05000366/LER-1981-084, Updated LER 81-084/03X-1:on 810903,N005 HPCI Steam Line Delta P Switch Found to Actuate at 204.5 Inches Water. Caused by Setpoint Drift.Barton Model 288A Switch Recalibr, Tested & Returned to Svc

From kanterella
Revision as of 07:47, 28 March 2020 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Updated LER 81-084/03X-1:on 810903,N005 HPCI Steam Line Delta P Switch Found to Actuate at 204.5 Inches Water. Caused by Setpoint Drift.Barton Model 288A Switch Recalibr, Tested & Returned to Svc
ML20070A724
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 11/30/1982
From: Tipps S
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20070A700 List:
References
LER-81-084-03X, LER-81-84-3X, NUDOCS 8212090335
Download: ML20070A724 (1)


LER-2081-084, Updated LER 81-084/03X-1:on 810903,N005 HPCI Steam Line Delta P Switch Found to Actuate at 204.5 Inches Water. Caused by Setpoint Drift.Barton Model 288A Switch Recalibr, Tested & Returned to Svc
Event date:
Report date:
3662081084R00 - NRC Website

text

NRC FORM 366 U. S. NUCLE A"1 CEIUL ATORY COMMISSION

h. -

LICENSEE EVENT REPORT UPDATE REPORT - PREVIOUS

. -- " % REPORT DATE 10/1/81 CONTROL BLOCK: l 1

l l l l l lh 6

(PLEASE PRINT CR TYPE ALL RE2Ul:E')INFORMATION) o i *lG l A lE lI lH l 2 lg 0 l0 l- l0LICENSE l0 l0 l0 l0 l- l0 l0 lgl 4l 1l 1l 1l ljgl67 CAT NUM8ER 25 l lg 58 7 W 9 LICENSEE CODE 14 15 26 LICENSE TYPE Jo con'T 7

o i 8

En"C 60l L l@l 61 0 l 5 DOCKETl0 l 0NUMBER l0 l 3 l 6 68l6 @l 69 01910 EVENT DATE 13 l 8 74l1 l@l 75 llREPORT ll 3l DATE 0l 8l 280l@

EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h O 2 While increasino power from 238 MWt, durina the performance of the "HPCIl l 0 l 31 STEAM LINE DELTA P INSTRUMENT F.T. AND C." procedure, the N005 HPCI l o 4 Bteam Line dp Switch was found to actuate at 204.5" H20. Tech. Specs. l O s Table 3.3.2-2, item 5.1. requires actuation at </= 300 percent of rated l 0'6 l flow (a do of </= 196" H2O) . Redundant switch, N004, was in tolerance. l 10171 Wlant operation and the health and safety of the public were not affected 10181 by this repetitive event (as last reported on LER 50-366/1980-041). l 7 8 g 80 DE CODE SU8C E COMPONENT CODE SU8 CODE S E 7

O 9 8

l S l F lh Wh [E_jh l Il Nl Sl Tl Rl Ulh [Sj@ [Z_J @

9 to 11 13 18 20 11 19

, SEQUEN TI AL OCCUR R E NCE REPOTT REVISION LE R 'RO EVENT YEAR REPORT NO. CODE TYPE N O.

h nUM R

_ 21 l8 l1 l 22 l-l 23 l0 l8 l4 26l 2d 27 l 0l 3l 28 29 W30

[ -j 31 Q32 K A ON PL T MET HOURS 27 SB IT FOR B. SUPPL R MANUFACTUREH .

W 3J

@lFl@34 Wg W@

35 M l0 l0 l0 lD l 31 40

{ g 41

] g 42

[Njg 43 lBl0l8l0lg 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O Rhe cause of this event has been attributed to setpoint drift. The l i i Iswitch, a Barton Model 288A, was recalibrated, successfully functionally l 1 2 l tested, and returned to service. An engineering study to find a means l g lof preventing or reducing the frequency of recurrence has recommended a l i 4 l Design Change. Recommended corrective measures are being evaluated. l 7 8 9 80 ST S  % POWER OTHE R ST ATUS ISCO RY DISCOVERY DESCRIPTION y (_Cj@ l 0 l 1 l 0 l@l NA l l B lgl Surveillance Testing l AETIVITY CO TENT LOCATION OF REMASE @

7 i e REM ASE@D OF AMOUNT 8 9

[z_1 10 11 NA REMASELz_1@l OF ACTIVITY 44 l

45 NA @l 80 l

PERSONNEL EMPOSURES NUMBE R TYPE DESCRIPTION i 7 l0l0l0l@lZl@l"

NA l

' PtnSONNEt INJU' IES NUMBER DESCRIP TION 7

i R 8 9 l0l0l0l@l 11 12 NA 80 l

LOSS OF OR DAMAGE TO F ACILITY TYPE DE SCRIPTION 1 9 [z j@l NA

%%h35 K821130 05000366 l 7 a v io g PDR 80 2 o gggutf@l

[N., DESCRIPTIONNA l lllllllllllljf 7 8 9 to 68 69 80 E NAME OF PREPARER PHONE: