IR 05000259/2018004

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NRC Integrated Inspection Report 05000259/2018004, 05000260/2018004, and 05000296/2018004
ML19031C915
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 01/31/2019
From: Masters A
NRC/RGN-II/DRP/RPB5
To: James Shea
Tennessee Valley Authority
Geanette D
References
IR 2018004
Download: ML19031C915 (24)


Text

ary 31, 2019

SUBJECT:

BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000259/2018004, 05000260/2018004, AND 05000296/2018004

Dear Mr. Shea:

On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. On January 18, 2019, the NRC inspectors discussed the results of this inspection with Mr. Lang Hughes and other members of your staff. The results of this inspection are documented in the enclosed report.

Three findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements.. We are treating these violations as noncited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or the significance of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Browns Ferry Nuclear Plant.

If you disagree with the cross-cutting aspect assignment or the finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555 0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at the Browns Ferry Nuclear Plant.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Anthony D. Masters, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68

Enclosure:

NRC Integrated Inspection Report 05000259/2018004, 05000260/2018004 and 05000296/2018004

REGION II==

Docket Nos.: 50-259, 50-260, and 50-296 License Nos.: DPR-33, DPR-52, and DPR-68 Report No.: 05000259/2018004, 05000260/2018004, AND 05000296/2018004 Enterprise Identifier: I-2018-004-0036 Licensee: Tennessee Valley Authority (TVA)

Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3 Location: Corner of Shaw and Nuclear Plant Road Athens, AL 35611 Dates: October 1, 2018 through December 31, 2018 Inspectors: T. Stephen, Senior Resident Inspector M. Kirk, Resident Inspector N. Hobbs, Resident Inspector D. Lanyi, Senior Operations Engineer S. Ninh, Senior Project Engineer P.Cooper, Reactor Inspector C. Smith, Construction Inspector Approved by: Anthony D. Masters, Chief Reactor Projects Branch 5 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring licensees performance by conducting quarterly integrated baseline inspections and an emergency preparedness program inspection at Browns Ferry Nuclear Plant, Units 1, 2, and 3 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC and self-revealed findings, violations, and additional items are summarized in the table below.

List of Findings and Violations High Crew Failure Rate During Annual Requalification Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green H.8 Procedure 71111.11 Systems FIN 05000259/2018004-01 Adherence Closed A self-revealed Green Finding was identified for a performance deficiency against the expected knowledge and abilities of licensed operators as demonstrated during the requalification examinations required by 10 CFR 55.59(a)(2). Specifically, the licensee had four (4) of fifteen (15) crews fail their annual simulator scenario examinations.

Failure to Control the Design of the High Pressure Coolant Injection (HPCI) Containment Isolation Circuitry Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green None 71153 Systems NCV 05000259/2018004-02 Closed A self-revealed Green non-cited violation of 10 CFR 50 Appendix B, Criterion III Design Control, was identified for the failure to control the design of the HPCI containment isolation circuitry. Specifically, the licensee added additional relays to the circuitry without fully evaluating the effect on the circuits design.

Failure to Establish Adequate Surveillance Test Procedures to Check Battery Category C Limits Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green None 71153 Systems NCV 05000259, 260, 296/2018004-03 Closed A self-revealed Green non-cited violation of TS 5.4.1.a, Procedures, required, in part, that written procedures be established, implemented, and maintained covering Emergency Power Sources (e.g., diesel generator, batteries) related to procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory Guide 1.33. Specifically, surveillance test procedures 0-SR-3.8.6.2(DG-A/B/C/D), Quarterly Check of Diesel Generator Battery and 0-SR3.8.4.4 (DG-A/B/C/D), Diesel Battery Performance Test, do not require a verfication of Technical Specification (TS) 3.8.6 Category C limits.

Additional Tracking Items Type Issue Number Title Report Status Section LER 05000259/2018-004- High Pressure Coolant Injection Declared 71153 Closed 00 Inoperable Due to Steam Supply Isolation LER 05000259/2018-005- Inoperability of Unit 1 and 2 Emergency 71153 Closed 00 Diesel Generators Results in Condition Prohibited by Technical Specifications

PLANT STATUS

Unit 1 operated at 83 percent rated thermal power (RTP) until October 14, 2018, when then plant was shut down for a planned refueling outage U1R12. The unit was restarted on November 20, 2018, and achieved 100 percent of the previously licensed RTP on November 29, 2018. Unit 1 performed power ascension testing associated with reaching the new Extended Power Uprate (EPU) 100 percent RTP for the rest of the inspection period.

Unit 2 operated at 100 percent RTP until October 12, 2018, when it reduced power to repair an oil leak on a recirculation pump. The unit returned to 100 percent RTP on October 19, 2018, and remained at 100 percent RTP for the remainder of the inspection period.

