L-99-079, Monthly Operating Repts for Apr 1999 for Beaver Valley Power Station,Units 1 & 2.With

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Monthly Operating Repts for Apr 1999 for Beaver Valley Power Station,Units 1 & 2.With
ML20206Q501
Person / Time
Site: Beaver Valley  FirstEnergy icon.png
Issue date: 04/30/1999
From: David Jones, Ostrowski K
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-99-079, L-99-79, NUDOCS 9905190145
Download: ML20206Q501 (8)


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Telephone (412) 393-6000 Nuclear Group L-99-079 P.O. Box 4 1

Shippingport, PA 15077-0004 May 7,1999 Beaver Valley Power Station  ;

Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operatina Report U. S. Nuclear Regulatory Commission Document ControlDesk Washington,DC 20555 Gentlemen:  ;

i In accordance with NRC Generic Letter 97-02, " Revised Contents of the Monthly j Operating Report", and Unit I and 2 Technical Specification 6.9.1.6, the " Monthly Operating i Report" is submitted for Unit 1 and Unit 2 for the month of April,1999.

Respectfully, b

  • l K. L. Ostrowski ',

i Division Vice President,

{

Nuclear Operations Group  !

and Plant Manager DTJ/stp Enclosures cc: NRC Regional Office King ofPrussia, PA The Nuclear Professionals 9905190145 990430 PDR ADOCK 05000334 R PDR t

UNIT SHUTDOWNS DOCKET NO. 50-334 UNIT NAME BVPS Unit #1 I DATE May 4,1999 COMPLETED BY David T. Jones TELEPHONE (412) 393-4962 REPORTING PERIOD: April 1999 j No. Date Type Duration Reason Method of Cause / Corrective Actions F: Forced (Hours) (1) Shuttin0 s: scheduled Down (2) Comments 6 990413 S 384.0 B 1 The Unit was shutdown for a planned I outage to complete required surveillance testing in accordance with Technical Specifications. i 7 990429 F 45.4 A 4 The. planned 16-day surveillance outage was extended due to delays caused by required repair of a Roador Plant Component Cooling Water System leak in the 18 Reactor Coolard Pump lower motor i bearing lobe oil cooler.

(1) Reason (2) Method A - Equipment Fagure (Eginin) 1 Monumi s MaintenanceorTest 2 ManuelTripIscram C - Refueling 3 AutomsecTrip/ Scram D Re0uistory Restridion 4 Continumbon E Ocerator Training / uoenes Ememinallon 5- other (Egimin)

F - Administrailwe G operamonalError(Emplain)

H other(Eginin)

SUMMARY

The Unit began the report period operating at approximately 98% output due to the 1A/1C Moisture l Separator Reheaters (MSRs) being out-of-service. The MSRs could not be returned to service l because their supply valve was inoperable due to a stem / plug separation which could not be repaired until the Unit was shutdown. Repair of the valve was planned for during the Unit 1 Surveillance Outage which vtarted on 04/13/99.

On 04/11/99 at 1707 hours0.0198 days <br />0.474 hours <br />0.00282 weeks <br />6.495135e-4 months <br />, the Unit commenced a power reduction to approximately 50% output to perform planned testing of the Main Steam Safety Valves (MSSVs). An output of approximately 48%

was achieved at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on 04/11/99. Following satisfactory completion of MSSV testing, the Unit began to increase power to approximately 62% output at 1156 hours0.0134 days <br />0.321 hours <br />0.00191 weeks <br />4.39858e-4 months <br /> on 04/12/99. An output of approximately 62% was achieved at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> on 04/12/99. This was done at the request of Duquesne Light Company System Operations prior to commencing the final power reduction and removing the Unit from service for the planned Unit i Surveillance Outage.

f i

UNIT SHUTDOWNS DOCKET NO. 50-334 UNIT NAME BVPS Unit #1 DATE May 4,1999 COMPLETED BY David T. Jones TELEPHONE (412) 393-4962 REPORTING PERIOD: April 1999 j

l 1

SUMMARY

(continted):

On 04/12/99 at 2104 hours0.0244 days <br />0.584 hours <br />0.00348 weeks <br />8.00572e-4 months <br />, the Unit commenced to shutdown for the planned Surveillance Outage.

