for the single unit LOOP and 0.024 for the dual unit LOOP common cause
failure factor.
- Mitigating equipment was assumed to be available once offsite power was
recovered. Potential unavailabilities of these components, due to degraded
ESW cooling flow, was not considered.
- The conditional probability of a large early release, given a core damage event
for an ice condenser containment, was assumed to be 0.4.
Using the NRCs SPAR model and the assumptions stated above, the inspectors and
NRC Headquarters staff determined that the per plant delta CDF value was dominated
by a dual unit LOOP event. The calculated dual unit LOOP delta CDF value was
determined to be 1.8E-05 per year (Yellow). For both the single and dual unit LOOP
events, the dominant sequence was a station blackout with a failure to recover AC
power before station battery depletion.
33
The inspectors and NRC Headquarters staff also evaluated the impact of this issue on
the LERF. Using a conditional probability of a large early release, given a core damage
event for an ice condenser containment, of 0.4, the staff determined the delta LERF for
the issue was 7.1E-06 (Yellow) for a dual unit LOOP.
The Regional Senior Risk Analyst and the NRC Headquarters staff concluded that the
risk significance of the inspection finding, based on the change in CDF due to internal
events and LERF considerations, to be Yellow. A Yellow finding represents a finding of
substantial safety significance.
b.4 Other ESW Support Systems
Component Cooling Water System
The CCW system provided cooling to heat exchangers in the following risk-significant
systems: residual heat removal, ECCS, spent fuel pool cooling, reactor coolant pump
thermal barrier, and containment air recirculating. Each Unit's CCW system was
arranged in three flow circuits: two parallel safeguards equipment trains, and one
miscellaneous services train which can be served by either safeguards train.
During the August 2001 debris intrusion event, ESW flow to the Unit 1 East and Unit 2
West CCW heat exchangers became degraded. Essential Service Water system flow
to the Unit 1 East CCW heat exchanger was as low as 2100 gpm but increased to
3900 gpm following cycling of the inlet and outlet ESW valves. The Unit 2 West CCW
heat exchanger ESW flow decreased to approximately 2400 gpm but improved to
approximately 5000 gpm following cycling of the ESW inlet and outlet valve. Section 9.8
of the UFSAR stated that the minimum ESW flow required to support post-accident
CCW heat loads was 5000 gpm, but up to 8700 gpm of ESW flow was required to
support normal operation and cooldown. Additionally, Section 9.5.2 of the UFSAR
stated that the CCW system was designed and analyzed to operate at CCW heat
exchanger outlet temperatures up to 120°F during cooldown and accident conditions.
Although debris intrusion reduced the maximum ESW flow capability for the Unit 1 East
and Unit 2 West CCW heat exchangers below design requirements, the inspectors
determined that the CCW heat exchanger outlet temperatures did not exceed the 120°F
analysis limit during the event.
Because Unit 1 was in Mode 5 at the time of the event, its CCW system supported
decay heat removal system operation, but it was not required to support post-accident
heat loads. Additionally, the debris intrusion event did not degrade flow to the Unit 1
West CCW train and reactor coolant system temperatures remained stable during the
event. Based on the availability of the opposite train and the stable reactor coolant
system operation during and immediately following the event, the inspectors determined
that the safety impact of degraded ESW flow to the Unit 1 East CCW heat exchanger
was minimal.
Because Unit 2 was in Mode 1 at the time of the degraded flow event, the licensee
entered TS 3.7.3.1 and placed the Unit in Mode 5 within the required TS limiting
condition for operation time limits. During the event, the Unit 2 East CCW train
remained available to provide cooling for normal operation and accident heat loads.
34
Based on the availability of the opposite CCW train and licensee compliance with
TS 3.7.3.1 for one inoperable CCW train, the inspectors determined that the safety
impact of degraded flow to the Unit 2 West CCW heat exchanger was minimal.