Unit 3 began the inspection period at 72 percent RTP until it shut down for a forced outage on October 10, 2018. The unit started up on October 10 and achieved 100 percent RTP on October 13, 2018, where it operated until October 21, 2018, when a manual scram was inserted due to a condenser tube leak. Unit 3 was restarted on October 28, 2018, and reached 100 percent RTP on November 5, 2018 where it remained for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment Partial Walkdown

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1, High Pressure Coolant Injection (HPCI) on December 12, 2018
(2) Unit 1, Hardened Containment Vent System (HCVS) on December 14, 2018

71111.05AQ - Fire Protection Annual/Quarterly Quarterly Inspection

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 1 Auxiliary Instrument Room, Fire Area 16-K on October 23, 2018
(2) Unit 3 Control Bay Chillers Room, Fire Area 16-A on October 24, 2018
(3) Units 1, 2 and 3, Fire Area YARD on November 6, 2018
(4) Unit 1, 2, and 3, Control Building Air Handling Unit Space and FLEX Storage Room, Fire Area 16P on November 15, 2018
(5) Unit 2 Electric Board Room 2B, Fire Area 08 on December 11, 2018

71111.08 - Inservice Inspection Activities

The inspectors evaluated boiling water reactor non-destructive testing by observing/reviewing the following examinations from October 22 - 25, 2018:

(1) Visual Examination a) Residual Heat Removal System Pipe Support (1-47B452-1476), ASME Class 2 (observed)b) Reactor Pressure Vessel Nuts and Bolts (N7-1-3-BC), ASME Class 1 (observed)c) Reactor Pressure Vessel Nuts and Washers (RPV-NUTS-1-01 thru 30), ASME Class 1 (observed)
(2) Ultrasonic Examination a) Reactor Pressure Vessel Nozzle (N6A-NV), ASME Class 2 (observed)
(3) Liquid Penetrant a) WO 118225266, Weld on 1-SHV-001-0512 (1-SW-911), ASME Class 3 (reviewed)

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification

The inspectors observed licensed operator requalification simulator training scenarios for the Group 3 operating crew on the Unit 2 and Unit 3 Simulators on October 1, 2018.

Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 Sample)

Annual Review of Licensee Requalification Examination Results: The inspectors completed an in-office review of the overall pass/fail results of the individual operating examinations, written examinations, and the crew simulator operating examinations on November 28, 2018.

Operator Performance (1 Sample)

The inspectors observed and evaluated the following

  • Unit 3 shutdown on October 6, 2018.
  • Unit 3 restart on October 10, 2018.
  • Unit 2 downpower to 12 percent RTP for drywell entry on October 12, 2018.
  • Unit 1 shutdown on October 14, 2018.
  • Unit 2 syncing to the grid on October 16, 2018.
  • Unit 1 power ascension and operation above previous licensed thermal power on December 17 & 18, 2018.

71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Unit 3, System 85, Control Rod Drive System
(2) Units 1, 2, and 3, Emergency Diesel Generator (EDG) Air Start System

71111.13 - Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Planned risk associated with Unit 1 high decay heat load during transition to shutdown cooling on October 14, 2018.
(2) Planned risk associated with timeframe from Unit 1 entry into Mode 5 (refueling) until flood-up of the reactor vessel on October 15, 2018.
(3) Planned risk associated with Unit 1 Reactor Vessel head lift on October 15, 2018.
(4) Shutdown risk associated with a Unit 1 Unplanned Operations with Potential for Draining the Reactor Vessel (OPDRV) during repairs of 1-PCV-85-23, Control Rod Drive pressure control valve, on November 7, 2018
(5) Shutdown risk associated with Unit 1 during OPDRV for replacing 1A Recirculation Pump seal while Fuel movements are in progress on November 11, 2018.

71111.15 - Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) C Standby Gas Treatment (SBGT) operability following failure to auto start after reaching

+2 during Unit 3 scram on October 6, 2018.

(2) Operability of B Main Steam line Inboard Isolation Valve Not Fully Open function following the identification of logic circuits for limits switches being crossed on October 7, 2018.
(3) EDG D AC Circulating Pump Low Flow following no indication of oil level in the lube oil gallery vent lower sightglass on November 6, 2018.
(4) Unit 1 HPCI operability after suction source unexpectedly swapped during pump test and discharge piping was overpressurized on November 21, 2018.
(5) Unit 1 Reactor Core Isolation Cooling (RCIC) prompt determination of operability following pressure transient that impacted RCIC turbine trip function on low suction pressure on December 5, 2018.

71111.18 - Plant Modifications

The inspectors evaluated the following plant modifications:

(1) Units 1, 2, and 3 temporary air conditioning unit installed in Communications Room while both permanent air conditioning units were out of service
(2) Reactor Recirculation Motor Replacement EPU Additional Changes per DCN 69389

71111.19 - Post Maintenance Testing

The inspectors evaluated the following post maintenance tests:

(1) Unit 1, post maintenance testing following installation on the Unit 1 Emergency High Pressure Makeup pump on October 16, 2018.
(2) EDG A post maintenance testing following STA switch replacement on November 1, 2018.
(3) Various Unit 1 integrated systems testing per 1-TI-700, 1-TI-701, 1-TI-130, and 1-TI-131 at extended power uprate conditions from October 28, 2018 to December 31, 2018

71111.20 - Refueling and Other Outage Activities

The inspectors evaluated the Unit 3 planned mid-cycle outage activities from October 6, 2018 through October 10, 2018.

