ML17342A380

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Responds to NRC 860102 Ltr Re Unresolved & Insp Followup Items Noted in Insp Repts 50-250/85-40 & 50-251/85-40. Corrective actions:Off-Normal Operating Procedure 0208.11 Changed to Clarify Immediate Operator Actions During Alarm
ML17342A380
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 01/31/1986
From: Woody C
FLORIDA POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
L-86-29, NUDOCS 8602190110
Download: ML17342A380 (76)


See also: IR 05000250/1985040

Text

F LORIDA POWER 5 LIGHT COMPANY JAN S 1 198S L-86-29 Dr.3.Nelson Grace Regional Administrator, Region II 101 Marietta Street, N.W.Suite 2900 Atlanta, Georgia 30323 Dear Dr.Grace: Re: Turkey Point Units 3 R 0 Docket Nos.50-25 51 Ins ection Re or 85-00 Florida Power R Light Company (FPL)hereby responds to NRC Inspection

Report Nos.50-250/85-00

and 50-251/85-00.

As requested by NRC Region II's letter dated 3anuary 2, 1986 forwarding

the subject Inspection

Report, the attachment

to this response includes FPL's plans for corrective

action for each unresolved

and inspector followup item identified

in the Report, and describes the actions taken or planned to improve the effectiveness

of FPL's management

control systems for each such item.While we recognize the need for prompt actions to improve the effectiveness

of management

control systems for the items addressed in the subject Inspection

Report, we also request that NRC's deliberations

on the attached response take account of the particular

circumstances

under which the inspection

results were obtained.The subject Inspection

Report describes the results of a follow-up inspection

conducted within less than two months of NRC's intensive Safety Systems Functional

Inspection (SSFI), which was itself unprecedented

in its depth and approach.Without diminishing

the importance

of the matters raised in the subject Report, we believe that the results of any new inspection

program, along with an immediate expansion of that program through regional followup inspection, should be interpreted

with caution.Moreover, the followup inspection

was conducted before FPL had completed and submitted its response to the SSFI.Many of the responses to the SSFI were still in progress and there had been insufficient

time for many of the corrective

actions taken or planned in response to the SSFI to become effective and be reflected in the followup inspection

results.We request in particular

that our December 6, 1985 response to the SSFI and the description

of corrective

actions planned or taken therein, be given consideration

in your deliberations.

In addition, we ask that you give consideration

to the fact that our ongoing corrective

action activities

have been adversely impacted by the demands imposed by the 2-week regional followup inspection.

8602i90iiO

860iSi PDR ADOCK 05000250 8 PDR uE I PEOPLE...SERVING PEOPLE

J!j~

We believe that the corrective

actions described in our response to the SSFI and in the attached response have been timely and will be effective.

We have implemented

appropriate

procedure revisions and demonstrated

the adequacy of systems and components

by analysis and/or test.Moreover, a significant

number of unresolved

items were already the subject of planned updating actions and at the time of the inspection

were still in progress toward satisfactory

resolution.

As we indicated in our December 6, 1985 response to the SSFI, the results of SSFI indicated a need to augment our ongoing, long-term Performance

Enhancement

Program (PEP)in regard to iVlaintenance

and Conf iguration Control.Additionally, the AFW System Availability/Reliability

Study and Safety System Reviews were viewed to be appropriate

and have been commenced.

These actions have been integrated

into our overall management

plan.We acknowledge

that the burden is on FPL to assure effective implementation

of that plan and we fully recognize and accept that responsibility.

At the same time, we ask that you give consideration

to the positive results of our longer term programs that are now beginning to emerge.As stated in our response to the SSFI, FPRL committed (letter L-85-372, dated September 30, 1985)to apply and implement appropriate

technical specification

requirements

to address the availability

and surveillance

testing of the two non-safety grade motor-drive

standby feedwater'pumps at Turkey Point.The Technical Specification

amendment request has been submitted to the NRC (L-86-03 dated 3anuary 30, 1986).Since the inspection

team concluded that there were no administrative

controls or Technical Specification

requirements

in place to assure the availability

of this system on demand, the team found it inappropriate

to give credit for this system during analysis of the inspection

findings.As stated in FPRL's letter L-85-372, however, these standby"pumps have been routinely run in accordance

with plant procedures".

In addition, backup power supply is obtainable

from five non-safety

grade diesel generators

rated at nominal 2500 kw each.These diesels can supply power directly to nuclear side loads via internal (site)cable runs independent

of the switchyard.

Based upon the foregoing factors, FPRL submits that it would be appropriate

for the capabilities

of the standby feedwater system to be taken into consideration

in the NRC's final analysis of its inspection

findings.A formal description

of the detailed scope of work to be completed by the AFW Availability/Reliability

study, discussed in our response to the SSFI, has been issued.A contractor

has been selected;the AFW Availability-Reliability

study is estimated to be completed within twelve (12)weeks.This study which includes reliability

modeling and an evaluation

of component failure contribution

to reliability, will provide a real time assessment

capability

for AFW system readiness.

A summary of this program is being presented to the Region II staff on 3anuary 31, 1986.FPL has undertaken

a two-phase Safety System review to assure that the concerns expressed in the inspection

report do not apply to the operations

and functions of other important safety systems, or that any appropriate

corrective

actions are promptly taken.The Phase I (Iriitial Assessment)

review has been completed by the Safety Engineering

Group.No system problems that might impede the functional

performance

of the systems selected for review were identified.

With the Phase I results as input for prioritization, FPL will now undertake the more formal and detailed, in-depth Phase II (Comprehensive

Assessment)

review of the selected systems.This review will encompass and

r~V

ensure pertinent design bases are clearly specified, providing additional

assurance that the systems will function as designed.Any necessary corrective

actions will be tracked to implementation.

Phase II has been scoped and scheduled and is estimated for completion

within two years of the commencement

af work activities.

Additionally, in order to more efficiently

control and implement design related issues at Turkey Point, a Site Engineering

Manager has been recently appointed to be responsible

for all site design activities.

As an indication

of the level of importance

assigned to this position, he will report directly to the Site Vice President.

In closing, we reemphasize

our commitment

to improving performance

and assuring that the corrective

actions described in the attached response are effective.

We are confident that our.corrective

actions, when viewed in the context of our overall PEP, will continue to achieve improved performance.

Very truly yours, C.O.Wo Group c resident Nuclear nergy COW/dh Attachment

cc: V.Stello, NRC Executive Director for Operations (Acting)H.R.Denton, Director NRR 3.M.Taylor, Director, NRC Office of Inspection

and Enforcement

J S.E.Elrod, Section Chief, Region II H.L.Thompson, 3r., Division Director, PWR Licensing Division A, NRR S.A.Varga, Director, Project Directorate

No.3, PWR Licensing Division A, NRR L.S.Rubenstein, Director, Project Directorate

No.2, PWR Licensing Division A, NRR D.G.McDonald, Senior Project.Manager, NRR H.F.Reis, Esquire L QD 20 No.of 4oP I~4~I 5 02/04/86 ACOSTA DOIRSY CRISLER PLUGGER SRELH HUTCHIHSON

HARSH NEEDH4H PEEBLES SHOPPH4N NILK YOUNG 4NDERSOH DRAIN DANEK CRANCIS HARPER K4RCH HILLER NUTNELL POTERALSKI

SPOONER NILLI4NS JP ARIAS CH4HLY EHSLHEIKR OOTCH HORRKLL KENT NOAD4 P4HZAHI RE IS VAULT CUSTODI4H NOOD4RD DARRON CONDERY PINCHER GOULDY HUENNISER KERN HcDONALD P4RKER RICHARDS VERDUCI YORK

IS

ATTACHMENT

Re: Turkey Point Units 3 R 0 Docket Nos.50-250, 50-251 Ins ection Re ort 85-00 FPL Res onse to Unresolved

Items and Ins ection Followu Items URI 85-00-01: Licensee Administrative

Procedure ADM 701, Section 5.8.1.8 requires that the root cause of equipment failure be identified

by the journeyman

on the completed P WO.The licensee's

failure to implement this procedural

requirement

is considered

an unresolved

item.~Res onse: 3ourneymen, Supervisors

and GEMS personnel have been directed to ensure that the"Analysis of the Cause or Reason" section of P WO's is completed.

