IR 05000293/2018003

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Integrated Inspection Report 05000293/2018003 and Independent Spent Fuel Storage Installation Inspection Report 07201014/2018001
ML18317A038
Person / Time
Site: Pilgrim, Holtec
Issue date: 11/13/2018
From: Anthony Dimitriadis
NRC/RGN-I/DRP/PB5
To: Brian Sullivan
Entergy Nuclear Operations
Dimitriadis A
References
IR 2018001, IR 2018003
Download: ML18317A038 (21)


Text

ber 13, 2018

SUBJECT:

PILGRIM NUCLEAR POWER STATION - INTEGRATED INSPECTION REPORT 05000293/2018003 AND INDEPENDENT SPENT FUEL STORAGE INSTALLATION INSPECTION REPORT 07201014/2018001

Dear Mr. Sullivan:

On September 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Pilgrim Nuclear Power Station (Pilgrim). On October 24, 2018, the NRC inspectors discussed the results of this inspection with you and other members of your staff.

The results of this inspection are documented in the enclosed report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Pilgrim. In addition, if you disagree with the cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at Pilgrim. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Anthony Dimitriadis, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Number: 50-293 License Number: DPR-35

Enclosure:

Inspection Report 05000293/2018003 and 07201014/2018001

Inspection Report

Docket Number: 50-293 License Number: DPR-35 Report Numbers: 05000293/2018003 and 07201014/2018001 Enterprise Identifier: I-2018-003-0061 Licensee: Entergy Nuclear Operations, Inc. (Entergy)

Facility: Pilgrim Nuclear Power Station (Pilgrim)

Location: Plymouth, Massachusetts Inspection Dates: July 1, 2018 to September 30, 2018 Inspectors: E. Carfang, Senior Resident Inspector B. Pinson, Resident Inspector P. Boguszewski, Project Engineer B. DeBoer, Health Physicist O. Masnyk Bailey, Health Physicist K. Mangan, Senior Resident Inspector S. Wilson, Health Physicist M. Hardgrove, Project Engineer Z. Hollcraft, Senior Resident Inspector J. Dolecki, Resident Inspector Approved By: Anthony Dimitriadis, Chief Reactor Projects Branch 5 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Entergys performance at Pilgrim by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC-identified and self-revealing findings, violations, and additional items are summarized in the table below.

List of Findings and Violations Failure to Identify an Adverse Condition Associated with Elevated Standby Gas Treatment System Accumulator Leakage Cornerstone Significance Cross-Cutting Inspection Aspect Results Section Barrier Integrity Green H.9 - Human 71111.19 NCV 05000293/2018003-01 Performance -

Closed Training The inspectors identified a Green non-cited violation (NCV) of Technical Specifications 3.7.B.1.c because Entergy exceeded the TS allowed outage time for the standby gas treatment system (SBGT) when the station did not identify an adverse condition associated with elevated air accumulator leakage in the system.

Additional Tracking Items Type Issue number Title Inspection Status Results Section SLIV 05000325/2018014-01 Surveillance Test on Other Closed NOV the Reactor Core Activities -

Isolation Cooling Temporary System Instructions,

Infrequent and Abnormal LER 05000293/2017-001-01 Reactor Building 71153 Closed Isolation Dampers Failed to Isolate LER 05000293/2017-002-00 Isolation of HPCI 71153 Closed LER 05000293/2017-003-01 Supplement to 71153 Closed Suppression Pool Declared Inoperable Due to High Water Level

LER 05000293/2018-001-00 Manual Reactor Scram 71153 Closed Due To Loss of One Offsite Transmission Line LER 05000293/2018-004-00 Automatic Emergency 71153 Closed Diesel Generator System Actuation Caused by Loss of Offsite Power LER 05000293/2018-005-00 Condition Prohibited by 71153 Closed Technical Specifications Involving Standby Gas Treatment System Pneumatic Leakage Rate