The inspectors evaluated refueling outage U1R12 activities from October 14, 2018 through November 22, 2018.

The inspectors evaluated the Unit 3 unplanned forced outage activities from October 21, 2018 through October 29, 2018.

71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: Routine

(1) 1-SR-3.3.6.1.5 for Primary Containment Isolation System Main Steamline High Flow Instrument Calibrations for Channels A1, A2, B1 and B2 per ECP 51243 Stage 12 associated with Extended Power Uprate (EPU) modification on October 15 - 21, 2018.
(2) 0-TI-322 for Residual Heat Removal Heat Exchanger Thermal Performance Testing on 2A and 2C RHR heat exchangers on October 3, 2018.
(3) 1-SR-3.6.1.3.6 for Main Steam Isolation Valve Fast Closure Test on November 5, 2018.

Containment Isolation (1 Sample)

(1) As Found and As Left Local Leak Rate Testing of 1-CKV-073-0045, HPCI System Check Valve that was completed during the Unit 1 Refueling Outage.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification The Resident inspectors verified licensee performance indicators submittals listed below for the period from October 1, 2017 through September 30, 2018.

(1) Units 1, 2, and 3 Scrams (IE 01)
(2) Units 1, 2, and 3 Scrams with Complications (IE04)
(3) Units 1, 2, and 3 Unplanned Downpowers > 20 percent (IE 03)

==71152 - Problem Identification and Resolution

Semiannual Trend Review (1 sample)

==

The inspectors reviewed the licensees corrective action program (CAP) for trends that might

===be indicative of a more significant safety issue.

Annual Follow-up of Selected Issues===

The inspectors reviewed the licensees implementation of its corrective action program related to Problem Identification & Resolution associated with Unit 1 Extended Power Uprate.

71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports

The inspectors evaluated the following licensee event reports (LER) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx :

(1) LER 05000259/2018-004, High Pressure Coolant Injection Declared Inoperable Due to Steam Supply Isolation
(2) LER 05000259, 260/2018-005, Inoperability of Unit 1 and 2 Emergency Diesel Generators Results in Condition Prohibited by Technical Specifications

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL

60855.1 - Operation of an Independent Spent Fuel Storage Installation (ISFSI)

(1) The inspectors also evaluated changes to ISFSI programs and procedures to verify that changes were made consistent with the license and/or certificate of compliance.

71004 - Power Uprate Summary of Power Uprate Inspection Samples Contained in this Report:

Integrated Plant Operations at the Uprated Power Level (Unit 1)

(1) Power ascension above previous thermal power limit and flow induced vibration data reviews (Section 71111.11).

Plant Modifications (Unit 1)

(1) Reactor Recirculation Motor Replacement EPU Additional Changes per DCN 69389 (Section 71111.18)

Monitor Major Integrated Tests (Unit 1)

(1) Various Unit 1 integrated systems testing per 1-TI-700, 1-TI-701, 1-TI-130 and 1-TI-131 at from October 28, 2018 to December 31, 2018 (Section 71111.19).

Post-Maintenance / Post-Modification or Surveillance Tests (Unit 1)

(1) 1-SR-3.3.6.1.5 for Primary Containment Isolation System Main Steamline High Flow Instrument Calibrations for Channels A1, A2, B1 and B2 per ECP 51243 Stage 12 associated with Extended Power Uprate (EPU) modification on October 15 - 21, 2018 (Section 71111.22)

Identification and Resolution of Problems (Unit 1)

(1) Problem Identification and Resolution related to EPU (Section 71152)

INSPECTION RESULTS

High Crew Failure Rate During Annual Requalification Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green H.8 71111.11 Systems FIN 05000259, 260, 296/2018004-01 Procedure Closed Adherence A self-revealed Green Finding was identified for a performance deficiency against the expected knowledge and abilities of licensed operators as demonstrated during the requalification examinations required by 10 CFR 55.59(a)(2). Specifically, the licensee had four

(4) of fifteen
(15) crews fail their annual simulator scenario examinations.

During the annual requalification testing during the Fall of 2018, four of fifteen crews failed the scenario portion of their annual operating exam. Each crew failed because they did not adequately address a single critical task in one of their scenarios.

