L-99-107, Monthly Operating Repts for June 1999 for Bvps,Units 1 & 2. with

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Monthly Operating Repts for June 1999 for Bvps,Units 1 & 2. with
ML20209F990
Person / Time
Site: Beaver Valley
Issue date: 06/30/1999
From: David Jones, Ostrowski K
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-99-107, NUDOCS 9907160201
Download: ML20209F990 (5)


Text

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'Af Telephone (412) 393-6000 Nuc ear G,roup L-99-107 Shippingport. PA 15077-0004 July 8,1999 Beaver Valley Power Station Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Re'3 ort U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

In accordance with NRC Generic Letter 97-02, " Revised Contents of the Monthly Operating Report", and Unit I and 2 Technical Specification 6.9.1.6, the " Monthly Operating Report" is submitted for Unit I and Unit 2 for the month ofJune 1999.

Respectf ,

jh he neo A K. L. Ostrowski -

Division Vice President, ,h Nuclear Operations Group and Plant Manager DTJ/ sip Enclosures cc: NRC Regional Office King ofPrussia, PA The Nuclear Professionals -

9907160201 990630 i

PDR ADOCK 05000334 R PDR

r 1 l . UNIT SHUTDOWNS DOCKET NO. 50-334 UNIT NAME BVPS Unit #1 DATE July 6,1999 COMPLETED BY David T. Jones TELEPHONE (412) 393-4962 REPORTING PERIOD: June 1999 No. Date Type Duration Reasora Method of Cause / Corrective Actions F: Forced (Hours) (1) Shutting s: I Down (2) Comments N i __ .~

, . NONE i l l l

l (1) Reason (2) Method A Equipment Failure (Explain) 1 Manual B - Maintenance or Test 2 ManualTrip/ Scram C . Refusinng 3 AutomaticTrip/ Scram D Regulatory Restriction 4 Continuation E Operator Training / Ucense Examinallon 5 other(Explain)

F Adminletrative G OperationalError(Explain) l H Other(Explain)

SUMMARY

The Unit began the report period operating at a nominal value of 100% output. At 0002 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> on

~ 06/01/99, a reduction in output was commenced per Duquesne Light Company (DLCO) System Operations request to load follow. An output of approximately 89% was achieved at 0106 hours0.00123 days <br />0.0294 hours <br />1.752645e-4 weeks <br />4.0333e-5 months <br /> on 06/01/99. The Unit continued to load follow at approximately 89% output until 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> on 06/01/99 when return to full power was commenced. A nominal value of 100% output was achieved at 0604 hours0.00699 days <br />0.168 hours <br />9.986772e-4 weeks <br />2.29822e-4 months <br /> on 06/01/99.- The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.

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OPERATING DATA REPORT l

DOCKET NO. 50-334 UNIT NAME: BVPS UNIT 01 REPORT DATE: 07/07/99 COMPLETED BY: DAVID T. JONES TELEPHCNE: (412) 393-4962

)

la. REPORTING PERIOD ' JUNE 1999

  • Notes *
1. ' DESIGN ELECTRICAL RATING (Not Mwe): 835 , ,
2. MAX. DEPENDABLE CAPACITY (Net Mwe): 810 [,,,,,,,,,,,,,,,,[

l THIS MONTH YEAR TO DATE CUMULATIVE 3a. HOURS IN REPORTING PERIOD: 720.0 4343.0 203063.0

3. NO. OF HRS. REACTOR WAS CRITICAL: 720.0 3499.0 132779.0
4. 1ERVICE HOURS GENERATOR ON LINE: ,720.0 3430.2 130461.9
5. UMT RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0
6. NET C ECTRICAL ENERGY GEN. (MWH): 588110.0. 2659800.0 96345692.0
7. GPOSS ELECT. ENERGY GEN. (MWH): 623010.0 2840630.0 103007405.0 8, GROSS THERMAL ENERGY GEN. (MWH): 1906371.0 8703685.0 318173462.5
9. UNIT AVAILABILITY FACTOR (%): 100.0 79.0 65.8
10. UNIT CAPACITY FACTOR (MDC) (%): 100.8 75.6- 60.6
11. UNIT FORCED OUTAGE RATE (%): 0.0 13.4 18.2 I'

i l

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a UNIT SHUTDOWNS DOCKET NO. 50-412