Auxiliary Feedwater Pump Room Cooling and Emergency Water Supply
The ESW system provided the safety-related water source to each AFW pump and
support cooling to the AFW pump room coolers. Following the debris intrusion event,
the licensee identified degraded performance of the Unit 1 East MDAFWP room cooler
and the Unit 2 West TDAFWP room cooler. At the time of the event, Unit 1 was
operating in Modes 4 and 5 and did not require the AFW system to support decay heat
removal. The inspectors evaluated the safety impact of degraded ESW flow on the
capability to provide secondary plant makeup to Unit 2. The inspectors considered the
following factors:
- The condensate storage tank provided the normal suction supply to the AFW
pumps and remained available during the event. Consequently, the inspectors
determined that the loss of the emergency AFW pump suction water supply from
the ESW system did not significantly impact the ability of the AFW system to
perform its safety function.
- The TDAFWP room is cooled by two 100 percent capacity coolers. Because the
Unit 2 East TDAFWP room cooler had adequate cooling capacity to maintain
TDAFWP room temperatures, the loss of the Unit 2 West TDAFWP room cooler
did not adversely impact the ability of the TDAFWP to perform its safety function.
during and immediately following the event. Consequently, the inspectors
determined that because of the availability of redundant trains of MDAFWPs
sufficient AFW system capability was available to support Unit 2 during this
event.
- The annunciator response procedures for high MDAFWP room temperature
included proceduralized compensatory actions for degraded room cooling.
Based on these factors, the inspectors concluded that the impact of the ESW debris
intrusion on the AFW system was minimal.
Control Room Air Conditioning System (CRAC)
The CRAC units provided cooling to maintain temperatures at which control room
equipment was qualified for the life of the plant. As stated in the bases for TS 3.7.5.1,
"Control Room Emergency Ventilation System," at control room temperatures less than
or equal to 102°F, vital control room equipment remained within the manufacturers
recommended operating range. The inspectors reviewed control room logs and
determined that control room temperatures did not exceed 80°F during and immediately
following the degraded ESW event. Based on the ability of the CRAC units to
adequately maintain control room temperatures, the inspectors determined that the
impact of this event on the control room ventilation system was minimal.
35
Containment Spray System
The primary purpose of the Containment Spray System is to spray cool water into the
containment atmosphere in the event of a loss-of-coolant to prevent containment
pressure from exceeding the design value. With the exception of alignment of the Unit 2
East CTS heat exchanger for ESW flushing on August 30, 2001, the ESW supplies to
the CTS heat exchangers were isolated during the event. Subsequent inspections and
engineering evaluations of the CTS system identified no significant fouling or
obstructions of flow. The inspectors concluded that the debris intrusion event had
minimal safety impact on the CTS system.
.5 Adequacy of Corrective Actions
a. Inspection Scope
The inspectors attended licensee meetings, interviewed personnel, observed
maintenance activities, reviewed testing plans, and performed system walkdowns as
part of the assessment of the adequacy of the licensees corrective actions for the
restoration of:
- Component Cooling Water System
- Other safety-related components served by ESW
b. Findings
The licensee established a series of recovery and support teams in order to identify
equipment, procedural and personnel performance issues that needed to be addressed
before the equipment could be restored to full service. The inspectors determined that
the licensees corrective actions were prompt, thorough, and effective.
The licensee inspected the cooling systems of all D/Gs immediately following the event.
For each D/G, the licensee inspected and cleaned (as necessary) both air after-coolers,
the lube oil cooler, the jacket water cooler, and supply piping.
In addition to cooling system inspection and cleaning, the licensee installed ESW
differential pressure instrumentation on each lube oil cooler to assist in the future
identification of cooling system blockage. The licensee also removed the automatic
opening control logic for the alternate D/G cooling ESW supply valves to preclude cross
train transport of debris into the D/G cooling systems.
Component Cooling Water System
The licensee removed the end bells of the Unit 1 East CCW heat exchanger and
performed inspections. The licensee identified sand, zebra mussel shells, and large
debris. The licensee considered large debris as debris that was greater than 1/8 inch.
The debris blocked approximately 10 percent of the tubes. The licensee removed the
36
debris and hydro-lanced the heat exchanger tubes. The ESW supply and return piping
for the CCW heat exchanger was cleaned as part of the overall system flush.