Corrective Action(s): Each crew was remediated and then successfully passed another set of simulator scenario evaluations. A Condition Report was written to document the high failure rate and to determine what the causes of the errors were. The licensee also performed a self-assessment that included a review of the causes of the failure. They identified the following causal factors:

  • Critical Parameter Control.
  • Main Control Room Board Awareness and Monitoring.
  • Understanding of Plant and System Response.
  • Emergency Operating Instruction (EOI)1 and EOI1A flowchart execution.
  • EOI entry and reentry for EOI entry conditions.
  • Procedure Use and Adherence.
  • Immediate Actions of Abnormal Operating Instruction (AOI)-701.

Note that the last five bulleted items are all part of the licensed operators ability to properly read and use their procedures.

Corrective Action Reference(s): Condition Report 1458831, Self-assessment, BFN-TRN-SA-19-009.

Performance Assessment:

Performance Deficiency: Failure of the operating crews to exhibit the expected knowledge and abilities of licensed operators as demonstrated during the requalification examinations required by 10 CFR 55.59(a)(2). Specifically, the licensee had four

(4) of fifteen
(15) crews fail their annual simulator scenario examinations.

Screening: The performance deficiency was more than minor because if left uncorrected, the performance deficiency could result in a more significant safety concern. Specifically, the failure of the operating crews to demonstrate the knowledge and abilities of licensed operators during an actual plant transient could result in placing the unit in a more significantly complex recovery condition.

Significance: Using Chapter 0609, Appendix I, Licensed Operator Requalification Significance Determination Process (SDP), the issue screened as having very low safety significance (Green) because the deficiency was identified and corrected in a timely manner.

Additionally, the deficiency existed in a small percentage of the licensed operators.

Cross Cutting Aspect: A cross cutting aspect of H.8 Procedure Aherence was assigned due to the direct cause of each of the operating crew failures was a failure to follow their emergency and abnormal procedures.

Enforcement:

The inspectors did not identify a violation of regulatory requirements associated with this finding.

Failure to Control the Design of the High Pressure Coolant Injection (HPCI) Containment Isolation Circuitry Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green None 71153 Systems NCV 05000259/2018004-02 Closed A self-revealed Green non-cited violation of 10 CFR 50 Appendix B, Criterion III Design Control, was identified for the failure to control the design of the HPCI containment isolation circuitry. Specifically, the licensee added additional relays to the circuitry without fully evaluating the effect on the circuits design.

On July 9, 2018, while surveillance procedure 1-SR-3.3.6.1.2(3B) , High Pressure Coolant Injection System Steam Supply Low Pressure Functional Test, an unexpected High Pressure Coolant Injection (HPCI) isolation occurred. The isolation was discovered at 1111 Central Daylight Time (CDT) during a walkdown of the Unit 1 Control Room when the Unit Operator identified that the inboard and outboard HPCI steam supply valves were closed.

It was determined that the valves had closed at approximately 0958 CDT during performance of 1-SR-3.3.6.1.2(3B). Unit 1 entered Technical Specifications (TS) Limiting Conditions for Operation (LCO) 3.5.1, ECCS - Operating, Condition C, at approximately 1111 CDT, which required restoring HPCI to operable status within 14 days and verification that Reactor Core Isolation Cooling (RCIC) is operable by administrative means. Following successful completion of the functional test, HPCI was placed in standby readiness lineup. The HPCI system was declared operable on July 10, 2018, at 1344 CDT. During the period of Primary Containment Isolation, the HPCI system was unable to perform its safety function. However, in an emergency, sufficient systems were available to provide the required safety functions.

The cause of the unexpected HPCI isolation during performance of the HPCI test was determined to be past operation of the steam supply low pressure switches at an electrical current level very near or above the manufacturer's rating, which resulted in degradation of the switch electrical contacts. The degradation eventually resulted in momentary contact closure during functional testing of an adjacent switch, which energized the downstream logic relays causing HPCI to isolate.

Corrective Action(s): Corrective actions were to replace the Unit 1 pressure switches that, either one of which, could have caused the spurious isolation. Work orders were initiated to replace these same pressure switches on Units 2 and 3. Additionally, the testing procedures for these pressure switches were revised to minimize the chances of a spurious HPCI steam supply isolation.

Corrective Action Reference(s): Condition Reports (CRs1429497 and CR1437895)

Performance Assessment:

Performance Deficiency: Failure to control the design of the HPCI containment isolation circuitry was a performance deficiency.

Screening: The performance deficiency was more-than-minor because it was associated with the design control attribute of the Mitigating Systems cornerstone and it adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage).

Specifically, the failure to control the design of the HPCI containment isolation circuitry resulted in the Unit 1 HPCI being declared inoperable during the period of July 9, 2018 at 1111 CDT to July 10, 2018 at 1344 CDT.

Significance: Using Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because the Unit 1 HPCI was able to be unisolated and was available for use following the spurious isolation signal.

Cross Cutting Aspect: No cross cutting aspect was assigned because this issue does not reflect the licensees current performance.

Enforcement:

Violation: 10 CFR 50 Appendix B, Criterion III Design Control, required, in part, that the design control measures shall provide for verifying or checking the adequacy of design by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program.

