IR 05000416/2012008

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IR 05000416-12-008; 06/25/2012 - 09/10/2012; Grand Gulf Nuclear Generating Station; Baseline Inspection, NRC Inspection Procedure 71111.21, Component Design Basis Inspection.
ML12283A353
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 10/09/2012
From: Thomas Farnholtz
Region 4 Engineering Branch 1
To: Mike Perito
Entergy Operations
References
IR-12-008
Download: ML12283A353 (56)


Text

UNITE D S TATE S NUC LEAR RE GULATOR Y C OMMI S SI ON ber 9, 2012

SUBJECT:

GRAND GULF NUCLEAR GENERATING STATION - NRC COMPONENT DESIGN BASIS INSPECTION REPORT 05000416/2012008

Dear Mr. Perito:

On September 10, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Grand Gulf Nuclear Station. The enclosed inspection report documents the inspection results which were discussed on September 10, 2012, with J. Browning, General Manager Plant Operations, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission=s rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Six NRC identified findings were identified during this inspection. All six of the findings were determined to have very low safety significance (Green). One of the findings was determined to be a Severity Level IV violation. All of the findings were determined to involve violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Grand Gulf Nuclear Station. The information you provide will be considered in accordance with Inspection Manual Chapter 0305. In addition, if you disagree with the characterization of the crosscutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at Grand Gulf Nuclear Station. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Thomas R. Farnholtz, Branch Chief Engineering Branch One Division of Reactor Safety Dockets No: 50-416 License No: NPF-29 Enclosure: Inspection Report 05000416/2012008 w/ Attachment: Supplemental Information cc w/ encl:

Electronic Distribution for Grand Gulf Nuclear Generating Station

SUMMARY OF FINDINGS

IR 05000416/2012008; 06/25/2012 - 09/10/2012; Grand Gulf Nuclear Generating Station; baseline inspection, NRC Inspection Procedure 71111.21, Component Design Basis Inspection.

The report covers an announced inspection by a team of five regional inspectors and two contractors. Six findings were identified. Five of the findings were of very low safety significance (Green) and one finding was assigned a Severity Level IV. The final significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified Findings

Cornerstone: Mitigating Systems

Green.

The team identified a Green non-cited violation of 10 CFR 50, Appendix B,

Criterion XI, Test Control, which states, in part, A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Specifically, prior to July 27, 2012, the licensees preventive maintenance Procedures 07-S-12-41, 07-S-12-42, and 07-S-12-61 failed to assure that the 4160 Vac circuit breakers would perform satisfactorily in service when the licensee performed maintenance prior to completing as-found tests to verify past operability of the circuit breakers. This finding has been entered into licensees corrective action program as Condition Reports CR-GGN- 2012-09035 and CR- GGN-2012-9103.

The team determined that failure to establish a test program which ensures that test and maintenance procedures associated with safety-related 4160 Vac circuit breakers would perform satisfactorily in service was a performance deficiency. This finding was more than minor because, if left uncorrected, it would lead to a more significant safety concern. Specifically, the failure to perform as-found tests prior to performing maintenance in preventive maintenance procedures was a significant programmatic deficiency which could cause unacceptable conditions to go undetected. Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of safety function. This finding had a crosscutting aspect in the area of human performance, resources component, because the licensee failed to ensure that test and maintenance procedures were complete, accurate, and up-to-date to assure nuclear safety. H.2(c) (1R21.2.1)

Green.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B,

Criterion XI, "Test Control," which states, in part, A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Specifically, prior to July 27, 2012, the licensee failed to establish a test program for 125 Vdc safety-related molded case circuit breakers incorporating the requirements of IEEE 308, to ensure the breakers would not degrade and would perform satisfactorily in service. The finding was entered into the licensees corrective action program as Condition Reports CR-GGN-2012-09030 and CR-GGN-2012-09175.

The team determined that the failure to establish a testing program incorporating the requirements of IEEE 308 was a performance deficiency. The finding was more than minor, because if left uncorrected, it would lead to a more significant safety concern.

Specifically, the failure to establish a testing program was a significant programmatic deficiency that would lead to missed opportunities to detect potential common cause failures from degradation of performance in more than one redundant safety division.

Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of safety function. This finding had a crosscutting aspect in the area of problem identification and resolution, corrective action program component; because the licensee failed to thoroughly evaluate problems such that resolutions address cause and extent of condition. Specifically, the licensee failed to thoroughly evaluate the extent of condition associated with previously identified NRC violation involving the failure to test 480 Vac molded case circuit breakers identified during the 2009 component design basis inspection. P.1(c) (1R21.2.2)

  • Severity Level IV. The team identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes, Tests and Experiments which states, in part, that a licensee shall obtain a license amendment pursuant to Section 50.90 prior to implementing a proposed change, test, or experiment if this activity would; result in more than a minimal increase in the likelihood of occurrence of a malfunction of a structure, system, or component important to safety previously evaluated in the final safety analysis report (as updated). Specifically, on August 18, 1987, the licensee implemented a change to the updated safety analysis report which limited credible passive failures in the standby service water system to pump and valve seal leakage without obtaining a license amendment. This finding was entered into the licensees corrective action program as Condition Report CR-GGN-2012-09267.

The team determined that the licensees failure to receive prior NRC approval for changes in licensed activities regarding single passive failure criteria for the standby service water system was a performance deficiency. The performance deficiency was evaluated using traditional enforcement because the finding had the ability to impact the regulatory process. The performance deficiency was more than minor because there was a reasonable likelihood that the change would require NRC review and approval prior to implementation. In accordance with the NRC Enforcement Manual, risk insights from the Inspection Manual Chapter 0609, Significance Determination Process, are used in determining the significance of 10 CFR 50.59 violations. Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the team determined that the finding represented a loss of system safety function in that the standby service water system could not meet its 30-day mission time to provide decay heat removal. Therefore, a Detailed Risk Evaluation was necessary. In accordance with Manual Chapter 0609, Appendix A, Section 6, Detailed Risk Evaluation, the senior reactor analyst evaluated the risk of the degraded condition that resulted from the finding. According to the Risk Assessment of Operational Events Handbook, Volume 1 - Internal Events, Section 4.1, Mission Time Modeling, in most events, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> is sufficient time to bring numerous resources to bear on core cooling.

In some events, the choice is conservative and the analysis results are overestimates.

Additionally, the analyst determined that Section 4.2 on increasing mission time was not applicable to the subject finding because the decrease in standby service water system water inventory would be obvious and there would be days to respond with makeup sources. Therefore, the analyst determined that the finding was of very low safety significance (Green) because, although the standby service water system could not provide 30 days of decay heat removal without operator action to provide makeup water to the system, it would have been able to complete its 24-hour risk significant mission time. Since the finding had very low safety significance, the finding was determined to be Severity Level IV, in accordance with the NRC Enforcement Policy. The finding does not have a crosscutting aspect because the most significant contributor to the finding does not reflect current licensee performance. (1R21.2.3)

Green.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, which states, in part, that Measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformance are promptly identified and corrected. Specifically, on July 12, 2012, the NRC informed the licensee of a violation of 10 CFR 50.59 requirements, but the licensee failed to promptly identify this as an adverse condition and enter this condition into their corrective action program until July 19, 2012. The finding was entered into the licensees corrective action program as CR-GGN-2012-10075.

The team determined that the licensees failure to promptly enter the NRC violation as condition adverse to quality into the corrective action program was a performance deficiency. This finding was more than minor because it adversely affected the design control attribute of the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee failed to promptly document a violation of 10 CFR 50.59, which delayed an operability evaluation that ultimately determined that compensatory measures were required to ensure that the standby service water system could perform its specified safety function for its entire mission time. Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the team determined that the finding represented a loss of system safety function in that the standby service water system could not meet its 30-day mission time to provide decay heat removal.

Therefore, a Detailed Risk Evaluation was necessary. In accordance with Manual

Chapter 0609, Appendix A, Section 6, Detailed Risk Evaluation, the senior reactor analyst evaluated the risk of the degraded condition that resulted from the finding.

