ML19338G195

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LER 80-076/03L-0:on 800923,flow Integrator Fq 7032 for Drywell Floor Sump Pump Was Not Operating.Cause Undetermined
ML19338G195
Person / Time
Site: Pilgrim
Issue date: 10/23/1980
From: Mcloughlin M
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19338G193 List:
References
LER-80-076-03L, LER-80-76-3L, NUDOCS 8010280579
Download: ML19338G195 (1)


Text

(777i LICENSEE EVENT REPORT

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o EVENT DESCRIPTION AND PROBABLE CONSEOUENCES IO I2I l On September 23, 1980 at approximate y 2210 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.40905e-4 months <br /> while operating the Drywell Floor  ;

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Sump Pump the operator noted that the associated Flow Integrator FQ 7032 was not l

,,,,,, operating. To determine the amount of unidentified reactor coolant leakage the

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alternate system as specified in Technical Specification Table 3.2.E was utilized. y l 0 (6 l l I 10171 l l 10181 I 80 I

7 8 9 E CODE SU CO E COMPONENT CODE SU8 CODE S E 1019l 7 8

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SEQt.;ENTIAL OCCURRENCE REPORT R EVISION LER EVENT YEAR R EPORT NO. CODE TYPE NO.

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,,,,,21 22 23 24 26 27 28 29 30 31 32 N C o ONP NT M TH HOURS S 8 i POR 8. SUP t.tE MA UFA RER lZl@lZl@ l35Z l@ lZ]@ l 010 l 0 l0 l lNl@ l42N l@ lNl@ lFl0l8l0l@

33 J4 36 31 40 41 43 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h li iO l l Instrument and Control personnel on two occasions inspected the integrator and found l

,i,,jl 'it functioning in its intended manner. No cause for the September 23 malfunction l

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ST 2d  % POWER OTHER STATUS IS RY D.SCOVERY OESCRIPTION N.A. Operational Event I115

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A$TiveTY CONTENT CELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE l1 l6l N.A. N.A.

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' PERSONNEL iNauNiES NUMBER DESCRIPTtON N.A.

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LOSS OP OR OAMAGE TO FACluTY TYPE ' OESCRIPTION g lZl@l N.A. l 7 8 9 10 30 e

N.A. llllllllllll lj 12101 ISSUE'l @DE CRIPTION l 68 o 80 s 7 e S0102805[.8l M. Thomas McLoughlin ,617-746-7900 _

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