Other Safety-Related Components Served by ESW
The licensee initiated a recovery team to specifically address the scope of corrective
action necessary to restore the ESW system to service. The team evaluated other
components served by ESW and recommended corrective actions. These corrective
actions included:
- Inspecting and cleaning the CRAC units as necessary. The air conditioners
were determined to be very clean with only minimal material.
- Inspecting and cleaning the AFW pump room coolers. The Unit 1 East
MDAFWP room cooler and one of the two room coolers to the Unit 2 TDAFWP
were identified to have significant blockage. These coolers were cleaned and
returned to service.
- The Unit 1 East ESW pump discharge strainer was opened and inspected. The
east strainer basket was determined to have significant damage and bypass.
The west strainer basket was determined to have some smaller amount of
bypass over the top of the basket. Both baskets were replaced.
- Two radiation monitors which drew sample flow from the ESW trains were
cleaned.
- Instrumentation connected to the Unit 1 East ESW system was inspected and
flushed.
- Portions of ESW piping that could not be inspected internally or were not
assured of achieving high flow rates during flushing activities were
Ultra-Sonically tested. The tests indicated that portions of the piping did contain
debris. For example, one 12 inch diameter pipe contained approximately
2 inches of debris. The licensee flushed the material from the system.
- The licensee performed an ESW system flow verification surveillance test in
order to ensure that all components served by the ESW system had been
restored to operable.
.6 Adequacy of Overall Corrective Actions to Address Recurrence of Sand/Silt Buildup
Problems
a. Inspection Scope
The inspectors attended licensee meetings, interviewed personnel, observed
maintenance activities, reviewed testing plans, and performed system walkdowns as
part of the assessment of the adequacy of the licensees overall corrective actions.
b. Findings
37
The inspectors reviewed the licensees corrective actions which included the following:
- all 8 ESW strainer baskets were inspected and replaced;
- detailed procedural guidance was given for strainer installation;
- a temporary modification to prevent the alternate ESW supply valves to the D/Gs
from going open on a D/G start was installed;
- the normal configuration of the alternate ESW supply valves to the D/Gs was
revised; and
- the new ESW strainer baskets received additional inspection to provide
reasonable assurance of the new strainer baskets structural capability.
The inspectors concluded that the licensees actions appeared reasonable to prevent
recurrence.
.7 Assessment of Interaction of the Maintenance Activities on the Non-Safety Related
Circulating Water System with Operation of the ESW System
a. Inspection Scope
At the time of the event, the CW center intake crib was isolated in order to repair
previously identified damage. The CW pump 13 discharge valve, 1-WMO-13, was
degraded and could not be fully closed. The plant had been operating for several
months with the center intake isolated. The inspectors assessed the interaction and
potential impact of these non-safety related issues on the functioning of the ESW
system.
38
b. Findings
The inspectors determined that CW system flow rates and configuration had a direct
impact upon the functioning of the safety-related ESW system. However, if the Unit 1
East ESW pump discharge strainer east basket had been performing as designed, large
debris would not have entered the ESW system and the operability of components
served by ESW would not have been challenged.
4OA4 Cross-Cutting Issues
.1 Human Performance Issues During Degraded ESW Flow Event
a. Inspection Scope
The inspectors assessed operator performance during the degraded ESW flow event
relative to the human performance cross-cutting issue. The inspectors reviewed control
room logs, plant process computer data, and control room chart recorder data. In
addition, the inspectors interviewed operators and reviewed operator statements.
b. Findings
The inspectors identified several weaknesses in the response of control room operators
to the degraded ESW flow event of August 29, 2001. These weaknesses involved
operator control board monitoring and procedural adherence. Specifically, the
inspectors identified the following issues:
- Upon identifying that both Unit D/Gs were inoperable due to low ESW flow, the
Unit 2 Senior Reactor Operator entered the action statement for TS 3.0.3. As
described in the TS bases, TS 3.0.3 delineated the measures to be taken for
those circumstances not directly provided for in the TS action statements. The
inspectors determined that, because TS 3.8.1.1.e addressed two inoperable
D/Gs, TS 3.0.3 was not the appropriate TS action statement to enter during this
event. The Unit Supervisor stated that he assumed that TS 3.0.3 would apply
with two inoperable D/Gs, and he did not read each TS 3.8.1.1 action statement.