As stated in Inspection

Report 85-00 (Page 0)"the inspector reviewed 15 safety related PWO's completed since the SSF inspection

and noted that all 15 had the root cause section completed as required".

Additionally, the Nuclear 3ob Planning System (N3PS), the development

of which has been underway since the inception of PEP, requires an identical section to be completed on the CRT screen.These actions will enhance root cause identification

and appropriate

corrective

action implementation.

N3PS, when fully automated, will automatically

datalog system equipment history.Field engineers are being added to all three maintenance

disciplines

to enhance corrective

actions after root cause identifications.

The inspection

report also credited the Turkey Point Emergency Response Team (ERT)for its capability

to identify root cause of failures which should"subsequently

reduce the repetitive

failures that have occurred at the Turkey Point Plant".Finally, the inspection

report recognizes

that"the automated PWO program which will provide trending information, the automated PM program, and the performance

based maintenance

training program, should also contribute

to a reduction in repetitive

equipment failures on a long-term basis".(IR85-00, Page q)

URI 85-00-02: The post maintenance

testing requirements

of Administrative

Procedure 0190.19 for instrument

and controls and electrical

areas were informally

completed without specific direction or documentation

on the associated

PWO's.This situation appears to be another example of failure to implement or provide adequate procedures

to control safety related activities.

~Ree onse: The Procedure Update Program (PUP)has been writing post-maintenance

testing requirements

into all PEP maintenance

procedures.

AP 0190.28,"Post Maintenance

Test Control" guidance, has been revised to cover IRC and electrical

maintenance

activities, as well as mechanical

maintenance.

PEP is being enhanced to incorporate

formal post-maintenance

testing criteria into the PWO and Maintenance

Procedures.

The SORP Post Maintenance

Guidance Document (Rev.A), issued in September 1985, will be evaluated for incorporation

and consolidation

of formal post-maintenance

testing criteria.This task is identified

as Project 9, Task 6 and is scheduled to be completed by March 31, 1986.

URI 85-00-03: The licensee failed to provide and implement adequate procedures

to ensure that independent

verification

was performed and documented

on the return to service of instrumentation

vital to the operation of two safety related systems, namely, auxiliary feedwater and backup nitrogen as required by NUREG-0737

Item I.C.6, confirmed by a NRC order dated July 10, 1981.This appears to represent another example of a failure to provide and/or implement adequate procedures

to control safety related activities.

~Res'nse: Procedure 0-ADM-031 (Independent

Verification)

dated July 12, 1985, Step 5.3.1 requires independent

verification

of the removal and return to service of components

controlled

by equipment clearance orders.Procedure 0-ADM-107 dated October 25, 1985 (Writer's Guide for Maintenance

Procedures), Step 5.8A.C gives directions

for independent

verification

for preparing maintenance

procedure.

As part of the PEP maintenance

activities, maintenance

and surveillance

procedures

are being revised to incorporate

instrument

alignment independent

verification.

URI 85-00-00: Licensee Procedure 0208.11, Of f Normal Operating Procedure (ONOP)Annuciator

Panel List-Panel I Station Service, contained erroneous operator action in the event of a low pressure alarm on the nitrogen backup system.The errors existed due to a failure to revise the procedure.

following modification

to the system per plant change/modification (PC/M)80-117.~Ree onse: Procedure (ONOP)0208.11 was changed to clarify immediate operator actions in the event of an alarm.It was approved by the Plant Nuclear Safety Committee (PNSC)on September 25, 1985.Further, EOP's have been revised to require operators to shift FCV's to manual from automatic control within 3 minutes of AFW actuation.

Power Plant Engineering

and Nuclear Energy Departments

met in December 1985 to discuss implementation

of the Standard Engineering

Package.As part of these discussions, an agreement was reached with respect to inter-departmental

coordination

of PC/Ms.Prior to initiation

of the design activity, Power Plant Engineering

and Nuclear Energy will schedule an operability

review meeting.This review will ensure that Engineering

is provided with the necessary system operating information.

This will facilitate

Engineering

providing more detailed guidance in the PC/M package concerning

operating and maintenance

procedures.

As part of the total design effort, Engineering

will review the plant procedures

revised by Nuclear Energy with respect to integration

with the design.This inter-department

coordination

will ensure that the pertinent plant procedures

are identified, reviewed and modified to reflect the new system configuration.

Guidance in this area is in the process of being formalized

in Engineering

and Nuclear Energy procedures.

I

URI 85-00-05: The FPRL Q-List (Quality Instruction

3PE-QI-2.3A)

did not designate the nitrogen backup system electrical

and instrumentation

components

as safety-related.Consequently, the requisite controls over maintenance

activities

were not applied to the component.

PC/M 80-117 correctly designated

the activities

performed under the modification

as safety-related;

however, the document verification

checklist contained in the PC/M failed to list the required changes to the Q-List.Although the checklist requires that changes to the Q-List be indicated, the entry under this item on the checklist was"Later." This apparent failure to adequately

revise the Q-List may represent another example of an inadequate

design control.This item is considered

unresolved

pending further NRC evaluation.

~Res ense: In regard to the design verification

process for the Q-List, FPL has recognized

that the current Q-List is a basic systems level document and is not intended to address individual

system components.

FPL previously

discussed this issue with the NRC (refer to Inspection

Report Nos.50-250/80-33

and 50-250/80-30), and has committed to the development

of an updated and more component specific Q-List.This new Q-List is data base effective as of November 15, 1985, and has been identified

for NRC review as Inspection

Followup Items 250/80-33-03

and 251/80-30-03.

The classification

of the nitrogen system components

has been evaluated by FPL and is reflected in the updated Q-List.Power Plant Engineering

has developed draft Quality Instructions

which define the requirements

for modifications

to and updating of the Turkey Point Q-List.These instructions

require that a Q-List impact review be performed.for all Turkey Point Plant Changes/Modifications (PC/Ms).They further provide the engineer with specific guidance on the mechanics of preparing changes to the computerized

Q-List Data Base.These procedures

will be in place by the end of February, 1986.The current Q-List represents

the plant as depicted on design documentation

current as of May, 1985.FPL's contractor

for the Q-List is being retained to update the Q-List to the now-current

documentation.

This effort is currently scheduled for completion

by August 1986.Power Plant Engineering

will then proceed to maintain the Q-List as a"living document" for future PC/Ms generated for Turkey Point.

URI 85-00-06: The nitrogen backup system PAID (Drawing 5610-M-339)

incorrectly

indicated that the system pressure regulators

were set at 55 psig.Although this drawing was listed in PC/M 80-117 as a drawing requiring update, a change at some point in the implementation

of the PC/M which modified the setpoint to 80 psig failed to ensure that the PdclD was again updated.This appears to be another example of inadequate

design control.This item is considered

unresolved

pending further NRC evaluation.

~Res onse: The pressure control valves were originally

set at 55 psig based on the original design of the plant which was not changed by the modifications

made under PCM-80-117.Drawing 5610-M-339, Sheet 1 of 1 reflected this setpoint.Although this setpoint was acceptable

based on vendor confirmation, the setpoint was adjusted to 80 psig after PCM 80-117 was implemented, to coincide with the normal air pressure operating range specified on the flow control valve data sheet.Due to an administrative

oversight, this change was not incorporated

on the referenced

drawing.The pressure setpoint shown on Drawing 5610-M-339

Sheet 1 of 1, Revision 15, is not a safety concern since the valve can operate at pressures significantly

less than 55 psig based on previous discussions

with the vendor and actual tests in the field.Therefore, the oversight did not affect the operability

of the Auxiliary Feedwater System.Changes are currently being proposed by the Drawing Update Group to improve drawing accuracy.These changes are scheduled to be implemented

by the end of 1986.Revision 17 of Drawing 5610-M-339

and Revision 8 of the associated

instrument

index sheet 5610-M-311

Sht 155 have been issued to reflect the current setpoint of 80 psig.

