IR 05000305/2012003

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IR 05000305-12-003, 04/01/2012 - 06/30/2012, Kewaunee Power Station; Plant Modifications, Outage Activities, Identification and Resolution of Problems, and Follow Up of Events and Notices of Enforcement Discretion
ML12223A195
Person / Time
Site: Kewaunee Dominion icon.png
Issue date: 08/09/2012
From: Reimer K
NRC/RGN-III/DRP/B2
To: Heacock D
Dominion Energy Kewaunee
References
IR-12-003
Download: ML12223A195 (62)


Text

gust 9, 2012

SUBJECT:

KEWAUNEE POWER STATION NRC INTEGRATED INSPECTION REPORT 05000305/2012003

Dear Mr. Heacock:

On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Kewaunee Power Station. The enclosed report documents the results of this inspection, which were discussed on July 3, 2012, with Mr. A. Jordan, the site Vice President, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

One NRC identified and two self-revealing findings of very low safety significance (Green) were identified during this inspection. These findings were determined to involve violations of NRC requirements. Additionally, the NRC has determined that a traditional enforcement Severity Level IV violation occurred. The NRC is treating these violations as non-cited violations (NCVs),

consistent with Section 2.3.2 of the Enforcement Policy.

If you contest these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, Region III; the Director, Office of Enforcement, U. S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Kewaunee Power Station.

If you disagree with a cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III; and the NRC Resident Inspector at the Kewaunee Power Station. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Documents Access and Management System (ADAMS),

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Branch Chief Branch 2 Division of Reactor Projects Docket No. 50-305 License No. DPR-43

Enclosure:

Inspection Report 05000305/2012003; w/Attachment: Supplemental Information

REGION III==

Docket No: 50-305 License No: DPR-43 Report No: 05000305/2012003 Licensee: Dominion Energy Kewaunee, Inc, Facility: Kewaunee Power Station Location: Kewaunee, WI Dates: April 1, 2012, through June 30, 2012 Inspectors: R. Krsek, Senior Resident Inspector K. Barclay, Resident Inspector J. Beavers, Emergency Preparedness Specialist J. Jandovitz, Project Engineer N. Shah, Project Engineer T. Bilik, Senior Reactor Inspector L. Jones, Reactor Engineer N. Feliz-Adorno, Reactor Engineer J. Cassidy, Senior Health Physicist D. Szwarc, Reactor Inspector Approved by: Kenneth Riemer, Branch Chief Branch 2 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

Inspection Report (IR) 05000305/2012003, 04/01/2012 - 06/30/2012, Kewaunee Power Station (KPS); Plant Modifications, Outage Activities, Identification and Resolution of Problems, and Follow-Up of Events and Notices of Enforcement Discretion.

This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. One Green finding and one Severity Level (SL) IV violation were identified by the inspectors and two Green findings were self-revealed. The three findings and the SL IV violation were considered non-cited violations (NCVs) of NRC regulations. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

NRC-Identified

and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

A finding of very low safety significance and associated NCV of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the failure to accomplish Temporary Modification (TMOD) 2012-11 in accordance with Work Order (WO) KW100894696 and the associated weld data sheet and map.

Specifically, licensee personnel failed to utilize the WO instructions, weld data sheet and weld map when welding a temporary NRC-approved clamp on American Society of Mechanical Engineers (ASME) Code Class 2 residual heat removal (RHR) piping. The failure to use the required documentation to perform the work resulted in the worker creating a second through wall leak on the ASME Code, Class 2 RHR piping upstream of valve RHR-600. The licensee entered the issue into its corrective action program (CAP) as condition report (CR) 472915 and permanently corrected both through wall leaks on the RHR system piping following the approval of a second proposed alternative, without incident on May 5, 2012. At the end of the inspection period, the licensee continued to perform an apparent cause evaluation (ACE) to determine the causes for the organizational failures that occurred.

The finding was determined to be more than minor in accordance with IMC 0612,

Power Reactor Inspection Reports, Appendix B, Issue Screening, dated December 24, 2009, because the finding was associated with the Mitigating Systems Cornerstone attribute of human error (pre-event) and adversely affected the cornerstone objective to ensure the reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors determined that the finding could be evaluated in accordance with IMC 0609,

Appendix G, Shutdown Operations SDP, dated February 28, 2005. The inspectors used Checklist 1, PWR Hot Shutdown Operation: Time to Core Boiling <2 Hours, contained in Attachment 1 and determined that the finding affected core heat removal guidelines I.B(1), Procedures, and I.C(2), Equipment. The inspectors screened the finding as very low safety significance (Green) because it did not degrade the licensees ability to establish an alternate core cooling path if decay heat removal could not be re-established and, therefore, did not require a phase 2 or phase 3 analysis. This finding has a cross-cutting aspect in the area of human performance, resources, because the licensee did not ensure supervisory and management oversight of work activities, including contractors, such that nuclear safety was supported. Specifically, the inspectors identified that the pre-job brief conducted by supervision and management for this work did not include a review of the WO, weld sheet, or weld map and did not convey accurate information regarding the significance of the activity, the type of weld to be performed and the system conditions where the weld was performed (H.4(c)).

(Section 1R18)

Green.

The inspectors identified a finding of very low safety significance (Green) and associated NCV of 10 CFR Part 50, Appendix R, Section III.G.3, for the licensees failure to provide adequate fire suppression coverage for fire zone AX-32. Specifically, the licensee failed to provide required fire suppression coverage for safe shutdown functions of source range monitoring, isolation of a steam generator (SG) blowdown line, and pressurizer level instrumentation in the cable spreading area. The licensee entered the issue into the CAP, designated manual backup from hose stations, and implemented an hourly fire watch for the radiation protection office (RP) in fire zone AX-32.

The inspectors determined that the finding was more than minor because the failure to provide suppression for redundant trains of safe shutdown equipment increased the likelihood that alternative shutdown methods would have to be used in the event of a fire. The finding was of very low safety significance based on a Phase 3 significance determination analysis. The finding has a cross-cutting aspect in the area of problem identification, corrective action program, because the licensee did not take appropriate corrective actions to address the inadequate suppression system in fire zone AX-32 (P.1(d)). (Section 4OA2.4)

Cornerstone: Barrier Integrity

Green.

A finding of very low safety significance (Green) and associated NCV of Technical Specification (TS) 5.4.1, Procedures, was self-revealed because procedure MCM-FH-001, Repair of the Fuel Transfer System, was inadequate. Specifically, the procedure did not contain torque specifications for tightening the upender frame cable clamps and, on April 23, the cable for the spent fuel pool (SFP) upender slipped through the cable clamps and allowed the upender containing a fuel assembly to descend approximately 12 inches. The licensee confirmed that no damage occurred to the fuel assembly and placed procedure MCM-FH-001 on administrative hold to prevent its use until it could be updated with the appropriate torque specifications. At the end of this inspection period, the licensee was performing an ACE to determine the causes of the event, and develop corrective actions.

The finding was determined to be more than minor because, if left uncorrected, the finding had the potential to lead to a more significant safety concern. Specifically, the upender containing the fuel assembly could have fallen from the near-full vertical position to the horizontal position. The inspectors evaluated the finding by applying the SFP questions in the Fuel Barrier column of Table 4a, located in IMC 0609,

Attachment 4, dated January 10, 2008. The inspectors answered "No" to all three questions and determined that the finding was of very low safety significance (Green).

The finding has a cross-cutting aspect in the areas of problem identification and resolution, operating experience (OE), because the licensee failed to communicate to affected internal stakeholders in a timely manner relevant external OE. Specifically, the licensee failed to discuss available and relevant OE related to the failure to appropriately torque cable clamps on an SFP upender (P.2(a)). (Section 1R20)

Cornerstone: Other

  • SL IV. A Severity Level (SL) IV NCV of 10 CFR Part 50.9(a), Completeness and Accuracy of Information, was identified by the inspectors for the failure of the licensee to provide complete and accurate information in all material respects to the Commission in licensee Request RR-2-3, dated April 29, 2012 (ADAMS Accession No. ML12122A138).

As part of a license amendment for a proposed temporary deviation from the requirements of 10 CFR 50.55a and ASME Code, Section XI, the licensee incorrectly stated the allowable leakage from the temporary clamp in transition from Mode 5 to 4 was governed by TS 5.5.2, Primary Coolant Sources Outside Containment, and proposed an allowable leakage value of 5.5 gallons per hour (gph). After licensee Request No. RR-2-3 was verbally approved by the NRC on April 30, 2012, the inspectors and NRC staff determined that the governing leakage requirement was no leakage in Mode 4 for the clamp as required by TS 3.4.13, Reactor Coolant System Operational Leakage.

The performance deficiency was determined to be more than minor in accordance with the NRC Enforcement Policy and Enforcement Manual because the NRC identified the performance deficiency, the NRC relied on the information provided in a licensing decision, and the misinformation was identified after the NRC relied on the information in its licensing decision. Because violations of 10 CFR 50.9 are considered to be violations that potentially impact the regulatory process, they are dispositioned using the traditional enforcement process instead of the ROP SDP. Because the performance deficiency, specifically a failure to submit complete and accurate information, was not an ROP finding per IMC 0612, Appendix B, Issue Screening, a cross-cutting aspect was not assigned to this violation. The severity of the violation was mitigated because of the facts surrounding the licensees implementation of Request No. RR-2-3.