PLANT STATUS

The unit began the inspection period at full power. On August 14, 2018, operators lowered power to approximately 40 percent to perform a thermal backwash of the main condenser, and returned the unit to full power on August 15, 2018. On August 17, 2018, operators lowered power to approximately 40 percent as a result of degrading main condenser parameters and elevated ultimate heat sink temperatures. On August 18, 2018, the unit was returned to approximately 90 percent. On August 19, 2018, operators lowered power to approximately 45 percent due to elevated ultimate heat sink temperatures, and returned the unit to approximately 90 percent on August 24, 2018. On August 27, 2018, operators lowered power to approximately 40 percent due to elevated ultimate heat sink temperatures, and returned the unit to approximately 90 percent on August 28, 2018. On August 30, 2018, operators lowered power to approximately 40 percent due to elevated ultimate heat sink temperatures, and returned the unit to approximately 95 percent power on September 6, 2018. On September 7, 2018, operators lowered power to approximately 70 percent due to elevated ultimate heat sink temperatures, and returned the unit to approximately 90 percent power on September 11, 2018. On September 12, 2018, operators lowered power to approximately 45 percent due to elevated ultimate heat sink temperatures, and returned the unit to full power on September 25, 2018. The unit remained at or near full power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess Entergys performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment Partial Walk down

The inspectors evaluated system configurations during partial walk downs of the following systems/trains:

(1) A SBGT system with B SBGT system out-of-service for emergent maintenance on July 18, 2018
(2) 'A' residual heat removal system pump with B residual heat removal system pump unavailable due to surveillance testing on August 16, 2018
(3) Instrument air during K-117 (diesel air compressor) system outage on August 23, 2018
(4) High pressure coolant injection valve alignment verification on August 30, 2018.

71111.05A/Q - Fire Protection Annual/Quarterly Quarterly Inspection

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Diesel driven fire pump on August 6, 2018
(2) Turbine generator auxiliaries and turbine truck lock on August 16, 2018
(3) A and B reactor building closed cooling water pump rooms on August 21, 2018
(4) Trash compacting facility on September 26, 2018
(5) Reactor core isolation cooling quadrant on September 27, 2018

71111.07 - Heat Sink Performance Heat Sink

The inspectors evaluated Entergys monitoring and maintenance of reactor building closed cooling water heat exchanger fouling evaluations performed on August 10, 2018.

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification

The inspectors observed and evaluated the following:

(1) The inspectors observed a simulator evaluation that involved an inadvertent initiation of high pressure coolant injection, a leak inside of containment, a manual scram, lockout of the A-1 Bus, a loss of feedwater injection, and emergency depressurization on September 12, 2018
(2) The inspectors observed a simulator evaluation that involved the failure of a control rod drive flow control valve, a malfunction of pressure regulation leading to oscillations, a failed open safety relief valve, an anticipated transient without scram, and standby liquid control initiation on September 12, 2018

Operator Performance (1 Sample)

The inspectors observed and evaluated activities associated with the following licensed operator performance in the control room:

(1) Main condenser thermal backwash with degraded condenser parameters on August 14, 2018
(2) Power ascension following degraded ultimate heat sink temperatures on August 28, 2018

71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) SBGT system
(2) Intake and emergency diesel generator roofs structural inspection
(3) Emergency switchgear ventilation system

71111.13 - Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Emergent corrective maintenance on 4160 volt bus A8 battery that resulted in station blackout diesel generator unavailability on July 30, 2018
(2) Elevated risk during B emergency diesel generator logic system functional testing on August 13, 2018
(3) Elevated risk for planned surveillance testing of the residual heat removal system on August 14, 2018
(4) Elevated risk during shutdown transformer and station blackout diesel generator planned maintenance on August 20, 2018
(5) Emergent corrective maintenance resulting in the unavailability of the standby liquid control system on September 14, 2018

