IR 05000334/2022001
ML22130A058 | |
Person / Time | |
---|---|
Site: | Beaver Valley |
Issue date: | 05/10/2022 |
From: | Matt Young NRC/RGN-I/DORS |
To: | Grabnar J Energy Harbor Nuclear Corp |
Young M | |
References | |
IR 2022001 | |
Download: ML22130A058 (20) | |
Text
May 10, 2022
SUBJECT:
BEAVER VALLEY POWER STATION, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000334/2022001 AND 05000412/2022001
Dear Mr. Grabnar:
On March 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Beaver Valley Power Station, Units 1 and 2. On April 20, 2022, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Beaver Valley Power Station, Units 1 and 2.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; and the NRC Resident Inspector at Beaver Valley Power Station, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Digitally signed by Matthew R.
Matthew R. Young Date: 2022.05.10 09:51:53 Young -04'00'
Matt R. Young, Chief Projects Branch 2 Division of Operating Reactor Safety Docket Nos. 05000334 and 05000412 License Nos. DPR-66 and NPF-73
Enclosure:
As stated
Inspection Report
Docket Numbers: 05000334 and 05000412 License Numbers: DPR-66 and NPF-73 Report Numbers: 05000334/2022001 and 05000412/2022001 Enterprise Identifier: I-2022-001-0053 Licensee: Energy Harbor Nuclear Corporation Facility: Beaver Valley Power Station, Units 1 and 2 Location: Shippingport, PA 15077 Inspection Dates: January 1, 2022 to March 31, 2022 Inspectors: G. Eatmon, Senior Resident Inspector R. Rolph, Resident Inspector C. Hobbs, Reactor Inspector Approved By: Matt R. Young, Chief Projects Branch 2 Division of Operating Reactor Safety Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Beaver Valley Power Station, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.
Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Not adhering to written procedure results in a manual reactor trip Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green [H.12] - Avoid 71153 NCV 05000412/2022001-01 Complacency Open/Closed A self-revealed Green NCV of Technical Specification 5.4.1, Administrative Controls,
Procedures, was identified when the licensee did not verify that the feed pump recirculating valves were locked open in accordance with plant startup procedures. This resulted in steam generator secondary side water level to increase and a manual reactor trip of Unit 2 on November 12, 2021.
Additional Tracking Items
Type Issue Number Title Report Section Status LER 05000412/2021-004-00 LER 2021-004-00 for Beaver 71153 Closed Valley Power Station, Unit 2,
Manual Reactor Trip LER 05000412/2021-002-00 LER 2021-002-00 for Beaver 71153 Closed Valley Power Station, Unit No. 2, Unit 2, Automatic Reactor Trip and Automatic Actuation of the Auxiliary Feedwater System LER 05000412/2021-003-00 LER 2021-003-00 for Beaver 71153 Closed Valley Power Station, Unit No. 2, Indications Identified During Reactor Vessel Head Inspection
PLANT STATUS
Unit 1 operated at or near rated thermal power for the entire inspection period.