The Unit was taken off-line at 0236 hours0.00273 days <br />0.0656 hours <br />3.902116e-4 weeks <br />8.9798e-5 months <br /> and Mode 2 was entered at 0312 hours0.00361 days <br />0.0867 hours <br />5.15873e-4 weeks <br />1.18716e-4 months <br /> on 04/13/99. As continuous rod insertion was ongoing to bnng the Unit into Mode 3, Control Banks "C" and "D" were l

inserted without incident, however, upon reaching 100 steps for Group 2 of Bank "B", an " urgent '

alarm" was received that inhibited further manual rod mobon The Unit was confirmed to have entered Mode 3 at 0347 hours0.00402 days <br />0.0964 hours <br />5.737434e-4 weeks <br />1.320335e-4 months <br /> on 04/13/99. At 0427 hours0.00494 days <br />0.119 hours <br />7.060185e-4 weeks <br />1.624735e-4 months <br /> on 04/13/99 with the reactor subentical, the reactor  !

trip breakers were manually opened and all rods fully inserted. The cause for the " urgent alarm" was ,

due to a failed card in the Rod Control System. The Unit began to cool down and Mode 4 was  !

entered at 1550 hours0.0179 days <br />0.431 hours <br />0.00256 weeks <br />5.89775e-4 months <br /> on 04/13/99. Cold shutdown (Mode 5) was entered at 2235 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.504175e-4 months <br /> on 04/13/99.

The Unit remained in Mode 5 to perform required shutdown surveillance testing in accordance with plant Technical Specifications.

l Upon completion of all required surveillance testing and repair of a Reactor Plant Component Cooling Water System leak in the 1B Reactor Coolant Pump lower motor beanng lube oil cooler, the Unit began to heat-up and entered Mode 4 at 1409 hours0.0163 days <br />0.391 hours <br />0.00233 weeks <br />5.361245e-4 months <br /> on 04/28/90. Mode 3 was entered at 0038 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br /> l on 04/29/99. Upon completing required startup testing, Mode 2 was entered at 1621 hours0.0188 days <br />0.45 hours <br />0.00268 weeks <br />6.167905e-4 months <br /> on j 04/30/99. The reactor was taken entical at 1715 hours0.0198 days <br />0.476 hours <br />0.00284 weeks <br />6.525575e-4 months <br />, and Mode 1 was entered at 1915 hours0.0222 days <br />0.532 hours <br />0.00317 weeks <br />7.286575e-4 months <br /> on l 04/30/99. The Unit continued with preparations for synchronization to the electncal grid, however, l continuing problems with the Main Unit Generator (MUG) Hydrogen Seal Oil System resulted in the Unit being taken back to hot shutdown status. Mode 2 was entered at 1106 hours0.0128 days <br />0.307 hours <br />0.00183 weeks <br />4.20833e-4 months <br /> and Mode 3 was l entered at 1141 hours0.0132 days <br />0.317 hours <br />0.00189 weeks <br />4.341505e-4 months <br /> on 05/01/99 in preparation for cleanup of the MUG Seal Oil System.

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l OPERATING DATA REPORT j DOCKET NO.: 50-334 UNIT NAME: BVPS UNIT #1 l REPORT DATE: 05/05/99 COMPLETED BY LAVID T. JONES TELEPHONE: (412) 393-4962 la. REPORTING PERIOD: -APRIL 1999

  • Notes *

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1. DESIGN ELECTRICAL RATING (Net Mwe): 835 , , )
2. MAX. DEPENDABLE CAPACITY (Net Mwe): 810

. * )

J I

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THIS MOffrH YEAR TO DATE CUMULATIVE l I

3a. HOURS IN REPORTING PERIOD: 719.0 2879.0 201599.0 i

3. NO. OF HRS. REACTOR WAS CRITICAL: 297.6 2193.8 131473.8 l
4. SERVICE HOURS GENERATOR ON LINE: 289.6 2130.9 129162.6 .

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S. UNIT RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0 l l

6. NET ELECTRICAL ENERGY GEN. (MWH): 212665.0 1643544.0 95329436.0 I
7. GROSS ELECT, ENERGY GEN. (MWH): 233185.0 1758634.0 101925409.0
8. GROSS THERMAL ENERGY GEN. (MWH): 716664.0 5386836.0 314856613.5  !

, 9. UNIT AVAILABILITY FACTOR (%): 40.3 74.0 65.6

10. UNIT CAPACITY FACTOR (MDC) (%): 36.5 70.5 60.4 l 11. UNIT FORCED OUTAGE RATE (%): 13.6 14.6 18.3 !

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f UNIT SHUTDOWNS i

DOCKET NO. 50-412 UNIT NAME BVPS UnM #2  ;

DATE May 4,1999 (

COMPLETED BY David T. Jones TELEPHONE (412) 393-4962 i REPORTING PERIOD: Acril 1999 )

1 No. Date Type Duration Reason Method of Cause / Corrective Ad6ons F: Forced (Hours) (1) Shutting s: scheduled Down (2) Comments 3 990401 S 165.0 C 4 The UnM remained shutdown for its planned 40 day seventh refueling outage.

