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{{#Wiki_filter:CATEGORY 1 REGULATOI INFORMATION DISTRIBUTIOAOYSTEM (RIDE)ACCESSION NBR:9806110219 DOC.DATE: 98/06/08 NOTARIZED:
{{#Wiki_filter:CATEGORY 1 REGULATOI INFORMATION DISTRIBUTIOAOYSTEM (RIDE)
NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G AUTH.NAME, AUTHOR AFFILIATION WIDAY,J.A.'ochester Gas 5 Electric Corp.RECIP.NAME s RECIPIENT AFFILIATION NRC-No Detailed Affiliation Given DOCKET 05000244
ACCESSION NBR:9806110219           DOC.DATE: 98/06/08 NOTARIZED: NO                     DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester                       G 05000244 AUTH. NAME,           AUTHOR AFFILIATION WIDAY,J.A.'ochester               Gas 5 Electric Corp.
RECIP.NAME       s   RECIPIENT AFFILIATION NRC - No Detailed     Affiliation     Given


==SUBJECT:==
==SUBJECT:==
Part 21 rept re receipt of refurbished DB-25 circuit breaker w/missing part from W Replacement Components Svcs on 98060 DISTRIBUTION CODE: IE19T'COPIES RECEIVED:LTR 1 ENCL 1 SIZE: TITLE: Part 21 Rept (50 DKT)C'OTES:License Exp date in accordance with 10CFR2,2.109(9/19/72)
Part 21 rept re receipt of refurbished DB-25 circuit breaker w/missing part from W Replacement Components Svcs on 98060                               C DISTRIBUTION CODE: IE19T 'COPIES RECEIVED:LTR               1 ENCL   1   SIZE:
.05000244 E RECIPIENT ID CODE/NAME PD1-1 PD INTERNA: FILE CENTE R DRPM/PECB/B RES/DET/EIB RGN2 RGN4 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME VISSING,G.
TITLE: Part 21 Rept (50 DKT)
NRR/DRPM/PECB PDR WARD, M.RGN1 RGN3 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 0 EXTERNAL: INPO RECORD CTR NRC PDR 1 1 1 1 NOAC SILVER,E NUDOCS FULL TXT 1, 1 1 1 D 0 U NOTE TO ALL NRIDS" RECIPIENTS:
Exp date   in accordance with 10CFR2,2.109(9/19/72)           . 05000244     'O E
PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 15 ENCL 15  
RECIPIENT            COPIES              RECIPIENT             COPIES ID CODE/NAME          LTTR ENCL          ID CODE/NAME         LTTR ENCL PD1-1 PD                 1      1      VISSING,G.                1      1              0 INTERNA: FILE     CENTE               1      1      NRR/DRPM/PECB            1      1 R   DRPM/PECB/B         1     1       PDR WARD, M.             1      1 RES/DET/EIB              1     1       RGN1                      1       1 RGN2                      1     1       RGN3                      1       1 RGN4                      1     1 EXTERNAL: INPO RECORD CTR NRC PDR 1
~IP 4 i~/f Jy.'i ply~>>I.',~q*'p'yg it POWER REACTOR EVENT NUMBER: 34363 FACILITY: GINNA UNIT:[1][][]RX TYPE:[1]W-2-LP NRC NOTIFIED BY: WHITE HQ OPS OFFICER: CHAUNCEY GOULD REGION: 1 STATE: NY NOTIFICATION DATE: NOTIFICATION TIME: EVENT DATE: EVENT TIME: LAST UPDATE DATE: 06/08/98 11:49[ET]06/08/98 00:00[EDT]
1 1
06/08/98 UNSPECIFIED PARAGRAPH EMERGENCY CLASS: NOT APPLICABLE 10 CFR SECTION: CCCC 21.21 NOTIFICATXONS RICHARD BARKLEY HODGE RDO NRR UNIT SCRAM CODE RX CRIT INIT PWR INIT RX MODE CURR PWR CURR RX MODE N Y 100 POWER OPERATION 100 POWER OPERATION EVENT TEXT THIS PART 21 INVOLVES RECEIVING A REFURBISHED DB-25 CIRCUIT BREAKER WITH A MISSING PART.THE LICENSEE RECEIVED A REFURBISHED DB-25 CIRCUIT BREAKER(REFURBISHED IN 1992')FROM WESTINGHOUSE REPLACEMENT COMPONENTS SERVICESI MONROEVILLE PA THE REFURBISHED BREAKER WAS RETURNED TO THE LICENSEE WITH A MISSING PIN IN THE OPERATING MECHANISM.
1 NOAC SILVER,E NUDOCS FULL TXT 1,
THE ABSENCE OF THXS PIN IS BELIEVED TO HAVE CONTRIBUTED TO THE FAILURE OF THE"SWP1B" CIRCUIT BREAKER TO CLOSE ON A MANUAL SIGNAL FROM THE MAIN CONTROL BOARD.THIS ALSO IMPLIES THAT THE POTENTIAL EXISTS FOR THE BREAKER NOT TO CLOSE ON AN AUTOMATIC DEMAND AND THEREFORE NOT BE AVAXLABLE TO PERFORM XTS SAFETY FUNCTIONS.
1 1
THERE ARE 41 PERMANENTLY XNSTALLED DB-25 BREAKERS IN THE SCREEN HOUSE AND TURBINE BUILDINGS AT THE SXTE.ALL OF THE REMAINXNG BREAKERS WERE VISUALLY INSPECTED TO VERIFY THE PIN IN QUESTION WAS INSTALLED.
1 D
NO OTHER BREAKERS WERE FOUND TO BE MISSING THE PIN.THE RESIDENT INSPECTOR WAS NOTIFIED.98061102i9 980608 PDR ADOCK 05000244 8 PDR
0 U
NOTE TO ALL NRIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR               15   ENCL   15