According to the Risk Assessment of Operational Events Handbook, Volume 1 - Internal Events, Section 4.1, Mission Time Modeling, in most events, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> is sufficient time to bring numerous resources to bear on core cooling. In some events, the choice is conservative and the analysis results are overestimates. Additionally, the analyst determined that Section 4.2 on increasing mission time was not applicable to the subject finding because the decrease in standby service water system water inventory would be obvious and there would be days to respond with makeup sources. Therefore, the analyst determined that the finding was of very low safety significance (Green) because, although the standby service water system could not provide 30 days of decay heat removal without operator action to provide makeup water to the system, it would have been able to complete its 24-hour risk significant mission time. This finding had a crosscutting aspect in the area of problem identification and resolution, corrective action program component, because the licensee failed to ensure that issues potentially impacting nuclear safety are promptly identified, fully evaluated, and that actions are taken to address safety issues, in a timely manner, commensurate with their safety significance. Specifically, the licensee did not implement a corrective action program with a low threshold for identifying issues completely, accurately, and in a timely manner commensurate with their safety significance. P.1(a) (1R21.2.3)

Green.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings which states, in part, that Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Specifically, from July 19, 2012, to July 29, 2012, the licensee failed correctly evaluate the operability of the standby service water system with a degraded or nonconforming condition and failed to document a sound basis for a reasonable expectation of operability of the standby service water system as required by Procedure EN-OP-104, Operability Determination Process. The finding was entered into the licensees corrective action program as Condition Report CR-GGN-2012-09356.

The team determined that the failure to implement the requirements of the operability determination process procedure was a performance deficiency. The finding was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems Cornerstone to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, the standby service water system was incapable of performing its specified safety function for the entire 30-day mission time without compensatory measures.

Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the team determined that the finding represented a loss of system safety function in that the standby service water system could not meet its 30-day mission time to provide decay heat removal. Therefore, a Detailed Risk Evaluation was necessary. In accordance with Manual Chapter 0609,

Appendix A, Section 6, Detailed Risk Evaluation, the senior reactor analyst evaluated the risk of the degraded condition that resulted from the finding. According to the Risk Assessment of Operational Events Handbook, Volume 1 - Internal Events, Section 4.1,

Mission Time Modeling, in most events, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> is sufficient time to bring numerous resources to bear on core cooling. In some events, the choice is conservative and the analysis results are overestimates. Additionally, the analyst determined that Section 4.2 on increasing mission time was not applicable to the subject finding because the decrease in standby service water system water inventory would be obvious and there would be days to respond with makeup sources. Therefore, the analyst determined that the finding was of very low safety significance (Green) because the standby service water system could would have been able to complete its 24-hour risk significant mission time although it could not provide 30 days of decay heat removal without operator action to provide makeup water to the system. This finding had a crosscutting aspect in the area of human performance, decision making component, because the licensee did not make decisions that demonstrated that nuclear safety was an overriding priority.

Specifically, the licensee did not make safety significant decisions using a systematic process to ensure safety is maintained. H.1(a) (1R21.2.3)

Green.

The team identified a Green non-cited violation of 10 CFR 50, Appendix B,

Criterion XI, Test Control, which states, in part, A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design document. Specifically, prior to July 27, 2012, the licensees safety-related 4160 Vac circuit breaker preventive maintenance Procedures 07-S-12-41, 07-S-12-42, and 07-S-12-61 failed to incorporate inspection and test requirements for minimum voltage tests, reduced voltage tests, and inspection of auxiliary switch relay contacts as established in the licensees circuit breaker maintenance program. This condition was entered into the licensees corrective action program as Condition Reports CR-GGN 2012-08885 and CR-GGN-2012-09111.

The team determined that the failure to incorporate required tests and inspections into preventive maintenance procedures for safety-related 4160 Vac circuit breakers was a performance deficiency. This finding was more than minor because, if left uncorrected, it would lead to a more significant safety concern. Specifically, the failure to incorporate the testing, cleaning, and inspection requirements into preventive maintenance procedures were a significant programmatic deficiency which could cause unacceptable conditions to go undetected. Using the Inspection Manual Chapter 0609, Appendix A,

The Significance Determination Process for Findings At-Power, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of safety function. This finding had a crosscutting aspect in the area of problem identification and resolution, operating experience component, because the licensee failed to use operating experience information, including vendor recommendations and internally generated lessons learned, to support plant safety. Specifically, the licensee did not implement and institutionalize operating experience through changes to processes, procedures, equipment, and training programs. P.2(b) (1R21.2.4)

REPORT DETAILS

REACTOR SAFETY

Inspection of component design basis verifies the initial design and subsequent modifications and provides monitoring of the capability of the selected components and operator actions to perform their design basis functions. As plants age, their design basis may be difficult to determine and important design features may be altered or disabled during modifications. The plant risk assessment model assumes the capability of safety systems and components to perform their intended safety function successfully.

This inspectable area verifies aspects of the Initiating Events, Mitigating Systems and Barrier Integrity cornerstones for which there are no indicators to measure performance.

1R21 Component Design Basis Inspection

To assess the ability of the Grand Gulf Nuclear Station equipment and operators to perform their required safety functions, the team inspected risk significant components and the licensees responses to industry operating experience. The team selected risk significant components for review using information contained in the Grand Gulf Nuclear Station probabilistic risk assessments and the U. S. Nuclear Regulatory Commissions (NRC) standardized plant analysis risk model. In general, the selection process focused on components that had a risk achievement worth factor greater than 1.3 or a risk reduction worth factor greater than 1.005. The items selected included components in both safety-related and nonsafety-related systems including pumps, circuit breakers, heat exchangers, transformers, and valves. The team selected the risk significant operating experience to be inspected based on its collective past experience.

.1 Inspection Scope

To verify that the selected components would function as required, the team reviewed design basis assumptions, calculations, and procedures. In some instances, the team performed calculations to independently verify the licensee's conclusions. The team also verified that the condition of the components was consistent with the design basis and that the tested capabilities met the required criteria.

The team reviewed maintenance work records, corrective action documents, and industry operating experience records to verify that licensee personnel considered degraded conditions and their impact on the components. For the review of operator actions, the team observed operators during simulator scenarios, as well as during simulated actions in the plant.

The team performed a margin assessment and detailed review of the selected risk-significant components to verify that the design basis have been correctly implemented and maintained. This design margin assessment considered original design issues, margin reductions because of modifications, and margin reductions identified as a result of material condition issues. Equipment reliability issues were also considered in the selection of components for detailed review. These included items such as failed performance test results; significant corrective actions; repeated

maintenance; 10 CFR 50.65(a)1 status; operable, but degraded, conditions; NRC resident inspector input of problem equipment; system health reports; industry operating experience; and licensee problem equipment lists. Consideration was also given to the uniqueness and complexity of the design, operating experience, and the available defense in-depth margins.

The inspection procedure requires a review of 15 to 25 total samples that include risk-significant and low design margin components, containment related components, and operating experience issues. The sample selection for this inspection was 16 components, 5 operating experience items, and 4 event based activities associated with the components. The selected inspection and associated operating experience items supported risk significant functions including the following:

a. Electrical power to mitigation systems: The team selected several components in the electrical power distribution systems to verify operability to supply alternating current (ac)and direct current

(dc) power to risk significant and safety-related loads in support of safety system operation in response to initiating events such as loss of offsite power, station blackout, and a loss-of-coolant accident with offsite power available. As such the team selected:
  • Division III 125 Vdc Battery and Safety Bus
  • Division III 4160 Vac Engineered Safety Feature Switchgear Bus 17 AC
  • Division III 480 Vac Load Center 17B01
  • Engineered Safety Feature Transformer 11
  • Power Range Neutron Monitoring System b. Mitigating systems needed to attain safe shutdown: The team reviewed components and supporting equipment required to perform the safe shutdown of the plant. As such the team selected:
  • Emergency Pump Room Fan Cooler T51-B001-C

.2 Results of Detailed Reviews for Components

.2.1 Division III Emergency Diesel Generator Output Circuit Breaker 152-1701

a. Inspection Scope

The team reviewed the updated safety analysis report, system description, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the division III 4160 Vac emergency diesel generator output breaker 152-1701. The team also performed walkdowns and conducted interviews with system engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Schematics and control wiring diagrams of record for the breaker.
  • Preventive maintenance procedures for the breaker.
  • Vendor manual and specifications for the breaker.
  • Load calculations of record and supporting documentation.
  • Calculations of record for protection settings and alarms.
  • Completion of last preventive maintenance work orders.
  • Breaker control power circuit and ancillary supporting component and equipment.

During the inspection, the licensee was conducting an apparent cause evaluation on the recent failure of circuit breaker 152-1701 documented under Condition Reports CR-GGN-2012-07922 and CR-GGN-2012-07935. Upon completion of the apparent cause evaluation, the NRC will review this failure and document the review in NRC Inspection Report 05000416/2012005.

b. Findings

1. Preconditioning of 4160 Vac Circuit Breaker for As-Found Tests

Introduction.

