ML17251A498: Difference between revisions

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=Text=
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{{#Wiki_filter:,.ACCELERATED DlS'JBUTION DEMONSTRATION SYSTEM~'PDOCKET05000244REGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:8905250264 DOC.DATE:
{{#Wiki_filter:,.ACCELERATED DlS'JBUTION DEMONSTRATION SYSTEM~'P DOCKET 05000244 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8905250264 DOC.DATE: 89/05/12 NOTARIZED:
89/05/12NOTARIZED:
NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION MECREDY,R.C.
NOFACIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester GAUTH.NAMEAUTHORAFFILIATION MECREDY,R.C.
Rochester Gas&Electric Corp.RECIP.NAME
Rochester Gas&ElectricCorp.RECIP.NAME
'ECIPIENT AFFILIATION MURLEY.,T.E.
'ECIPIENT AFFILIATION MURLEY.,T.E.
OfficeofNuclearReactorRegulation, Director(Post870411R
Office of Nuclear Reactor Regulation, Director (Post 870411 R


==SUBJECT:==
==SUBJECT:==
Part21reptredefectconsisting ofinterference betweenmechanical sealpumpingring6pumpdischarge housing.jDISTRIBUTION CODE:IEISDCOPIESRECEIVED:LTR 2ENCL(SIZE:DTITLE:Part21Rept(50DKT)NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
Part 21 rept re defect consisting of interference between mechanical seal pumping ring 6 pump discharge housing.j DISTRIBUTION CODE: IEISD COPIES RECEIVED:LTR 2 ENCL (SIZE: D TITLE: Part 21 Rept (50 DKT)NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
05000244SRECIPIENT IDCODE/NAME PD1-3LAJOHNSON,A INTERNAL:
05000244 S RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: AEOD/DOA IRM TECH ADV NRR CRUTCHFIELD NRR/DEST/ADE 8H NRR/DLPQ/PEB 10 NRR/DRI B 9D R 01 RGN1 RGN3 RGN5 EXTERNAL: INPO RECORD CTR NRC PDR COPIES LTTR ENCL 1 0 1 1 1 1 l." 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DS P/TPAB IRM/DCTS/DAB NRR VARGA,S NRR/DEST/ADS 7E NRR/DOEA/GCB 11 NUDOCS-ABSTRACT RES/DSIR/EIB RGN2 RGN4 LPDR NSIC SILVER,E COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1.1 R I S h NOIR'IO ALL"RIDS" RECZPIENIS
AEOD/DOAIRMTECHADVNRRCRUTCHFIELD NRR/DEST/ADE 8HNRR/DLPQ/PEB 10NRR/DRIB9DR01RGN1RGN3RGN5EXTERNAL:
~PLEASE HELP US TO REDUCE HASTE!CONI'ACI'IHE DOCUMENI'XNIROL DESK, ROOM Pl-37 (EXT.20079)IO ELIMINATE RXlR NAME FRCH DZSTRIK7XXON LTSTS FOR DOCUMENTS YOU DON'T HEZD9 D S TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 25 "Cg~znr rzzzn/'PIE//I//jfll PAINE ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER, N.K 14649 0001 TCLCPHONF Ance cooL 7ie 546.2700 May 12, 1989 Dr.Thomas E.Murley, Director Office of Nuclear Reactor Regulation U.S.Nuclear Regulatory Commission 8'ashi ngton, DC 20555
INPORECORDCTRNRCPDRCOPIESLTTRENCL101111l."111111111111111111111RECIPIENT IDCODE/NAME PD1-3PDAEOD/DSP/TPABIRM/DCTS/DAB NRRVARGA,SNRR/DEST/ADS 7ENRR/DOEA/GCB 11NUDOCS-ABSTRACT RES/DSIR/EIB RGN2RGN4LPDRNSICSILVER,ECOPIESLTTRENCL11111111111111111111111.1RIShNOIR'IOALL"RIDS"RECZPIENIS
~PLEASEHELPUSTOREDUCEHASTE!CONI'ACI'IHE DOCUMENI'XNIROL DESK,ROOMPl-37(EXT.20079)IOELIMINATE RXlRNAMEFRCHDZSTRIK7XXON LTSTSFORDOCUMENTS YOUDON'THEZD9DSTOTALNUMBEROFCOPIESREQUIRED:
LTTR26ENCL25 "Cg~znrrzzzn/'PIE//I//jfll PAINEROCHESTER GASANDELECTRICCORPORATION o89EASTAVENUE,ROCHESTER, N.K146490001TCLCPHONF AncecooL7ie546.2700May12,1989Dr.ThomasE.Murley,DirectorOfficeofNuclearReactorRegulation U.S.NuclearRegulatory Commission 8'ashington,DC20555