CPV 4'l ROCHESTER GAS AND ELECTRlC CORPORATION 88 EASTA VENUE, JOS6PH A, WIOAY Phrs Monocot Gbno Nuclear Pkre 4'i~3Q~....e Wl ROCHESTER, H.Y.14649-0001 TCLKPHONK AREA CCOK TM 848'2700 June 8, 1998 U.S.Nuclear Regulatory Commission Operations Center Facsimile Number 301-816-5151 Telephone Number 301-816-5100
                                      ~ IP 4 i~/ fJy.'i ply~>> I. ', ~ q*'p 'yg it
 
POWER REACTOR                                        EVENT NUMBER:  34363 FACILITY: GINNA                          REGION: 1  NOTIFICATION DATE: 06/08/98 UNIT:      [1] [ ] [ ]                  STATE: NY  NOTIFICATION TIME: 11:49 [ET]
RX TYPE: [1] W-2-LP                                  EVENT DATE:        06/08/98 EVENT TIME:        00:00[EDT]
NRC NOTIFIED BY: WHITE                              LAST UPDATE DATE:  06/08/98 HQ OPS  OFFICER:  CHAUNCEY GOULD NOTIFICATXONS EMERGENCY CLASS: NOT APPLICABLE 10 CFR SECTION:                                      RICHARD BARKLEY        RDO CCCC 21.21                UNSPECIFIED PARAGRAPH HODGE                  NRR UNIT  SCRAM CODE RX  CRIT INIT  PWR  INIT RX MODE    CURR PWR    CURR RX MODE N          Y      100      POWER OPERATION    100    POWER OPERATION EVENT TEXT THIS PART 21 INVOLVES RECEIVING A REFURBISHED DB-25 CIRCUIT BREAKER WITH A MISSING PART.
THE LICENSEE RECEIVED A REFURBISHED DB-25 CIRCUIT BREAKER(REFURBISHED IN 1992') FROM WESTINGHOUSE REPLACEMENT COMPONENTS SERVICESI MONROEVILLE PA THE REFURBISHED BREAKER WAS RETURNED TO THE LICENSEE WITH A MISSING PIN IN THE OPERATING MECHANISM. THE ABSENCE OF THXS PIN IS BELIEVED TO HAVE CONTRIBUTED TO THE FAILURE OF THE "SWP1B" CIRCUIT BREAKER TO CLOSE ON A MANUAL SIGNAL FROM THE MAIN CONTROL BOARD.      THIS ALSO IMPLIES THAT THE POTENTIAL EXISTS FOR THE BREAKER NOT TO CLOSE ON AN AUTOMATIC DEMAND AND THEREFORE NOT BE AVAXLABLE TO PERFORM XTS SAFETY FUNCTIONS.      THERE ARE 41 PERMANENTLY XNSTALLED DB-25 BREAKERS IN THE SCREEN HOUSE AND TURBINE BUILDINGS AT THE SXTE. ALL OF THE REMAINXNG BREAKERS WERE VISUALLY INSPECTED TO VERIFY THE PIN IN QUESTION WAS INSTALLED. NO OTHER BREAKERS WERE FOUND TO BE MISSING THE PIN.
THE RESIDENT INSPECTOR WAS NOTIFIED.
98061102i9 980608 PDR  ADOCK 05000244 8              PDR
 
CPV   4' l
4'i~3Q
                                                                                  ~....e Wl ROCHESTER GAS AND ELECTRlC CORPORATION    88 EASTA VENUE, ROCHESTER, H.Y. 14649-0001 JOS6PH A, WIOAY                                                              TCLKPHONK Phrs Monocot                                                          AREA CCOK TM 848'2700 Gbno Nuclear Pkre                                                June 8, 1998 U.S. Nuclear Regulatory Commission Operations Center Facsimile Number 301-816-5151 Telephone Number 301-816-5100


==Subject:==
==Subject:==
Initial Notification of 10 CFR Part 21 Defect R.E.Ginna Nuclear Power Plant Docket No.50-244 Xn accordance with 10 CFR Part 21, Reporting of Defects and Noncompliance, Section 21 (d)(3)(i), which requires"Initial notification by facsimile", the enclosed initial notification is provided.Written notification, in accordance with 10 CFR Pazt 21, Section 21 (d)(3)(ii), will be provided by July 2, 1998.'ery truly yours, a.d se h A.Widay Enclosures  
Initial Notification of   10 CFR   Part 21 Defect R.E. Ginna Nuclear Power Plant Docket No. 50-244 Xn accordance   with 10 CFR Part 21, Reporting of Defects and Noncompliance,   Section 21 (d) (3) (i), which requires "Initial notification by facsimile", the enclosed initial notification is provided. Written notification, in accordance with 10 CFR Pazt 21, Section 21 (d) (3) (ii), will be provided by July 2, 1998.'ery truly     yours, a.d se h A. Widay Enclosures
 
Page 1
    ,10CFR21  INITIAL FACSIMILE NOTIFXCATION NAME AND ADDRESS      OF  THE  INDIVZDUAL INFORMING THE COMMISS ZON i NAME:      Joseph A. Widay ADDRESS:  Rochester Gas a Electric, Corporation 89 East Avenue Rochester, New York 14649 IDENTIFICATION OF THE FACILITY, THE ACTIVITY, OR THE BASXC COMPONENT SUPPLXED FOR SUCH FACILXTY WHICH FAILS TO COMPLY OR CONTAINS A DEFECTS The facility is    the R.E. Ginna Nuclear Power Plant. The basic DB-25 circuit breaker.
component    is  a Westinghouse                            This component    was installed at Ginna Statio'n in a Class 1E Safety Related 480 Volt AC bus. The breaker was the power supply feed breaker for the "B" Service Water Pump (52/SWPlB).
IDENTIFICATZON OF THE FIRM CONSTRUCTING THE FACILITY OR SUPPLYXNG THE BASiC COMPONENT WHICH FAILS TO COMPLY OR CONTAINS A DEFECT:
The DB-25  circuit  breaker were refurbished by:
Westinghouse Replacement Component Services Westinghouse Electric Corporation Nuclear Services Division Haymaker and Northern Pike    Road Monroeville, PA 15146 The  current refurbishment site is:
Westinghouse Electric Corporation Assembly 5. Test Facility Cheswick Site 2000 Cheswick Avenue Cheswick, PA 15024-1358 NATURE OF THE DEFECT OR FAILURE TO COMPLY AND THE SAFETY HAZARD WHICH IS CREATED OR COULD BE CREATED BY SUCH DEFECT OR FAILURE TO COMPLY:
The  refurbished DB-25 circuit breaker was returned to Ginna Station with a missing pin in the operating mechanism. The absence of this pin is believed to have contributed to the failure of the SWP1B circuit breaker to close on a manual signal from the Main Control Board. This implies that the potential exists that the breaker would not close on an auto demand and therefore not be available to perform its safety function(s).