Contrary to the above, the licensee failed to ensure that the design changes that added additional relays to the HPCI containment isolation circuitry were fully evaluated. This evaluation should have ensured that the circuitry did not have current flows that were at the maximum allowed design limits for the installed relays.

Enforcement Actions: This violation is being treated as a Non-Cited Violation (NCV),consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Establish Adequate Surveillance Test Procedures to Check Battery Category C Limits Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green None 71153 Systems NCV 05000259, 260, 296/2018004-03 Closed A self-revealed Green non-cited violation of TS 5.4.1.a, Procedures, required, in part, that written procedures be established, implemented, and maintained covering Emergency Power Sources (e.g., diesel generator, batteries) related to procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory Guide 1.33. Specifically, surveillance test procedures 0-SR-3.8.6.2(DG-A/B/C/D), Quarterly Check of Diesel Generator Battery and 0-SR3.8.4.4 (DG-A/B/C/D), Diesel Battery Performance Test, do not require a verfication of Technical Specification (TS) 3.8.6 Category C limits.

On July 2, 2018, the licensee discovered that the last performed surveillance on the C EDG Battery had recorded the specific gravity of Battery Cell 20 at 1.204. This was 0.025 less than the average battery cell specific gravity of 1.229. The difference in specific gravity between the individual cell and the average cell was more than the BFN Unit 1 and Unit 2 TS Limiting Conditions for Operation (LCO) 3.8.6, Table 3.8.6-1, Category C, limit of 0.020.

TS LCO 3.8.4 requires that Unit 1 and 2 EDG DC subsystems be operable in Modes 1, 2, and

3. TS LCO 3.8.4 Condition C states that, with one or more EDG DC electrical power

subsystems inoperable (including the DG battery), the associated EDG must immediately be declared inoperable.

TS LCO 3.8.1 Condition H states that, with two required Unit 1 and 2 EDGs inoperable, action must be taken to restore all but one Unit 1 and 2 EDG to operable status. During the time when C EDG was inoperable, there were two periods where B EDG was inoperable for longer than two hours.

TS LCO 3.8.1 Condition I states that if required actions and completion times are not met for Condition A, B, C, D, E, F, or H, action must be taken to be in Mode 3 within twelve hours, and to be in Mode 4 within thirty-six hours.

A review of surveillances performed on June 6, 2018, determined that the specific gravity of C EDG Battery Cell 20 was 1.204. This was 0.025 below the average cell specific gravity of 1.229, and did not meet the requirements of Table 3.8.6-1. Therefore, the C EDG Battery was inoperable by LCO 3.8.6, and the C EDG was inoperable by LCO 3.8.4. A past operability evaluation determined that, because of a declining trend in Cell 20 specific gravity, the battery would be considered inoperable from the date of its last satisfactory surveillance on April 10, 2018, to June 4, 2018, when the EDG was declared inoperable for its planned maintenance window. During this time, the Required Actions of TS LCO 3.8.6 Condition B; TS LCO 3.8.4 Condition C; and TS LCO 3.8.1 Conditions B, H, and I were not completed.

Therefore, BFN was in violation of its TS during this time.

Surveillance test procedures 0-SR-3.8.6.2(DG-A/B/C/D), Quarterly Check of Diesel Generator Battery and 0-SR3.8.4.4 (DG-A/BC/D, Diesel Battery Performance Test did not specify to check the Category C limits.

Corrective Action(s): Corrective actions were to replace the battery cell, to issue an Operations Standing Order ensuring TS 3.8.6 Category C limits are met when quarterly SRs are performed on DG batteries, to revise battery surveillance requirement (SR) procedures, and to revise Unit 1, 2, and 3 TS 3.8 to address the discrepancy between the SR and the TS 3.8.6 LCO Condition B required action.

Corrective Action Reference(s): Condition Reports (CRs1429012 and CR1434547)

Performance Assessment:

Performance Deficiency: Failure to Establish Adequate Surveillance Test Procedures to Check Battery Category C Limits was a performance deficiency.

Screening: The performance deficiency was more-than-minor because it was associated with the procedure quality attribute of the Mitigating Systems cornerstone and it adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage).

Specifically, the failure to establish adequate surveillance test procedures to check battery Category C limits resulted in the C EDG inoperable during the period of April 10 to June 14, 2018.

Significance: Using Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because the entire battery bank was sufficient to supply the power necessary for C EDG to perform its safety function for its seven-day mission time.

Cross Cutting Aspect: No cross cutting aspect was assigned because this violation did not reflect current licensee performance.

Enforcement:

Violation: TS 5.4.1.a, Procedures, required, in part, that written procedures be established, implemented, and maintained covering Emergency Power Sources (e.g., diesel generator, batteries) related to procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory Guide 1.33.

