IR 05000458/1997099

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SALP Rept 50-458/97-99 for 950730-970201
ML20138Q071
Person / Time
Site: River Bend Entergy icon.png
Issue date: 03/03/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20138Q070 List:
References
50-458-97-99, NUDOCS 9703060113
Download: ML20138Q071 (6)


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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE REPORT RIVER BEND STATION 50-458/97-99 BACKGROUND The SALP Board convened on February 5,1997, to assess the nuclear safety performance of the River Bend Station for the period July 30,1995, through February 1,1997. The Board was conducted in accordance with Management Directive 8.6, " Systematic Assessment of Licensee Performance." The Board members included: K. E. Brockman, Acting Director, Division of Reactor Safety (Chairperson); A. T. Howell, Acting Director, Division of Reactor Projects; and W. D. Beckner, Director, Project Directorate IV-1, Office of Nuclear Reactor Regulation. This assessment was reviewed and approved by the Acting Regional Administrato Functional Areas and Ratinas

Current Previous Operatior. s 2 2 ,

Maintenance 2 2 l Engineering 2 2 Plant Support 2 1 1 OPERATIONS Safety performance in this functional area continued to be good, with the licensee improving both equipment operating performance and plant procedures. Operators responded well to non-routine plant challenges and events. Despite generally strong performance in this area, there were numerous operator errors that were particularly evident in the area of configuration control. While the operator training programs continued to be effective, operator performance in the simulator was not as good as it was in the control room. Self-assessment and corrective action activities were effective in i improving performance in the areas of hardware, programs, and procedure Throughout the assessment period, operations management emphasized the elimination of material condition deficiencies which had previously challenged the plant operators. The number of operator workarounds, which included items such as inoperable automatic functions, was significantly reduced and maintained at a manageable level. As a result of ;

the procedure upgrade program, there were few problems involving procedural weaknesse Operators responded conservatively to equipment problems, as demonstrated during the plant shutdown in response to electrical noise spikes on the intermediate range monitors not being completely understood. However, while there were no operator errors which resulted in plant scrams or transients, licensee actions to correct numerous operator errors 9703060113 970303 PDR ADOCK 05000458 0 PDR

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-2-caused by inattention to detail, a problem area discussed in the last SALP report, were not fully effective. Examples of these errors which occurred during bo"h routine power and refueling operations, included an emergency chiller which was not properly aligned for standby operation and a mispositioned fuel assembl Overall training effectiveness was considered to be good. Appropriate and offective performance by licensed operator candidates and the operating crews was noted during the examinations and requalification inspection conducted early in the assessment perio However, a number of individual and crew performance problems, specifically in the areas of command and control and the use of emergency operating procedures, were identified in the simulator during subsequent requalification training and the biennial emergency response exercise. These problems reflected individual operator performance weaknesses which, in the past, may have been masked by overall crew performance. Notwithstanding these problems, the licensee was effective in identifying and initiating corrective actions to address these weaknesse By emphasizing safety, problem identification improved. Through the implementation of the corrective action program, the implementation of improvement initiative action plans, and the utilization of special teams to review significant events, the licensee corrected or significantly improved a number of problem areas involving plant hardware, processes, and procedures. However, the corrective actions to reduce the number of operator errors have not yet been fully effectiv The performance rating in the Plant Operations functional area was determined to be Category Ill. MAINTENANCE Performance in this functional area was catermined to be good. Improvements were noted in plant material condition and several maintenance programs. While the skill and expertise of the craft personrM ontinued to be an overall strength, individual performanco shortcomings were isntified in the conduct of surveillance and inservice testing. There were also occasions where both maintenance and surveillance procedures did not provide an adequate level of detail. The planning and scheduling of maintenance activities was determined to be effective; however, tnere were instances where the integration of risk considerations into emergent work was lacking. Corrective actions developed in response to maintenance-related events and self-assessments were of mixed qualit : The licensee continued to improve overall maintenance effectiveness, and the excellent material condition of the plant was evidence of these efforts. Emphasis was placed on clearly communicating performance expectations and establishing personal accountability for the material condition of the plant. The skill of the individual craft personnel remained a program strength; however, there were instances where inattention to detail, lack of detail in work procedures, and procedural non-complance resulted in losses of configuration control and the improper conduct of work.

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l Two exceptions were identified to, what were otherwise, quality naaintenance programs --

surveillance and inservice testing. Surveillance testing repeatedly cha!!enged the licensee; and, while improvements were noted in the quality of the individual surveillance procedures, the conduct of surveillance activities did not meet management expectations or, in severalinstances, regulatory requirements. This was due, in part, to the difficulties associated with the implementation of the improved standard technical specifications. One forced shutdown was attributed to a missed battery surveillance during the assessment period. Significant performance concerns were also identified in the conduct of the inservice testing program, resulting in numerous technical specification required tests not being conducte The planning and scheduling of maintenance activities improved from the previous assessment period, and effectively integrated risk assessment into the work package '

development process. However, there were instances where the planning and scheduling of emergent work activities did not receive proper risk consideration. Examples include the plant being shutdown with multiple trains of the residual heat removal system being inoperable, and the high and low pressure core spray systems being concurrently inoperabl The programs for self-assessment and corrective actions provided mixed results. The quality assurance organization conducted intrusive and, generally, effective audits of specific work activities, and programmatic self-assessments were used to address the major performance issues. External subject matter experts were often used to help provide broader and more objective reviews. However, there were several examples, such as the failure to ensure that pressure transmitters were environmentally qualified, where the

corrective actions for identified performance problems did not preclude their recurrence.