4 990407 F 101.0 C 4 Completion of the seventh refueling outage was extended for 101 hours0.00117 days <br />0.0281 hours <br />1.669974e-4 weeks <br />3.84305e-5 months <br /> to repair a stem / plug separation in the 'A' Atmospheric Steam Dump Valve, and to complete startup testing prior to synchronization.

5 990412 S 2.0 8 5 The UnN was removed from service to permit planned turbine overspeed trip testing (the reador remained crMical) 6 990412 F 13.1 A 4 Following the turbine overspeed trip test, the Main ExcNer ground test circuit brush contact failure was repaired, and two cards l

were replaced in the EH Control Cabinet to resolve an inability to raise Turbine speed I

above 1800 rpm for synchronization.

I (1) Reseen (2) Method A Equipment FeBure(Eglein) 1 Manuel l B Maintenance er Test 2- Manuel Trip / Scram i C Rerueling 3- Automenc Trip / serem D - Regulatory ResMcGlon 4- Cordinusuon E - Operator Training / Unense Eneminellen 5 Other(E@)

F - Administreihe G OperebonelEner(Eglein) i H - Other (Eglein)

(Continued next page)

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l UNIT SHUTDOWNS DOCKET NO. 50-412 UNIT NAME 8VPS UnN 82 DATE _ May 4,1999 COMPLETED BY David T. Jones TELEPHONE (412) 393-4962 REPORTING PERIOD: Acril 1999

SUMMARY

The Unit began the report penod shutdown in Mode 5 whde its seventh refuelmg outage continued Following comd: tion of refuelmg outage activities and shutdown surveillance testing, the Unit began to heat-up and entered Mode 4 at 0146 hours0.00169 days <br />0.0406 hours <br />2.414021e-4 weeks <br />5.5553e-5 months <br /> on 04/05/99. The planned 40 day seventh refueleg outage was forced to be extended beginnmg on 04/07/99 at 2159 hours0.025 days <br />0.6 hours <br />0.00357 weeks <br />8.214995e-4 months <br /> due to ongoing repairs of a stem / plug separation which occurred on the 'A' Atmospheric Steam, Dump Valve. Followmg completion of repairs to the 'A' Atmosphenc Steam Dumo Valve, the Unit entered Mode 3 at 0218 hours0.00252 days <br />0.0606 hours <br />3.604497e-4 weeks <br />8.2949e-5 months <br /> on 04/09/99. Following completion of required Mode 3 surveillance testing, Mode 2 was entered at 0142 hours0.00164 days <br />0.0394 hours <br />2.347884e-4 weeks <br />5.4031e-5 months <br />, the reactor was taken entical at 0338 hours0.00391 days <br />0.0939 hours <br />5.588624e-4 weeks <br />1.28609e-4 months <br />, and Mode 1 was entered at 1958 hours0.0227 days <br />0.544 hours <br />0.00324 weeks <br />7.45019e-4 months <br /> on 04/11/99. The Unit was synchroruzad to the electncal grid at 0302 hours0.0035 days <br />0.0839 hours <br />4.993386e-4 weeks <br />1.14911e-4 months <br /> on 04/12/99 officially ending the seventh refueling outage.

The Unit was subsequently removed from service at 1309 hours0.0152 days <br />0.364 hours <br />0.00216 weeks <br />4.980745e-4 months <br /> on 04/12/99 to pomwt planned turbine overspeed trip testing. Followng a successful turbine overspeed trip test, e previous Main Exater ground test orcust brush contact fadure was repaired, and replacement of two cards in the EH Control Cabinet was performed to resolve an inability to raise Turbine speed above 1800 rpm for synchronization. The Unit was then re-synchronized to the electrical grid at 0413 hours0.00478 days <br />0.115 hours <br />6.828704e-4 weeks <br />1.571465e-4 months <br /> on 04/13/99 and output was escalated to approximately 29%. Following completion of a flux map at approximately 29% output, the Unit commenced to increase output to approximately 50% at 2037 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.750785e-4 months <br /> on 04/14/99.