Contrary to the above, the licensee failed to establish adequate surveillance test procedures to check battery Category C limits as required by TS 3.8.6, Table 3.8.6-1, Category C limits for a long time. This resulted in the C EDG inoperable during the period of April 10 to June 14, 2018, which was longer than the LCO 3.8.1 Condition B, 7 day allowed outage time.

Also, during this time, there were two periods where a second Unit 1 and 2 DG was inoperable for longer than the two hours allowed by TS LCO 3.8.1, Condition H.

Enforcement Action: This violation is being treated as a Non-Cited Violation (NCV),consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors confirmed that proprietary information was controlled to protect from public disclosure.

  • On January 18, 2019, the quarterly resident inspector inspection results were presented to Mr. Lang Hughes , and other members of the licensee staff.

DOCUMENTS REVIEWED

IP 71111.04

Procedures

0-GOI-300-1/ATT-5, Unit 1 Reactor Building Operator Round Logs, Revision 260

0-GOI-300-1/ATT-16, Unit 1 Operator at the Controls Duty Station Checklist, Revision 15

1-OI-73, High Pressure Coolant Injection System, Revision 30

1-OI-73/ATT-1, High Pressure Coolant Injection System Attachment 1 Valve Lineup Checklist,

Revision 17

1-OI-73/ATT-2, High Pressure Coolant Injection System Attachment 2 Panel Lineup Checklist,

Revision 17

1-OI-73/ATT-3, High Pressure Coolant Injection System Attachment 3 Electrical Lineup

Checklist, Revision 15

Drawings

1-47E812-1, Flow Diagram High Pressure Coolant Injection, Revision 47

2-47E2847-10, Mechanical I&C Flow Diagram Control Air System, Revision 1

3-47E865-12, ASME Section XI Heating & Ventilating Air Flow Code Class Boundaries,

Revision 9

Other Documents

BFN-50-7073, High Pressure Coolant Injection System, Revision 31

CR 1429497

WO 119827193

CR 1463399

CR 1469446

CR 1428829

CR 1428037

WO 119695449

IP 71111.05

Procedures

FPR-Volume 2, Fire Protection Report Volume 2, Revision 61

NPG-SPP-18.4.7, Control of Transient Combustibles, Revision 12

NPG-SPP-01.3, Housekeeping, Revision 6

NPG-SPP-18.4.8, Control of Ignition Sources (Hot Work), Revision 7

Other Documents

NFPA 805 Fire Protection Report, Appendix F, Fire Area 16, Revision 2

MDN0009992012000100, Browns Ferry Nuclear Plant, Units 1, 2, and 3, Fire Risk Evaluations,

Revision 8

MDQ099920110009, NFPA 805 Transition - Fire Area Designation - Appendix A, Revision 7

Drawings

3-47E216-71-1, NFPA 805 Physical Analysis Units Plan El. 606.0, 617.0 and 621.0, Revision 0

0-47E216-64, NFPA 805 Fire Areas, Revision 0

0-47E216-64-1, NFPA 805 Physical Analysis Units, Revision 0

IP 71111.08

Procedures

N-UT-78, PDI Generic Procedure for the Manual Ultrasonic Examination of Reactor Pressure

Vessel Welds PDI-UT-6, Rev. 9

N-UT-90, Generic Procedure for the Ultrasonic Detection and Sizing of Reactor Pressure Vessel

Nozzle to Shell Welds and Nozzle Inner Radius, Rev. 3

N-VT-1, Visual Examination Procedure for ASME Section XI Preservice and Inservice, Rev.48

0-SI-4.6.G, Inservice Inspection Program, Rev. 3

0-TPP-ENG-376, Containment Inservice Inspection Program, Rev. 0

Condition Reports

CR 1460144

Drawings

1-CHM-2102-A, Closure Head Assembly Weld Locations, Rev. 0

1-CHM-2001-C, Vessel Stud Locations, Rev. 1

47B452-1476, Residual Heat Removal System Pipe Support, Rev. 3

UT-W-0174, 22 Deg Beam, Rev. A

UT-W-0175, 22 Deg Beam, Rev. A

UT-W-0176, 26 Deg Beam, Rev. A

UT-W-0177, 35 Deg Beam, Rev. A

UT-W-0178, 35 Deg Beam, Rev. A

UT-W-0179, 40 Deg Beam, Rev. A

UT-W-0180, 40 Deg Beam, Rev. A

Other Documents

BF-19, Calibration Block As-Built Verification, 4/16/97

BFN-MNT-55A-15-008, Weld Program Self Assessment, 9/2/15

Certificate of Qualification: S. Sawatzky

CRP-ENG-FSA-17-004, Inservice Inspection Self Assessment, 9/14/17

IR-2013-535, EPRI Browns Ferry Nozzle Inner Corner Radius and Nozzle to Shell Weld