URI 85-00-07: The NRC Region II inspectors

walked down additional

portions of the licensee's

AFW and related systems for Unit 0.The inspectors

observed penetrations

into the AF W headers which were identified

as an abandoned in-place nitrogen blanket system.This system, at one time, provided a means of introducing

nitrogen into the AFW system and subsequently

into the Unit 0 steam generators.

The inspectors

reviewed Turkey Point Procedure 0-OP-075 to determine if the nitrogen system isolation valves (00-0-1610C, 00-0-16108, 00-0-1283, and 00-0-1280)were identified

in the valve alignment attachment.

The aforementioned

valves did not appear in this attachment.

Turkey Point Procedure 0-ADM-031 dated December 10, 1980, Independent

Verification, states that independent

verification

shall be applied to auxiliary feedwater system applicable

procedures.

This condition appears to be another example of an inadequate

procedure.

This item is, considered

unresolved

pending further NRC evaluation.

~Res onse: Independent

verification

of the nitrogen blanket system valve alignment is not considered

to be required by procedure 0-ADM-031.

Valve alignment of the nitrogen blanket system connected to the Train 1 AFW feedwater lines on Unit 0 is addressed in Operating Procedure O-OP-065.3"Nitrogen Gas Supply System".This procedure identifies

these valves to be in the closed position for normal operation.

These valves are tagged and the tags are checked once per month.This system has been reviewed for its necessity for tie-in to the auxiliary feedwater system.It was determined

that this system is no longer required and is scheduled for removal by PC/M 85-181 during the curr'ent Unit 0 refueling outage.

URI 85-00-08: Apparently

no licensee evaluation

had been or was intended to be performed on the scaffolding

around the AFW FCV's.Housekeeping

procedures

AP 0103.11 and ASP-13 appeared to be inadequate.

~Res onse: A system is being established

to provide a means to better control scaffolding.

A scaffolding

permit will be required (except in containment

where other close out controls exist and on secondary system areas which do not directly impact safety related systems)prior to erecting a scaffold which will involve a review by operations'personnel.

This system will address the NRC concerns from page 18 and 19 of the Inspection

Report.This scaffolding

Control System will be proceduralized

in Backfit Procedure ASP-26 by February 28, 1986 and in AP 0103.11 by March 31, 1986.

URI 85-00-09: Emergency Operating Procedures

20000, revision dated August 23, 1985, and 20007, revision dated August 26, 1985, did not provide adequate guidance for the control room operators to assure the required 286 gpm of auxiliary feedwater is delivered to each unit within three minutes in the event of a two-unit trip with only one AFW pump available as specified by the Shared Auxiliary Feedwater System, System Description

and Design Basis, Revision I, dated 3anuary 31, 1985.This appears to be another example of failure to provide adequate procedures.

This item is considered

unresolved

pending further NRC evaluation.

'~Res onse: Emergency Operating Procedure 20000 (Loss Of Offsite Power)revision dated December 26, 1985, provides a note following step 5.3.1.This note provides guidance to assure the required AFW flow is provided in the event of a two unit trip.Emergency Operating Procedure 20007 (Loss Of All A.C.Power)revision dated October 30, 1985 provides a note following step 5.2A.This note provides guidance to assure the required AFW flow is provided in the event of a two unit trip>>

i

URI 85-00-10: The licensee apparently

failed to perform an adequate safety evaluation

with regards to PC/M 80-117, in that at the time of PC/M implementation, the auxiliary feedwater system steam vent valves analysis was not performed for the condition of steam vent valve failure at low pressure conditions.

This item is considered

unresolved

pending further NRC evaluation.

~Res onse: The classification

of steam vent valves as non-safety

related components

is consistent

with the original design basis for the plant and was not changed by PCM 80-117.Therefore, ANSI N05.2.11 was not applicable

to either the original design of the vent valve or the subsequent

modifications.

A design analysis was performed prior to the modification

as documented

in Calculation

MO8-162-02, dated November 20, 1981 to justify operation of the AFW system assuming failure of these non-safety

related valves.The calculation

was based on the scenario during the initial operating conditions

of the Auxiliary Feedwater System with maximum steam pressure in the system.This case was considered

bounding for the range of system operation during a transient.

In response to NRC concerns, a confirmatory

analysis has been performed at the lowest steam operating conditions (at the time the RHR System is put into operation)

which has confirmed previous engineering

judgement.

This analysis is documented

in Calculation

MOS-062-02, dated October 11, 1985.The analysis demonstrated

and confirmed adequate steam supply to the Auxiliary Feedwater pump turbines is the event of a complete failure of the steam vent line.The selection of the setpoint for the steam vent valve on the new steam supply header was based on the setpoint established

under the original plant design for the vent valve in the existing header.At the time the new header was added, as an exact duplicate of the existing header, the setpoint of the original steam valve was specified for the new valve.There was no reason to question the validity of, the original valve setpoint since the new valve was functionally

identical.

As stated previously, a design analysis has been performed which confirms the system's operability

with the vent open at low steam pressure.In any event the subject valves will be removed as discussed in the response to URI-85-00-11.

A 0

FP@L is conducting

a design review of the steam vent valve function.This review is expected to be complete by December 30, 1985.The review will address the following questions:

(1)are the vent valves needed for the present auxiliary feedwater system design?(2)What was'the reason for the 150 psi setpoint?(3)If the vent valves are required for system operability, can the 150 psi setpoint be reduced?The result of the design review and the licensee's

actions will be inspected at a future date as an inspector followup item.~Res onse: As part of our AFW system enhancement

task team project (Item 8), we have reviewed the design basis for the original,AFW

steam header leakoff valves to determine their applicability

to our present system.The results of this evaluation

are documented

in Bechtel letter SFB-2107 dated December 19, 1985.The original Turkey Point Auxiliary Feedwater System contained pumps driven by low pressure steam turbines.In order to avoid over speeding and tripping of the turbines upon initial startup, the turbine pressure control valves were maintained

closed.To start the pumps, the steam isolation valves (MOV->>-1003, MOV-~-1000, MOV-+-1005)

were opened and the common steam supply line was pressurized.

A pressure switch, located in the steam supply line then furnished a signal to open the pressure control valves at the turbine inlet to start the pumps.Normally open auxiliary feedwater steam vent valves (CV-"-6008, CV-+-2910)

were provided downstream

of the steam supply isolation valves to prevent pressurization

of the steam supply line, due to isolation valve leakage.Pressurization

of the steam line, as a result of isolation valve leakage, would cause undesirable

cycling of the pressure control valves as well as the pumps.The normally closed pressure control valves at the turbines were removed when the new high pressure turbines were installed.

The new turbines were provided with motorized trip and throttle valves as well as governors with ramp bushings.The motorized trip and throttle valves are normally maintained

open.The governor with ramp bushing will prevent overspeed tripping of the turbine upon initial starting.Therefore, the Auxiliary Steam Vent Valves are no longer required to prevent pressurization

of the steam supply line as a result of isolation valve leakage, and undesirable

cycling of the pressure control valve.As a result of this evaluation, PC/M's85-199 (Unit 3)and 85-200 (Unit 0)are being prepared to remove the vent valves from the system.This modification

is scheduled for implementation

in Unit 0 during the currerit refueling outage.

50

V RI-85-00-12:

Procedure 3-OSP-075.1, dated August 7, 1985, did not adequately

verify that i41OVs 3-1000 and 3-1005 were independently

capable of opening all their associated

AFW flow control valves as designed.The upgrade of Procedures

3-OSP-075.1 and O-OSP-075.1

dated August 1985 required opening both steam supply valves together which fails to ensure that either MOV 3-1000 or MOV 3-1005 could open all associated

flow control valves in trains 1 and 2 thus ensuring a feedwater flowpath.10 CFR 50, Appendix B, Criterion XVI, requires that measures shall be established

to assure that conditions

adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances

are promptly identified

and corrected.

The aforementioned

procedure upgrade performed appears to represent an inadequate

corrective

action to a previously

identified

violation.

This item is considered

unresolved

pending further iXRC evaluation.