The team identified a Green non-cited violation of 10 CFR 50, Appendix B, Criterion XI, Test Control, involving the licensees failure to establish a test program which demonstrates that components will perform satisfactorily in service. Specifically, the licensee failed to record as-found test values prior to performing maintenance for 4160 Vac circuit breakers.

Description.

The team reviewed six-year preventive maintenance procedures for 4160 Vac circuit breakers. During the review, the team identified that Procedure 07-S-12-41,Inspection and Testing of ITE 5 KV Circuit Breakers, Procedure 07-S-12-42, Inspection and Testing of Westinghouse DHP 4.16KV Circuit Breakers, and Procedure 07-S-12-61, Inspection of GE Magna Blast Circuit Breakers, directed maintenance personnel to clean, adjust, and manipulate the physical condition of 4160 Vac circuit breaker contacts, insulators, and other critical circuit breaker components before performing an as-found test to determine if the circuit breakers would have performed their intended design function.

For example, Procedure 07-S-12-61, Inspection of GE Magna Blast Circuit Breakers, Section 7.1, Breaker Cleaning and Inspection, directs maintenance personnel to clean and inspect the circuit breaker. In particular, Step 7.1.8, states, Remove the interrupter and box barriers. Inspect the movable arcing contacts, stationary arcing contacts, movable primary contacts, and stationary primary contacts. If contacts are burned and pitted, file smooth with a contact file. Step 7.1.8 is completed before any as-found tests are performed to verify the operability of the critical components of the circuit breaker, such as main contact resistance, main contact gap, and insulation resistance.

The team reviewed the data sheet resulting from the December 16, 2011, tests and preventative maintenance performed on 4160 Vac circuit breaker 152-1701 using Procedure 07-S-12-61. Those results show that maintenance personnel documented the same results for as-found and as-left for multiple tested parameters; therefore, the team determined that the procedure could mask existing conditions such as unacceptable contact resistance, setpoint drift, and mechanical binding. Additionally, the procedure resulted in the inability to verify past operability of circuit breaker 152-1701.

Analysis.

The team determined that failure to establish a test program which ensures that test and maintenance procedures associated with safety-related 4160 Vac circuit breakers would perform satisfactorily in service was a performance deficiency. This finding was more than minor because, if left uncorrected, it would lead to a more significant safety concern. Specifically, the failure to perform as-found tests prior to performing maintenance in preventive maintenance procedures was a significant programmatic deficiency which could cause unacceptable conditions to go undetected.

Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of safety function. This finding had a crosscutting aspect in the area of human performance, resources component, because the licensee failed to ensure that test and maintenance procedures were complete, accurate, and up-to-date to assure nuclear safety. H.2(c)

Enforcement.

The team identified a Green non-cited violation of 10 CFR 50, Appendix B, Criterion XI, Test Control, which states, in part, A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Contrary to the above, the licensee failed to establish a test program that assured that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service was identified and performed in accordance with written test procedures which incorporated the requirements and acceptance limits contained in applicable design documents. Specifically, prior to July 27, 2012, the licensees preventive maintenance Procedures 07-S-12-41, 07-S-12-42, and 07-S-12-61 failed to assure that the 4160 Vac circuit breakers would perform satisfactorily in service when the licensee performed maintenance prior to completing as-found tests to verify past operability of the circuit breakers. This finding was entered into the licensees corrective action program as Condition Reports CR-GGN- 2012-09035 and CR- GGN-2012-9103. Because this

finding is of very low safety significance and has been entered into the licensees corrective action program, this violation is being treated as a non-cited violation consistent with the NRC Enforcement Policy: NCV 05000416/2012008-01, Preconditioning of 4160 Vac Circuit Breakers for As-Found Tests.

.2.2 Division III 125 Vdc Battery and Safety Bus 11DC

a. Inspection Scope

The team reviewed the updated safety analysis report, system description; the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the division III 125 Vdc battery and associated safety bus. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Calculations that established the basis for battery loading and sizing.
  • Voltage drop calculations, short circuit calculations, and coordination studies.
  • Results of the recent surveillance tests and maintenance activities to determine inclusion of vendor recommendations and industry standards.
  • Separation criteria, configuration, and installation to confirm separation of safety-related and nonsafety-related loads.
  • Visible material condition and configuration of the components.
  • Calculations and vendor documents addressing required heat removal performance requirements during design and maximum ambient temperature conditions.
  • Recent temperature data recorded in the division III switchgear and battery rooms.
  • Evaluation of the potential impact of elevated temperatures on safety-related equipment located within the division III switchgear and battery rooms under accident conditions.

b. Findings

1. Failure to Establish a Testing Program for Safety-Related 125 Vdc Circuit Breakers

Introduction.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, involving the licensees failure to establish a test program which incorporates test requirements and acceptance limits contained in applicable design documents. Specifically, the licensee failed to establish a periodic test program for safety-related 125 Vdc molded case circuit breakers which incorporated the requirements of IEEE Standard 308, Standard Criteria for Class 1E Power Systems for Nuclear Power Generating Stations.

Description.

Grand Gulf Nuclear Station Updated Safety Analysis Report, Section 8.3, Onsite Power Systems, states, in part, that all Class 1E power systems conform to IEEE Standard 308. IEEE Standard 308 requires, in part, that testing shall be performed at scheduled intervals to: 1) Detect within practical limits the deterioration of the

equipment toward an unacceptable condition, and 2) Demonstrate that standby equipment and other components that are not exercised during normal operation of the station are operable.

For a sample of division III 125 Vdc molded case circuit breakers associated with 125 Vdc distribution center 11DC, the team requested the preventive maintenance procedures for maintaining and periodically testing the circuit breakers. Additionally, the team requested the associated records from the last maintenance and testing performed for these breakers.

The sample selected by the team included the following division III breakers:

  • 72-11C01 (bus supply breaker from battery - GE Type TFK)
  • 72-11C03 (bus supply breaker from charger 1C3 - GE Type TFK)
  • 72-11C11 (DG 13 field flash - GE Type TEB)
  • 72-11C12 (4160 V switchgear bus 17AC control power - GE Type TEB)
  • 72-11C13 (DG 13 engine control power - GE Type TEB)
  • 72-11C14 (DG 13 protective relaying - GE Type TEB)

In response to the teams request, the licensee stated that testing of 125 Vdc molded case circuit breakers was not included in their preventive maintenance program. To address the teams concern, the licensee initiated CR-GGN-2012-09030 for the division III 125 Vdc molded case circuit breakers. The licensee subsequently initiated CR-GGN-2012-09175 to extend their evaluation to division I and II 125 Vdc molded case circuit breakers that support the division I and II engineered safety features and safe shutdown functions.

Analysis.

The team determined that the failure to establish a testing program incorporating the requirements of IEEE 308 was a performance deficiency. The finding was more than minor, because if left uncorrected, it would lead to a more significant safety concern. Specifically, the failure to establish a testing program was a significant programmatic deficiency that would lead to missed opportunities to detect potential common cause failures from degradation of performance in more than one redundant safety division. Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of safety function. This finding had a crosscutting aspect in the area of problem identification and resolution, corrective action program component; because the licensee failed to thoroughly evaluate problems such that resolutions address cause and extent of condition. Specifically, the licensee failed to thoroughly evaluate the extent of condition associated with a previously identified NRC violation involving the failure to test 480 Vac molded case circuit breakers identified during the 2009 component design basis inspection. P.1(c)

Enforcement.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion XI, "Test Control," which states, in part, A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in

accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Contrary to the above, the licensee failed to establish a test program that assured that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service was identified and performed in accordance with written test procedures which incorporated the requirements and acceptance limits contained in applicable design documents. Specifically, prior to July 27, 2012, the licensee failed to establish a test program for 125 Vdc safety-related molded case circuit breakers incorporating the requirements of IEEE 308, to ensure the breakers would not degrade and would perform satisfactorily in service. The finding was entered into the licensees corrective action program as Condition Reports CR-GGN-2012-09030 and CR-GGN-2012-09175.

Because this finding is of very low safety significance and has been entered into the licensees corrective action program, this violation is being treated as a non-cited violation consistent with the NRC Enforcement Policy: NCV 05000416/2012008-02, Failure to Establish a Testing Program for Safety-Related 125 Vdc Circuit Breakers.

.2.3 Division I Standby Service Water System Pump

a. Inspection Scope

The team reviewed the updated safety analysis report, design basis documents, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the division I standby service water pump. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component to perform its desired design basis function.