Examinations, February 2013

NOI No. U1R11-010, 1-CHM-0992, N4A Nozzle to Shell Weld, 10/19/16

Report of Calibration: Certificate No. 149799, 157826

S/N 791719, Certificate of Compliance Reference Block, 7/15/83

Transducer Certification: L97-160223-001, L97-160223-002, L97-160223-003, L97-160223-004,

L97-160223-005, L97-160223-006

Visual Acuity:

D. Sawatzky,

Work Orders/ Work Request

WO 111003075

WO 118225266

WO 119208457

WO 119208531

IP 71111.11

Procedures

OPDP-1, Conduct of Operations, Revision 42

1-TI-700, EPU Master Startup Test Instruction, Revision 0

1-TI-701, EPU Vibration Monitoring, Revision 2

Other Documents

Simulator Exam LOR-Exam-70, Revision 1

LOR-Exam-73, Revision 1

Condition Report 1458831, Self-assessment, BFN-TRN-SA-19-009

IP 71111.12

Procedures

NPG-SPP-03.4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting -

10CFR50.65, Revision 3

0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -

10CFR50.65, Revision 51

System Health Reports for System 85, Control Rod Drive System

3-ARP-25-4094, Panel 25-4094 Alarm Response Procedure, Revision 26

Other Documents

CR 1324057

CR 1262865

CR 1297105

CR 1262869

CR 1262500

CR 1360357

CR 1379196

CR 1388223

POE for CR 1388223

DEC 72557

CR 1402765

CR 1392756

CR 1401351

CR 1399415

CR 1429818

CR 1435915

WO 119779323

CR 1454563

CR 1463088

WO 119991812

CR 1455803

CR 1466873

CR 1466899

CR 1466811

CR 1466092

CR 1466105

CR 1471423

CR 1467190

IP 71111.13

Procedures:

BFN-ODM-4.18 Protected Equipment, Revision 21

MSI-0-000-LFT001, Lifting Instructions for the Control of Heavy Loads, Revision 74

MSI-0-000-LFT002, Rigging Equipment and Portable Hoist Control, Inspection and Testing,

Revision 23

MSI-0-001-VSL001, Reactor Vessel Disassembly and Reassembly, Revision 124

1-POI-200.5, Operations with Potential for Draining the Reactor Vessel/Cavity, Revision 10

NPG-SPP-10.6, Infrequently Performed Test or Evolution, Revision 1

Other Documents:

Unit 1 Cycle R12 Outage Safety Plan

WO 119144094

CR 1464276

WO 119482671

Operator Logs on November 7, 2018

IP 71111.15

Procedures:

OPDP-8, Operability Determination Process and Limiting Conditions for Operation Tracking,

Revision 24

3-SR-3.3.1.1.8(5), MSIV Closure - RPS Trip Channel Functional Test, Revision 19

3-SR-3.3.1.1.14(5 II), MSIV Closure - RPS Trip Logic System Functional Test (Channel B1/B2),

Revision 2

0-OI-82, Standby Diesel Generator System, Revision 167

1-SR-3.3.5.2.4(FT), RCIC System Logic Functional Test, Revision 10

Drawings:

0-45E772-1, Wiring Diagram 480V Stby Gas Trtmt TN C Schematic Diagram, Revision 23

3-730E915-1, Reactor Protection System, Revision 26

3-730E915-10, Reactor Protection System, Revision 29

3-47E801-1, Unit 3, Flow Diagram Main Steam, Revision 40

0-47E861-8 Flow Diagram - Cooling System and Lubricating Oil System Standby Diesel

Generator D, Revision 17

1-47E610-71-1, Mechanical Control Diagram RCIC System, Revision 20

1-45E626-2, Wiring Diagram Reactor Core Isolation Cooling System Schematic Diagram,

Revision 14

Other Documents:

CR 1454001

Past Operability Evaluation for CR 1454001

CR 1380403

WO 119934934

WO 119345859

Operator Log dated 10/6

CR 1451961

CR 1452457

CR 1454334

CR 1454521

WO 119912747

WO 119909104

CR 1463538

EMD-ESI Diesel Generator Owners Group Operating Practice Guidance: Loss of Circulating

and/or Turbocharger / Soak Back Oil Pump approved July 11, 2006

BFN-50-7082 Standby Diesel Generator Design Criteria Document, Revision 29

CR 1469109

CR 1469263

CR 1469946

MDQ0073880139, High Pressure Coolant Injection (HPCI) System - Design Temperatures and

Pressures, Revision 18

CR 1473324

CR 1473326

CR 1473399

CR 1472655

WO 120063402

WO 120067817

IP 71111.18

Procedures

NPG-SPP-09.5 Temporary Modifications Temporary Configuration Changes, Revision 14

Drawings

1-729E841-4, Elementary Diagram Jet Pump Instrumentation, Revision 7

1-47E605-208, Mechanical Component Scales and Misc Details for Control Panel 1-9-4,

Revision 0

1-47E605-228, Mechanical Component Scales and Misc Details for Control Panel 1-9-8,