71111.15 - Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) B emergency diesel generator elevated lube oil temperature (CR 2018-5698) on July 11, 2018
(2) SBGT system operable with compensatory measures on July 23, 2018
(3) Outboard main steam isolation valve terminal blocks in J623, J624, J625, and J626 environmental qualification service life extension after missed planned maintenance on July 30, 2018
(4) Shutdown transformer operability with degraded A8 battery on August 1, 2018
(5) B emergency diesel generator operability following high jacket water temperatures on August 6, 2018
(6) Station blackout diesel generator functionality with A8 battery degraded on August 9, 2018
(7) Primary containment operability following leak on feedwater check valve 62B on September 10, 2018

71111.18 - Plant Modifications

The inspectors evaluated the following temporary or permanent modifications:

(1) Temporary modification (EC 78705) to de-energize SV-L-58 and SV-L-67 to change the pressure boundary in the SBGT system on July 23, 2018
(2) A8 battery replacement (EC 78963) on August 20, 2018

71111.19 - Post Maintenance Testing

The inspectors evaluated post maintenance testing for the following maintenance and repair activities:

(1) SBGT system compressed air system leak repairs on July 24, 2018
(2) Cathodic protection installation on August 7, 2018
(3) A8 battery replacement on August 20, 2018
(4) F15 vacuum switch replacement on August 21, 2018
(5) Main steam isolation valve 2D limit switch repair on September 4, 2018
(6) B standby liquid control squid valve cartridge replacement on September 14, 2018

71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: Routine

(1) 8.M.2-3.6.5, Neutron Monitoring System Flow Converter Functional and Calibration Test on July 10, 2018
(2) 3.M.3-47.1, A Emergency Diesel Generator Turbo Assist Air Compressor Load Shed Functional Test on August 27, 2018
(3) 8.M.2-2.10.1, Core Spray Pump 'A' Logic System Functional Test on September 5, 2018

In-service (1 Sample)

(1) A core spray pump quarterly operability test on September 4, 2018

71114.06 - Drill Evaluation Drill/Training Evolution

The inspectors observed a simulator training evolution drill, and exercise performance evaluation for licensed operators on September 12,

RADIATION SAFETY

71124.02 - Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls Verification of Dose Estimates and Exposure Tracking Systems

The inspectors reviewed the current annual collective dose estimate, basis methodology, and measures to track, trend, and reduce occupational doses for ongoing work activities.

The inspectors evaluated the adjustment of exposure estimates, or re-planning of work. The inspectors reviewed post-job ALARA evaluations. The inspectors reviewed the whole body counter calibration and weekly quality control records.

Implementation of ALARA and Radiological Controls (1 Sample)

The inspectors reviewed radiological work controls and ALARA practices during the observation of in-plant work activities. The inspectors verified use of shielding, contamination controls, airborne controls, radiation work permit controls, and other work controls were consistent with ALARA plans. The inspectors ensured that work-in-progress reviews were performed in a timely manner and adjustments made to the ALARA estimates when appropriate. The inspectors reviewed the results achieved against the intended ALARA estimates to confirm adequate implementation and oversight of radiological work controls. The inspectors also verified that the ALARA staff was involved with emergent work activities and were revising both dose estimates and ALARA controls in the associated radiation work permits and ALARA plans, as appropriate. The inspectors reviewed ALARA Committee Meeting Minutes, station dose exposure estimates for 2017-2018, radiation work permit planning and dose estimates, dose estimate adjustments, source term reduction efforts, and total effective dose equivalent ALARA evaluations for activities in airborne areas.

Radiation Worker Performance (1 Sample)

The inspectors observed radiation worker and radiation protection technician performance during radiological work in the Radwaste Truck Lock area while workers removed the resin fill head and performed radiological surveys. The observations were conducted to evaluate worker ALARA performance according to specified work controls and procedures.

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation Engineering Controls

The inspectors evaluated the airborne controls and monitoring. The inspectors observed temporary ventilation system setups and portable airborne radioactivity monitoring systems, and verified the stations established alarm set points for evaluating levels of airborne for both beta and alpha emitting radionuclides. The inspectors also observed the required ventilations systems associated with safe shutdown of the plant. The systems and system health report were reviewed with the system engineer.