Specifically, the team reviewed:

  • Work orders and corrective action program documents.
  • System design criteria.
  • Piping and instrumentation diagrams and structural drawings.
  • Technical specifications.
  • Standby service water system operating and alarm response instructions.
  • Plant operations manual for chemical additions to plant systems.

b. Findings

1. Failure to Obtain NRC Approval for a Change to Credible Passive Failures in the

Standby Service Water System

Introduction.

The team identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes, Tests, and Experiments, involving the licensees failure to obtain a license amendment, pursuant to 10 CFR 50.90, prior to implementing a change to the standby service water system passive failure analysis. Specifically, the licensee changed the final safety analysis report (as updated) to limit credible post-accident, non-

electrical passive failures in the standby service water system to pump or valve seal leakage without submitting or obtaining a license amendment.

Description.

On July 12, 2012, while reviewing the Grand Gulf Nuclear Station Updated Final Safety Analysis Report, Chapter 9.2, Water Systems, the team identified a footnote that states: Credible non-electrical passive failures post-accident are limited to pump or valve seal leakage. A piping failure concurrent with the accident is not considered credible as noted in subsection 9.2.1.6, References 2 and 3. The team requested the document that approved this change. The licensee produced Change Notice 3758.

In Change Notice 3758, the licensee performed a 10 CFR 50.59 safety evaluation. In this evaluation, the licensee answered that there were no unreviewed safety questions; therefore, the licensee was not required to submit the change to the NRC for approval, and subsequently, the licensee implemented the change. This change modified the original final safety analysis report to include the footnote referenced above in addition to several mark-ups in Table 9.2-1, Standby Service Water System Passive Failure Analysis, which removed pipe ruptures, heat exchanger tube ruptures, or pipe fitting ruptures as credible passive failures.

Title 10 CFR 50.59, Changes, Tests, and Experiments, was revised and became effective on March 13, 2001. The NRC issued a Regulatory Issue Summary 2001-03, dated January 23, 2001, that stated, in part, that licensees may implement the revised rule at a time later than March 13, 2001. In a letter dated March 5, 2001, Entergy Operations, Inc. informed the NRC that Grand Gulf Nuclear Station would implement the revised rule on July 2, 2001, and those evaluations begun before July 2, 2001 would be processed and completed in accordance with the old rule. Since the licensee approved the 10 CFR 50.59 safety evaluation on August 18, 1987, the evaluation was performed under the requirements of the old rule.

However, the team determined that the licensee answered one of the questions in the safety evaluation incorrectly. Specifically, in Part III - Unreviewed Safety Question of the safety evaluation, the licensee responded No to Question 3, which states, Increase the probability of a malfunction of equipment important to safety previously evaluated in the FSAR. The team determined that the answer to the question was Yes because the change significantly relaxed the licensees licensing basis for credible passive failures in the accident analysis.

Because the licensee performed the safety evaluation under the old 10 CFR 50.59 regulations, the team also reviewed the change as it applies to the revised regulations.

The team determined that the change resulted in more than a minimal increase in the likelihood of occurrence of a malfunction of a structure, system, or component important to safety. According to NEI 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, departures from the design, fabrication, construction, testing and performance standards as outlined in the General Design Criteria are not compatible with a "no more than minimal increase" standard. Specifically, the change was a departure from 10 CFR Part 50, Appendix A, Criterion 44, Cooling Water, which requires that the safety function of the standby service water system can be

accomplished, assuming a single failure. Therefore, the team determined that prior NRC review and approval was required under the old and revised rule.

On July 19, 2012, the licensee entered this concern into their corrective action program as Condition Report CR-GGN-2012-09267.

Analysis.

The team determined that the licensees failure to receive prior NRC approval for changes in licensed activities regarding single passive failure criteria for the standby service water system was a performance deficiency. The performance deficiency was evaluated using traditional enforcement because the finding had the ability to impact the regulatory process. The performance deficiency was more than minor because there was a reasonable likelihood that the change would require NRC review and approval prior to implementation. In accordance with the NRC Enforcement Manual, risk insights from the Inspection Manual Chapter 0609, Significance Determination Process, are used in determining the significance of 10 CFR 50.59 violations. Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the team determined that the finding represented a loss of system safety function in that the standby service water system could not meet its 30-day mission time to provide decay heat removal. Therefore, a Detailed Risk Evaluation was necessary. In accordance with Manual Chapter 0609, Appendix A, Section 6, Detailed Risk Evaluation, the senior reactor analyst evaluated the risk of the degraded condition that resulted from the finding. According to the Risk Assessment of Operational Events Handbook, Volume 1 - Internal Events, Section 4.1, Mission Time Modeling, in most events, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> is sufficient time to bring numerous resources to bear on core cooling.

In some events, the choice is conservative and the analysis results are overestimates.

Additionally, the analyst determined that Section 4.2 on increasing mission time was not applicable to the subject finding because the decrease in standby service water system water inventory would be obvious and there would be days to respond with makeup sources. Therefore, the analyst determined that the finding was of very low safety significance (Green) because, although the standby service water system could not provide 30 days of decay heat removal without operator action to provide makeup water to the system, it would have been able to complete its 24-hour risk significant mission time. Since the finding had very low safety significance, the finding was determined to be Severity Level IV, in accordance with the NRC Enforcement Policy. The finding does not have a crosscutting aspect because the most significant contributor to the finding does not reflect current licensee performance.

Enforcement.

The team identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes, Tests and Experiments which states, in part, that a licensee shall obtain a license amendment pursuant to Section 50.90 prior to implementing a proposed change, test, or experiment if this activity would result in more than a minimal increase in the likelihood of occurrence of a malfunction of a structure, system, or component important to safety previously evaluated in the final safety analysis report (as updated). Contrary to the above, the licensee failed to obtain a license amendment pursuant to Section 50.90 prior to implementing a proposed change that resulted in more than a minimal increase in the likelihood of occurrence of a malfunction of a structure, system, or component important to safety. Specifically, on August 18, 1987, the licensee implemented a change to the updated safety analysis

report which limited credible passive failures in the standby service water system to pump and valve seal leakage without obtaining a license amendment. This finding was entered into the licensees corrective action program as Condition Report CR-GGN-2012-09267. Because this finding was determined to be of very low safety significance and has been entered into the licensees corrective action program, this violation is being treated as a non-cited violation consistent with the NRC Enforcement Policy: NCV 05000416/2012008-03, Failure to Obtain NRC Approval for a Change to Credible Passive Failures in the Standby Service Water System.

2. Failure to Promptly Enter an NRC Violation Regarding the Standby Service Water

System into the Corrective Action Program

Introduction.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, involving the licensees failure to promptly enter an NRC violation regarding the standby service water system into the corrective action program.

Description.

On July 12, 2012, the inspection team identified a violation of 10 CFR 50.59, Changes, Tests, and Experiments, regarding a change to credible post-accident, non-electrical passive failures in the standby service water system.

Specifically, the change limited credible passive failures to pump and valve seal leakage.

Pipe, pipe fitting, and heat exchanger tube ruptures were no longer deemed credible. At this time, the team informed the licensee of the violation and questioned the licensee whether or not the standby service water system and ultimate heat sink remained operable, given the single failure of a pipe, pipe fitting, or heat exchanger tube rupture.

The licensee then reviewed the change to determine whether or not they agreed with the 10 CFR 50.59 violation. On July 19, 2012, the licensee entered this condition into their corrective action program as Condition Report CR-GGN-2012-09267.

Procedure EN-LI-102, Corrective Action Process, provides examples of adverse conditions requiring initiation of a condition report in Attachment 9.2. Attachment 9.2 lists regulatory issues, potential or actual NRC violations, as adverse conditions. In addition, EN-LI-102 states that the condition is expected to be promptly documented in a condition report. Because the 10 CFR 50.59 violation constituted a regulatory issue, the team determined that the licensee was required to enter the condition promptly into their corrective action program on July 12, 2012.

Subsequently, on July 29, 2012, the licensee performed an operability evaluation regarding the single passive failure aspect of the violation and concluded that the standby service water system was unable to perform its specified safety function for its entire mission time without compensatory measures. In effect, the seven-day delay in documenting the condition delayed evaluation of the standby service water systems ability to withstand single failures and, ultimately, implementation of compensatory measures necessary for the standby service water system to perform its specified safety function.

Analysis.

