ML20137V429

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Monthly Operating Repts for Nov 1985
ML20137V429
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 11/30/1985
From: Kanick B, Thornberry R
PACIFIC GAS & ELECTRIC CO.
To:
NRC
References
NUDOCS 8602190563
Download: ML20137V429 (9)


Text

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OPERATING DATA REPORT DOCKET N0. 50-275 DATE 12/06/85 COMPLETED BY Bob Kanick TELEPHONE (805)595-7351 OPERATING STATUS

1. Unit Name: Diablo Canyon Unit 1
2. Reporting Period: November 1985
3. Licensed Thermal Power (MWt): 3338

-4. Nameplate Rating (Gross MWe): 1137

5. Design Electrical Rating (Net MWe): 1086
6. Maximum Dependable Capacity (Gross MWe): 1125**
7. Maximum Dependable Capacity (Net MWe): 1073**
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

N/A

9. Power Level To W."-h Restricted, If Any (Net MWe): N/A
10. Reasons For Restrictions, If Any: None This Month Yr-to-Date Cumulative
11. Hours In Reporting Period 720 4990.3 4990.3*
12. Number Of Hours Reactor Was Critical 486.3 4658.8 4658.8*
13. Reactor Reserve Shutdown Hours 0.0 0.0 0.0
14. Hours Generator On-Line 479.3 4613.8 4613.8*
15. Unit Reserve Shutdown Hours 0.0 0.0- 0.0
16. Gross Thermal Energy Generated (MWH) 1523963 14635460 14635460
17. Gross Electrical Energy Generated (MWH) 504600 4870432 4870432
18. Net Electrical Energy Generated (MWH) 475559 4625090 4625090
19. Unit Service Factor 66.6 92.5 92.5
20. Unit Availability Factor 66.6 92.5 92.5
21. Unit Capacity Factor (Using MDC Net) 61.6- 86.4 86.4
22. Unit Capacity Factor (Using DER Net) 60.8 85.3 85.3
23. Unit Forced Outage Rate 33.4 7.5 7.5
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
25. If Shut Down At End Of Report Period, Est. Date of Start-up: N/A
26. Units In Test Status (Prior to Consnercial Operation): N/A
  • As of commercial operation on 5-7-85 at 0243.
    • These values are predictions - actual values are to t,e determined by operating experience during the first year of commercial operation.

860219056385g-75 PDR ADOCK O pg l

DC0455 //

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' OPERATING DATA' REPORT y

i DOCKET.NO. 323 DATE 12/06/85-COMPLETED BY- Bob Kanick TELEPHONE (805)595-7351-OPERATING STATUS i 1.:~ Unit Name: Diablo Canyon Unit 2

2. -Reporting Period: November 1985 i 3. . Licensed Thermal Power- (MWt): 3411 f 4. _ Nameplate Rating-(Gross MWe): N

! 5. Design ~ Electrical Rating-(Net-MWe): 1119

6. Maximum-DependableCapacity(GrossMWe): 1145***
7. ' Maximum Dependable Capacity (Net MWe)
1093***-

If Changes Occur in capacity Ratings (Items Number 3 Through 7) Since Last Report,

~

~8.

t Give Reasons:

I N/A

9. Power Level to Which Restricted, If Any (Net MWe): N/A
. 10. . Reasons For Restrictions, If Any
None

. This Month Yr-to-Date Cumulative

11. Hours In Reporting Period 720 5137 5137*

l 12. Number Of Hours Reactor Was Critical 558.8 1301.3 1301.3*

1 13. Reactor Reserve Shutdown Hours 0.0 0.0 0.0

! 14. Hours Generator On-Line 510.5 725.8 725.8*

15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 4 16. Gross Thermal Energy Generated (MWH) 916009 1150184 1150184*

j 17. Gross Electrical Energy Generated (MWH) 281500 332400 332400*

j 18. Net Electrical Energy Generated (MWH) 248463 218158 218158*

19. Unit Service Factor N/A**
20. Unit Availability Factor N/A**

4 21. Unit Capacity Factor (Using MDC Net) N/A**

22. Unit Capacity Factor (Using DER Net) N/A**

i 23. Unit Forced Outage Rate N/A**

24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration.of Each)
. N/A
25. If Shut Down At End Of Report' Period, Est. Date of Start-up:
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY July 1985 August 1985 INITIAL ELECTRICITY October-1985 October 1985 COMMERCIAL OPERATION January 1986
  • Cumulative totals started _on the April 26, 1985 (Date of effectiveness of Low Power License).

j- **- These sections not applicable until commencement of comercial operation.

i *** These values are predictions - actual values are.to be determined by operating i experience during the first year of commercial operation.