Use of Respiratory Protection Devices (1 Sample)

The inspectors evaluated the respiratory protection program. The inspectors reviewed the stations ALARA reviews and the storage, selection, and use of respiratory protection devices and verified that air used in supplied air devices meets or exceeds Grade D quality. The inspectors also reviewed the qualifications of several individuals to ensure the individuals were qualified to use respiratory protections devices.

Self-Contained Breathing Apparatus for Emergency Use (1 Sample)

The inspectors evaluated the self-contained breathing apparatus program. The inspectors verified that selected personnel who are required to use self-contained breathing apparatus were trained and qualified and that the control room was stocked with an adequate variety of respirator face pieces.

71124.05 - Radiation Monitoring Instrumentation Walk Downs and Observations

The inspectors evaluated radiation monitoring instrumentation during plant walk downs to include the following:

(1) Portable survey instruments
(2) Radiation area monitors and continuous air monitors
(3) Personnel contamination monitors, portal monitors, and small article monitors
(4) High range monitors

Calibration and Testing Program (1 Sample)

The inspectors evaluated Entergys calibration and testing program. The inspectors specifically assessed the following instruments and equipment:

(1) Laboratory instrumentation
(2) Post-accident monitoring instrumentation
(3) Portal monitors, personnel contamination monitors, and small article monitors
(4) Portable survey instruments, area radiation monitors, and air samplers/continuous air monitors
(5) Instrument calibrators
(6) Calibration and check sources
(7) Electronic alarming dosimeters

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification The inspectors verified Entergys performance indicators submittals listed below for the period from July 1, 2017 through June 30, 2018.

(1) High pressure injection systems
(2) Heat removal systems
(3) Residual heat removal systems

71152 - Problem Identification and Resolution Annual Follow-up of Selected Issues

The inspectors reviewed Entergys implementation of its corrective action program related to the following issues:

(1) Condition Reports CR-PNP-2018-2144, Loss of Offsite Power during March 14, 2018 blizzard and CR-PNP-2018-2393, Startup Transformer Oil Analysis
(2) Condition Report CR-PNP-2016-08657, High Pressure Coolant Injection inoperable, high vibrations on P4H
(3) Condition Reports CR-PNP-2017-8678 and CR-PNP-2017-9140, NRC cross-cutting aspects exceeding the threshold in problem identification and resolution areas

71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000293/2017-001-01, Reactor Building Isolation Dampers Failed to Isolate (ADAMS Accession No. ML17220A065). The inspectors reviewed the updated LER submittal. The circumstances surrounding this LER are documented in Inspection Report 05000293/2017002, Section 4OA3.2.
(2) LER 05000293/2017-002-00, Isolation of HPCI (ADAMS Accession No. ML17163A179).

The circumstances surrounding this LER are documented in EA-17-143 (ADAMS Accession No. ML18052B084)

(3) LER 05000293/2017-003-01, Supplement to Suppression Pool Declared Inoperable Due to High Water Level (ADAMS Accession No. ML17325A984). The inspectors reviewed the updated LER submittal. The circumstances surrounding this LER are documented in Inspection Report 05000293/2017002, Section 4OA3.1.
(4) LER 05000293/2018-001-00, Manual Reactor Scram Due To Loss of One Offsite Transmission Line (ADAMS Accession No. ML18079A105). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.
(5) LER 05000293/2018-004-00, Automatic Emergency Diesel Generator System Actuation Caused by Loss of Offsite Power (ADAMS Accession No. ML18152A864). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.
(6) LER 05000293/2018-005-00, Condition Prohibited by Technical Specifications Involving Standby Gas Treatment System Pneumatic Leakage Rate (ADAMS Accession No. ML18260A084). The circumstances surrounding this LER are documented in the Inspection Results section of this report.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL 60855.1 - Operation of an Independent Spent Fuel Storage Installation The inspectors evaluated Pilgrims independent spent fuel storage installation cask loadings on July 9-18, 2018. Specifically, the inspectors observed the following activities:

- Fuel selection and fuel loading

- Heavy load movement of HI-TRAC and loaded multi-purpose canister

- Closure welding and non-destructive weld evaluations

- Transfer and transport evolutions

- Radiological field surveys 92702 - Follow Up on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, and Alternate Dispute Resolution Confirmatory Orders During the week of July 9, 2018, the inspectors performed an onsite review of Pilgrims records related to corrective actions taken in response to a Severity Level IV Notice of Violation (NOV) issued to Entergy. On February 27, 2018, the NRC issued a Severity Level IV NOV of a condition of its NRC license as specified in the facility technical specifications (VIO 05000293/2018014, NRC Office of Investigation Report 1-2017-011, ADAMS Accession No. ML18052B084). Specifically, the inspectors reviewed procedures, corrective action program documents, and casual evaluations. The inspectors also conducted interviews with Entergy staff within Maintenance and Operations discussing the high pressure coolant injection isolation event and the corrective actions taken by Entergy.

INSPECTION RESULTS

Observation 71152 Annual Follow-up of Selected Issues The inspectors reviewed two adverse condition analyses performed on the March 13, 2018, loss of offsite power due to the startup transformer failure. The startup transformer lockout was the result of an internal arc from three high impendence faults. The inspectors reviewed the corrective actions taken to address the issues and concluded that both analyses were of sufficient technical depth to understand adverse weather challenges to the switchyard. The corrective action to replace the startup transformer addressed concerns of potential transformer degradation caused by the faults, and a review of past storm conditions validated Pilgrims severe weather procedure requirements.

Observation 71152 Annual Follow-up of Selected Issues The inspectors reviewed the root cause analysis and corrective actions taken to address increased vibrations on the high pressure coolant injection main pump outboard bearing in the horizontal direction. The inspectors concluded that the analysis was of sufficient technical depth to identify the causes of the increased vibration and that the corrective actions to add mass to change the resonance frequency of the pump addressed the problem and reduced vibrations to within the expected range.

Observation 71152 Annual Follow-up of Selected Issues The inspectors evaluated two of Entergys common cause analysis (CR-PNP-2017-8678 and CR-PNP-2017-9140) to review corrective actions to address exceeding the NRC threshold for cross-cutting aspects in the area of Problem Identification and Resolution. Inspectors reviewed corrective actions, conducted interviews, and reviewed a sampling of condition reports and work orders to verify the corrective action program was being implemented as required by EN-LI-102, Corrective Action Program.

Inspectors reviewed the causal factors related to site prioritization of work and management practices to focus resources on the correct items. As part of the backlog reduction plan, extensive walk downs of systems were performed by operators and engineers, as well as review of condition reports for adverse conditions. Inspectors identified that Entergy, in an effort to reduce the backlog numbers, incorrectly categorized several condition reports as non-adverse. Inspectors sampled 19 random condition reports from a list of over 500 condition reports downgraded from adverse to non-adverse, and identified nine as being adverse conditions per EN-LI-102. EN-LI-102, Section 3.0.2, defines an adverse condition as affecting a) design basis, b) licensing basis, c) regulations and commitments, and f)equipment required to support safety-related equipment as defined by the functionality process in EN-LI-104, Self-Assessment and Benchmark Process. By placing condition reports in a less significant category, less stringent controls are in place to ensure timely corrective actions are made, in accordance with EN-LI-102. Corrective actions 5, 6, and 7 of CR-PNP-2017-8678 directed the cancellation of non-adverse corrective actions greater than 180 days old, unless completion is deemed appropriate by the responsible manager.

Inspectors then validated that the items categorized incorrectly as non-adverse had valid work orders in the work management system. Forty of approximately 500 work orders were reviewed, and only two items were found incorrectly classified as non-adverse with cancelled work orders. One was for a non-safety-related fire protection valve that would not completely isolate and the other for a high energy line break barrier that was degraded. For both items the inspectors determined that the equipment was degraded but remained functional.