The inspectors noted that TS 3.8.1.1.e specified additional actions not covered
by TS 3.0.3, such as demonstrating the operability of offsite power sources. In
this case, the licensee complied with the action time limits specified in
TS 3.8.1.1.e; thus, there was no impact from the failure to enter the appropriate
TS action statement.
- Based on a review of Plant Process Computer data and control room chart
recorder data, the inspectors concluded that indications of degraded ESW
system performance (i.e., ESW flow below UFSAR minimum) were available to
the control room operators at least 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> prior to the initial identification of
degraded ESW flow to the D/Gs and CCW heat exchangers. Operations head
instruction OHI-4017, "Control Board Monitoring," Step 4.2.8, required, in part
that control boards shall be monitored for changing indications, adverse trends,
and abnormal indications and Step 4.2.4 stated that during normal plant
operations, the reactor operator should perform a walkdown of all control room
39
panels every 60 minutes. The inspectors determined that the control room
operators failure to effectively implement the recommendations contained in
OHI-4017 contributed to the failure to promptly identify degraded ESW system
performance.
- Based on a review of CCW system temperatures recorded on chart recorder
1-SG-10, the inspectors determined that the Unit 1 East CCW heat exchanger
outlet temperature exceeded the 95°F abnormal temperature alarm setpoint for
over 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. Annunciator response procedure 01-OHP 4024.104, Drop 85,
"East CCW Hx Discharge Temp Abnormal," Step 3.3, stated that if the CCW
heat exchanger outlet temperature cannot be maintained less than 95°F, enter
Abnormal Procedure 01-OHP 4022.016.001, "Malfunction of the CCW System."
Although the reactor operator reported receipt of the associated abnormal
temperature alarm, the control room operators did not enter Abnormal Procedure
01-OHP 4022.016.001, contrary to instructions contained in 01-OHP 4024.104.
- Although the Unit 1 East CCW outlet abnormal temperature alarm actuated
during the event, receipt of the alarm and the operators subsequent difficulty in
controlling CCW temperature were not recorded in the control room log and not
effectively communicated to the operations shift management. The inspectors
determined that the operators failure to log receipt of the CCW abnormal
temperature alarm and effectively communicate this abnormal condition was not
consistent with instructions contained in OHI-2212 and OHI-4017. Specifically,
OHI-2212, Step 4.5.7 required, in part, that the actuation of significant
annunciators and unexpected system transients shall be contained in the control
room log and OHI-4017, Step 4.2.11, required, in part, that the US shall be
notified immediately of any indication that is not responding as expected.
The inspectors determined that the failure to adequately apply TS requirements and
implement procedures associated with control board monitoring, logkeeping, and
annunciator response had a credible impact on safety and therefore were more than a
minor concern. Specifically, these issues could reasonably result in the failure to identify
and promptly correct degradation of safety related equipment and therefore impact the
reliability and availability of a safety system. Because these performance deficiencies
contributed to delays in identifying degradation of the ESW and CCW mitigating
systems, the inspectors determined that these human performance weaknesses were
associated with the mitigating systems cornerstone. Although this issue adversely
impacted the licensee's response to the August 29, 2001 event, none of the
performance deficiencies directly resulted in the actual loss of safety system function or
the loss of a single safety system train for greater than its TS allowed outage time.
Consequently, the inspectors concluded that this issue was of very low safety
significance (Green).
Technical Specification 6.8.1 required, in part, that written procedures shall be
implemented for those activities recommended in Appendix "A" of RG 1.33, Revision 2.