An output of approximately 47% was achieved at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on 04/15/99 to permit required surveillance testing of the Main Steam Safety Valves. Followng satisfactory completion of Main Steam Safety Valve testing, the Unit commenced to increase output to approximately 75% st 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> on 04/15/99. An output of approximately 73% output was achieved at 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> on 04/15/99. Followmg completion of a flux map at approximately 73% output, the Unit commenced to increase output to approximately 90% at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> on 04/17/99. An output of approximately 90%

was achieved at 2140 hours0.0248 days <br />0.594 hours <br />0.00354 weeks <br />8.1427e-4 months <br /> on 04/17/99. Following a heat balance and an adjustment to the nuclear instrumentation, an output of approximately 100% was achieved at 0254 hours0.00294 days <br />0.0706 hours <br />4.199735e-4 weeks <br />9.6647e-5 months <br /> on 04/19/99.

The Unit continued to operate at a nominal value of 100% output until 1313 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />4.995965e-4 months <br /> on 04/23/99 when output was reduced to approximately 99% to support Main Unit Turbine (MUT) Govemor Valve testing. This was required following switching of Govemor Valve No.1 and No. 4 control sequencing to reduce flow induced vibrations on the No.1 and No. 3 MUT Throttle Valves. Following satisfactory MUT Govemor Valve testing, the Unit was retumed to a nominal value of 100% output at 1901 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.233305e-4 months <br /> on 04/23/99.

The Unit continued to operate at a nommal value of 100% outlyut until 1556 hours0.018 days <br />0.432 hours <br />0.00257 weeks <br />5.92058e-4 months <br /> on 04/26/99.

Output was reduced by approximately 2% to gain extra margin as a conservative measure in order to prevent a possible turbine runback during the re-scaling of Loop i Delta-T/Tavg. Following completion of the re-scaling, the Unit was retumed to a nominal value of 100% output at 0540 hours0.00625 days <br />0.15 hours <br />8.928571e-4 weeks <br />2.0547e-4 months <br /> on 04/27/99.

The Unit condnued to operate at a nominal value of 100% output for the remainder of the report period.

OPERATING DATA REPORT DOCKET NO.: 50-412 UNIT NAME: BVPS UNIT 02 REPORT DATE: 05/05/99 COMPLETED BY: DAVID T. JONES TELEPHONE: (412) 393-4962 I

la. REPORTING PERIOD: APRIL 1999 [ Notes

1. DESIGN ELECTRICAL RATING (Not Mwe): 836 [ ,
2. MAX. DEPENDABLE CAPACITY (Net Mwe): 820 ,,,,,,,,,,,,,,,,,,

THIS MONTH YEAR TO DATE CUMULATIVE 3a. HOURS IN REPORTING PERIOD: 719.0 2879.0 100382.0

3. NO. OF HRS. REACTOR MAS CRITICAL: 476.4 1844.2 79440.5 4, SERVICE HOURS GENERATOR ON LINE: 437.9 1803.9 78833.0
5. UNIT RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0
6. NET ELECTRICAL ENERGY GEN. (MWH): 297870.0 1437090.0 60837672.0
7. GROSS ELECT. ENERGY GEN. (MWH): 322990.0 1522192.0 64379144.0
8. GROSS THERMAL ENERGY GEN. (MWH): 392357.0 S88363.C i W 93118.0

'9. UNIT AVAILABILITY FACTOR (%): 67,.9 62.7 78.5

10. UNIT CAPACITY FACTOR (MDC) (%): 50.5 60.9 73.6
11. UNIT FORCED OUTAGE RATE (%): 20.7 5.9 12.2 l

DUQUESNE LIGHT COMPANY Beaver Valley Power Station f

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Nuclear Power Division DISTRIBUTION MONTHLY OPERATING REPORT J. E. Cross (BV-A)

S. C. Jain (BV-A)

K. L. Ostrowski (SOSB-7)

B. T. Tuite (BV-OP)

R. L. Hansen (SOSB-5)

W. R. Kline (SEB-3)

M. S. Ackerman (BV-A)

J. B. Macdonald (SOSB-6)

S. H. Hall (BV-QA)

J. M. Sasala (BV-A)

D. Kern (NRC)(BV-TLD)

A. J. Fenwick (BV-A)

D. E. Donawitz (SEB-2)

A.J.Bevan (BV-ERF)

Electricite' De France P. W. Eselgroth (NRC)

J. A. Hultz (Ohio Edison)

T. A. Flower (Ohio Edison)

INPO Records Center R. C. Maiers (PA Dept. of Environmental Resources)

D. Jacobson (First Energy)  ;

J. Rinckel (First Energy) i R. Prijatel (First Energy) ,

D. Sherman (American Nuclear Insurers)  ;

B. Lewis (McGraw-Hill, Inc.)

S. J. McMutrie (9-408/4117th Avenue)

A. F. Baker (10-470/4117th Avenue)

R. E. Duckworth (SEB-2)

Licensing File (DK Sullivan) (BV-A)

Central File (1)