ML20009E791

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LER 81-032/03L-0:on 810619,reactor Coolant Leak Detection Air Sampling Sys C-19 Declared Inoperable.Caused by Valves Sticking in Closed Position Due to Dirt in Sys Check Valves. Valves Disassembled & Cleaned
ML20009E791
Person / Time
Site: Pilgrim
Issue date: 07/20/1981
From: Mcloughlin M
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20009E790 List:
References
LER-81-032-03L, LER-81-32-3L, NUDOCS 8107280447
Download: ML20009E791 (1)


Text

I NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: l t

l l I I l lh 6

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) {

l O l t l l Mj A l P l P l S l 1 l@l 0 l 0 l- l 0 l 0 l 0 l 0 l 0 l - l 0 l 250 !@l i4 15 Lica!NSE NUMBER 26 4 lLICENSE 1 l 1 TYPEl 1l JO1]@l57 l C T 58 l@

7 8 9 LICENSEE COOE CON'T

" " i 10111 7 8 SObRC[ 60 l L l@! 015 61 l 0 l- 1012 l 689 I 3 DOCKET NUM' Ea 69 @lEVENT0 l OATE 6 l 1 l 9 l 81 1 hlREPORT 74 75 al 712101 DAT E RI 1l@

80 EVENT DESCRIPTION ANO PROS ABLE CONSEQUENCES h io l2l l On June 19, 1981 at 1445 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.498225e-4 months <br />, the Reactor Coolant Leak Detection Air Sampling l

, o ,3 ; ;

System (C-19) was declared inoperable. Instrument and Control personnel were l l l

Io l4l l immediately dispatched to repair the unit. During the event the drywell sumos l [

i l0 is j l were operable. C-19 was repaired and returned to service at approximately 2032 I i ggI hours on the same day. The unir. has operated satisfactorily since rhnt t-i mo . l i

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10181 I 80 7 8 9

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0 400E S SC E COMPONENT CODE SL8 COD'E SU E 10191 7 8 Ic IT l@ lid @ LrJ@ l vi Al r i vi vi xl@ l cl@ LAJ @

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SEQUENTIAL OCCURRENCE REPORT R E VISION ,

_ EVENT YEAR R EPORT NO. COOE TYPE NO.

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.,21 2 23 24 26 27 28 29 30 31 32 TAK N AC ON ChP NT ME HOURS S Bf ITT PG B. SUPPLIE YANLFACT REN l x i@LZ_j@

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36 l of of of of 3/ 40 Ls.1@

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43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h ji 10 l l This event was caused by dirt in the system check valves which caused the valves  !

[i )i l l to stick in the closed position. The check ,alves were dinn==nmhind <lonnna I g,,7i l and reassembled. This is an isolated event. I Ii1311 ..

I l i 14 1l 80 7 8 9 ST S  % POWER OTHER STATUS ISCO RY DISCOVERY DESCRIPTION 11 15 l l E j@ l1 l 0 l0 l@[ N.A. l lAl@l Operational Event -

l l 7 8 ' " '

A$TIVITY CO' TENT l RELEAsEO OP RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE N.A. l l N.A. I l

i 11161 7 8 9 l Z l @tol Zl@[ 1 44 45 80 PERSONNEL EXPOSURES NUVSER TYPE DESCRIPTION

[i j 7 l l 0 l 0 l 0 l@l Z l@l N.A.

PERSONNE L INJU IES NUR sR DESCRIPTION li la l l 0 l C ')J@l12 N.A.

i 7 8 9 1 LOS3 OF C MAGE TO FACILITY TYPE cRIPTION

  • lig [ZJ@j N.A. '

! 89_ 10 8107200447 810720

' NRC USE ONLY PDR ADOCK 05000293 l

ISSUE gjO SCRiPTiON @ S 10 PDR N^ ),),IIIIIIIIIIIl j 3

7 8.t NAME OF PREPARER M. T. McLoughlin pgOyg. 6 U-M4W 2

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