Therefore, in accordance with IMC 0612, Issue Screening, these performance deficiencies were not considered more-than-minor because, each cancelled work order, by itself, did not adversely affect a cornerstone objective, could not be considered a precursor to a significant event, did not affect a performance indicator result, and if left uncorrected would not have the potential to lead to a more significant safety concern. Entergy entered the items into the corrective action program and inspectors verified valid work orders were written.

Observation 92702 Follow Up on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, and Alternate Dispute Resolution Confirmatory Orders The inspectors concluded that Entergy staff completed a timely and adequate evaluation to identify the causes of the traditional enforcement violation. Entergys corrective actions included additional observations by management of the Maintenance department, disciplinary action against the three Nuclear Controls Technicians involved in the event, and the Pilgrim Leadership Team developed and implemented a Human Performance Events Response Plan in April 2017. The Human Performance Events Response Plan consisted of four focus areas:

Organizational Alignment, Reinforcement of Expectations, Field Presence, and Culpability.

The inspectors concluded that Entergys actions were timely, appropriate, and sufficient to address the identified deficiency.

Failure to identify an Adverse Condition associated with elevated Standby Gas Treatment System accumulator leakage Cornerstone Significance Cross-Cutting Report Aspect Section Barrier Green H.9 - Human 71111.19 Integrity NCV 05000293/2018003-01 Performance -

Closed Training The inspectors identified a Green non-cited violation of Technical Specifications 3.7.B.1.c because Entergy exceeded the TS allowed outage time for the standby gas treatment system when the station did not identify an adverse condition associated with elevated air accumulator leakage in the system.

Description:

On June 26, 2018, the B train of SBGT was declared inoperable following a System Engineers identification of elevated air accumulator leakage above the calculated design limit of 1.99 psi/day, and Limiting Condition for Operation (LCO) 3.7.B.1.c was entered (CR-PNP-2018-5428). During plant operation, adequate air pressure must be available in the SBGT accumulators to reposition dampers and to maintain dampers in the correct position following cycling. If air pressure is reduced below the required limit, there may not be enough force to reposition and maintain the required position of dampers for the systems full mission time of 30 days. The B train was declared inoperable because when accumulator pressure is lost, dampers fail to a closed position. The A train of SBGT was not affected because the A train dampers that are required to maintain operability fail in the open position. As a result, the A train of SBGT maintains its ability to perform its specified safety function when accumulator pressure is lost. The leakage was addressed through the corrective action program and an Operations standing order (Standing Order 18-09) was developed as a corrective action, and made effective on June 29, 2018. The standing order stated that Operations has been tasked with real time evaluation of SBGT accumulator pressure drop tracking, and a spreadsheet for data entry and calculation was provided to the Operations Department.

On July 17, 2018, the B train of SBGT was again declared inoperable following identification of air accumulator leakage above the design limit contained in calculation M896, Capacity Increase Evaluation for SBGT Receivers, and LCO 3.7.B.1.c was entered. A seven day action statement to restore the inoperable train of SBGT to operable was also initiated. On July 23, 2018, day five of the seven day LCO action statement, while reviewing the Operations spreadsheet used for tracking and evaluating SBGT air accumulator leakage, NRC inspectors determined that, as directed by Standing Order 18-09, operators did not properly evaluate and identify an adverse condition: SBGT air accumulator leakage was elevated above the calculated design leakage limit on July 14, 2018, and a condition report had not been initiated to identify the condition.

During subsequent review of historical data, it was determined that the leak rate in the SBGT system exceeded the allowable rate on July 2, 2018. Therefore, the seven day LCO action statement was exceeded on July 9, 2018.

Entergy procedure EN-LI-102, Corrective Action Program, defines adverse condition as, in part, a general term which includes Conditions Adverse to Quality plus undesirable conditions related to design basis, licensing basis, and equipment required to support safety related equipment, among other things. EN-LI-102 also states that Employees and contractors are required to initiate CRs for Adverse Conditions.

