IR 05000334/2018002
ML18218A187 | |
Person / Time | |
---|---|
Site: | Beaver Valley |
Issue date: | 08/02/2018 |
From: | Matt Young NRC/RGN-I/DRP/PB6 |
To: | Bologna R FirstEnergy Nuclear Operating Co |
References | |
IR 2018002 | |
Download: ML18218A187 (17) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION ust 2, 2018
SUBJECT:
BEAVER VALLEY POWER STATION, UNIT NOS. 1 AND 2 - INTEGRATED INSPECTION REPORT 05000334/2018002 AND 05000412/2018002
Dear Mr. Bologna:
On June 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Beaver Valley Power Station, Units 1 and 2. On July 26, 2018, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
The NRC inspectors did not identify any finding or violation of more than minor significance.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Matthew Young, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos.: 50-334 and 50-412 License Nos.: DPR-66 and NPF-73
Enclosure:
Inspection Report 05000334/2018002 and 05000412/2018002
Inspection Report
Docket Numbers: 50-334 and 50-412 License Numbers: DPR-66 and NPF-73 Report Numbers: 05000334/2018002 and 05000412/2018002 Enterprise Identifier: I-2018-002-0067 Licensee: FirstEnergy Nuclear Operating Company (FENOC)
Facility: Beaver Valley Power Station, Units 1 and 2 Location: Shippingport, PA 15077 Inspection Dates: April 1, 2018 to June 30, 2018 Inspectors: J. Krafty, Senior Resident Inspector B. Pinson, Senior Resident Inspector (Acting)
S. Horvitz, Resident Inspector R. Rolph, Health Physicist E. Andrews, Health Physicist J. Kulp, Senior Reactor Inspector D. Kern, Senior Reactor Inspector S. Shaffer, Senior Project Engineer Z. Hollcraft, Senior Resident Inspector Approved By: M. Young, Chief Reactor Projects Branch 6 Division of Reactor Projects Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring FirstEnergy Nuclear
Operating Companys (FENOCs) performance at Beaver Valley Power Station Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
No findings or more-than-minor violations were identified.
PLANT STATUS
Unit 1 began the inspection period shutdown in a planned refueling and maintenance outage (1R25).
1R25 was completed on May 10, 2018, and the unit was returned to 100 percent power
on May 13, 2018. On June 28, 2018, power was reduced to 76 percent to address an emergent condenser tube leak. On June 29, 2018, power was further reduced to 47 percent and remained there for the remainder of the inspection period due to degrading chemistry conditions in the steam generators.
Unit 2 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess FENOCs performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection Summer Readiness
The inspectors evaluated summer readiness of offsite and alternate AC power systems from June 4 through June 7, 2018.
71111.04 - Equipment Alignment Partial Walkdown
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 1, fuel pool cooling system following core offload on April 24, 2018
- (2) Unit 1, recirculation spray system while outside recirculation spray was out of service on April 25, 2018
- (3) Unit 1, residual heat removal system during reactor core reload on April 28, 2018
- (4) Unit 2, B spent fuel pool cooling system during A spent fuel pool cooling pump maintenance on May 22, 2018
Complete Walkdown (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the Unit 1 Quench Spray system on May 7, 2018.
71111.05Q - Fire Protection Annual/Quarterly Quarterly Inspection
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Unit 1, purge duct and steam generator blowdown area, fire area SG/PD, on April 5, 2018
- (2) Unit 1, potentially contaminated area shop, fire area SB-1, on April 5, 2018
- (3) Unit 1, reactor containment building, fire area RC-1, on April 17, 2018
- (4) Unit 1, hot lab and radiation protection offices, fire areas SB-2 and CL-1, on April 21, 2018
- (5) Unit 2, DF switchgear room, fire area 2-SB-2, on April 26, 2018
71111.06 - Flood Protection Measures Internal Flooding
The inspectors evaluated internal flooding mitigation protections in the Unit 2 auxiliary building on June 25, 2018.