(Section 4OA3.1)

Licensee-Identified Violations

No violations were identified.

REPORT DETAILS

Summary of Plant Status

Kewaunee Power Station (KPS) operated at full power until April 6, 2012, when they shut down the reactor for a planned refueling outage. The licensee completed the refueling outage on May 10 and returned to full power on May 13, 2012, until the end of the inspection period, except for brief downpowers to conduct planned maintenance and surveillance activities.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • EDG B after testing;
  • safety injection (SI) train A with train B OOS;
  • auxiliary building ventilation; and,
  • component cooling water (CCW) train A.

The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures and system diagrams to determine the appropriate system lineup. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers, and entered them into the CAP with the appropriate significance characterization.

Documents reviewed are listed in the Attachment to this report.

These activities constituted five partial system walkdown samples as defined in IP 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Routine Resident Inspector Tours

a. Inspection Scope

The inspectors conducted fire protection (FP) walkdowns, which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant fire zones:

  • fire zone AX-30, relay room and loft;
  • fire zone AX-32 cable spreading room;
  • fire zones TU-92 and TU-93, diesel generator (DG) 1B and day tank rooms;
  • fire zone TU-95B, switchgear bus 1-61 and 1-62 room and AFW area; and,

The inspectors reviewed areas to assess if the licensee had implemented an FP program that adequately controlled combustibles within the plant, effectively maintained fire detection and suppression capability, maintained passive FP features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable FP equipment, systems, or features, in accordance with the licensees fire plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the Attachment to this report, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP. Documents reviewed are listed in the Attachment to this report.

These activities constituted five quarterly fire protection inspection samples as defined in IP 71111.05-05.

b. Findings

No findings were identified.

1R07 Triennial Heat Sink Performance

.1 Triennial Review of Heat Sink Performance

a. Inspection Scope

The inspectors reviewed operability determinations, completed surveillances, vendor manual information, associated calculations, performance test results, and inspection results associated with the battery room B cooler and SW system. These components were chosen based on their risk significance in the licensees probabilistic safety analysis, their important safety-related (SR) mitigating system support functions, and their operating history.

For the selected cooler, the inspectors reviewed testing, inspection, maintenance, and monitoring of biotic fouling and macrofouling programs relied upon to ensure proper heat transfer. This was accomplished by verifying:

(1) the selected test method was consistent with accepted industry practices, or equivalent;
(2) the test conditions were consistent with the selected methodology; and
(3) the test acceptance criteria were consistent with the design basis values. In addition, the inspectors reviewed the results of heat exchanger performance testing and verified that the test results appropriately considered:
(1) differences between testing conditions and design conditions; and
(2) test instrument inaccuracies. The inspectors also verified trending of test results to confirm the test frequency was sufficient to detect degradation prior to loss of heat removal capabilities below design basis values. In addition, the inspectors verified that the condition and operation of the heat exchangers were consistent with design assumptions in heat transfer calculations and applicable descriptions in the USAR.

The inspectors verified the structural integrity of the underwater ultimate heat sink (UHS), SR SW system, and their subcomponents such as piping, intake screens, pumps, and valves, by reviewing tests or other equivalent methods used to ensure availability to in-plant cooling water systems. The inspectors reviewed completed surveillances, associated calculations, chemistry monitoring program, sedimentation/fouling monitoring procedures, CRs, and WOs to assess the condition of the UHS and SW system. In addition, the inspectors conducted walkdowns of the SW intake and discharge structures and the SW pump rooms to assess the general condition of the system.

The inspectors also reviewed design changes associated to the UHS and SR SW system and assessed their impact to procedures relied upon to mitigate the loss of either the UHS or the SW system. Also, the inspectors reviewed documentation associated with the monitoring of pump performance for potential strong-pump vs. weak-pump interaction. In addition, the inspectors reviewed CRs related to heat exchanger and heat sink performance issues to assess the licensees threshold for identifying issues and to evaluate the effectiveness of the corrective actions.

These inspection activities constituted two triennial heat sink inspection samples as defined in IP 71111.07-05.

b. Findings

No findings were identified.

1R08 Inservice Inspection (ISI) Activities

From April 9 through 19, 2012, the inspectors conducted a review of the implementation of the licensees Inservice Inspection (ISI) Program for monitoring degradation of the reactor coolant system (RCS), SG tubes, emergency feedwater systems, risk-significant piping and components, and containment systems.

The inspections described in Sections 1R08.1, 1R08.2, R08.3, IR08.4, and 1R08.5 below constituted one inservice inspection sample as defined in IP 71111.08-05.

.1 Piping Systems Inservice Inspection

a. Inspection Scope

The inspectors observed the following non-destructive examinations mandated by the ASME Code, Section XI, to evaluate compliance with the ASME Code, Sections XI and V requirements; and if any indications and defects were detected, to determine if these were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement.

  • ultrasonic examination (UT) of a Class 2, 3-inch pipe-to-elbow weld, AFW-W120, AFW line;
  • UT of a Class 2, 3-inch elbow-to-pipe weld, AFW-W121, AFW line;
  • magnetic particle examination (MT) of a Class 2, 3-inch pipe-to-elbow weld, AFW-W120, AFW line;
  • MT of a Class 2, 3-inch pipe-to-elbow weld, AFW-W121, AFW line;
  • visual testing (VT) -3 of a Class 3 SW pump (APSW-1A1) supports, APSW-1A1-SI; and,
  • VT -3 of a Class 3 SW pump (APSW -1A2) supports, APSW-1A2-SI.

During the prior outage non-destructive surface and volumetric examinations, the licensee did not identify any relevant/recordable indications. Therefore, no NRC review was completed for this inspection procedure attribute.

The inspectors reviewed the following pressure boundary welds completed for risk significant systems since the beginning of the last refuelling outage to determine if the licensee applied the pre-service non-destructive examinations and acceptance criteria required by the Construction Code and ASME Code, Section XI. Additionally, the inspectors reviewed the welding procedure specification and supporting weld procedure qualification records to determine if the weld procedure was qualified in accordance with the requirements of Construction Code and the ASME Code, Section IX.

  • ISIM-891-2/AFW-W201 and W202, AFW 3-inch pipe-to-valve and valve-to-pipe welds code class 2; and,
  • RHR system welds 50, 51 and 52, 2-inch sock-o-let, 2-inch insert socket weld to 3/4-inch relief valve RHR 701, ASME Code, Class 2.

b. Findings

No findings were identified.

.2 Reactor Pressure Vessel Upper Head (RPVUH) Penetration Inspection Activities

a. Inspection Scope

No exams were required this outage. Therefore, no NRC review was completed for this inspection procedure attribute.

b. Findings

No findings were identified.

.3 Boric Acid Corrosion Control

a. Inspection Scope

On April 6, 2011, the inspectors observed the licensee staff performing VT examinations of the RCS within containment to determine if these examinations focused on locations where boric acid (BA) leaks can cause degradation of safety significant components.

The inspectors reviewed the following licensee evaluations of RCS components with BA deposits to determine if degraded components were documented in the CAP. The inspectors also evaluated corrective actions for any degraded RCS components to determine if they met the component Construction Code, ASME Code, Section XI, and/or NRC-approved alternative.

  • boric acid evaluation (BAE) CR419401; RC-402, Sampling System; April 7, 2011;
  • BAE CR415609; FE-27136, RHR, HX 1A/1B to Penetrations 10, 48, and RHR-SFP Interconns; March 18, 2011; and,
  • BAE CR418730; 6-inch Valve ICS-7A, Containment Spray Pump 1A Discharge Piping to Pen. 29N; March 26, 2011.

The inspectors reviewed the following corrective actions related to evidence of BA leakage to determine if the corrective actions completed were consistent with the requirements of the ASME Code, Section XI, and 10 CFR Part 50, Appendix B, Criterion XVI.

  • CR416828, Light Dry White Boric Acid Residue on No. 1 RCP Seal Housing Bolts, February 28, 2011.

b. Findings

No findings were identified.

.4 Steam Generator Tube Inspection Activities

a. Inspection Scope

No examination was required pursuant to the TSs and none was conducted during the current refueling outage (RFO). Therefore, no NRC review was completed for this inspection procedure attribute.

b. Findings

No findings were identified.

.5 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI-related problems entered into the licensees CAP and conducted interviews with licensee staff to determine if:

  • the licensee had established an appropriate threshold for identifying ISI-related problems;
  • the licensee had performed a root cause (if applicable) and taken appropriate corrective actions; and,
  • the licensee had evaluated operating experience and industry generic issues related to ISI and pressure boundary integrity.

The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. Documents reviewed are listed in the Attachment to this report.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification

a. Inspection Scope

On June 25, 2012, the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification training to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan (EP) actions and notifications.

The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program simulator sample as defined in IP 71111.11.