Revision 1

1-45E1718-21, Wiring Diagram Panel 1-PNLA-261-25 Connection Diagram, Revision 3

Documents

CR 1462646

DCN 69389, Reactor Recirculation Motor Replacement EPU Additional Changes, Revision A

IP 71111.19

Procedures

PMTI-71399-002, EHPM Pump RPV Injection Test at Low Pressure Conditions, Revision 1

BFN-0-BKR-211-000A/022 Test MJ (52 STA) Contacts Breaker 1818 (4KV SD BD A/22),

Revision 0

1-TI-130, Main Steam Pressure Control, Revision 3

1-TI-131, Feedwater Level Control System, Revision 2

Other Documents

CR 1459327

CR 1459329

WO 119968348

IP 71111.20

Procedures

3-SR-3.4.9.1(1) Reactor Heatup and Cooldown Rate Monitoring, Revision 26

Other Documents

Unit 1 Cycle R12 Outage Safety Plan

Daily outage status documents for Units 1, 2, and 3 from October 5, 2018 until November 21,

2018

IP 71111.22

Procedures

1-SI-4.7.A.2.g-3/3a, Primary Containment Local Leak Rate Test Reactor Feedwater Line A:

Penetration X-9A, Revision 8 and Revision 9

WO Instructions, Revision 0 for WO 118762701 (1-PDIS-001-0013A), WO 119057073 (1-PDIS-

001-0013B), WO 119057078 (1-PDIS-001-0013C) and WO 119057082 (1-PDIS-001-0013D)

0-TI-322 RHR Heat Exchanger Performance Testing, Revision 5

1-SR-3.3.6.1.5(1C/A1), Primary Containment Isolation System Main Steamline High Flow

Instruments Channel A1 Calibration, Revisions 7 and 8

1-SR-3.3.6.1.5(1C/B1), Primary Containment Isolation System Main Steamline High Flow

Instruments Channel B1 Calibration, Revisions 6 and 7

1-SR-3.3.6.1.5(1C/A2), Primary Containment Isolation System Main Steamline High Flow

Instruments Channel A2 Calibration, Revisions 7 and 8

1-SR-3.3.6.1.5(1C/B2), Primary Containment Isolation System Main Steamline High Flow

Instruments Channel B2 Calibration, Revisions 8 and 9

1-SR-3.6.1.3.6 Main Steam Isolation Valve Fast Closure Test, Revision 10

Drawings

1-47E803-1, Mechanical Flow Diagram Reactor Feedwater, Revision 43

1-47E801-1, Mechanical Flow Diagram Main Steam, Revision 26

1-730E927-7, Primary Cntmt Isln Sys, Revision 26

1-45E671-1, Wiring Diagram RPS Div IA Analog Trip Units Schematic Diagrams, Revision 9

Other Documents

WO 118942972

WO 118942990

CR 1458509

0-TI-360, Containment Leak Rate Programs, Revision 44

WO 118762701

WO 119057073

WO 119057078

WO 119057082

Engineering Change Package 51243 Stage 12

EDQ 0001920425, Setpoint and Scaling Calculation for 1/3-D013A-D, -25A-D, -36A-D, -50A-D,

Revision 9

1-SIMI-1B, Main Steam System Scaling and Setpoint Documents, Revision 27

BFN-VTD-R369-0120, Alphaline Model 1153 Series D Pressure Transmitters for Nuclear

Service Product Manual, Revision 4

BFN-VTD-R369-0170, Trip/Calibration System Model 710DU, Revision 1

WO 119444529

WO 119225915

WO 118936572

WO 119226585

WO 118936573

WO 119226681

WO 118936576

WO 119227456

WO 118936577

IP 71151

Procedures

NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7

Other Documents

Units 1, 2 and 3 ROP PI Summary

Operator Logs from October 1, 2017 until September 30, 2018

IP 71152

Procedures

NPG-SPP-22.300, Corrective Action Program, Revision 12

Other Documents

CR 1463391

CR 1457235

CR 1461049

CR 1468492

CR 1460208

CR 1462654

CR 1466811

IP 71153

Procedures

1-SR-3.3.6.1.2(3B) High Pressure Injection System Steam Supply Low Pressure Functional,

Revision 7

0-SR-3.8.4.4(DG C), DG C Battery Performance Test, Revision 0018

0-SR-3.8.6.2(DG C), Quarterly of Diesel Generator C Battery, Revision 0007

Other Documents

LER 50-259/2018-004-00 High Pressure Coolant Injection Declared Inoperable due to Steam

Supply Valve Isolation, Revision 0

BFN0EQIPS 003, BFN Environmental Qualification Binder; May 28, 2013 update

CR 1427962

CR 1434547

LER 05000259, 260, 296/2018-005

IP 60855

Procedures

MSI-0-079-DCS300.4, Hi Storm 100 and Hi-Trac 125D Site Transportation, Revision 10

21