Page 1 ,10CFR21 INITIAL FACSIMILE NOTIFXCATION NAME AND ADDRESS OF THE INDIVZDUAL INFORMING THE COMMISS ZON i NAME: ADDRESS: Joseph A.Widay Rochester Gas a Electric, Corporation 89 East Avenue Rochester, New York 14649 IDENTIFICATION OF THE FACILITY, THE ACTIVITY, OR THE BASXC COMPONENT SUPPLXED FOR SUCH FACILXTY WHICH FAILS TO COMPLY OR CONTAINS A DEFECTS The facility is the R.E.Ginna Nuclear Power Plant.The basic component is a Westinghouse DB-25 circuit breaker.This component was installed at Ginna Statio'n in a Class 1E Safety Related 480 Volt AC bus.The breaker was the power supply feed breaker for the"B" Service Water Pump (52/SWPlB).
0 ',
IDENTIFICATZON OF THE FIRM CONSTRUCTING THE FACILITY OR SUPPLYXNG THE BASiC COMPONENT WHICH FAILS TO COMPLY OR CONTAINS A DEFECT: The DB-25 circuit breaker were refurbished by: Westinghouse Replacement Component Services Westinghouse Electric Corporation Nuclear Services Division Haymaker and Northern Pike Road Monroeville, PA 15146 The current refurbishment site is: Westinghouse Electric Corporation Assembly 5.Test Facility Cheswick Site 2000 Cheswick Avenue Cheswick, PA 15024-1358 NATURE OF THE DEFECT OR FAILURE TO COMPLY AND THE SAFETY HAZARD WHICH IS CREATED OR COULD BE CREATED BY SUCH DEFECT OR FAILURE TO COMPLY: The refurbished DB-25 circuit breaker was returned to Ginna Station with a missing pin in the operating mechanism.
JVI'0 CPU iPPV i4           4 ~ ~ ~ ~ ~ ~ ~
The absence of this pin is believed to have contributed to the failure of the SWP1B circuit breaker to close on a manual signal from the Main Control Board.This implies that the potential exists that the breaker would not close on an auto demand and therefore not be available to perform its safety function(s).
  ~
0',
~
JVI'0 CPU iPPV i4~~4~~~~~~~page 2 VI.'VI I.THE DATE ON WHICH THE INFORMATION OF SUCH DEFECT OR FAILURE TO COMPLY WAS OBTAINED~'The information was obtained on May 3.3, 1998.An attempt was made to start the"B" Service Water Pump during testing and it failed to close on a manual signal from the Main Contxol Board.During the troubleshooting the missing part was discovered..
page 2 THE DATE ON WHICH THE INFORMATION OF         SUCH DEFECT OR FAILURE TO COMPLY WAS OBTAINED~
IH THE CASE OF A BASIC COMPONENT WHICH CONTAINS A DEFECT OR FAILS TO COMPLY, THE NUMBER AND LOCATION.OF ALL SUCH COMPONENTS IN USE AT, SUPPLIED FOR, OR BEING SUPPLIED FOR GINNA STATXON-There are forty-one, permanently installed DB-25 bxeakers in the Screen House and Turbine Buildings at Ginna Station.Of these, eleven bxeakers axe Class lE Safety Related.THE CORRECTIVE ACTION WHICH HAS BEEN, IS BEING, OR WILL BE TAKEN;THE NAME OF THE INDIVIDUAL OR ORGANIZATION RESPONSIBLE FOR THE ACTION;AND THE LENGTH OF TIME THAT HAS BEEN OR WILL BE TAKEN TO COMPLETE THE ACTION: A spare DB-25 circuit breaker was inspected, tested and installed to restore the"B" Service Water Pump to service.All of the xemaining DB-25 breakers were visually inspected to verify that the pin in question was installed.
                                                    '
No other breakers were found to be missing the pin.ANY ADVICE RELATED TO THE DEFECT OR FAILURE TO COMPLY ABOUT THE FACILITY, ACTIVITY, OR BASIC COMPONENT THAT HAS BEEN, IS BEINGS OR WILL BE GIVEN TO PURCHASERS OR LXCENSEES:
The information was obtained on May 3.3, 1998. An attempt was made   to start the "B" Service Water Pump during testing and it failed to close on a manual signal from the Main Contxol Board. During the troubleshooting the missing part was discovered..
Both in-service and receipt inspections can verify the presence of the pin in question.Xt should be noted that the"B" Service Hater Pump breaker was refurbished in 1992.TOTAL P.83}}
VI.          IH THE CASE OF A BASIC COMPONENT WHICH CONTAINS A DEFECT OR FAILS TO COMPLY, THE NUMBER AND LOCATION .OF ALL SUCH COMPONENTS IN USE AT, SUPPLIED FOR, OR BEING SUPPLIED FOR GINNA STATXON-There are forty-one, permanently installed DB-25 bxeakers in the Screen House and Turbine Buildings at Ginna Station. Of these, eleven bxeakers axe Class lE Safety Related.
            'VII .      THE CORRECTIVE ACTION WHICH HAS BEEN, IS BEING, OR WILL BE TAKEN; THE NAME OF THE INDIVIDUAL OR ORGANIZATION RESPONSIBLE FOR THE ACTION; AND THE LENGTH OF TIME THAT HAS BEEN OR WILL BE TAKEN TO COMPLETE THE ACTION:
A   spare DB-25       circuit breaker was inspected, tested and installed to restore the "B" Service Water Pump to service.
All of the xemaining DB-25 breakers were visually inspected to verify that the pin in question was installed. No other breakers were found to be missing the pin.
ANY ADVICE RELATED TO THE DEFECT OR FAILURE TO COMPLY ABOUT THE FACILITY, ACTIVITY, OR BASIC COMPONENT THAT HAS BEEN, IS BEINGS OR WILL BE GIVEN TO PURCHASERS OR LXCENSEES:
Both in-service and receipt inspections can verify the presence of the pin in question.           Xt should be noted that the "B" Service Hater Pump breaker was refurbished in 1992.
TOTAL P.83}}