Unit 2 began the inspection period at rated thermal power. On February 25, 2022, the unit experienced a transient that reduced power to 97 percent due to a cooling tower pump over current trip. The unit was returned to rated thermal power later that same day and remained at or near rated thermal power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)
The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of extreme cold temperatures for the following systems on January 19 through 20, 2022:
(1)
- Unit 1 reactor plant river water in the main intake structure
- Unit 2 service water in the main intake structure
- Unit 1 standby river water and the Unit 2 service water in the alternate intake structure
- Unit 2 demineralized water storage tank instrumentation enclosure
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 1, steam driven auxiliary feed water system on February 16, 2022
- (2) Unit 2, low head safety injection system, train 'B' on March 1, 2022
- (3) Unit 1, auxiliary feedwater system, train 'A' on March 16, 2022
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated system configurations during a complete walkdown of the dedicated auxiliary feed water system in the turbine building of Unit 1 on February 8 and 9, 2022
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Unit 1, Diesel Generator 2 Room on February 1, 2022
- (2) Unit 1/Unit 2, main intake structure screen area on February 7, 2022
- (3) Unit 1, AE and DF emergency switchgear rooms on February 15, 2022
- (4) Unit 1/Unit 2, main intake pump cubicles for Unit 1 reactor plant river water, Unit 2 service water, and common fire pumps on February 28, 2022
- (5) Unit 2, East and West 735 cable vaults, fire compartments 2-CV-1 and 2-CV-2 on March 10, 2022
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
- (1) Unit 1, primary auxiliary building elevations 735'-6" flooding due to primary river water line break and impact on charging pump cubicles with access from the 735-6 elevation on February 22, 2022
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)
(1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the Unit 1 control room during flux mapping and '1C' reactor plant river water pump test on B header per 1OST-30.6B on March 11, 2022, and in the Unit 2 control room during
'21B service water pump test per 2OST-30.3 on March 11, 2022
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated Unit 2 operators on March 11, 2022, respond to:
- Multiple instrument failures, 'B' main feedwater pump trip, reactor trip and recovery actions to stabilize the unit in Mode 3
- Fire in the west communications room with spurious action of the 'B' quench spray system, the DF emergency bus de-energize, and emergency action level declaration of an Unusual Event
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (2 Samples)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:
- (1) Unit 2, unexpected control room annunciator for diesel generator 1 electrical fault due to lockout relay, 86-ESGADX1, actuated due to differential current relay, 87-VE210, spuriously actuated, and classified as a functional failure of the Unit 2 emergency diesel generators and support systems (system 36A) on January 3, 2022
- (2) Unit 2, deficient solder joints on universal logic boards for train 'A' of the solid state protection system that interrupted the power range neutron flux permissive and associated power range trip block signals, resulting in a reactor trip, and was classified as a condition monitoring failure of the universal driver card, and transitioned the system to maintenance rule (a)(1) on January 28, 2022
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Unit 2, orange risk due to less than or equal to an 8-hour limiting condition for operation while the 2-1 battery charger was swapped out for the 2-7 battery charger on January 18 and 19, 2022
- (2) Unit 1, emergent work control and risk management when diesel generator number 1 fuel oil transfer pump tripped twice on thermal overload on February 2, 2022
- (3) Unit 2, 21A cooling tower pump motor emergent investigation and replacement due to motor fire during the week of March 7, 2022
- (4) Unit 1 and Unit 2, auxiliary intake dredging, an infrequently performed test or evolution, upstream of the main intake with the most limiting contingency of river water/service water intake structure loss during the week of March 28, 2022
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) Unit 1, quench spray pump 'A', 1QS-P-1A, increased outboard mechanical seal leakage on January 17, 2022
- (2) Unit 2, steam generator A atmospheric steam dump valve discovered with 100 percent automatic demand setpoint and placed in remote manual control on January 28, 2022
- (3) Unit 2, inflatable seal for inner-connecting flood door between pump bay C and pump bay D in the main intake structure was not able to maintain pressure during Flood Door Seal System Operability Check (1/2OST-30.21B) on February 23, 2022
- (4) Unit 1, surveillance frequency exceeded the 92-day requirement for containment penetration verification identified on March 11, 2022
71111.18 - Plant Modifications
Severe Accident Management Guidelines Update (IP Section 03.03) (1 Sample)
- (1) Unit 1 and Unit 2 committed to update the Severe Accident Mitigation Guidelines when the pressurized water reactor owners group generic severe accident technical guidelines were issued in accordance with NEI 14-01, Emergency Response Procedures and Guidelines for Beyond Design Basis Events and Severe Accidents, and the inspectors completed review of the validation and integration of severe accident guidelines in accordance with the process outlines in NEI 14-01 on March 4, 2022
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:
- (1) Unit 1, diesel generator 2 monthly surveillance after fuel oil transfer pump '1C' motor inspection and lubrication on January 4, 2022
- (2) Unit 2, 2OST-13.3, test of the recirculation spray pump, '21A', after preventative maintenance on the pump motor on January 18, 2022
- (3) Unit 1, 1OST-30.2, reactor plant river water pump '1A' test, after pump seal replacement on February 9 through 11, 2022
- (4) Unit 2, diesel generator 2, lube oil sample Test Oil result evaluation from after planned surveillance on February 9, 2022
- (5) Unit 2, diesel generator 2 rocker arm lube oil pressure switch calibration (2ICP-36-PS221-2) on March 8, 2022
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:
Surveillance Tests (other) (IP Section 03.01) (1 Sample)
- (1) Unit 1, Manual Isolation and Control Room Emergency Ventilation System (CREVS)test, 1/2OST-44A.11A/B, train 'A' and train 'B', specifically the manual Control Room Emergency Air Supply Actuation Train 'A'/'B' push button test, on February 21, 2022 for 'A' train and March 7, 2022 for 'B' train
Inservice Testing (IP Section 03.01) (1 Sample)
- (1) Unit 1, 1OST-13.2, train B quench spray pump [1QS-P-1B] on February 28, 2022
71114.06 - Drill Evaluation
Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)
The inspectors evaluated:
- (1) Red Team integrated drill major event sequence was loss of offsite power, dropped rod group with manual reactor trip, loss of coolant accident inside containment, containment radiation levels increase, then loss of containment and radiation release on March 10,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) ===
- (1) Unit 1 for the period of January 1, 2021 through December 31, 2021
- (2) Unit 2 for the period of January 1, 2021 through December 31, 2021 IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)
(2 Samples)
- (1) Unit 1 for the period of January 1, 2021 through December 31, 2021
- (2) Unit 2 for the period of January 1, 2021 through December 31, 2021
IE04: Unplanned Scrams with Complications Sample (IP Section 02.03) (2 Samples)
- (1) Unit 1 for the period of January 1, 2021 through December 31, 2021
- (2) Unit 2 for the period of January 1, 2021 through December 31, 2021
71152A - Annual Follow-Up Problem Identification and Resolution Annual Follow-Up of Selected Issues (Section 03.03)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Reliability issues with Movable Incore Detector System at Unit 1 and Unit 2
71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)
The inspectors evaluated the following licensee event reports (LERs):
- (1) LER 05000412/2021-003-00, Unacceptable Indications Identified During Reactor Vessel Head Inspection (ADAMS Accession No. ML21354A405). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors did not identify a violation of NRC requirements.
- (2) LER 05000412/2021-002-00, Unit 2 Automatic Reactor Trip and Automatic Actuation of the Auxiliary Feedwater System (ADAMS Accession No. ML21337A224). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors did not identify a violation of NRC requirements.
- (3) LER 05000412/2021-004-00, Unit 2 Manual Reactor Trip (ADAMS Accession No. ML22011A283). The inspection conclusions associated with this LER are documented in this report under Inspection Results Section 71153.
Personnel Performance (IP Section 03.03) (1 Sample)
- (1) The inspectors evaluated licensee performance during a Unit 2 transient that reduced power to 97 percent due to a cooling tower pump over current trip on February 25,
INSPECTION RESULTS
Observation: Reliability issues with Movable Incore Detector System at Unit 1 71152A and Unit 2 The inspectors performed an in-depth review of Beaver Valley Power Station corrective actions to address reliability issues for the Movable Incore Detector System (MIDS) at both Beaver Valley Unit 1 and Beaver Valley Unit 2. The MIDS system is functionally the same at both Beaver Valley units, and utilizes five insertable fission chamber detectors to take axial neutron flux maps of the reactor core. The Unit 1 and Unit 2 Licensing Requirements Manual specification 3.3.7 describes the functional characteristics for the system, which are during power ascension following a refueling of the reactor core, thirty-eight thimble tube locations are required to be accessible, with at least two locations in the same core quadrant. Following completion of power ascension to 100 percent full power, and once core conditions are stable, the number of required accessible thimble tube locations drops down to twenty-five, with at least three locations in the same core quadrant required to be accessible, for the system to be considered functional. Full core flux maps are required monthly by various technical specification surveillances during the fuel cycle. When a full core flux map is taken with less than thirty-eight core locations, a penalty is calculated by the core monitoring computer system, and applied to the thermal limit peaking factors specified in the Core Operating Limits Report for the current reactor fuel cycle. Non-functionality of MIDS during reactor startup has the potential to prevent completion of power ascension to 100 percent full power. Non-functionality of MIDS during fuel cycle operation has the potential for a technical specification surveillance for a full core flux map to not be completed within the specified time allowed by the surveillance frequency control program.