~Res onse: Technical Specification 3.8.0 provides LCO's for AFW trains.The procedure cited in the finding provided instructions

which did in fact test the capability

of the trains of AFW.iVo requirement

was known to test the valves independently.

Procedure 3/0-OSP-075.1 now requires that each MOV is independently

verified capable of opening all FCV's.The steam supply MOV's (1003,1000

and 1005),are designed to trigger a switch upon opening to activate solenoids to allow operation of the flow control valves.Opening of each MOV will allow operation of all six flow control valves (three for each train).The violation identified

in Report Nos.50-250/80-35

and 50-251/80-36

addressed the failure to visuaLly verify the flow control valves would operate as designed.This previous violation did not explicitly

require verification

that the MOV's were independently

capable of opening all associated

AFW flow control valves.FPL conducted a procedure upgrade to include visual verification

of valve operation.

Procedures

3-OSP-075.1

and O-OSP-075.1

are followed to insure operability

of each train of auxiliary feedwater.

Operating valves 1000 and 1005 together verified operability

of train 1.However, these procedures

now require that each MOV is independently

verified to be capable of opening all FCV's.This will insure more prompt identification

of individual

component failure.

I

URI 85-00-13: Failure to meet a committment

in a FPL letter dated December 20, 1979 to install adequate communications

and DC lighting to support local AFW operations

during testing and during control room inaccessibility

is unresolved

pending further NRC evaluation.

~Res onse: FPL's letter dated 3uly 22, 1980 indicated that AFW system modificaitons

had negated the need to add DC lighting or a sound powered phone link and thus FPL did not consider the December 20, 1979 committment

to remain in effect.Nevertheless, DC lighting for the AFW pump area, feedwater platforms, and normal steam isolation valves has been completed, and a sound powered phone link between the AFW pump area and the control room will be complete by 3une 1986.

.C I

URI 85-00-10: The control room inaccessibility

procedure 0-ONOP-103

dated August 7, 1985, did not address the local operation of train 2 of the AFW system.This apparent failure to provide an adequate procedure to cover a safety related activity is unresolved

pending further NRC evaluation.

The procedure also did not provide instructions

on how to locally reset and restart a tripped AFW pump.~Res onse: Procedure O-ONOP-103, Control Room Inaccessibility, will be revised as follows: Prior to taking any operator actions at Train 1 of the AFW System, the operator will be directed to check the AFW flow gauges to determine train operability

and report the resulting finding to the Plant Supervisor

-Nuclear.2e A PC/M has been submitted to provide a means (reach rod)to make the instrument

air isolation valves for Train 2 of the AFW System easier to operate.A procedure change will be made as necessary to incorporate

any PC/ill induced information

into the procedure.

3.Instructions

and setpoints will be incorporated

to provide guidance to the operator of how to obtain proper flow to the steam generator utilizing a single AFW pump.Instructions

will be incorporated

to address balancing of the AFW System flow to provide a flow rate of 286 gpm to each unit in the.'vent only one pump is operable concurrent

with a dual unit trip.This will be the same as presently delineated

in EOP 20000 and 20007.5.Instructions

will be incorporated

to provide instructions

to the operator for locally resetting and restarting

a tripped AFW System pump One item of disagreement

with the report should be noted though.Isolation of the nitrogen valves at Train 1 of the AFW System does not isolate nitrogen to the Train 2 valves, therefore, the valve operation isolating nitrogen to Train 2 should not be deleted as stated in the report.No procedure change will be made.

IFI 85-00-15: A review of the training and procedural

improvements

for assurance that the plant can be safely controlled

from outside the control ro'om will be made at a later date by an NRC evaluated walkthrough

of the entire control room inaccessibility

procedure.

~Res onse: Extensive training for'perators and operator trainees on control room inaccessibility

has been conducted.

Each shift crew has conducted a walkthrough

of the procedure.

In addition this subject will be part of the next requalification

cycle training scheduled to start in March-1986.As indicated in the inspection

report"The upgrade in lighting communications, procedural

improvements;

and additional

training and walkthroughs

to be conducted by the license should provide reasonable

assurance that the plant can be safely controlled

from outside the control room."

IFI 85-00-16: Post-accident

radiation zone map 5177-119-SK41-I

dated April 27, 1981 indicates two of the AFW pumps would be in a very high radiation environment

for a Unit 3 LOCA.In addition, although dose rate instruments

are being kept in the control room, it appears that there is no guidance as to their use.~Res onse: The AFW pumps are not required for mitigation

of a large break LOCA on the affected unit.Should the pumps be required for the opposite unit, the personnel that would be required to take action on the two pumps would be staged in the onsite support center, where health physics review of tasks in the high radiation zone would be evaluated prior to dispatching

individuals

into the zones.All personnel required to work in radiation areas are trained to operate radiation detection instruments

and are aware of actions to be taken for high readings on the instruments.

In addition, FPL will conduct a review of the basis for the radiation map in question.

URI 85-00-17: Administrative

Procedure 0103.3, Control and Use of Temporary Systems Alteration, dated 3anuary 31'98k'ection

5.8 states, the Plant Nuclear Safety Committee (PNSC)is responsible

for reviewing applicable

nuclear safety-related

temporary system alterations

within 10 days of the Plant Supervisor-Nuclear

approval date.Apparently, the licensee's'PNSC

failed to review and document TSA 3-80-11-75, TSA 3/0-85-8-75, TSA3/0-80-99-75

and TSA 3/0-80-100-75

within the prescribed

time period.This appears to be another example of failure to implement approved procedures, and it is considered

unresolved

pending further NRC evaluation.

~Res onse: The TSA procedure (0-ADM-503)

has been revised 3anuary 10, 1986, to require prior PNSC review of TSA's for equipment in service or component substitution.

The 10 day review now applies only to TSA's implemented

on equipment or systems out of service or covered by a clearance.

This enhancement

of management

controls should reduce the likelihood

of recurrence.

~%

U RI-85-00-18:

Apparently, the licensee failed to perform an adequate safety evaluation

on TSAs 3-80-11-75, 3/0-80-99-75, 3/0-85-8-75

and 3/0-80-100-75, Removal of AF W Covernor Speed Control Systems, in that the safety evaluations

did not evaluate the mechanical

reliability

of the AFW pumps being operated under constant speed conditions.

This item is considered

unresolved

pending further NRC evaluation.

~Res onse: A safety evaluation

was conducted for these TSAs in accordance

with AP 0103.3.However, the mechanical

reliability

of the pumps operating at a constant speed within the previously

analyzed operating range was not addressed.

To enhance management

control of TSA evaluations, the Procedure (0-ADM-503)

has now been changed so that TSAs for equipment in service will be reviewed by the PNSC prior to installation.

The AFW pumps and turbines are designed to operate up to a normal operating speed of 5900 RPM.The governor on the turbine driver is installed and set to maintain speed at a high speed setpoint of 5900 RPM.It, is capable of receiving an external signal to vary turbine speed between 3200-5900 RPM...Until recently, an external air signal was provided by a differential

pressure controller

which maintained

a constant pressure drop across the flow control valves.Failure of this controller

resulted in the turbine being required to operate at constant speed.Removal of the differential

pressure controller

would also have resulted in the turbine operating at constant speed..This operating mode is within the previously

analyzed operating range for both the turbine and pump.The designed mechanical

reliability

of the equipment is not considered

to be reduced for that reason.

I

URI 85-00-19: It appears that the licensee failed to take prompt and adequate corrective

action to ensure that manual isolation valves 3-20-028 and 0-20-028, the common isolation valves for redundant safety-related

condensate

storage tank level instruments

were properly administratively

controlled.

This item is considered

unresolved

pending further NRC evaluation.