Regulatory Guide 1.33, "Quality Assurance Program Requirements," Revision 2,
Appendix "A," recommended, in part, that written procedures cover the following
activities: (1) authorities and responsibilities for safe operation, (2) log entries, and
(3) abnormal, off normal or alarm conditions. The inspectors determined that
40
OHI-2212, "Narrative and Miscellaneous Logkeeping"; OHI-4017, "Control Board
Monitoring"; and 01-OHP 4024.104, "Annunciator #104 Response: Essential Service
Water and Component Cooling"; were written to implement the requirements of
TS 6.8.1. Contrary to TS 6.8.1, the control room operators failed to implement the
instructions contained in (1) OHI-2212, step 4.5.7, (2) OHI-4017, steps 4.2.8 and 4.2.11,
and (3) 01-OHP.4024.104, drop 85, step 3.3, during the degraded ESW event of
August 29, 2001. Specifically, the operators failed to (1) monitor the control boards for
changing indications, adverse trends, and abnormal indications, (2) effectively
communicate receipt of an abnormal temperature alarm for the CCW heat exchanger,
and (3) enter the CCW abnormal operating procedure as directed by the abnormal
temperature alarm response procedure. Because of the very low safety significance,
this violation is being treated as a Non-Cited Violation consistent with Section VI.A of the
NRC Enforcement Policy (NCV 50-315-01-17-02(DRP); 50-316-01-017-02(DRP)). This
violation is in the licensees corrective action program as CR 01250062.
4OA6 Meeting
Exit Meeting
The inspector presented the inspection results to licensee management listed below on
May 17, 2002. The licensee acknowledged the findings presented. No proprietary
information was identified.
41
KEY POINTS OF CONTACT
Licensee
G. Arent, Manager, Regulatory Affairs
C. Bakken, Senior Vice President, Nuclear Generation
G. Bourlodan, Plant Programs Manager
R. Gaston, Regulatory Affairs Compliance Supervisor
J. Gebbie, System Engineering Manager
J. Giessner, Assistant Manager, Operations
S. Greenlee, Director, Nuclear Technical Services
N. Jackiw, Regulatory Affairs
C. Lane, Inservice Inspection Supervisor
E. Larson, Manager, Operations
R. Meister, Regulatory Affairs
J. Molden, Reliability Programs
D. Moul, Assistant Manager, Operations
T. Noonan, Director, Performance Assurance
J. Pollock, Site Vice President and Acting Plant Manager
R. Smith, Assistant Director, Plant Engineering
L. Weber, Performance Assurance
D. Wood, RadChem Environmental Manager
T. Woods, Regulatory Affairs
NRC
Geoffrey Grant, Director, Division of Reactor Projects
Steven Reynolds, Deputy Director Division of Reactor Projects
Anton Vegel, Branch Chief Reactor Projects Branch 6
Sonia Burgess, Senior Reactor Analyst, Division of Reactor Safety
42
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
50-315/01-17-01 AV Essential Service Water strainer maintenance instructions not
50-316/01-17-01 appropriate to the circumstances.
50-315/01-17-02 NCV Human performance weaknesses during the degraded essential
50-316/01-17-02 service water event of August 29, 2001 associated with control
board monitoring and procedural adherence.
Closed
50-315/01-17-02 NCV Human performance weaknesses during the degraded essential
50-316/01-17-02 service water event of August 29, 2001 associated with control
board monitoring and procedural adherence.