On March 11, 2022, the Unit 1 MIDS was functional with twenty-six core locations accessible for flux map readings including the "Calibrate" position, leaving a margin of two thimble tube locations before non-functionality of the system. The licensee has identified various causes for the reduction in the number of accessible thimble tube locations on Unit 1 during the current fuel cycle. The causes include failed fission chamber detectors, thimble tube leakage, and thimble tube blockage. Actions are ongoing to restore thimble tube locations to functional status on Unit 1. The Unit 2 MIDS was also functional on March 11, 2022, with forty-six thimble tube locations accessible. Eleven thimble tube locations were restored to functional status following thimble tube cleaning in the Unit 2 fall 2021 refueling outage. No performance deficiencies were identified by the inspectors.
Corrective Action References: CR-2021-04211, CR-2021-05894, CR-2021-08585, CR-2022-01246 Not adhering to written procedure results in a manual reactor trip Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green [H.12] - Avoid 71153 NCV 05000412/2022001-01 Complacency Open/Closed A self-revealed Green NCV of Technical Specification 5.4.1, Administrative Controls, Procedures, was identified when the licensee did not verify that the feed pump recirculating valves were locked open in accordance with plant startup procedures. This resulted in steam generator secondary side water level to increase and a manual reactor trip of Unit 2 on November 12, 2021.
Description:
On November 12, 2021, at 1007, during Unit 2 startup activities following the Unit 2 refueling outage (2R22), the reactor operator manually tripped the reactor due to secondary side high steam generator water level greater than 85 percent in accordance with BVPS-OPS-0024, "Transient Response Guidelines". Following the trip, operators recovered control of steam generator water level and stabilized the reactor in Mode 3.
Rising steam generator water level occurred due to main feed pump recirculation valves oscillating open and closed. The recirculating valves oscillated because they were not locked in the open position and moved on demand as the turbine valve testing caused the steam dump valves to oscillate open and closed. Each time the recirculating valves closed due to demand; the feed water pumps pumped more water into the secondary side of the steam generators. The plant startup procedure, 2OM-52.4A, Raising Power from 5 percent to Full Load Operation, steps 6.b. and 6.c, state to place the main feed pump recirculation valve key lock switches in the open position. These steps were initialed completed when in fact the key lock switches for 2FWR-FCV-150A and 150B were in the auto position and not in the open position as required by procedure.
The licensee entered the issue into their corrective action program (CR-2021-08663 and CR-2021-08670). They conducted an initial investigation and review per NOP-LP-2601, Procedure/Work Instruction use and Adherence. Subsequently, an event review was conducted in accordance with 1/2-ADM-0703, Event Review. The licensee determined, based on its human performance investigation, that operators did not adequately use the human performance tools: self-checking, verify and validate, proper 3-way communication, and procedure use and adherence. The review and initial investigation concluded that the apparent cause was operators did not adhere to the plant startup procedure and the direct cause was leaving the feed water recirculating valves in the auto position instead of placing them in the locked open position. Licensee corrective actions included: change the procedure to include an action verb in the step and implementing an operations leadership plan.
Corrective Action References: CR-2021-08663, CR-2021-08670
Performance Assessment:
Performance Deficiency: The inspectors determined that not verifying the key lock switch for 2FWR-FCV-150A and 150B was placed in the locked open position, in accordance with 2OM-52.4A, Raising Power from 5 percent to Full Load Operation," was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Configuration Control attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, on November 12, 2021, the licensee failed to follow plant procedures and verify key lock switches were in the open position for the main feed pump recirculating valves before proceeding with turbine startup and valve testing during plant startup and lead to a manual reactor trip.