~Res onse: s The design bases for the addition of the redundant condensate

storage tank level indication

system, installed under PCM 80-77, was based on the connection

to the tank being a passive portion of the system which allowed the redundant monitors to be on a common tap.This approach is considered

acceptable

since a single passive failure of this line or the isolation valve is not a design basis for Turkey Point.Prior to the implementation

of PCM 80-77, the condensate

storage tank was provided with a single level transmitter

downstream

of Isolation Valve 028.When the redundant level indication

system was added downstream

of Valve 028, it was assumed that the operation of the valve was adequately

controlled

by administrative

procedure since PCM 80-77 did not modify either the tap off the tank or the valve.The need to control the isolation valve was not addressed in PCM 80-77 since the valve was existing and performing

the same function, and Operating Procedure 7001.1 administratively

controls Valve 028 in the open posi tion.In advertent closure of Valve 028 would create the potential for the operator to have misleading

information

concerning

the condensate

storage tank level.However, this is not considered

to be a significant

safety concern since there are other independent

methods of determining

tank level which would have alerted the operator to recognize that the level indication

system was not functioning

properly.Level Switch LS-3/0-1503, which is safety related, alerts the operator that the minimum Technical Specification

volume of 185,000 gallons is remaining in the tank, would be available since it is not associated

with this level tap.Should the condensate

storage tank reach this level, the operator would have noted a discrepancy

in the level readings and taken corrective

action.Also, control room alarms are available to alert operators with respect to tank level.The condensate

storage tank Technical Specification

also requires, by definition, a minimum volume of water for nineteen hours of Auxiliary Feedwater System'operation.

With the Auxiliary Feedwater System in operation and drawing on the inventory of the condensate

storage tank, the operator would have noticed that the condensate

storage tank level (as indicated by the redundant transmitters

and" checked by log readings)was not decreasing

during this time period and questioned

the validity of the level indication;

appropriate

corrective

action could have been taken.In addition, both condensate

storage tanks are normally aligned to the Auxiliary Feedwater pump suction.Assuming Valve 028 was inadvertently

closed on one tank, the level on the opposite tank would be operable.Since the levels in the

URI 85-00-19 (continued):

two tanks will decrease at approximately

the same rate, a disparity between the levels in the two tanks would have been recognized

by the operators and appropriate

corrective

action could have been taken.It should also be noted that the design modification

process has been substantially

improved since the time this modification

was implemented

in~recognition

of the need to coordinate

changes in the plant with operations

and maintenance

personnel.

A program for the review of proposed plant modifications

has recently been established

to ensure that the effects on operating documents, procedures

and administrative

controls are accommodated

in the design prior to approval of the PCM by the Plant Nuclear Safety Committee (PNSC).Engineering

personnel are also currently on controlled

distribution

for the plant operating procedures, which provides the design.engineer with a better insight into the actual operation of the system and the potential impact of modifications

of the system.Also, utilization

of Standard Engineering

Packages should greatly aid this area.As noted in the NRC report, Valve 028 has been locked open.In addition, the associated

drawings have been revised to show this valve locked open by administrative

control and the valve has been added to the locked valve list.Administrative

Procedure AP0103.5 (Administrative

Control of Valves, Locks and Switches)provides instruction

for placing valves, locks and switches under administrative

control when it is necessary to lock the valve or switch to prevent inadvertent

misoperation

of the valve or switch.These valves were added to the procedure revision approved November 13, 1985.

I

URI-85-00-20:

The apparent failure to ensure that procedure 3/O-OP-018.1, Condensate

Storage Tank, a safety-related

procedure was approved for release by authorized

personnel and appropriately

distributed

prior to the cancellation

of OP-7001.1, is considered

unresolved

pending further NRC evaluation.

~Res onse: This is considered

an isolated case which occurred due to the complexity

of the specific change.In this case several procedures

were being issued to replace one old procedure.

Because one of the replacement

procedures

was undergoing

review in a different section of the plant staff, the old procedure was inadvertently

cancelled when the remaining replacement

procedures

were issued.Administrative

Procedure 0109.7 provides guidance for the PUP group to cancel procedures

as new replacement

procedures

are generated.

IFI 85-00-21: The inspector noted several examples where cancelled procedures

were referenced

in other procedures

still in use.The inspector was informed by the licensee that at present there is no method for cross-referencing

procedures

to ensure that a cancelled or changed procedure does not affect another procedure.

The inspector informed the licensee that the development

of a method to ensure all procedures

are properly updated could be of benefit.This is an inspector followup item.~Res onse: It is currently the procedure writer's responsibility

to ensure that cancelled or changed procedures

do not affect another procedure.

FPL is considering

a proposal for a computer cross referencing

system.It is expected that a decision will be made on this potential enhancement

by March 15, 1986.

URI 85-00-22: The apparent failure to evaluate the impact of design changes on the AFW control system on the nitrogen consumption

rate is considered

an unresolved

item pending further NRC evaluation.

~Res onse:.The modification

to split the nitrogen backup system into two headers was issued for implementation

under the original scope of PCM 80-117 as shown on Drawing 5610-M-339/80-55, Revision 2, dated 3anuary 15, 1982.This design was established

by engineering

judgement (although not fully documented)

based on a technical evaluation

of the original design basis for the nitrogen backup system in consideration

of the following factors: o The total number of flow control valves supplied by the on-line bottles in the split system was half of that in the original design.The original design had one bottle on line serving six flow control valves.The modified system resulted in one bottle on line serving three flow control valves.o The total nitrogen consumption

for the modified system was significantly

less than the original system.The air consumption

rate of original flow control valves was 1.0 scfm per valve, as compared to the air consumption

rate for the replacement

valves of 0.26 scfm, based on the original regulator setpoint of 55 psig.o The pump differential

pressure controllers

were installed and operable, and maintaining

the design pressure drop across the flow control valves.On this basis, valve oscillations

were not an operational

problem.o The design flow rate through each flow control valve was 200 gpm.o The low pressure alarm setpoint for the nitrogen bottle system at the time the PCM was issued was 1005 psig, which allowed 15 minutes for the operator to take the necessary action to valve-in a new bottle.o Air operated hand controll'ers

for the flow control valves supplied by the backup nitrogen were removed from the system as defined in the scope of work under PCM 80-55.The split of the nitrogen system into separate trains under the original scope of PCM 80-117 was considered

acceptable

within the parameters

of the original design basis for this system.However, in response to NRC concerns with the engineering

judgement used as a basis for this modification, a detailed analysis of the nitrogen backup system was performed, based on the original design parameters

described above and worse case results of previous tests performed on the system.The results of this analysis are documented

in Calculation

MO8-062-05, Revision 0, dated November 1, 1985.This analysis demonstrates

that sufficient

nitrogen should have been available from the valved-in bottles in the

I

split system to permit the system to operate for more than 20 minutes without operator action following receipt of a low level alarm at 1005 psi.Based on these results, the split of the nitrogen system was confirmed to be consistent

with the original design basis and operating procedures

for the system.Responses to the specific NRC review team concerns are discussed below: o The NRC review team indicated that a steady-state

consumption

rate of 0.26 scfm was utilized in evaluating

the nitrogen consumption

rate for the new flow control valves, instead of a rate of 0.36 scfm.The 0.26 scfm-consumption

rate was based on the original regulator setpoint of 55 psig.As discussed above, Calculation

MO8-062-05

was prepared to analyze the available nitrogen from the split system.This analysis included a steady-state consumption

rate greater than 0.36 scfm to account for system leakage and the change in the regulator setpoint to 80 psig, and confirmed the acceptability

of the split system.o The NRC review team concluded that the assumption

of instantaneous

steady-state

operations

was not consistent

with the as-designed

valve response.As discussed above, the analysis supporting

the split nitrogen system was based on the original plant design features which limited flow control valve oscillations.

This is consistent

with the vendor's technical literature

which indicates that the valves quickly reach their setpoint with virtually no overshoot.

However, several changes were made to this system after PCM 80-117 was released for implementation, which induced oscillations

in the flow control valves and resulted in a subsequent

increase in the nitrogen demand for the system.These changes were unrelated to the original scope of PCM 80-117 and included the following:

1.The dif ferential pressure controllers

on the Auxiliary Feedwater System were disconnected

due to maintenance

problems with these components

and difficulties

in obtaining spare parts, which resulted in an increased pressure differential

across the flow control valves.This increased pressure differential

resulted in oscillation

in the flow control valves, and in increase in the nitrogen consumption

rate under test conditions

witnessed by the NRC review team.Removal of the pressure controllers

was justified by analysis on the basis that the excessive differential

pressure across since the steam generator pressure would rapidly rise to the safety valve setpoint.Under this condition, the pressure drop across the flow control valve would be essentially

the same regardless

of whether the differential

pressure controller

was installed.