71111.07 - Heat Sink Performance Heat Sink
The inspectors evaluated FENOCs monitoring and maintenance of the Unit 1 C recirculation spray heat exchanger performance.
71111.08 - Inservice Inspection Activities
The inspectors evaluated pressurized water reactor non-destructive examination and welding activities by reviewing the following examinations from April 23, 2018 to April 26, 2018.
- (1) Volumetric Examinations a) Manual ultrasonic testing of reactor coolant butt weld DLW-LOOP1-S-01 b) Manual ultrasonic testing of socket welded drain line RC-51 This review pertained to examinations performed in accordance with MRP-146, Materials Reliability Program Management of Thermal Fatigue in Normally Stagnant Non-Isolable Reactor Coolant System Branch Lines.
c) Manual ultrasonic testing of socket welded drain line RC-53 This review pertained to examinations performed in accordance with MRP-146, Materials Reliability Program Management of Thermal Fatigue in Normally Stagnant Non-Isolable Reactor Coolant System Branch Lines.
- (2) Visual Examinations a) Enhanced Visual Testing (VT1) of the core barrel upper flange weld This review pertained to examinations performed in accordance with MRP-227, Pressurized Water Reactor Internals Inspection and Evaluation Guidelines.
b) General visual examination of containment liner c) System leakage test (VT2) of charging system risk informed segment CH-130 d) System leakage test (VT2) of safety injection bolted connection BC-1SI-53 e) General visual examination (VT3) of reactor head penetration #49 area
- (3) Surface Examination (PT/MT)a) Magnetic particle test of river water system piping segment WR-20 butt welds This review involved welding activities associated with a pressure boundary risk significant system.
- (4) The inspectors reviewed the welding activities associated with the replacement of section WR-20 of river water system piping.
- (5) The inspectors evaluated FENOCs boric acid corrosion control program performance.
- (6) The inspectors performed an independent walkdown of accessible portions of the containment liner and moisture barrier.
- (7) The inspectors reviewed FENOCs performance in evaluating and removing a boric acid deposit following its discovery on the reactor vessel head.
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification
The inspectors observed and evaluated a crew of licensed operators in the Unit 1 simulator during licensed operator training conducted in preparation for upcoming plant evolutions on
===April 9, 2018.
Operator Performance (1 Sample)===
The inspectors observed and evaluated the shutdown for refueling outage 1R25 and draining of the reactor coolant system for refueling at Unit 1 on April 14, 2018, and April 17, 2018.
71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Unit 2, safety injection system
- (2) Unit 2, 4160V station service electrical system
- (3) 10 CFR 50.65 (a)(3) Periodic Evaluation for the period of July 1, 2015, through
February 28, 2017 Quality Control (2 Samples)
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:
- (1) Unit 1, RD-1MS-1 leak injection repair (2X phenolic sealant material) on May 24, 2018
- (2) Unit 2, replacement of C charging pump breaker cubicle parts on June 5, 2018
71111.13 - Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unit 1, yellow shutdown risk for decay heat removal while reactor coolant system is depressurized and drained to flange on April 18 and 19, 2018
- (2) Unit 1, yellow shutdown risk for decay heat removal and spent fuel pool cooling during core offload with only one component cooling water heat exchanger available on April 21, 2018
- (3) Unit 1, yellow shutdown risk for decay heat removal while reactor coolant system is depressurized and drained to flange on May 3, 2018
- (4) Unit 1, elevated risk for turbine driven auxiliary feedwater pump testing on May 8, 2018
- (5) Unit 2, elevated risk for 2A station system service transformer deluge testing on May 17, 2018
71111.15 - Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Unit 1, low head safety injection snubber clearance gaps between load pins and pipe clamps on April 17, 2018
- (2) Unit 1, turbo charger air intake filter rack broken support on 1-1 emergency diesel generator on April 25, 2018