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power.
Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. Based on the licensee's human performance investigation, operators used control board indication, which only provides the current position of the valves, to base a decision and sign off the procedure that the valves were in a locked open position. Operators did not use appropriate human performance tools during implementation of the of the applicable startup procedure.
Enforcement:
Violation: Technical Specification 5.4.1, Administrative Controls, Procedures," states, in part, that written procedures shall be established, implemented, and maintained covering the following activities:
a. The applicable procedures recommended in Regulatory Guide 1.33, Quality Assurance Program Requirements, Revision 2, Appendix A, February 1978.
Regulatory Guide 1.33 Revision 2, Appendix A, February 1978, Section 3 lists procedures for startup.
Licensee procedure 2OM-52.4A, "Raising Power from 5 percent to Full Load Operation," was established to cover activities for startup. Procedure 2OM-52.4A directed that the key lock switches for 2FWRFCV-150A and 150B be verified in the locked open position.
Contrary to the above, on November 12, 2021, the key lock switches for 2FWRFCV-150A and 150B were not verified in the locked open position. This resulted in steam generator secondary side water level to increase above 85 percent and caused a manual reactor trip.
Enforcement Action: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On March 11, 2022, the inspectors presented the Reliability issues with the Movable Incore Detector System at Unit 1 and Unit 2 inspection results to Mr. Mark Manoleras, Director, Site Engineering, and other members of the licensee staff.
- On April 20, 2022, the inspectors presented the integrated inspection results to Mr. John Grabnar and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.01 Corrective Action 2021-01186
Documents 2021-02608
22-00519
Procedures U1/U2-OST-45.1 Extreme Cold Weather Protection Verification Revision
2dsssss
71111.04 Drawings RM-0411-001 Valve Oper NO Diagram Low/High Head Safety Injection Revision 23
RM-0424-001 Valve Oper No Diagram Feedwater System Revision 20
RM-0424-002 Valve Oper No Diagram Feedwater System Revision 20
RM-0424-003 Valve Oper No Diagram Feedwater System Revision 16
Procedures 1OM-24.4.W Emergency Use Of [1FW-P-2] Turbine-Driven Auxiliary Feed Revision 3
Pump
1OM-53A.1.2-K Dedicated AFW Pump[1FW-P-4] Startup Revision 4
1OST-24.2 Motor Driven Auxiliary Feed Pump Test [1FW-P-3A] Revision 58
1OST-24.3 Motor Driven Auxiliary Feed Pump Test [1FW-P-3B] Revision 55
1OST-24.4 Steam Turbine-Driven Auxiliary Feed Pump Test Revision 65
1OST-24.7 Dedicated Auxiliary Feed Pump [1FW-P-4] Test Revision 18
1OST-24.9 Turbine-Driven AFW Pump [1FW-P-2] Operability Test Revision 63
2OST11.2 Low Head Safety Injection Pump [2SIS*P21B] Test Revision 34
RM-0424-002 Valve Oper No Diagram Feedwater System Revision 20
Work Orders 200618427 Inspection of chain operated handwheel
200640863 Retorque MOV packing
200798277 Install Safety Tether on Chainwheel Hub
200798278 Install Safety Tether on Chainwheel Hub
200819451 AFW Pump FW-P-4 Test
200825078 Dedicated aux FW panel 2 pb not working (to display the
motor outboard bearing temperature)
200851923 Threaded Operator Stripped
200852945 Template schedule Loop/Calibra/Check
