L-98-096, Monthly Operating Repts for Apr 1998 for Bvps,Units 1 & 2

From kanterella
Jump to navigation Jump to search
Monthly Operating Repts for Apr 1998 for Bvps,Units 1 & 2
ML20247G046
Person / Time
Site: Beaver Valley
Issue date: 04/30/1998
From: Brandt R, David Jones
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GL-97-02, GL-97-2, L-98-096, L-98-96, NUDOCS 9805200119
Download: ML20247G046 (5)


Text

. _ _ _ - - _ _ . _ _ . - _ - - _ - - - - - - _ . - . _--.

l l

.? At3 Telephone (412) 393-6000 Nu e wp L-98-096 ShippinDport. PA 15077-0004 May 7,1998 Beaver Valley Power Station Unit 1 - Docket No. 50-334, License No. DPR-66 l Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Report l

U. S. Nuclear Regulatory Commission Document Control Desk Washington,DC 20555 Gentlemen:

In accordance with NRC Generic Letter 97-02, " Revised Contents of the Monthly Operating Report", and Unit I and 2 Technical Specification 6.9.1.6, the " Monthly Operating Report" is submitted for Unit I and Unit 2 for the month of April,1998.

Respectfully,

}s~<b R. D. Brandt Division Vice President, Nuclear Operations Group and Plant Manager l

DTJ/slp Enclosures ^ '.o AvL /

cc: NRC Regional Office

-[{

j' kf /

King ofPrussia, PA The Nuclear Professionals 9805200119 980430 PDR ADOCK 05000334 R PDR E---_-

, UNIT SHUTDOWNS DOCKET NO. 50-334 UNIT NAME BVPS Unit #1 DATE May 4,1998 COMPLETED BY David T. Jones i

TELEPHONE (412) 393-4962 l REPORTING PERIOD: Aoril 1998 i

( No. Date Type Duration Reason Method of Cause / Corrective Actions F: Forced (Hours) (1) Shutting s: scheduled Down (2) Comments 9 980401 F 719.0 H 4 The Unit remained shutdown in Mode 5 to l

continue with modifications to the Power l

Operated Relief Valves (PORVs) Nitrogen

' Supply Subsystem, and to resolve Technical Spec:fication compliance issues including a change to the Technical Specifications to allow post-modification testing of the PORVs.

l (1) Reason (2) Method A- Equipment Feiture (Eglein) 1 Manuel l B - Maestenance or Test 2 MonumiTrip/ Scram C Refuellng 3 AutomaticTrip/ Scram j D ReguietoryRestriction

' 4- Continuation E Operator Training / Ucense Emmination 5 Other(Eglein)

F - Administrative G OperationalError(Eglein)

H - Other(E@h)

SUMMARY

The Unit remained shutdown in Mode 5 for the entire month of April 1998.

l OPERATING DATA REPORT DOCKET NO.: 50-334 UNIT NAME: BVPS UNIT #1 REPORT DATE: 05/04/98 COMPLETED BY: DAVID T. JONES TELEPHONE: (412) 393-4962 1a. REPORTING PERIOD: APRIL 1998

  • Notes *
1. DESIGN ELECTRICAL RATING (Net MWe): 835 *
2. MAX. DEPENDABLE CAPACITY (Net MWe): 810 *
  • THIS MONTH YEAR TO DATE CUMULATIVE 3a HCURS IN REPORTING PERIOD: 719.0 2879.0 192839.0 I
3. NO. OF HRS. REACTOR WAS CRITICAL: 0.0 279.7 125941.9
4. SERVICE HOURS GENERATOR ON LINE: 0.0 240.5 123714.0
5. UNIT RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0
6. NET ELECTRICAL ENERGY GEN. (MWH) : 0.0 126184.0 90984767.0

! 1. GROSS ELECT. ENERGY GEN. (MWH): 0.0 147694.0 97296890.0

8. GROSS THERMAL ENERGY GEN. (MWH): 0.0 468225.0 300738029.5 l 9. UNIT AVAILABILITY FACTOR (%): 0.0 8.4 65.7
10. UNIT CAPACITY FACTOR (MDC) (%) : 0.0 5.4 60.4
11. UNIT FORCED OUTAGE RATE (%) : 100.0 91.3 17.3 i

~

. UNIT SHUTDOWNS i

DOCKET No. 50-412

! UNIT NAME BVPS Unit #2 DATE May 4,1998

! COMPLETED BY David T. Jones April 1998 TELEPHONE (412) 393-4962 REPORTING PERIOD:

No. Date Type Duration Reason Method of Cause / Corrective Actions l F: Forced (Hours) (1) Shutting l s: Scheduled Down (2) Comments 7 980401 F 719.0 H 4 The Unit remained shutdown in Mode 5 to resolve Technical Specification compliance issues including a change to the Technical Specifications to allow post-maintenance testing of the Power Operated Relief Valves (PORVs) which were completed being repaired in February 1998.

(1) Reason (2) Method A Equipment FeMure(Eglein) 1. Manuel B - Maintenance or Test 2. Manuel Trip / m C . Refueling 3 Automatic Trip / scram D ReguistoryRestriction 4. Continuation E - operator Training / License Examination 5. other (Explain)

F Administrative G . operational Error (Explain)

H - other (Explain)

SUMMARY

The Unit remained shutdown in Mode 5 for the entire month of April 1998.

l l

I

t

, . 1

. 1 1

i

  • OPERATING DATA REPORT DOCKET NO.: 50-412

' UNIT NAME: BVPS UNIT #2 REPORT DATE: 05/04/98  !

COMPLETED BY: DAVID T. JONES i

TELEPHONE: (412) 393-4962 l

l 1a. REPORTING PERIOD: APRIL 1998

  • Notes *
1. DESIGN ELECTRICAL RATING (Net MWe): 836 *
  • i *
  • l 2.

MAX. DEPENDABLE CAPACITY (Net MWe) : 820 *

  • j THIS MONTH YEAR TO DATE CUMULATIVE 3a. HOURS IN REPORTING PERIOD: 719.0 2879.0 91622.0
3. NO. OF HRS. REACTOR WAS CRITICAL: 0.0 0.0 75344.5
4. SERVICE HOURS GENERATOR ON LINE
0.0 0.0 74849.4 l
5. UNIT RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0
6. NET ELECTRICAL ENERGY GEN. (MWH): 0.0 l

0.0 57647298.0 l

7. GROSS ELECT. ENERGY GEN. (MWH): 0.0 0.0 61001672.0  ;
8. GROSS THERMAL ENERGY GEN. (MWH) : 0.0 0.0 186886473.0
9. UNIT AVAILABILITY FACTOR (%) : 0.0 0.0 81.7
10. UNIT CAPACITY FACTOR (MDC) (%) : 0.0 0.0 76.4 l
11. UNIT FORCED OUTAGE RATE (%) : 100.0 100.0 8.7

/.

l L

.