The team determined that the licensees failure to promptly enter the NRC violation as a condition adverse to quality into the corrective action program was a

performance deficiency. This finding was more than minor because it adversely affected the design control attribute of the Mitigating Systems Cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee failed to promptly document a violation of 10 CFR 50.59, which delayed an operability evaluation that ultimately determined that compensatory measures were required to ensure that the standby service water system could perform its specified safety function for its entire mission time. Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the team determined that the finding represented a loss of system safety function in that the standby service water system could not meet its 30-day mission time to provide decay heat removal.

Therefore, a Detailed Risk Evaluation was necessary. In accordance with Manual Chapter 0609, Appendix A, Section 6, Detailed Risk Evaluation, the senior reactor analyst evaluated the risk of the degraded condition that resulted from the finding.

According to the Risk Assessment of Operational Events Handbook, Volume 1 - Internal Events, Section 4.1, Mission Time Modeling, in most events, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> is sufficient time to bring numerous resources to bear on core cooling. In some events, the choice is conservative and the analysis results are overestimates. Additionally, the analyst determined that Section 4.2 on increasing mission time was not applicable to the subject finding because the decrease in standby service water system water inventory would be obvious and there would be days to respond with makeup sources. Therefore, the analyst determined that the finding was of very low safety significance (Green) because, although the standby service water system could not provide 30 days of decay heat removal without operator action to provide makeup water to the system, it would have been able to complete its 24-hour risk significant mission time. This finding had a crosscutting aspect in the area of problem identification and resolution, corrective action program component, because the licensee failed to ensure that issues potentially impacting nuclear safety are promptly identified, fully evaluated, and that actions are taken to address safety issues, in a timely manner, commensurate with their safety significance. Specifically, the licensee did not implement a corrective action program with a low threshold for identifying issues completely, accurately, and in a timely manner commensurate with their safety significance. P.1(a)

Enforcement.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, which states, in part, that Measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformance are promptly identified and corrected. Contrary to the above, the licensee failed to promptly identify a condition adverse to quality. Specifically, on July 12, 2012, the NRC informed the licensee of a violation of 10 CFR 50.59 requirements, but the licensee failed to promptly identify this as an adverse condition and enter this condition into their corrective action program until July 19, 2012. The finding was entered into the licensees corrective action program as Condition Report CR-GGN-2012-10075. Because this finding is of very low safety significance and has been entered into the licensees corrective action program, this violation is being treated as a non-cited violation consistent with the NRC Enforcement Policy:

NCV 05000416/2012008-04, Failure to Promptly Enter an NRC Violation Regarding the Standby Service Water System into the Corrective Action Program.

3. Failure to Follow Operability Determination Process Procedure

Introduction.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings involving the licensees failure to implement requirements of Procedure EN-OP-104, Operability Determination Process.

Description.

On July 12, 2012, the inspection team identified a violation of 10-CFR 50.59, Changes, Tests, and Experiments, regarding a change to credible, post-accident, non-electrical single passive failures in the standby service water system.

Specifically, the change limited credible single passive failures to pump and valve seal leakage. The Updated Final Safety Analysis Report no longer included pipe, pipe fitting, and heat exchanger tube ruptures as credible failures. On July 12, 2012, the team informed the licensee of the violation and inquired as to whether or not the standby service water system and ultimate heat sink remained operable, given the single passive failure of a pipe, pipe fitting, or heat exchanger tube rupture.

On July 19, 2012, the licensee agreed with the teams determination regarding the 10-CFR 50.59 violation and entered the condition into their corrective action program as Condition Report CR-GGN-2012-09267. Consequently, the licensee performed an immediate operability determination, using Procedure EN-OP-104, Operability Determination Process, concluding that the standby service water system and ultimate heat sink were OPERABLE based on the justification that No Degraded or Nonconforming Conditions exist per EN-OP-104, Revision 6, Attachment 9.1, Table 1.

In addition, the described condition does not render standby service water system inoperable, due to the low probability of a passive failure.

The team reviewed the initial operability determination and disagreed with the licensees conclusion of OPERABLE. First, because the condition questioned the ability of a technical specification required system to meet the single failure criterion, the standby service water system was potentially in noncompliance with the requirements of 10 CFR Part 50, Appendix A, Criterion 44, Cooling Water. For this condition, 9.1, Table 1, allows the following permissible classifications: OPERABLE-DEGRADED or NONCONFORMING, OPERABLE-OPERABILITY EVALAUATION, INOPERABLE, or INOPERABLE-OPERABILITY EVALUATION. Second, EN-OP-104 states that it is not acceptable to use Probabilistic Risk Assessment for making operability determinations. The team requested that the licensee rescreen the immediate operability determination.

On July 24, 2012, the licensee screened the condition as OPERABLE-OPERABILITY EVALUATION based on engineering input. OPERABLE-OPERABILITY EVALUATION is a condition where a technical specification structure, system, or component has a reasonable expectation of performing its specified safety function; however, a more thorough technical analysis is necessary to support the initial conclusion. Engineering input is technical information that can be used by the shift manager for operability determinations. Engineering judgment is a determination based on engineering principles, objective evidence, or available data that provide a reasonable expectation

that the structure, system, or component will perform its normal and design function until a detailed analysis can be performed. Furthermore, the supporting basis for the reasonable expectation of operability should provide a high degree that the structure, system, or component remains operable.

The team reviewed the second operability determination. The team disagreed with the licensees conclusion that the standby service water system remained in an OPERABLE-OPERABILITY EVALUATION classification because reasonable expectation of operability was not established. First, the licensee used engineering judgment to assume a reasonable expectation of operability. According to EN-OP-104, if Engineering Judgment is used, a sound basis must be documented. A sound basis for reasonable expectation of operability was never documented. Second, the team calculated that the cooling water inventory margin in the standby service water system was less than 50 gallons per minute averaged over the mission time yet the leak detection capability of the standby service water system was 1,200 gallons per minute.

Therefore, any undetected leak above 50 and below 1,200 gallons per minute would render the standby service water system incapable of performing its specified safety function.

On July 29, 2012, the licensee completed the final operability determination. The evaluation concluded that the standby service water system could not meet its specified safety function for a 30-day mission time without compensatory measures. Therefore, the licensee implemented compensatory measures to maintain operability and changed the permissible classification to OPERABLE-COMPENSATORY MEASURE, which is a condition where a technical specification structure, system, or component is operable but a degraded or nonconforming condition exists that requires compensatory measures.

The licensee entered this condition into their corrective action program as Condition Report CR-GGN-2012-09356.

Analysis.

The team determined that the failure to implement the requirements of the operability determination process procedure was a performance deficiency. The finding was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems Cornerstone to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, the standby service water system was incapable of performing its specified safety function for the entire 30-day mission time without compensatory measures.

Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the team determined that the finding represented a loss of system safety function in that the standby service water system could not meet its 30-day mission time to provide decay heat removal. Therefore, a Detailed Risk Evaluation was necessary. In accordance with Manual Chapter 0609, Appendix A, Section 6, Detailed Risk Evaluation, the senior reactor analyst evaluated the risk of the degraded condition that resulted from the finding. According to the Risk Assessment of Operational Events Handbook, Volume 1 - Internal Events, Section 4.1, Mission Time Modeling, in most events, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> is sufficient time to bring numerous resources to bear on core cooling. In some events, the choice is conservative and the analysis results are overestimates. Additionally, the analyst determined that Section 4.2 on increasing mission time was not applicable to the subject finding because the

decrease in standby service water system water inventory would be obvious and there would be days to respond with makeup sources. Therefore, the analyst determined that the finding was of very low safety significance (Green) because the standby service water system could have been able to complete its 24-hour risk significant mission time although it could not provide 30 days of decay heat removal without operator action to provide makeup water to the system. This finding had a crosscutting aspect in the area of human performance, decision making component, because the licensee did not make decisions that demonstrated that nuclear safety was an overriding priority. Specifically, the licensee did not make safety significant decisions using a systematic process to ensure safety is maintained. H.1(a)

Enforcement.

The team identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings which states, in part, that Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Contrary to the above, the licensee failed to accomplish activities affecting quality in accordance with prescribed procedures. Specifically, from July 19, 2012, to July 29, 2012, the licensee failed to correctly evaluate the operability of the standby service water system with a degraded or nonconforming condition and failed to document a sound basis for a reasonable expectation of operability of the standby service water system as required by Procedure EN-OP-104, Operability Determination Process. The finding was entered into the licensees corrective action program as Condition Report CR-GGN-2012-09356.

Because this finding is of very low safety significance and has been entered into the licensees corrective action program, this violation is being treated as a non-cited violation consistent with the NRC Enforcement Policy: NCV 05000416/2012008-05, Failure to Follow Operability Determination Process Procedure.