Corrective Actions: Instructions detailing the evaluation of SBGT air accumulator leakage have been incorporated into station procedure 2.2.50, Standby Gas Treatment, Revision 76, and Entergy performed an Adverse Condition

Analysis.

Additionally, Licensee Event Report 2018-005-00, Condition Prohibited by Technical Specifications Involving Standby Gas Treatment System Pneumatic Leakage Rate, was submitted on September 12, 2018.

Corrective Actions Reference: CR-PNP-2018-6103

Performance Assessment:

Performance Deficiency: Entergy personnel failed to identify an adverse condition associated with elevated air accumulator leakage in the SBGT system when readily available information indicated system degradation.

Screening: This performance deficiency is more than minor because it is associated with the Human Performance attribute of the Barrier Integrity cornerstone, and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events.

Significance: The inspectors assessed the significance of the finding using IMC 0609.04, Initial Characterization of Findings, and IMC 0609, Appendix A, Exhibit 3, Barrier Integrity Screening Questions. The inspectors determined that this finding was of very low safety significance (Green) because the performance deficiency only represented a degradation of the radiological barrier function provided by the SBGT system.

Cross-Cutting Aspect: The cause of the finding was assigned a cross-cutting aspect of Human Performance - Training because the organization was not provided adequate training regarding the conduct of the additional monitoring directed for the SBGT system performance. [H.9]

Enforcement:

Violation: Technical Specifications 3.7.B.1, Standby Gas Treatment System, requires, in part, that when one train of the Standby Gas Treatment System is made or found to be inoperable for any reason, continued reactor operation is permissible only during the succeeding seven days providing that within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> all active components of the other standby gas treatment train are verified to be operable and the diesel generator associated with the operable train is operable. Additionally, Technical Specification 3.7.B.1.c states that if the system is not made fully operable within 7 days, reactor shutdown shall be initiated and the reactor shall be in cold shutdown within the next 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Contrary to the above, on July 14, 2018, Entergy personnel failed to identify elevated air accumulator leakage and evaluate its effects on the SBGT system operability. Specifically, on July 14, 2018, a Senior Reactor Operator did not identify that the SBGT air accumulator leakage was elevated above the limits specified in design calculation M896, Capacity Increase Evaluation for SBGT Receivers. As a result, Entergy did not evaluate the operability of the system, and did not enter Technical Specification 3.7.B.1.c for one train of the SBGT system inoperable due to elevate system air accumulator leakage and did not take action to restore the system to service within seven days or to initiate a reactor shutdown and place the reactor in cold shutdown within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. On July 21, 2018, Entergy did not initiate a reactor shutdown, and the reactor was not in cold shutdown within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

Inspectors verified no proprietary information was retained or documented in this report.

On July 12, 2018, the inspectors presented the inspection results to Mr. Drayton Pitts, General Manager of Plant Operations, and other members of Entergys staff.

On July 18, 2018, the inspectors presented Independent Spent Fuel Storage Installation inspection results to Mr. Brian Sullivan, Site Vice President, and other members of Entergys staff.

On August 30, 2018, the inspectors presented the inspection results to Mr. Brian Sullivan, Site Vice President, and other members of Entergys staff.

On October 24, 2018, the inspectors presented the results associated with the resident inspector quarterly baseline inspection results to Mr. Brian Sullivan, Site Vice President, and other members of Entergys staff.

DOCUMENTS REVIEWED

71111.11

Procedures

EN-OP-115, Conduct of Operations

Miscellaneous

Simulator Scenario SES-2010-09, Revision 4

Simulator Scenario SES-2014-03, Revision 3

71111.12

Procedures

EN-DC-205, Maintenance Rule Monitoring, Revision 5

71111.13

Procedures

EN-WM-104, On-line Risk Assessment, Revision 16

71111.15

Procedures

EN-OP-104, Operability Determination Process, Revision 16

71111.18

Procedures

EN- DC-115, Engineering Change Process, Revision 25

EN- DC-136, Temporary Modifications, Revision 17

Maintenance Orders/Work Orders

506016

71111.19

Procedures

3.M.4-121, GH-Bettis Actuator Refurbishment, Revision 28

8.M.2-7.1.19, Leak rate Test of Air Supply for Standby Gas Treatment System Dampers,