Revision as of 17:50, 29 October 2019

Part 21 Rept Re Receipt of Refurbished DB-25 Circuit Breaker W/Missing Part from W Replacement Components Svcs on 980608. Spare DB-25 Circuit Breaker Was Inspected,Tested & Installed to Restore B Swp to Svc
ML17265A318
Person / Time
Site: Ginna Constellation icon.png
Issue date: 06/08/1998
From: Widay J
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC
References
REF-PT21-98 NUDOCS 9806110219
Download: ML17265A318 (10)


Text

CATEGORY 1 REGULATOI INFORMATION DISTRIBUTIOAOYSTEM (RIDE)

ACCESSION NBR:9806110219 DOC.DATE: 98/06/08 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME, AUTHOR AFFILIATION WIDAY,J.A.'ochester Gas 5 Electric Corp.

RECIP.NAME s RECIPIENT AFFILIATION NRC - No Detailed Affiliation Given

SUBJECT:

Part 21 rept re receipt of refurbished DB-25 circuit breaker w/missing part from W Replacement Components Svcs on 98060 C DISTRIBUTION CODE: IE19T 'COPIES RECEIVED:LTR 1 ENCL 1 SIZE:

TITLE: Part 21 Rept (50 DKT)

Exp date in accordance with 10CFR2,2.109(9/19/72) . 05000244 'O E

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-1 PD 1 1 VISSING,G. 1 1 0 INTERNA: FILE CENTE 1 1 NRR/DRPM/PECB 1 1 R DRPM/PECB/B 1 1 PDR WARD, M. 1 1 RES/DET/EIB 1 1 RGN1 1 1 RGN2 1 1 RGN3 1 1 RGN4 1 1 EXTERNAL: INPO RECORD CTR NRC PDR 1