- (3) Unit 1, primary drains discharge containment isolation valve TV-1DG-108A failed drop test on May 7, 2018
- (4) Unit 1, MOV-1RW-113A, river water inlet motor operated valve on 1-1 emergency diesel generator heat exchanger over thrust condition on June 6, 2018
- (5) Unit 1 and 2, evaluation of thermal sleeve wear in control rod drive mechanisms as a result of Westinghouse Part 21 on June 11, 2018
71111.18 - Plant Modifications
The inspectors evaluated the following temporary or permanent modifications:
- (1) Engineering Change Package 16-0535-004,005 - Unit 1 permanent installation of RCS level indication cabling
- (2) Engineering Change Package 16-0368-003,004 - Unit 1 emergency diesel generator air start system upgrades
- (3) Part/Component Equivalent Replacement Package PERP-001350 - Unit 1 BV-MOV-1RW-113A/B/C & D1 Wedge Pin Material Upgrade and Upstream Disc Hole Provision
71111.19 - Post Maintenance Testing
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
- (1) Unit 2, A control room emergency air conditioning unit motor repairs on March 26, 2018
- (2) Unit 1, 1-2 emergency diesel generator planned maintenance on April 22, 2018
- (3) Unit 1, high head safety injection system planned maintenance on May 2, 2018
- (4) Unit 1, 1-1 emergency diesel generator planned maintenance on May 2, 2018
- (5) Unit 1, pressurizer power operated relief valve, PCV-1RC-455D, adjustments on May 8, 2018
- (6) Unit 1, containment penetration 1X-2 relief valve replacement on May 11, 2018
- (7) Unit 2, C charging pump breaker cubicle parts replacement on June 8, 2018
- (8) Unit 2, A service water train strainer overhaul on June 11, 2018
71111.20 - Refueling and Other Outage Activities
The inspectors evaluated Unit 1 refueling outage (1R25) activities from April 15 through May 10, 2018
71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: Routine
- (1) 2OST-13.2, quench spray pump 2QSS*P21B test on April 10, 2018
- (2) 1BVT1.21.2, trevitest method for main steam safety valve setpoint check on April 14, 2018
- (3) 1OST-36.3, No. 1 emergency diesel generator automatic test on April 15, 2018
- (4) 1OST-11.14A, low head safety injection full flow test on April 20, 2018
Containment Isolation Valve (1 Sample)
- (1) 1OST-47.153, Type C leak test - Penetration #90 (Containment Purge Exhaust) on May 4,
RADIATION SAFETY
71124.01 - Radiological Hazard Assessment and Exposure Controls Radiological Hazard Assessment
The inspectors reviewed recent plant radiation surveys and for radiological hazards to onsite workers or members of the public. The inspectors evaluated assessments and controls for new radiological hazards.
Instructions to Workers (1 Sample)
The inspectors evaluated instructions provided to workers.
Radiological Hazards Control and Work Coverage (1 Sample)
The inspectors evaluated in-plant radiological conditions during facility walk-downs and observation of radiological work activities. The inspectors assessed whether posted surveys, radiation work permits, worker radiological briefings, the use of continuous air monitoring and dosimetry monitoring were consistent with the present conditions.
High Radiation Area and Very High Radiation Area Controls (1 Sample)
The inspectors evaluated risk-significant high radiation area and very high radiation area controls including postings and physical barriers.
Radiation Worker Performance and Radiation Protection Technician Proficiency (1 Sample)
The inspectors evaluated radiation worker and radiation protection technician radiological performance.
71124.02 - Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls Verification of Dose Estimates and Exposure Tracking Systems
===The inspectors evaluated dose estimates and exposure tracking.
Radiation Worker Performance===
The inspectors evaluated radiation worker and radiation protection technician performance.
71124.03 - In-Plant Airborne Radioactivity Control and Mitigation Engineering Controls
The inspectors evaluated engineering controls for in-plant airborne radioactivity.
71124.04 - Occupational Dose Assessment Source Term Characterization
The inspectors evaluated FENOCs source term characterization.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification The inspectors verified FENOCs performance indicator submittals listed below for the period from April 1, 2017, through March 31, 2018.
- (1) Unit 1 and 2 Safety System Functional Failures
- (2) Unit 1 and 2 Emergency AC Power System Mitigating System Performance Index
- (3) Unit 1 and 2 High Pressure Injection System Mitigating System Performance Index
71152 - Problem Identification and Resolution Annual Follow-up of Selected Issues
The inspectors reviewed FENOCs implementation of its corrective action program related to the following issues:
- (1) Condition Report 2018-00134, Unit 2 low head safety injection system A surveillance test unable to be completed due to frozen recirculation line
- (2) Condition Reports 2017-04061, 2017-07350, Unit 1 chilled water maintenance rule (a)(1)goals and 2017-10581, Unit 1 compressed air maintenance rule (a)(1) goals
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL Impact of Financial Conditions on Continued Safe Performance In that the licensee's parent company, FirstEnergy Solutions, was under bankruptcy protection/reorganization during the inspection period, NRC Region I conducted reviews of processes at Beaver Valley. Using the flexibilities in the baseline inspection program, the inspectors evaluated several aspects of FENOCs operations to assess whether any identified plant performance issues could be related to the station's financial condition. The factors reviewed included:
- (1) impact on regulatory required plant staffing,
- (2) corrective maintenance backlog,
- (3) changes to the planned maintenance schedule,
- (4) corrective action program implementation, and
- (5) reduction in outage scope, including risk-significant modifications. In particular, the inspectors assessed whether FENOC personnel continued to identify problems at an appropriate threshold and enter these problems into the corrective action program for resolution. The inspectors also assessed whether FENOC continued to develop and implement corrective actions commensurate with the safety significance of the problems identified.
INSPECTION RESULTS
Observations 71152 The inspectors noted that the corrective actions for the (a)(1) goals approved for the Unit 1 chilled water system and compressed air system in CR 2017-04061, 2017-07350, and 2017-10581 did not examine the process for determining if the (a)(1) goals were reasonable. As a result, the inspectors reviewed the (a)(1) goals for five systems currently in (a)(1) and three systems recently returned to (a)(2) to determine whether the (a)(1) goals approved in other systems were reasonable. The inspectors noted that four out of the five (a)(1) systems and all three (a)(2) systems had (a)(1) goals that allowed a higher frequency of failure than their respective (a)(2) performance criteria. The four (a)(1) systems were Unit 1 auxiliary feedwater and area ventilation and Unit 2 chilled water and compressed air. The three (a)(2) systems were emergency response facility substation, structures, and Unit 2 heat trace. The inspectors determined that these goals were not reasonable because the systems could be returned to (a)(2) after meeting their (a)(1) goals and their performance may not meet their (a)(2) performance criteria. Although there is a requirement to have goals when a system is in (a)(1), the inspectors found no requirement that specifies criteria for (a)(1) goals. Therefore, the inspectors concluded that there was no performance deficiency. The inspectors also reviewed the performance of the three (a)(2) systems during their (a)(1) monitoring period and determined that their performance justified their return to (a)(2).
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On July 26, 2018, the inspectors presented the quarterly resident inspector inspection results to Mr. Richard Bologna, Site Vice President, and other members of the Beaver Valley Power Station staff.
DOCUMENTS REVIEWED
Miscellaneous
Unit 1 Main Generator and Transformer Maintenance Rule Monthly Monitoring Spreadsheet,
May 2018
Unit 1 4KV Station Service System Monthly Monitoring Spreadsheet, May 2018
Unit 1 Emergency Diesel Generators System Monthly Monitoring Spreadsheet, May 2018
Unit 2 4KV Station Service System Monthly Monitoring Spreadsheet, May 2018
Unit 2 Emergency Diesel Generators System Monthly Monitoring Spreadsheet, May 2018
Unit 2 Main Generator and Transformer Maintenance Rule Monthly Monitoring Spreadsheet,
May 2018
Condition Reports (*initiated in response to inspection)
2018-03417 2018-03473 2018-03655 2018-03964
2018-03424 2018-03508 2018-03718
2018-03465 2018-03523 2018-03877
2018-03469 2018-03554 2018-03889*
Maintenance Order/Work Order
200694327
NDE Reports
1BVT 1.45.1, Containment Structural Integrity Test Results, dated May 5, 2018
BOP-MT-18-011, BV-WR-20: Two Butt Welds and 12 Lug Removal Areas, dated April 22, 2018
BOP-VT-18-033, Reactor Head Penetration #49 Area, dated April 30, 2018
Remote Visual Inspection Record, Core Support Barrel Upper Flange Weld 1, dated
May 29, 2018
UT-18-1008, Butt Weld DLW-LOOP1-7-S-01, dated April 23, 2018
UT-18-1009, Socket Welded Drain Line RC-51-1502-Q1, dated April 23, 2018
UT-18-1010, Socket Welded Drain Line RC-53-1502-Q1, dated April 23, 2018
VT-18-1015, RI-ISI Segment CH-130, dated April 20, 2018
VT-18-1019, Bolted Connection BC-1SI-53, dated April 17, 2018
Engineering Evaluation
Evaluation of the Boric Acid Deposit Discovered on Beaver Valley Unit 1 Reactor Head
Penetration 49, dated April 29, 2018
Miscellaneous
200695327, Weld Data Sheet for WR-20-FW-3, Revision 0
200695327, Weld Data Sheet for WR-20-FW-4, Revision 0
ASME Code Case, N729-4, Alternative Examination Requirements for PWR Reactor Vessel
Upper Heads with Nozzles having Pressure-Retaining Partial-Penetration Welds,
Section XI, Division 1, dated June 22, 2012
Boric Acid Corrosion Control Leak Inspection, RPV Head (As Found - 2), dated April 28, 2018
Boric Acid Corrosion Control Leak Inspection, RPV Head (As Found), dated April 28, 2018
Boric Acid Corrosion Control Leak Inspection, RPV Head (As Left), dated April 29, 2018
FENOC Vision Examination for B0897, dated October 6, 2017
Condition Reports
2015-12933 2015-14482 2017-05211 2018-00134
2015-13292 2017-04691 2017-05923
Work Orders
200573214 200676806 200751271
200665722 200689230
Miscellaneous
ECP-18-0117-001, Temporary Gland Seal Rupture Disk Injection Leak Repair, Revision 0
Unit 2 System 11 Monthly Monitoring Spreadsheet, June 2018
Periodic Assessment of Maintenance Rule Program, Beaver Valley Power Station, July 1, 2015
through February 28, 2017
NOP-ER-3004-3, Maintenance Rule Failure Review Form for CR 2015-14914, October 31, 2015
Unit 2 System 36B Maintenance Rule Review for May 2018, May 16, 2018
Condition Reports
2018-03836 2018-04130 2018-04131 2018-04637
Miscellaneous
Beaver Valley Key Shutdown Defense-in-Depth Turnover Checklist, April 18, 2018
Beaver Valley Key Shutdown Defense-in-Depth Turnover Checklist, April 19, 2018
Defense-in-Depth Protected Equipment, April 18, 2018
Defense-in-Depth Protected Equipment, April 19, 2018
Beaver Valley Key Shutdown Defense-in-Depth Turnover Checklist, April 21, 2018
Defense-in-Depth Protected Equipment, April 21, 2018
Beaver Valley Key Shutdown Defense-in-Depth Turnover Checklist, May 3, 2018
Defense-in-Depth Protected Equipment, May 3, 2018
Beaver Valley Unit 1 Week 05/07/18, Preliminary ICDP Profile for Mode 3 Entry, Revision 0
Beaver Valley Unit 2 Week 05/14/18, T-0 ICDP Profile, Revision 0
Risk Management Plan for 200696943 TR-2A Dry Test 2OST-33.10E
Condition Reports
2018-03496 2018-03498 2018-03824 2018-04186
2018-03497 2018-03544 2018-04033 2018-04820
Work Orders
200748598 200749021 200749224
Miscellaneous
601161892
601166499
601163268
Condition Reports
2018-04004 2018-04033 2018-04186
Work Orders
200687691 200716160 200749224
200687692 200748968 200749225
200716158 200749021 200749226
Condition Reports
2018-02461 2018-03824 2018-04033 2018-04068
2018-03785 2018-03916 2018-04034 2018-04076
2018-03818 2018-04004 2018-04067 2018-04113
Work Orders
200573214 200676806 200695390 200698200
200646499 200687691 200697579 200744746
200665722 200687692 200697982 200748540
200668183 200689230 200697989 200749070
Miscellaneous
601162956
Condition Reports
2018-03355 2018-04213 2018-04848
Miscellaneous
NOP-LP-1009-02, Fatigue Assessment dated April 18, 2018
Empcenter work hours for selected operations and maintenance personnel April 9 through
June 20, 2018
Condition Report
2018-03786
Work Orders
200669679 200698482
Miscellaneous
601161753
Condition Reports (*initiated in response to inspection)
2017-05620 2018-01074 2018-03723
2017-05782 2018-03382 2018-03882*
Surveys
103410, dated April 25, 2018 at 0400
103410, dated April 25, 2018 at 0900
Condition Report (*initiated in response to inspection)
2018-03894*
Air Samples
18-0072 18-0073 18-0074
Condition Reports (*initiated in response to inspection)
2017-09748 2018-03375 2018-03463 2018-03795*
Condition Reports
2018-00793 2018-03457
Miscellaneous
SA-BN-2017-0574, DMC3000 Implementation, dated May 24, 2017
SA-BN-2017-0686, Fleet Radiation Protection External Dosimetry Program, dated
November 16, 2017
NIST NVLAP Accreditation Letter for Lab Code 200750-0, August 16, 2016
71151
Miscellaneous
Unit 1 MSPI Emergency AC Power Systems, April 2017 through March 2018
Unit 1 MSPI High Pressure Injection System, April 2017 through March 2018
Unit 1 Safety System Functional Failures, April 2017 through March 2018
Unit 1 System 07 Maintenance Rule Monthly Monitoring Spreadsheet, May 2018
Unit 1 System 36A Maintenance Rule Monthly Monitoring Spreadsheet, May 2018
Unit 2 MSPI Emergency AC Power Systems, April 2017 through March 2018
Unit 2 MSPI High Pressure Injection System, April 2017 through March 2018
Unit 2 Safety System Functional Failures, April 2017 through March 2018
Unit 2 System 07 Maintenance Rule Monthly Monitoring Spreadsheet, May 2018
Unit 2 System 36A Maintenance Rule Monthly Monitoring Spreadsheet, May 2018
71152
Condition Reports
2015-07271 2017-07350 2018-00080 2018-00147
2017-04061 2017-10581 2018-00142 2018-00570
Miscellaneous
Maintenance Rule (a)(1) Evaluation for CR 2013-07662
Maintenance Rule (a)(1) Evaluation for CR 2014-00448
Maintenance Rule (a)(1) Evaluation for CR 2014-00555
Maintenance Rule (a)(1) Evaluation for CR 2014-05866
Maintenance Rule (a)(1) Evaluation for CR 2014-10156
Maintenance Rule (a)(1) Evaluation for CR 2015-07271
Maintenance Rule (a)(1) Evaluation for CR 2015-08084
Maintenance Rule (a)(1) Evaluation for CR 2015-16299
Maintenance Rule (a)(1) Evaluation for CR 2016-01044
Maintenance Rule (a)(1) Evaluation for CR 2017-06161
Maintenance Rule (a)(1) Evaluation for CR 2017-07122
Maintenance Rule (a)(1) Evaluation for CR 2017-08759
Maintenance Rule (a)(1) Evaluation for CR 2017-11702
Maintenance Rule (a)(2) Evaluation for CR 2014-05866
Maintenance Rule (a)(2) Evaluation for CR 2016-05285
Unit 1 System 24B Monthly Monitoring Spreadsheet, May 2018