DC0455

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_v AVERAGE DAILY UNIT POWER'LEVELL - -

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' DOCKET lNO.- 50-275

' UNIT : Diablo Canyon Unit-1

_ _-DATE. '12/06/85 Bob Kanick

' COMPLETED BY~ -

. TELEPHONE ~ -(805)595-7351-

MONTH-. i November ~ 19851

' DAY: AVERAGE DAILY POWER LEVEL' DAY- ' AVERAGE DAILY POWER LEVELL

.(MWe-Net).  :(MWe-Net) 1  : 17 1049 2- -6 18 1070 3 -5 19 1066 4 -5 20 1070:

5 -5 21 1065:

6 -13 22 1066 -

7 -25 23 1074 8 -36 24 :1020 9 -46 25' 1070 10 -39 26 1066 11 258 27~ 1069 12 -642: 28' 1057 13 1039 29 1066 14 1066 30 1063 15 -1068 16- 1062

' INSTRUCTIONS

On this format, list the ' average daily unit power level in MWe-Net.for each day. in the .

.raporting month.. Compute to the: nearest whole megawatt. : -

y iDC0455 ,

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y; 5 ' .;  :. '_ x ,

-AVERAGE DAILY UNIT' POWER LEVELI J

- .' DOCKET; NO. 50-323-UNIT- -Diablo Canyon Unit 2

-DATE. 12/06/85 -

-COMPLETED BY' Bob Kanick.

. -TELEPHONE' (805)595-7351

~

MONTH
November 1985 DAY- AVERAGE DAILY POWER LEVEL.- DAY- AVERAGE DAILY POWER LEVEL

.(MWe-Net) -(MWe-Net) 1 205 J17 782 2 443 18 724 3 '446 19 304 1 4 439 20 342-5 416 21 453 6 320- 22 699

, 7 -46 23 325 8 -33 24 543

9 71 25 691 10 421 26 754 11 421 27' -39 l- 12 433 28 -38

'~

13 229 29 -38 14- 30 4 15 350 16- 766

]

-INSTRUCTIONS. l 1 ,

On this format, list the average. daily. unit power level in MWe-Net for
each day in the reporting month. Compute t,o the nearest whole megawatt.

DC04551

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' UNIT SHUTDOWNS AND POWER REDUCTIONS .

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  • 5 ^~c Paga 1 of.1 DOCKET NO. '50-275' UNIT NAME Diabla Cany n Unit It- --a, DATE 12/06/85 ~ .J

COMPLETED BYu D.P. SI5K- '

REPORT MONTH ' NOVEMBER'1985 :TELEPHONEi (805)595-7351-Method of Lfcensee System -Component. Cause & Corrective- y Duration 2 3

~ Event -

. Action to-Typel i(Hours) 4 5 '?

No. ' Da te - Reason Shutdown . Report # Code ' Code  ! Preventi~ Recurrence" 1- 10/30/85 S- 240.8 A 4 NA SG TBG'- . Unit was shutdown to'. clear;up steam -

' generator .and condensate' water . ._l.'

chemistry after a~ main' condenseritube?

leak.

n: :p 4

T

)

1 2 3' . 4 '

F: .. Forced - Reason:. . ' Method: Exhibit:GT- Instructions':

S: 1 Scheduled- .A-Equipment Failure (Explain)' .1-Manual for: Preparation of-Data-

- B-Maintenance or . Test 2-Manual Scram - Entry Sheets for Licensee,

'C-Refueling- . 3-Automatic' Scram - EventReport'(LER). File.

D-Regulatory Restriction Continuation from- (NUREG-1022)! '

E-Operator Training & License. Examination previous? month

'F-Administrative .

5-Power reduction- '

! 5 i-G-Operational Error-(Explain) :6,7,8-N/A" Exhibit I - Same Source 1 H-Other(Explain)- 9-Other

.DC0455

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UNIT SHUTDOWNS AND POWER REDUCTIONS e, i Page 1 of 2 DOCKET NO. 50-323 UNIT NAME Diablo Canyon Unit 2<

DATE 12/06/85 COMPLETED BY D.P. SISK REPORT MONTH NOVEMBER 1985 TELEPHONE (805)595-7351 -

l Method of Licensee System Component Cause & Corrective Duration 2 3 Event 4 5 Action to No. Date Type l (Hours) Reason Shutdown Report # Code Code Prevent Recurrence 1 10/31 S 6.9 8 4 NA NA NA Generator Testing l

2 11/06 F 55.0 B 3 2-85-013 NA NA Slow response of turbine interceptor valves resulted in a low-low steam generator level reactor trip. -To l

prevent recurrence, the turbine l interceptor valves hydraulic system was modified to improve interceptor valve response time per Westinghouse recommendations.