==Subject:==
==Subject:==
Notificat'ion of10CFRPart'1R.E.GinnaNuclearPowerStationDocketNo.50-244LicenseeNo.DPR-18
Notificat'ion of 10CFR Part'1 R.E.Ginna Nuclear Power Station Docket No.50-244 Licensee No.DPR-18  


==DearMr.Murley:==
==Dear Mr.Murley:==
Rochester GasandElectricissubmitting theattached10CFRPart21Evaluation andNotification.
Rochester Gas and Electric is submitting the attached 10CFR Part 21 Evaluation and Notification.
Thenotification concernsadefectindesignoftwo(2)ResidualHeatRemovalPumpssuppliedbyPacificPump,Inc.ofLosAngeles,CA.Thedefectconsistofaninterference betweenthemechanical sealpumpingringandthepumpdischarge housing.Thedefective designedpumpingringswereinstalled in1969,duringtheconstruction phase,asaresultofamechanical sealmodification.Themechanical sealwassuppliedbyCranePackingCompany.Duetothedateofoccurrence, thecondition istechnically not10CFRPart21reportable.
The notification concerns a defect in design of two (2)Residual Heat Removal Pumps supplied by Pacific Pump, Inc.of Los Angeles, CA.The defect consist of an interference between the mechanical seal pumping ring and the pump discharge housing.The defective designed pumping rings were installed in 1969, during the construction phase, as a result of a mechanical seal modi fi cati on.The mechanical seal was suppli ed by Crane Packing Company.Due to the date of occurrence, the condition is technically not 10CFR Part 21 reportable.
However,duet'othesignificance of'hepotential pumpdegradation, Rochest'er GasandElectricissubmit'ting voluntary notification.
However, due t'o the significance of'he potential pump degradation, Rochest'er Gas and Electric is submit'ting voluntary notification.
Specificinformation regarding failureident'ificationandcorrective act'iontakenaredetailedontheenclosedAtt'achment'.
Specific information regarding fai lure i dent'ifi cation and corrective act'i on taken are detailed on the enclosed Att'achment'.
Shouldfurtherinformation berequired, pleasecontactMr.ThomasMarlow,SuperintendentofGinnaSupportServiceson315/524-4446.
Should further information be required, please contact Mr.Thomas Marl ow, Superi ntendent of Gi nna Support Servi ces on 315/524-4446.
S905250264 890Si2ADOCK05000244PDC Page210CFRPart21May12,1989Verytrulyyours,RobertC.MeredGeneralManagerNuclearProduction xc'r.WilliamT.Russell,RegionalAdministrator U.S.NuclearRegulatory Commission RegionI475Allendale RoadKingof'russia, PA2.9406zc:GinnaSeniorResidentInspector I
S905250264 890Si2 ADOCK 05000244 PDC Page 2 10CFR Part 21 May 12, 1989 Very truly yours, Robert C.Me red General Manager Nuclear Production xc'r.William T.Russell, Regional Administrator U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of'russia, PA 2.9406 zc: Ginna Senior Resident Inspector I
Attachment IName:Title:Facility:
Attachment I Name: Title: Facility: Docket No.: Robert C.Mecredy General Manager Nuclear Production R.E.Ginna Nuclear Power Plant 50-244 Basic Component:
DocketNo.:RobertC.MecredyGeneralManagerNuclearProduction R.E.GinnaNuclearPowerPlant50-244BasicComponent:
Supplier: Sub-Suppli er: Nature of Defect: RHR Pumps Pacific Pump Inc., Los Angeles, CA Crane Packing Company Mechanical seal pump ring interference with pump discharge housing.In discussion wi th Original Equipment Manufacturer, discovered during a root cause i nvesti gati on, there was a di mensi onal tolerance issue between the originally supplied mechanical seal outside diameter and the pump casing bore inside diameter.It was determined the mechanical seals were changed out during the plant construction phase and replaced with an alternate mechanical seal.Apparently, at this time, the original pumping ring was replaced with a new style ring with no attention paid to the impact of this change with respect to pump casing bore inside diameter.Date obtained: Rubbing between the pumping ring and the pump housing could cause degradation to the pumping ring with the potential for damage to the pump rotating assembly.Condition is technically not Part 22 violation due to date of occurrence (prior to 2978).April 28, 2989 Basic Components Affected: Number: Locati on: 2 Auxiliary Building, Sub-basement Corrective Action: Machined outside diameter of pumping ring at supplier<s direction to permit proper placement in pump discharge housing.
Supplier:
Responsible Individual for Action: Thomas A.Marlow, Superintendent Ginna Support Services Time to Complete Action: Action was completed on both pumps Apri l 29, 1989.Advice Related to Defect': Vendor supplied repair direction.
Sub-Suppli er:NatureofDefect:RHRPumpsPacificPumpInc.,LosAngeles,CACranePackingCompanyMechanical sealpumpringinterference withpumpdischarge housing.Indiscussion withOriginalEquipment Manufacturer, discovered duringarootcauseinvestigation,therewasadimensionaltolerance issuebetweentheoriginally suppliedmechanical sealoutsidediameterandthepumpcasingboreinsidediameter.
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Itwasdetermined themechanical sealswerechangedoutduringtheplantconstruction phaseandreplacedwithanalternate mechanical seal.Apparently, atthistime,theoriginalpumpingringwasreplacedwithanewstyleringwithnoattention paidtotheimpactofthischangewithrespecttopumpcasingboreinsidediameter.
Dateobtained:
Rubbingbetweenthepumpingringandthepumphousingcouldcausedegradation tothepumpingringwiththepotential fordamagetothepumprotatingassembly.
Condition istechnically notPart22violation duetodateofoccurrence (priorto2978).April28,2989BasicComponents Affected:
Number:Location:2Auxiliary
: Building, Sub-basement Corrective Action:Machinedoutsidediameterofpumpingringatsupplier<sdirection topermitproperplacement inpumpdischarge housing.
Responsible Individual forAction:ThomasA.Marlow,Superintendent GinnaSupportServicesTimetoCompleteAction:Actionwascompleted onbothpumpsApril29,1989.AdviceRelatedtoDefect':Vendorsuppliedrepairdirection.
0II}}

Revision as of 14:47, 7 July 2018

Part 21 Rept Re Degradation to Pumping Ring from RHR Pumps Supplied by Pacific Pump,Inc & Mechanical Seal Supplied by Crane Packing Co.Conditon Technically Not 10CFR21 Reportable Due to 1978 Date of Occurrence
ML17251A498
Person / Time
Site: Ginna Constellation icon.png
Issue date: 05/12/1989
From: MECREDY R C
ROCHESTER GAS & ELECTRIC CORP.
To: MURLEY T E
Office of Nuclear Reactor Regulation
References
REF-PT21-89, REF-PT21-89-079-000 PT21-89-079-000, PT21-89-79, NUDOCS 8905250264
Download: ML17251A498 (7)


Text

,.ACCELERATED DlS'JBUTION DEMONSTRATION SYSTEM~'P DOCKET 05000244 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8905250264 DOC.DATE: 89/05/12 NOTARIZED:

NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME AUTHOR AFFILIATION MECREDY,R.C.

Rochester Gas&Electric Corp.RECIP.NAME

'ECIPIENT AFFILIATION MURLEY.,T.E.

Office of Nuclear Reactor Regulation, Director (Post 870411 R

SUBJECT:

Part 21 rept re defect consisting of interference between mechanical seal pumping ring 6 pump discharge housing.j DISTRIBUTION CODE: IEISD COPIES RECEIVED:LTR 2 ENCL (SIZE: D TITLE: Part 21 Rept (50 DKT)NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).

05000244 S RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: AEOD/DOA IRM TECH ADV NRR CRUTCHFIELD NRR/DEST/ADE 8H NRR/DLPQ/PEB 10 NRR/DRI B 9D R 01 RGN1 RGN3 RGN5 EXTERNAL: INPO RECORD CTR NRC PDR COPIES LTTR ENCL 1 0 1 1 1 1 l." 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DS P/TPAB IRM/DCTS/DAB NRR VARGA,S NRR/DEST/ADS 7E NRR/DOEA/GCB 11 NUDOCS-ABSTRACT RES/DSIR/EIB RGN2 RGN4 LPDR NSIC SILVER,E COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1.1 R I S h NOIR'IO ALL"RIDS" RECZPIENIS

~PLEASE HELP US TO REDUCE HASTE!CONI'ACI'IHE DOCUMENI'XNIROL DESK, ROOM Pl-37 (EXT.20079)IO ELIMINATE RXlR NAME FRCH DZSTRIK7XXON LTSTS FOR DOCUMENTS YOU DON'T HEZD9 D S TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 25 "Cg~znr rzzzn/'PIE//I//jfll PAINE ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER, N.K 14649 0001 TCLCPHONF Ance cooL 7ie 546.2700 May 12, 1989 Dr.Thomas E.Murley, Director Office of Nuclear Reactor Regulation U.S.Nuclear Regulatory Commission 8'ashi ngton, DC 20555

Subject:

Notificat'ion of 10CFR Part'1 R.E.Ginna Nuclear Power Station Docket No.50-244 Licensee No.DPR-18

Dear Mr.Murley:

Rochester Gas and Electric is submitting the attached 10CFR Part 21 Evaluation and Notification.

The notification concerns a defect in design of two (2)Residual Heat Removal Pumps supplied by Pacific Pump, Inc.of Los Angeles, CA.The defect consist of an interference between the mechanical seal pumping ring and the pump discharge housing.The defective designed pumping rings were installed in 1969, during the construction phase, as a result of a mechanical seal modi fi cati on.The mechanical seal was suppli ed by Crane Packing Company.Due to the date of occurrence, the condition is technically not 10CFR Part 21 reportable.

However, due t'o the significance of'he potential pump degradation, Rochest'er Gas and Electric is submit'ting voluntary notification.

Specific information regarding fai lure i dent'ifi cation and corrective act'i on taken are detailed on the enclosed Att'achment'.

Should further information be required, please contact Mr.Thomas Marl ow, Superi ntendent of Gi nna Support Servi ces on 315/524-4446.

S905250264 890Si2 ADOCK 05000244 PDC Page 2 10CFR Part 21 May 12, 1989 Very truly yours, Robert C.Me red General Manager Nuclear Production xc'r.William T.Russell, Regional Administrator U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of'russia, PA 2.9406 zc: Ginna Senior Resident Inspector I

Attachment I Name: Title: Facility: Docket No.: Robert C.Mecredy General Manager Nuclear Production R.E.Ginna Nuclear Power Plant 50-244 Basic Component:

Supplier: Sub-Suppli er: Nature of Defect: RHR Pumps Pacific Pump Inc., Los Angeles, CA Crane Packing Company Mechanical seal pump ring interference with pump discharge housing.In discussion wi th Original Equipment Manufacturer, discovered during a root cause i nvesti gati on, there was a di mensi onal tolerance issue between the originally supplied mechanical seal outside diameter and the pump casing bore inside diameter.It was determined the mechanical seals were changed out during the plant construction phase and replaced with an alternate mechanical seal.Apparently, at this time, the original pumping ring was replaced with a new style ring with no attention paid to the impact of this change with respect to pump casing bore inside diameter.Date obtained: Rubbing between the pumping ring and the pump housing could cause degradation to the pumping ring with the potential for damage to the pump rotating assembly.Condition is technically not Part 22 violation due to date of occurrence (prior to 2978).April 28, 2989 Basic Components Affected: Number: Locati on: 2 Auxiliary Building, Sub-basement Corrective Action: Machined outside diameter of pumping ring at supplier<s direction to permit proper placement in pump discharge housing.

Responsible Individual for Action: Thomas A.Marlow, Superintendent Ginna Support Services Time to Complete Action: Action was completed on both pumps Apri l 29, 1989.Advice Related to Defect': Vendor supplied repair direction.

0 II