Discussed
None
43
LIST OF ACRONYMS USED
AEP American Electric Power
AFW Auxiliary Feedwater System
ATR Administrative Technical Requirement
CCW Component Cooling Water
CDF Core Damage Frequency
CFR Code of Federal Regulations
CR Condition Report
CRAC Control Room Air Conditioning
CTS Containment Spray System
CW Circulating Water
D/G Emergency Diesel Generator
DRP Division of Reactor Projects
EAL Emergency Action Level
ECC Emergency Condition Categories
EOP Emergency Operating Procedure
ESW Essential Service Water
FIN Finding
JO Job Order
HELB High Energy Line Break
IC Initiating Condition
IMC Inspection Manual Chapter
LOOP Loss of Off-Site Power
MDAFWP Motor Driven Auxiliary Feedwater Pump
MHP Maintenance Head Procedure
NRC Nuclear Regulatory Commission
NRR Nuclear Reactor Regulation
OA Other Activities
OHI Operations Head Instruction
OHP Operations Head Procedure
PDR Public Document Room
PMI Plant Managers Instruction
PMP Plant Managers Procedure
PMT Post-maintenance Testing
PPC Plant Process Computer
PRA Probability Risk Assessment
SDP Significance Determination Process
SEC Site Emergency Coordinator
SRA Senior Reactor Analysts
SRO Senior Reactor Operator
SSC Structures, Systems, and Components
STP Surveillance Test Procedure
TBD To Be Determined
TDAFWP Turbine Driven Auxiliary Feedwater Pump
44
TS Technical Specification
UFSAR Updated Final Safety Analysis Report
URI Unresolved Item
US Unit Supervisor
VIO Violation
45
LIST OF DOCUMENTS REVIEWED
Work Requests/Job Orders
JO 01095031 Unit 2 Traveling Water Screen Driving Inspection
JO 01242065 Inspect and Clean Unit 1 ESW and Circulating
Water Pump Bays
JO 01244049 Open and clean 1-HV-ACR-1 (North CRAC)
JO 01244055 Drain and flush 1-HV-AFP-EAC, Unit 1 East
MDAFWP room cooler
JO 01244059 Inspect, clean, and flush 1-HV-AFP-T1AC, the
Unit 1 east TDAFWP room cooler
JO 01244069 Inspect/clean ESW side of heat exchanger
1-QT-110-AB
JO 01244071 Inspect/clean ESW side of heat exchanger
1-QT-110-CD
JO 01244072 Inspect/clean ESW side of heat exchanger
1-QT-131-AB
JO 01244073 Inspect/clean ESW side of heat exchanger
1-QT-131-CD
JO 01244089 Open/inspect/flush 2-HV-ACR-1 (North CRAC)
JO 01244092 2-HV-AFP-WAC Drain and Flush West Cooler
JO 01244094 2-HV-AFP-T2AC Drain and Flush T2AC Cooler
JO 01244097 Inspect/clean ESW side of heat exchanger
2-QT-110-CD
JO 01244099 Inspect/clean ESW side of heat exchanger
2-QT-131-CD
JO 01244096 Inspect/clean ESW side of heat exchanger
2-QT-110-AB
JO 01244098 Inspect/clean ESW side of heat exchanger
2-QT-131-AB
JO R0088138 Unit 1 Screenhouse Diving, Cleaning and Repairs
JO R0100035 2-HE-18W Open Shell Side of Heat Exchanger
for Inspection
46
JO R0210330 Open shell side of 1-HE-18E for inspection
(Unit 1 East CTS heat exchanger)
JO R021036 Unit 1 Screenhouse Diving, Cleaning and Repairs
JO R0217652 Inspect and clean 1-HE-15E (Unit 1 East CCW
heat exchanger)
JO R0096582 Inspect and clean 1-HE-15W (Unit 1 West CCW
heat exchanger)
Condition Reports (CRs)
CR 00273076 Silts/sand from the lake settling out in the dead September 28, 2000
leg section of ESW piping
CR 00295037 1-PP-7W-MTR Failed To Start October 21, 2000
CR 01019031 SA-2001-REA-003, Perform Zebra Mussel January 19, 2001
Assessment During Year 2001
CR 01242007 2-ESW-162-CD Emergency Diesel Jacket Water August 30, 2001
Cooler QT-131-CD tube side vent valve is
blocked and could not be flushed out
CR 01242008 Procedural Deficiency in 02 OHP August 30, 2001
4030.STP.022E, the ESW system test - Step
4.30.3, which aligns the north CRAC for flushing
is missing from the procedure
CR 01242009 2-ESW-163-CD, the Unit 2 CD D/G jacket water August 30, 2001
cooler tube side drain, is clogged and not allowing
flow to pass when opened
CR 01242010 2-ESW-162-AB Emergency Diesel Jacket Water August 30, 2001
Cooler QT-131-AB tube side vent valve is blocked
and could not be flushed out
CR 01242013 Slit/mud intrusion into Unit 1 and 2 ESW systems August 29, 2001
renders CCW and D/G inoperable
CR 01243013 2-HV-AFP-T2AC, the Unit 2 West TDAFWP room August 31, 2001
cooler, does not appear to be functioning
CR 01243015 Unit 1 East auxiliary feedwater pump room cooler August 31, 2001
flow (56 gpm) was less then minimum required
(57 gpm)
47
CR 01243036 Both Unit 1 and Unit 2 D/Gs declared inoperable August 29, 2001
due to low ESW flow. This resulted in Unit 1
entering a RED shutdown risk path.