1 1

1 NOAC SILVER,E NUDOCS FULL TXT 1,

1 1

1 D

0 U

NOTE TO ALL NRIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 15 ENCL 15

~ IP 4 i~/ fJy.'i ply~>> I. ', ~ q*'p 'yg it

POWER REACTOR EVENT NUMBER: 34363 FACILITY: GINNA REGION: 1 NOTIFICATION DATE: 06/08/98 UNIT: [1] [ ] [ ] STATE: NY NOTIFICATION TIME: 11:49 [ET]

RX TYPE: [1] W-2-LP EVENT DATE: 06/08/98 EVENT TIME: 00:00[EDT]

NRC NOTIFIED BY: WHITE LAST UPDATE DATE: 06/08/98 HQ OPS OFFICER: CHAUNCEY GOULD NOTIFICATXONS EMERGENCY CLASS: NOT APPLICABLE 10 CFR SECTION: RICHARD BARKLEY RDO CCCC 21.21 UNSPECIFIED PARAGRAPH HODGE NRR UNIT SCRAM CODE RX CRIT INIT PWR INIT RX MODE CURR PWR CURR RX MODE N Y 100 POWER OPERATION 100 POWER OPERATION EVENT TEXT THIS PART 21 INVOLVES RECEIVING A REFURBISHED DB-25 CIRCUIT BREAKER WITH A MISSING PART.

THE LICENSEE RECEIVED A REFURBISHED DB-25 CIRCUIT BREAKER(REFURBISHED IN 1992') FROM WESTINGHOUSE REPLACEMENT COMPONENTS SERVICESI MONROEVILLE PA THE REFURBISHED BREAKER WAS RETURNED TO THE LICENSEE WITH A MISSING PIN IN THE OPERATING MECHANISM. THE ABSENCE OF THXS PIN IS BELIEVED TO HAVE CONTRIBUTED TO THE FAILURE OF THE "SWP1B" CIRCUIT BREAKER TO CLOSE ON A MANUAL SIGNAL FROM THE MAIN CONTROL BOARD. THIS ALSO IMPLIES THAT THE POTENTIAL EXISTS FOR THE BREAKER NOT TO CLOSE ON AN AUTOMATIC DEMAND AND THEREFORE NOT BE AVAXLABLE TO PERFORM XTS SAFETY FUNCTIONS. THERE ARE 41 PERMANENTLY XNSTALLED DB-25 BREAKERS IN THE SCREEN HOUSE AND TURBINE BUILDINGS AT THE SXTE. ALL OF THE REMAINXNG BREAKERS WERE VISUALLY INSPECTED TO VERIFY THE PIN IN QUESTION WAS INSTALLED. NO OTHER BREAKERS WERE FOUND TO BE MISSING THE PIN.

THE RESIDENT INSPECTOR WAS NOTIFIED.

98061102i9 980608 PDR ADOCK 05000244 8 PDR

CPV 4' l

4'i~3Q

~....e Wl ROCHESTER GAS AND ELECTRlC CORPORATION 88 EASTA VENUE, ROCHESTER, H.Y. 14649-0001 JOS6PH A, WIOAY TCLKPHONK Phrs Monocot AREA CCOK TM 848'2700 Gbno Nuclear Pkre June 8, 1998 U.S. Nuclear Regulatory Commission Operations Center Facsimile Number 301-816-5151 Telephone Number 301-816-5100

Subject:

Initial Notification of 10 CFR Part 21 Defect R.E. Ginna Nuclear Power Plant Docket No. 50-244 Xn accordance with 10 CFR Part 21, Reporting of Defects and Noncompliance, Section 21 (d) (3) (i), which requires "Initial notification by facsimile", the enclosed initial notification is provided. Written notification, in accordance with 10 CFR Pazt 21, Section 21 (d) (3) (ii), will be provided by July 2, 1998.'ery truly yours, a.d se h A. Widay Enclosures