2.Another change which induced oscillations

in the flow control valves was the reduction in the auxiliary feedwater flow rate from 600 gpm to 373 gpm.This reduced flow rate resulted from a Westinghouse

reanalysils

of the feedwater flow requirements

as documented

in

Westinghouse

letter W-PTP-62, dated 3une 3, 1982.As a result of this change, the setpoint for the flow control valves were revised to 125 gpm.Reduction in the setpoint compounded

the oscillation

problems in the flow control valves since the design basis for the system was established

at 200 gpm.Subsequent

to this change, a review of the valve oscillation

problem was made during field testing of this system.These tests confirmed that the control valves performed satisfactorily

under the original design condition of 200 gpm flow at 25 psi differential.

However, oscillating

control valve action was experienced

when the system was tested at the reduced flow rate of 125 gpm and the auxiliary feedwater pumps running at maximum speed.As a result of these tests, modifications

were recommended

to eliminate the valve oscillation

problems.It is anticipated

that new valve trim will be installed by the upcoming refueling outages for each unit.o The NRC review team noted that the reduction in the low pressure alarm setpoint from 1000 psi to 500 psi did not appear to be based on a documented

analysis.This change was made based on a field performance

test conducted on March 1, 1980.The criteria developed for the test was based on steady state operation of the valves on the understanding

that valve oscillations

were not a design basis for the system consistent

with the vendor's technical literature

which indicates that the valves quickly reach their setpoint with virtually no overshoot and the oscillations

identified

during testing would be eliminated

by subsequent

modifications

to the valves.The amount of time required for valving in the next bottle upon actuation of the low level alarm was established

at 10 minutes based on discussions

with plant operations

personnel.

A total of six flow control valves were included in the test to add conservatism

to the setpoint since only three valves are aligned to one open bottle in the new system arrangement.

Also, the valves operated for approximately

15 minutes based on the 500 psig setpoint which was considered

another safety factor margin for the setpoint.On this basis, the test is considered

to be a satisfactory

method of establishing

the low pressure alarm setpoint, in lieu of a documented

analysis.The NRC's concerns with the volume of available nitrogen to the flow control valves are directly related to the valve oscillation

problems witnessed during the inspection.

However, as discussed previously, valve oscillations

are not considered

a safety concern since the high differential

pressure across the flow control valves not expected to exist when the system responds to a design basis accident.FPRL has pursued resolution

of this problem in a systematic

manner through coordination

with its architect-engineer.

NRC's final evaluation

of its inspection

findings should give due recognition

to the fact that this problem was identified

by FPL prior to the inspection

and that design modifications

were in progress.

When the NRC audit identified

increased N2 consumption

due to the valve oscillations

noted during testing, FPL reanalyzed

the nitrogen system and revised the low pressure setpoint to 1350 psig, to allow a minimum of ten minutes for the operator to valve-in bottles based on a conservative

assumption

of valve oscillation

and with no credit taken for placing the valves in the manual mode.The low pressure alarm has been temporarily

reset in the field to this revised setpoint, and the appropriate.design documents have been revised.A surveillance

procedure to dynamically

test the nitrogen back-up system is currently being prepared and is scheduled for issuance by April 30, 1986.When implemented, this test should identify any detrimental

effects on nitrogen consumption

created by modifications

to the AFW system.

l

IF I 85-00-23: The AP 190.15, Document Verification

Checklist, is still not being completed under Step 5 which requires that changes to the"Q" List be listed.The entry on PC/M 83-117 contains"to be determined

by FPRL." Although the PC/M has been turned over and completely

closed out, necessary changes to the"Q" List have not been evaluated.

Plant personnel stated that this was due to the development

of the new, component level"Q"-List which will soon be issued.This check has been neglected on PC/Ms which have been processed during the"Q"-List development.

Once the"Q"-List has been promulgated, engineering

procedures

will be developed for maintenance

of the"Q"-List through evaluations

of system modifications.

This item will be left as an inspector followup item to verify appropriate

procedures

and responsibilities

are developed.

~Res onse: Turkey Point Plant and Power Plant Engineering

procedures

are currently in the process of review and modification

to incorporate

the new component level Q-List.At Turkey Point Plant, the Q-List Task Team has identified

the Administrative

Procedures

which will require modification.

The Procedures

have been marked up with the team's recommended

changes.A meeting will be scheduled for the end of January to discuss these proposed changes with Maintenance, Operations, QC, Procurement, and Procedure Update.At that time, an incorporation

schedule will be developed.

Power Plant Engineering

has developed draft Quality Instructions

for Q-List use and maintenance.

A meeting will be scheduled for the beginning of February to discuss comments on these procedures.

These procedures

are expected to be finalized and implemented

the end of February.Since the new Q-List reflects plant documentation

current as of May, 1985, there exists a"del'ta" between the Q-List and up to date documentation.

The Q-List contractor

is being retained to update the Q-List for FPL and this effort is expected to be complete by August 1986.Power Plant Engineering

will then proceed with future updates of the Q-List.Engineering

and plant personnel are now using the computerized

Q list.Training is underway and for the interim period while the new Q list is being fully implemented, the plant is also checking the PNSC approved prior Q list in addition to the new list.

IF I 85-00-20: The licensee is preparing an engineering

evaluation

addressing

how iong the AFW system must operate without operator action in the automatic flow control mode and subsequently

in the remote-manual

mode.This evaluation

will necessarily

impact on the required volume of stored nitrogen.It was also noted that the licensee is planning to add an additional

five-bottle

nitrogen supply so each train will have five bottles available.

The results of the engineering

evaluation

and the additional

nitrogen supplies will be tracked as an inspector followup item.~Res onse: The original nitrogen backup system for the auxiliary feedwater flow control valves consisted of five nitrogen bottles to supply motive power for six flow control valves.Original calculations

concluded that the five bottle station would provide sufficient

capacity for two hours of valve operation, however this was not a design basis requirement

for the system.The nitrogen station is designed to allow sufficient

time for bottle change out while maintaining

system operation.

A recent review of the present system has resulted in the preparation

of PC/M's to install additional

bottle stations for each unit to extend the presently sufficient

time to change out bottles during AFW system operation with the N2 station in use.The additional

bottle station for Unit 0 is scheduled for installation

during the current refueling outage.An evaluation

to more clearly address the operator action requirements

for the system is presently being prepared for incorporation

into the AFW system design basis document.

URI-85-00-25:

The inspector noted that a portion of the nitrogen system that was outside of the scope of NCR 301-85 was supported at intervals greater than the 36 inches specified by the licensee's"Design Guide for Seismic Class I'Instrument

Tubing Installation" for stainless steel tubing.This document is FPRL's specification

No.5177-3711, Revision 2.The requirement

for a maximum unsupported

span of 36 inches is adopted from the ASME Code Section III.Contrary to this design requirement, the inspector measured two adjacent supports that were 01 inches and 03 inches apart.Not only do these exceed the licensee's

seismic Class I requirements;

but the instrument

tubing was not attached to the central support between these two spans which creates a section of unsupported

tubing approximately

85 inches in length.The inspector also found a section of unsupported

stainless steel instrument

tubing in Unit 0 of 01 inches in length.Pending further review of the circumstances

which resulted in the nitrogen system not being seismically

supported, this item is considered

unresolved.

~Res onse: All of the specific support conditions

identified

during the inspection

have been evaluated and the system has been determined

operable based upon functionality

criteria.To further identify potentially

unsupported

connections

to the auxiliary feedwater system and other safety systems, FPL has initiated a program to walkdown and"as built" all 2 inch and under piping associated

with these systems not evaluated under IE Bulletin 79-10.