Revision 6

Condition Reports

2018-6047 2018-6103

Maintenance Orders/Work Orders

505808 506016 508933

71124.02

Procedures

6.5-337, Pilgrim Nuclear Power Station Calibration of the Telepole Survey Meter, Revision 9

EN-RP-105, Radiological Work Permits, Revision 18

EN-RP-110, ALARA Program, Revision 14

EN-RP-110-03, Collective Radiation Exposure (CRE) Reduction Guidelines, Revision 4

EN-RP-110-04, Radiation Protection Risk Assessment Process, Revision 7

EN-RP-301, Radiation Protection Instrument Control, Revision 11

Condition Reports

2018-0318 2018-0440 2018-1615 2018-3664 2018-4631 2018-4643

2018-5899

ALARA Reviews and Reports

PNPS Radiological Support Group 1st Quarter 2018 Self-Assessment Report, dated April 1,

2018

RWP 2018064, THERMEX System Operations, Training, Repairs, Adjustments, and Filter

Changes. Includes HRAs, Revision 00

71124.03

Procedures

EN-RP-501, Respiratory Protection Program, Revision 5

71124.05

Procedures

6.5-170, Calibration of Ventilation System Radiation Monitors Using ARM Type

Sensor/Converters, Revision 31

6.5-307, Calibration of the Eberline RO-2/RO-2A or RO-20 Ion Chamber, Revision 20

6.5-341, Calibration of Electronic Dosimeters, Revision 18

6.6-001, Use of the Technical Operations Model 682 and Model 773 Gamma Instrument

Calibrators, Revision 5

6.6-002, Use of the GE Gamma Calibrator for the ARMS, Revision 4

6.6-113, Source Calibration, Revision 12

6.6-116, Source Calibration of the Containment High Radiation Monitoring System, Revision 22

6.69-003, Use of the Shepherd Model 28, Model 78, and Model 423 Gamma Calibrators,

Revision 5

8.M.2-4.6, Offgas Post-Treatment Radiation Monitors Functional Test, Revision 12

Condition Reports

2018-2547 2018-2793 2018-5787 2018-6870

Miscellaneous

2018 RP FSA - Pre-NRC Inspection, IP 71124.05, Radiation Monitoring Instrumentation, dated

July 12, 2018

71152

Procedures

2.1.42, Operation during Severe Weather, Revision 39

SEP-PNPS-IST-001, PNPS In-service Pump and Valve Testing Program, Revision 6

Condition Reports

2013-1066 2013-6088 2013-6620 2013-8334 2013-8338 2014-0243

2014-0899 2014-1877 2014-4342 2014-5404 2014-6585 2015-0619

2015-0952 2015-4218 2015-6009 2015-6287 2015-6701 2015-6773

2015-7572 2015-8845 2016-10039 2016-10386 2016-2609 2016-2657

2016-3315 2016-3349 2016-3598 2016-3922 2016-4140 2016-5856

2016-7625 2016-8657 2016-8657 2017-0301 2017-10030 2017-1512

2017-1625 2017-2609 2017-4162 2017-4910 2017-6616 2017-7871

2017-8481 2017-8678 2018-4183 2018-6254

Maintenance Orders/Work Orders

00468389 52520927 52510846

Miscellaneous

8.5.4.1, High Pressure Coolant Injection System Pump and Valve Quarterly and Biennial

Comprehensive Operability, performed 8/11/18

MSI TR-161881, Entergy - Pilgrim Nuclear Plant Station High Pressure Coolant Injection Pump

Vibration Testing, Revision 0

60855.1

Procedures

2.2, Multi-Purpose Canister Loading, Revision 4

2.4, Multi-Purpose Canister Stack up and Transfer, Revision 4