Page 1

,10CFR21 INITIAL FACSIMILE NOTIFXCATION NAME AND ADDRESS OF THE INDIVZDUAL INFORMING THE COMMISS ZON i NAME: Joseph A. Widay ADDRESS: Rochester Gas a Electric, Corporation 89 East Avenue Rochester, New York 14649 IDENTIFICATION OF THE FACILITY, THE ACTIVITY, OR THE BASXC COMPONENT SUPPLXED FOR SUCH FACILXTY WHICH FAILS TO COMPLY OR CONTAINS A DEFECTS The facility is the R.E. Ginna Nuclear Power Plant. The basic DB-25 circuit breaker.

component is a Westinghouse This component was installed at Ginna Statio'n in a Class 1E Safety Related 480 Volt AC bus. The breaker was the power supply feed breaker for the "B" Service Water Pump (52/SWPlB).

IDENTIFICATZON OF THE FIRM CONSTRUCTING THE FACILITY OR SUPPLYXNG THE BASiC COMPONENT WHICH FAILS TO COMPLY OR CONTAINS A DEFECT:

The DB-25 circuit breaker were refurbished by:

Westinghouse Replacement Component Services Westinghouse Electric Corporation Nuclear Services Division Haymaker and Northern Pike Road Monroeville, PA 15146 The current refurbishment site is:

Westinghouse Electric Corporation Assembly 5. Test Facility Cheswick Site 2000 Cheswick Avenue Cheswick, PA 15024-1358 NATURE OF THE DEFECT OR FAILURE TO COMPLY AND THE SAFETY HAZARD WHICH IS CREATED OR COULD BE CREATED BY SUCH DEFECT OR FAILURE TO COMPLY:

The refurbished DB-25 circuit breaker was returned to Ginna Station with a missing pin in the operating mechanism. The absence of this pin is believed to have contributed to the failure of the SWP1B circuit breaker to close on a manual signal from the Main Control Board. This implies that the potential exists that the breaker would not close on an auto demand and therefore not be available to perform its safety function(s).

0 ',

JVI'0 CPU iPPV i4 4 ~ ~ ~ ~ ~ ~ ~

~

~

page 2 THE DATE ON WHICH THE INFORMATION OF SUCH DEFECT OR FAILURE TO COMPLY WAS OBTAINED~

'

The information was obtained on May 3.3, 1998. An attempt was made to start the "B" Service Water Pump during testing and it failed to close on a manual signal from the Main Contxol Board. During the troubleshooting the missing part was discovered..

VI. IH THE CASE OF A BASIC COMPONENT WHICH CONTAINS A DEFECT OR FAILS TO COMPLY, THE NUMBER AND LOCATION .OF ALL SUCH COMPONENTS IN USE AT, SUPPLIED FOR, OR BEING SUPPLIED FOR GINNA STATXON-There are forty-one, permanently installed DB-25 bxeakers in the Screen House and Turbine Buildings at Ginna Station. Of these, eleven bxeakers axe Class lE Safety Related.

'VII . THE CORRECTIVE ACTION WHICH HAS BEEN, IS BEING, OR WILL BE TAKEN; THE NAME OF THE INDIVIDUAL OR ORGANIZATION RESPONSIBLE FOR THE ACTION; AND THE LENGTH OF TIME THAT HAS BEEN OR WILL BE TAKEN TO COMPLETE THE ACTION:

A spare DB-25 circuit breaker was inspected, tested and installed to restore the "B" Service Water Pump to service.

All of the xemaining DB-25 breakers were visually inspected to verify that the pin in question was installed. No other breakers were found to be missing the pin.

ANY ADVICE RELATED TO THE DEFECT OR FAILURE TO COMPLY ABOUT THE FACILITY, ACTIVITY, OR BASIC COMPONENT THAT HAS BEEN, IS BEINGS OR WILL BE GIVEN TO PURCHASERS OR LXCENSEES:

Both in-service and receipt inspections can verify the presence of the pin in question. Xt should be noted that the "B" Service Hater Pump breaker was refurbished in 1992.

TOTAL P.83