~1

URI 85-00-26 Consideration

for NPSH was not documented

in the FPRL calculation, Low Level Alarm on Condensate

Storage Tank, dated November 15, 1979, and the calculation

inadequately

identified

the necessary assumptions

and"design inputs.An informal, undated, untitled, annotated sketch was presented by the licensee as evidence of NPSH consideration, which had not been properly referenced

in the November 15, 1979, calculation.

The sketch lacked proper identification

and detail to permit an understandable

review.It appears that the licensee failed to adequately

document all assumptions

and design inputs for FP2L's calculation

of November 15, 1979, on the Low Level Alarm on Condenste Storage Tank.This item is considered

unresolved

pending further NRC evaluation.

~Res onse: The in'spection

report stated that"...the preparer appeared to have assumed that the minimum NPSH would be below the instrument

tap, because the analysis calculated

the height above the instrument

tap which corresponds

to 20 minutes of water at a usage rate of 600 gpm with a 10'actor for conservation.

The team independently

confirmed that the NPSH is well below the instrument

tap and the design is not deficient".

Engineering

has found evidence on the microfilm records which indicates that NPSH was considered

in the original calculation.

However, this consideration

for NPSH was not documented

in the FPL calculation

dated November 15, 1979.Calculation

MO3-062-01, dated October 1, 1985, was recently performed to confirm that the required NPSH water level for flows anticipated

at the end of the cooldown transient is below the instrument

tap level as assumed in the original calculation.

The new calculation

confirmed the results of the original calculation,.and

therefore the equipment and associated

condensate

tank level setpoints are acceptable.

Enhanced documentation

of calculation

assumptions

are being pursued for both internally

and contractor-developed

calculations.

Quality Instruction

revisions have been or are in the process of being issued to provide enhanced controls for documentation

of calculational

assumptions

and inputs for both internal and contractor-developed

calcula'tions.

I

URI 85-00-27: The inspector located two subsequent

examples of OTSCs which were processed as a change of intent.On November 12, 1985, the PNSC reviewed and the plant manger approved OTSC No.3730 to TOP 206, Reactor Protection

System Periodic Test (Unit 0).The change of intent guidelines

checklist indicated that this change did alter the intent of the original procedure.

This procedure change was made in response to IE Bulletin 85-02.On November 12, 1985, the PNSC also reviewed and the plant manager approved OTSC No.3733 to AP 103.12, Notification

of Significant

Events to the NRC.The change of intent guidelines

checklist indicated that this change did alter the intent of the original procedure.

This procedure change was also made in response to IE Bulletin 85-02.The conduct of these two temporary procedure changes is being further reviewed by the NRC and considered

an unresolved

item.~Res onse: Administrative

Procedure 0109.3 (On the Spot Changes to Procedures)

is being revised to differentiate

between temporary changes made in accordance

with Technical Specification 6.8 and on the spot changes made with prior PNSC approval.The temporary change instructions

will strengthen

controls so that no changes to the intent of procedures

will be made under this portion of the procedures.

Because prior PNSC approved OTSC will be given all required safety reviews, change of intent will be allowed for this type procedure change.

I

IF I 85-00-28: A review of the new maintenance

training and the qualification

tracking system will be an inspector followup item.~Res ense: FPL personnel will be available to discuss the new maintenance

training and the qualification

tracking systems during the implementation

and upon completion

of the project.

URI 35-00-29: There appears to be a difference

in the philosophy

between the manufacturer's

recommended

motor overload heater size and the size chosen by the licensee in order to agree with Regulatory

Guide 1.106.This item will require further review by NRC and is identified

as an unresolved

item.~Ree onse: As stated in our previous response to this item contained in our letter L-S5-039, Turkey Point has made no commitment

to utilize the Limitorque

sizing recommendations

for overload heaters.Our current design meets the general intent of Reg.Guide 1.106.The overload heaters are sized by the heater manufacturer

using his standard sizing criteria and the applicable

plant motor data.We have however, determined

that we will re-evaluate

our philosophy

on overload heater sizing in accordance

with the Limitorque

sizing recommendations

and Regulatory

Guide 1.106, taking whatever action is required.

URI 85-00-30: The safety system functional

inspection

team inspector expressed concern that the MOVs would not function under the conditions

as stated in the manufacturer's

letter and therefore requested a review of the manufacturer's

calculations

or that testing be performed at the low voltage conditions

to verify acceptability.

Additionally, the reduced voltage will result in an increased operating travel time.This added time should be reviewed to determine if any ISI requirements

are affected.This item will be unresolved

until a review of the manufacturer's

calculations

or testing of these MOVs at reduced voltage is accomplished.

~Res onse: As stated in our previous response to this item contained in our letter L-85-039, calculation

5177-062-EOI

was prepared utilizing a very conservative

starting current of 53 amps.Subsequently

this calculation

has been reviewed utilizing the Limitorque

data for starting current and the results indicate that the voltage at all of the subject valves will exceed 90V.This reduced voltage at MOV-0-1003 will result in a slightly increased stroke time which based upon a preliminary

investigation

should not adversely affect the design basis for the Auxiliary Feedwater System.FPL is preceeding

with preparation

of a revision to calculation

5177-062-EOI

utilizing the Limitorque

data for starting current and also with a formal review'o determine what effect, if any, increased MOV stroke time may have on the design basis for the Auxiliary Feedwater System.These items are expected to be completed by February 21, 1986.

'I

URI 85-00-31: The safety system functional

inspection

team expressed concern regarding the operation of a second steam vent valve that had been added between the steam admission valves and the AFW pump turbine.Bechtel Power Corporation

calculations

No.MO8-062-02

approved September 30, 1985 (for low steam pressure conditions)

and No.MO8-162-02, approved November 20, 1981 (for high steam pressure conditions)

indicate that a 17'argin of steam is available with the 3/0" vent valve open which would be the condition for loss of AC.This item will remain unresolved

pending review of the calculations

by the NRC.~Res onse: The non-safety

related classification

for the steam vent valve added under PC/M 80-117 is consistent

with the original design basis for the plant.As discussed previously

in response to item 85-00-10, a detailed analysis was performed prior to equipment installation (Bechtel calculation

MO8-162-02

approved November 20, 1981)which confirmed the capability

of the AFW system to operate if the vent valve failed open.Bechtel calculation

M-08-062-02

approved September 30, 1985 was performed to confirm previous engineering

judgement and insure system operability

with the failed vent for the full operating range of the system.On this basis, there has no reason to power the steam vent from a safety related power source and powering the valve from a non safety AC source is considered

acceptable.

To support the NRC review, the referenced

calculations

are available at the Turkey Point Plant site.

1

URI 35-00-32: It appears that the low nitrogen pressure switches were not reviewed during the Seismic Qualification

of Auxiliary Feedwater System evaluation.

The licensee advises that these switches arg part of the original design and therefore, not designed or considered

safety-related.

However, current plant emergency operating procedures

require action by the operator upon receipt of the nitrogen low pressure alarm.Additionally, consideration

must be given to the fact that the nitrogen system is a backup system and the status of backup system should be known at all times.Since there appears to be confusion as to the safety-related

application

of these switches, this item is unresolved

pending further NRC review.~Res onse: As stated in our previous response to this item contained in our letter L-35-039, the design modifications

for the Auxiliary Feedwater System utilized the pressure switches and annunciation

system installed under the original plant construction, which were neither designed nor maintained

as nuclear safety-related.

As a result, the separation

criteria for these components

was not changed from the original design basis of the plant, and ANSI N05.2.11 does not apply.However, we have determined

that this system will be redesigned

as part of the Auxiliary Feedwater System upgrade which involves the addition and relocation

of the Auxiliary Feedwater Nitrogen Stations.This redesign will consist of the installation

of new qualified pressure switches, indicators

and wiring thereto.A pressure switch at each station will be alarmed in the Control Room with a trouble light and will be of a safety grade design.

~s~URI 85-40-33: The inspector reviewed Tech Spec.0.8.2.b and determined

that it requires the licensee to monthly perform an equalizing

charge on each battery and to take specific gravity and the voltage readings of each cell.It is Plant Procedure 9600.1 which implements

this requirement.