3 11/09 F 14.1 G 3 2-85-015 NA NA Personnel error. Operators closed a main feed pump recirculation valve before all four feedwater regulating valves were in automatic.

4 11/13 S 1.0 8 1 NA NA NA Generator Testing 5 11/13 S 40.0 B 1 NA NA NA Generator Testing 1 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee l C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuation from (NUREG-1022)

E-0perator Training & License Examination previous month F-Administrative 5-Power reduction 5 .

G-Operational Error (Explain) 6,7,8-N/A Exhibit I - Same Source H-0ther (Explain) 9-Other DC0455

UNIT SHUTDOWNS AND POWER REDUCTIONS ,* '*

Page 2 of 2 DOCKET N0. 50-323 UNIT NAME Diablo Cany n Unit 2, .

DATE 12/06/85 COMPLETED BY D.P. SISK REPORT MONTH NOVEMBER 1985 TELEPHONE (805)595-7351 -

Licensee System Component Cause & Corrective y

Duration 2 Methodof Event Action to No. Date Type (Hours) Reason Shutdown Report # Code Code Prevent Recurrence 6 11/26 F 92.4 A 3 2-85-016 NA NA During a load rejection test from 75 to 25 per cent power, unit experienced a low-low steam generator level reactor trip and hi steam flow / low S/G Press safety injection.

7 11/28 F --

A 2,3 2-85-017 NA NA With reactor at 0.5 per cent power and turbine latched with air / oil relay cut out, the air / oil relay was cut in which caused a momentary steam flow / feed flow bistable to pick up. This coincident with low level bistable already in caused a reactor trip. The duration of the initiating signal was so short that reactor trip breaker B did not open.

Subsequent testing and discussion witis the vendor, Westinghouse, have confirmed that the reactor protection system and the trip breakers functioned properly and no anomalies exist.

1 2 3 4 F:- Forced Reason: Method: Exhibit G - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuation from (NUREG-1022)

E-Operator Training & License Examination previous month F-Administrative 5-Power reduction 5 G-Operational Error (Explain) 6,7,8-N/A Exhibit I - Same Source H-0ther (Explain) 9-Other DC0455

. -PACIFIC GAS AND E LE C T RIC CCMPANY

, DIABLO CANYON PCWER PLANT 3

PO. Box 56 Avila Beach, Cahfomia 93424 (805) 595-7351 lllllllll R.C. THORNBERRY PLANT MANAGER December 6, 1985 Office of Management Information and Program Control U.S. Nuclear Regulatory Commission Washington, DC 20555 RE: Docket No. 50-275 and 50-323 License No. DPR-80 and DPR-82 Monthly Operating Report for November,1985 Gentlemen:

Enclosed are the completed monthly operating report forms for Diablo Canyon Units 1 and 2 for November, 1985. This report is submitted in accordance with Section 6.9.1.7 of the Units 1 and 2 Technical Specifications.

Sincerely, f8 ROBERT C. THORNBERRY RCT:lah Enclosures cc Mr. John B. Martin, Regional Administrator '

Region V - USNRC DC0044 1

r MONTHLY NARRATIVE REPORT 0F OPERATION AND MAJOR MAINTENANCE EXPERIENCE This report describes the operating and major maintenance experience for the month of November, 1985. This narrative report was prepared by the plant staff and is submitted in accordance with Section 6.9.1.7 of the Units 1 and 2 Technical Specifications.

On November 1, 1985 Unit 2 was paralleled to the grid On November 6, 1985 Unit 2 experienced a reactor trip On November 9, 1985 Unit 2 was paralleled to the grid On November 9, 1985 Unit 2 experienced a reactor trip On November 9, 1985 Unit 2 was paralleled to the grid On November 11, 1985 Unit I was paralleled to the grid after a 12 day outage On November 13,1985 Unit 2 was separated from the grid for generator testing On November 13, 1985 Unit 2 was paralleled to the grid On November 13,1985 Unit 2 experienced a reactor trip On November 15, 1985 Unit 2 was paralleled to the grid On November 18,1985 Uriit 2 reduced power to 30% to replace condensate polisher resins On November 26, 1985 Unit 2 experienced a reactor trip On November 28,1985 Unit 2 experienced a reactor trip On November 30, 1985 Unit 2 was paralleled to the grid Unit 1 operated this month with a unit availability factor of 66.6% and a unit capacity factor of 61.6%. At the start of the month, Unit I was shutdown for 10 days to clean up secondary water chemistry.

There were no major safety related maintenance activities performed for Unit 1 or Unit 2 in the month of November,1985.

No challenges to the PORVs or Steam Generator Safety Valves have been made.

DC0455