200852956 Lubricate valve operator per PMP
200859369 Sample both pump oil reservoirs
200873583 Obtain oil sample from each motor lube oil reservoir
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.05 Corrective Action 2022-02256
Documents
Resulting from
Inspection
Procedures 1/2-ADM-1900 Fire Protection Program Revision 48
1/2-ADM-1901 Fire Protection Pre-Fire Plan Administrative Control Revision 4
1PFP-DGBX-735- Pre-fire Plan for Diesel Generator 2 Room Fire Compartment Revision 2
DG-2 1-DG-2
1PFP-INST-705- Pump Cubicles, Pre-Fire Plan Fire Compartment 3-IS-1, 2, 3, Revision 2
Pump 4
1PFP-INST-705- Pre-Fire Plan Fire Compartment 3-IS-6 Revision 2
SCREEN
1PFP-SRVB-713- AE Switchgear Room, Pre-Fire Plan Fire Compartment 1-ES-1 Revision 3
AE
1PFP-SRVB-713- DF Switchgear Room, Pre-Fire Plan Fire Compartment 1-ES- Revision 2
DF 2
BVPS FSA Beaver Valley Fire Safety Analysis Report Revision 2
U1/U2-ADM-1900 Fire Protection Program Revision 48
U1/U2-ADM-1905 Control of Transient Combustible and Flammable
71111.06 Miscellaneous Design Analysis PAB Flood Level Resulting from REJ-18 Failure 12/16/1987
Calculation 8700-
30-19
Procedures 1-MSM-M-33-300 Unit 1 Flood Seals Visual Inspection effective
4/9/2018
1/2-PIP-M16 Unit 1/Unit 2 Penetration Seals Revision 11
71111.11Q Miscellaneous BV2 Power Block Fire, Lesson Plan G-OTLC-22-2S- Revision 0
PBFIRE_BV2
Procedures 1OST-30.6B Reactor Plant River Water Pump 1C Test on Train 'B' Header Revision 48
2OST-30.3 Service Water Pump [2SWS*P21B] Test Revision 53
71111.12 Corrective Action 2021-07409
Documents 2021-08199
21-09369
Miscellaneous Maintenance Rule Failure Evaluation for CR2021-070409 11/4/2021
Maintenance Rule (a)(1) Evaluation for CR-2021-07409 1/28/2022
Inspection Type Designation Description or Title Revision or
Procedure Date
Unit 2, Maintenance Rule System Basis Document, Reactor 9/15/2021
Control and Protection System (01)
Unit 2 Westinghouse Solid State Protection System Technical Revised
Manual 2/19/2019
Maintenance Rule Failure Review Form for CR2021-09360
Unit 2 Emergency Diesel Generator & Support Systems, System 26A Revision 8
Maintenance Rule
System Basis
Document
Work Orders 2008
71111.13 Corrective Action 2022-00415
Documents 2022-00801
Miscellaneous Risk Management Plan 2/25/2022
Job Safety Analysis 3/7/22
Beaver Valley Unit 1 Week 1/31/2022, T-0 Rev1 ICDP Profile
2CWS-21A/B/C/D Allis-Chalmers Motor Lift Plan
2CWS-21A/B/C/D Westinghouse Motor Lift Plan
Procedures 1/2OM-30.4A.E Unit1/2 River Water and Service Water Operation While Revision 6
Dredging Near Intake and Alternate Intake Structures
1OM- River Water/Main Intake Structure Loss Revision 9
53C.4.1.30.2
2OM- Service Water/Main Intake Structure Loss Revision 9
53C.4.2.30.1
2OM.39.4.O Spare Battery Charger Operationx for BAT*2-1 Revision 6
NOP-LP-2601 Procedure/Work Instruction USE and Adherence Revision 6
71111.15 Corrective Action 2022-00357
Documents 2022-00430
22-00661
22-01425
22-02020
Miscellaneous Temporary Log for Seal Leakage for EER 601345084 once
per 8 hrs
Visual Examination System Leakage (VT-2) for System 13 4/15/2020
Inspection Type Designation Description or Title Revision or
Procedure Date
Engineering Evaluation Request Notification 601345084 1/17/2022
Email from Robert Garver to Gwynne Eatmon on 2/17/2022,
regrading Safety Bushing Controlled Leakoff
1OST-47.2 completed
surveillance
on
2/24/2021