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The performance rating in the Maintenance functional area was determined to be *

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j IV. ENGINEERING

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l Performance in this functional area continued to improve during the assessment period and i

was determined to be good. Management expectations were clearly communicated to the

engineering staff. Engineering workloads were effectively controlled and maintained at i manageable levels. Communications between departments and control of work efforts j were very good. Difficulties encountered early in the assessment period with the corrective action program were corrected. Engineering training was good and system
engineers were required to be certified on systems prior to assignment.

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, The quality of design engineering was considered to be good. Effective practices concerning permanent and temporary plant modifications, engineering calculations, and integrating probabilistic risk analysis insights into planned plant activities were c,bserve There were also examples of design control problems and instances where changes to the I ('

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f acility were not properly translated into procedures and calculations. As an example, the licensee had classified the spent fuel pool gates as safety related, but had failed to j establish measures to ensure that they would be maintained as safety related. The licensee's efforts to reduce the number of temporary modifications in the plant was considered a strength.

i Engineering programs and procedures were good, with notable exceptions in the i engineering support provided to the inservice and surveillance testing programs. The

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weaknesses in the inservice testing program had been identified previously as part of the Long-Term Performance improvement Plan, but were not effectively corrected. Support for the surveillance testing program was lacking in the areas of procedural detail, test data review, and assurance of adequate program implementation. A proposed request for

enforcernent discretion relative to a missed station battery surveillance did not provide the

necessary technical justification, and an otherwise strong motor-operated valve program

}' missed opportunities to identify and correct design deficiencies previously identified and resolved at other Entergy site The system engineering function was determined to be a strength. System engineers were highly qualified, knowledgeable of their systems, and communicated well with other plant i

disciplines, instances of good ettention to detail and a questioning attitude were noted,

indicating that the engineering staff was, overall, providing consistent and effective support for plant operations. However, there were isolated instances of poor plant engineering support for operability evaluations and inadequate corrective actions. One

, example included an operability evaluation of the fuel building filtration charcoal following exposure to volatile organic compounds which reached a non-conservative determinatio Effective follow-up to industry events and operating experience was observed. Self-assessments were effective in identifying weaknesses and, in most cases, resulted in effective corrective action The performance rating in the Engineering functional area was determined to be Category PLANT SUPPORT Performance in this functional area declined over the assessment period, but remained good overall. Strong performance in the areas of radioactive waste effluent management, environmental monitoring, solid radioactive waste management and transportation, and security were overshadowed by radiological protection implementation weaknesses, particularly during the refueling outage, and poor performance during the biennial emergency response exercise. Corrective actions were implemented by the licensee in rcsponse to these problems, but have not yet been verified for their overall effectivenes Plant housekeeping continued to be excellent and the fire protection program was effective.

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5-General!y, performance in the radiological controls area was good but declined from the previous assessment period. The decline was attributed to the personnel performance problems identified with the implementation of the radiological protection program. These problems included instances of trained workers entering the radiologically controlled area without wearing proper dosimetry, and radiation protection personnel failing to properly post radiation, high radiation, and airborne activity areas. In addition, there were numerous personnel contamination events that occurred during the refueling outage. The licensee !

has initiated corrective actions for these problems. In addition, the licensee's effective ;

implementation of the as-low-as reasonably-achievable (ALARA) program included a 1 number of technicalinitiatives to reduce worker exposur The licensee effectively implemented the liquid and gaseous radioactive waste effluent program, and the initiation of a waste volume reduction program resulted in a significant reduction of liquid radioactive waste. The reduction of solid radioactive waste resulted, in part, from excellent housekeeping practices. Implementation of the radiological environmental monitoring program was also at a high leve Performance in the emergency preparedness area declined during the assessment perio i During the annual program evaluation, performance problems with event classification, !

notifications, and dose assessment were identified. During the biennial exercise, additional !

performance problems were noted in the control room simulator and, especially, in the l emergency operations f acility. In response, the licensee developed a comprehensive short- l term action plan and long-term program enhancements. Performance improved during a l licensee-initiated redemonstration exercise, particularly in the emergency operations i facility. Emergency response facilities were maintained in a state of operational readiness; however, the licensee had not fully considered the implications associated with their plans to relocate emergency response personnel to the control room in the event that the operational and technical support centers became uninhabitabl The implementation of the security program continued to be strong. The installed vehicle barrier system conformed to NRC requirements and was capable of protecting vital plant equipment. The licensee properly tested and maintained security equipment. Repairs were conducted in a timely manner. The licensee submitted security plan changes in accordance with NRC requirements, and security procedures conformed to the security plan. The security organization effectively implemented compensatory measures when require Isolated instances involving security officer inattentiveness and improper logging of security events were identifie Plant housekeeping continued to be strong during the assessment period. Because of excellent housekeeping practices during the refueling outage, the post-outage recovery of plant cleanliness was particularly effective. The fire protection program was implemented in an effective manne '

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-6-Quality assurance audits in the radiological protection and security areas were performance based and thorough. In contrast, self-assessment activities in the emergency preparedness area were not effective in identifying significant performance problems before and during the biennial exercis The performance rating in the Plant Support functional ares was determined to be Category !

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