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Observation of Heightened Activity or Risk

a. Inspection Scope

On April 8, 2012, the inspectors observed the Control Room observation of reactor coolant system (RCS) draindown from the pressurizer to 6 inches below the reactor vessel flange. This was an activity that required heightened awareness or was related to increased risk. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of procedures;
  • control board and equipment manipulations; and
  • oversight and direction from supervisors.

The performance in these areas was compared to pre-established operator action expectations, procedural compliance and task completion requirements. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator heightened activity/risk sample as defined in IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated degraded performance issues involving 4160-Volt breaker charging spring motors.

The inspectors verified the licensee's actions to address system performance or condition problems in terms of the following areas, as necessary:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2), or appropriate and adequate goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly maintenance effectiveness sample as defined in IP 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and SR equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • risk assessments for CCW maintenance on May 24; and,
  • risk assessments for EDG testing and SW pump breaker maintenance on June 11.

These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstone. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified that plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Documents reviewed are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted four samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functional Assessments

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • CR478109, Potential Non-Conformance Source Range Detector Sensitivity;
  • OD315, Revision 1, Potential Nonconservative TS Actions For FQ;
  • CR468976, Accumulator Leak Rate Test Procedures M&TE Inaccuracy Extent Of Condition; and,
  • CR475077, Potential Inconsistency Between Locked Rotor Accident Analysis And EOP ES.

The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and USAR to the licensees evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee had identified and corrected any deficiencies associated with operability evaluations. Documents reviewed are listed in the to this report.

This operability inspection constituted four samples as defined in IP 71111.15-05.

b. Findings

No findings were identified.

1R18 Plant Modifications

.1 Plant Modifications

a. Inspection Scope

The inspectors reviewed the following modifications:

The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety evaluation screening against the design basis, the USAR, and the TSs, as applicable, to verify that the modification did not affect the operability or availability of the affected systems. The inspectors, as applicable, observed ongoing and completed work activities to ensure that the modifications were installed as directed and consistent with the design control documents; the modifications operated as expected; post-modification testing adequately demonstrated continued system operability, availability, and reliability; and that operation of the modifications did not impact the operability of any interfacing systems. As applicable, the inspectors verified that relevant procedure, design, and licensing documents were properly updated. For commercial grade dedications, the inspectors also reviewed the appropriateness of the critical characteristics selected for the dedication process and verified that the licensees testing or acceptance method for the critical characteristics was appropriate. Documents reviewed are listed in the to this report.

This inspection constituted two temporary modification samples as defined in IP 71111.18-05.

b. Findings

Failure to Utilize Work Instructions For An NRC-Approved Piping Code Repair

Introduction:

A finding of very low safety significance and associated NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the failure to accomplish TMOD 2012-11 in accordance with WO KW100894696 and the associated weld data sheet and map. Specifically, licensee personnel failed to utilize the WO instructions, weld data sheet, and weld map when welding a temporary NRC-approved clamp on ASME Code, Class 2 RHR piping. The failure to use the required documentation to perform the work resulted in the worker creating a second through wall leak on the ASME Code, Class 2 RHR piping upstream of valve RHR-600.

Description:

On April 25, 2012, with the reactor in Mode 5, the licensee identified dry white BA accumulated around a socket weld upstream of RHR valve RHR-600 and initiated CR472226. Valve RHR-600 was located in the auxiliary building on the common discharge piping for the RHR system to the reactor for decay heat removal when the plant was shut down. On April 27, 2012, while removing the dry BA, a pinhole leak was discovered with a constant spray in the toe of the socket weld (the weld starting and stopping point) where the 3/4-inch RHR pipe from valve RHR-600 was welded to the sock-o-let for the larger diameter common discharge piping for the RHR system to the reactor. The licensee initiated CR472654, and the Shift Manager declared both trains of RHR inoperable due to the through wall leak on ASME Code, Class 2 piping and entered the TS Action Condition 3.4.7.C, which required the licensee to restore operability immediately.

Initially, on April 27, 2012, the licensee believed they could implement the ASME Boiler and Pressure Vessel Code, Section XI, 1998 Edition, 2000 Addenda, IWA-4133, which allowed the use of a mechanical clamping device to repair pressure boundary piping in accordance with ASME Code, Section XI, Appendix IX. However, the inspectors noted to the licensee that ASME Code, Section XI, Appendix IX, Article IX-1000(c)(2), stated that clamping devices shall not be used on portions of a piping system that forms the containment boundary. The inspectors also noted that the USAR Table 5.2-3, Reactor Containment Vessel Penetrations, listed valve RHR-600 as the outside containment barrier for Penetration Number 10, and the newly discovered leak was upstream of this containment isolation valve (CIV). The licensee concurred and pursued a proposed alternative to the code through a temporary deviation to the Code, which required prior NRC approval.

The licensee held conference calls with the NRC on April 28 and April 29, regarding the licensees proposed alternative. On April 29, the licensee submitted Request No. RR-2-3 (ADAMS Accession No. ML12122A138) seeking NRCs approval to install a clamp on the leak, transition to Mode 4 to isolate the leak while allowing one train of RHR to be operable for injection, and then implementing the permanent repair prior to transitioning to Mode 3. At approximately 1:30 a.m. on April 30, 2012, the NRC verbally approved the licensees implementation of proposed alternative Request No. RR-2-3.

Shortly thereafter, the licensee commenced installation of the clamping device described in TMOD 2012-11 via WO KW100894696.

Work progressed successfully with installation of the clamping device and injection of sealant into the clamp to minimize leakage. The last remaining step to complete WO KW100894696 was to perform a fillet weld on the top of the clamp to the pipe. The welders were briefed, and 45 minutes prior to the end of their shift, work commenced on the final WO step to fillet weld the clamp to the 3/4-inch pipe. As the welder struck an arc to make the initial weld puddle, he noted that water started spraying from the pipe and notified another worker that conditions had changed and they needed to leave the area.

Non-destructive examination personnel immediately confirmed that a second through-wall leak was created when the welder burned through the 3/4-inch pipe.

The inspectors conducted interviews with several licensee personnel involved with the work following the incident and reviewed the associated WO for implementation of TMOD 2012-11. As a result of the interviews and review of the associated documentation, the inspectors concluded the following facts had occurred:

  • the welder believed he was welding on Schedule 80 pipe at minimal system pressure and adjusted his equipment for this pipe thickness, when in fact the 3/4-inch pipe was Schedule 40 (half the wall thickness) and the system was at approximately 350 pounds per square inch gauge (psig);
  • the welder stated that had he known the system pressure was high, regardless of pipe schedule, he would not have attempted a weld;
  • the welder and those interviewed that were at the pre-job brief did not review the WO, weld sheet and weld map; and those documents were not covered in detail at the pre-job brief;
  • the weld area was not cleaned prior to the start of the weld within 2 inches of the weld area as the WO stated, and this was not corrected by either the welder or the Quality Control representative;
  • according to the licensees procedures on welding, this particular weld and the weld sheet were required to be designated as a critical weld and were not; therefore, additional required information was not indicated on the weld sheet;
  • the welder and those at the pre-job brief thought this was a seal weld vice a fillet weld, which the WO, weld data sheet and weld map required; and,
  • inspectors also questioned why this activity wasnt treated as an infrequent, complex or critical evolution brief, vice a normal pre-job brief.

Therefore, based on the inspectors interviews of personnel and documentation review, the inspectors concluded that the licensee personnel performing the work, including supervisors, failed to conduct an adequate pre-job brief and did not conduct the work in accordance with the approved WO instructions, weld sheet and weld map. Interviews conducted by the licensee as part of the event investigation corroborated the inspectors assessment.

Analysis:

The inspectors determined that the failure to utilize the WOs and associated documentation to execute the work was contrary to 10 CFR Part 50, Appendix B, Criterion V, and was a performance deficiency warranting a significance evaluation.

The finding was determined to be more than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated December 24, 2009, because the finding was associated with the Mitigating Systems Cornerstone attribute of human error (pre-event) and adversely affected the cornerstone objective to ensure the reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the failure to utilize the approved WO resulted in the creation of a second through wall leak in ASME Code, Class 2 common RHR discharge piping upstream of valve RHR-600 that was unisolable in the current mode of operation.

The inspectors determined that the finding could be evaluated in accordance with IMC 0609, Appendix G, Shutdown Operations SDP, dated February 28, 2005.

The inspectors used Checklist 1, PWR Hot Shutdown Operation: Time to Core Boiling

<2 Hours, contained in Attachment 1 and determined that the finding affected core heat removal guidelines I.B(1), Procedures, and I.C(2), Equipment. The inspectors screened the finding as very low safety significance (Green) because it did not degrade the licensees ability to establish an alternate core cooling path if decay heat removal could not be re-established and, therefore, did not require a phase 2 or phase 3 analysis.

This finding has a cross-cutting aspect in the area of human performance, resources, because the licensee did not ensure supervisory and management oversight of work activities, including contractors, such that nuclear safety was supported. Specifically, the inspectors identified that the pre-job brief conducted by supervision and management for this work did not include a review of the WO, weld sheet, or weld map and did not convey accurate information regarding the significance of the activity, the type of weld to be performed and the system conditions where the weld was performed (H.4(c)).