Calculation 8700- BVPS Intake Structure Cubicles Internal Flood Analysis Revision 2
DMC-3443
Procedures 1/2OM-48.1I Technical Specification Compliance Revision 37
1/2OST-30.21B Group 2 Flood Door Seal System Operability Check Revision 16
1OST-13.1 Quench Spray Pump (1QS-P-1A) Test Revision 47
1OST-47.2 Containment Penetration Verification Revision 45
2OST-47.3M Containment Penetration and ASME Valve Test - Work Week Revision 43
Work Orders 200802193
71111.18 Miscellaneous Procedure Approval Form, Diagnostic Process Guidelines, effective
Tracking no. 18-00589 02/27/2019
Procedure Approval Form, Initial Response, Tracking no. 18- effective
00550 02/28/2019
Procedure Approval Form, Initial Response, Tracking no. 18- effective
00535 02/27/2019
Procedure Approval Form, Diagnostic Process Guidelines, effective
Tracking no. 18-00601 02/28/2019
71111.19 Corrective Action 2022-01044
Documents
Corrective Action 2022-01250 Two of the sealants to be used for the seal replacement were
Documents expired
Resulting from
Inspection
Drawings RM-0413-001 Valve Poer No Diagram Recirculation Spray System Revision 12
Miscellaneous TestOil Industrial Analysis for 2EGS-EG2-2-ER 02/11/2022
Vender Manual Colt Industries, Operation and Maintenance Manual for dated
2502.190-230- Emergency Diesel Generators 08/7/2019
Inspection Type Designation Description or Title Revision or
Procedure Date
001
Procedures 1CMP-M-30-001 River Water Pump Overhaul Revision 15
1MSP-36.32-E No 1C Diesel Generator Fuel Oil Transfer Pump Motor and 12/27/2005
Linestarter Inspection
1OST-30.2 Reactor Plant River Water Pump 1A Test Revision 67
1OST-36.2 Operating Surveillance Test, Diesel Generator No. 2 Monthly Revision 86
Test
2ICP-36-PS211-2 Diesel Generator 2-2 Rocker Arm Lube Oil Pressure Switch effective
Calibration 1/31/2022
2OST-13.3 Recirculation Spray Pump[2RSS*P21A] Dry Test Revision 15
Work Orders 200812266
200870816 Reactor Plant River Water Pump 1A
71111.22 Corrective Action 2022-00314
Documents 2022-01563
Procedures 1/2OST-44A.11A Areas Ventilation System - Control Area Operating Revision 16
Surveillance Test, Train 'A' Manual Isolation/CREVS System
Test
1/2OST-44A.11B Areas Ventilation System - Control Area Operating Revision 16
Surveillance Test, Train 'B' Manual Isolation/CREVS System
Test
1OST-13.2 Quench Spray [1QS-P-1B] Test Revision 50
71114.06 Corrective Action 2022-01973
Documents 2022-01990
22-01996
71151 Corrective Action 2022-01595
Documents
71152A Calibration 1RST-49.2 Power Distribution Limit Check 01/20/2022
Records 1RST-49.2 Power Distribution Limit Check 01/06/2022
2RST-49.2 Power Distribution Limit Check 02/03/2022
2RST-49.2 Power Distribution Limit Check 03/03/2022
Corrective Action 2020-05984,
Documents 2020-06555,
21-03866,
21-04211,
Inspection Type Designation Description or Title Revision or
Procedure Date
21-05205,
21-05894,
21-07339,
21-07881,
21-08585,
21-08943,
22-00841,
22-01246
Miscellaneous ITS Beaver Valley Power Station, Improved Standard Technical 04/20/20
Specifications
LRM Beaver Valley Unit 1 Licensing Requirements Manual Revision 105
LRM Beaver Valley Unit 1 Licensing Requirements Manual Revision 95
Procedures ISIE-ECP-3 Flux Thimble Examination Program Revision 8
ML-FOP-013 Beaver Valley Flux Thimble Tube Cleaning Revision 1
Work Orders 200543039,
200645597,
200701649,
200763754,
200763896,
200796262
71153 Corrective Action 2022-01512
Documents
17