.2.4 Division III 4160 Vac Engineered Safety Feature Switchgear Bus 17AC

a. Inspection Scope

The team reviewed the updated safety analysis report, design basis documents, the current system health report, calculations, maintenance and test procedures, and condition reports associated with the division III 4160 Vac engineered safety feature switchgear bus 17AC. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Maintenance history to verify the monitoring and correction of potential degradation.
  • Calculations for electrical distribution system load flow/voltage drop, short-circuit, and electrical protection and coordination.
  • Protective device settings and circuit breaker ratings to confirm adequate selective protection and coordination of connected equipment during worst-case short circuit conditions.
  • Circuit breaker preventive maintenance, inspection, and testing procedures to confirm inclusion of relative industry operating experience and vendor recommendations.
  • Results of completed preventive maintenance on 4160 Vac switchgear and breakers.
  • Degraded voltage and loss of voltage relay protection scheme and circuit breaker control logics that initiate automatic bus transfers.
  • NRC Information Notice 1993-091, Misadjustment Between General Electric 4.16-KV Circuit Breakers and Their Associated Cubicles , dated December 3, 1993

b. Findings

1. Failure to Incorporate Test and Inspection Requirements for 4160 Vac Circuit Breakers

into Preventive Maintenance Procedures

Introduction.

The team identified a Green non-cited violation of 10 CFR 50, Appendix B, Criterion XI, Test Control, involving the licensees failure to establish a test program which incorporated test requirements and acceptance limits contained in applicable design documents. Specifically, the licensee failed to incorporate minimum control voltage drop-out tests, reduced voltage tests, and inspection of auxiliary contacts in safety-related 4160 Vac circuit breaker preventive maintenance procedures.

Description.

The licensees 4160 Vac circuit breaker maintenance and testing program was established using Preventive Maintenance Basis Template, EN-Switchgear-Medium Voltage - 1 KV to 7KV, Revision 3. This 4160 Vac preventive maintenance basis template establishes the cleaning, inspection, and testing program which incorporates requirements from vendor documents and Electrical Power Research Institute guideline TR-112814, Reduced Voltage Testing of Low and Medium Voltage Breakers. The Breaker - Detailed Inspection, Cleaning, and Testing task lists the types of inspection and tests that should be incorporated into the 4160 Vac circuit breaker testing procedures. Listed in this section are requirements for minimum control voltage tests, reduced voltage tests, and measuring resistance and cleaning of relay contacts.

The team reviewed preventive maintenance procedures for the 4160 Vac circuit breakers used in the engineered safety feature electrical buses. During this review, the team identified that Procedure 07-S-12-41,Inspection and Testing of ITE 5 KV Circuit Breakers, Procedure 07-S-12-42, Inspection and Testing of Westinghouse DHP 4.16KV Circuit Breakers, and Procedure 07-S-12-61, Inspection of GE Magna-Blast Circuit Breakers, did not incorporate testing or inspection of the minimum voltage drop-out settings, reduced voltage settings, and inspection and resistance measurement of auxiliary switch contact relays.

The team determined that the preventive maintenance Procedures 07-S-12-41, 07-S-12-42, and 07-S-12-61 did not incorporate required tests or inspections that would

provide assurance that all testing required to demonstrate that structures, systems and components will perform satisfactorily in service.

Analysis.

The team determined that the failure to incorporate required tests and inspections into preventive maintenance procedures for safety-related 4160 Vac circuit breakers was a performance deficiency. This finding was more than minor because, if left uncorrected, it would lead to a more significant safety concern. Specifically, the failure to incorporate the testing, cleaning, and inspection requirements into preventive maintenance procedures were a significant programmatic deficiency which could cause unacceptable conditions to go undetected. Using the Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, the issue screened as having very low safety significance (Green) because it was a design or qualification deficiency that did not represent a loss of safety function. This finding had a crosscutting aspect in the area of problem identification and resolution, operating experience component, because the licensee failed to use operating experience information, including vendor recommendations and internally generated lessons learned, to support plant safety. Specifically, the licensee did not implement and institutionalize operating experience through changes to processes, procedures, equipment, and training programs. P.2(b)

Enforcement.

The team identified a Green non-cited violation of 10 CFR 50, Appendix B, Criterion XI, Test Control, which states, in part, A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design document. Contrary to the above, the licensee failed to establish a test program that assured that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service was identified and performed in accordance with written test procedures which incorporated the requirements and acceptance limits contained in applicable design document. Specifically, prior to July 27, 2012, the licensees safety-related 4160 Vac circuit breaker preventive maintenance Procedures 07-S-12-41, 07-S-12-42, and 07-S-12-61 failed to incorporate inspection and test requirements for minimum voltage tests, reduced voltage tests, and inspection of auxiliary switch relay contacts as established in the licensees circuit breaker maintenance program. This condition was entered into the licensees corrective action program as Condition Reports CR-GGN 2012-08885 and CR-GGN-2012-09111. Because this finding is of very low safety significance and has been entered into the licensees corrective action program, this violation is being treated as a non-cited violation consistent with the NRC Enforcement Policy: NCV 05000416/2012008-06, Failure to Incorporate Test and Inspection Requirements for 4160 Vac Circuit Breakers into Preventive Maintenance Procedures.

.2.5 Division III Emergency Diesel Generator 13

a. Inspection Scope

The team reviewed the updated safety analysis report, system description, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the division III emergency diesel generator 13. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component to perform its desired design basis function.

Specifically, the team selectively reviewed:

  • Component maintenance history and corrective action history to confirm the licensee was appropriately monitoring potential degradation.
  • Calculations for the diesel generator loading, voltage, and frequency conditions, including load flow and voltage regulation.
  • Control logic and circuits for the starting and loading of the diesel generator.
  • The range of ambient temperature conditions and their basis for the diesel generator and electrical auxiliaries.
  • The visible material condition and configuration of the components.
  • The off-normal emergency procedure for back-feed of power from the Division III diesel generator to either the Division I or Division II 4160 V bus.

b. Findings

No findings of significance were identified.

.2.6 Division III 480 Vac Load Center 17B01

a. Inspection Scope

The team reviewed the updated safety analysis report, system description, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the division III 480 Vac Load Center 17B01. The team also performed walkdowns and conducted interviews with system engineering personnel to ensure the capability of this component to perform its desired design basis function.

Specifically, the team reviewed:

  • Vendor installation and maintenance manuals.
  • Electrical distribution system load flow/voltage drop, short circuit, and electrical protection and coordination calculations.
  • Protective device settings and circuit breaker ratings to confirm operation during worst-case short circuit conditions.
  • Circuit breaker preventive maintenance inspection and testing procedures to determine adequacy relative to industry and vendor recommendations.

b. Findings

No findings of significance were identified.

.2.7 Engineered Safety Features Transformer 11

a. Inspection Scope

The team reviewed the updated safety analysis report, system description, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the engineered safety features transformer 11. The team also performed walkdowns and conducted interviews with system engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Voltage tap settings, nameplate data, and protective relay settings, and loading requirements.
  • Recently completed transformer preventive maintenance.
  • Steady state loading calculation and protection.
  • Metering and relay diagram and instrumentation.
  • Relay protection, relay coordination, and short circuit calculations.
  • Test performance records and the result of dissolved oil gas and Doble test analysis.

b. Findings

No findings of significance were identified.

.2.8 Power Range Neutron Monitoring System

a. Inspection Scope

The team reviewed the updated safety analysis report, system description, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the power range neutron monitoring system. The team also performed walkdowns and conducted interviews with system engineering personnel to ensure the capability of this component to perform its desired design basis function.

Specifically, the team selectively reviewed:

  • The safety evaluation report to confirm that the installation of the system conformed to the safety evaluation report acceptance criteria.
  • The engineering change package and implementing work orders.
  • Fiber optic cable installation.
  • Features provided for electromagnetic compatibility, physical separation, and independence.
  • Precautions for electrostatic discharge and software configuration control.
  • Site acceptance tests and condition reports initiated during site installation.

b. Findings

No findings of significance were identified.

.2.9 High Pressure Core Spray Pump 1E22-C001

a. Inspection Scope

The team reviewed the updated safety analysis report, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the high pressure core spray pump 1E22-C001. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component perform its desired design basis function. Specifically, the team reviewed:

  • General Electric design specification data sheets defining the system design requirements.
  • Pump calculation addressing the available net positive suction head during system suction from the suppression pool and condensate storage tank at design temperature limits.
  • Quarterly functional test procedures and test results used to monitor potential high pressure core spray pump degradation.

b. Findings

No findings of significance were identified.