. . UNIT NAME BVPS Unit #2 DATE July 6,1999 COMPLETED BY Devid T. Jones TELEPHONE (412) 393-4962 REPORTING PERIOD. June 1999 No. Date Type- Duration Reason Method of Cause / Corrective Actions F: Forced (Hours) (1) Shutting s: Down (2) Comments scheduled NONE (1) Reason (2) Method A Equipment Failure (Explain) 1 Manual B MaintenanceorTest 2 ManualTrip/ Scram C Refueling 3. Automouc Trip / Scram D RegulatoryRestriction 4 - Continuation E Operator Training / Ucense Examination 5. other (Explain)

F Administrative G OperanonalError(Explain)

H . Other (Explain)

J

SUMMARY

]

The Unit began the report period operating at a nominal value of 100% output. The Unit continued to i operate at a nominal value of 100% output until 1027 hours0.0119 days <br />0.285 hours <br />0.0017 weeks <br />3.907735e-4 months <br /> on 06/16/99 when output was reduced by l approximately 1%. This was done to gain extra margin as a conservative measure in order to prevent I a possible turbine runback during the calibration of Loop lll Delta-T/Tavg while possible spiking was occurring on the Loop I channel of Overpressure / Delta-T. Following completion of the calibration, the l Unit was retumed to a nominal value of 100% output at 1911 hours0.0221 days <br />0.531 hours <br />0.00316 weeks <br />7.271355e-4 months <br /> on 06/17/99.

The Unit continued to operate at a nominal value of 100% output until 06/26/99. With unusually warm i and humid atmospheric conditions present, incremental load reductions to approximately 95% output j

~

were commenced at 1520 hours0.0176 days <br />0.422 hours <br />0.00251 weeks <br />5.7836e-4 months <br /> to stabilize Condenser hotwell conditions due to the heat transfer

- capability of the Cooling Tower being slightly below design. Once conditions in the Condenser hotwell had improved, the Unit was retumed to a nominal value of 100% output at 0519 hours0.00601 days <br />0.144 hours <br />8.581349e-4 weeks <br />1.974795e-4 months <br /> on 06/27/99.

With unusually warm and humid atmospheric conditions still present, incremental load reductions to approximately 95% output were commenced again at 1535 hours0.0178 days <br />0.426 hours <br />0.00254 weeks <br />5.840675e-4 months <br /> on 06/27/99. Once conditions in the Condenser hotwell had improved, the Unit was retumed to a nominal value of 100% output at 2348 hours0.0272 days <br />0.652 hours <br />0.00388 weeks <br />8.93414e-4 months <br /> ~on 06/27/99. With unusually warm and humid atmospheric conditions still present, incremental load reductions to approximately 95% output were commenced again at 1542 hours0.0178 days <br />0.428 hours <br />0.00255 weeks <br />5.86731e-4 months <br /> on 06/28/99. Once conditions in the Condenser hotwell had improved, the Unit was retumed to a nominal value of 100% output at 0458 hours0.0053 days <br />0.127 hours <br />7.572751e-4 weeks <br />1.74269e-4 months <br /> on 06/29/99. The Unit continued to operate a nominal value of 100% output for the remainder of the report period.

t OPERATING DATA REPORT DOCKET NO.: 50-412 UNIT NAME: BVPS UNIT #2 REPORT DATE: 07/07/99 COMPLETED BY DAVID T. JONES TELEPHONE: (412) 393-4962 la. REPORTING PF.RIOD: JUNE 1999

  • Notes *
1. DESIGN ELECTRICAL RATING (Not Mwe): 836

[

2. MAX. DEPENDABLE CAPACITY (Not Mwe): 820 ,,,,,,,,,,,,,,,,,[

THIS MONTH YEAR TO DATE CUMULATIVE 3a. HOURS IN REPORTING PERIOD: 720.0 4343.0 101846.0

3. NO. OF HRS. REACTOR WAS CRITICAL: 720.0 3308.2 80904.5
4. SERVICE HOURS GENERATOR ON LINE: , 720.0 3267.9 80297.0
5. UNIT RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0
6. NET ELECTRICAL ENERGY GEN. (MWH): 591189.0 2647049.0 62047631.0
7. GROSS ELECT. ENERGY GEN. (HWM): 622472.0 2795506.0 65652458.0
8. GROSS THERMAL ENERGY GEN. (MWH) : 1902982.0 8460806.0 200965561.0 J 9. UNIT AVAILABILITY FACTOR (%): 100.0 75.2 78.8 I
10. UNIT CAPACITY FACTOR (MDC) (%): 100.1 74.3 74.0
11. UNIT FORCED OUTAGE RATE (%): 0.0 3.4 12.0

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