Enforcement:

Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

Contrary to the above, on April 30, 2012, the licensee failed to accomplish TMOD 2012-11 on ASME Code, Class 2 RHR piping upstream of valve RHR-600, an SR component, in accordance with WO KW100894696 and the associated weld data sheet and map. Specifically, licensee personnel failed to utilize the weld data sheet, weld map, and WO instructions when welding a temporary clamp on ASME Code, Class 2 RHR piping, which resulted in the creation of a second through wall leak on the ASME Code, Class 2 RHR piping upstream of valve RHR-600. Because this violation was of very low safety significance and it was entered into the licensees CAP as CR472915, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000305/2012003-01; Failure to Utilize Work Order for Temporary Weld Repair on ASME Code, Class 2 Piping).

On May 5, 2012, the licensee permanently corrected both through wall leaks on the RHR system piping without incident following the NRC approval of a second proposed alternative in Request No. RR-2-4, dated May 3, 2012 (ADAMS Accession No. ML12125A279) and supplemented on May 4, 2012 (ADAMS Accession No. ML12129A279). At the end of the inspection period, the licensee continued to perform an ACE to determine the causes for the organizational failures that occurred.

1R19 Post-Maintenance Testing

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance testing (PMT) activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:

  • fan coil unit (FCU) A PMT following coil replacement, CR468367, FCU AFW Pump A on April 10;
  • SW pump breaker testing after breaker lockout relay maintenance on June 11;
  • MPM-CRN-006, Auxiliary Building Crane Main and Auxiliary Host Lower Block;
  • SI pump run after inspect/clean/megger of motor;
  • OP-KW-STP-FW-001, Fast Bus Transfer Feedwater Pump Circuit Special Test Procedure on April 12;
  • SOP-AFW-05B-30, Turbine-Driven Auxiliary Feedwater Pump Curve Development and Cavitation Venturi Calibration on May 7; and,
  • Troubleshooting of SI Pump Suction Void on June 27.

These activities were selected based upon the SSCs ability to impact risk. The inspectors evaluated these activities for the following, as applicable: the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing; temporary modifications or jumpers required for test performance were properly removed after test completion; and test documentation was properly evaluated. The inspectors evaluated the activities against documents such as TSs, USAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications, to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with PMTs to determine whether the licensee had identified problems and entered them in the CAP, and that the problems were corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted seven post-maintenance testing samples as defined in IP 71111.19-05.

b. Findings

No findings were identified.

1R20 Outage Activities

.1 Refueling Outage Activities

a. Inspection Scope

The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the RFO, conducted April 6, 2012, through May 13, 2012, to confirm that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth.

During the RFO, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage activities listed below:

  • licensee configuration management, including maintenance of defense-in-depth commensurate with the OSP for key safety functions and compliance with the applicable TS when taking equipment out of service;
  • implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing;
  • installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error;
  • controls over the status and configuration of electrical systems to ensure that TS and OSP requirements were met, and controls over switchyard activities;
  • controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system;
  • reactor water inventory controls including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss;
  • controls over activities that could affect reactivity;
  • licensee fatigue management, as required by 10 CFR 26, Subpart I;
  • refueling activities, including fuel handling and sipping to detect fuel assembly leakage;
  • startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing; and,
  • licensee identification and resolution of problems related to RFO activities.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one RFO sample as defined in IP 71111.20-05.

b. Findings

Loose Cable Clamp Caused Loaded Spent Fuel Upender to Unintentionally Lower

Introduction:

A finding of very low safety significance (Green) and associated NCV of TS 5.4.1, Procedures, was self-revealed because procedure MCM-FH-001, Repair of the Fuel Transfer System, was inadequate. Specifically, the procedure did not contain torque specifications for tightening the upender frame cable clamps and, on April 23, the cable for the spent fuel pool upender slipped through the cable clamps and allowed the upender containing a fuel assembly to descend approximately 12 inches.

Description:

On April 23, while refueling the reactor, the licensee loaded a fuel assembly into the SFP upender. While lowering the upender from the vertical position to the horizontal position, the licensee received an underload alarm light for the SFP upender.

The licensee appropriately stopped work, and identified that the cable had slipped through two cable clamps and was no longer attached to the upender frame. The licensee transferred the fuel assembly to the reactor side, where it was inspected satisfactorily and placed in the appropriate location in the core. Further investigation by the licensee determined that procedure MCM-FH-001 did not contain the 45-foot-pound torque specification for the upender cable clamps; and when the licensee replaced the cables in February 2012, utilizing procedure MCM-FH-001, they did not tighten the cable clamps to the appropriate torque recommended by the vendor. The licensee repaired the cable and reloaded the core without further incident.

The licensee identified that a procedure change had been submitted for procedure MCM-FH-002, Fuel Handling Equipment Maintenance to include the 45-foot-pound torque checks as part of the upender inspection; however, the procedure change was considered an enhancement and was still waiting to be implemented when the upender failure occurred in April. The licensee determined that even if procedure MCM-FH-002 had been updated prior to the January inspection that it would not have prevented the incident because the inspection in procedure MCM-FH-002 was not required to be re-performed after the cable replacement using procedure MCM-FH-001 in February.

The licensee placed procedure MCM-FH-001 on administrative hold to prevent its use until it could be updated with the appropriate torque specifications. The licensee was performing an ACE at the conclusion of this inspection period.

Analysis:

The inspectors determined that not having the appropriate torque specifications in procedure MCM-FH-001 was a performance deficiency warranting a significance evaluation. The finding was determined to be more than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated December 24, 2009, because, if left uncorrected, the finding had the potential to lead to a more significant safety concern. Specifically, the upender containing the fuel assembly could have fallen from the near-full vertical position to the horizontal position during the approximate 220 previous upender cycles. The inspectors concluded this finding was associated with the Barrier Integrity Cornerstone. The inspectors evaluated the finding by applying the SFP questions in the Fuel Barrier column of Table 4a, located in IMC 0609, Attachment 4, dated January 10, 2008. The inspectors answered "No" to all three questions and determined that the finding was of very low safety significance (Green).

The finding has a cross-cutting aspect in the areas of problem identification and resolution, operating experience (OE), because the licensee failed to communicate to affected internal stakeholders in a timely manner relevant external OE. Specifically, the licensee failed to discuss available and relevant OE related to the failure to appropriately torque cable clamps on a SFP upender (P.2(a)).

Enforcement:

The TS Section 5.4.1, Procedures, requires, in part, that written procedures shall be implemented covering the applicable procedures recommended in Regulatory Guide (RG) 1.33, Revision 2, Appendix A, dated February 1978. The RG 1.33, Appendix A, Paragraph 9.c, states, in part, that procedures for the repair or replacement of equipment should be prepared prior to beginning work. The licensee established procedure MCM-FH-001, Repair of the Fuel Transfer System, as an implementing procedure for repair the SFP upender.

Contrary to the above, from February 7, 2008 through April 23, 2012, procedure MCM-FH-001 was inadequate. Specifically, Step 5.3.1.f did not contain torque specifications for tightening the upender frame cable clamps. Because this violation was of very low safety significance and it was entered into the licensees CAP as CR471928, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000305/2012003-02; Loose Cable Clamp Caused Loaded Spent Fuel Upender to Unintentionally Lower).

The licensee placed procedure MCM-FH-001 on administrative hold to prevent its use until it could be updated with the appropriate torque specifications, and confirmed that no damage occurred to the fuel assembly. The licensee consulted with the fuel vendor who performed analysis to demonstrate the fuel assembly was acceptable for use. At the end of this inspection period, the licensee was performing an ACE to determine the causes of the event, and developing corrective actions.

1R22 Surveillance Testing

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • OP-KW-OSP-RHR-002A, RHR pump A full test at refueling shutdown on April 10 (IST);
  • OSP-DGE-004B, EDG B elevated load and load rejection test on April 27 (Routine);
  • OP-KW-OSP-AFW-002, TDAFW pump full flow on May 7 (Routine);
  • MA-KW-ISP-RC-017B-1, pressurizer level calibration on May 18 (Routine);
  • OP-KW-OSP-SI-006B, train B SI pump and valve test on May 23 (IST);
  • NF-KW-RET-002, low power physics test on May 23 (Routine); and,
  • SP-55-155A, engineered safeguards train A logic channel test on May 30 (Routine).

The inspectors considered the following test attributes, if applicable, while they observed in-plant activities and reviewed procedures and associated records:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
  • were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;
  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency was in accordance with TSs, the USAR, procedures, and applicable commitments;
  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
  • test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for IST, testing was performed in accordance with the applicable version of ASME code, Section XI, and reference values were consistent with the system design basis;
  • where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
  • where applicable for SR instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
  • where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
  • prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
  • equipment was returned to a position or status required to support the performance of its safety functions; and,
  • all problems identified during the testing were appropriately documented and dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted six routine surveillance testing samples and three inservice testing samples as defined in IP 71111.22, Sections -02 and -05.

b. Findings

No findings were identified.