.2.10 High Pressure Core Spray Suppression Pool and Condensate Storage Tank Suction

Valves 1E22-F001 and 1E22-F015

a. Inspection Scope

The team reviewed the updated safety analysis report, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the high pressure core spray suppression pool and condensate storage tank suction valves 1E22-F001 and 1E22-F015. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component perform its desired design basis function. Specifically, the team reviewed:

  • General Electric design specification data sheets defining the system design requirements.
  • Quarterly valve test procedure and surveillance results as part of the inservice testing program.
  • Accident analysis calculation of a postulated loss of offsite power with a concurrent lost of coolant accident resulting in a catastrophic failure of the condensate storage tank.

b. Findings

No findings of significance were identified.

.2.11 High Pressure Core Spray Minimum Flow Valve 1E22-F012

a. Inspection Scope

The team reviewed the updated safety analysis report, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the high pressure core spray minimum flow valve 1E22-F012. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component to perform its desired design basis function.

Specifically, the team reviewed:

  • General Electric design specification data sheets defining the system design requirements.
  • Quarterly valve test procedure and surveillance results as part of the inservice testing program.
  • Engineering design change package addressing the increase in minimum rate of flow.
  • Logic and wiring diagrams for minimum flow valve 1E22-E012.
  • Vendor installation and maintenance manuals.

b. Findings

No findings of significance were identified.

.2.12 Low Pressure Core Spray Pump 1E21-C001

a. Inspection Scope

The team reviewed the updated safety analysis report, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the low pressure core spray pump 1E21-C001. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Safety-related calculations addressing required low pressure core spray pump performance requirements during design basis accidents.
  • Calculations addressing the uncertainties of the instruments used to verify pump performance during required technical specification surveillances.
  • Surveillance procedures and test results used to monitor potential low pressure core spray pump degradation.
  • Safety-related calculations and surveillance tests addressing the performance of associated low pressure core spray injection valve.
  • Safety-related calculation determining the maximum differential pressure across the associated low pressure core spray injection valve.

b. Findings

No findings of significance were identified.

.2.13 Residual Heat Removal Pump 1E12-C002A

a. Inspection Scope

The team reviewed the updated safety analysis report, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the residual heat removal pump 1E12-C002A. The team also performed walkdowns and conducted interviews with engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Corrective action program documents and system health reports.
  • System design criteria.
  • Piping and instrumentation diagrams.
  • Technical specifications and bases document.

b. Findings

No findings of significance were identified.

.2.14 Emergency Diesel Generator 13 Ventilation

a. Inspection Scope

The team reviewed the updated safety analysis report, system description, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the division III emergency diesel generator ventilation system. The team also performed walkdowns and conducted interviews with

engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Safety-related calculations addressing required heat removal performance requirements during design ambient temperature conditions.
  • Safety-related calculations addressing required heat removal performance requirements during postulated maximum ambient temperature conditions.
  • Ventilation fan flow data recorded after fan blade adjustments.

b. Findings

No findings of significance were identified.

.2.15 Emergency Pump Room Fan Cooler T51-B001-C

a. Inspection Scope

The team reviewed the updated safety analysis report, design basis documents, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the emergency pump room fan cooler T51B001-C.

The team also performed walkdowns and conducted interviews with system and design engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Corrective action program documents.
  • Piping and instrumentation diagrams.
  • System design criteria and health reports.
  • Vendor documentation.

b. Findings

No findings of significance were identified.

.2.16 Division I Residual Heat Removal Heat Exchanger

a. Inspection Scope

The team reviewed the updated safety analysis report, design basis documents, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with the division I residual heat removal heat exchanger.

The team also performed walkdowns and conducted interviews with system engineering personnel to ensure the capability of this component to perform its desired design basis function. Specifically, the team reviewed:

  • Work orders and corrective action program documents.
  • System design criteria and system health reports.
  • Corrective action program reports to verify the monitoring and correction of potential degradation, operability evaluations and Root/Apparent Cause evaluations
  • Piping and instrumentation diagrams.

b. Findings

No findings of significance were identified.

.3 Results of Reviews for Operating Experience:

.3.1 Inspection of NRC Information Notice 1987-10, Potential for Water Hammer during

Restart of Residual Heat Removal Pumps

a. Inspection Scope

The team reviewed the licensees evaluation of Information Notice 1987-10 Potential for Water Hammer during Restart of Residual Heat Removal Pumps to verify that the review adequately addressed the industry operating experience. The team verified that the licensees evaluation adequately addressed the issues in the Information Notice.

The team verified that the licensee implemented changes to the system operating instructions based on recommendations given in the evaluations.

b. Findings

No findings of significance were identified.

.3.2 Inspection of NRC Inspection of Information Notice 1993-091 Misadjustment between

General Electric 4.16 kV Circuit Breaker and their Associated Cubicles

a. Inspection Scope

The team reviewed the licensees evaluation of Information Notice 1993-091, Misadjustment between General Electric 4.16-KV Circuit Breaker and their Associated Cubicles, to verify that the review adequately addressed the industry operating experience. The team verified that the licensees evaluation adequately addressed the issues in the information notice. The team verified that the licensee assured that Procedure 07-S-12-61, Inspection of GE Magna Blast Circuit Breakers, Revision 6 prevented the concerns addressed in the Information Notice.

b. Findings

No findings of significance were identified.

.3.3 Inspection of NRC Information Notice 2005-30, Safe Shutdown Potentially Challenged

by Unanalyzed Internal Flooding Events and Inadequate Design

a. Inspection Scope

The team reviewed the licensees evaluation of Information Notice 2005-30, Safe Shutdown Potentially Challenged by Unanalyzed Internal Flooding Events and Inadequate Design, to verify that the review adequately addressed the industry operating experiences discussed in the information notice. The team reviewed the licensees existing evaluation and performed independent reviews of plant areas to verify adequate protection from postulated internal flooding events.

b. Findings

1. Potential Internal Flooding Caused by Circulation Water System Failure

Introduction.

The inspectors identified an unresolved item related to the licensees evaluation of internal flooding events resulting from the postulated failure of circulating water system components in the turbine building. Specifically, the licensees design basis flooding analyses were based on comparing the volume of the circulating water system to the volumes of the affected buildings and did not consider the effect of closed doors between the flood source in the Unit 1 turbine building, the canceled Unit 2 turbine building, and the radwaste building.

Description.

The inspectors reviewed Calculation M6.3.051, Circulating Water System-Calculate Revised Plant Flooding Elevations Due to Aux Cooling Tower, Revision B, to verify that the postulated failure of circulating water system components in the turbine building would not affect safety-related equipment required for achieving safe shutdown. This calculation assumes that the entire inventory of the circulating water system, 13.4 million gallons, is released into the Unit 1 turbine building due to a circulating water system failure and determines the resulting flood elevations. The calculation does not consider postulated flood flow rates; it is a steady state calculation based on the total circulating water system inventory being contained within the plant buildings. The calculation includes an assumption that the Unit 2 turbine building volume would be available to accommodate floodwater because the passage/corridor between the Unit 1 and Unit 2 turbine buildings is not watertight. In addition, the maximum flood elevation is calculated based on the volume of the radwaste building being available to accommodate floodwater. The sliding door between the Unit 1 turbine building and the radwaste building is not addressed in the calculation. Based on these assumptions, the calculation determines that the bounding flood elevation is 104.0 feet, and that the flood will not reach safety-related equipment located in the control building at elevation 111 feet. The calculation also determines that the bounding flood elevation would reach 111.4 feet in the control building if the volume of the Unit 2 turbine building were not considered. These calculated flood elevations do not include the additional volume contributed by 23,200 gallon per minute makeup from the plant service water system to the circulating water system. The calculation concludes that operator action to stop the makeup flow within 70 minutes is acceptable due to the margin available in the calculation.

The inspectors questioned the assumptions of this calculation; especially the assumption that buildings connected by passageways that are not watertight would flood coincidently with each other. The inspectors asked if the expected leak rate between the Unit 1 turbine building, the Unit 2 turbine building, and the radwaste building through large sliding doors would be sufficient to limit the maximum flood elevation in the control building which is connected to the Unit 1 turbine building with a conventional door.