CR 01243038 Evaluate August 30, 2001, greater than 20 August 30, 2001
percent power reduction on Unit 2 due to
degraded ESW flow for potential Maintenance
Rule impact
CR 01243039 PRA analysis of Unit 2 indicates yellow risk status August 30, 2001
in that the west CCW heat exchanger is not
receiving the required 5000 gpm ESW flow
CR 01244010 1-WMO-12 circulating water pump PP-2-2 September 1, 2001
discharge shutoff valve
CR 01244011 1-WMO-11 Circulating Water Pump PP-2-1 August 31, 2001
Discharge Shutoff Valve
CR 01244016 Wood, mussel shells, and debris larger than September 1, 2001
expected identified during inspection on the Unit 1
east CCW heat exchanger
CR 01244019 Degraded ESW flow documented in CR September 1, 2001
01242013 may indicate that the GL 89-13
program is inadequate
CR 01245030 During inspection of Unit 1 East ESW pump September 2, 2001
discharge strainer baskets, large bypass flow
paths were identified.
CR 01246015 Forced outage schedule does not match actual September 3, 2001
work planning and execution for Unit 1 West
ESW pump work
CR 01247001 Declaration of unusual event during the Unit 1 September 3, 2001
and Unit 2 ESW restriction event on August 29,
2001 would have been prudent
CR 01247041 Open, inspect and clean 1-HV-AFP-WAC (Unit 1 September 4, 2001
west MDAFWP room cooler) to determine extent
of ESW debris intrusion
CR 01247050 NRC identified several human performance September 4, 2001
weaknesses during the ESW fouling event of
August 29, 2001. These included weaknesses in
communication, possible training deficiencies for
abnormal procedures, inconsistent log keeping
and control board monitoring
48
CR 01247054 Due to potential debris buildup within ESW September 4, 2001
system, it is necessary to flush ESW piping
CR 01247055 AFW room coolers have been found to be September 4, 2001
blocked with debris (zebra mussel shells)
CR 01248001 Potential of debris build-up within the ESW September 4, 2001
system upstream of the D/G aircooler 3-way
valves
CR 01248002 Flush piping upstream of D/G aftercooler 3-way September 4, 2001
valves WRV-727 and WRV-725
CR 01250062 NRC identified several operational issues September 7, 2001
associated with the August 29, 2001 degraded
ESW flow event, including: command and
control, control board monitoring, log keeping,
use of technical specifications, conservative
decision making, event reconstruction,
emergency plan implementation, and procedural
usage
CR 01251003 Performance Assurance identified that operators September 7, 2001
failed to establish mode constraint for operability
issues identified during the extent of condition
investigation for the ESW flow degradation event
of August 29, 2001
CR 01251022 The downstream pipe of the Unit 1 East CTS heat September 8, 2001
exchanger shell side vent is blocked
CR 01251029 In-Service testing on the Unit 1 East ESW pump September 8, 2001
indicated rapid degradation
CR 01253005 Quarantine was lost on the Unit 1 East ESW September 9, 2001
strainer east basket. The basket had been
placed in the scrap metal trash bin and taken to
the scrap yard
CR 01260022 1-QT-131-CD diesel generator jacket water heat September 17, 2001
exchanger open, cleaned, and closed with 2
tubes blocked with debris