1EP6 Drill Evaluation

.1 Emergency Preparedness Drill Observations

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on May 17, 2012, and a hostile action base drill on June 19, 2012, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the Emergency Operations Facility on May 17, 2012, and in the simulator and Site Relocation Facility on June 19, 2012, to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the CAP. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment to this report.

These emergency preparedness drill inspections constituted two drill samples as defined in IP 71114.06-05.

b. Findings

No findings were identified.

RADIATION SAFETY

2RS1 Radiological Hazard Assessment and Exposure Controls

This inspection constituted a partial sample as defined in IP 71124.01-05.

.1 Radiological Hazard Assessment (02.02)

a. Inspection Scope

The inspectors reviewed the radiological surveys from selected plant areas and evaluated whether the thoroughness and frequency of the surveys where appropriate for the given radiological hazard.

The inspectors conducted walkdowns of the facility, including radioactive waste processing, storage, and handling areas to evaluate material conditions and performed independent radiation measurements to verify conditions.

The inspectors selected the following radiologically risk-significant work activities that involved exposure to radiation.

  • transfer canal diving activities;
  • upper internal lift;
  • reactor head lift and set; and,
  • reactor cavity decontamination.

For these work activities, the inspectors assessed whether the pre-work surveys performed were appropriate to identify and quantify the radiological hazard and to establish adequate protective measures. The inspectors evaluated the radiological survey program to determine if hazards were properly identified, including the following:

  • identification of hot particles;
  • the presence of alpha emitters;
  • the potential for airborne radioactive materials, including the potential presence of transuranics and/or other hard-to-detect radioactive materials;
  • the hazards associated with work activities that could suddenly and severely increase radiological conditions and that the licensee has established a means to inform workers of changes that could significantly impact their occupational dose; and,
  • severe radiation field dose gradients that can result in non-uniform exposures of the body.

The inspectors observed work in potential airborne areas and evaluated whether the air samples were representative of the breathing air zone. The inspectors evaluated whether continuous air monitors were located in areas with low background to minimize false alarms and were representative of actual work areas. The inspectors evaluated the licensees program for monitoring levels of loose surface contamination in areas of the plant with the potential for the contamination to become airborne.

b. Findings

No findings were identified.

.2 Instructions to Workers (02.03)

a. Inspection Scope

The inspectors selected various containers holding non-exempt licensed radioactive materials that may cause unplanned or inadvertent exposure of workers, and assessed whether the containers were labeled and controlled in accordance with 10 CFR 20.1904, Labeling Containers, or met the requirements of 10 CFR 20.1905(g), Exemptions To Labeling Requirements.

The inspectors reviewed the following radiation work permits (RWPs) used to access high radiation areas and evaluated the specified work control instructions or control barriers.

  • RWP 12-0306; Diving Evolutions in SFP Transfer Canal and All Support Activities;
  • RWP 12-0255; Refueling Activities; and,
  • RWP 12-0207; Decon, Laundry and Shielding.

For these RWPs, the inspectors assessed whether allowable stay times or permissible dose (including from the intake of radioactive material) for radiologically significant work under each radiation work permit were clearly identified. The inspectors evaluated whether electronic personal dosimeter alarm set-points were in conformance with survey indications and plant policy.

For work activities that could suddenly and severely increase radiological conditions, the inspectors assessed the licensees means to inform workers of changes that could significantly impact their occupational dose.

b. Findings

No findings were identified.

.3 Contamination and Radioactive Material Control (02.04)

a. Inspection Scope

The inspectors observed locations where the licensee monitors potentially contaminated material leaving the radiological control area and inspected the methods used for control, survey, and release from these areas. The inspectors observed the performance of personnel surveying and releasing material for unrestricted use and evaluated whether the work was performed in accordance with plant procedures and whether the procedures were sufficient to control the spread of contamination and prevent unintended release of radioactive materials from the site. The inspectors assessed whether the radiation monitoring instrumentation had appropriate sensitivity for the type(s) of radiation present.

b. Findings

No findings were identified.

.4 Radiological Hazards Control and Work Coverage (02.05)

a. Inspection Scope

The inspectors evaluated ambient radiological conditions (e.g., radiation levels or potential radiation levels) during tours of the facility. The inspectors assessed whether the conditions were consistent with applicable posted surveys, radiation work permits, and worker briefings.

The inspectors evaluated the adequacy of radiological controls, such as required surveys, RP job coverage (including audio and visual surveillance for remote job coverage), and contamination controls. The inspectors evaluated the licensees use of electronic personal dosimeters in high noise areas as high radiation area monitoring devices.

The inspectors assessed whether radiation monitoring devices were placed on the individuals body consistent with licensee procedures. The inspectors assessed whether the dosimeter was placed in the location of highest expected dose or that the licensee properly employed an NRC-approved method of determining effective dose equivalent.

The inspectors reviewed the application of dosimetry to effectively monitor exposure to personnel in high-radiation work areas with significant dose rate gradients.

The inspectors reviewed the following RWPs for work within airborne radioactivity areas with the potential for individual worker internal exposures.

  • RWP 12-0255; Refueling Activities; and,
  • RWP 12-0207; Decon, Laundry, and Shielding.

For these RWPs, the inspectors evaluated airborne radioactive controls and monitoring, including potential for significant airborne levels (e.g., grinding, grit blasting, system breaches, entry into tanks, cubicles, and reactor cavities). The inspectors assessed barrier (e.g., tent or glove box) integrity and temporary high-efficiency particulate air (HEPA) ventilation system operation.

b. Findings

No findings were identified.

.5 Radiation Worker Performance (02.07)

a. Inspection Scope

The inspectors observed radiation worker performance with respect to stated RP work requirements. The inspectors assessed whether workers were aware of the radiological conditions in their workplace and the RWP controls/limits in place, and whether their performance reflected the level of radiological hazards present.

b. Findings

No findings were identified.

.6 Radiation Protection Technician Proficiency (02.08)

a. Inspection Scope

The inspectors observed the performance of the RP technicians with respect to all RP work requirements. The inspectors evaluated whether technicians were aware of the radiological conditions in their workplace and the RWP controls/limits, and whether their performance was consistent with their training and qualifications with respect to the radiological hazards and work activities.

b. Findings

No findings were identified.

2RS2 Occupational As-Low-As-Is-Reasonably-Achievable (ALARA) Planning and

Controls (71124.02) This inspection constituted a partial sample as defined in IP 71124.02-05.

.1 Radiological Work Planning (02.02)

a. Inspection Scope

The inspectors selected the following work activities of the highest exposure significance.

  • diving evolutions in SFP Xfer canal and all support activities;
  • refueling activities; and,
  • decon, laundry, and shielding.

The inspectors reviewed the ALARA work activity evaluations, exposure estimates, and exposure mitigation requirements. The inspectors determined whether the licensee reasonably grouped the radiological work into work activities, based on historical precedence, industry norms, and/or special circumstances.

The inspectors assessed whether the licensees planning identified appropriate dose mitigation features; considered alternate mitigation features; and defined reasonable dose goals. The inspectors evaluated whether the licensees ALARA assessment had taken into account decreased worker efficiency from use of respiratory protective devices and/or heat stress mitigation equipment (e.g., ice vests). The inspectors determined whether the licensees work planning considered the use of remote technologies (e.g., teledosimetry, remote visual monitoring, and robotics) as a means to reduce dose and the use of dose reduction insights from industry operating experience and plant-specific lessons learned. The inspectors assessed the integration of ALARA requirements into work procedure and radiation work permit documents.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

This inspection constituted a partial sample as defined in IP 71124.03-05.

.1 Engineering Controls (02.02)

a. Inspection Scope

The inspectors reviewed airborne monitoring protocols by selecting installed systems used to monitor and warn of changing airborne concentrations in the plant and evaluated whether the alarms and setpoints were sufficient to prompt licensee/worker action to ensure that doses are maintained within the limits of 10 CFR Part 20 and the as-low-as-is-reasonably-achievable concept.

The inspectors assessed whether the licensee had established trigger points (e.g., the Electric Power Research Institutes (EPRIs) Alpha Monitoring Guidelines for Operating Nuclear Power Stations) for evaluating levels of airborne beta-emitting (e.g.,

plutonium-241) and alpha-emitting radionuclides.

b. Findings

No findings were identified.

.2 Use of Respiratory Protection Devices (02.03)

a. Inspection Scope

For those situations where it is impractical to employ engineering controls to minimize airborne radioactivity, the inspectors assessed whether the licensee provided respiratory protective devices such that occupational doses are ALARA. The inspectors selected work activities where respiratory protection devices were used to limit the intake of radioactive materials, and assessed whether the licensee performed an evaluation concluding that further engineering controls were not practical and that the use of respirators is ALARA. The inspectors also evaluated whether the licensee had established means (such as routine bioassay) to determine if the level of protection (protection factor) provided by the respiratory protection devices during use was at least as good as that assumed in the licensees work controls and dose assessment.

The inspectors selected several individuals assigned to wear a respiratory protection device and observed them donning, doffing, and functionally checking the device as appropriate. Through interviews with these individuals, the inspectors evaluated whether they knew how to safely use the device and how to properly respond to any device malfunction or unusual occurrence (loss of power, loss of air, etc.).