During the inspection, the licensee performed Calculation M6.3.051-001, Circulating Water Systems - Calculate Revised Unit 1 Turbine Building and Unit 1 Control Building Flooding Elevations, Revision 0. This calculation was performed to address the inspectors questions documented in Condition Report CR-GGN-2012-9424. This calculation was a transient analysis of the flood level considering the closed sliding doors between the Unit 1 turbine building and the Unit 2 turbine building and the Unit 1 turbine building and radwaste building. The calculation considered the gaps around the closed doors, and included the contribution of the makeup flow from the plant service water system to the circulating water system.

However, Calculation M6.3.051-001, revision 0 was based on a limited flowrate from an expansion boot failure in the circulating water system. The calculation used the methodology of NRC Branch Technical Position MEB 3-1 to predict the maximum flow from a failed circulating water system expansion joint. Applying the MEB 3-1 methodology to the 10-foot diameter expansion joint results in a postulated crack of 5-feet long and 1-inch wide. This crack results in a calculated flowrate of approximately 15,500 gpm. Based on this limited flowrate, the calculation determined that the maximum flood elevation would be approximately 104 feet.

The inspectors question the applicability of NRC Branch Technical Position MEB 3-1 to nonsafety-related expansion joints and asked the licensee to determine the maximum flood flowrate that would not exceed a flood elevation of 111 feet. In response to these questions, the licensee performed an informal analysis and determined that a flowrate of approximately 75,000 gpm or greater would result in exceeding a flood elevation in the Unit 1 turbine building, potentially communicating with the control building. The licensee also stated that they considered the application of the MEB 3-1 methodology to the expansion joints to be consistent with their licensing basis (UFSAR Section 3.6a.2.1)and that a gross failure of the expansion joint is highly unlikely since the expansion joint in reinforced with steel belts and leakage would be through a local defect. They also stated that the metal shield covering the expansion joints would serve to limit flow from the expansion joint failure, but did not provide the expected flowrate from a large failure of an expansion joint within the metal shield.

The inspectors performed a review of licensing basis documentation related to flooding resulting from failures of circulating water components and did not identify any specific value for the maximum flood flowrate or the maximum postulated failure size in an expansion joint. Grand Gulf Nuclear Station Update Safety Analysis Report, Section 10.4.5.3, describes the potential of the entire volume of the circulating water system flooding the Unit 1 turbine building, discusses a potential gross failure in the circulating water system, and describes the maximum circulating water system flowrate

but does not specifically address the maximum postulated flood flowrate from a circulating water system failure.

The inspectors determined that design basis calculation M6.3.051, Revision B did not adequately verify that the postulated failure of circulating water system components in the turbine building would not affect safety-related equipment required for achieving safe shutdown. This steady state calculation did not consider the effects of closed doors on the maximum flood level in the control building. Calculation M6.3.051-001, Revision 0 was a transient analysis that did address the effects of the closed doors. However, this calculation was based on calculating a limited flood flowrate by applying the methodology of NRC Branch Technical Position MEB 3-1 to non safety-related circulating water system expansion joints. The inspectors were not able to determine if this methodology was consistent with the licensing basis during the period of the inspection. Resolution of this issue will require determining the maximum flowrate resulting from the postulated failure of a circulating water system component in the turbine building and verifying that the resulting flood elevation will not affect safety-related equipment required for achieving safe shutdown.

The inspectors have discussed this design and licensing basis issue with NRC staff in the Office of Nuclear Reactor Regulation. Due to complexity of establishing the appropriate design and licensing bases for this issue, this item is considered unresolved pending further NRC review to determine if a finding exists. This will be tracked as URI 05000416/2012008-07, Internal Flooding Caused by Circulation Water System Failure.

.3.4 Inspection of Information Notice 2007-34 Operating Experience Regarding Electric

Circuit Breakers

a. Inspection Scope

The team reviewed the licensees evaluation of NRC Information Notice 2007-34, Operating Experience Regarding Electrical Circuit Breakers, to verify that the review adequately addressed the industry operating experiences discussed in the information notice. The team verified that the licensees evaluation adequately addressed the operating experience and inadequate maintenance practices identified in the Information Notice. The licensee initiated TEAR 2007-0667 to address the inadequate maintenance practices addressed in the Information Notice. The team verified that the licensees corrective actions were adequate to prevent inadequate preventive maintenance from occurring.

b. Findings

No findings of significance were identified.

.3.5 Inspection of NRC Information Notice 2012-01 Seismic Considerations - Principally

Issues Involving Tanks

a. Inspection Scope

The team reviewed the licensees response to Information Notice 2012-01, Seismic Considerations - Principally Issues Involving Tanks, to verify that the review adequately addressed the industry operating experience. The team verified that the licensees review, documented in Condition Reports CR-GGN-2012-03716 and CR-GGN-2011-07337, adequately addressed the issues in the Information Notice. The team verified that the licensee evaluated the human performance errors identified in the Information Notice, and had procedural steps in place that would prevent those errors from occurring.

b. Findings

No findings of significance were identified.

.4 Results of Reviews for Operator Actions

The team selected risk-significant components and operator actions for review using information contained in the licensees probabilistic risk assessment. This included components and operator actions that had a risk achievement worth factor greater than two or Birnbaum value greater than 1E-6.

a. Inspection Scope

For the review of operator actions, the team observed operators during simulator scenarios associated with the selected components as well as observing simulated actions in the plant.

The selected operator actions were:

  • Plant stabilization during station blackout conditions (Scenario)
  • Control room evacuation due to toxic gas (Scenario)

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

The team reviewed actions requests associated with the selected components, operator actions and operating experience notifications. In addition, this report contains the following issue that has problem identification cross-cutting aspects.

4OA6 Meetings, Including Exit

On July 26, 2012, the team leader presented the preliminary inspection results to Mr. M.

Perito, Vice President, and other members of the licensees staff. On September 10, 2012, the team leader conducted a telephonic final exit meeting with J. Browning, General Plant Manager Operations, and other members of the licensee's staff. The licensee acknowledged the findings during each meeting. While some proprietary information was reviewed during this inspection, no proprietary information was included in this report.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

M. Bacon, Superintendent
J. Browning, General Manager, Plant Operations
D. Chipley, Electrical Design Engineering
J. Edwards, Site Representative, South Mississippi Electric
J. Giles, Manager, Training
J. Hixson, Electrical Design Engineering
D. Hollis, Electrical Design Engineering
K. Howard, Manager, Projects
M. Humphries, Programs Engineer, Circuit Breakers, Relays, and Motors
D. Jones, Manager, Design Engineering
C. Loyd, Supervisor, System Engineering
J. Miller, Manager, Operations
J. Nadeau, Manager, Corrective Actions & Assessment
M. Novogoratz, System Engineer, PRNMS
C. Perino, Manager, Licensing
M. Perito, Site Vice President, Operations
G. Phillips, Supervisor, Design Engineering, Instrumentation & Control
A. Pittman, PRA Engineer, Fuels and Analysis
M. Richey, Director, Nuclear Safety Assurance
M. Runion, Manager, Maintenance
A. Sayre, System Engineer, 125 VDC system
R. Scarbrough, Licensing Specialist, Licensing
J. Seiter, Senior Licensing Specialist, Licensing
R. Sumners, System Engineer, Diesel Generator
T. Tankersly, Manager, Quality Assurance
T. Thurmon, Supervisor, Design Engineering, Mechanical
R. Turcotte, Superintendent, Security
D. Wiles, Director, Engineering
C. Williams, Supervisor, Design Engineering, Electrical

NRC personnel

D. Loveless, Senior Reactor Analyst
S. M. Wong, Senior Reactor Analyst
B. Rice, Resident Inspector
R. Smith, Senior Resident Inspector

-1- Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000416/2012008-01 NCV Preconditioning of 4160 Vac Circuit Breakers for As-Found Tests (1R21.2.1)
05000416/2012008-02 NCV Failure to Establish a Testing Program for Safety-Related 125 Vdc Circuit Breakers (1R21.2.2)
05000416/2012008-03 NCV Failure to Obtain NRC Approval for a Change to Credible Passive Failures in the Standby Service Water System (1R21.2.3)
05000416/2012008-04 NCV Failure to Promptly Enter an NRC Violation Regarding the Standby Service Water System into the Corrective Action Program (1R21.2.3)
05000416/2012008-05 NCV Failure to Follow Operability Determination Process Procedure (1R21.2.3)
05000416/2012008-06 NCV Failure to Incorporate Test and Inspection Requirements for 4160 Vac Circuit Breakers into Preventive Maintenance Procedures (1R21.2.4)

Opened

05000416/2012008-07 URI Potential Internal Flooding Caused by Circulation Water System Failure (1R21.3.3)

LIST OF DOCUMENTS REVIEWED