CR 01268045 Dedication Plan HP-1015 is inconsistent with the September 25, 2001
requirement of 12 EHP-5043-CGD-001
P-00-05677 Essential Service Water Radiation Monitors
(WRA-3500, WRA-3600, WRA-4500 and WRA-
4600) ESW Lines Are Plugged With Sand And
Silt
49
Other Documents
Control Room Operator Logs August 29, 2001 -
August 30, 2001
Final Expanded System Readiness Report April 3, 2000
- ESW System (Unit 2)
PMI-7033 Application and Use of Design Basis, Revision 0
Single Failure Criterion, Engineering
Design Bases, and Current Licensing
Basis
OHI-2212 Narrative and Miscellaneous Logkeeping Revision 4
OHI-4017 Control Board Monitoring Revision 0
01 OHP 4021.016.003 Operation of the Component Cooling Revision 15
Water System During System Startup and
Power Operation
12 OHP 4021.019.001 Operation of the Essential Service Water Revision 23
System
01-OHP 4022.016.001 Malfunction of the CCW System Revision 2
01-OHP-4024-104 Annunciator #104 Response: Essential Revision 12
Service Water and Component Cooling
02-OHP 4022.019.001 ESW System Loss/Rupture Revision 2
01-OHP 4024.113 Annunciator #113 Response: Steam Revision 6
Generator 1 and 2
01-OHP 4024.114 Annunciator #114 Response: Steam Revision 6
Generator 3 and 4
01-OHP-4024.120 Annunciator #120 Response: Station Revision 10
Auxiliary CD
01- OHP CD Diesel Generator Operability Test Revision 16
4030.STP027CD (Train A)
PMP 5030.001.005 Essential Service Water System Revision 0
Inspection Program
Drawing 12-3652 Screen House Plant At EL, 546'-0" Plan Revision 5
To
Column 18-West Portion
Drawing 12-3653 Screen House Plant At EL, 546'-0" Plan Revision 4
To Column 9-West Portion
50
Drawing 12-5776-Y Screen Housing Piping, Misc. Sections,
Units 1 And 2
12 MHP 5021.019.003 Essential Service Water Strainer Revision 4
Maintenance
Calculation Auxiliary Feedwater Pump Room Heat-Up Revision 0
TH-00-05 Temperatures
Design Information Expected D/G Loading During a LOOP Revision 0
Transmittal Event Only
DIT B-02217-00
EVAL- Calculation of Pressure Spike in ESW Revision 0
MD-02-ESW-092-N System Due to Pressure Pulse (Column
Rejoining)
EVAL- Failure Analysis of Strainer Basket (CR Revision 0
MD-01-ESW-095-N 01242013, CR 01245030)
EVAL- Reduction in ESW Temperature to Revision 0
MD-02-ESW-089-N Accommodate Reduced Flowrate to ESW
Components
Calculation Results of Operating the Diesel Generator Revision 0
ENSM980327JDJ Lube Oil Cooler & Jacket Water Cooler at
Elevated ESW Temperatures
Dedication Plan No. Essential Service Water (ESW) Strainer Revision 4
HP-1015 Parts
OP-1-5113 Flow Diagram Essential Service Water Revision 70
OP-1-5113A Flow Diagram Essential Service Water Revision 2
OP-1-5119A Flow Diagram Circulating Water, Priming Revision 60
System And Screen Wash, Unit 1
OP-12-5119 Flow Diagram Circulating Water, Priming Revision 50
System And Screen Wash, Units 1 And 2
OP-2-5113 Flow Diagram Essential Service Water Revision 63
OP-2-5113A Flow Diagram Essential Service Water Revision 4
OP-1-5151C Flow Diagram Emergency Diesel Revision 42
Generator "CD"
Technical Report Debris Intrusion Into the Essential Service Revision 0
NTS-2002-010-REP Water System - Probabilistic Evaluation
51
Technical Report ESW Debris Intrusion Event Evaluation Revision 0
NTS-2002-002-REP
52