However, it appears that this Technical Specif ication requirement

is more applicable

to lead antimony batteries which were the original type of batteries installed at Turkey Point.The Gould-GNB manual recommends

that lead calcium batteries should be given an equalize charge only when needed.The inspector also observed that Plant Operating Procedure 9600.1 identifies

two different float voltages for the Gould-GNB NCX type batteries.

The inspector questioned

the licensee about the acceptability

of Tech Spec 0.8.2.b and about what effects this monthly equalize charge may have on the lead calcium batteries.

The licensee indicated that they would contact the vendor to determine the acceptability

of the current licensee requirements.

This item is identified

as unresolved

item pending licensee and NRC evaluation.

~Res onse: We have contacted the battery manufacturer, Gould, with regards to the acceptability

of Technical Specification 0.8.2.b and the effect<he monthly equalizing

charge may have on the lead calcium batteries.

Gould has stated that the overcharging

of the batteries at IOOVDC once a month does not have any appreciable

effect on the battery qualified life.In order to clarify the battery charging requirements, a Technical Specification

change to provide for an as-needed equalizing

change will be submitted by March 31, 1986.This date revises that provided in our letter, L-85-039, dated December 6, 1985.This time extension allows for a more thorough review of the requirements

and better coordination

with the Standard Technical Specification

Project.

J y~

URI 85-00-30: Technical Specification 0.8.2.b states that monthly, each battery shall be given an equalizing

charge, and afterwards

specific gravity and voltage readings shall be taken and recorded for each cell.It appears that Plant Operating Procedure 9600.I dated August 7, 1985, was inadequate

in that it did not contain vendor recommendations

for compensating

cell specific gravity readings for electrolyte

temperature

and level.Furthermore, the procedure did not contain acceptance

criteria for the specific gravity readings.This item is considered

unresolved

pending further NRC evaluation.

~Res onse: Plant Operating Procedure 9600.1 dated December 0, 1985 was revised to require specific gravity correction

for electrolyte

temperature

and level.This procedure was also revised to contain acceptance

criteria for the specific gravity readings.This procedure change had been planned prior to the inspection, but had not been completed.

sl.)~~

The original battery specification

and the specification

for the new batteries required a capacity of supplying the specified loads for one hour without the battery terminal voltage falling below 105 VDC.It should be noted that the testing of the batteries did not meet the intent of the specification

design requirements

nor the acceptance

criteria identified

in the FSAR.This appears to be another example of an inadequate

procedure since test procedures

for the initial testing of batteries 3A and 36 did not require load testing that verifies that the commitments

of the FSAR or the design specifications

were met.This item is considered

unresolved

pending further NRC evaluation.

~Res onse: FPL considers that the present one-half hour battery service test is adequate to demonstrate

that the.battery is capable of performing

its intended safety function.This is based on the assurance described in the Bases for the Technical Specification, that considering

any single failure, battery charging current should be supplied in one-half hour or less.However, we are evaluating

the discussion

in the FSAR to determine if the present battery test should be modified.

k g 4

URI 85-00-36: Mechanical

maintenance

personnel were uncertain regarding the type of grease-to be used in MOV gearboxes.

This was considered

a problem for two reasons.First, the mixing of different types of grease in the gearbox could cause hardening or separation

of the lubricant.

The potential for this exists at Turkey Point because its preventive

maintenance

instructions

for Limitorque

gearboxes specify the use of Texaco Marfac, while these same Limitorques

have been supplied with either Exxon Nebula EPO or EPI or Sun 50 EP lubricants.

Secondly, the only Limitorque

lubricant that meets the environmental

qualification

requirements

of 10 CFR 50.09 at Turkey Point is Exxon Nebula EPO or EPI.~Res onse: Exxon Nebula is, for MOV's inside containment, the only Limitorque (MOV'earbox)lubricant that currently meets the environmental

qualification

requirements

of 10 CFR 50.09.Preventive

Maintenance

instructions

for Limitorque

gearboxes, which specified the use of Texaco Marfac, have been pulled and are no longer in use at Turkey Point.The Lubrication

Manual's current revision specifies usage of only environmentally

qualified grease.This manual is now a PNSC reviewed document.MOV gearbox grease has been sampled and changed as appropriate.

Additionally, an Engineering

Evaluation

has been performed and forwarded to the Region II Administrator

on November 27, 1985 (L-85-008)

documenting

the justification

for prior limited operation with various greases in Limitorque

Valve Actuators.

In addition, instructions

were in the process of being revised to address this issue when the inspection

team reviewed this issue.The CEMS planners, who make up the work packages, were not uncertain about the type of grease to be used.Finally the grease guns used for maintenance

are now in a controlled

system..

A C~Ii

URI 85-00-37: During the AFW system walkdown, a Region II NRC inspector observed that the governor oil in the licensee's"A" AFW pump appeared to be different than that in the"B" and"C" turbine governors.

The inspector requested any licensee controls or historical

data along with vendor information

which would identify the control oil in the governors.

The licensee did produce the vendor manual with specific oil requirements;

however, the licensee had to have performed an oil analysis to determine the oil in the governors.

This analysis established

that a Texaco lOW'oil was being used in the"A" AFW governor and Texaco 30W in the"B" and"C" governor.The inspector expressed concern regarding whether the oil met vendor recommendations.

It was later determined

by the licensee that the Texaco 10W did not meet'vendor temperature

recommendations

for the licensee's

AFW operation.

This item is considered

unresolved

pending further NRC evaluation.

~Res onse: To address the concern regarding apparent difference

between the oil used in the"A" AFW turbine governor and that in the"B" and"C" turbine governors, we have sent samples for analysis to determine the specific oil used in each turbine governor.The results of the analyses identified

that the"A" AFW turbine governor contained an SAE 10 weight oil (similar to Texaco Regal 32 used on site)and the"B"'and"C" turbine governors contained an SAE 20 weight oil (similar to Texaco Regal 68 used on site).To determine the correct oil to use in the AFW turbine governors, it is necessary to define the governor oil operating temperature

range.Preliminary

data was taken during turbine operation on November 25, 1985 to determine governor oil operating temperature.

Comparing the data and specific oil weight to'information

provided in Woodward Governor Company Manual 25071C,"Oils for hydraulic controls" it was concluded that both oils are acceptable

for use in the AF W turbine governors.

To determine the optimum oil for use in the AFW turbine governors, we have developed a governor testing program which will provide additional

information

to be used for oil selection.

(~'~o v

IFI 85-00-38: For the AFW flow control valves to meet the requirements

of the present"FAIL-SAFE" test, they must be successfully

exercised full open, then closed from the control room with visual verification

at the valve.The power is not removed, nor is the air/nitrogen

supplies isolated.ASME Code Section XI, Division 1, IWV-3015, Fail-Safe Valves states, when practical, valves with fail-safe actuators shall be tested by observing the operation of the valves upon loss of actuator power.If these valves cannot be tested once every 3 months, they shall be tested during each cold shutdown;in case of frequent cold shutdowns, these valves need not be tested more often than once every 3 months.As of November 22, 1985, a request for engineering

assistance

was being generated by the Turkey Point Nuclear Technical Department

for the review of the present fail-safe testing method for these valves, identification

of inadequacies

in the fail-safe testing procedure, and development

of a method for proper fail-safe testing of these valves.This will be an inspector followup item.~Res onse: The auxiliary feedwater control values are designed to fail in the closed position by spring action on loss of air or power, For these valves to pass a fail-safe test in accordance

with IWV-3015 of Section XI of ASME boiler and pressure vessel code, valves with fail-safe actuators shall be tested by observing"operation

of these valves upon loss of actuator power.Present plant procedures

3/0-OSP-075.1 and 3/O-OSP-075.2

require these valves to be exercised full open, then closed from the control room with visual verification

at the valve to address the code requirement.

Additionally, the valves are verified in the closed position when the testing is terminated

and the steam supply MOV's (1003, 1000 and 1005)for that unit are closed which isolates power to the solenoids.

A review of the present fail-safe testing is being performed to assure compliance

with Section XI and subsequent

recommendation

for any testing modifications

will be provided by March 28, 1986.

K