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness

4OA1 Performance Indicator Verification

.1 Mitigating Systems Performance Index - Emergency AC Power System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - Emergency Alternating Current (AC) Power System performance indicator (PI) for the period from the second quarter 2011 through the first quarter 2012.

To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the licensees operator narrative logs, MSPI derivation reports, CRs, and event reports from the second quarter 2011 through the first quarter 2012 to validate the accuracy of the submittals. The inspectors also reviewed the licensees CAP to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI emergency AC power system sample as defined in IP 71151-05.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index - High Pressure Injection System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - High Pressure Injection System PI for the period from the second quarter 2011 through the first quarter 2012.

To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the licensees operator narrative logs, CRs, MSPI derivation reports, and event reports from the second quarter 2011 through the first quarter 2012 to validate the accuracy of the submittals. The inspectors also reviewed the licensees CAP to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the to this report.

This inspection constituted one MSPI high pressure injection system sample as defined in IP 71151-05.

b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index - Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for the period from the second quarter 2011 through the first quarter 2012. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the licensees operator narrative logs, CRs, MSPI derivation reports, and event reports from the second quarter 2011 through the first quarter 2012 to validate the accuracy of the submittals. The inspectors also reviewed the licensees CAP to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI heat removal system sample as defined in IP 71151-05.

b. Findings

No findings were identified.

.4 Mitigating Systems Performance Index - Residual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI -RHR System PI for the period from the second quarter 2011 through the first quarter 2012. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the licensees operator narrative logs, CRs, MSPI derivation reports, and event reports from the second quarter 2011 through the first quarter 2012 to validate the accuracy of the submittals. The inspectors also reviewed the licensees CAP to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI residual heat removal system sample as defined in IP 71151-05.

b. Findings

No findings were identified.

.5 Mitigating Systems Performance Index - Cooling Water System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Cooling Water System PI for the period from the second quarter 2011 through the first quarter 2012. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the licensees operator narrative logs, CRs, MSPI derivation reports, and event reports from the second quarter 2011 through the first quarter 2012 to validate the accuracy of the submittals. The inspectors also reviewed the licensees CAP to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI cooling water system sample as defined in IP 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed included: identification of the problem was complete and accurate; timeliness was commensurate with the safety significance; evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent-of-condition reviews, and previous occurrences reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations are included in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a screening of items entered into the licensees CAP. This review was accomplished through inspection of the stations daily CR packages.

These daily reviews were performed by procedure as part of the inspectors daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue.

The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.2, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the 6-month period of December 2011 through May 2012, although some examples expanded beyond those dates where the scope of the trend warranted.

The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

This review constituted one semi-annual trend inspection sample as defined in IP 71152-05.

b. Findings

No findings were identified.

.4 Selected Issue Follow-up Inspection: Corrective Actions to Address NCV

05000305/2006016-05, Acceptability of Cable Spreading Area Suppression System

a. Inspection Scope

During a routine FP walkdown in the cable spreading area (fire area AX-32), the inspectors questioned the adequacy of the fire suppression system. The inspectors determined that the NRC had previously issued NCV 05000305/2006016-05 for an inadequate fire suppression system in the area. As a result, the inspectors reviewed the licensees corrective actions addressing the NCV. Documents reviewed are listed in the to this report.

This review constituted one in-depth problem identification and resolution sample as defined in IP 71152-05.

b. Findings

Failure to Provide Adequate Suppression in Cable Spreading Area

Introduction:

The inspectors identified a finding of very low safety significance (Green)and associated NCV of 10 CFR Part 50, Appendix R, Section III.G.3, for the licensees failure to provide adequate fire suppression coverage for fire zone AX-32. Specifically, the licensee failed to provide required fire suppression coverage for safe shutdown functions of source range monitoring, isolation of a SG blowdown line, and pressurizer level instrumentation in the cable spreading area.

Description:

Fire zone AX-32 included the cable spreading area and the RP office and associated facilities. The cable spreading area is located at the 616-foot elevation of the auxiliary building directly above the RP office. The floor of the cable spreading area consists of 20-gauge metal decking. The inspectors determined that a potential fire in the RP office could present a fire hazard to safe shutdown cables located in the cable spreading area.

Fire zone AX-32 contained both trains of safe shutdown cables and the requirements of 10 CFR Part 50, Appendix R, Section III.G.3, were applicable to the area. As a result the area was required to have fire detection and a fixed fire suppression system installed. The cable spreading area had a wet-pipe suppression system designed to protect a number of cable trays in the cable spreading area. However, the inspectors identified three safe shutdown functions with redundant cable trains located in fire zone AX-32 that lacked fire suppression. Adequate suppression was not provided for cables associated with source range flux monitoring, isolation of the SG B blowdown line, and pressurizer level indication. The inspectors were concerned that a fire in the cable spreading area or in the RP office could damage safe shutdown cables in the cable spreading area. The RP office area contained fire detection but no suppression system in the main portion of the office area.

The NRC had previously documented an NCV associated with the inadequacy of the suppression system in 2006 (IR 05000305/2006016, ADAMS Accession Number ML070260124). In response to the NCV, the licensee revised the Fire Prevention Tour procedure (FPP-08-12) Section 5.3.t, to maintain the cable spreading area free of transient combustibles unless an evaluation was performed by Fire Protection Engineering. In addition, Section 5.3.u of the procedure specified that the RP office area shall maintain combustible materials ALARA. The licensee replaced numerous open bookshelves in the RP office with enclosed bookshelves. In addition, the licensee issued CA072147, Initiate Modification to Provide Additional Suppression Coverage for the HP Area, on April 9, 2008, to install a fire suppression system in the RP office.

However, the licensee determined in June 2009, as documented in CA072147, that the installation of additional fire suppression in the RP office was an enhancement and should be tracked on the Plant Health Improvement List. The licensees CAP documented on June 25, 2009, that all assignments were complete for CA072147. As a result of the classification of the modification as an enhancement the modification had not been approved by the site as of June 30, 2012.

The licensee also requested a vendor to perform a fire modeling evaluation of the suppression system in the cable spreading area (EPM Report No. P1919-023-002, Review of Cable Spreading Room Suppression, Revision 0). The fire modeling evaluation considered various fire sizes in the RP office and their impact on cables in the cable spreading area. The evaluation showed that a 2.5 megawatt (MW) fire would not damage cables, but that a 7 MW fire could. The fire sizes were chosen based on a review of fire test studies and the combustibles present in the RP office. The damage to the cables would occur due to excessive heat flux as a result of failure of the 20-gauge metal decking. The vendor determined that a 7 MW fire could result in the cables being subjected to heat flux values upwards of 21.5 kilowatts per meter squared (kW/m2). The damage threshold for thermoset cables (cables of concern were thermoset cables) is 11 kW/m2 as documented in NUREG/CR-6850, Fire PRA Methodology for Nuclear Power Facilities.

The vendor provided several recommendations for the licensee to consider in addressing the potential fire hazards:

  • installation of an automatic sprinkler system in compliance with National Fire Protection Association (NFPA) standard for the installation of sprinkler systems (NFPA 13).
  • modification of the fire suppression in the cable spreading area or administrative controls for minimizing transient combustibles in the cable spreading area, and
  • reduction of combustibles in the RP office area.

The licensees completed corrective actions did not include the installation of a fire suppression system in the RP office or a modification of the suppression system in the cable spreading area. The inspectors reviewed the vendors fire modeling evaluation and did not identify any concerns.

Subsequently, the licensee performed evaluation FPEE-049, Adequacy of Partial Area Suppression/Detection, Revision 5, in accordance with Generic Letter 86-10, Implementation of Fire Protection Requirements. The licensee determined that the, evaluation of the in-situ combustibles in the radiation protection office on El. 606-foot found that, realistically, the expected heat release rate for a fire in the area would be bounded by the 2.5 MW fire scenarios analyzed in the Fire Dynamics Simulator (FDS)models. As previously discussed, the fire modeling evaluation determined that cable damage would not occur with a 2.5 MW fire in the RP office. The licensee further concluded that, administrative controls have been established to provide assurance that the level of combustibles in AX-32 will be maintained at acceptable levels.

The inspectors performed walkdowns of fire zone AX-32 during this inspection period and expressed concerns with the amount of in-situ combustibles located in the RP office.

The inspectors pointed out to the licensee that at least one workstation in the RP office appeared to contain a higher amount of combustible materials than a workstation in a referenced study. The National Institute of Standards and Technology (NIST) published a study, NIST Special Publication SP-1021, documenting a two-sided workstation that developed a 3.3 MW fire. This study was referenced in the vendors fire modeling evaluation and the fire size exceeded the licensees bounding fire size of 2.5 MW. The inspectors discussed their concerns with the licensees use of a 2.5 MW bounding fire size in evaluation FPEE-049. The licensee issued CR478600, NRC NCV Proposed for Inadequate Fixed Fire Suppression for Fire Zone AX-32, dated June 12, 2012, and determined that the in-situ combustible loading for the area could produce approximately a 3.5 MW fire. The licensees immediate corrective actions were to designate manual backup from hose stations and implement an hourly fire watch in the RP office.

The inspectors determined that the licensee did not properly consider the impact of transient combustibles in the RP office on the cable spreading area above. As a result, after the initial licensee efforts to reduce the in-situ combustibles in the RP office the amount of combustible materials increased until the time of the inspectors observations during this inspection period.

Analysis:

The inspectors determined that failure to provide adequate fire suppression coverage for fire zone AX-32 was contrary to 10 CFR Part 50, Appendix R, Section III.G.3, and was a performance deficiency. Specifically, the licensee failed to provide fixed fire suppression for redundant cables or equipment located within fire zone AX-32 for source range neutron flux monitoring, isolation of the SG B blowdown line, and pressurizer level indication.

The finding was determined to be more than minor because it was associated with the Mitigating Systems Cornerstone attribute of Protection Against External Factors (Fire)and affected the cornerstone objective of ensuring the capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).

Specifically, the failure to provide suppression for redundant trains of safe shutdown equipment increased the likelihood that alternative shutdown methods would have to be used in the event of a fire.

In accordance with IMC 0609, Significance Determination Process, 0609.04, Phase 1 - Initial Screening and Characterization of Findings, Table 3b, the inspectors determined the finding degraded the FP defense-in-depth strategies. Therefore, screening under IMC 0609, Appendix F, Fire Protection Significance Determination Process, was required. The inspectors determined that the finding impacted the Fixed FP Systems category.

Based on review of IMC 0609, Appendix F, Attachment 2, Degradation Rating Guidance Specific to Various Fire Protection Program Elements, the inspectors determined the degradation rating to be high because the existing wet-pipe water spray system did not protect both trains of safe-shutdown equipment. The duration factor was 1.0, based on the duration of the degradation being greater than 30 days per Table 1.4.1, Duration Factors.

An overall fire frequency of 1.7E-3 per year was assigned based on information from IMC 0609, Appendix F, Attachment 4, Fire Ignition Source Mapping Information: Fire Frequency, Counting Instructions, Applicable Fire Severity Characteristics, and Applicable Manual Fire Suppression Curves, based on the high amount of transient combustibles in the RP office.

The Region III Senior Reactor Analyst (SRA) noted that none of the affected components were explicitly modeled in the Kewaunee Standardized Plant Analysis Risk (SPAR) model. Qualitatively, fire detection and manual fire suppression were available in the vicinity of the affected cable trays. In the event of a fire, it is expected that the detectors will alarm and the fire brigade will respond to extinguish the fire in its incipient stages.

To address the risk quantitatively, the SRA performed a bounding Phase 3 internal events SDP evaluation of the finding using Systems Analysis Programs for Hands-On Integrated Reliability Evaluations (SAPHIRE) Version 8.0.7.18 and the Kewaunee SPAR model (Version 8.20). The SRA performed a Transient initiating event analysis with failure of main steam isolation valve MS-1B to close as a surrogate for the failure of the SG B blowdown line. The result was an estimated conditional core damage probability (CCDP) of 9.35E-8. When the fire frequency was included, the total risk result was significantly less than 1E-6. The dominant SPAR Model sequence involves an anticipated transient without scram (ATWS) sequence. As such, the SRA concluded that the finding be best characterized as having a very low risk significance (Green).

This finding has a cross-cutting aspect in the area of problem identification and resolution, corrective action program, because the licensee did not take appropriate corrective actions to address the inadequate suppression system in fire zone AX-32.

Specifically, the licensee determined in June 2009, that the installation of additional fire suppression in the RP office was an enhancement; and since that time, had not scheduled a modification. In addition, the licensee did not ensure that the amount of in-situ combustibles in the RP office was kept as low as possible. (P.1(d))

Enforcement:

Title 10 CFR 50.48(b)(2) requires, in part, that all nuclear power plants licensed to operate prior to January 1, 1979, must satisfy the applicable requirements of Appendix R to this part, including specifically the requirements of Sections III.G, III.J, and III.O. Appendix R, Section III.G.3 requires, in part, that alternative of dedicated shutdown capability and its associated circuits, independent of cables, systems, or components in the area, room, or zone under consideration should be provided where the protection of systems whose function is required for hot shutdown does not satisfy the requirement of paragraph G.2 of this section. In addition, fire detection and a fixed fire suppression system shall be installed in the area, room, or zone under consideration.

Contrary to the above, from June 30, 2008 until June 30, 2012, the licensee failed to provide adequate fire suppression coverage for fire zone AX-32. Specifically, the licensee failed to provide fixed fire suppression for redundant cables or equipment located within fire zone AX-32 for source range neutron flux monitoring, isolation of the SG B blowdown line, and pressurizer level indication.

Because this violation was of very low safety significance and it was entered into the licensees CAP as CR478600, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000305/2012003-03;; Failure to Provide Adequate Suppression in Cable Spreading Area).

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1 EN47871, Both Trains of RHR Declared Inoperable on April 27, 2012

a. Inspection Scope

The inspectors reviewed the plants response to the discovery of a through wall pipe leak on the common discharge line for RHR on April 27, 2012. Documents reviewed in this inspection are listed in the Attachment to this report.

This event follow-up review constituted one sample as defined in IP 71153-05.

b. Findings

Incorrect Leakage Requirement Submitted For A Proposed Temporary Pipe Clamp

Introduction:

A SL IV NCV of 10 CFR Part 50.9(a), Completeness and Accuracy of Information, was identified by the inspectors for the failure of the licensee to provide complete and accurate information in all material respects to the Commission in licensee Request RR-2-3, dated April 29, 2012 (ADAMS Accession No. ML12122A138). As part of a license amendment for a proposed temporary deviation from the requirements of 10 CFR 50.55a and ASME Code, Section XI, the licensee incorrectly stated the allowable leakage from the temporary clamp in transition from Mode 5 to 4 was governed by TS 5.5.2, Primary Coolant Sources Outside Containment, and proposed an allowable leakage value of 5.5 gph. After licensee Request No. RR-2-3 was verbally approved by the NRC on April 30, 2012, the inspectors and NRC staff determined that the governing leakage requirement was no leakage in Mode 4 for the clamp as required by TS 3.4.13, Reactor Coolant System Operational Leakage.

Description:

On April 25, 2012, with the reactor in Mode 5, the licensee identified dry white BA accumulated around a socket weld upstream of RHR valve RHR-600, and initiated CR472226. Valve RHR-600 was located in the auxiliary building on the common discharge piping for the RHR system to the reactor for decay heat removal when the plant was shut down. On April 27, 2012, while removing the dry BA, a pinhole leak was discovered with a constant spray in the toe of the socket weld (the weld starting and stopping point) where the 3/4 inch RHR pipe from valve RHR-600 was welded to the sock-o-let for the larger diameter common discharge piping for the RHR system to the reactor. The licensee initiated CR472654 and the Shift Manager declared both trains of RHR inoperable due to the through wall leak on ASME Code, Class 2 piping and entered the TS Action Condition 3.4.7.C, which required the licensee to restore operability immediately.

Initially on April 27, 2012, the licensee believed they could implement the ASME Boiler and Pressure Vessel Code, Section XI, 1998 Edition, 2000 Addenda, IWA-4133, which allowed the use of a mechanical clamping device to repair pressure boundary piping in accordance with ASME Code, Section XI, Appendix IX. However, the inspectors noted to the licensee that ASME Code, Section XI, Appendix IX, Article IX-1000(c)(2) stated that clamping devices shall not be used on portions of a piping system that forms the containment boundary. The inspectors also noted that the USAR Table 5.2-3, Reactor Containment Vessel Penetrations, listed valve RHR-600 as the outside containment barrier for Penetration Number 10, and the newly discovered leak was upstream of this CIV. The licensee concurred and pursued a proposed alternative to the code through a temporary deviation to the Code, which required prior NRC approval.

The licensee held conference calls with the NRC on April 28 and April 29 regarding the licensees proposed alternative. On an April 28 teleconference with the licensee, the NRC staff requested that the licensee address in their submittal the applicable leakage requirements for the temporary clamp in Modes 5 and 4, in accordance with their license and TS. On April 29, the licensee submitted Request No. RR-2-3 (ADAMS Accession No. ML12122A138) seeking NRCs approval to install a clamp on the leak, transition to Mode 4 to isolate the leak while allowing one train of RHR to be operable for injection, and then implementing the permanent repair prior to transitioning to Mode 3. The licensees submittal stated that the allowable leakage for transition from Modes 5 to 4 was governed by the System Integrity Program, required by TS 5.5.2, Primary Coolant Sources Outside Containment, and proposed a commitment to ensure leakage was below 5.5 gph. Following the approval by the NRC staff at approximately 1:30 a.m. on April 30, 2012, the licensee commenced installing the approved temporary clamp and encountered implementation difficulties (See Section 1R18.1), which required the licensee to stop work on the clamp installation.

Further review by the NRC inspectors and NRC TS Branch staff on Monday, April 30, 2012, raised a question regarding the location of the leak on the common RHR discharge piping and the applicable TS for leakage proposed by the licensee.

Specifically, while in Mode 4, the leakage from the common RHR discharge piping in the auxiliary building could be considered RCS operational leakage; and TS Limiting Condition for Operation 3.4.13, states, in part, that no pressure boundary leakage was allowed. The TS Section 1.1 defines pressure boundary leakage as leakage (except primary to secondary leakage) through a nonisolable fault in an RCS component body, pipe wall, or vessel wall. In addition, 10 CFR 50.2, Definitions, defines reactor coolant pressure boundary, in part, as all those pressure-containing components of pressurized water nuclear power reactors such as piping, which are connected to the RCS, up to and including the outermost CIV in system piping which penetrates primary reactor containment. The inspectors and NRC TS Branch staff verified that this definition in 10 CFR 50.2 was in effect prior to the issuance of the Kewaunee Operating License in December 1973, and therefore was applicable to the licensees implementation of TSs.

In addition, the inspectors and NRC TS Branch staff concluded the pinhole weld leak upstream of valve RHR-600 (defined in the USAR Table 5.2-3 ad the outermost CIV for containment penetration No. 10) was a nonisolable fault because isolation of the common discharge piping for RHR decay heat removal would result in a loss of a key safety function, core cooling, and therefore could not be isolated due to operational conditions. While the RHR system was inoperable due to the pinhole leak in the piping, the RHR system was still available to perform its key safety function of core cooling in Mode 5.

The inspectors and NRC staff then discussed with the licensee the applicability of TS 3.4.13 to the allowable leakage from the proposed temporary clamps for transition from Mode 5 to 4.

Analysis:

The inspectors determined that the failure to provide complete and accurate information in all material respects in accordance with 10 CFR 50.9 was a performance deficiency warranting a significance evaluation.

The performance deficiency was determined to be more than minor in accordance with the NRC Enforcement Policy and Enforcement Manual because the NRC identified the performance deficiency, the NRC relied on the information provided in a licensing decision, and the misinformation was identified after the NRC relied on the information in its licensing decision. Because violations of 10 CFR 50.9 are considered to be violations that potentially impact the regulatory process, they are dispositioned using the traditional enforcement process instead of the ROP SDP. Because the performance deficiency, a failure to submit complete and accurate information, was not an ROP finding per IMC 0612, Appendix B, Issue Screening, a cross-cutting aspect was not assigned to this violation.

Enforcement:

Title 10 CFR Part 50.9, Completeness and Accuracy of Information, paragraph

(a) requires, in part, that information provided to the Commission by a licensee shall be complete and accurate in all material respects.

Contrary to the above, on April 29, 2012, as part of a license amendment for a proposed temporary deviation from the requirements of 10 CFR 50.55a and ASME Code, Section XI, the licensee incorrectly stated the allowable leakage from the temporary clamp in transition from Mode 5 to 4 was governed by TS 5.5.2, Primary Coolant Sources Outside Containment, and proposed an allowable leakage value of 5.5 gph.

After licensee Request No. RR-2-3 was approved by the NRC, the inspectors and NRC staff determined that the governing leakage requirement was no leakage in Mode 4 for the clamp as required by TS 3.4.13, Reactor Coolant System Operational Leakage.

+This information was material, in that, the NRC staff would not have approved a leakage value of 5.5 gph for the temporary clamp on April 30, 2012, with this additional information. The severity of the violation was mitigated because of the facts surrounding the licensees implementation of Request No. RR-2-3. Because this violation was not repetitive or willful, and was entered into the licensees CAP as CR478732, this violation is being treated as a SL IV NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000305/2012003-04; Incorrect Leakage Requirement Submitted For A Proposed Temporary Pipe Clamp).

Following the licensees unsuccessful field implementation of Request No. RR-2-3 (see Section 1R18.1 of this Report), and subsequent discussion with NRC inspectors and staff, the licensee withdrew the request on May 3, 2012 (ADAMS Accession No. ML12125A300). On May 5, 2012, the licensee permanently corrected both through wall leaks on the RHR system piping without incident following the NRC approval of a second proposed alternative in Request No. RR-2-4, dated May 3, 2012 (ADAMS Accession No. ML12125A279) and supplemented on May 4, 2012 (ADAMS Accession No. ML12129A279). At the end of the inspection period, the licensee continued to perform a causal evaluation regarding this violation.

.2 EN47873, Both Trains of RHR Declared Inoperable on April 30, 2012

a. Inspection Scope

The inspectors reviewed the plants and operator response to the discovery of a second through wall pipe leak on the common discharge line for RHR on April 30, 2012.

Documents reviewed in this inspection are listed in the Attachment to this report.

This event follow-up review constituted one sample as defined in IP 71153-05.

b. Findings

No findings were identified.

.3 (Closed) Licensee Event Report (LER) 05000305/2012-004-00: Pressure Boundary

Leakage from Socket Weld on 3/4-Inch Pipe to Sample Valve RHR-600 The LER 05000305/2012-004-00 was reviewed for completeness and accuracy upon issuance on June 21, 2012. The event that occurred, circumstances that surrounded the event, and performance deficiencies that occurred, are discussed in detail in Sections 1R18 and 4OA3.1 of this report, as a result of the inspectors activities.

Therefore, this LER is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

4OA6 Management Meetings

.1 Exit Meeting Summary

On July 3, 2012, the inspectors presented the inspection results to A. Jordon, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • the results of the inservice inspection with Mr. R. Simmons, Plant Manager, on April 18, 2012;
  • the inspection results for the areas of radiological hazard assessment and exposure controls; and occupational as-low-as-reasonably-achievable (ALARA)planning and controls, with Mr. R. Simmons, Plant Manager, on April 27, 2012;
  • the heat sink performance Inspection with Mr. S. Yuen, Director of Engineering, and other members of the licensee staff on May 18, 2012.

The inspectors confirmed that none of the potential report input discussed was considered proprietary. Proprietary material received during the inspection was returned to the licensee.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

B. Koehler, Engineering Equipment Reliability Supervisor
D. Vorpahl, Engineering
J. Gadzala, Regulatory Assurance Representative
J. Jannsen, Engineering
P. Bukes, ISI Program Engineer
R. Repshas, Licensing
R. Simmons, Plant Manager
T. Olson, Engineering Programs Manager
J. Stafford, Safety and Licensing Director
T. Olsowy, Corrective Action
K. Morris, Security Manager
J. Palmer, Training Manager
C. Edwards, Maintenance
D. Lawrence, Operations Manager
K. Phillips, Outage and Planning
D. Shannon, Radiation Protection

Mark Aulik, Design Engineering Manager

Nuclear Regulatory Commission

K. Riemer, Branch Chief, Reactor Projects Branch 2
A.M. Stone, Branch Chief, Reactor Safety, Engineering Branch 2
D. Alley, Senior Materials Engineer
K. Barclay, Resident Inspector
J. Collins, Senior Materials Engineer
R. Dennig, Branch Chief
K. Feintuch, Project Manager
I. Frankl, Senior Reactor Systems Engineer
R. Grover, Reactor Systems Engineer
M. Hamm, Reactor Systems Engineer
D. Hills, Branch Chief
M. Holmberg, Branch Chief
J. Jandovitz, Project Engineer
R. Krsek, Senior Resident Inspector
T. Lupold, Branch Chief
W. Lyon, Senior Reactor Engineer, Nuclear
J. Neurauter, Senior Reactor Inspector
J. Patel, Reliability And Risk Analyst
H. Peterson, Branch Chief
C. Schulten, Senior Reactor Engineer
N. Shah, Project Engineer
A. Ulses, Branch Chief
J. Wallace, Materials Engineer
M. Ziolkowski, Reactor Engineer

Attachment

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

05000305/2012003-01 NCV Failure to Utilize Work Order for Temporary Weld Repair on ASME Code, Class 2 Piping (Section 1R18)
05000305/2012003-02 NCV Loose Cable Clamp Caused Loaded Spent Fuel Upender to Unintentionally Lower (Section 1R20)
05000305/2012003-03 NCV Failure to Provide Adequate Suppression in Cable Spreading Area (Section 4OA2.4)
05000305/2012003-04 NCV Incorrect Leakage Requirement Submitted For A Proposed Temporary Pipe Clamp (Section 4OA3.1)

Closed

05000305/2012003-01 NCV Failure to Utilize Work Order for Temporary Weld Repair on ASME Code, Class 2 Piping (Section 1R18)
05000305/2012003-02 NCV Loose Cable Clamp Caused Loaded Spent Fuel Upender to Unintentionally Lower (Section 1R20)
05000305/2012003-03 NCV Failure to Provide Adequate Suppression in Cable Spreading Area (Section 4OA2.4)
05000305/2012003-04 NCV Incorrect Leakage Requirement Submitted For A Proposed Temporary Pipe Clamp (Section 4OA3.1)
05000305/2012-004-00 LER Pressure Boundary Leakage from Socket Weld on 3/4-Inch Pipe to Sample Valve RHR-600 (Section 4OA3.3)

Attachment

LIST OF DOCUMENTS REVIEWED